97-15827. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 62, Number 117 (Wednesday, June 18, 1997)]
    [Notices]
    [Pages 33117-33142]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 97-15827]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person. This biweekly notice includes 
    all notices of amendments issued, or proposed to be issued from May 23, 
    1997, through June 6, 1997. The last biweekly notice was published on 
    June 4, 1997 (62 FR 30629).
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission
    
    [[Page 33118]]
    
    take this action, it will publish in the Federal Register a notice of 
    issuance and provide for opportunity for a hearing after issuance. The 
    Commission expects that the need to take this action will occur very 
    infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By July 18, 1997, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1) (i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Baltimore Gas and Electric Company, Docket No. 50-317, Calvert Cliffs 
    Nuclear Power Plant, Unit No. 1, Calvert County, Maryland
    Date of amendment request: May 16, 1997
    
        Description of amendment request: The modification involves 
    replacing the service water (SRW) heat exchangers with new plate and 
    frame heat exchangers having increased thermal performance capability. 
    The saltwater (SW) and SRW piping configuration will be modified as 
    necessary to allow proper fit-up to the new components. A flow control 
    scheme to throttle saltwater flow to the heat exchangers and the 
    associated bypass lines will be added.
    
    [[Page 33119]]
    
    Saltwater strainers with an automatic flushing arrangement will be 
    added upstream of each heat exchanger. The majority of the physical 
    work associated with this modification is restricted to the SRW pump 
    room.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Would not involve significant increase in the probability or 
    consequences of an accident previously evaluated.
        None of the systems associated with the proposed modification 
    are accident initiators. The SW and SRW Systems are used to mitigate 
    the effects of accidents analyzed in the UFSAR [Updated Final Safety 
    Analysis Report]. The SW and SRW Systems provide cooling to safety-
    related equipment following an accident. They support accident 
    mitigation functions; therefore, the proposed modification does not 
    increase the probability of an accident previously evaluated.
        The proposed modification will increase the heat removal 
    capacity of the SRW System. The design provided under this activity 
    ensures that the safety features provided by the SW and SRW are 
    maintained, and in some instances enhanced; i.e., the availability 
    of important-to-safety equipment required to mitigate the 
    radiological consequences of an accident described in the UFSAR is 
    enhanced by the flexibility and increased thermal margin provided 
    with this design.
        The redundant cooling capacity of the SW and SRW Systems have 
    not been altered. Furthermore, the proposed activity will not 
    change, degrade, or prevent actions described or assumed in any 
    accident described in the UFSAR. The proposed activity will not 
    alter any assumptions previously made in evaluating the radiological 
    consequences of any accident described in the UFSAR. Therefore, the 
    consequences of an accident previously evaluated in the UFSAR have 
    not increased.
        Therefore, the proposed modification does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated.
        The proposed activity involves modifying the SW and SRW System 
    components necessary to support the installation of new SRW heat 
    exchangers. None of the systems associated with this modification 
    are identified as accident initiators in the UFSAR. The SW and SRW 
    Systems are used to mitigate the effects of accidents analyzed in 
    the UFSAR. None of the functions required of the SRW or SW System 
    have been changed by this modification. This activity does not 
    modify any system, structure, or component such that it could become 
    accident initiator, as opposed to its current role as an accident 
    mitigator.
        Therefore, the proposed change does not create the possibility 
    of a new or different type of accident from any accident previously 
    evaluated.
        3. Would not involve a significant reduction in a margin of 
    safety.
        The safety design basis for the SW and SRW Systems is the 
    availability of sufficient cooling capacity to ensure continued 
    operation of equipment during normal and accident conditions. The 
    redundant cooling capacity of these systems, assuming a single 
    failure, is consistent with assumptions used in the accident 
    analysis.
        The design, procurement, installation, and testing of the 
    equipment associated with the proposed modification are consistent 
    with the applicable codes and standards governing the original 
    systems, structures, and components. The design of instruments and 
    associated cabling ensures that physical and electrical separation 
    of the two subsystems is maintained. Common-mode failure is not 
    introduced by this activity. The equipment is qualified for the 
    service conditions stipulated for that environment. New cable and 
    raceways for this design will be installed in accordance with 
    seismic design requirements. The additional electrical load has been 
    reviewed to ensure the load limits for the vital 1E buses are not 
    exceeded. The circuits and components related to the control valves 
    control loops are safety-related, and are similar to those used for 
    the other safety-related flow control functions. The proposed 
    modification will not have any adverse effects on the safety-related 
    functions of the SW and SRW Systems.
        For the above reasons, the existing safety bases have not been 
    altered by the proposed modification. This activity will not reduce 
    the margin of safety as it exists now. In fact, the margin of safety 
    has been increased by this activity due to the increase in the 
    thermal capacity of the dual train design and the increased 
    availability of safety-related components.
        Therefore, this proposed modification does not significantly 
    reduce the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Alexander W. Dromerick, Acting Director.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    Date of amendment request: April 23, 1997
    
        Description of amendment request: The proposed changes would revise 
    surveillances 4.3.2.1.1.a, 4.3.2.1.4.b, 4.3.2.1.6.g, 4.3.2.1.10a, 
    4.3.2.1.10.b, and 4.7.3.b.3 to provide enhanced descriptions of the 
    tests being performed and the tested components.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        This change clarification does not involve a significant hazards 
    consideration for the following reasons:
        (1) The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The components affected by the proposed changes are not 
    initiators of any accident previously evaluated. The proposed 
    changes to specification 4.3.2.1 items affect only the description 
    of the testing and make no changes in actual operation or testing. 
    The sample heat exchanger valves isolate on receipt of a Safety 
    Injection signal and that feature is unaffected by the additional 
    testing in the proposed change. Therefore, there is no increase in 
    the probability or consequence of a previously analyzed accident.
        (2) The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes to the surveillance frequencies do not 
    involve physical alterations or additions to plant equipment or 
    alter the manner in which safety-related systems function or are 
    normally operated. The additional testing proposed for the sample 
    heat exchanger valves demonstrates the proper operation of a design 
    feature but does not operate the valve in any new way. Therefore, 
    the proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        (3) The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        The proposed changes to specification 4.3.2.1 clarify existing 
    testing. The additional testing for the CCW [component cooling 
    water] surge tank level instrumentation adds two components to the 
    surveillance documentation. Therefore, there is no reduction in the 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    [[Page 33120]]
    
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Mark Reinhart, Acting.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    Date of amendment request: April 14, 1997
    
        Description of amendment request: The proposed amendments would 
    revise TS 3/4.3.8, ``Feedwater/Main Turbine Trip System Actuation 
    Instrumentation'' by changing the minimum channels required from 3 to 
    4. This change reflects a modification that is being installed to 
    correct a design deficiency that could have resulted in a failure to 
    trip the feedwater pumps and main turbine on high water level due to 
    the loss of one of the two instrument lines. The modification adds an 
    auxiliary contact to the trip system logic resulting in an additional 
    channel. The licensee is also proposing to modify the TS action 
    statements for inoperable channels to be similar to TS 3.3.1, ``Reactor 
    Protection System.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because:
        The proposed Technical Specification (TS) change will resolve 
    the common instrument line failure (break) from preventing reactor 
    high water level trip of Feedwater Pumps and Main Turbine. It will 
    not change the probability of occurrence of any accidents, because 
    this instrumentation is not an accident initiator. This 
    instrumentation resolves a potential concern regarding the results 
    of an instrument line break in conjunction with a Feedwater 
    Controller Failure Maximum Demand, which has been postulated and 
    analyzed separately, but are not required to be analyzed in 
    combination, as is described in Chapter 15 of the LaSalle UFSAR. 
    There will not be any increase in probability of feedwater transient 
    (postulated feedwater controller failure with assumed simultaneous 
    failure of one high level trip channel of Feedwater/Main Turbine 
    Trip Actuation Instrumentation), nor an instrument line break. The 
    design change associated with this TS change will prevent the 
    failure of the level 8 trip of Feedwater Pumps and Main Turbine due 
    to loss of common variable water leg of level instrument channels 
    ``B'' and ``C''. Thus there is a slight increase [in] the 
    reliability of the high level trip by assuring that a single 
    instrument failure, including a failure of a sensing line, will not 
    prevent a level 8 trip. The Feedwater/Main Turbine Trip on Reactor 
    Vessel Water Level-High, Level 8, mitigates the consequences of the 
    transient, Feedwater Controller Failure Maximum Demand, due to the 
    main turbine trip with subsequent Turbine Stop Valve closure scram 
    and Reactor Recirculation Pump Trip. This limits the neutron flux 
    peak and fuel thermal transients so that no fuel damage occurs. MCPR 
    remains at or above the operating limit and peak centerline fuel 
    temperature increase is small. The consequences of an accident will 
    not increase, because the redundancy of the instrumentation portion 
    of the Trip Function is somewhat increased.
        TS 3.3.8 limiting Condition for Operation (LCO) Actions b and c 
    are proposed to be changed to be similar to the LCO for TS 3.3.1, 
    Reactor Protection System Action b.1 to assure trip capability, 
    while being consistent with the allowed outage times of current TS 
    3.3.8. Also, the proposed action statements and allowed outage times 
    are consistent with LCO 3.3.2.2, ``Feedwater and Main Turbine High 
    Water Level Trip Instrumentation'', of NUREG 1433, Revision 1, 
    Standard Technical Specifications, General Electric Plants, BWR4, 
    dated April 1995. The limit on continued plant operation of 72 hours 
    in current Action c.1, is overly restrictive, since with one 
    inoperable channel tripped and one Operable channel, the Trip 
    Function is restored to the same status as current Action b.1 (one 
    more instrument failure will cause a failure to actuate on high 
    reactor water level). Therefore, although the proposed Actions are 
    increasing the allowed outage time for the case with only one 
    remaining Operable channel, from 72 hours to 7 days, the level of 
    protection for automatic trip capability is maintained except for a 
    2 hour period during which trip capability may not exist. In 
    addition, like current Action b.1, the proposed Actions assure that 
    the longest time that automatic trip capability failure due to 
    another instrument failure will exist is 7 days. Therefore, the 
    potential for failure of the Feedwater/Main Turbine trip on reactor 
    vessel high water level may be slightly increased, but is not 
    significant considering the non-safety-related Feedwater Pump and 
    Main Turbine trips are not and are not required to be single-failure 
    proof.
        Based on the above, the proposed amendments will not increase 
    the probability or consequences of any accident previously 
    evaluated.
        (2) Create the possibility of a new or different kind of 
    accident from any accident previously evaluated because:
        The Feedwater/Main Turbine trip is a non-safety function in the 
    non-safety-related feedwater system. The high water level trip is an 
    equipment protective action preventing main steam carry over in the 
    main steam from damaging the main turbine and preventing high 
    pressure liquid discharge through the safety relief valve discharge 
    lines in case of a feedwater transient due to a controller failure 
    to maximum demand. The trip system is not designed to any applicable 
    standards or regulatory guides or 10CFR50 Appendix A General Design 
    Criteria per UFSAR Table 7.1-2. The trip system is not designed nor 
    required to meet the single failure criteria. This is a non-safety/
    non-divisional trip actuation required in Operating Condition 1, Run 
    Mode, such that high integrity of the trip is maintained. The 
    feedwater system is not required to mitigate the consequences of 
    accidents.
        The design change associated with this TS change will increase 
    the reliability of the trip logic. This is accomplished by assuring 
    that a failure of a sensing line will not prevent or cause a level 8 
    trip. The failure of Feedwater/Main Turbine channel ``C'' trip 
    channel will not have any impact on the RCIC system nor Feedwater/
    Main Turbine channels ``A'' & ``B'', because the added signal is 
    isolated by a safety-related relay. The 2 out of 3 logic for the 
    trip is maintained.
        In addition, the changes to the action statements of the 
    specification do not allow a condition that could cause the 
    actuation instrumentation to fail in a different manner.
        Based on the above, the proposed change will not create the 
    possibility of a new or different kind [of accident] from any 
    accident or transient previously evaluated.
        (3) Involve a significant reduction in the margin of safety 
    because:
        The proposed TS change will not prevent tripping of Feedwater/
    Main Turbine or cause false trips. The existing 2 out of 3 logic 
    trip is maintained and does not affect existing failure modes or 
    introduce new failure modes. This change will prevent failure of 
    level 8 trip of Feedwater Pumps and Main Turbine upon loss of common 
    variable water leg for Reactor Vessel Water Level-High, Level 8, 
    instrument channels ``B'' & ``C'' and will slightly increase 
    reliability of the trip logic. Failure of the non-safety-related 
    trip logic will not impact any safety-related system, structure, or 
    component.
        The changes to the TS LCO Action statements is consistent with 
    the existing actions, while minimizing the time that automatic trip 
    capability is not maintained. The change from 72 hours allowed 
    operation with one channel Operable and only one channel tripped to 
    7 days is consistent with the current allowed outage time for only 
    one channel inoperable and not tripped, so any change to the margin 
    of safety provided by the current action requirements is minor.
        Based on the above, the proposed TS change does not involve a 
    significant reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    
    [[Page 33121]]
    
    
    Commonwealth Edison Company, Docket Nos. 50-254 and 50-265, Quad Cities 
    Nuclear Power Station, Units 1 and 2, Rock Island County, Illinois
    Date of amendment request: May 1, 1997
    
        Description of amendment request: This request changes Technical 
    Specification (TS) Surveillance Requirement (SR) 4.9.A.8.b by 
    clarifying the load value for the emergency diesel generator to be 
    equal to or greater than the largest single load and revise the 
    frequency and voltage requirements during performance of the test.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because of the 
    following:
        The proposed changes represent a clarification of the intent of 
    the performance of the largest single emergency load rejection 
    surveillance for the diesel generator. These changes allow for 
    simulated testing that will more closely duplicate actual emergency 
    loading conditions. By removing the specific load value requirement 
    from the surveillance, the test can be performed using the actual 
    largest load in the same plant configuration that would exist during 
    an actual accident scenario. Verification of the steady-state 
    voltage and frequency within the required time limits provides 
    confidence that the diesel generator can successfully recover from 
    this transient. This provides greater assurance that the diesel 
    generator is capable of performing its intended design function 
    during an accident and the subsequent recovery. The changes to the 
    surveillance requirement will not significantly increase the 
    consequences of an accident previously evaluated.
        The diesel generator's design function is to mitigate the 
    consequences of an accident by providing an independent onsite 
    source of alternate AC power with the capacity for operation of 
    systems required to shutdown the reactor and maintain it in a safe 
    shutdown condition until offsite power is restored. The diesel 
    generator and its associated subsystems are not assumed in any 
    safety analysis to initiate any accident sequence for Quad Cities 
    Station; therefore, the probability of an accident previously 
    evaluated is not increased by the proposed amendment.
        (2) Create the possibility of a new or different kind of 
    accident from any accident previously evaluated because:
        The proposed changes do not create the possibility of a new or 
    different kind of accident previously evaluated for Quad Cities 
    Station. The changes revise the largest single emergency load 
    rejection surveillance test acceptance criteria for the diesel 
    generator. This load rejection transient for the diesel generator is 
    bounded by a previously performed accident analysis. This analysis 
    assumes the loss of one diesel generator due to loss of 125 VDC 
    control power for the duration of a LOCA combined with a LOOP. The 
    diesel generator's design function is to mitigate the consequences 
    of an accident by providing an independent onsite source of 
    alternate AC power with the capacity for operation of systems 
    required to shutdown the reactor and maintain it in a safe shutdown 
    condition until offsite power is restored. Only one diesel generator 
    is required to perform this function per unit. Performance of the 
    Surveillance Requirement as proposed provides greater assurance that 
    the diesel generator is capable of performing its intended design 
    function during an accident and the subsequent recovery. No 
    significant changes to existing testing or new modes of facility 
    operation are proposed by this change. The proposed changes maintain 
    at least the present level of operability. Therefore, the proposed 
    changes do not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        (3) Involve a significant reduction in the margin of safety 
    because:
        The proposed amendment is required to ensure the diesel 
    generator is tested in accordance with the design basis 
    requirements. The changes represent a revision to the test 
    acceptance criteria for performance of the largest single emergency 
    load rejection surveillance for the diesel generator. This is a 
    possible transient for the diesel generator that is bounded by a 
    previously performed accident analysis. The proposed changes do not 
    adversely affect the capability of the diesel generator to perform 
    its design function. This function is to mitigate the consequences 
    of an accident by providing an independent onsite source of 
    alternate AC power with the capacity for operation of systems 
    required to shutdown the reactor and maintain it in a safe shutdown 
    condition until offsite power is restored. Performance of the 
    Surveillance Requirement as proposed provides greater assurance that 
    the diesel generator is capable of performing its intended design 
    function during an accident and the subsequent recovery. Existing 
    plant safety margins or the reliability of the equipment assumed to 
    operate in the safety analysis are not changed. The proposed changes 
    have been evaluated at Quad Cities and found to be acceptable for 
    use based on system design, safety analysis requirements and 
    operational performance. Since the changes maintain the necessary 
    levels of system reliability, the proposed changes do not involve a 
    significant reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Dixon Public Library, 221 
    Hennepin Avenue, Dixon, Illinois 61021.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    Date of amendment request: May 27, 1997.
    
