97-12148. Public Service Electric & Gas Company, Philadelphia Electric Company, Delmarva Power and Light Company, Atlantic City Electric Company, Salem Nuclear Generating Station, Units 1 and 2; Environmental Assessment and Finding of No Significant ...  

  • [Federal Register Volume 62, Number 90 (Friday, May 9, 1997)]
    [Notices]
    [Pages 25675-25677]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 97-12148]
    
    
    -----------------------------------------------------------------------
    
    NUCLEAR REGULATORY COMMISSION
    
    [Docket Nos. 50-272 and 50-311]
    
    
    Public Service Electric & Gas Company, Philadelphia Electric 
    Company, Delmarva Power and Light Company, Atlantic City Electric 
    Company, Salem Nuclear Generating Station, Units 1 and 2; Environmental 
    Assessment and Finding of No Significant Impact
    
        The U.S. Nuclear Regulatory Commission (the Commission) is 
    considering issuance of a license amendment for Facility Operating 
    Licenses Nos. DPR-70 and DPR-75, issued to Public Service Electric and 
    Gas Company (PSE&G, the licensee), for operation of the Salem Nuclear 
    Generating Station, Units 1 and 2 (Salem Units 1 and 2).
        The facility consists of two pressurized-water reactors located at 
    the licensee's site in Salem County, New Jersey.
    
    Environmental Assessment
    
    Identification of Proposed Action
    
        The proposed action would change Technical Specification (TS) 
    3.4.3, ``Relief Valves,'' for Salem Unit 1, and TS 3.4.5, ``Relief 
    Valves,'' for Salem
    
    [[Page 25676]]
    
    Unit 2, to ensure that the automatic capability of the power operated 
    relief valves (PORVs) to relieve pressure is maintained when these 
    valves are isolated by closure of the block valves.
        The proposed action is in accordance with the licensee's 
    application for amendment dated January 31, 1997, as supplemented by 
    letter dated March 14, 1997.
    
    The Need for the Proposed Action
    
        In June of 1990, the NRC issued Generic Letter (GL) 90-06 entitled 
    ``Resolution of Generic Issue 70, `Power-Operated Valve and Block Valve 
    Reliability,' and Generic Issue 94 `Additional Low-Temperature 
    Overpressurization Protection For Light-Water Reactors.''' This GL was 
    issued to increase the reliability of the PORVs and block valves to 
    assure that they would function as required for certain transients and 
    accidents including Steam Generator Tube Rupture (SGTR), low 
    temperature overpressurization protection, and plant cooldown. One of 
    the actions required by the GL was to revise the limiting conditions 
    for operation (LCO) of the PORVs and block valves in the TSs.
        PSE&G complied by submitting a request to change the TSs, by letter 
    NLR-N93163 dated December 8, 1993, which was incorporated in the Salem 
    Unit 1 and 2 licenses via Amendments 150 and 130, dated April 7, 1994, 
    respectively. The submitted request and amendments were based on the 
    guidance provided in the GL and also later revisions that were made to 
    the LCO under NUREG-1431, ``Standard Technical Specifications 
    Westinghouse Plants,'' Revision 0, dated September 1992. One of the 
    changes afforded by NUREG-1431 was to allow PORV isolation provided the 
    PORVs are capable of manual operation based on the mitigation of a 
    Steam Generator Tube Rupture event; whereas, the TSs recommended in GL 
    90-06 addressed isolation only for valves with excessive seat leakage.
        In June of 1993, Westinghouse issued Nuclear Safety Advisory 
    letter, NSAL 93-013, which addressed the Inadvertent Safety Injection 
    (SI) Actuation at Power event and informed plants that potential 
    nonconservative assumptions were used in evaluating the Inadvertent SI 
    analyses. Westinghouse determined that crediting PORV operation could 
    be a potential solution for the mitigation of this event. The spurious 
    operation of the SI System at power is classified as a Condition II 
    event, a fault of moderate frequency, as referenced in Salem's Updated 
    Final Safety Analysis Report (UFSAR) Section 15.2.14. A Condition II 
    event should result in a reactor shutdown with the plant being capable 
    of returning to operation.
        PSE&G has determined that an inadvertent SI at power could cause 
    the pressurizer to become water-solid if the resulting injection of 
    borated water is not terminated. In the event that the pressurizer 
    becomes fully water-solid, timely PORV actuation successfully mitigates 
    the event. However, without automatic operation of the PORVs, the 
    Reactor Coolant System (RCS) pressure may increase to the lift setpoint 
    of the pressurizer safety relief valves before the PORVs are manually 
    opened. The Salem pressurizer safety valves are not designed to relieve 
    water. It is postulated, therefore, that one or more of the valves 
    could fail to completely reseat if relieving a water-solid pressurizer. 
    A resulting unisolable loss of RCS inventory has been analyzed in 
    Salem's UFSAR as a Condition III event.
        A review of the current Salem TSs indicates that a TS revision is 
    necessary to preclude the possibility of operating with PORVs that can 
    only be cycled manually. PSE&G's re-analysis of the Inadvertent SI at 
    Power performed to support resolution of NSAL 93-013, credits operator 
    action to unblock the PORVs, if necessary. However, once unblocked it 
    is unlikely that operator actions can be readily accomplished to 
    manually cycle the PORVs such that the pressurizer safety valve 
    pressure is not reached. Therefore, PSE&G submitted the proposed TS 
    changes by letter dated January 31, 1997, to incorporate the results of 
    PSE&G's analysis (i.e., to credit automatic operation of PORVs for an 
    Inadvertent SI event), into the TSs.
    
