X96-10619. Biweekly Notice  

  • [Federal Register Volume 61, Number 119 (Wednesday, June 19, 1996)]
    [Notices]
    [Pages 31171-31192]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X96-10619]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from May 24, 1996, through June 7, 1996. The last 
    biweekly notice was published on June 5, 1996 (61 FR 28604).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By July 19, 1996, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a
    
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    petition for leave to intervene shall be filed in accordance with the 
    Commission's ``Rules of Practice for Domestic Licensing Proceedings'' 
    in 10 CFR Part 2. Interested persons should consult a current copy of 
    10 CFR 2.714 which is available at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC and at 
    the local public document room for the particular facility involved. If 
    a request for a hearing or petition for leave to intervene is filed by 
    the above date, the Commission or an Atomic Safety and Licensing Board, 
    designated by the Commission or by the Chairman of the Atomic Safety 
    and Licensing Board Panel, will rule on the request and/or petition; 
    and the Secretary or the designated Atomic Safety and Licensing Board 
    will issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, 
    and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: April 25, 1996
        Description of amendment request: The proposed amendment would 
    change the definition of Operable-Operability, revise Technical 
    Specifications (TSs) and associated Bases Section for TSs 3.5.F.1, 
    ``Core and Containment Cooling systems,'' TSs 3.9.B.1, 3.9.B.2, 
    3.9.B.3, 3.9.b.4, ``Auxiliary Electrical System,'' and TSs 3.7.B.1.a, 
    c, and e, and 3.7.b.2.a, c, and e, ``Standby Gas Treatment System and 
    Control Room High Efficiency Air Filtration System,'' and delete TSs 
    4.5.F.1, ``Core and Containment Cooling Systems,'' and 3.7.B.1.f, 
    ``Standby Gas Treatment System and Control Room High Efficiency Air 
    Filtration System.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Operation of PNPS [Pilgrim Nuclear Power Station] in accordance 
    with the proposed license amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated because of the following:
        Definition of ``Operable-Operability''
        Definitions perform a supporting function for other sections of 
    the TS. The definition of ``Operable-Operability'' affects the 
    manner
    
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    in which the requirements for a Limiting Condition for Operation 
    (LCO) and its associated remedial actions are applied when a support 
    system is inoperable. This definition re-affirms the principle that 
    a system is operable when it is capable of performing its specified 
    function and when all necessary support systems are also capable of 
    performing their related support functions. The corollary is that a 
    system is inoperable when it is not capable of performing its 
    specified function or when a necessary support system is not capable 
    of performing its related support function.
        No changes are being made to the plant design, system 
    configuration, or method of operation. The proposed change does not 
    affect the ability of the AC power sources to perform their required 
    safety functions nor affect the ability of the features they support 
    to perform their respective safety functions. Therefore, the 
    proposed change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        EDG [Emergency Diesel Generator]
        An Individual Plant Examination (IPE) for Internal Events was 
    submitted to the NRC in response to Generic Letter 88-20 in 
    September 1992. The IPE was used to quantify the overall impact of 
    the proposed 14 day allowed outage time on core damage frequency. 
    Part III provides the results of a comprehensive Probabilistic 
    Safety Assessment (PSA) of the impact of the proposed AOTs [allowed 
    outage times] for the EDGs and Startup and Shutdown transformers. As 
    shown in Part III, there is not a significant increase in risk due 
    to the proposed change. Thus the proposed change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The existing specification 3.9.B.1 is being separated into two 
    segments (a and b) because of the proposed and different AOTs for 
    the Startup and Shutdown transformers. As a result of the PSA, the 
    AOT for the Startup transformer (a) is reduced from 7 days to 72 
    hours, while the AOT for the Shutdown transformer (b) remains at 7 
    days. The reduction of the AOT from 7 days to 3 days is based on the 
    relative risk importance of the Startup transformers support to the 
    balance of plant systems. Similarly, an additional reduction from 72 
    hours to 48 hours is proposed in the AOT for a simultaneous loss of 
    both the Startup transformer and an EDG (TS 3.9.B.4.b) based upon 
    the Startup transformer's contribution to risk in relation to the 
    EDG 14-day AOT risk assessment analysis and that two power sources 
    have been removed from the associated bus. The AOT reductions 
    represent a measurable decrease in risk as assessed in the PSA. 
    Thus, the probability or consequences of an accident previously 
    evaluated are not significantly increased.
        The current technical specifications allow one EDG to be out of 
    service for three days based on the availability of the SUT [startup 
    transformer] and SDT [shutdown transformer] and the fact that each 
    EDG carries sufficient engineered safeguards equipment to cover all 
    design basis accidents. With one EDG out of service and a Loss of 
    Offsite Power (LOOP) condition, the capability to power vital and 
    auxiliary system components remains available via the other EDG, and 
    for one train of ESF equipment via the SDT for all operating, 
    transient and accident conditions. Increasing the EDG AOT to 14 days 
    provides flexibility in the maintenance and repair of the EDGs. The 
    EDG unavailability will be monitored and trended in accordance with 
    the Maintenance Rule. The PSA analyses supports the change to a 14 
    day AOT for the EDGs based on an insignificant increase in overall 
    risk. Implementation of the proposed change is expected to result in 
    less than a one percent increase in the baseline core damage 
    frequency (2.84E-05/yr), which is considered to be insignificant 
    relative to the underlying uncertainties involved with probabilistic 
    safety assessments. Additional conditions are added to the Standby 
    Liquid Control, Standby Gas Treatment, and Control Room High 
    Efficiency Air Filtration systems requiring the EDG associated with 
    these systems to remain operable while in the 14 day EDG AOT. Thus, 
    the 14 day EDG AOT does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Eliminating the 4.5.F.1 requirement for daily testing of the 
    operable diesel generator when the redundant diesel generator 
    becomes inoperable is consistent with the guidance provided in 
    Generic Letter 93-05. The change does not affect the ability of the 
    emergency diesel generator to perform on demand, and by actually 
    lowering the number of demands to demonstrate operability, reduces 
    the probability of equipment failure. The redundant EDG will remain 
    in service during the entire period of inoperability of the out-of-
    service EDG. If a common cause failure cannot be ruled out, the 
    redundant EDG will be tested to assure operability. The proposed 
    revisions do not involve a significant change to the plant design or 
    operation, only to the manner in which remaining equipment is 
    confirmed to be operable, which is consistent with NRC guidance. 
    Thus operation of PNPS in accordance with the proposed license 
    amendment will not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The 3.9.B.1 and 2 requirements to demonstrate both EDGs and 
    associated emergency buses operable are deleted. This change is 
    based on the NRC guidance provided in item 10.1 of Generic Letter 
    93-05, ``Line-Item Technical Specification Improvements to Reduce 
    Surveillance Requirements for Testing During Power Operation.'' 
    Revising the methods for verifying EDG and emergency bus operability 
    does not physically alter the plant or have an affect on the 
    probability or consequences of an accident previously evaluated. 
    Deleting the testing requirements for an EDG when the other EDG is 
    inoperable does not increase the probability or consequences of an 
    accident previously evaluated because the reliability program and 
    routinely performed TS surveillances continue to provide the added 
    assurance sought by the testing. The elimination of this testing 
    will serve to improve the overall reliability of the EDGs. Since the 
    proposed change does not affect the design or negatively affect the 
    performance of the EDGs, the change will not result in a significant 
    increase in the consequences or probability of an accident 
    previously analyzed.
        SGT [Standby Gas Treatment] and CRHEAF [Control Room High 
    Efficiency Air Filtration]
        During normal plant operation, with one SGT or CRHEAF subsystem 
    inoperable, the inoperable subsystem must be restored to operable 
    status in 7 days. In this condition, the remaining operable SGT or 
    CRHEAF subsystem is adequate to perform the required radioactivity 
    release control function. However, the overall system reliability is 
    reduced because a single failure in the operable subsystem could 
    result in the radioactivity release control function not being 
    adequately performed. The 7 day completion time is based on 
    consideration of such factors as the availability of the operable 
    redundant SGT subsystem and the low probability of a DBA [design 
    basis accident] occurring during this period.
        If the SGT or CRHEAF subsystem cannot be restored to operable 
    status within 7 days when in the Run, Startup, or Hot Shutdown MODE, 
    the plant must be brought to a MODE in which the LCO does not apply. 
    To achieve this status, the plant must be brought to at least Hot 
    Shutdown within 12 hours and to Cold Shutdown within 36 hours. The 
    allowed completion times are reasonable, based on operating 
    experience, to reach the required plant conditions from full power 
    conditions in an orderly manner and without challenging plant 
    systems.
        Current TS governing refueling operations restrict fuel movement 
    if one train of SGTS or one train of CRHEAF are inoperable. In this 
    condition the remaining operable SGT and CRHEAF trains are adequate 
    to perform the required radioactivity release control functions. 
    However, the overall system reliability is reduced because a single 
    failure in the operable train could result in the radioactivity 
    release control function of the systems not being adequately 
    performed. New requirements are added that require if one train of 
    SGT or CRHEAF is inoperable, the redundant train of SGT or CRHEAF 
    must be demonstrated to be operable within 2 hours. This 
    substantiates the availability of the operable trains. Fuel handling 
    is limited only to the following 7 days and if the inoperable train 
    is not returned to an operable condition within that time frame, the 
    operable SGT train is placed in operation or fuel handling 
    activities are suspended. For CRHEAF, after 7 days, the operable 
    subsystem is demonstrated operable in accordance with existing 
    surveillances on a daily basis. The proposed changes do not modify 
    system design, use, or configuration in a manner different from 
    their original design and therefore do not involve a significant 
    increase in the consequences or probability of an accident 
    previously analyzed.
        The revisions to make the SGT and CRHEAF TS sections similar in 
    wording are made to enhance usability and alleviate possible 
    confusion. These changes are strictly editorial, have no impact, and 
    do not alter
    