        Description of amendment request: The proposed amendments would 
    delete from the Technical Specifications (TS) of each unit the 
    specified minimum volume of borated water available to the Standby 
    Makeup Pump; the minimum volume is already specified in other parts of 
    the TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Will the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        No. This amendment to the Catawba TS maintains the necessary 
    minimum volume of borated water available to mitigate a design basis 
    SSS [standby shutdown system] event through a 72 hour period. 
    Eliminating TS Surveillance 4.7.13.3a.2 does not increase the 
    probability or consequences of any previously evaluated accident, 
    since an adequate borated water source for the SMP [standby makeup 
    pump] is continued to be required by other existing TS.
        (2) Will the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        No. This amendment to the Catawba TS continues to ensure that 
    the necessary minimum volume of borated water is available to 
    mitigate an SSS event. The SSS is required to mitigate certain 
    previously evaluated design basis fire, security, and other events. 
    This amendment does not create the possibility of a new or different 
    kind of accident from any accident previously evaluated. This 
    amendment changes the TS applicable to an accident mitigating 
    function and does not impact any accident initiator, either new, 
    different, or previously evaluated.
        (3) Will the change involve a significant reduction in a margin 
    of safety?
        No. This amendment continues to ensure that the necessary 
    minimum volume of borated water is available to mitigate an SSS 
    design basis event. The available minimum volume is maintained well 
    above the design basis requirement. Since the source of borated 
    water that is available to supply the SMP continues to be controlled 
    by existing TS (TS 3.7.13.3a.1 and 3.9.10), which both envelope the 
    current 112,320 gallons, sufficient volume has been and will 
    continue
    
    [[Page 33122]]
    
    to be present to meet design basis requirements. Therefore, no 
    reduction in a margin of safety will result from the changes 
    proposed in this amendment.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730.
        Attorney for licensee: Mr. Paul R. Newton, Legal Department 
    (PB05E), Duke Power Company, 422 South Church Street, Charlotte, North 
    Carolina 28242-0001.
        NRC Project Director: Herbert N. Berkow.
    
    Duke Power Company, et al., Docket No. 50-414, Catawba Nuclear Station, 
    Unit 2, York County, South Carolina
    Date of amendment request: May 27, 1997
    
        Description of amendment request: The proposed amendment would 
    delete from the Technical Specification of Unit 2 requirements 
    regarding steam generator tube sleeving and repair. These requirements 
    are not applicable to the Westinghouse Model D5 steam generators used 
    by Unit 2.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Will the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        No. This amendment to the Catawba Unit 2 Technical 
    Specifications will have no impact on operation of the facility 
    since the change will delete steam generator repair methods that are 
    not applicable to the Catawba Unit 2 steam generators and have not 
    been used to repair the Catawba Unit 2 steam generators.
        (2) Will the change create the possibility of a new or different 
    type of accident from any accident previously evaluated?
        No. This amendment will delete steam generator repair methods 
    that are not applicable and have not been used. Therefore, the 
    proposed changes will not create the possibility of a new or 
    different accident.
        (3) Will the change involve a significant reduction in the 
    margin of safety?
        No. This amendment will delete steam generator repair methods 
    that are not applicable and have not been used. There will be no 
    impact on safety margins as a result of these changes.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730.
        Attorney for licensee: Mr. Paul R. Newton, Legal Department 
    (PB05E), Duke Power Company, 422 South Church Street, Charlotte, North 
    Carolina 28242.
        NRC Project Director: Herbert N. Berkow.
    
    Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf Nuclear 
    Station, Unit 1, Claiborne County, Mississippi.
    Date of amendment request: May 7, 1997.
    
        Description of amendment request: The amendment request would 
    eliminate selected response time testing (RTT) surveillance 
    requirements (SRs) from the Technical Specifications (TSs) for certain 
    components of the following systems: reactor protection system (SR 
    3.3.1.1.15), primary containment and drywell isolation instrumentation 
    (SR 3.3.6.1.8), and emergency core cooling system (SRs 3.5.1.8 and 
    3.5.2.7).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. No significant increase in the probability or consequences of 
    an accident previously evaluated results from this change.
        The purpose of the proposed Technical Specification (TS) change 
    is to eliminate response time testing (RTT) requirements for 
    selected components in the Reactor Protection System (RPS), Primary 
    Containment and Drywell Isolation Instrumentation, and Emergency 
    Core Cooling System (ECCS) actuation instrumentation. The Boiling 
    Water Reactor Owners' Group (BWROG) has completed an evaluation 
    which demonstrates that [RTT] is redundant to the other TS-required 
    testing. These other tests, in conjunction with actions taken in 
    response to NRC Bulletin 90-01, ``Loss of Fill-Oil in Transmitters 
    Manufactured by Rosemount,'' and Supplement 1 [to the bulletin], are 
    sufficient to identify failure modes or degradations in instrument 
    response time and ensure operation of the associated systems within 
    acceptable limits. There are no known failure modes that can be 
    detected by [RTT] that cannot also be detected by the other TS-
    required testing. This evaluation was documented in NEDO-32291-A, 
    ``System Analyses for Elimination of Selected Response Time Testing 
    Requirements,'' October 1995. EOI [The licensee] has confirmed the 
    applicability of this evaluation to Grand Gulf Nuclear Power Station 
    (GGNS). In addition, EOI will complete the actions identified in the 
    NRC staff's Safety Evaluation of NEDO-32291-A.
        Elimination of [ECCS] RTT during MODES 4 and 5 [(i.e., cold 
    shutdown and refueling, respectively)] is acceptable since there are 
    no design basis accidents in MODES 4 and 5 for which the ECCS High 
    Pressure Core Spray (HPCS) system is required to initiate within a 
    specified period of time. The requirement to maintain [ECCS] 
    OPERABLE during Modes 4 and 5 is preserved in the affected Technical 
    Specification. The ECCS RTT required by SR 3.5.1.8 (applicable 
    during MODES 1, 2, and 3, [or power operation, startup, and hot 
    shutdown, respectively]) is adequate to identify any operability 
    problems with the ECCS HPCS system. In addition, during MODES 4 and 
    5, the probability and consequences of accidents are reduced due to 
    the pressure and temperature limitations of these MODES.
        Because of the continued application of other TS-required tests 
    such as channel calibrations, channel checks, channel functional 
    tests, and logic system functional tests, the response time of these 
    systems [listed in the first paragraph] will be maintained within 
    the acceptance limits assumed in the plant [(GGNS)] safety analyses 
    and required for successful mitigation of an initiating event. The 
    proposed changes do not affect the capability of the associated 
    systems to perform their intended function within their required 
    response time, nor do the proposed changes themselves affect the 
    operation of any equipment.
        As a result, EOI has concluded that the proposed changes do not 
    involve a significant increase in the probability or the 
    consequences of an accident previously evaluated.
        2. This change would not create the possibility of a new or 
    different kind of accident from any [accident] previously evaluated.
        The proposed changes only apply to the testing requirements for 
    the components [in the systems] identified above and do not result 
    in any physical change to these or other components [in other 
    systems] or their operation. As a result, no new failure modes are 
    introduced. Therefore, the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. This change would not involve a significant reduction in a 
    margin of safety.
        The current TS-required response times are based on the minimum 
    allowable values assumed in the plant [(GGNS)] safety analyses. 
    These analyses conservatively establish the margin of safety. As 
    described above, the proposed changes do not affect the capability 
    of the associated systems to perform their intended function within 
    the allowable response time used as the basis for the plant safety 
    analyses. The potential failure modes for the components within the 
    scope of this request were evaluated for
    
    [[Page 33123]]
    
    impact on instrument response time. This evaluation confirmed that, 
    with the exception of loss of fill-oil of Rosemount transmitters, 
    the remaining TS-required testing is sufficient to identify failure 
    modes or degradations in instrument response times and ensure 
    operation of the instrumentation within the scope of this request is 
    within acceptable limits. The actions taken in response to NRC 
    Bulletin 90-01 and Supplement 1 [to the bulletin] are adequate to 
    identify loss of fill-oil failures of Rosemount transmitters. As a 
    result, it has been concluded that plant and system response to an 
    initiating event will remain in compliance with the assumptions of 
    the [GGNS] safety analysis. Elimination of RTT for ECCS HPCS system 
    in MODES 4 and 5 does not reduce the margin of safety since there 
    are no design basis events in MODES 4 and 5 requiring this system to 
    respond in [a] specified period of time from onset of the event. 
    Response time testing required by SR 3.5.1.8 (applicable during 
    MODES 1, 2, and 3) is adequate to identify any equipment or 
    operability concerns).
        Further, although not explicitly evaluated, the proposed changes 
    will provide an improvement to plant safety and operation by 
    reducing the time safety systems are unavailable, reducing the 
    potential for inadvertent safety system actuation, reducing plant 
    shutdown risk, limiting radiation exposure to plant personnel [that 
    would be due to the RTT], and eliminating the diversion of key 
    personnel resources to conduct unnecessary testing. Therefore, EOI 
    concluded that this request will result in an overall increase in 
    the margin of safety.
    
    [Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.]
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502.
        NRC Project Director: William D. Beckner.
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    Date of amendment request: May 24, 1997.
    
        Description of amendment request: The proposed amendment will 
    modify Technical Specification (TS) 3/4.7.4, Ultimate Heat Sink (UHS), 
    Table 3.7-3, by incorporating more restrictive dry cooling tower (DCT) 
    fan requirements, and it will change the wet cooling tower water 
    consumption in the TS Bases. This proposed amendment seeks to modify 
    the TS to be consistent with revised design basis calculations.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: No.
        The proposed change modifies the UHS TS by not allowing 
    operation with less than 12 DCT fans per DCT. This change is 
    necessary to adequately preserve the assumptions and limits of the 
    revised UHS design basis calculations. These calculations conclude 
    that the UHS is capable of dissipating the maximum peak heat load 
    resulting from the limiting design bases accident (i.e., large break 
    LOCA [large break loss of coolant accident]). The proposed change 
    does not directly affect any material condition of the plant that 
    could directly contribute to causing an accident or that could 
    contribute to the consequences of an accident. The proposed change 
    ensures that the mitigating effects of the UHS will be consistent 
    with the design basis analysis. Therefore, the proposed change will 
    not involve a significant increase in the probability or 
    consequences of any accident previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different type of 
    accident from any accident previously evaluated?
        Response: No.
        The proposed change modifies the UHS TS to be consistent with 
    revised design basis calculations. The UHS TS is being modified to 
    eliminate operation with less than 12 DCT fans per DCT. The proposed 
    change will not alter the operation of the plant or the manner in 
    which the plant is operated. Therefore, the proposed change will not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: No.
        The proposed change modifies the UHS TS by not allowing 
    operation with less than 12 DCT fans per DCT. The proposed change 
    preserves the margin of safety by ensuring that the UHS will be 
    capable of dissipating the maximum design basis accident heat load 
    with adequate margin. Therefore, the proposed change will not 
    involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502.
        NRC Project Director: William D. Beckner.
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    Date of amendment request: May 24, 1997
    
        Description of amendment request: The proposed amendment will 
    modify Technical Specifications (TS) 3.1.1.1, 3.1.1.2, 3.10.1 and 
    Figure 3.1-1 by removing the cycle dependent boron concentration and 
    boration flow rate from the Action Statements and removing the ``RWSP 
    at 1720 ppm'' curve from the figure. A change to TS Bases 3/4.1.1.1 and 
    3/4.1.1.2 has been included to support this change.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: No.
        The Shutdown Margin requirements are determined by the reload 
    analysis performed every cycle. The Cycle 9 reload analysis has 
    determined that the current Shutdown Margin requirements are 
    acceptable. The proposed change eliminates the reference to 1720 ppm 
    in the Action Statement because 1720 is not adequate to ensure that 
    the Shutdown Margin requirements are met at the beginning of cycle. 
    The proposed Action Statement will continue to ensure that in the 
    event the Shutdown Margin requirements are not met, boration will be 
    immediately initiated to restore the Shutdown Margin to within 
    limits.
        Therefore, the proposed change will not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different type of 
    accident from any accident previously evaluated?
        Response: No.
        The proposed change does not change the design or configuration 
    of the plant nor does it change how boration systems are operated 
    during normal or accident conditions. It
    
    [[Page 33124]]
    
    ensures that the Shutdown Margin requirements for accidents already 
    evaluated are promptly restored in the event that the requirements 
    are not met.
        Therefore, the proposed change will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: No.
        The proposed change has not decreased the amount of Shutdown 
    Margin required. The current Shutdown Margin requirements have been 
    validated by the Reload Analysis for Cycle 9 and are adequate to 
    ensure that the reactor can be made subcritical from all operating 
    conditions, transients, and design basis events. The proposed change 
    ensures that the Shutdown Margin requirements are promptly restored 
    in the event that they are not met. As such, the proposed change 
    ensures that the current margin of safety is maintained.
        Therefore, the proposed change will not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502.
        NRC Project Director: William D. Beckner.
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    Date of amendment request: June 3, 1997
    
        Description of amendment request: The proposed amendment requests a 
    change to the ACTION Requirements for Technical Specification 3/4.3.2 
    for the Safety Injection System Sump Recirculation Actuation Signal 
    (RAS). The proposed change will revise the allowed outage time for a 
    channel of RAS to be in the tripped condition from ``prior to entry 
    into the applicable MODE(S) following the next COLD SHUTDOWN'' to the 
    more restrictive time limit of 48 hours and adds a shutdown 
    requirement. Additionally, the 3.0.4 exemption is being removed from 
    the ACTION for the tripped condition. A change to the Technical 
    Specification Basis Section 3/4.3.2 has also been included.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: No.
        The proposed revision to the TS changes the allowed outage time 
    that a channel of RAS can be in the tripped condition from a maximum 
    of approximately 18 months when one channel is inoperable and 92 
    days when two channels are inoperable to 48 hours. If a channel were 
    in the tripped condition and a single failure occurred (that of one 
    other channel of RAS), a premature [refueling water storage pool] 
    RWSP low level signal would be generated. During a Design Basis 
    Accident with a containment high pressure condition causing the RWSP 
    outlet check valves to seat, this single failure would prevent the 
    contents of the RWSP from being injected into the reactor coolant 
    system and possibly resulting in failure of both trains of 
    [Emergency Core Cooling System] ECCS and [Containment Spray] CS. 
    Additionally, this would cause the [Low Pressure Safety Injection] 
    LPSI pumps to stop. Reducing the time that a channel of RAS can be 
    placed in the tripped condition will reduce the probability of this 
    scenario occurring during a Design Basis Accident. Since the allowed 
    outage time for a channel of RAS is being limited to 48 hours, this 
    is considered an off-normal operation and a single failure is not 
    required to be postulated during a Design Basis Accident in the 
    accident analysis. Reducing the time the channel can be placed in 
    the tripped condition and thus, the exposure time to this scenario, 
    would not be an accident initiator. The proposed change of being 
    more conservative in the time and condition limits in the TS will 
    not affect the assumptions, design parameters, or results of any 
    accident previously evaluated.
        Therefore, the proposed change will not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different type of 
    accident from any accident previously evaluated?
        Response: No.
        The proposed change does not change the design or configuration 
    of the plant. The proposed change provides a more conservative 
    allowed outage time for the channel to be in the tripped condition. 
    There has been no physical change to plant systems, structures or 
    components nor will the proposed change reduce the ability of any of 
    the safety-related equipment required to mitigate Anticipated 
    Operational Occurrences or accidents. In fact, this change will 
    potentially increase the ability of safety related equipment to 
    perform its functions. The configuration required by the proposed 
    specification is permitted by the existing specification.
        Therefore, the proposed change will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: No.
        The proposed change provides a more conservative allowed outage 
    time for the channel to be in the tripped condition. By reducing the 
    allowed outage time, the probability is reduced that a single 
    failure (that of a failure of one channel of RAS with one channel in 
    the tripped condition) would occur that would cause the suction to 
    be prematurely supplied by the Safety Injection System Sump, 
    potentially disabling the [High Pressure Safety Injection] HPSI and 
    CS pumps, and stopping of the LPSI pumps. Therefore, the only change 
    to the margin of safety would be an increase. Since the allowed 
    outage time for a channel of RAS is being limited to 48 hours, this 
    is considered an off-normal operation and a single failure is not 
    required to be postulated during a Design Basis Accident in the 
    accident analysis. The proposed changes do not affect the limiting 
    conditions for operation or their bases.
        Therefore, the proposed change will not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502.
        NRC Project Director: William D. Beckner.
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, Linn 
    County, Iowa
    Date of amendment request: May 9, 1997
    