    Environmental Impacts of the Proposed Action
    
        As indicated in Salem UFSAR Section 15.2.4, ``Spurious Operation of 
    The Safety Injection System at Power,'' the results of this transient 
    do not lead to fuel cladding damage and thus no fission products are 
    released. The proposed changes to the TSs assure that post transient 
    reactor coolant system pressure relief will continue to be 
    controllable; thus, no change in the transient result will occur. 
    Accordingly, no changes are being made in the types of any effluent 
    that may be released offsite, and there is no significant increase in 
    the allowable individual or cumulative occupational radiation exposure. 
    Accordingly, the Commission concludes that there are no significant 
    radiological environmental impacts associated with the proposed action.
        With regard to potential nonradiological impacts, the proposed 
    action involves features located entirely within the restricted area as 
    defined in 10 CFR Part 20. It does not affect nonradiological plant 
    effluents and has no other environmental impact. Accordingly, the 
    Commission concludes that there are no significant nonradiological 
    environmental impacts associated with the proposed action.
    
    Alternatives to the Proposed Action
    
        Since the Commission has concluded there is no measurable 
    environmental impact associated with the proposed action, any 
    alternatives with equal or greater environmental impact need not be 
    evaluated. The principal alternative to the action would be to deny the 
    request. Such action would not change any current environmental 
    impacts. The environmental impacts of the proposed action and the 
    alternative action are similar.
    
    Alternative Use of Resources
    
        This action does not involve the use of any resources not 
    previously considered in the Final Environmental Statement related to 
    the operation of Salem Nuclear Generating Station Units 1 and 2, dated 
    April 1973.
    
    Agencies and Persons Consulted
    
        In accordance with its stated policy, on April 15, 1997, the staff 
    consulted with the New Jersey State official, Mr. R. Pinney, of the New 
    Jersey Department of Environmental Protection and Energy, regarding the 
    environmental impact of the proposed action. The State official had no 
    comments.
    
    Finding of No Significant Impact
    
        Based upon the environmental assessment, the Commission concludes 
    that the proposed action will not have a significant effect on the 
    quality of the human environment. Accordingly, the Commission has 
    determined not to prepare an environmental impact statement for the 
    proposed action.
        For further details with respect to the proposed action, see the 
    licensee's letter dated January 31, 1997, and supplement dated March 
    14, 1997, which are available for public inspection at the Commission's 
    Public Document Room, The Gelman Building, 2120 L Street, NW., 
    Washington, DC and at the local public document room located at the 
    Salem Free Library, 112 West Broadway, Salem, New Jersey 08079.
    
        Dated at Rockville, Maryland, this 2nd day of May 1997.
    
    
    [[Page 25677]]
    
    
        For the Nuclear Regulatory Commission.
    John F. Stolz,
    Director, Project Directorate I-2, Division of Reactor Projects--I/II, 
    Office of Nuclear Reactor Regulation.
    [FR Doc. 97-12148 Filed 5-8-97; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
05/09/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
97-12148
Pages:
25675-25677 (3 pages)
Docket Numbers:
Docket Nos. 50-272 and 50-311
PDF File:
97-12148.pdf