    [[Page 31174]]
    
    technical content or meaning of the specifications. These editorial 
    changes do not involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The operation of PNPS in accordance with the proposed license 
    amendment will not create the possibility of a new or different kind 
    of accident from any accident previously evaluated because of the 
    following:
        Definition of ``Operable-Operability''
        The revised definition redefines the AC power needs to allow 
    either onsite or offsite power available for systems/subsystems to 
    be considered operable. This does not compromise the level of safety 
    already afforded to such systems/subsystems because the functional 
    operability requirements continue to be assured through the 
    technical specifications applicable to such systems/subsystems. AC 
    power availability continues to be assured through existing and 
    proposed surveillances and action statements applicable to AC power 
    systems. Reducing the need for both onsite and offsite power sources 
    in order to consider operable, the systems/subsystems powered by 
    these AC power sources, provides additional operational flexibility 
    by allowing redundant systems/subsystems to still be considered 
    ``operable'' within the requirements of their functional operability 
    requirements. No new change or modes of plant operation are 
    involved. Therefore, operation in accordance with the revised 
    definition does not introduce any new or different kind of accident 
    from any accident previously evaluated.
        EDG
        The proposed amendment will extend the action completion/allowed 
    outage time for an inoperable emergency diesel generator from 72 
    hours to 14 days. The EDGs are designed as backup AC power sources 
    for essential safety systems in the event of loss of offsite power. 
    The proposed AOT does not change the conditions, operating 
    configurations or minimum amount of operating equipment assumed in 
    the safety analysis for accident mitigation. The EDGs and AC 
    equipment are not accident initiators. No change is being made in 
    the manner in which the EDG's provide plant protection. No new modes 
    of plant operation are involved. An extended AOT for one EDG does 
    not increase the probability of occurrence of a new or different 
    kind of accident previously evaluated. The PSA results concluded 
    that the risk contribution of the EDG AOT extension is 
    insignificant.
        The current Pilgrim Technical Specifications requiring immediate 
    and daily testing of the redundant operable EDG is based on the 
    assumption that the increased testing provides additional assurance 
    that the equipment is available should it be needed. Industry 
    experience indicates that repetitive testing can place demands and 
    wear on the EDG without necessarily providing additional confidence 
    of availability. Also, the new surveillance requires verification 
    that offsite power is available and that a common cause failure is 
    not present. These actions provide assurance that the required 
    emergency buses can be energized with no loss of functions to 
    mitigate accident or transient conditions. In addition, Pilgrim has 
    implemented an EDG reliability program to maintain reliability of 
    EDGs. The proposed change does not introduce any new mode of plant 
    operation or new accident precursors, involve any physical 
    alterations to plant configurations, or make changes to system set 
    points that could initiate a new or different kind of accident. 
    Therefore, operation in accordance with the proposed change does not 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
        The AOT for an inoperable Startup Transformer is reduced from 7 
    days to 72 hours based upon the PSA that was performed to 
    quantitatively assess the risk impact of the proposed amendment. The 
    proposed reduction in AOT improves overall AC power source 
    availability because the SUT will potentially be inoperable for 
    shorter time periods. Therefore, reducing the AOT does not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        SGT and CRHEAF
        The SGT system is designed to filter radioactive materials from 
    the secondary containment following a postulated DBA or fuel 
    handling accident prior to release to the environment to ensure 
    compliance with 10 CFR 100 limits.
        The CRHEAF is designed to filter intake air for the control room 
    atmosphere during conditions when normal intake air may be 
    contaminated.
        The proposed revisions do not affect the ability of the SGTS or 
    CRHEAF to perform their intended function, do not create the 
    possibility of a new or different kind of accident from the loss of 
    coolant or fuel handling accidents previously analyzed, and do not 
    modify system configuration, use, or design. Therefore, operating 
    Pilgrim in accordance with this change will not create the 
    possibility of a new or different kind of accident from any accident 
    previously analyzed.
        The revisions to make the SGT and CRHEAF TS sections similar in 
    wording are made to enhance usability and alleviate possible 
    confusion. These changes are strictly editorial, have no impact, and 
    do not alter technical content or meaning of the specifications. 
    These editorial changes do not create the possibility of a new or 
    different kind of accident from any previously analyzed.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The operation of PNPS in accordance with the proposed license 
    amendment will not involve a significant reduction in a margin of 
    safety because of the following:
        Definition of ``Operable-Operability''
        The implementation of the ``Operability'' definition clarifies 
    the relationship between AC power supplies and the operability 
    status of the equipment requiring AC power. No change is being made 
    in which the plant systems relied upon in the safety analyses 
    provide plant protection. Plant safety margins are maintained 
    through the limitations established in the TS LCOs. Since there will 
    be no significant reduction to the physical design or operation of 
    the plant there will be no significant reduction to any of these 
    margins.
        EDG
        Operation of PNPS in accordance with the proposed license 
    amendment will not involve a significant reduction in a margin of 
    safety. As shown in Part III [of the application dated April 25, 
    1996], incorporation of the proposed change involves an 
    insignificant reduction in the margin of safety.
        The proposed changes do not significantly reduce the basis for 
    any technical specification related to the establishment of, or the 
    maintenance of, a safety margin nor do they require physical 
    modifications to the plant. Additional conditions are added to the 
    Standby Liquid Control, Standby Gas Treatment, and Control Room High 
    Efficiency Air Filtration systems requiring the diesel generator 
    associated with the redundant operable trains of these systems to 
    remain operable while in the 14 day EDG AOT. Moreover, the PSA 
    results showed that the risk contribution of extending the AOT for 
    an inoperable EDG is insignificant. The reduction in the AOT for the 
    SUT could improve availability, therefore, reducing overall risk. 
    Likewise the proposed changes in the deletion of testing have no 
    impact on the safety margin.
        As previously stated, implementation of the proposed changes is 
    expected to result in an insignificant increase in: (1) power 
    unavailability to the emergency buses (given that a loss of offsite 
    power has occurred), and (2) core damage frequency. Implementation 
    of the proposed changes does not increase the consequences of a 
    previously analyzed accident nor significantly reduce a margin of 
    safety. Functioning of the EDGs and the manner in which limiting 
    conditions of operation are established are unaffected.
        SGT and CRHEAF
        SGT and CRHEAF contribute to the margin of safety by supporting 
    the secondary containment system during fuel handling by mitigating 
    the consequences of a fuel handling event. Allowing fuel movement to 
    continue as established in the LCOs does not involve a significant 
    reduction in the margin of safety because the first line of defense, 
    the other SGT and CRHEAF trains will be operable. The proposed 
    change will allow placing the Operable SGT subsystem in operation, 
    or in the case of CRHEAF, conducting daily testing, as an 
    alternative to suspending movement of irradiated fuel. This 
    alternative is less restrictive than the existing requirement, 
    however, the proposed requirements ensure that the remaining 
    subsystem is operable, that no failures that could prevent actuation 
    have occurred, and that any failure would be readily detected. The 
    proposed change does not result in a significant reduction in a 
    margin of safety because it allows operations which have the 
    potential for releasing radioactive material to the secondary 
    containment to continue only if the system designed to mitigate the
    
    [[Page 31175]]
    
    consequences of this release is functioning. Proper operation of 
    only one SGT or one CRHEAF subsystem is sufficient to mitigate the 
    consequences of any analyzed accident. Therefore, this change does 
    not change any of the assumptions in the accident analysis and does 
    not involve a significant reduction in a margin of safety.
        The revisions to make the SGT and CRHEAF TS sections similar in 
    wording are made to enhance usability and alleviate possible 
    confusion. These changes are strictly editorial, have no impact, and 
    do not alter technical content or meaning of the specifications. 
    These editorial changes do not involve a significant reduction in 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Jocelyn A. Mitchell, Acting
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of amendment request: April 22, 1996
        Description of amendment request: The licensee is proposing to 
    change the technical specifications to reflect a revision to the 
    overload cutoff limit on the manipulator crane inside the containment 
    at the Haddam Neck Plant. Due to a change in fuel design and supplier, 
    the heaviest fuel assembly design starting in Cycle 20 will be the 
    Westinghouse-supplied LOPAR design. Therefore, the heaviest combination 
    beginning in Cycle 20 will be the Westinghouse LOPAR fuel assembly with 
    a full-length rod cluster control assembly (RCCA) inserted. It will now 
    be used as the standard for the overload cutoff limit on the 
    manipulator crane.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. [The proposed change does not] involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change will revise the method of determining the 
    overload cutoff limit for the manipulator crane. The actual absolute 
    value of the cutoff limit will not be increased and will not affect 
    the [probability] of any plant accidents.
        Since there is no actual increase in the absolute overload 
    cutoff limit, there will be no adverse effects to the crane, cables, 
    or associated hardware. Therefore, there is no impact on the crane's 
    ability to perform its intended function. Even though the net 
    lifting forces on an individual assembly have increased 25 pounds, 
    the limit is within the recommended Westinghouse guidelines with 
    respect to fuel handling and will not result in potential damage to 
    assembly grids during fuel handling activities.
        As such, CYAPCO [Connecticut Yankee Atomic Power Company] has 
    concluded that these changes do not involve an increase in the 
    probability or consequences of an accident previously evaluated.
        2. [The proposed change does not] create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The changes conservatively revise the method of determining the 
    overload cutoff limit for the manipulator crane. There is no impact 
    on the basic functioning of plant systems or equipment. Therefore, 
    the change does not create a malfunction that is different from 
    those previously evaluated.
        As such, the proposed changes described above do not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. [The proposed change does not] involve a significant 
    reduction in a margin of safety.
        The proposed revisions in the methodology for determining the 
    overload cutoff limit for the manipulator crane is conservative and 
    in accordance with vendor standards. The changes do not adversely 
    affect any equipment credited in the safety analysis. Also, the 
    changes do not adversely affect the probability or consequences of 
    any plant accident, including the fuel handling accident or offsite 
    doses associated with those accidents.
        As such, the proposed changes have no significant impact on a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270
        NRC Project Director: Phillip F. McKee
    
    Duke Power Company, Docket Nos. 50-413 and 50-414, Catawba Nuclear 
    Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: December 14, 1995, as supplemented by 
    letter dated May 16, 1996
        Description of amendment request: The proposed amendments would 
    change the Technical Specifications (TS) to improve the TS Action 
    Statements and Surveillance Requirements for diesel generators in 
    accordance with the recommendations and guidance in Generic Letter 93-
    05, Generic Letter 94-01, NUREG-1366, and NUREG-1431. The proposed 
    amendments would also incorporate technical and administrative changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Criterion 1
        Operation of the facilities in accordance with the requested 
    amendments will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. 
    Improvements to the LCOs [limiting condition for operation] and 
    surveillance requirements for the emergency diesel generators do not 
    affect their capability to provide emergency power to plant vital 
    instruments and safety related equipment. In fact, these 
    improvements make the diesel generators more reliable since they 
    significantly reduce the amount of wear and stress due to excessive 
    and unnecessary testing. The proposed monthly testing of the diesel 
    generator continues to ensure that the system is ready for service 
    when needed. The fast starts and fast loadings continue to ensure 
    that the timing and loading requirements for engineered safety 
    features actuation are met. The proposed changes do not affect any 
    of the design basis accident analyses previously evaluated. 
    Therefore, these proposed changes do not involve any increase in the 
    probability or consequences of any accident previously evaluated. 
    The proposed changes are fully consistent with the recommendations 
    and guidance contained in GL [Generic Letter] 93-05, GL 94-01, 
    NUREG-1366, NUREG-1431, and are compatible with plant operating 
    experience.
        Criterion 2
        Operation of the facilities in accordance with the requested 
    amendments will not create the possibility of a new or different 
    kind of accident from any accident previously evaluated. The 
    proposed changes in fact improve the reliability of the diesel 
    generators by eliminating unnecessary wear and stress. Improved 
    reliability decreases the failure probability which also decreases 
    the probability of an accident not previously evaluated. None of the 
    requested amendments increase the common mode failure probability 
    thus would not increase the chance of both EDG's [emergency diesel
    
    [[Page 31176]]
    
    generators] for a particular nuclear unit being out of service 
    simultaneously. The proposed changes are fully consistent with the 
    recommendations and guidance contained in GL 93-05, GL 94-01, NUREG-
    1366, NUREG-1431, and are compatible with plant operating 
    experience.
        Criterion 3
        Operation of the facilities in accordance with the requested 
    amendments will not involve a significant reduction in a margin of 
    safety. The proposed monthly testing of the diesel generators 
    continues to ensure that the system is ready for service when 
    needed. The fast starts and fast loadings continue to ensure that 
    the timing and loading requirements for engineered safety features 
    actuation are met. The proposed changes improve the reliability of 
    the diesel generators. Implementation of the Maintenance Rule also 
    ensures continued reliability of the diesel generators. No margin of 
    safety is decreased as a result of these TS changes.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf 
    Nuclear Station, Unit 1, Claiborne County, Mississippi and Docket 
    No. 40-458, River Bend Station, Unit 1, West Feliciana Parish, 
    Louisiana
    