        Description of amendment request: The proposed amendment would 
    revise the definitions of Limiting Safety System Setting (LSSS) and 
    Instrument/Channel Calibration to reference a new program being added 
    to the Technical Specification (TS) (Section 6.13) for the control of 
    instrument setpoints.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards
    
    [[Page 33125]]
    
    consideration, which is presented below:
    
        1. The proposed TS amendment will not significantly increase the 
    probability or consequences of any previously-evaluated accidents.
        The proposed changes will not result in any direct hardware 
    changes. The change only adds a program to the TS for the 
    establishment and control of instrumentation setpoints that is 
    consistent with current DAEC [Duane Arnold Energy Center] practice. 
    The Instrument Setpoint Control Program is based upon a methodology 
    for the calculation of instrument setpoints that conforms to the 
    guidelines of Regulatory Guide 1.105, Rev. 2. The methodology 
    ensures that adequate margin exists between the normal plant 
    operating conditions and actual instrument setpoints to preclude 
    spurious plant/equipment trips. As a result, the proposed program 
    establishes the criteria for changes in instrument setpoints to 
    ensure that such changes will not result in unnecessary plant 
    transients. Consequently, the probability of any previously-analyzed 
    event is not increased by this change.
        The role of the instrumentation and their associated setpoints 
    is in detecting and mitigating plant events and thereby limiting the 
    consequences of any previously-analyzed event. The LSSS[NTSP] and 
    corresponding LTPO[AV] have been developed in accordance with the 
    DAEC Instrument Setpoint Control Program criteria to ensure that the 
    instrumentation remains capable of mitigating events as described in 
    the safety analyses and that the results and consequences described 
    in the safety analyses remain bounding. Therefore, these changes do 
    not involve a significant increase in the consequences of an 
    accident previously evaluated.
        2. The proposed changes will not create a new or different kind 
    of accident from those previously evaluated.
        The proposed changes will not change the method or manner of 
    plant operation, in particular, calibration of TS-required 
    instrumentation. The use of the proposed TS program for the control 
    of changes to instrument setpoints does not impact safe operation of 
    the DAEC in that the design and safety analysis limits will continue 
    to be satisfied. The proposed TS program involves no system 
    additions or physical modifications, other than setpoint changes. 
    Any setpoint changes must conform to the criteria set forth in the 
    TS Instrument Setpoint Control Program. The instrument setpoints are 
    developed using a methodology that conforms to the guidelines 
    contained in Regulatory Guide 1.105, Rev. 2 to ensure the affected 
    instrumentation remains capable of mitigating accidents and 
    transients. Since operational methods remain unchanged and the 
    instrument setpoints have been evaluated to maintain the plant 
    within existing design basis criteria, no new or different type of 
    accident is created.
        3. The proposed change will not result in a significant 
    reduction in any margin of safety.
        The proposed TS program establishes the DAEC Instrument Setpoint 
    Control Program, which is based upon an NRC-approved methodology. 
    The program establishes the controls and criteria used to establish 
    and revise instrument setpoints. The setpoint calculations use the 
    uncertainties associated with the DAEC instrumentation and actual 
    DAEC physical data and operating practices to ensure the validity of 
    the resulting LTPO[AV] and LSSS[NTSP]. The methodology is based upon 
    combining the uncertainties of the associated channels and takes 
    into account calibration accuracy, instrument uncertainties, drift, 
    etc. The use of this methodology for establishing these setpoints 
    ensures that the design and/or safety analysis limits are not 
    exceeded in any transient or accident. Therefore, the proposed 
    change does not involve a significant reduction in the margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, SE., Cedar Rapids, Iowa 52401.
        Attorney for licensee: Jack Newman, Al Gutterman, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036-5869.
        NRC Project Director: Gail H. Marcus.
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, Linn 
    County, Iowa
    Date of amendment request: May 9, 1997
    
        Description of amendment request: The proposed amendment would 
    revise the definition of Limiting Condition for Operation (LCO) to 
    address the situation when systems, components, etc., are removed from 
    service or otherwise made inoperable during secondary modes of 
    operation, without requiring entry into the LCO actions.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed TS amendment will not significantly increase the 
    probability or consequences of any previously evaluated accidents.
        The proposed change merely adds criteria to the TS that are 
    consistent with the original design and licensing basis assumptions. 
    Operation in secondary modes of operation (such as surveillance 
    testing, torus cooling mode (test line-up) or Residual Heat Removal 
    system, and use of High Pressure Coolant Injection system or Reactor 
    Core Isolation Cooling system in test line-up for reactor pressure 
    control during transients) is assumed in the safety analysis report 
    (Ref. UFSAR Section 6.3.4.2.1 and 7.3.4.2). Because no changes in 
    actual equipment operation or testing are being made as part of this 
    change, the probability of any event which could be induced by such 
    operation or testing is not increased. Also, the change will ensure 
    that the time such equipment is removed from service is kept very 
    short in duration, either through existing TS Allowed Outage Time 
    (AOT) notes or administratively by procedures. This is consistent 
    with the assumption that the time in such secondary modes of 
    operation (i.e., safe test interval) is much shorter than the 
    allowable repair time (i.e., LCO time). Therefore, the proposed 
    change will not significantly increase the probability of any 
    previously evaluated accident.
        The uniform application of the new TS criteria will further 
    ensure that the plant remains within the original design and 
    licensing basis assumptions for equipment removed from service 
    during secondary modes of operation. In particular, in the special 
    case where testing also removes the redundant system, train, 
    component, etc., from service, these criteria ensure that both 
    affected systems, trains, etc., are properly controlled. This is 
    acceptable because the time in such secondary modes of operation is 
    very short in duration, such that the impact on the overall 
    availability/reliability is insignificant. Therefore, the 
    consequences of any previously analyzed accident are not 
    significantly increased by this change.
        2. The proposed changes will not create a new or different kind 
    of accident from those previously evaluated.
        The proposed changes will not add a new or different kind of 
    accident because the plant will not be operated in a different way. 
    Operation in secondary modes has been previously evaluated and found 
    to be acceptable (Ref. General Electric reports APED-5736: Guideline 
    for Determining Safe Test Intervals and Repair Times for Engineered 
    Safeguards, and NEDO-10739: Methods for Calculating Safe Test 
    Intervals and Allowable Repair Times for Engineered Safeguard 
    Systems). The proposed change merely adds criteria to the TS that 
    are consistent with the assumptions contained within these 
    evaluations. Consequently, no new or different accidents are 
    postulated as a result of this proposed change.
        3. The proposed change will not result in a significant 
    reduction in any margin of safety.
        Because the criteria being added to the TS enforce the 
    assumptions of the evaluations that form the basis of the existing 
    TS (Ref. TS Bases 4.1, 4.2, and 3.5), the proposed change will not 
    result in a significant reduction in any margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cedar Rapids Public Library,
    
    [[Page 33126]]
    
    00 First Street, SE., Cedar Rapids, Iowa 52401.
        Attorney for licensee: Jack Newman, Al Gutterman, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036-5869.
        NRC Project Director: Gail H. Marcus.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald 
    C. Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan
    Date of amendment requests: December 20, 1996
    
        Description of amendment requests: The proposed amendments would 
    reduce the frequency and scope of reactor coolant pump flywheel 
    inspections.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        We have evaluated the proposed T/S changes and have determined 
    they do not represent a significant hazards consideration based on 
    the criteria established in 10 CFR 50.92(c). Operation of Cook 
    Nuclear Plant in accordance with the proposed amendment will not:
        1. Involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        This change will reduce the frequency and scope of the 
    surveillance testing on the reactor coolant pump flywheels. 
    Operating power plants have been inspecting their flywheels for over 
    20 years with no flaws identified which affect flywheel integrity. 
    Past examinations performed to satisfy T/S 4.4.10.1 have not 
    revealed any cracking of flywheel plates at Cook Nuclear Plant. 
    Crack extension over a 60 year service life is negligible. 
    Structural reliability studies have shown that eliminating 
    inspections after 10 years of plant life will not significantly 
    change the probability of failure. Most flaws which could lead to 
    failure would be detected during preservice inspection or, at worst, 
    early in plant life, and crack growth over plant life is negligible. 
    As stated in the SER associated with WCAP-14535, assuming an initial 
    crack of 10% of the distance from the keyway to the flywheel outer 
    radius and a maximum fatigue crack growth, ASME margins would be 
    maintained during the 10-year inspection period. Therefore, the 
    change in test frequency will not endanger public health or safety. 
    For these reasons, it is our belief the proposed changes do not 
    involve a significant increase in the probability or consequences of 
    a previously evaluated accident.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The changes will not introduce any new modes of plant operation, 
    nor will any physical changes to the plant be required. Thus, the 
    changes will not create the possibility of a new or different kind 
    of accident from any accident previously analyzed or evaluated.
        3. Involve a significant reduction in a margin of safety.
        This change will reduce the frequency and scope of the 
    surveillance testing on the reactor coolant pump flywheels. 
    Operating power plants have been inspecting their flywheels for over 
    20 years with no flaws identified which affect flywheel integrity. 
    Past examinations performed to satisfy T/S 4.4.10.1 have not 
    revealed any cracking of flywheel plates at Cook Nuclear Plant. 
    Crack extension over a 60 year service life is negligible. 
    Structural reliability studies have shown that eliminating 
    inspections after 10 years of plant life will not significantly 
    change the probability of failure. Most flaws which could lead to 
    failure would be detected during preservice inspection or at worst 
    early in plant life, and crack growth over plant life is negligible. 
    As stated in the SER associated with WCAP-14535, assuming an initial 
    crack of 10% of the distance from the keyway to the flywheel outer 
    radius and a maximum fatigue crack growth, ASME margins would be 
    maintained during the 10-year inspection period. For these reasons, 
    it is our belief the proposed changes do not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Gail H. Marcus.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile Point 
    Nuclear Station, Unit 2, Oswego County, New York
    Date of amendment request: April 30, 1997
    
        Description of amendment request: The proposed amendment would 
    remove Technical Specifications (TSs) regarding meteorological 
    monitoring instrumentation in accordance with NRC Generic Letter (GL) 
    95-10, ``Relocation of Selected Technical Specification Requirements 
    Related to Instrumentation.'' Specifically, the amendment would delete 
    TS 3/4.3.7.3, ``Meteorological Monitoring Instrumentation,'' including 
    associated TS Tables 3/4.3.7.3-1, and TS Bases 3/4.3.7.3. The TS Index 
    would be revised to show these deletions. The deletion of TS 3.3.7.3 
    would also eliminate the requirement that a Special Report to be 
    submitted to the NRC pursuant to TS 6.9.2 when one or more 
    meteorological monitoring instrumentation channels is inoperable for 
    more than 7 days. The licensee states that the deleted requirements 
    would be relocated to the Updated Safety Analysis Report (USAR), except 
    that the special reporting requirement would be discontinued as the 
    licensee would continue to evaluate future inoperability of 
    meteorological instrumentation for reportability in accordance with 10 
    CFR 50.72 and 10 CFR 50.73. The licensee will also insert the word 
    ``nominal'' in the relocated tables in the USAR to indicate that the 
    meteorological instrumentation elevations of 30 and 200 feet are 
    nominal elevations (this change would be made because, as the licensee 
    reported in LER 96-14, the actual locations of the air temperature 
    monitoring instruments are 26.8 feet and 194.8 feet and the actual 
    locations of the wind indicator (speed and direction) monitoring 
    instruments are 30.9 feet and 199.4 feet). As stated in GL 95-10, the 
    NRC staff has determined that meteorological monitoring instrumentation 
    does not serve such a primary protective function as to warrant 
    inclusion in the TS in accordance with 10 CFR 50.36 criteria. Thus, in 
    GL 95-10, the NRC staff established that relocation of the 
    meteorological instrumentation requirements to the USAR (whereby 
    changes are controlled by the licensee pursuant to 10 CFR 50.59) is 
    acceptable.
        Basis for proposed no significant hazards consideration 
    determination:
        As required by 10 CFR 50.91(a), the licensee has provided its 
    analysis of the issue of no significant hazards consideration, which is 
    presented below:
    
        1. The operation of Nine Mile Point Unit 2 [NMP2], in accordance 
    with the proposed amendment, will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The NMP2 meteorological monitoring instrumentation is used to 
    provide data for use in radioactive dose assessment with respect to 
    routine or accidental releases of radioactive materials to the 
    atmosphere. The deletion of the special reporting requirements is an 
    administrative change. The subject special reporting requirements 
    serve no nuclear related protective function. The relocation of the 
    meteorological monitoring instrumentation requirements from the TSs 
    to the USAR, and the addition of the word nominal to the USAR and 
    tables, will not increase the probability of an accident since the 
    specification applies only to monitoring instrumentation. This also 
    is an administrative change and does not reduce the effectiveness of 
    the current instrumentation requirements. The meteorological 
    monitoring instrumentation
    
    [[Page 33127]]
    
    requirements are not precursors to any accident previously 
    evaluated. According to the NRC Staff (GL 95-10), the meteorological 
    monitoring instrumentation does not serve to ensure the plant is 
    operated within the bounds of initial conditions assumed in any 
    design basis accidents or transients previously evaluated, or that 
    the plant will be operated to preclude transients or accidents. In 
    addition, the meteorological monitoring instrumentation does not 
    function as part of the primary success path of a safety sequence 
    analysis used to demonstrate that the consequences of these events 
    are within the appropriate acceptance criteria. Therefore, the 
    proposed changes do not significantly increase the probability or 
    consequences of an accident previously evaluated.
        2. The operation of Nine Mile Point Unit 2, in accordance with 
    the proposed amendment, will not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        The proposed deletion of the special reporting requirements is 
    an administrative change. The subject special reporting requirements 
    serve no nuclear related protective function. The proposed change 
    also removes meteorological monitoring instrumentation 
    specifications from the NMP2 TSs. This also is an administrative 
    change and does not reduce the effectiveness of the current 
    instrumentation requirements. The relocation of the meteorological 
    instrumentation requirements to the USAR, and the addition of the 
    word nominal to the USAR and tables, will not create the possibility 
    of a new or different kind of accident since the specification only 
    applies to monitoring instrumentation. The NRC Staff has concluded 
    in GL 95-10 that the provisions of the meteorological monitoring 
    instrumentation specifications are not related to dominant 
    contributors to plant risk. The NMP2 meteorological instrumentation 
    is used to provide data for use in radioactive dose assessment with 
    respect to routine or accidental releases of radioactive materials 
    to the atmosphere. Since no physical modification to the plant is 
    being performed, and no changes to actual plant operations are 
    required by the change, removal of the specifications from the NMP2 
    TSs will not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        3. The operation of Nine Mile Point Unit 2, in accordance with 
    the proposed amendment, will not involve a significant reduction in 
    a margin of safety.
        The proposed deletion of the special reporting requirements is 
    an administrative change. The subject special reporting requirements 
    serve no nuclear related protective function. The proposed removal 
    of the instrumentation requirements from the NMP2 TSs is also an 
    administrative change and does not reduce the effectiveness of the 
    current instrumentation requirements. The relocation of the 
    meteorological instrumentation requirements to the USAR, and the 
    addition of the word nominal to the USAR and tables, will not 
    involve a reduction in a margin of safety since the specification 
    only applies to monitoring instrumentation. The instrumentation will 
    continue to meet the requirements of Regulatory Guide 1.23, and the 
    offsite dose calculations will continue to use the actual measured 
    elevation differences. In GL 95-10, the NRC Staff concluded (1) That 
    the meteorological monitoring instrumentation does not function as 
    part of the primary success path of a safety sequence analysis, and 
    (2) that the meteorological monitoring instrumentation 
    specifications are not related to dominant contributors to plant 
    risk. Therefore, the removal of the meteorological monitoring 
    instrumentation specifications from the NMP2 TSs will not result in 
    a significant reduction in any margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: Alexander W. Dromerick, Acting Director.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-245, Millstone 
    Nuclear Power Station, Unit No. 1, New London County, Connecticut
    Date of amendment request: May 15, 1997
    