        Date of amendment request: April 18, 1996, as supplemented by 
    letter dated June 4, 1996
        Description of amendment request: The licensee has proposed to (1) 
    amend Limiting Condition for Operation (LCO) 3.10.6 and Surveillance 
    Requirement 3.10.6.3, and (2) add a Surveillance Requirement 3.10.6.4 
    of the Technical Specifications (TSs) for the Grand Gulf Nuclear 
    Station, Unit 1, and the River Bend Station, Unit 1, to allow another 
    method of fuel movement and loading in the core when control rods are 
    removed or withdrawn from defueled core cells. Currently, LCO 3.10.6 
    allows only fuel loading as part of the approved spiral reloading 
    sequence to prevent fuel loading into core cells in which the control 
    rod has been removed or withdrawn. This amendment request does not 
    withdraw this approved method, revise the frequency of performing the 
    surveillance during fuel loading, or alter the method of verifying the 
    fuel is being loaded in compliance with the approved method. Grand Gulf 
    Unit 1 and River Bend Unit 1 are both General Electric (GE) Boiling 
    Water Reactor (BWR)-6 plants, the latest version of the GE design 
    series.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Entergy Operations, Inc. [(EOI)] propose[d] to change the 
    current Grand Gulf Nuclear Station (GGNS) and River Bend Station 
    (RBS) Technical Specifications [(TSs)]. The specific proposed change 
    is to add an additional method of performing fuel loading into LCO 
    3.10.6, ``Multiple Control Rod Withdrawal - Refueling''. The 
    proposed change would allow fuel loading [in the core] if a positive 
    means of assuring fuel assemblies cannot be loaded into a core cell 
    with a withdrawn or removed control rod is in effect. [Currently, 
    the TSs for both plants allow fuel assembles to be loaded in 
    compliance with an approved spiral reload sequence which is used to 
    ensure the reactivity additions are minimized. Spiral loadings 
    encompass reloading a core cell on the edge of a continuous fueled 
    region.]
        The Commission has provided standards for determining whether a 
    no significant hazards consideration exists as stated in 10 CFR 
    50.92(c). A proposed amendment to an operating license involves no 
    significant hazards consideration if operation of the facility in 
    accordance with the proposed amendment would not: (1) involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated; or (3) involve a significant reduction in a margin of 
    safety.
        Entergy Operations, Inc. [EOI] has evaluated the no significant 
    hazards consideration in its request for this license amendment and 
    determined that no significant hazards consideration results from 
    this change. In accordance with 10 CFR 50.91(a), Entergy Operations, 
    Inc. [EOI] is providing the analysis of the proposed amendment 
    against the three standards in 10 CFR 50.92(c). A description of the 
    no significant hazards consideration determination follows:
        I. The proposed change does not significantly increase the 
    probability or consequences of an accident previously evaluated.
        The refueling interlocks (i.e., the refueling equipment and one-
    rod-out interlocks) allowed to be bypassed by Technical 
    Specification [TS] LCO 3.10.6 are explicitly assumed in the analysis 
    of the control rod removal error or fuel loading error during 
    refueling. This analysis evaluates the consequences of control rod 
    withdrawal during refueling. Criticality and, therefore, subsequent 
    prompt reactivity excursions are prevented during the insertion of 
    fuel, provided all control rods are fully inserted during the fuel 
    insertion. The refueling interlocks accomplish this by preventing 
    loading fuel into the core with any control rod withdrawn, or by 
    preventing withdrawal of a rod from the core during fuel loading.
        LCO 3.10.6 allows multiple control rod withdrawals, control rod 
    removals, associated control rod drive (CRD) removal, or any 
    combination of these, and the ``full in'' position indication input 
    to the refueling interlocks is allowed to be bypassed for each 
    withdrawn control rod if all fuel has been removed from the cell. 
    This supports the GGNS Updated Final Safety Analyses Report (UFSAR) 
    and RBS Updated Safety Analyses Report (USAR) analyses since, with 
    no fuel assemblies in the core cell, the associated control rod has 
    no reactivity control function and does not need to remain inserted. 
    Prior to reloading fuel into the cell, however, the associated 
    control rod must be inserted to ensure that an inadvertent 
    criticality does not occur, as evaluated in the analysis.
        The Technical Specification [TS] requirements prohibiting fuel 
    loading was placed in the Technical Specifications [TSs] for GGNS 
    and RBS as part of the originally enforced Technical Specification 
    [TS] requirements to resolve NRC concerns identified in IE 
    Information Notice No. 83-35, ``Fuel Movement with Control Rods 
    Withdrawn at BWRs,'' (IEN 83-35). IEN 83-35 details instances where 
    fuel assemblies were loaded into core cells while the control rod 
    was withdrawn and discusses that the General Electric Company (GE) 
    had issued Service Information Letter (SIL) No. 372.
        SIL No. 372 discusses a potential event where 8 fuel assemblies 
    are loaded into 2 [two] adjacent core cells where the control rods 
    are withdrawn and no action is taken to recover from the errors. In 
    this SIL GE identified that the probability of such an event 
    occurring was extremely low but potentially slightly higher than 
    10-6 probability of the event even further to where it need not 
    be considered credible (i.e., below 10-6 per reactor year), GE 
    recommended that the additional administrative control of 
    prohibiting loading fuel with withdrawn rods be enforced.
        The proposed change will only provide an additional way to meet 
    the intent of the original GE recommendation. [The currently 
    approved method is listed in LCO 3.10.6 and Surveillance Requirement 
    3.10.6.3.]. The proposed change will provide the additional 
    allowance to perform fuel loading only if an additional positive 
    means of assuring fuel assemblies cannot be loaded into a core cell 
    with a withdrawn or removed control rod is in effect. The positive 
    means will entail a physical barrier such that, even if refueling 
    procedures were violated and an attempt was made to load a fuel 
    assembly into a core cell with a withdrawn or removed control rod, 
    the action would be prevented. This requirement provides sufficient 
    additional restrictions to meet the intent of the GE recommendation 
    to add additional administrative controls to prevent the postulated 
    event from occurring.
        The probability of an inadvertent criticality occurring will 
    continue to be precluded by
    
    [[Page 31177]]
    
    the same number of layers of administrative controls [as the 
    currently approved method]; therefore, the proposed change does not 
    significantly increase the probability or consequences of an 
    accident previously evaluated.
        II. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The administrative changes in the Technical Specification [TS] 
    requirements do not involve a change in the design of the plant. The 
    proposed requirements will continue to ensure that fuel is not 
    loaded into a core cell that is associated with a removed or 
    withdrawn control rod.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        III. The proposed change does not involve a significant 
    reduction in a margin of safety.
        The margin of safety associated with criticality events during 
    fuel handling is provided by the event being a non credible event. 
    The proposed change will only provide an additional means to meet 
    the same intent of ensuring that the event is of such low 
    probability as to be considered non credible. The proposed change 
    will provide the additional allowance to perform fuel loading only 
    if an additional positive means of assuring fuel assemblies cannot 
    be loaded into a core cell with a withdrawn or removed control rod 
    is in effect. The positive means will entail a physical barrier such 
    that even if refueling procedures were violated and an attempt was 
    made to load a fuel assembly into a core cell with a withdrawn or 
    removed control rod the action would be prevented. This requirement 
    provides sufficient additional restrictions to ensure that the event 
    is of such low probability as to be considered non credible.
        The probability of an inadvertent criticality occurring will 
    continue to be precluded by the same number of layers of 
    administrative controls [as the currently approved method]; 
    therefore, this change does not reduce the level of safety imposed 
    by the current Technical Specification [TS] requirements.
        Therefore, the proposed changes do not cause a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: (1) Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120, for Grand Gulf 
    Nuclear Station and (2) Government Documents Department, Louisiana 
    State University, Baton Rouge, LA 70803, for River Bend Station.
        Attorney for licensee: (1) Nicholas S. Reynolds, Esquire, Winston 
    and Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502, 
    for Grand Gulf Nuclear Station and (2) Mark Wetterhahn, Esq., Winston & 
    Strawn, 1400 L Street, N.W., Washington, DC 20005, for River Bend 
    Station.
        NRC Project Director: William D. Beckner
    
    Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf 
    Nuclear Station, Unit 1, Claiborne County, Mississippi
    
        Date of amendment request: May 9, 1996
        Description of amendment request: The amendment request would allow 
    allow the licensee to perform the surveillance of the relief mode of 
    operation of each of the 20 safety/relief valves (S/RVs) on the 4 main 
    steam lines without physically lifting the disk off the seat at power. 
    The proposed changes are to Surveillance Requirements (SRs) 3.4.4.3, 
    Safety/Relief Valves, 3.5.1.7, Automatic Depressurization System 
    Valves, and 3.6.1.6.1, Low-Low Set Valves, of the Technical 
    Specifications, and the changes would state that the required operation 
    of the valve to verify is that the relief-mode actuator strokes when 
    the valve is manually actuated. Each S/RV is a Dikkers, 8 X 10, direct-
    acting, spring loaded, safety valve with attached pneumatic actuator 
    for relief-mode operation. Eight of the S/RVs use the relief mode to 
    perform the Automatic Depressurization System (ADS) function. Also, six 
    S/RVs, two of which are also ADS S/RVs, use the relief mode to perform 
    the Low-Low Set valve function. The licensee also proposed changes to 
    the Bases of the Technical Specifications that are associated with the 
    above proposed changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below: The Dikkers S/RV provides 
    pressure relief based on the principle of vertically moving the stem 
    that attaches directly to the valve disk. The force that provides the 
    stem movement is provided by one of two sources; the vessel pressure 
    directly against the force of the stem spring (safety mode), or the 
    pneumatic actuator arm against the force of the stem spring (relief 
    mode). ASME Boiler and Pressure Vessel Code requires testing the safety 
    mode of operation once every five year operating cycle. Once a safety 
    valve is installed, the safety mode is never tested while the S/RV is 
    installed in the plant. The testing of the relief mode of operation for 
    a direct-acting S/RV provides verification that the control functions 
    of electrical and pneumatic connections have been properly reconnected, 
    and that the actuator arm will provide the necessary force to operate 
    the S/RV.
        This proposed change provides verification of proper control 
    connections by requiring the pneumatic and electrical controls to 
    cycle the actuator arm on each S/RV after installation in the 
    drywell. The test population of S/RVs removed each outage for safety 
    setpoint testing will be tested in the relief mode. This testing 
    will demonstrate that the installed S/RVs will function properly in 
    the relief mode. The remaining installed S/RVs will continue to be 
    tested for proper system function. As presently required by GGNS 
    Technical Specifications and administrative procedures, proper 
    operation of the solenoid control block will be demonstrated by 
    providing an open signal to each S/RV, with a check to verify that 
    each solenoid valve repositions. Verification of proper solenoid 
    valve operation, in addition to the proper relief-mode operation of 
    the test population, provides assurance that the S/RV will perform 
    as expected when control air pressure is applied to the solenoid 
    valve control block.
        Entergy Operations, Inc. is proposing that the Grand Gulf 
    Nuclear Station Operating License be amended to perform the 
    surveillance of each safety relief valve (S/RV) relief mode of 
    operation without physically lifting the disk off the seat at power.
        During the refueling outage, a sample population of the S/RVs 
    will be removed for safety-mode setpoint testing in accordance with 
    the GGNS IST program, using ASME Boiler and Pressure Vessel Code, 
    Section XI. Each of these removed S/RVs will be tested in the relief 
    mode to verify that the pneumatic actuator functions correctly, and 
    this test sample will be used to provide assurance that the 
    installed S/RV pneumatic actuators will function properly. After the 
    test sample of S/RVs has been replaced with recertified spares, and 
    S/RV controls have been connected, the upper stem nut that couples 
    the valve stem to each newly- installed S/RV's pneumatic actuator 
    will be moved up the stem to allow an uncoupled actuation of the 
    relief-mode actuator. Control air pressure to each actuator will be 
    reduced from normal system pressure to prevent damaging the 
    pneumatic relief-mode actuator. The actuator will be remotely 
    operated from the control room, as required by current test methods, 
    and visual verification will be performed for proper actuator 
    response and range of motion. After proper actuator operation has 
    been verified, the upper stem nut will be returned to its operating 
    stem location. Verification of proper system logic controls and 
    function for every installed S/RV will continue to be performed, as 
    required by Technical Specifications.
        The commission has provided standards for determining whether a 
    no significant hazards consideration exists as stated in 10 CFR 
    50.92(c). A proposed amendment to an operating license involves no 
    significant hazards if the operation of the facility in accordance 
    with the proposed amendment would not: (1) involve a significant 
    increase
    