        Description of amendment request: The proposed amendment would 
    revise Technical Specification Sections 3.1 and 4.1 ``Reactor 
    Protection System'' and the associated Bases to remove run mode 
    intermediate range monitor high flux/inoperative with the associated 
    average power range monitor downscale scram trip function and 
    incorporate editorial revisions.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The operation of Millstone Nuclear Power Station, Unit No. 1, 
    in accordance with the proposed amendment, will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        No physical change is being made to any systems or components 
    that are credited in the safety analysis, therefore there is no 
    change in the probability or consequences of any accident analyzed 
    in the UFSAR [Updated Final Safety Analysis Report].
        The design basis accident applicable to the startup power region 
    is the Control Rod Drop Accident (CRDA). The UFSAR does not credit 
    the RUN Mode IRM [intermediate range monitor] High Flux/Inoperative 
    with the associated APRM [average power range monitor] downscale 
    scram Trip Function (IRM RUN Mode SCRAM) in the termination of this 
    accident. Accident mitigation is provided by the APRM 120% power 
    scram. Therefore, elimination of the IRM RUN Mode SCRAM function has 
    no adverse affect on previously evaluated accidents.
        The Continuous Control Rod Withdrawal Error (CWE) transient is 
    terminated by the Rod Block Monitor (RBM) in the RUN Mode. The APRM 
    Reduced High Flux Scram provides the primary STARTUP Mode protection 
    in conjunction with the IRMs and limits the consequences of this 
    transient. Therefore, elimination of the IRM RUN Mode SCRAM function 
    has no effect on the consequences of this transient.
        Clarification of the LCO [limiting condition for operation] RPS 
    [reactor protection system] Table aligns requirements with Limiting 
    Safety System Settings. Further revisions to LCO 3.1 Reactor 
    Protection System Table 3.1.1 and associated TS [technical 
    specification] bases to clarify APRM Trip Functions do not alter the 
    required trip functions. Deletion of RUN requirement and associated 
    Action B for Reduced High Flux fixes an editorial error introduced 
    in a previous amendment. This trip function is not effective with 
    the mode switch in the RUN position and removal does not alter the 
    neutron monitoring requirements credited in the accident analyses.
        Adding a new surveillance to verify SRM [source range monitor]/
    IRM/APRM overlap will enhance neutron monitoring during startups and 
    shutdowns and does not have an adverse affect on previously 
    evaluated accidents.
        None of the proposed changes will affect any of the rod blocks 
    or other precursor events to either the CRDA or CWE. Therefore, 
    there is no change in the probability of any accident previously 
    analyzed.
        2. The operation of Millstone Nuclear Power Station, Unit No. 1, 
    in accordance with the proposed amendment, will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The proposed changes affect only the operations of neutron 
    monitoring and protective systems (IRM and APRM) which provide 
    indication and mitigation actions only. Operation of these systems 
    does not create the possibility for new precursors (such as 
    reactivity) which would introduce a new or different kind of 
    accident from any accident previously evaluated.
        Additionally, the proposed changes do not affect the ability of 
    those systems required to mitigate previously evaluated accidents 
    during the modes they are credited.
        3. The operation of Millstone Nuclear Power Station, Unit No. 1, 
    in accordance with the proposed amendment, will not involve a 
    significant reduction in a margin of safety.
        The only scram function that the UFSAR takes credit for in the 
    mitigation of the limiting accident (control rod drop accident) is 
    the APRM 120% power scram which is not
    
    [[Page 33128]]
    
    affected by this change. Only the IRM RUN Mode SCRAM, for which the 
    UFSAR takes no credit in the termination of any analyzed event, is 
    removed by this change. Removal of the IRM RUN Mode SCRAM will avoid 
    the need to operate the plant in a ``half scram'' condition with the 
    potential for an inadvertent plant transient. For these reasons, the 
    change does not involve a significant reduction in a margin of 
    safety.
        The Continuous Control Rod Withdrawal Error (CWE) transient is 
    terminated by the Rod Block Monitor (RBM) in the RUN Mode. When 
    initiated from the STARTUP Mode, the consequences of a CWE are 
    limited by the APRM Reduced High Flux scram in conjunction with the 
    IRM scram function. Therefore eliminating the TS requirement for the 
    IRM RUN Mode SCRAM will not reduce the margin of safety for this 
    transient.
        Clarification of the LCO RPS Table aligns requirements with 
    Limiting Safety System Settings. Further revisions to LCO 3.1 
    Reactor Protection System Table 3.1.1 and associated TS bases to 
    clarify APRM Trip Functions do not alter the required trip 
    functions. Deletion of the RUN requirement and associated Action B 
    for Reduced High Flux corrects an editorial error introduced in a 
    previous amendment. This trip function is not effective with the 
    mode switch in the RUN position and removal does not alter the 
    neutron monitoring requirements credited in the accident analyses.
        Adding a new surveillance to verify SRM/IRM/APRM overlap will 
    enhance neutron monitoring during startups and shutdowns and 
    consequently does not involve a significant reduction in a margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community--Technical College, 574 New London Turnpike, 
    Norwich, CT 06360, and the Waterford Library, ATTN: Vince Juliano, 49 
    Rope Ferry Road, Waterford, CT 06385.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Deputy Director: Phillip F. McKee.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, Millstone 
    Nuclear Power Station, Unit No. 2, New London County, Connecticut
    Date of amendment request: May 20, 1997
    
        Description of amendment request: This submittal supersedes the 
    January 22, 1996, submittal which was previously noticed on February 
    28, 1996 (61 FR 7554). The proposed change would relocate the 
    containment isolation valve (CIV) list, Table 3.6-2, from the Technical 
    Specifications to the Technical Requirements Manual (TRM). This change 
    would affect Technical Specification Sections 1.8.1.b, 4.6.1.1.a, 
    3.6.3.1, 4.6.3.1.1, and 4.6.3.1.2, and Basis Section 3/4.6.3. A note at 
    the bottom of Table 3.6-2 regarding the CIVs that are subject to 
    administrative controls is retained in the Technical Specifications by 
    relocating it to Sections 1.8.1.b and 3.6.3.1. This change is being 
    performed in accordance with Generic Letter 91-08, which provides 
    guidance for removal of component lists from the Technical 
    Specifications.
        Additionally, a change to provide relief in the surveillance 
    requirement in Section 4.6.1.1.a is included. The change allows valves, 
    blind flanges, and deactivated automatic valves located inside the 
    containment and are locked, sealed, or otherwise secured in the closed 
    position to be verified closed prior to entering Mode 4 from Mode 5, if 
    not performed within the previous 92 days. The current requirements 
    check the valve position once per 31 days.
        TS Bases Section 3/4.6.3 is updated to reflect the removal and 
    relocation of the CIV list to the TRM. Also, details of the 
    administrative controls for operating CIVs while in Modes 1 through 4 
    are added to Bases Section 3/4.6.3.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change to relocate the containment isolation valve 
    (CIV) list will not result in any hardware or equipment operating 
    changes. The proposed change is based on Generic Letter (GL) 91-08 
    and merely relocates the CIV table and removes all references to the 
    table. The relocation of the CIV table from the Technical 
    Specifications does not affect the operability requirements of any 
    of the listed valves. Technical Specifications will still continue 
    to require the CIVs to be operable. The LCO [limiting condition for 
    operation] and surveillance requirements for the valves will remain 
    in Technical Specifications. The CIV table will be relocated to the 
    Millstone Unit No. 2 Technical Requirements Manual (TRM), which is 
    controlled in accordance with 10 CFR 50.59. This change does not 
    alter the design, function, or operation of the valves involved. 
    Thus, there is no significant affect on the possibility or 
    consequences of any previously evaluated accident.
        The change to Surveillance Requirement (SR) 4.6.1.1.a will allow 
    the valves, blind flanges and deactivated automatic valves located 
    inside the containment that are locked, sealed, or otherwise secured 
    in the closed position to be verified closed prior to entering Mode 
    4 from Mode 5, if not performed within the previous 92 days, instead 
    of the current 31 day requirement. This means that the surveillance 
    interval could be as long as the entire operating cycle, depending 
    on whether entry into Mode 5 is required during the cycle. The 
    change in the surveillance frequency (increase in time from 31 days 
    to not less than 92 days and only prior to entering Mode 4 from Mode 
    5) recognizes that these valves are operated under administrative 
    controls and probability of misalignment is low. This provides 
    adequate assurance that the containment function assumed in the 
    accident analysis will be maintained. Therefore, there is no 
    significant affect on the probability or consequences of any 
    previously evaluated accident. This proposed change to SR 4.6.1.1.a 
    is consistent with NUREG-1432 Standard Technical Specifications for 
    Combustion Engineering Pressurized Water Reactors Revision 1 (SR 
    3.6.3.4).
        The information added to the Bases will provide additional 
    guidance to ensure the plant is operated correctly. This information 
    will not result in any new approaches to plant operation. Therefore, 
    there is not significant affect on the probability or consequences 
    of any previously evaluated accident.
        These proposed changes do not alter the design, function, or 
    operation of the valves involved. Therefore, there is no significant 
    increase in the probability or consequence of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The change to relocate the CIV list from the Technical 
    Specifications to the TRM will not impose any different operational 
    or surveillance requirements, nor will the change remove any such 
    requirements. Adequate control will be maintained. Furthermore, as 
    stated above, the proposed change does not alter the design, 
    function, or operation of the valves involved, and therefore does 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The change to SR 4.6.1.1.a reduces the surveillance frequency 
    for valves, blind flanges and deactivated automatic valves located 
    inside the containment. It does not alter the design, function, or 
    operation of the valves. Therefore, it does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The information added to the Bases will provide additional 
    guidance to ensure the plant is operated correctly. This information 
    does not alter the design, function, or operation of the valves 
    involved. Therefore, it does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes will not reduce the margin of safety since 
    they have no impact on any safety analysis assumption. The proposed 
    changes do not decrease the scope
    
    [[Page 33129]]
    
    of equipment currently required to be operable or subject to 
    surveillance testing, nor do the proposed changes affect any 
    instrument setpoints or equipment safety functions.
        The effectiveness of Technical Specifications will be maintained 
    since the change will not alter function or operability requirements 
    for any CIV. In addition, the relocation of the valve list is 
    consistent with the guidance provided in GL 91-08, and the change to 
    the surveillance interval is consistent with NUREG-0212 Standard 
    Technical Specifications for Combustion Engineering Pressurized 
    Water Reactors Revision 2 (LCO 3.6.1.1) and NUREG-1432 Standard 
    Technical Specifications for Combustion Engineering Pressurized 
    Water Reactors Revision 1 (LCO 3.6.3).
        The information added to the Bases is consistent with the 
    guidance provided in GL 91-08 and NUREG-1432 Standard Technical 
    Specifications for Combustion Engineering Pressurized Water Reactors 
    Revision 1. The intent of the Technical Specifications will be met 
    since this information will not result in any new approaches to 
    plant operation.
        Therefore, there is no significant reduction in a margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community--Technical College, 574 New London Turnpike, 
    Norwich, CT 06360, and the Waterford Library, ATTN: Vince Juliano, 49 
    Rope Ferry Road, Waterford, CT 06385.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Deputy Director: Phillip F. McKee.
    
    Northeast Nuclear Energy Company (NNECO), et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    Date of amendment request: May 9, 1997
    
        Description of amendment request: The proposed amendment would 
    revise the shutdown margin requirements and add Technical Specification 
    3/4.3.5 to provide the limiting condition for operation (LCO) and 
    surveillance requirements for the shutdown margin monitors. The 
    proposed amendment would also make administrative changes and revise 
    the associated Bases section.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        NNECO has reviewed the proposed changes in accordance with 10 
    CFR 50.92 and has concluded that the change does not involve a 
    significant hazards consideration (SHC). The bases for this 
    conclusion is that the three criteria of 10 CFR 50.92(c) are not 
    satisfied. The proposed changes do not involve [an] SHC because the 
    changes would not: 
        1. Involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        The proposed Technical Specification changes will revise the 
    current shutdown margin requirements for Modes 3, 4 and 5 in Figures 
    3.1-1, 3.1-2, 3.1-3, 3.1-4 and 3.1-5 and allow for additional 
    boration of the RCS [reactor coolant system] as directed by 
    Specification 3.3.5. The new Shutdown Margin requirements are based 
    on re-analyses of the Boron Dilution Event provided by Westinghouse. 
    In the re-analyses, assumptions were modified in order to justify 
    the operability of the Shutdown Margin Monitor for count rates which 
    are lower than currently allowed. The proposed Shutdown Margin 
    requirements for Modes 3, 4 and 5 will continue to assure that the 
    operator has a minimum of 15 minutes from the alarm to loss of 
    shutdown margin during an assumed Boron Dilution Event.
        The proposed change also adds Technical Specification 3/4.3.5 to 
    provide the LCO and Surveillance Requirements for the Shutdown 
    Margin Monitors. LCO 3.3.5 refers to the Core Operating Limits 
    Report (COLR) which will specify the minimum count rate/alarm ratio 
    requirements in order to consider the Shutdown Margin Monitors 
    operable. The LCO also directs the additional boration of the RCS in 
    order to allow the Shutdown Margin Monitors to be considered 
    operable for lower count rates. Also, a footnote (**) is included in 
    Specification 3/4.3.5 to make the Specification treatment of the 
    valves consistent with the Mode 6 and Mode 5-loops drained 
    requirements.
        Due to the addition of Technical Specification 3/4.3.5, the 
    related Bases information is added as BASES Section 3/4.3.5. 
    Additionally, the Bases information for the Shutdown Margin Monitors 
    which is currently in BASES Section 3/4.3.1 is moved to the added 
    BASES Section 3/4.3.5. This Bases information is also revised to be 
    consistent with the added Specification 3/4.3.5.
        Also, due to the addition of Technical Specification 3/4.3.5, 
    the guidance related to the Shutdown Margin Monitor in Tables 3.3-1 
    and 4.3-1 is deleted to avoid redundancy.
        Additionally, Section 3/4.1.2 of the Bases is revised so that it 
    refers to Figure 3.1-4 (Shutdown Margin for Mode 5/filled) instead 
    of Figure 3.1-5 (Shutdown Margin for Mode 5/drained). This change 
    will make the Bases consistent with the ACTION statement 
    requirements of Technical Specifications 3.1.2.2 and 3.1.2.6.
        Finally, Reference 12 (NUSCO-152, Addendum 4) is added to the 
    list of references in Section 6.9.1.6.b. The addition of this 
    reference is considered administrative and is not related to or 
    required by the changes proposed for the Shutdown Margin 
    requirements or Shutdown Margin Monitors.
        The new requirements for increased Shutdown Margin (Figures 3.1-
    1 to 3.1-5) and additional boration (LCO 3.3.5) continue to assure 
    that the operator will have a response time of at least 15 minutes 
    to mitigate the consequences of a Boron Dilution Event. The 
    implementation of the new requirements does not alter the alignment 
    of any plant equipment and therefore, the change cannot increase the 
    probability or consequences of any previously analyzed accident.
        The proposed changes will not adversely affect the assumptions 
    or results of other FSAR [Final Safety Analysis Report] accident 
    analysis and it is concluded that this change is safe. The changes 
    do not adversely affect any equipment credited in the safety 
    analysis.
        Based upon the re-analyses of the boron dilution event, revised 
    plant operating requirements (shutdown margin) are generated to 
    maintain the required operator action time. Therefore, there is no 
    effect on the probability of occurrence or consequences of 
    previously evaluated accidents.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequence of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed Shutdown Margin requirements for Modes 3, 4 and 5 
    (Figures 3.1-1 to 3.1-5 and additional boration as per Specification 
    3.3.5) will continue to assure that the operator has a minimum of 15 
    minutes from the alarm to loss of shutdown margin during an assumed 
    Boron Dilution Event. Additionally, the use of these revised 
    requirements allows the Shutdown Margin Monitor to be considered 
    operable for count rates which are lower than currently allowed.
        The changes do not introduce any new failure modes or 
    malfunctions since the changes implement revised, more conservative 
    plant operating requirements (shutdown margin) which are based on 
    re-analyses of the Boron Dilution Event. Also, the changes do not 
    eliminate any existing requirements.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed Shutdown Margin requirements for Modes 3, 4 and 5 
    (Figures 3.1-1 to 3.1-5 and additional boration as per Specification 
    3.3.5) will continue to assure that the operator has a minimum of 15 
    minutes from the alarm to loss of shutdown margin during an assumed 
    Boron Dilution Event. Additionally, the use of these revised 
    requirements allows the Shutdown Margin Monitor to be considered 
    operable for count rates...which are lower than currently allowed.
        The re-analyses of the Boron Dilution Event demonstrated that 
    the required
    
    [[Page 33130]]
    
    operator action time is maintained. As such, the re-analyses will 
    become the ``analysis of record'' for the Boron Dilution Event in 
    Modes 3, 4 and 5. The Boron Dilution Event analysis is documented in 
    FSAR Chapter 15.4.6.
        The re-analyses of the Boron Dilution Event and the proposed 
    revisions to the Technical Specifications do not adversely affect 
    the results of the current FSAR accident analysis and therefore, it 
    is concluded that this change is safe. Additionally, the change does 
    not adversely affect any equipment credited in the safety analysis.
        The changes do not have an adverse impact on the protective 
    boundaries and there is no reduction in the margin of safety as 
    specified in the Technical Specifications. Thus, this proposed 
    change does not involve a significant reduction in the margin of 
    safety.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        In conclusion, based on the information provided, it is 
    determined that the proposed changes do not involve an SHC.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Deputy Director: Phillip F. McKee.
    