    [[Page 31178]]
    
    in the probability or consequences of an accident previously 
    evaluated; or (2) create the possibility of a new or different kind 
    of accident from any accident previously evaluated; or (3) involve a 
    significant reduction in a margin of safety.
        Entergy Operations has evaluated the no significant hazards 
    considerations in its request for a license amendment. In accordance 
    with 10 CFR 50.91(a), Entergy Operations, Inc. is providing the 
    following analysis of the proposed amendment against the three 
    standards in 10 CFR 50.92:
        a. No significant increase in the probability or consequences of 
    an accident previously evaluated results from this change.
        Each refueling outage, a test sample of the population of S/RVs 
    is removed from the plant to perform testing as required by ASME 
    Boiler and Pressure Vessel Code, Section XI. These S/RVs will be 
    stroked in the relief mode during as-found testing, and are 
    therefore verified to operate properly when each S/RV stem is raised 
    by the relief-mode pneumatic actuator. This proposed surveillance 
    verifies proper S/RV relief-mode operation of all installed S/RVs 
    based upon this test sample. This testing, in conjunction with 
    replacement of each S/RV prior to the end of its expected service 
    life, provides reasonable assurance that the installed S/RVs will 
    perform as well as the test population of S/RVs.
        After the S/RVs have been replaced in the plant, and after all 
    controls are reconnected, the relief-mode actuator on each newly-
    installed S/RV will be uncoupled from the S/RV stem, and stroked. 
    This actuator stroke will verify that no damage has occurred to the 
    relief-mode actuator during S/RV transportation from its storage 
    location to its operating location. The direct coupling of the valve 
    stem to disk provides assurance that proper relief actuation will 
    occur when the actuator is operated. The safety-mode components are 
    completely encased within the valve body and bonnet, which provides 
    a rugged structure to prevent damage to these components. The 
    remaining installed S/RVs will continue to be tested for proper 
    control system function as previously required by Technical 
    Specifications. The direct coupling of the S/RV stem to disk 
    provides assurance that proper relief-mode actuation will occur when 
    the actuator is operated. The safety mode of the GGNS S/RVs is not 
    affected by a malfunction of the relief-mode components.
        Blockage of each S/RV discharge line will be prevented by the 
    same Foreign Material Exclusion (FME) controls that exist for other 
    reactor vessel and support systems. These FME controls, combined 
    with the horizontal orientation of the S/RV discharge piping mating 
    surfaces, provide reasonable assurance that discharge line blockage 
    will not occur.
        Therefore, no significant increase in the probability or 
    consequences of an accident previously evaluated results from this 
    proposed change.
        b. This change would not create the possibility of a new or 
    different kind of accident from any previously analyzed.
        The proposed change demonstrates that each S/RV will perform its 
    intended relief-mode function, which is the intent of the present 
    surveillance. The relief mode of S/RV operation is demonstrated to 
    be operable based upon successful performance of a test population, 
    S/RV component service life, and existing Technical Specification 
    surveillances. No new failure mechanisms to the relief- mode of 
    operation are introduced, as the proposed surveillance verifies 
    relief actuator operability. Plant FME controls, combined with the 
    horizontal orientation of the S/RV discharge piping mating flange, 
    provides reasonable assurance that discharge line blockage will not 
    occur. This proposed change does not add any new systems, 
    structures, or components, nor does it introduce new S/RV operating 
    modes.
        Therefore, this change would not create the possibility of a new 
    or different kind of accident from any previously analyzed.
        c. This change would not involve a significant reduction in the 
    margin of safety.
        This proposed change will verify that the relief mode of all 
    installed S/RVs will operate properly based upon demonstrated relief 
    mode performance of a sample of S/RVs. The failure mode of the S/RV 
    relief function would require a failure of either the pneumatic 
    actuator, lifting linkage, or solenoid block. Each of these items 
    has been verified to have a service life exceeding the replacement 
    cycle of each S/RV. Therefore, proper operation of a sample 
    population of S/RVs provides reasonable assurance that the remaining 
    S/RVs would perform identically, within the original margin of 
    expected S/RV operability. In addition, each S/RVFEs solenoid block 
    and control functions will continue to be tested and cycled each 
    refueling outage. The removal of the valve stroke surveillance for 
    all S/RVs does not increase the possibility of valve malfunction, 
    since valve stroke is verified during the as-found testing of the 
    sample population of S/RVs. This proposed surveillance test reduces 
    the number of S/RV actuations, and therefore, reduces challenges to 
    the system both mechanically and thermally. Also, the proposed 
    alternative method of testing reduces the possibility of a stuck-
    open S/RV, since this proposed method will not stroke the S/RVs with 
    the reactor pressurized during reactor power operations.
        Therefore, this change would not involve a significant reduction 
    in the margin of safety.
        Based on the above evaluation, Entergy Operations, Inc. has 
    concluded that operation in accordance with the proposed amendment 
    involves no significant hazards considerations.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf 
    Nuclear Station, Unit 1, Claiborne County, Mississippi
    
        Date of amendment request: May 31, 1996
        Description of amendment request: The amendment would provide an 
    alternative method to compensate for inoperable refueling equipment 
    interlocks. The alternative method would be to insert a control rod 
    withdrawal block and verify that all control rods are fully inserted; 
    however, the control rods required to be inserted would not apply to 
    those control rods withdrawn in accordance with LCO 3.10.6, ``Multiple 
    Control Rod Withdrawal -Refueling.'' The amendment would add an 
    additional Required Action for Limiting Condition for Operation (LCO) 
    3.9.1, ``Refueling Equipment Interlocks,'' of the Technical 
    Specifications (TSs) for Grand Gulf Nuclear Station, Unit 1 (GGNS). The 
    alternative method then could be used to respond to inoperable 
    interlocks instead of only the current method of halting in-vessel fuel 
    movement with equipment associated with the inoperable interlock.
        The proposed change does not remove the current Required Action 
    method for LCO 3.9.1 and does not change the surveillance requirements 
    on the refueling equipment. The licensee has also provided changes to 
    the Bases of the TSs for the proposed amendment.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The licensee has proposed the amendment for the TSs for 
    both GGNS and River Bend Station (RBS). References made to the RBS TSs 
    and to RBS in the licensee's analysis of no significant hazards 
    consideration have been removed and replaced by [...]. The licensee's 
    analysis is presented below:
        Entergy Operations, Inc. proposes to change the current Grand 
    Gulf Nuclear Station (GGNS) [...] Technical Specifications. The 
    specific proposed change adds additional acceptable Required Actions 
    to the Actions of LCO 3.9.1, ``Refueling Equipment Interlocks,'' 
    [for inoperable interlocks]. The additional Required Actions will 
    add an alternative [method] to [the current method of] suspending 
    fuel movement in the reactor vessel when the refueling interlocks 
    are inoperable. The requested alternative is to insert a control rod 
    withdrawal block
    
    [[Page 31179]]
    
    immediately and verify all control rods required to be inserted are 
    fully inserted. [The control rods required to be inserted would not 
    apply to control rods withdrawn in accordance with LCO 3.10.6, 
    ``Multiple Control Rod Withdrawal--Refueling.'']
        The Commission has provided standards for determining whether a 
    no significant hazards consideration exists as stated in 10 CFR 
    50.92(c). A proposed amendment to an operating license involves no 
    significant hazards consideration if operation of the facility in 
    accordance with the proposed amendment would not: (1) involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated; or (3) involve a significant reduction in a margin of 
    safety.
        Entergy Operations, Inc. has evaluated the [criteria for] no 
    significant hazards consideration in its request for this license 
    amendment and determined that no significant hazards consideration 
    results from this change. In accordance with 10 CFR 50.91(a), 
    Entergy Operations, Inc. is providing the analysis of the proposed 
    amendment against the three standards in 10 CFR 50.92(c). A 
    description of the no significant hazards consideration 
    determination follows:
        I. The proposed change does not significantly increase the 
    probability or consequences of an accident previously evaluated.
        The refueling interlocks are explicitly assumed in the GGNS 
    Updated Final Safety Analyses Report (UFSAR) [...] analysis of the 
    control rod removal error or fuel loading error during refueling. 
    This analysis evaluates the probability and consequences of control 
    rod withdrawal during refueling. Criticality and, therefore, 
    subsequent prompt reactivity excursions are prevented during the 
    insertion of fuel, provided all control rods are fully inserted 
    during the fuel insertion. The refueling interlocks accomplish this 
    by preventing loading fuel into the core with any control rod 
    withdrawn, or by preventing withdrawal of a rod from the core during 
    fuel loading.
        When the refueling interlocks are inoperable the current method 
    of preventing the insertion of fuel when a control rod is withdrawn 
    is to prevent fuel movement. This method is currently required by 
    the Technical Specifications. An alternate method to ensure that 
    fuel is not loaded into a cell with the control rod withdrawn is to 
    prevent control rods from being withdrawn and verify that all 
    control rods required to be inserted are fully inserted. The 
    proposed actions will require that a control rod block be placed in 
    effect thereby ensuring that control rods are not subsequently 
    inappropriately withdrawn. Additionally, following placing the 
    control rod withdrawal block in effect, the proposed actions will 
    require that all required control rods be verified to be fully 
    inserted. This verification is in addition to the requirements to 
    periodically verify control rod position by other Technical 
    Specification requirements. These proposed actions will ensure that 
    control rods are not withdrawn and cannot be inappropriately 
    withdrawn because an electrical or hydraulic block to control rod 
    withdrawal is in place. Like the current requirements the proposed 
    actions will ensure that unacceptable operations are blocked (e.g., 
    loading fuel into a cell with a control rod withdrawn [would be 
    blocked]).
        The proposed additional acceptable Required Actions provide the 
    same level of assurance that fuel will not be loaded into a core 
    cell with a control rod withdrawn as the current Required Action or 
    the Technical Specification Surveillance Requirement.
        Therefore, the proposed change does not significantly increase 
    the probability or consequences of an accident previously evaluated.
        II. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The change in the Technical Specification requirements does not 
    involve a change in plant design. The proposed requirements will 
    continue to ensure that fuel is not loaded into the core when a 
    control rod is withdrawn except following the requirements of LCO 
    3.10.6, ``Multiple Control Rod Removal--Refueling,'' which is 
    unaffected by this change.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        III. The proposed change does not involve a significant 
    reduction in a margin of safety.
        As discussed in the Bases for the affected Technical 
    Specification requirements, inadvertent criticality is prevented 
    during the insertion of fuel provided all control rods are fully 
    inserted during the fuel insertion. The refueling interlocks 
    function to support the refueling procedures by preventing control 
    rod withdrawal during fuel movement and the inadvertent loading of 
    fuel when a control rod is withdrawn.
        The proposed change will allow the refueling interlocks to be 
    inoperable and fuel movement to continue only if a control rod 
    withdrawal block is in effect and all required control rods are 
    verified to be fully inserted. These proposed Required Actions 
    provide the same level of protection as the refueling interlocks by 
    preventing a configuration which could lead to an inadvertent 
    criticality event. The refueling procedures will continue to be 
    supported by the proposed required actions because control rods 
    cannot be withdrawn and as a result fuel cannot be inadvertently 
    loaded when a control rod is withdrawn.
        Therefore, the proposed changes do not cause a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf 
    Nuclear Station, Unit 1, Claiborne County, Mississippi
    
        Date of amendment request: May 31, 1996, as supplemented by letter 
    dated May 2, 1996.
        Description of amendment request: The amendment request would 
    revise the current reactor vessel material surveillance program 
    schedule for GGNS. This is the schedule for withdrawing surveillance 
    capsules from the reactor vessel for testing to measure the impact of 
    neutron irradiation of the vessel material and is required by Section 
    III.B.3 of Appendix H, ``Reactor Vessel Material Surveillance Program 
    Requirements,'' of 10 CFR Part 50. The schedule must be approved by the 
    Nuclear Regulatory Commission (NRC) before implementation.
        For GGNS, there are three surveillance capsules inside the reactor 
    vessel, each of which contains specimens of the reactor vessel 
    material. The first capsule was removed from the reactor vessel on May 
    7, 1995, during the 7th refueling outage. Because no useful data is 
    expected from testing the material specimens in the first capsule, the 
    request would allow the first capsule to be placed back into the 
    vessel.
        As part of revising the schedule, the licensee is also renumbering 
    the three surveillance capsules so that the capsule removed at the 7th 
    refueling outage becomes the third capsule when it is placed back in 
    the vessel. The proposed change would, however, not extend the time 
    that the next capsule (the renumbered first capsule) would be withdrawn 
    from the GGNS reactor vessel.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Entergy Operations, Inc., proposes to change the withdrawal 
    schedule for the reactor vessel material surveillance capsules [and 
    renumber the capsules]. The revised schedule for withdrawal of the 
    surveillance capsules is withdrawal of the first capsule at 24 
    Effective Full Power Years. The withdrawal schedule for the second 
    capsule is to be determined at a later date. The third capsule which 
    was withdrawn on May 7, 1995 is to be returned to reactor vessel 
    during
    
    [[Page 31180]]
    
    the Fall, 1996 outage and retained as a standby. [The current 
    schedule for withdrawal of the three capsules is 8 and 24 Effective 
    Full Power Years for the first two capsules, and the third capsule 
    is a spare with no specific schedule for withdrawal.]
        The Commission has provided standards for determining whether a 
    no significant hazards consideration exists as stated in 10 CFR 
    50.92(c). A proposed amendment to an operating license involves no 
    significant hazards consideration if operation of the facility in 
    accordance with the proposed amendment would not: (1) involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated; or (3) involve a significant reduction in a margin of 
    safety.
        In consideration of the October 4, 1995, decision of the Atomic 
    Safety and Licensing Board concerning an amendment request from 
    Perry Nuclear Power Plant, Entergy Operations, Inc. has evaluated 
    the no significant hazards consideration in its request for a change 
    to the withdrawal schedule required by 10 CFR 50, Appendix H, and 
    determined that no significant hazards consideration results from 
    this change. In accordance with 10 CFR 50.91(a), Entergy Operations, 
    Inc. is providing the analysis of the proposed amendment against the 
    three standards in 10 CFR 50.92(c):
        I. The proposed change does not significantly increase the 
    probability or consequences of an accident previously evaluated.
        The change revises the withdrawal schedule for the reactor 
    vessel material surveillance capsules and returns a withdrawn 
    capsule to the reactor vessel. The capsules [only contain specimens 
    of the reactor vessel material and] are not an initiator of any 
    previously analyzed accident. The withdrawal or return of the 
    surveillance capsule does not effect the probability or consequences 
    of any previously analyzed accident. Extending the time for 
    withdrawal of the first capsule and returning the withdrawn capsule 
    to the vessel do not adversely affect the pressure temperature limit 
    curves for the reactor vessel. Regulatory Guide 1.99 [, ``Effects of 
    Residual Elements on Predicted Radiation Damage to Reactor Vessel 
    Materials,''] is currently used to prepare the pressure temperature 
    limit curves and is inherently conservative for boiling water 
    reactors (BWRs)[, as GGNS]. The current pressure temperature limit 
    curves will continue to be adhered to. Additionally, [GGNS] 
    participates in the supplemental test program designed to 
    significantly increase the amount of BWR surveillance data. [This 
    program has supplemental capsules which were installed in the Cooper 
    and Oyster Creek Nuclear Power Plants, which contain the limiting 
    GGNS weld and plate vessel material, and which will be withdrawn in 
    1996, 2000, and 2002.] This program will be used to complement the 
    GGNS surveillance program such that postponement of the capsule 
    withdrawals will have minimal impact on the understanding of the 
    irradiation effects on the GGNS vessel.
        [The licensee stated in its May 2, 1996, letter that testing of 
    the specimens in the removed capsule may not provide useful 
    indicators of the damage to the vessel material because the low 
    neutron fluence on the vessel and the good material chemistry will 
    result in a minimal null-ductility temperature shift. Testing the 
    material specimens will destroy them; however, placing the capsule 
    back in the vessel will allow the specimens to have more irradiation 
    until useful data could be obtained from testing the specimens.]
        Therefore, the proposed change does not significantly increase 
    the probability or consequences of an accident previously evaluated.
        II. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Returning the withdrawn capsule to the vessel and postponing the 
    withdrawal of the first capsule do not contribute to the possibility 
    of a new or different kind of accident or [plant] malfunction from 
    those previously analyzed [in the Updated Final Safety Analysis 
    Report for GGNS]. Failure of the reactor vessel is not a credible 
    accident since the vessel itself is a highly reliable component. 
    This change does not affect that determination. The potential for 
    reactor vessel cracking will be adequately assessed by the proposed 
    withdrawal schedule.
        [The licensee stated in its May 2, 1996, letter that testing of 
    the specimens in the removed capsule may not be useful indicators of 
    the damage to the vessel material because the low neutron fluence on 
    the vessel and good material chemistry will result in a minimal 
    shift.]
        In addition, the results from the supplemental test program will 
    provide indication of the condition of the vessel until the data 
    from the first GGNS capsule[, withdrawn and tested,] are available. 
    The proposed change provides the same level of confidence in the 
    integrity of the vessel. The pressure temperature curves are 
    currently controlled by the Technical Specifications and are 
    determined using the conservative methodology in Regulatory Guide 
    1.99. Therefore, the possibility of failure of the reactor vessel is 
    not increased. The proposed change does not involve a change in the 
    design of the plant. The current pressure temperature limit curves 
    are inherently conservative and will continue to be adhered to.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        III. The proposed change does not involve a significant 
    reduction in a margin of safety.
        The current pressure temperature limit curves [for the reactor 
    vessel] are inherently conservative and provide sufficient margin to 
    ensure the integrity of the reactor vessel. The [proposed] changes 
    do not adversely affect these curves. The supplemental test program 
    will be used to complement the GGNS surveillance program such that 
    postponement of the capsule withdrawal [and testing] will have 
    minimal impact on the understanding of irradiation effects on the 
    GGNS vessel. The capsules removed in 1996 as part of the 
    supplemental program will have a [neutron] fluence higher than the 
    25% of the design life fluence used in establishing the original 
    GGNS [reactor vessel material surveillance program] schedule; 
    therefore, the use of the supplemental test program results will 
    meet the intent of the original test schedule.
        Therefore, the proposed changes do not result in a significant 
    reduction in the margin of safety.
        Based on the above evaluation, Entergy Operations, Inc. has 
    concluded that operation in accordance with the proposed change 
    involves no significant hazards consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Dates of amendment request: March 21, 1996, and May 13, 1996
        Description of amendment request: The licensee proposed to change 
    the Turkey Point Units 3 and 4 Technical Specifications (TS) to 
    relocate the requirements of the Radiological Effluent Technical 
    Specifications (RETS) to other documents.
        The proposed amendments would relocate the LIMITING CONDITIONS FOR 
    OPERATION (LCO) and SURVEILLANCE REQUIREMENTS associated with the RETS 
    in accordance with GL 89-01, NUREG-1301, and NUREG-1431, Rev. 1. The 
    definition in TS 1.15, ``Members of the Public,'' would be deleted 
    since it is already located in 10 CFR Part 20 and has been inserted 
    into the Offsite Dose Calculation Manual (ODCM). The definitions for 
    the ODCM and Process Control Program (PCP) would be relocated to the 
    Administrative Controls section of the TS. TS 3/4.3.3.5 and the 
    radioactive gaseous effluent portion of TS 3/4.3.3.6 and associated 
    tables, instrumentation operational conditions, remedial actions and 
    surveillance requirements would be controlled through the ODCM or PCP 
    and associated procedures. Technical
    
    [[Page 31181]]
    