    Northeast Nuclear Energy Company (NNECO), et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    Date of amendment request: May 14, 1997
    
        Description of amendment request: Technical Specification 
    Surveillance Requirement 4.8.2.1.c.4 requires that each battery charger 
    be tested to verify that it can supply a specified current at 125 
    volts. The proposed amendment would increase the required test voltage.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        NNECO has reviewed the proposed revision in accordance with 
    10CFR50.92 and has concluded that the revision does not involve a 
    significant hazards consideration (SHC). The basis for this 
    conclusion is that the three criteria of 10CFR50.92(c) are not 
    satisfied. The proposed revision does not involve [an] SHC because 
    the revision would not:
        1. Involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        The proposed changes to Technical Specification Surveillance 
    4.8.2.1.c.4 to increase the required test voltage for the battery 
    chargers from 125 volts to greater than or equal to 132 volts is 
    consistent with the design criteria of the chargers and performing 
    battery charger surveillance testing does not significantly increase 
    the probability of an accident previously evaluated. The proposed 
    changes to increase the required test voltage for the battery 
    chargers provides the necessary assurance that the battery chargers 
    will function as required in previous evaluations and does not 
    significantly increase the consequence of an accident previously 
    evaluated.
        Therefore, the proposed revision does not involve a significant 
    increase in the probability or consequence of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes to Technical Specification Surveillance 
    4.8.2.1.c.4 to increase the required test voltage for the battery 
    chargers from 125 volts to greater than or equal to 132 volts does 
    not change the operation of the battery chargers during normal or 
    accident evaluations.
        Therefore, the proposed revision does not create the possibility 
    or a new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed change to Technical Specification Surveillance 
    4.8.2.1.c.4 to increase the required test voltage for the battery 
    chargers from 125 volts to greater than or equal to 132 volts 
    provides assurance that the battery chargers are capable of 
    supplying the largest combined demands of the various steady state 
    loads, plus the current required to recharge its battery, which has 
    undergone a duty cycle discharge, to its fully charged condition in 
    less than 24 hours.
        Therefore, the proposed revision does not involve a significant 
    reduction in a margin of safety.
        In conclusion, based on the information provided, it is 
    determined that the proposed revision does not involve an SHC.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Deputy Director: Phillip F. McKee.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    Date of amendment request: March 3, 1997 as supplemented by letter 
    dated May 5, 1997. The May 5, 1997, supplement revised the proposed no 
    significant hazards consideration entirely
    
        Description of amendment request: The proposed changes to the Hope 
    Creek (HC) Technical Specifications (TSs) would: (1) Change TS 3/4.3.1, 
    ``Reactor Protection System Instrumentation,'' TS 3/4.3.2, ``Isolation 
    Actuation Instrumentation,'' and TS 3/4.3.3, ``Emergency Core Cooling 
    System Actuation Instrumentation'' to include additional information 
    concerning response time testing; (2) Change TS 4.0.5 to reference 
    inservice inspection and test requirements; (3) Change TS 3/4.6.1, 
    ``Primary Containment,'' and associated Bases to reflect a design 
    modification; (4) Change TS 3/4.7.7, ``Main Turbine Bypass System,'' to 
    specify a new operability requirement; and (5) Change the Bases for TS 
    3/4.8, ``Electrical Power Systems.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed changes for the TS related to response time testing 
    reflect testing methodologies that were approved by the NRC in 
    Amendment No. 85 to the Hope Creek TS. These proposed TS revisions 
    involve: (1) no hardware changes; (2) no significant changes to the 
    operation of any systems or components in normal or accident 
    operating conditions; and (3) no changes to existing structures, 
    systems or components. Therefore, these changes will not increase 
    the probability of an accident previously evaluated. Since the plant 
    systems associated with these proposed changes will still be capable 
    of: (1) meeting all applicable design
    
    [[Page 33131]]
    
    basis requirements; and (2) retain the capability to mitigate the 
    consequences of accidents described in the HC [Updated Final Safety 
    Analysis Report] UFSAR, the proposed changes were determined to be 
    justified. As a result, these changes will not involve a significant 
    increase in the consequences of an accident previously evaluated.
        The proposed changes to Surveillance Requirement 4.0.5 do not 
    alter the current requirements for the Hope Creek inservice 
    inspection and inservice testing programs and are considered to be 
    editorial in nature. These proposed TS revisions involve: (1) no 
    hardware changes; (2) no significant changes to the operation of any 
    systems or components in normal or accident operating conditions; 
    and (3) no changes to existing structures, systems or components. 
    Therefore, these changes will not increase the probability of an 
    accident previously evaluated. Since the plant systems associated 
    with these proposed changes will still be capable of: (1) Meeting 
    all applicable design basis requirements; and (2) retain the 
    capability to mitigate the consequences of accidents described in 
    the HC UFSAR, the proposed changes were determined to be justified. 
    As a result, these changes will not involve a significant increase 
    in the consequences of an accident previously evaluated.
        The proposed changes to the drywell and suppression chamber 
    purge system are being made to justify design modifications to that 
    system. As discussed in NRC Notice of Violation 50-354/96-10-01, 
    this design modification replaced isolation valves containing 
    resilient material seals with metal seated valves under 10CFR50.59. 
    As a result of this modification, a 24 month frequency has been 
    implemented to perform Type C tests on these new metal seated 
    valves. PSE&G has concluded that the 24 month frequency is 
    appropriate for the new valves since: (1) This frequency is imposed 
    by Surveillance Requirement 4.6.1.2.d, which is applicable to 
    similar containment isolation valves in Table 3.6.3-1 that penetrate 
    the primary containment; and (2) concerns raised about severe 
    environment-induced degradation and frequent use for the previously 
    installed resilient seal material valves are not applicable to the 
    replacement metal seat valves. PSE&G has concluded that the valve 
    modification was an enhancement to the Hope Creek design that did 
    not impact the isolation capability of the drywell and suppression 
    chamber purge system. No significant changes were made to the 
    operation of these valves in normal or accident operating 
    conditions. As a result, these changes will not increase the 
    probability of an accident previously evaluated. Since the plant 
    systems associated with these proposed changes will still be capable 
    of: (1) Meeting all applicable design basis requirements; and (2) 
    retain the capability to mitigate the consequences of accidents 
    described in the HC UFSAR, the proposed changes were determined to 
    be justified. As a result, these changes will not involve a 
    significant increase in the consequences of an accident previously 
    evaluated.
        The proposed changes to [Limiting Condition for Operation] LCO 
    3.7.7 establish consistent and appropriate requirements for main 
    turbine bypass valve operability requirements. These changes do not 
    impact the assumptions contained in these UFSAR analyses since they 
    do not change the manner in which Hope Creek is currently permitted 
    to operate. Since the ACTION Statement for LCO 3.7.7 already allows 
    indefinite continued operation below 25% of RATED THERMAL POWER with 
    an inoperable main turbine bypass valve system, the proposed 
    modification to the APPLICABILITY statement for this LCO does not 
    involve: (1) Hardware changes; (2) significant changes to the 
    operation of any systems or components in normal or accident 
    operating conditions; or (3) changes to existing structures, systems 
    or components. Therefore these changes will not increase the 
    probability of an accident previously evaluated. Since the plant 
    systems associated with these proposed changes will still be capable 
    of: (1) meeting all applicable design basis requirements; and (2) 
    retain the capability to mitigate the consequences of accidents 
    described in the HC UFSAR, the proposed changes were determined to 
    be justified. As a result, these changes will not involve a 
    significant increase in the consequences of an accident previously 
    evaluated.
        The proposed changes to the HC emergency diesel generator (EDG) 
    TS Bases [Change 5--Bases for TS 3/4.8, ``Electrical Power 
    Systems''] include information contained in the Safety Evaluation 
    Report for Technical Specification Amendment No. 75. This 
    information concerns the bases for the allowed-outage-time (AOT) for 
    the C and D EDGs. Concerning the revisions to planned C and D EDG 
    outages, PSE&G believes that implementation of 10CFR50.65 
    requirements to monitor EDG unavailability will provide an 
    acceptable and more clearly defined method for maintaining EDG 
    availability within acceptable limits. As stated in PSE&G's letter 
    LR-N97167, dated March 21, 1997, Hope Creek will not plan C or D EDG 
    outages that exceed 72 hours if the total unavailability of the EDG 
    will be greater than 720 hours on a 12 month rolling basis. The 
    proposed TS revisions involve: (1) no hardware changes; (2) no 
    significant changes to the operation of any systems or components in 
    normal or accident operating conditions; and (3) no changes to 
    existing structures, systems or components. Therefore these changes 
    will not increase the probability of an accident previously 
    evaluated. Since the plant systems associated with these proposed 
    changes will still be capable of: (1) Meeting all applicable design 
    basis requirements; and (2) retain the capability to mitigate the 
    consequences of accidents described in the HC UFSAR, the proposed 
    changes were determined to be justified. As a result, these changes 
    will not involve a significant increase in the consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes for the TS related to response time testing 
    reflect testing methodologies that were approved by the NRC in 
    Amendment No. 85 to the Hope Creek TS and are being made to clarify 
    the licensing basis for performing response time testing. The 
    proposed changes will not adversely impact the operation of any 
    safety related component or equipment. Since the proposed changes 
    involve: (1) No hardware changes; (2) no significant changes to the 
    operation of any systems or components; and (3) no changes to 
    existing structures, systems or components, there can be no impact 
    on the occurrence of an accident previously evaluated. Furthermore, 
    there is no change in plant testing proposed in this change request 
    that could initiate an event. Therefore, these changes will not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        The proposed changes to Surveillance Requirement 4.0.5 do not 
    alter the current requirements for the Hope Creek inservice 
    inspection and inservice testing programs and are considered to be 
    editorial in nature. The proposed changes will not adversely impact 
    the operation of any safety related component or equipment. Since 
    the proposed changes involve: (1) No hardware changes; (2) no 
    changes to the operation of any systems or components; and (3) no 
    changes to existing structures, systems or components, there can be 
    no impact on the occurrence of an accident previously evaluated. 
    Furthermore, there is no change in plant testing proposed in this 
    change request that could initiate an event. Therefore, these 
    changes will not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        The proposed changes to the drywell and suppression chamber 
    purge system are being made to justify design modifications to that 
    system. As discussed in NRC Notice of Violation 50-354/96-10-01, 
    this design modification replaced isolation valves containing 
    resilient material seals with metal seated valves under 10 CFR 
    50.59. As a result of this modification, a 24 month frequency has 
    been implemented to perform Type C tests on these new metal seated 
    valves. PSE&G has concluded that the 24 month frequency is 
    appropriate for the new valves since: (1) This frequency is imposed 
    by Surveillance Requirement 4.6.1.2.d, which is applicable to 
    similar containment isolation valves in Table 3.6.3-1 that penetrate 
    the primary containment; and (2) concerns raised about severe 
    environment-induced degradation and frequent use for the previously 
    installed resilient seal material valves are not applicable to the 
    replacement metal seat valves. PSE&G has concluded that the valve 
    modification was an enhancement to the Hope Creek design that did 
    not impact the isolation capability of the drywell and suppression 
    chamber purge system. Since the proposed changes will not adversely 
    impact the operation of any safety related component or equipment, 
    there can be no impact on the occurrence of any accident. 
    Furthermore, there is no change in plant testing proposed in this 
    change request that could initiate an event. Therefore, these 
    changes will not create the possibility of a
    
    [[Page 33132]]
    
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes to LCO 3.7.7 establish consistent and 
    appropriate requirements for main turbine bypass valve operability 
    requirements. These changes do not impact the assumptions contained 
    in these UFSAR analyses since they do not change the manner in which 
    Hope Creek is currently permitted to operate. Since the ACTION 
    Statement for LCO 3.7.7 already allows indefinite continued 
    operation below 25% of RATED THERMAL POWER with an inoperable main 
    turbine bypass valve system, the proposed modification to the 
    APPLICABILITY statement for this LCO does not involve: (1) hardware 
    changes; (2) significant changes to the operation of any systems or 
    components in normal or accident operating conditions; or (3) 
    changes to existing structures, systems or components. The proposed 
    changes will not adversely impact the operation of any safety 
    related component or equipment. Since the proposed changes involve: 
    (1) no significant hardware changes; (2) no significant changes to 
    the operation of any systems or components; and (3) no changes to 
    existing structures, systems or components, there can be no impact 
    on the occurrence of any accident. Furthermore, there is no change 
    in plant testing proposed in this change request that could initiate 
    an event. Therefore, these changes will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes to the HC emergency diesel generator (EDG) 
    TS Bases [Change 5--Bases for TS \3/4\.8, ``Electrical Power 
    Systems''] include information contained in the Safety Evaluation 
    Report for Technical Specification Amendment No. 75. This 
    information concerns the bases for the allowed-outage-time (AOT) for 
    the C and D EDGs. Concerning the revisions to planned C and D EDG 
    outages, PSE&G believes that implementation of 10CFR50.65 
    requirements to monitor EDG unavailability will provide an 
    acceptable and more clearly defined method for maintaining EDG 
    availability within acceptable limits. As stated in PSE&G's letter 
    LR-N97167, dated March 21, 1997, Hope Creek will not plan C or D EDG 
    outages that exceed 72 hours if the total unavailability of the EDG 
    will be greater than 720 hours on a 12 month rolling basis. The 
    proposed changes will not adversely impact the operation of any 
    safety related component or equipment. Since the proposed changes 
    involve: (1) No hardware changes; (2) no significant changes to the 
    operation of any systems or components; and (3) no changes to 
    existing structures, systems or components, there can be no impact 
    on the occurrence of any accident. Furthermore, there is no change 
    in plant testing proposed in this change request which could 
    initiate an event. Therefore, these changes will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes for the TS related to response time testing 
    reflect testing methodologies that were approved by the NRC in 
    Amendment No. 85 to the Hope Creek TS. No changes are being made to 
    methodologies with this proposal. Therefore, the changes contained 
    in this request do not result in a significant reduction in a margin 
    of safety.
        The proposed changes to Surveillance Requirement 4.0.5 do not 
    alter the current requirements for the Hope Creek inservice 
    inspection and inservice testing programs and are considered to be 
    editorial in nature. Therefore, the changes contained in this 
    request do not result in a significant reduction in a margin of 
    safety.
        The proposed changes to the drywell and suppression chamber 
    purge system are being made to reflect design modifications that 
    have been installed. This design modification replaced isolation 
    valves containing resilient material seals with metal seated valves 
    under 10 CFR 50.59. PSE&G has concluded that the 24 month frequency 
    is appropriate for the new valves since: (1) this frequency is 
    imposed by Surveillance Requirement 4.6.1.2.d, which is applicable 
    to other containment isolation valves in Table 3.6.3-1 that 
    penetrate the primary containment; and (2) concerns raised about 
    severe environment-induced degradation and frequent use for the 
    previously installed resilient seal material valves are not 
    applicable to the replacement metal seat valves. The valve 
    modification was an enhancement to the Hope Creek design that did 
    not impact the isolation capability of the drywell and suppression 
    chamber purge system, and does not result in a significant reduction 
    in a margin of safety.
        The proposed changes to LCO 3.7.7 establish consistent and 
    appropriate requirements for main turbine bypass valve operability 
    requirements. These changes do not impact the assumptions contained 
    in these UFSAR analyses since they do not change the manner in which 
    Hope Creek is currently permitted to operate. Since the ACTION 
    Statement for LCO 3.7.7 already allows indefinite continued 
    operation below 25% of RATED THERMAL POWER with an inoperable main 
    turbine bypass valve system, the proposed modification to the 
    APPLICABILITY statement for this LCO would be editorial in nature. 
    Therefore, the changes contained in this request do not result in a 
    significant reduction in a margin of safety.
        The HC TS Bases [Change 5--Bases for TS \3/4\.8, ``Electrical 
    Power Systems''] will be revised to include information contained in 
    the Safety Evaluation Report for Technical Specification Amendment 
    No. 75. This information concerns the bases for the allowed-outage-
    time (AOT) for the C and D emergency diesel generators (EDGs). PSE&G 
    believes that implementation of 10 CFR 50.65 requirements to monitor 
    EDG unavailability limits will provide an acceptable and more 
    clearly defined method for maintaining EDG availability within 
    acceptable limits and not result in a significant reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070.
        Attorney for licensee: M. J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: John F. Stolz.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    Date of amendment request: May 19, 1997
    