    Specification Administrative Control sections would contain the 
    programmatic controls for the ODCM and PCP. The remaining portion of TS 
    3.3.3.6 would retain the operational conditions, remedial actions, and 
    surveillance requirements for the explosive gas monitor 
    instrumentation.
        The procedural details of the current TS on radioactive effluents 
    and radiological environmental monitoring would be deleted. Associated 
    operational conditions, remedial actions and surveillance requirements 
    presently in the Technical Specifications would be controlled through 
    the ODCM or PCP.
        Administrative changes to the TS were also proposed due to 
    paragraph and section numbering changes and relocations associated with 
    the proposed technical changes.
        New sections TS 6.8.4f and 6.8.4g were proposed to provide 
    programmatic controls for the Radiological Effluents Controls Program 
    and the Radiological Environmental Monitoring Program.
        TS 6.9.1.3 and TS 6.9.1.4 would be simplified and the reporting 
    details now contained in these specifications would be relocated to the 
    ODCM or PCP with the exception of the requirement to report licensee-
    initiated changes to the PCP in the Annual Radioactive Effluent Release 
    Report.
        New record retention requirements changes for the ODCM and PCP 
    would be added to TS 6.10.3q.
        In summary, as provided in the guidance, the current technical 
    content of the specifications which would be transferred to the ODCM or 
    the PCP. New programmatic controls for radioactive effluents and 
    radioactive effluent monitoring would be added to the TS, as well as 
    further clarification to the definitions of the ODCM and PCP. The 
    Technical Specification requirements for Gas Decay Tanks and Explosive 
    Gas Mixture would be relocated to the Plant Systems section of the TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
        (1)Operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The changes being proposed are administrative in nature in that 
    they relocate Technical Specification requirements associated with 
    RETS from the Technical Specifications to the ODCM or PCP. These 
    changes are in accordance with the recommendations contained in GL 
    89-01, NUREG 1301, and NUREG 1431 Rev. 1. The only change being made 
    to existing requirements or commitments are administrative in 
    nature. The proposed changes do not involve any change to the 
    configuration or method of operation of any plant equipment that is 
    used to mitigate the consequences of an accident, nor do they affect 
    any assumptions or conditions in any of the accident analyses. Since 
    the accident analyses remain bounding, their probability or 
    consequences are not adversely affected. Therefore, the probability 
    or consequences of an accident previously evaluated are not 
    affected.
        (2) Operation of the facility in accordance with the proposed 
    amendments would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The changes being proposed are administrative in nature in that 
    they relocate Technical Specification requirements associated with 
    RETS from the Technical Specifications to the ODCM or PCP. These 
    changes are in accordance with the recommendations contained in GL 
    89-01, NUREG 1301, and NUREG 1431, Rev. 1. The only change being 
    made to existing requirements or commitments are administrative in 
    nature. The proposed changes do not involve any change to the 
    configuration or method of operation of any plant equipment used to 
    mitigate the consequences of an accident.
        Therefore, the possibility of a new or different kind of 
    accident from any accident previously evaluated would not be 
    created.
        (3) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant reduction in a margin of 
    safety.
        The changes being proposed are administrative in nature in that 
    they relocate Technical Specification requirements associated with 
    RETS from the Technical Specifications to the ODCM or PCP. These 
    changes are in accordance with the recommendations contained in GL 
    89-01, NUREG 1301, and NUREG 1431, Rev. 1. The only change being 
    made to existing requirements or commitments are administrative in 
    nature. All technical content is preserved. The operating limits and 
    functional capabilities of the affected systems, structures, and 
    components are unchanged by the proposed amendments.
        Therefore, a significant reduction in a margin of safety would 
    not be involved.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199
        Attorney for licensee: J. R. Newman, Esquire, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036
        NRC Project Director: Frederick J. Hebdon
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Dates of amendment request: May 28, 1996
        Description of amendment request: The licensee proposed to change 
    the Turkey Point Units 3 and 4 Technical Specifications (TS) to change 
    the licensed qualifications of the Operations Manager. The proposed 
    change would delete the qualification option that the Operations Manger 
    could have held a Senior Reactor Operator License on a boiling water 
    reactor and replace it with an option that this individual could have 
    completed the Turkey Point Nuclear Plant Senior Management Operation 
    Training Course (i.e., certified at an appropriate simulator for 
    equivalent senior operator knowledge level).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The change being proposed is administrative in nature, addresses 
    organizational personnel qualification issues, and does not affect 
    assumptions contained in plant safety analyses, the physical design 
    and/or operation of the plant, or Technical Specifications that 
    preserve safety analysis assumptions.
        The individual Florida Power & Light Company (FPL) chooses to 
    fill the position of Operations Manager will have extensive 
    educational and management- level nuclear power experience meeting 
    the criteria of ANSI N18.1-1971. The Operations Supervisor and 
    Nuclear Plant Supervisors maintain SRO licenses on Turkey Point. The 
    current Technical Specifications do not require the Operations 
    Manager to hold an SRO License at Turkey Point. The current 
    Technical Specifications permit the Operations Manager to have held 
    an SRO License on another plant. The proposed change will continue 
    to require that the Operations Manager has completed the Turkey 
    Point Nuclear Plant Senior Management Operations Training Course if 
    the incumbent did not previously hold an SRO license. The Turkey 
    Point Nuclear Plant Senior Management Operations Training Course 
    ensures that the Operations Manager has the training on plant-
    specific systems
    
    [[Page 31182]]
    
    and procedures at Turkey Point and a knowledge level equivalent to 
    the license requirements for operations management.
        The on-shift Operations' organization is, and will continue to 
    be, supervised and directed by the Operations Supervisor, who is 
    currently required by Technical Specification 6.2.2.h. to hold an 
    SRO License.
        Additionally, the proposed changes do not impact or change, in 
    any way, the minimum on-shift manning or qualifications for those 
    individuals responsible for the actual licensed operation of the 
    facility as required by 10 CFR 50.54(l).
        Based on the above, the proposed changes do not affect the 
    probability or consequences of accidents previously analyzed.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The change being proposed is administrative in nature, addresses 
    personnel qualification issues, does not affect assumptions 
    contained in plant safety analyses, the physical design and/or 
    operation of the plant, or Technical Specifications that preserve 
    safety analysis assumptions.
        The proposed changes address organizational and qualifications 
    issues related to the criteria used for assignment of individuals to 
    the Operations organization off-shift management chain of command. 
    Since the proposed change does not impact or change, in any way, the 
    minimum on-shift manning or qualifications for those individuals 
    responsible for the actual licensed operation of the facility, 
    operation of the facility in accordance with the proposed amendment 
    would not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        The proposed change addresses organizational and qualification 
    issues related to the criteria used for assignment of individuals to 
    the Operations organization off-shift management chain of command. 
    The proposed change does not impact or change, in any way, the 
    minimum on-shift manning or qualifications for those individuals 
    responsible for the actual licensed operation of the facility.
        FPL's operating organization at Turkey Point Plant is shown on 
    Figure 1-2, Appendix A of the NRC-approved FPL Topical Quality 
    Assurance Report (TQAR). Since changes to the TQAR are governed by 
    10 CFR Sec. 50.54(a)(3), any changes to the TQAR that reduce 
    commitments previously accepted by the NRC require approval by the 
    NRC prior to implementation.
        While the Operations Manager is responsible for the plant's 
    operating organization, his responsibilities also include management 
    of the plant's Health Physics and Chemistry departments. The 
    Operations organization is supervised and directed by the Operations 
    Supervisor, who is required by Technical Specification 6.2.2.h. to 
    hold a Senior Reactor Operator License. The Turkey Point Units 3 and 
    4 Technical Specifications do not require that the Operations 
    Manager maintain an SRO License (nor even that the incumbent has 
    ever held a Senior Reactor Operator License at Turkey Point). The 
    Turkey Point Technical Specification 6.3.1, FACILITY STAFF 
    QUALIFICATIONS, will ensure that, other than license certification, 
    the individual filling the Operations Manager position has the 
    requisite education, training, and experience for the management 
    position.
        As a result, operation of the facility in accordance with the 
    proposed amendment would not involve a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199
        Attorney for licensee: J. R. Newman, Esquire, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036
        NRC Project Director: Frederick J. Hebdon
    
    GPU Nuclear Corporation and Saxton Nuclear Experimental 
    Corporation, Docket No. 50-146, Saxton Nuclear Experimental 
    Facility (SNEF), Bedford County, Pennsylvania
    
        Date of amendment request: February 2, 1996, as supplemented on 
    February 28, April 24 and May 24, 1996.
        Description of amendment request: The proposed amendment would (1) 
    increase the scope of work permitted within the exclusion area at the 
    SNEF to include action preparatory to major component and facility 
    decommissioning limited to asbestos removal, removal of defunct plant 
    electrical services, and installation of decommissioning support 
    facilities and systems such as heating, ventilation, and air 
    conditioning,
        (2) eliminate administrative access controls requiring that the 
    grating covering the auxiliary compartment stairwell and rod room 
    door remain locked except for authorized entry, and (3) revise the 
    facility layout diagram to allow the exclusion area to consist of, 
    at a minimum, the containment vessel, and at a maximum, extend to 
    the SNEF outer security fence, and to include on the diagram the 
    footprint of the proposed decommissioning support facilities.
        Basis for proposed no significant hazards Consideration 
    Determination: As required by 10 CFR 50.91(a), the licensees have 
    provided their analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes do not involve a significant hazards 
    considerations because the changes would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The SNEF ended power operation in May 1972, and the reactor core 
    has been removed. In its present condition, the only accidents 
    applicable to the site are fire, flooding, and radiological hazard. 
    The additional activities associated with the expansion of the 
    permissible work scope will not involve a significant increase in 
    the probability or consequences of a fire. There is no effect on the 
    probability or consequences of flooding nor would there be a 
    significant increase in the probability or consequences of an 
    offsite radiological hazard. The relocation of administratively 
    controlled accesses in accordance with the revised wording and the 
    proposed clarification of the facility layout diagram would have no 
    affect on analyzed accidents. Activities associated with the 
    construction of the decommissioning support facilities and the 
    existence of the completed buildings depicted on the revised figure 
    will not involve a significant increase in the probability or 
    consequences of a fire, flood, or radiological hazard. The proposed 
    changes identified by this technical specification change request do 
    not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        For the reasons discussed in 1 above, the possibility of a new 
    or different kind of accident from any accident previously evaluated 
    will not be created by the performance of the activities delineated 
    in the proposed revised technical specifications. There is similarly 
    no possibility of a new or different kind of accident from any 
    accident previously evaluated that would result from relocation of 
    administratively controlled accesses within the containment vessel; 
    from the flexibility to relocate/modify the exclusion area fence or 
    from the identification of the footprint, construction and existence 
    of the completed decommissioning support facilities.
        3. Involve a significant reduction in a margin of safety.
        For the reasons discussed in 1 above, none of the proposed 
    changes involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the analysis of the licensees and, based 
    on this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Saxton Community Library, 911 
    Church Street, Saxton, Pennsylvania 16678 Attorney for the Licensee: 
    Ernest L. Blake, Jr., Esquire, Shaw, Pittman, Potts, and Trowbridge, 
    2300 N Street, NW, Washington, DC 20037
    
    [[Page 31183]]
    
        NRC Project Director: Seymour H. Weiss
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, 
    and Entergy Operations, Inc., Docket No. 50-458, River Bend 
    Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: May 20, 1996
        Description of amendment request: The proposed amendment would 
    revise the Facility Operating License No. NPF-47 and Appendix C to the 
    license to reflect the name change from Gulf States Utilities Company 
    to Entergy Gulf States, Inc.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        I. The proposed change does not significantly increase the 
    probability or consequences of an accident previously evaluated.
        The proposed change documents changing the legal name of the 
    company. The proposed change will not affect any other obligations. 
    The company will still own all of the same assets, serve the same 
    customers, and all existing obligations and commitments will 
    continue to be honored.
        Therefore, the proposed change does no significantly increase 
    the probability or consequences of an accident previously evaluated.
        II. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The administrative changes in the Operating License requirements 
    do not involve any change in the design of the plant.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        III. The proposed change does not involve a significant 
    reduction in a margin of safety.
        The proposed change is administrative in nature, as described 
    above, therefore, this change does not reduce the level of safety 
    imposed by any current requirements.
        Therefore, the proposed changes do not cause a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005
        NRC Project Director: William D. Beckner
    
    Northeast Nuclear Energy Company (NNECO), Docket No. 50-245, 
    Millstone Nuclear Power Station, Unit 1, New London County, 
    Connecticut
    