    Description of amendment request: The proposed amendment would change 
    Technical Specification (TS) 3.7.1.3, ``Ultimate Heat Sink'' to reflect 
    that continued plant operation depends upon the association of ultimate 
    heat sink (UHS) temperature and safety system availability. The 
    requirements of TS 3.7.1.1, ``Safety Auxiliaries Cooling System 
    (SACS)'', TS 3.7.1.2, ``Station Service Water System (SSWS)'' and TS 
    3.8.1.1, ``Electrical Power Systems'' would be revised to reflect the 
    revised TS 3.7.1.3. In addition, the Bases for \3/4\.7.1, ``Service 
    Water Systems'' would be appropriately revised.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed TS revisions related to SSWS/SACS and the emergency 
    diesel generators (EDGs) [TS 3.7.1.1, TS 3.7.1.2, and TS 3.8.1.1] 
    involve no hardware changes and no changes to existing structures, 
    systems or components. The additional system configuration limits and 
    changes to the operation of SSWS/SACS/EDGs are being made to ensure 
    that SSWS/SACS can remove required heat loads during design basis 
    accidents and transients with the proposed UHS river water temperature 
    and level limits. The link to the UHS LCO in the proposed SSWS/SACS/EDG 
    TS ACTION Statements and the proposed revisions to the SACS ACTION 
    Statement for one inoperable SACS subsystem ensure that the plant is 
    directed to enter a safe shutdown condition whenever the capability to
    
    [[Page 33133]]
    
    mitigate design basis accidents and transients is lost. Since the SSWS/
    SACS/EDGs will still remain capable of meeting all applicable design 
    basis requirements and retaining the capability to mitigate the 
    consequences of accidents described in the HC UFSAR, the proposed 
    changes were determined to be justified. As a result, these changes 
    will not increase the probability of an accident previously evaluated 
    nor significantly increase in the consequences of an accident 
    previously evaluated.
        The proposed TS revisions related to UHS [TS 3.7.1.3] involve no 
    hardware changes and no changes to existing structures, systems or 
    components. The additional system configuration limits and changes 
    to the operation of UHS supported systems are being made to ensure 
    that the UHS can remove required heat loads during design basis 
    accidents and transients with the proposed UHS river water 
    temperature and level limits. The proposed UHS TS ACTION Statements 
    ensure that the plant is directed to enter a safe shutdown condition 
    whenever the capability to mitigate design basis accidents and 
    transients is lost. The proposed changes to the UHS TS surveillance 
    requirements to increase monitoring of the river water temperature 
    at 82 deg.F adequately ensures that the actions required when river 
    temperatures exceed 85 deg.F are taken as appropriate. Since the UHS 
    will still remain capable of meeting all applicable design basis 
    requirements and retaining the capability to mitigate the 
    consequences of accidents described in the HC UFSAR, the proposed 
    changes were determined to be justified. As a result, these changes 
    will not increase the probability of an accident previously 
    evaluated nor significantly increase in the consequences of an 
    accident previously evaluated.
        With the approval of the proposed changes to the SSWS/SACS/EDG/
    UHS TS, the proposed TS Bases changes are considered to be editorial 
    in nature. As a result, the proposed Bases changes will not increase 
    the probability of an accident previously evaluated nor 
    significantly increase in the consequences of an accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes to the SSWS/SACS/EDG TS contained in this 
    submittal will not adversely impact the operation of any safety 
    related component or equipment. Since the proposed changes involve 
    no hardware changes and no changes to existing structures, systems 
    or components, there can be no impact on the potential occurrence of 
    any accident due to new equipment failure modes. The additional 
    system configuration limits and changes to the operation of SSWS/
    SACS/EDGs imposed by the proposed changes ensure that SSWS/SACS and 
    the UHS can remove required heat loads during design basis accidents 
    and transients with the proposed UHS river water temperature and 
    level limits. Furthermore, there is no change in plant testing 
    proposed in this change request which could initiate an event. 
    Therefore, these changes will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes to the UHS TS contained in this submittal 
    will not adversely impact the operation of any safety related 
    component or equipment. Since the proposed changes involve no 
    hardware changes and no changes to existing structures, systems or 
    components, there can be no impact on the potential occurrence of 
    any accident due to new equipment failure modes. The additional 
    system configuration limits imposed by the proposed UHS LCO ensure 
    that supported systems can remove required heat loads during design 
    basis accidents and transients with the proposed UHS river water 
    temperature and level limits. Furthermore, there is no change in 
    plant testing proposed in this change request which could initiate 
    an event. The proposed changes to the UHS TS surveillance 
    requirements to increase monitoring of the river water temperature 
    at 82  deg.F adequately ensures that the actions required when river 
    temperatures exceed 85  deg.F are taken as appropriate. Therefore, 
    these changes will not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        With the approval of the proposed changes to the SSWS/SACS/EDG 
    UHS TS, the proposed TS Bases changes are considered to be editorial 
    in nature. As a result, the proposed Bases changes will not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes for the TS related to the SSWS/SACS/EDGs 
    establish consistent and appropriate requirements for SSWS/SACS/EDG 
    and UHS operability requirements. The additional system 
    configuration limits and changes to the operation of SSWS/SACS/EDG 
    are being made to ensure that SSWS/SACS can remove required heat 
    loads during design basis accidents and transients with the proposed 
    UHS river water temperature and level limits. The link to the UHS 
    LCO in the proposed SSWS/SACS/EDG TS ACTION Statements and the 
    revision to the SACS ACTION Statement for one inoperable SACS 
    subsystem ensure that the plant is directed to: (1) enter a safe 
    shutdown condition whenever the capability to mitigate design basis 
    accidents and transients is lost; or (2) enter a conservatively 
    short period of continued operation when system redundancy is 
    reduced. Since the SSWS/SACS/EDG will still remain capable of 
    meeting all applicable design basis requirements and retaining the 
    capability to mitigate the consequences of accidents described in 
    the HC UFSAR, the proposed changes contained in this submittal were 
    determined to not result in a significant reduction in a margin of 
    safety.
        The proposed changes for the TS related to the UHS ensure 
    continued capability of the UHS to mitigate the consequences of 
    design basis accidents and transients. The additional SSWS/SACS 
    configuration limits and changes to the operating limits of the UHS 
    ensure that the UHS can remove required heat loads during design 
    basis accidents and transients with the proposed river water 
    temperature and level limits. The proposed UHS TS ACTION Statements 
    ensure that the plant is directed to: (1) enter a safe shutdown 
    condition whenever the capability to mitigate design basis accidents 
    and transients is lost; or (2) enter a conservatively short period 
    of continued operation when supported system redundancy is reduced. 
    Since the UHS will still remain capable of meeting all applicable 
    design basis requirements and retaining the capability to mitigate 
    the consequences of accidents described in the HC UFSAR, the 
    proposed changes contained were determined to not result in a 
    significant reduction in a margin of safety.
        With the approval of the proposed changes to the SSWS/SACS/UHS 
    TS, the proposed TS Bases changes are considered to be editorial in 
    nature. As a result, the proposed bases changes will not result in a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
        Attorney for licensee: M. J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: John F. Stolz.
    
    South Carolina Electric & Gas Company (SCE&G), South Carolina Public 
    Service Authority, Docket No. 50-395, Virgil C. Summer Nuclear Station, 
    Unit No. 1, Fairfield County, South Carolina
    Date of amendment request: May 21, 1997
    
        Description of amendment request: The proposed amendment would 
    revise the Virgil C. Summer Nuclear Station Technical Specifications 
    (TS), Surveillance Requirements (SRs), to change the methodology for 
    testing the charcoal adsorbers in (1) the control room normal and 
    emergency air handling system (TS 3/4.7.6), and (2) the spent fuel pool 
    ventilation system (TS 3/4.9.11), by reference to the methodology of 
    ASTM D 3803-1989 from the ANSI STD N509-1980.
        The proposed reference testing methodology to ASTM D 3803-1989 for 
    the control room is at a relative humidity of 70% and 30 degrees C with 
    methyl iodide penetration of < 2.5%.="" the="" proposed="" reference="" testing="" methodology="" to="" astm="" d="" 3803-1989="" for="" [[page="" 33134]]="" the="" spent="" fuel="" pool="" is="" at="" a="" relative="" humidity="" of="" 95%="" and="" 30="" degrees="" c="" with="" a="" methyl="" iodide="" penetration="" of="">< 2.5%.="" basis="" for="" proposed="" no="" significant="" hazards="" consideration="" determination:="" as="" required="" by="" 10="" cfr="" 50.91(a),="" the="" licensee="" has="" provided="" its="" analysis="" of="" the="" issue="" of="" no="" significant="" hazards="" consideration,="" which="" is="" presented="" below:="" 1.="" does="" the="" change="" involve="" a="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated?="" the="" proposed="" change="" revises="" the="" methodology="" for="" testing="" the="" charcoal="" adsorbers="" in="" the="" control="" room="" normal="" and="" emergency="" air="" handling="" system="" and="" the="" spent="" fuel="" pool="" ventilation="" system="" (engineered="" safeguards="" feature="" [esf]="" air="" handling="" units)="" to="" the="" updated="" standard="" test="" method="" for="" nuclear-grade="" carbon.*="" *="" *.="" the="" charcoal="" adsorbers="" are="" not="" initiators="" of="" any="" analyzed="" event.*="" *="" *="" the="" charcoal="" adsorbers="" will="" be="" tested="" to="" the="" updated="" version="" of="" the="" approved="" standard,="" which="" generally="" contains="" more="" stringent="" testing="" requirements.="" the="" change="" does="" not="" affect="" the="" operation="" of="" the="" esf="" air="" handling="" units.="" the="" new="" testing="" requirements="" will="" continue="" to="" ensure="" that="" the="" esf="" air="" handling="" units="" will="" be="" capable="" of="" performing="" their="" safety="" function="" and="" meeting="" the="" assumptions="" in="" the="" safety="" analysis="" [final="" safety="" analysis="" report="" (fsar)].="" the="" change="" does="" not="" affect="" the="" mitigation="" capabilities="" of="" any="" component="" or="" system="" nor="" does="" it="" affect="" the="" assumptions="" relative="" to="" the="" mitigation="" of="" accidents="" or="" transients.="" therefore,="" the="" change="" does="" not="" involve="" a="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" 2.="" does="" the="" change="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated?="" the="" proposed="" change="" revises="" the="" methodology="" for="" testing="" the="" charcoal="" adsorbers="" in="" the="" control="" room="" normal="" and="" emergency="" air="" handling="" system="" and="" the="" spent="" fuel="" pool="" ventilation="" system="" *="" *="" *="" to="" the="" updated="" standard="" test="" method="" for="" nuclear-grade="" carbon.="" the="" change="" does="" not="" involve="" a="" significant="" change="" in="" the="" design="" or="" operation="" of="" the="" plant.="" the="" changes="" do="" not="" involve="" a="" physical="" alteration="" of="" the="" plant="" (no="" new="" or="" different="" type="" of="" equipment="" will="" be="" installed),="" or="" new="" or="" unusual="" operator="" actions.="" no="" new="" or="" different="" accident="" scenarios,="" transient="" precursors,="" failure="" mechanisms,="" or="" limiting="" single="" failures="" will="" be="" introduced="" as="" a="" result="" of="" this="" change.="" therefore,="" the="" change="" does="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" 3.="" does="" this="" change="" involve="" a="" significant="" reduction="" in="" margin="" of="" safety?="" the="" proposed="" change="" revises="" the="" methodology="" for="" testing="" the="" charcoal="" adsorbers="" in="" the="" control="" room="" normal="" and="" emergency="" air="" handling="" system="" and="" the="" spent="" fuel="" pool="" ventilation="" system="" *="" *="" *="" to="" the="" updated="" standard="" test="" method="" for="" nuclear-grade="" carbon.="" testing="" of="" the="" charcoal="" adsorbers="" in="" the="" esf="" air="" handling="" units="" to="" the="" new="" standard="" will="" continue="" to="" ensure="" the="" systems="" perform="" their="" design="" function.="" the="" increase="" in="" the="" allowed="" penetration="" percentage="" does="" not="" affect="" the="" accident="" analysis="" because="" testing="" requirements="" are="" more="" stringent="" and="" the="" higher="" allowed="" percentages="" continue="" to="" be="" below="" the="" assumptions="" of="" the="" safety="" analysis="" [fsar].="" therefore,="" the="" change="" does="" not="" involve="" a="" significant="" reduction="" in="" a="" margin="" of="" safety.="" the="" nrc="" staff="" has="" reviewed="" the="" licensee's="" analysis="" and,="" based="" on="" this="" review,="" it="" appears="" that="" the="" three="" standards="" of="" 10="" cfr="" 50.92(c)="" are="" satisfied.="" therefore,="" the="" nrc="" staff="" proposes="" to="" determine="" that="" the="" amendment="" request="" involves="" no="" significant="" hazards="" consideration.="" local="" public="" document="" room="" location:="" fairfield="" county="" library,="" 300="" washington="" street,="" winnsboro,="" sc="" 29180.="" attorney="" for="" licensee:="" randolph="" r.="" mahan,="" south="" carolina="" electric="" &="" gas="" company,="" post="" office="" box="" 764,="" columbia,="" south="" carolina="" 29218.="" nrc="" project="" director:="" gordon="" edison,="" acting.="" southern="" nuclear="" operating="" company,="" inc.,="" docket="" nos.="" 50-348="" and="" 50-="" 364,="" joseph="" m.="" farley="" nuclear="" plant,="" units="" 1="" and="" 2,="" houston="" county,="" alabama="" date="" of="" amendments="" request:="" may="" 27,="" 1997="" description="" of="" amendments="" request:="" the="" proposed="" amendments="" would="" revise="" the="" applicable="" modes="" for="" source="" range="" nuclear="" instrumentation="" (technical="" specification="" 3/4.3.1,="" ``reactor="" trip="" system="" instrumentation''),="" provide="" allowances="" for="" an="" exception="" to="" the="" requirements="" for="" the="" state="" of="" the="" power="" supplies="" for="" residual="" heat="" removal="" system="" discharge="" to="" charging="" pump="" suction="" valves="" following="" mode="" changes="" (technical="" specification="" 3/4.5.2,="" ``eccs="" subsystems--="">avg greater than 350 deg.F'' and 3/4.5.3, ``ECCS 
    Subsystems--Tavg less than 350 deg.F''), and delete cycle-
    specific guidance concerning manual emergency engineered safety feature 
    function input checks.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) The proposed changes do not significantly increase the 
    probability or consequences of an accident previously evaluated in 
    the FSAR [Final Safety Analysis Report]. The purposes for 
    repositioning the breakers/disconnects for MOVs [motor-operated 
    valves] 8706A and 8706B are to ensure that the ECCS [Emergency Core 
    Cooling System] System is aligned properly such that the assumptions 
    used in the safety analyses are met and to prevent possible 
    overpressurization of the charging pump suction line piping. The 
    likelihood of a severe transient occurring in this time frame is 
    very small and has to be weighed against the possibility of over 
    pressurizing the CVCS [Chemical and Volume Control System] charging 
    pump suction piping. The allowance of a 4 hour time period to 
    perform the required alignment appropriately weighs this risk. 
    Changing the applicability of the requirement to have indication 
    from a Source Range Nuclear Instrument available to agree with the 
    design of the plant does not change the physical design of the plant 
    or affect any assumptions used in accident analyses and, therefore, 
    has no effect on the probability or consequences of an accident 
    previously evaluated in the FSAR. The allowance of 1 hour to perform 
    the Source Range Channel Check upon reaching P-6 from Mode 2 is 
    consistent with the current basis for a source range channel 
    inoperable. Therefore, these changes do not involve a significant 
    increase in the consequences of an accident previously evaluated.
        (2) The proposed changes to the Technical Specifications do not 
    increase the possibility of a new or different kind of accident than 
    any accident already evaluated in the FSAR. No new limiting single 
    failure or accident scenario has been created or identified due to 
    the proposed changes. Safety-related systems will continue to 
    perform as designed. Therefore, the proposed changes do not create 
    the possibility of a new or different kind of accident from any 
    previously evaluated.
        (3) The proposed changes do not involve a significant reduction 
    in the margin of safety. The margin of safety is not significantly 
    reduced due to the proposed changes to the breaker/disconnect 
    positioning requirements of TS [Technical Specifications] 3/4.5.2 
    and 3/4.5.3 when transitioning between Modes 3 and 4. The likelihood 
    of either a severe transient occurring in Mode 3 or the possible 
    overpressurization of the CVCS charging pump suction line by the RHR 
    [residual heat removal] system in Mode 4 is very small. Changing the 
    Applicability of the requirement to have indication from a Source 
    Range Nuclear Instrument available to agree with the design of the 
    plant does not change the physical design of the plant or affect any 
    assumptions used in accident analyses and, therefore, has no effect 
    on the margin of safety. These proposed changes are technically 
    consistent with the requirements and standard format of NUREG-1431, 
    Revision 1. Performing the source range channel check within 1 hour 
    upon reaching P-6 from Mode 2 does not change the physical design of 
    the plant or affect any assumptions used in accident analyses and, 
    therefore, also does not [a]ffect the margin of safety. Thus, the 
    proposed changes do not involve a significant reduction in the 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff
    