        Date of amendment request: April 25, 1996
        Description of amendment request: The change modifies the 
    calibration requirement for the source range monitors and intermediate 
    range monitors by noting that the sensors are excluded.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Pursuant to 10 CFR 50.92, NNECO has reviewed the proposed change 
    and concludes that the change does not involve a significant hazards 
    consideration (SHC) since the proposed change satisfies the criteria 
    in 10 CFR 50.92(c). That is, the proposed change does not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        By removing the requirement for sensor calibration the function 
    and safety performance of these systems will not be affected. 
    Existing surveillances, operator verification of overlap and system 
    interlocks ensure correct system performance without sensor 
    calibration.
        Therefore, based on the above, the proposed change to the 
    Technical Specifications does not involve a significant increase in 
    the probability or consequences of any previously analyzed accident.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        This change does not cause the source range monitors (SRM) or 
    the intermediate range monitors (IRM) to function any differently 
    than intended by design and, therefore, does not create the 
    possibility of a new or different kind of accident. The Technical 
    Specification change deletes a Technical Specification requirement 
    which could not literally be complied with for one component and 
    that has no effect on the functional performance of the SRMs or 
    IRMs.
        Therefore, this change will not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        This change corrects a Technical Specification requirement which 
    could not literally be complied with for one component and that has 
    no effect on the functional performance of the SRMs or IRMs. 
    Instrument calibrations and functional checks are still performed 
    during each refueling outage to assure adequate system performance.
        Therefore, this change has no impact on the margin to safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360, and Waterford Library, ATTN: Vince Juliano, 49 Rope 
    Ferry Road, Waterford, CT 06385.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment requests: February 14, 1996
        Description of amendment requests: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Power Plant (DCPP), Unit Nos. 1 and 2, to revise 30 TS and add two new 
    TS surveillance requirements to support implementation of extended fuel 
    cycles at DCPP, Unit Nos. 1 and 2. The specific TS changes proposed 
    include those for 9 trip actuating device tests, 12 fluid system 
    actuation tests, and 11 miscellaneous tests. Two of the fluid system 
    actuation tests are proposed new TS surveillance requirements. The TS 
    changes also include the addition of a new frequency notation, ``R24, 
    REFUELING INTERVAL,'' to Table 1.1 of the TS. Also, a revision that 
    applies to all subsequent TS changes involves revising the Bases 
    section of TS 4.0.2 to change the surveillance frequency from an 18-
    month surveillance interval to at least once each refueling interval.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or
    
    [[Page 31184]]
    
    consequences of an accident previously evaluated.
        The surveillance interval notation addition in TS Table 1.1 and 
    the updated TS 4.0.2 Bases section are administrative changes that 
    do not affect the probability or consequences of accidents.
        The 30 proposed TS surveillance interval increases from 18 to 24 
    months do not alter the intent or method by which the inspections, 
    tests, or verifications are conducted, do not alter the way any 
    structure, system, or component functions, and do not change the 
    manner in which the plant is operated. The surveillance, 
    maintenance, and operating histories indicate that the equipment 
    will continue to perform satisfactorily with longer surveillance 
    intervals. Few surveillance and maintenance problems were 
    identified. No problems recurred, with the exception of those 
    associated with the pressurizer heater emergency breakers, which 
    will continue to be surveilled on a quarterly frequency until they 
    are replaced.
        There are no known mechanisms that would significantly degrade 
    the performance of the evaluated equipment during normal plant 
    operation. All potential time-related degradation mechanisms have 
    insignificant effects in the timeframe of interest (24 months +25 
    percent, or 30 months). Based on the past performance of the 
    equipment, the probability or consequences of accidents would not be 
    significantly affected by the proposed surveillance interval 
    increases.
        The 24-month surveillance intervals for the two new TS proposed 
    to verify that the CCW [component cooling water] and ASW [auxiliary 
    saltwater] pumps will start automatically are based on an evaluation 
    of historical operation, maintenance, and surveillance data for the 
    pumps. These historical data are available because the pumps have 
    been operated, maintained, and tested on 18- month intervals in 
    accordance with procedures since initial plant startup. These new 
    surveillances represent additional TS requirements to ensure the CCW 
    and ASW pumps start when required. No known degradation mechanisms 
    would significantly affect the ability of the pumps to start over 
    the timeframe of interest (30 months maximum). Based on the past 
    performance of the equipment, these proposed new TS would not affect 
    the probability or consequences of accidents.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The surveillance interval notation addition in TS Table 1.1 and 
    the updated TS 4.0.2 Bases section are administrative changes that 
    do not affect the type of accidents possible.
        For the 30 proposed TS changes involving surveillance interval 
    increases from 18 to 24 months, the surveillance and maintenance 
    histories indicate that the equipment will continue to effectively 
    perform its design function over the longer operating cycles. 
    Additionally, the increased surveillance intervals do not result in 
    any physical modifications, affect safety function performance or 
    the manner in which the plant is operated, or alter the intent or 
    method by which surveillance tests are performed. Only a few 
    problems have been identified and generally have not recurred. All 
    potential time-related degradations have insignificant effects in 
    the timeframe of interest. The proposed surveillance interval 
    increases would not affect the type of accidents possible.
        The 24-month surveillance intervals for the two new TS proposed 
    to verify starting of the CCW and ASW pumps are based on an 
    evaluation of historical operation, maintenance, and surveillance 
    data. These new TS represent additional requirements to ensure the 
    CCW and ASW pumps start when required. No known degradation 
    mechanisms would significantly affect the ability of the pumps to 
    start over the timeframe of interest. These proposed new TS would 
    not affect the type of accidents possible.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The surveillance interval notation addition in TS Table 1.1 and 
    the updated TS 4.0.2 Bases section are administrative changes that 
    do not affect the margin of safety.
        For the 30 proposed TS changes involving 18- to 24-month 
    surveillance interval increases, evaluation of historical 
    surveillance and maintenance data indicates there have been only a 
    few problems experienced with the evaluated equipment.
        There are no indications that potential problems would be cycle-
    length dependent or that potential degradation would be significant 
    for the timeframe of interest and, therefore, increasing the 
    surveillance interval will have little, if any, impact on safety. 
    There is no safety analysis impact since these changes will have no 
    effect on any safety limit, protection system setpoint, or limiting 
    condition for operation, and there are no hardware changes that 
    would impact existing safety analysis acceptance criteria. Safety 
    margins would not be significantly affected by the proposed 
    surveillance interval increases.
        As previously noted, the 24-month surveillance intervals for the 
    two new TS are based on an evaluation of historical data, represent 
    additional requirements, and are not believed to be significantly 
    affected by potential time-dependent degradation. As such, these 
    proposed new TS would not affect any margin of safety.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: William H. Bateman
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment requests: May 9, 1996
        Description of amendment requests: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Power Plant Unit Nos. 1 and 2 by revising Technical Specifications (TS) 
    3/4.3.2, ``Engineered Safety Features Actuation System 
    Instrumentation,'' and 3/4.6.2, ``Containment Spray System.'' The 
    changes would clarify the description of the initiation signal required 
    for operation of the containment spray system at Diablo Canyon Power 
    Plant (DCPP) and correctly incorporate changes made in previous license 
    amendments. All of the changes are administrative in nature.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Revising the description of the containment spray (CS) 
    initiating signal clarifies the design of the plant and provides 
    uniformity across the Technical Specifications (TS) associated with 
    the CS initiation function. The enhanced description does not affect 
    system operation or performance, nor the probability of any event 
    initiators. The changes do not affect any engineered safety feature 
    actuation setpoints or accident mitigation capabilities.
        The administrative changes to TS 3/4.3.2, Table 4.3-2, correct 
    the column headings and restore test frequency notation. The changes 
    only revise the TS to correspond with previously issued license 
    amendments (LAs).
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
    
    [[Page 31185]]
    
        The administrative changes in the description of the CS 
    initiating signal provide uniformity across the TS associated with 
    the spray system. There are no design, operation, maintenance, or 
    testing changes associated with the administrative changes.
        The administrative changes to TS 3/4.3.2, Table 4.3-2, correct 
    the column headings and restore test frequency notation. The changes 
    only revise the TS to correspond with previously issued LAs.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The administrative changes in CS signal description are not 
    associated with any design, operation, maintenance, or testing 
    revisions.
        The administrative changes to TS 3/4.3.2, Table 4.3-2, correct 
    the column headings and restore test frequency notation. The changes 
    only revise the TS to correspond with previously issued LAs.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: William H. Bateman
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260, and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2, and 3, Limestone County, 
    Alabama
    
        Date of amendment request: May 20, 1996 (TS 373)
        Description of amendment request: The proposed amendment revises 
    the technical specifications to incorporate a 24-hour delay in 
    implementing the action requirements due to a missed surveillance 
    requirement when the action requirements provide a restoration time 
    that is less than 24 hours. This change also clarifies that the time 
    limit of the action requirements applies from the point in time it is 
    identified a surveillance has not been performed and not at the time 
    that the allowed surveillance interval was exceeded. The licensee 
    claims this amendment is consistent with generic guidance.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        A. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed amendment to TS definition 1.0.LL is in accordance 
    with the guidance of GL 87-09 and NUREG 1433, Revision 1. The 
    proposed change will allow BFN to continue operation for an 
    additional 24 hours after discovery of a missed surveillance. The 
    change being proposed does not affect the precursor for any accident 
    or transient analyzed in Chapter 14 of the BFN Updated Final Safety 
    Analysis Report. The proposed change does not reflect a revision to 
    the physical design and/or operation of the plant. Therefore, 
    operation of the facility in accordance with the proposed change 
    does not affect the probability or consequences of an accident 
    previously evaluated.
        B. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed amendment to TS definition 1.0.LL is in accordance 
    with the guidance of GL 87-09 and NUREG 1433, Revision 1. The 
    proposed change will allow the plant to continue operation for an 
    additional 24 hours after discovery of a missed surveillance. The 
    change being proposed will not change the physical plant or the 
    modes of operation defined in the facility license. The change does 
    not involve the addition or modification of equipment, nor do they 
    alter the design or operation of plant systems. Therefore, operation 
    of the facility in accordance with the proposed change does not 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
        C. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The proposed amendment to TS definition 1.0.LL is in accordance 
    with the guidance of GL 87-09 and NUREG 1433, Revision 1. The 
    proposed change does not affect plant safety analysis or change the 
    physical design or operation of the plant. The proposed change will 
    allow the plant up to 24 hours to perform a missed surveillance. The 
    overall effect is a net gain in plant safety by avoiding unnecessary 
    shutdowns and the associate system transients due to missed 
    surveillance. Therefore, operation of the facility in accordance 
    with the proposed change does not involve a significant reduction in 
    a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Athens Public Library, South 
    Street, Athens, Alabama 35611
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET llH, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: May 8, 1996
        Description of amendment request: The proposed amendment would 
    revise Kewaunee Nuclear Power Plant (KNPP) Technical Specification (TS) 
    5.3, ``Reactor,'' and TS 5.4, ``Fuel Storage,'' by removing the 
    enrichment limit for reload fuel and imposing fuel storage restrictions 
    on the spent fuel storage racks and the new fuel storage racks. The 
    revised TS are structured consistent with the Westinghouse Standard 
    Technical Specifications and the fuel storage restrictions are based on 
    the criticality analyses used to support TS Amendment 92 dated March 7, 
    1991.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes were reviewed in accordance with the 
    provisions of 10 CFR 50.92 to determine that no significant hazards 
    exist. The proposed changes will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The criticality analysis which was performed in support of 
    Technical Specification Amendment 92, dated March 7, 1991, 
    demonstrated that adequate margins to criticality can be maintained 
    with fuel enrichments up to 49.2 grams of U235 per axial 
    centimeter stored in the New Fuel Storage Racks and enrichments up 
    to 52.3 grams of U235 per axial centimeter stored in the Spent 
    Fuel Storage Racks.
        The bounding cases of the analysis demonstrated that keff 
    remains less than 0.95 in the Spent Fuel Storage Racks and the New 
    Fuel Storage Racks if flooded with unborated water. The bounding 
    cases of the analysis also demonstrated that keff remains less 
    than 0.98 in the New Fuel Storage Racks if moderated by optimally 
    misted moderator. Therefore, the 49.2 grams of U235 per axial 
    centimeter enrichment is acceptable for storage in the New Fuel 
    Storage Racks and 52.3 grams of U235 per axial centimeter for 
    storage in the Spent Fuel Storage Racks.
        The only other accident that needs to be considered is a fuel 
    handling accident. Since the mass of the fuel assembly would not be 
    appreciably altered by the increased fuel
    