    [[Page 33135]]
    
    proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302.
        Attorney for licensee: M. Stanford Blanton, Esq., Balch and 
    Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham, 
    Alabama 35201.
        NRC Project Director: Herbert N. Berkow.
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 50-
    364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston County, 
    Alabama
    Date of amendments request: May 28, 1997
    
        Description of amendments request: The proposed amendments would 
    insert a footnote in Technical Specification (TS) Surveillance 
    Requirement 4.8.1.1.2.e, to clarify that load rejection testing of the 
    shared emergency diesel generator set on either unit may be used to 
    satisfy TS 4.8.1.1.2.e surveillance requirements for both units.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed changes clarify that load rejection testing of the 
    shared emergency diesel generator set is only required once per five 
    years, and that testing of the shared EDG [emergency diesel 
    generator] set on one unit may be used to satisfy SR [Surveillance 
    Requirement] 4.8.1.1.2.e requirements for both units. These changes 
    do not affect the probability or consequences of an accident. There 
    are no changes being made to the emergency diesel generator testing 
    program. These changes simply clarify the existing test program and 
    the intent of the test requirements.
        Therefore, the proposed TS changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes clarify that load rejection testing of the 
    shared emergency diesel generator set is only required once per five 
    years, and that testing of the shared EDG set on one unit may be 
    used to satisfy SR 4.8.1.1.2.e requirements for both units. No new 
    testing configuration is being proposed that could create the 
    possibility of any new or different kind of accident from any 
    accident previously evaluated. There are no changes being made to 
    the emergency diesel generator testing program. These changes simply 
    clarify the existing test program and the intent of the test 
    requirements.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The proposed changes clarify that load rejection testing of the 
    shared emergency diesel generator set is only required once per five 
    years, and that testing of the shared EDG set on one unit may be 
    used to satisfy SR 4.8.1.1.2.e requirements for both units. A 
    similar technical specification change has been previously approved 
    by the NRC for Hatch Nuclear Plant. The technical specification 
    bases and the Final Safety Analysis Report have been reviewed. 
    Clarification of the testing requirements has no effect on the 
    margin of plant safety since no reduction in the test program is 
    involved.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302.
        Attorney for licensee: M. Stanford Blanton, Esq., Balch and 
    Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham, 
    Alabama 35201.
        NRC Project Director: Herbert N. Berkow.
    
    The Cleveland Electric Illuminating Company, Centerior Service Company, 
    Duquesne Light Company, Ohio Edison Company, Pennsylvania Power 
    Company, Toledo Edison Company, Docket No. 50-440, Perry Nuclear Power 
    Plant, Unit 1, Lake County, Ohio
    Date of amendment request: May 2, 1997.
    
        Description of amendment request: The proposed change would 
    continue to allow entry into Operational Conditions 1, 2, and 3 with 
    the inboard main steam isolation valve (MSIV) leakage control subsystem 
    inoperable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        This License Amendment application proposes a revision to the 
    exception to Limiting Condition for Operation (LCO) 3.0.4 as it 
    applies to the Technical Specification (TS) for the MSIV Leakage 
    Control System (LCS). This revision is proposed to permit completion 
    of activities necessary to implement the most appropriate permanent 
    resolution for the issues that resulted from the elimination of the 
    secondary containment bypass leakage path through the Main Steam 
    Line drains. In addition, the revision clarifies that the exception 
    only applies to the Inboard MSIV LCS subsystem. The drains will 
    remain in their current configuration, which seals off the secondary 
    containment bypass leakage path. The sealed drain path results in a 
    temporary inoperability of the Inboard MSIV LCS subsystem when the 
    plant is operated below 50 percent rated thermal power (RTP), due to 
    condensate build-up in the bottom of the steam lines between the 
    MSIVs. The requested 3.0.4 exception is necessary to permit plant 
    startups with this temporary inoperability. The exception to LCO 
    3.0.4 simply permits use of the existing Action statement (Condition 
    A of LCO 3.6.1.9) during MODE changes.
        The probability of occurrence of a previously evaluated accident 
    is not affected by the proposed revision of the LCO 3.0.4 exception 
    since no change to the plant or to the manner in which the plant is 
    operated is involved. The existing plant configuration will be 
    maintained, and possible concerns resulting from that configuration 
    have been analyzed. The extra weight of the water pooled between the 
    MSIVs was analyzed with respect to piping supports and seismic 
    considerations and was found to be acceptable, and condensate that 
    is carried past the outboard MSIVs will be drained to the condenser 
    by drain connections downstream of the outboard MSIVs before it can 
    reach the turbine. The temporary inoperability of the Inboard MSIV 
    LCS subsystem when below 50 percent RTP has no impact on accident 
    initiation probability, since the MSIV LCS does not serve to prevent 
    accidents, but is only used in mitigating the consequences of Loss 
    of Coolant Accidents (LOCAs) that have already occurred.
        The consequences of an accident are not affected in that the 
    Outboard MSIV LCS subsystem will be available to perform the MSIV 
    LCS function by mitigating the consequences of a LOCA during the 
    temporary period in which the Inboard MSIV LCS subsystem is 
    unavailable. Condensate that is carried past the outboard MSIVs will 
    be drained to the condenser by drain connections downstream of the 
    outboard MSIVs; therefore, no impairment of the Outboard MSIV LCS 
    subsystem will result from condensed water. The Required Action and 
    Completion Time for one inoperable MSIV LCS subsystem remains the 
    same, and limits plant operation to the previously established 30-
    day Allowable Outage Time. The Required Action if both subsystems of 
    MSIV LCS were to become inoperable also remains the same. The MSIV 
    function of isolating the Main Steam Lines is also unaffected by the 
    existing plant
    
    [[Page 33136]]
    
    configuration, since MSIV performance will not be affected by the 
    existence of accumulated water in the bottom of the steam lines 
    between the MSIVs during plant operation below 50 percent RTP. 
    Therefore, if necessary, the Main Steam Lines will be isolated, and 
    leakage past the MSIVs will be routed for filtration as in the 
    design-basis radiological analyses, and the safety and radiological 
    consequences of previously evaluated accidents will remain 
    unaffected.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change to permit inoperability of the Inboard MSIV 
    LCS subsystem during periods of startup and power ascension to 50 
    percent RTP and during shutdown below 50 percent RTP does not create 
    the possibility of a new or different kind of accident from any 
    previously evaluated. The Inboard MSIV LCS subsystem is only 
    credited during a large-break LOCA wherein Reactor Coolant System 
    depressurization occurs. The temporary unavailability of the Inboard 
    MSIV LCS subsystem can be mitigated by operation of the Outboard 
    MSIV LCS subsystem. The amendment to the TS is an administrative 
    change that does not involve change to the current plant design or 
    methods of operation. No new plant equipment failure modes or 
    accident initiators are introduced by the LCO 3.0.4 exception.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The response to a large-break LOCA will not be affected since 
    the Outboard MSIV LCS subsystem can be assumed to be available 
    during the limited period of time that the Technical Specifications 
    permit the Inboard subsystem to be unavailable. Allowing entry into 
    MODES 1, 2, and 3 while utilizing the existing Condition A and 
    Required Action A.1 does not reduce the margin of safety since the 
    Completion Time allowed for that Condition is not increased. The 
    proposed change will have no adverse impact on the reactor coolant 
    system pressure boundary nor will other system protective boundaries 
    or safety limits be affected.
    
        The NRC staff has reviewed the licensees' analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Gail H. Marcus.
    
    The Cleveland Electric Illuminating Company, Centerior Service Company, 
    Duquesne Light Company, Ohio Edison Company, Pennsylvania Power 
    Company, Toledo Edison Company, Docket No. 50-440, Perry Nuclear Power 
    Plant, Unit 1, Lake County, Ohio
    Date of amendment request: May 2, 1997
    
        Description of amendment request: The proposed change would allow 
    the leakage rate of one or more main steam lines to be up to 35 
    standard cubic feet per hour (scfh), as long as the total leakage rate 
    through all four main steam lines is less than or equal to 100 scfh.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change involves the deletion of the portion of 
    Technical Specification Surveillance Requirement (SR) 3.6.1.3.10 
    that states the increased leakage rate of less than or equal to 35 
    scfh for an individual main steam line is only acceptable for 
    Operating Cycle 6, and a deletion of the restriction that a main 
    steam line leakage rate of less than or equal to 35 scfh is 
    acceptable for only one main steam line. The overall main steam line 
    leakage limit of less than or equal to 100 scfh for all four main 
    steam lines is not being revised.
        The MSIV [main steam isolation valve] leakage is not an 
    initiator of an accident, including the steam line rupture accident. 
    Therefore, the probability of an accident previously evaluated has 
    not changed.
        The consequences of interest are the radiological dose 
    consequences following a large-break Loss of Coolant Accident 
    (LOCA). This is the event which the regulatory guidance requires to 
    be evaluated using the extremely conservative source term 
    assumptions of Regulatory Guide 1.3, ``Assumptions Used for 
    Evaluating the Potential Radiological Consequences of a Loss of 
    Coolant Accident for Boiling Water Reactors.'' Since the overall 
    main steam line leakage rate of less than or equal to 100 scfh for 
    all four main steam lines is not being revised, the radiological 
    consequences of an accident previously evaluated has not changed.
        Therefore, the probability or consequences of an accident 
    previously evaluated have not significantly increased.
        2. The proposed change would not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        This proposed change does not physically alter the plant or 
    systems or equipment in the plant, or the method for operation of 
    the plant. Therefore, the proposed change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed change will not involve a significant reduction 
    in the margin of safety.
        The proposed change does not revise the overall combined leakage 
    rate of less than or equal to 100 scfh for all four main steam lines 
    that is permitted in the present Specification. It is the combined 
    main steam line penetration leakage rate that is assumed in the 
    radiological accident analyses. Thus, although individual steam line 
    leakage rates may be less than or equal to 35 scfh, as long as 
    overall leakage of the four main steam lines is maintained at its 
    current value of less than or equal to 100 scfh, the proposed change 
    does not reduce the margin of safety.
        Therefore, the proposed change does not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensees' analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Gail H. Marcus.
    
    Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339, 
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    Date of amendment request: November 9, 1987, as supplemented March 31, 
    1988, June 8, 1992 and February 4, 1997
    
        Description of amendment request: The proposed changes would revise 
    the Technical Specifications (TS) for the North Anna Power Station (NA 
    1&2). The changes would reformat the operability and surveillance 
    requirements for the intermediate range (IR) channels to be consistent 
    with NUREG-0452, Revision 4, ``Standard Technical Specifications (STS) 
    for Westinghouse Pressurized Water Reactors'' (Fall 1981), which is 
    applicable to NA 1&2. Also, the proposed changes would revise the 
    nominal IR high flux trip setpoint. The IR nuclear flux trips provide 
    backup reactor core protection during reactor startup. There is no 
    operating condition under which the IR trip provides sole overpower 
    protection. It is a backup trip only, and no credit is taken for the 
    trip in the NA 1&2 Updated Final Safety Analysis Report (UFSAR). 
    Operating experience at NA 1&2 has shown the IR channel response to be 
    sensitive to core loading patterns, varying core burnups, and control 
    rod positions, and the variability in the channel response had made it 
    difficult to maintain the channels in proper calibration. Therefore, 
    the proposed change would
    
    [[Page 33137]]
    
    elevate the nominal IR high flux trip setpoint from a current 
    equivalent to 25% of rated thermal power to a current equivalent to 35% 
    of rated thermal power.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    [The proposed changes would not:]
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated. There is no 
    adverse impact on the safety analysis (since no credit is taken for 
    the trips in the existing analyses), and no degradation of the 
    protection system redundancy or reliability. This latter conclusion 
    is based on sensitivity studies which show that the effectiveness of 
    the flux trip system in protecting against the low power reactivity 
    excursions examined in the FSAR is not sensitive to realistic 
    variations in the actual flux trip setpoint.
        2. Create the probability of a new or different kind of accident 
    from any accident previously identified, since the severity of the 
    analyzed accidents is unchanged, and since only a change to a 
    setpoint and the associated surveillance requirements for the 
    reactor protection system is involved.
        3. Involve a significant reduction in a margin of safety, since 
    none of the safety analysis input or assumptions are changed, nor 
    are the probability nor the consequences of any previously analyzed 
    accidents increased.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: Brenda Mozafari (Acting).
    
    Previously Published Notices of Consideration of Issuance of Amendments 
    to Facility Operating Licenses, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York 
    Date of application for amendment: March 31, 1997
    
        Brief description of amendment: The proposed amendment would remove 
    containment isolation valve 863 from Technical Specification Table 3.6-
    1, ``Non-Automatic Containment Isolation Valves Open Continuously or 
    Intermittently for Plant Operation.''
        Date of publication of individual notice in Federal Register: May 
    15, 1997 (62 FR 26823).
        Expiration date of individual notice: June 16, 1997.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    Date of amendment request: April 25, 1997
    
        Brief description of amendment request: The proposed amendment 
    changes to revise Technical Specification 3.5.2 to eliminate the flow 
    path from the residual heat removal system to the reactor coolant 
    system hot legs that is specified in Limiting Condition for Operation 
    3.5.2.c.2.
        Date of publication of individual notice in Federal Register: May 
    14, 1997 (62 FR 26574).
        Expiration date of individual notice: June 13, 1997.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    Public Service Electric & Gas Company, Docket No. 50-311, Salem Nuclear 
    Generating Station, Unit No. 2, Salem County, New Jersey
    Date of amendment request: May 1, 1997
    
        Brief description of amendment request: The proposed amendment 
    would revise Technical Specification (TS) 3/4.7.7, ``Auxiliary Building 
    Exhaust Air Filtration System,'' and add a new TS Section 3/4.7.11, 
    ``Switchgear and Penetration Area Ventilation System.'' The change to 
    TS 3/4.7.7 would allow for an increase in the allowed outage time from 
    7 to 14 days when one auxiliary building exhaust fan is inoperable. The 
    new TS 3/4.7.11 addresses the support function this system provides to 
    other necessary safety support components.
        Date of publication of individual notice in Federal Register: May 
    15, 1997 (62 FR 26826).
        Expiration date of individual notice: June 16, 1997.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    Date of amendment request: May 14, 1997
    
        Brief description of amendment request: Your application proposes 
    changes to revise Technical Specification Surveillance Requirement 
    4.7.6.1.d.1 to indicate that the specified acceptable filter 
    differential pressure (DP) is to be measured across the filter housing 
    and to change the filter DP acceptance value from less than or equal to 
    3.5 inches water gauge to less than or equal to 2.70 inches water 
    gauge.
        Date of publication of individual notice in Federal Register: May 
    29, 1997 (62 FR 29158).
        Expiration date of individual notice: June 30, 1997.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing in connection with these 
    actions was
    
    [[Page 33138]]
    
    published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    Date of application for amendment: November 26, 1997
    
        Brief description of amendment: The amendment revises Technical 
    Specifications Definition 1.M, ``Primary Containment Integrity,'' Note 
    6 on Table 3.2.A for the high flow main steam line instrumentation, 
    Table 3.2.D for a typographical error, Table 3.2.F to reflect a change 
    made in instrument type for the suppression chamber water temperature 
    instrumentation, Table 3.2.F to reflect modifications made to 
    suppression chamber bulk and local temperature instrumentation, Bases 
    Section 3/4.6G to remove an obsolete reference to Group I welds, and 
    Bases Section 3/4.7.A to remove ``high radiation'' from the description 
    of Primary Containment Group 1 initiation signals. In addition, this 
    amendment includes changes made to the Bases Section 3.10, ``Core 
    Alterations,'' as noted by BECo letter dated March 7, 1997.
        Date of issuance: May 28, 1997.
        Effective date: May 28, 1997.
        Amendment No.: 172.
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 12, 1997 (62 
    FR 6568). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 28, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
    Commonwealth Edison Company, Docket Nos. 50-254 and 50-265, Quad Cities 
    Nuclear Power Station, Units 1 and 2, Rock Island County, Illinois
    Date of application for amendments: June 10, 1996, as supplemented by 
    letter dated February 17, 1997
    
        Brief description of amendments: The amendments change the 
    Technical Specifications to reflect the transition from General 
    Electric Company (GE) to Siemens Power Corporation (SPC) as the fuel 
    supplier for the Quad Cities Nuclear Power Station, Units 1 and 2. In 
    addition, as an administrative action by the Commission that only 
    involves the format of the licenses and does not authorize any 
    activities outside the scope of the application and supplement, the NRC 
    has amended the licenses to include an Appendix C that lists additional 
    license conditions. The additional license condition as a result of the 
    review of this application reflects the relocation of the contents of 
    TS 5.4 to the Updated Final Safety Analysis Report.
        Date of issuance: May 23, 1997.
        Effective date: Immediately, to be implemented within 60 days.
        Amendment Nos.: 177 and 175.
        Facility Operating License Nos. DPR-29 and DPR-30: The amendments 
    revised the Licenses, Technical Specifications and Updated Final Safety 
    Analaysis Report.
        Date of initial notice in Federal Register: August 28, 1996 (61 FR 
    44355). The February 17, 1997, submittal provided additional clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated May 23, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Dixon Public Library, 221 
    Hennepin Avenue, Dixon, Illinois 61021.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    Date of application for amendment: August 29, 1995, as supplemented 
    August 7, 1996, and January 10, 1997
    
        Brief description of amendment: The amendment revises Technical 
    Specifications to incorporate the commitments made in connection with 
    Amendment No. 183, which allowed the installation of laser welded 
    sleeves inside of defective steam generator tubes.
        Date of issuance: May 20, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 192.
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 8, 1995 (60 FR 
    56365) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 20, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam Neck 
    Plant, Middlesex County, Connecticut
    Dates of application for amendment: December 24, 1996, and January 31, 
    1997
    
        Brief description of amendment: Changes Administrative Controls 
    Section of the Technical Specifications to implement revised management 
    responsibilities and titles that reflect the permanently shut down 
    status of the plant.
        Date of issuance: May 22, 1997.
        Effective date: Effective May 22, 1997, to be implemented within 60 
    days of issuance.
        Amendment No.: 191.
        Operating License No. DPR-61: Amendment revised the Technical 
    Specifications.
        Date of initial notice in Federal Register: March 26, 1997 (62 FR 
    14460) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 22, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457.
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, Beaver 
    Valley Power Station, Unit Nos. 1 and 2, Shippingport, Pennsylvania
    Date of application for amendments: March 10, 1997
    
        Brief description of amendments: These amendments modify Unit No. 1 
    Technical Specification (TS) 5.2.1 to add ZIRLO as fuel assembly 
    material
    
    [[Page 33139]]
    
    and add reference to the Nuclear Regulatory Commission approved Topical 
    Report WCAP-12610, ``Vantage+ Fuel Assembly Reference Core Report,'' to 
    TS 6.9.1.12 for both units.
        Date of issuance: May 23, 1997.
        Effective date: Both units, as of date of issuance, to be 
    implemented within 60 days.
        Amendment Nos.: 203 and 84.
        Facility Operating License Nos. DPR-66 and NPF-73: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 9, 1997 (62 FR 
    17231) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 23, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: B.F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001.
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    Date of amendment request: February 5, 1997, as supplemented by letter 
    dated March 26, 1997
    
        Brief description of amendment: The amendment changes the Appendix 
    A Technical Specifications for Waterford Steam Electric Station, Unit 
    3, by revising Technical Specifications 3.1.2.7, 3.1.2.8, 3.5.1, 3.5.4, 
    3.9.1, and Bases 3/4.1.2. The changes will increase the minimum boron 
    concentration in the Safety Injection Tanks and the Refueling Water 
    Storage Pool from 1720 to 2050 ppm.
        Date of issuance: May 29, 1997, to be implemented within 60 days.
        Effective date: May 29, 1997.
        Amendment No.: 129.
        Facility Operating License No. NPF-38: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 26, 1997, (62 FR 
    14461) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 29, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile Island 
    Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    Date of application for amendment: June 28, 1996, as supplemented March 
    11, 1997
    
        Brief description of amendment: The amendment revises Three Mile 
    Island, Unit 1, Technical Specifications to permit the use of 10 CFR 
    50, Appendix J, Option B, Performance-Based Containment Leakage 
    Testing.
        Date of issuance: May 27, 1997.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 201.
        Facility Operating License No. DPR-50. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 31, 1996 (61 FR 
    40019) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 27, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Law/Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY), Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, Docket 
    Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, Matagorda 
    County, Texas
        Date of amendment request: August 8, 1996
    
        Brief description of amendments: The amendments allowed the 
    transition from Mode 4 to Mode 3 with the turbine-driven auxiliary 
    feedwater pump inoperable and allowed a 72-hour period after the entry 
    into Mode 3 to complete all necessary operability testing.
        Date of issuance: May 27, 1997.
        Effective date: May 27, 1997, to be implemented within 30 days.
        Amendment Nos.: Unit 1--Amendment No. 87; Unit 2--Amendment No. 74.
        Facility Operating License Nos. NPF-76 and NPF-80: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 28, 1996 (61 FR 
    44359) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 27, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488.
    
    Northeast Nuclear Energy Company, Docket No. 50-245, Millstone Nuclear 
    Power Station, Unit 1, New London County, Connecticut
    Date of application for amendment: March 6, 1997
    
        Brief description of amendment: The amendment revises the Technical 
    Specifications on allowed outage times for certain protective 
    instrumentation and also for reactor building access control. The 
    amendment adopts, in part, guidance from NUREG-0123, ``Standard 
    Technical Specifications for General Electric Boiling Water Reactors 
    (BWR/5),'' Revision 3, and NUREG-1433, ``Standard Technical 
    Specifications General Electric Plants BWR/4,'' Revision 1.
        Date of issuance: May 28, 1997.
        Effective date: As of the date of issuance, to be implemented 
    within 90 days.
        Amendment No.: 101.
        Facility Operating License No. DPR-21: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 26, 1997 (62 FR 
    14462) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 28, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut 06360 and at the Waterford Library, ATTN: Vince 
    Juliano, 49 Rope Ferry Road, Waterford, Connecticut 06385.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
        Date of application for amendment: March 31, 1997
    
        Brief description of amendment: The amendment modifies Technical 
    Specification Surveillance 4.7.1.2.1.b, which requires the testing of 
    the auxiliary feedwater motor-driven and turbine-driven pumps on 
    recirculation flow at least once per 92 days. The amendment also makes 
    changes to the appropriate Bases section.
        Date of issuance: May 29, 1997.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 139.
        Facility Operating License No. NPF-49: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 23, 1997 (62 FR 
    19832) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 29, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center,
    
    [[Page 33140]]
    
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut 06360, and the Waterford Library, ATTN: Vince 
    Juliano, 49 Rope Ferry Road, Waterford, Connecticut 06385.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    Date of application for amendment: March 31, 1997
    
        Brief description of amendment: The amendment separates the 
    required testing of motor-operated valve thermal overload protection 
    into two new surveillances.
        Date of issuance: May 29, 1997.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 140.
        Facility Operating License No. NPF-49: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 23, 1997 (62 FR 
    19833) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 29, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut 06360, and the Waterford Library, ATTN: Vince 
    Juliano, 49 Rope Ferry Road, Waterford, Connecticut 06385.
    
    Portland General Electric Company, et al., Docket No. 50-344, Trojan 
    Nuclear Plant, Columbia County, Oregon
    Date of application for amendment: January 16, 1997, as supplemented on 
    February 24, 1997
    
        Brief description of amendment: This amendment revises the license 
    to delete the prohibition on moving a spent fuel assembly shipping cask 
    into the Fuel Building.
        Date of issuance: May 19, 1997.
        Effective date: This license amendment is effective as of the date 
    of issuance (May 19, 1997), but shall be implemented within 30 days of 
    issuance.
        Amendment No.: 196.
        Facility Operating License No. NPF-1: The amendment revised the 
    license.
        Date of initial notice in Federal Register: March 26, 1997 (62 FR 
    14467).
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Branford Price Millar Library, 
    Portland State University, 934 S.W. Harrison Street, P.O. Box 1151, 
    Portland, Oregon 97207.
    
    Portland General Electric Company, et al., Docket No. 50-344, Trojan 
    Nuclear Plant, Columbia County, Oregon
    Date of application for amendment: January 28, 1997
    
        Brief description of amendment: This amendment changes the 
    Permanently Defueled Technical Specifications to delete the requirement 
    for NRC prior approval to changes in the Certified Fuel Handler's 
    Training Program.
        Date of issuance: May 23, 1997.
        Effective date: May 23, 1997.
        Amendment No.: 197.
        Possession-Only License No. NPF-1: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 9, 1997 (62 FR 
    17241).
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Branford Price Millar Library, 
    Portland State University, 934 S.W. Harrison Street, P.O. Box 1151, 
    Portland, Oregon 97207.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San 
    Diego County, California
    Date of application for amendments: April 15, 1997
    
        Brief description of amendments: These amendments revise 
    Surviellance Requirement 3.8.1.8 of Technical Specifications (TS) 
    3.8.1, ``AC Sources--Operating,'' for San Onofre Nuclear Generating 
    Station (SONGS), Units 2 and 3. The TS change will allow the licensee 
    to credit overlap testing to validate the capability of the alternate 
    offsite power source.
        Date of issuance: June 2, 1997.
        Effective date: June 2, 1997.
        Amendment Nos.: Unit 2--136; Unit 3--128.
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 1, 1997 (62 FR 
    23811) The Commission's related evaluation of the amendments is 
    contained in a Safety E valuation dated June 2, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713.
    
    Tennessee Valley Authority, Docket No. 50-390 Watts Bar Nuclear Plant, 
    Unit 1, Rhea County, Tennessee
    Date of application for amendment: January 10, 1997, as supplemented 
    May 2 and May 15, 1997
    
        Brief description of amendment: The amendment modifies the Watts 
    Bar Nuclear Plant (WBN) Unit 1 Technical Specifications (TS) in order 
    to implement 10 CFR Part 50, Appendix J, Option B, by referring to 
    Regulatory Guide 1.163, ``Performance-Based Containment Leakage-Test 
    Program.''
        Date of issuance: May 27, 1997.
        Effective date: May 27, 1997.
        Amendment No.: 5.
        Facility Operating License No. NPF-90: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 29, 1997 (62 FR 
    4356) The May 2 and May 15, 1997 letters provided clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated May 27, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, TN 37402.
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek 
    Generating Station, Coffey County, Kansas
    Date of amendment request: March 18, 1997
    
        Brief description of amendment: This amendment revises Technical 
    Specification Surveillance Requirement 4.5.2.c to clarify when a 
    containment entry visual inspection is required. This change reduces 
    the visual inspection requirement to at least once daily and is in 
    accordance with the guidance provided in Generic Letter 93-05, ``Line-
    Item Technical Specifications Improvements to Reduce Surveillance 
    Requirements for Testing During Power Operation.''
        Date of issuance: May 28, 1997.
        Effective date: May 28, 1997, to be implemented within 30 days of 
    the date of issuance.
        Amendment No.: 105.
        Facility Operating License No. NPF-42. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 23, 1997 (62 FR 
    19839) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 28, 1997.
        No significant hazards consideration comments received: No.
        Local Public Document Room locations: Emporia State University,
    
    [[Page 33141]]
    
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621.
    
    Notice of Issuance of Amendments To Facility Operating Licenses and 
    Final Determination of No Significant Hazards Consideration and 
    Opportunity for a Hearing (Exigent Public Announcement or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By July 18, 1997, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC, and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific
    
    [[Page 33142]]
    
    sources and documents of which the petitioner is aware and on which the 
    petitioner intends to rely to establish those facts or expert opinion. 
    Petitioner must provide sufficient information to show that a genuine 
    dispute exists with the applicant on a material issue of law or fact. 
    Contentions shall be limited to matters within the scope of the 
    amendment under consideration. The contention must be one which, if 
    proven, would entitle the petitioner to relief. A petitioner who fails 
    to file such a supplement which satisfies these requirements with 
    respect to at least one contention will not be permitted to participate 
    as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1) (i)-(v) and 2.714(d).
    
    Commonwealth Edison Company, Docket No. STN 50-456, Braidwood Station, 
    Unit No. 1, Will County, Illinois
    Date of application for amendment: Two submittals dated May 23, 1997
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 4.5.2.b.1 to include the use of ultrasonic testing 
    (UT) to verify that the emergency core cooling system (ECCS) is 
    completely filled with water. For the ECCS subsystems with high point 
    vent valves in direct communication with the operating systems, UT is 
    acceptable in lieu of physically opening the vents.
        Date of Issuance: May 23, 1997.
        Effective date: Immediately, to be implemented within 30 days.
        Amendment No.: 83.
        Facility Operating License No. NPF-72: The amendment revised the 
    TSs.
        Public comments requested as to proposed no significant hazards 
    consideration: No.
        The Commission's related evaluation of the amendment, finding of 
    emergency circumstances, and final determination of no significant 
    hazards consideration are contained in a Safety Evaluation dated May 
    23, 1997.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690.
        Local Public Document Room location: Wilmington Public Library, 201 
    S. Kankakee Street, Wilmington, Illinois 60481.
        NRC Project Director: Robert A. Capra.
    
    Commonwealth Edison Company, Docket No. STN 50-454, Byron Station, Unit 
    No. 1, Ogle County, Illinois
    Date of application for amendment: May 24, 1997, as supplemented on May 
    31, 1997
    
        Brief description of amendment: The amendment revises Technical 
    Specification 4.5.2.b.1 to include the use of ultrasonic testing (UT) 
    to verify that the emergency core cooling system (ECCS) is completely 
    filled with water. For the ECCS subsystems with high point vent valves 
    in direct communication with the operating systems, UT is acceptable in 
    lieu of physically opening the vents. This amendment supersedes NOED 
    No. 97-6-010 for Byron, Unit 1, which was granted on May 23, 1997.
        Date of Issuance: June 1, 1997.
        Effective date: Immediately, to be implemented within 30 days.
        Amendment No.: 90.
        Facility Operating License No. NPF-37: The amendment revised the 
    TS. Public comments requested as to proposed no significant hazards 
    consideration: No.
        The Commission's related evaluation of the amendment, finding of 
    emergency circumstances, and final determination of no significant 
    hazards consideration are contained in a Safety Evaluation dated June 
    1, 1997.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690.
        Local Public Document Room location: Byron Public Library District, 
    109 N. Franklin, P.O. Box 434, Byron, Illinois 61010.
        NRC Project Director: Robert A. Capra.
    
        Dated at Rockville, Maryland, this 11th day of June, 1997.
    
        For The Nuclear Regulatory Commission.
    Jack W. Roe,
    Director, Division of Reactor Projects III/IV, Office of Nuclear 
    Reactor Regulation.
    [FR Doc. 97-15827 Filed 6-17-97; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Effective Date:
5/28/1997
Published:
06/18/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
97-15827
Dates:
May 28, 1997.
Pages:
33117-33142 (26 pages)
PDF File:
97-15827.pdf