    [[Page 31186]]
    
    enrichment, the probability of this accident occurring is not 
    changed. The consequences of a fuel handling accident also would not 
    be affected by the use of higher fuel enrichment since the fission 
    product inventories in a fuel assembly are not a significant 
    function of initial fuel enrichment. This accident was analyzed in 
    the criticality analysis which was performed in support of Technical 
    Specification Amendment 92, dated March 7, 1991.
        It should be noted that any changes in the nuclear properties of 
    the reactor core that may result from higher fuel enrichments would 
    be analyzed in the appropriate reload analysis.
        The administrative relocation of information to licensee 
    controlled documents (i.e., USAR) conforms to NRC policy for the 
    content of technical specifications and does not increase the 
    probability or consequences of an accident.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        As discussed above, the only safety issue significantly affected 
    by the proposed change is the criticality analysis of the Spent Fuel 
    Storage Racks and the New Fuel Storage Racks. Since it has been 
    demonstrated that kG2eff remains below 0.95 and 
    0.98, respectively, in those areas, no new or different accident 
    would be created through the use of fuel enrichments up to 52.3 
    grams of U235 per axial centimeter at the Kewaunee Nuclear 
    Power Plant. Administrative controls will ensure that only fuel 
    enriched to 49.2 grams of U235 per axial centimeter or less 
    will be placed into the New Fuel Storage Racks.
        The relocation of information to licensee controlled documents 
    does not create the possibility of a new or different kind of 
    accident.
        3. Involve a significant reduction in the margin of safety.
        Since the criticality analyses have shown that increasing the 
    allowable weight percent enrichment to 52.3 grams of U235 per 
    axial centimeter would not increase keff above 0.95 in the 
    Spent Fuel Storage Racks and increasing the allowable weight percent 
    enrichment to 49.2 grams of U235 per axial centimeter would not 
    increase keff above 0.98 in the New Fuel Storage Racks, it is 
    concluded that this proposed change would not reduce the margin of 
    safety. Any changes in the nuclear properties of the reactor core 
    that may result from higher fuel enrichments would be analyzed in 
    the appropriate reload analysis to ensure compliance with applicable 
    reload considerations and requirements.
        Relocation of information to licensee controlled documents is an 
    administrative action and therefore does not reduce the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, Wisconsin 54311-7001
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P. O. Box 1497, Madison, Wisconsin 53701-1497
        NRC Project Director: Gail H. Marcus
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: May 17, 1996
        Description of amendment request: The proposed amendments would 
    modify Technical Specification Section 3/4.4.5, Steam Generators, 3/
    4.4.6, Reactor Coolant System Leakage, and associate Bases to allow the 
    installation of tube sleeves as an alternative to plugging to repair 
    defective steam generator tubes.
        Date of individual notice in the Federal Register: May 29, 1996 (61 
    FR 26936)
        Expiration date of individual notice: June 28, 1996
        Local Public Document Room location:  Wharton County Junior 
    College, J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 
    77488 Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
        Date of application for amendment: April 24, 1996
        Brief description of amendment request: The proposed amendment 
    would modify Technical Specifications (TSs) 5.3.1 and 6.9.3.2 to 
    reflect use of new fuel obtained from ABB/Combustion Engineering, and 
    to incorporate staff-approved core reload analysis computer programs 
    (codes). Date of individual notice in Federal Register: May 1, 1996 (61 
    FR 19326)
        Expiration date of individual notice: May 31, 1996
        Local Public Document Room location:  Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    [[Page 31187]]
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units 1, 2, and 3, Maricopa County, Arizona
    
        Date of application for amendments: January 5, 1996, as 
    supplemented by letters dated April 19, May 1, and May 10, 1996.
        Brief description of amendments: The amendments revise the 
    operating licenses and Technical Specification (TS) Section 1.26 to 
    increase the authorized rated thermal power. The amendments also revise 
    TS 4.1.1.4, 3.1.3.4, and 3.2.6 (Figure 3.2-1) to lower the allowable 
    reactor coolant system cold leg temperature limits for each of the 
    three Palo Verde Nuclear Generating Station units, and TS 3.4.2.1 and 
    3.4.2.2 to lower the pressurizer safety valve setpoints for Units 1 and 
    3 to support the increased power operation. The Unit 2 pressurizer 
    safety valve setpoints in TS 3.4.2.1 and 3.4.2.2 were revised in 
    Amendment 78, approved March 28, 1995, to the same values being 
    requested for Units 1 and 3 in this submittal.
        Date of issuance: May 23, 1996
        Effective date: May 23, 1996, to be implemented for Unit 1 within 
    30 days of issuance; to be implemented for Unit 2 within 30 days of 
    issuance; to be implemented for Unit 3 within 45 days as of the date of 
    issuance, except for the pressurizer safety valve setpoints change 
    which are effective prior to startup from Unit 3's sixth refueling 
    outage.
        Amendment Nos.: Unit 1 - 108; Unit 2 - 100; Unit 3 - 80
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Operating Licenses and Technical Specifications.
        Date of initial notice in Federal Register: February 28, 1996 (61 
    FR 7544) The April 19, May 1, and May 10, 1996, supplemental letters 
    provided additional clarifying information and did not change the 
    initial no significant hazards consideration determination. The 
    Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated May 23, 1996. No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson 
    Steam Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of application for amendment: January 31, 1996.
        Brief description of amendment: This amendment revises the 
    Technical Specifications Section 4.4 to allow the use of 10 CFR Part 
    50, Appendix J, Option B, Performance-Based Containment Leakage Rate 
    Testing.
        Date of issuance: May 28, 1996
        Effective date: May 28, 1996
        Amendment No. 169
        Facility Operating License No. DPR-23. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 28, 1996 (61 
    FR 7545) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 28, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: November 15, 1995, as 
    supplemented by letters dated March 15, and April 10, 1996
        Brief description of amendments: The amendments revise the 
    Technical Specifications and the associated Bases to increase the 
    setpoint tolerance of the main steam safety valves (MSSVs) from plus or 
    minus 1% to plus or minus 3%, to incorporate a requirement to reset the 
    as-left MSSV lift settings to within plus or minus 1% following 
    surveillance testing, and to delete two obsolete footnotes.
        Date of issuance: May 31, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 146 and 140
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 20, 1995 (60 
    FR 65676). The March 15 and April 10, 1996 letters provided clarifying 
    information that did not change the scope of the November 15, 1995 
    application and the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated May 31, 1996. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: January 12, 1995, as 
    supplemented by letter dated June 29, 1995
        Brief description of amendments: The amendments revise and clarify 
    portions of Technical Specification Section 6.0, ``Administrative 
    Controls.''
        Date of issuance: May 30, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 145 and 139
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 24, 1995 (60 
    FR 58109) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 30, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: April 3, 1996
        Brief description of amendments: The amendments revise the 
    Technical Specifications and the associated Bases to provide that if 
    neither Train A or Train B of the hydrogen igniter is operable in any 
    one containment region, there is an allowance of 7 days to restore one 
    hydrogen igniter to operable status, or be in hot shutdown within the 
    next 6 hours.
        Date of issuance: June 3, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 147 and 141
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 16, 1996 (61 FR 
    16649) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 3, 1996 No significant 
    hazards consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    [[Page 31188]]
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: May 19, 1995, as supplemented by letter 
    dated December 7, 1995
        Brief description of amendment: The amendment revised the 
    recombiner surveillance requirements to conform with the staff guidance 
    provided in NUREG-1432, ``Standard Technical Specifications Combustion 
    Engineering Plants.''
        Date of issuance: June 5, 1996
        Effective date: June 5, 1996
        Amendment No.: 119
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 3, 1996 (61 FR 
    180) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 5, 1996. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-
    389, St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
    
        Date of application for amendments: January 4, 1996
        Brief description of amendments: These amendments rectify a 
    discrepancy in Technical Specification 3.5.3, and provide assurance 
    that administrative controls for High Pressure Safety Injection pumps 
    remain effective in the lower operational modes.
        Date of Issuance: May 30, 1996
        Effective Date: May 30, 1996
        Amendment Nos.: 143 and 183
        Facility Operating License Nos. DPR-67 and NPF-16: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 14, 1996 (61 
    FR 5813) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 30, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-
    389, St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
    
        Date of application for amendments: November 22, 1995
        Brief description of amendments: These amendments upgrade existing 
    TS 3/4.4.6.1 for the Reactor Coolant System Leakage Detection Systems 
    by adopting the Standard Technical Specifications for Combustion 
    Engineering Plants to both St. Lucie Units.
        Date of Issuance: May 30, 1996
        Effective Date: May 30, 1996
        Amendment Nos.: 144 and 84
        Facility Operating License Nos. DPR-67 and NPF-16: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 22, 1996 (61 FR 
    1629) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 30, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of application for amendment: March 28, 1996 (TSCR 234)
        Brief description of amendment: The amendment modifies Technical 
    Specification pages 3.1-5 and 3.1-16 to indicate 40 percent of the 
    rated reactor thermal power as the anticipatory reactor scram bypass 
    setpoint on turbine trip or generator load rejection.
        Date of Issuance: June 4, 1996
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment No.: 184
        Facility Operating License No. DPR-16. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 24, 1996 (61 FR 
    18167) The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated June 4, 1996 No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio Central Power and Light Company, City of Austin, Texas, 
    Docket No. 50-498, South Texas Project, Unit 1, Matagorda County, 
    Texas
    
        Date of amendment request: January 22, 1996, as supplemented April 
    4 and May 2, 1996
        Brief description of amendment: The amendment modified the steam 
    generator tube plugging criteria in TS 3/4.4.5, Steam Generators, the 
    allowable primary-to-secondary leakage in TS 3/4.4.6.2, Operational 
    Leakage, and the associated Bases. These changes allowed the 
    implementation of alternate steam generator tube plugging criteria for 
    the tube support plate/tube intersections for Unit 1.
        Date of issuance: May 22, 1996
        Effective date: May 22, 1996
        Amendment No.: 83
        Facility Operating License No. NPF-76. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 16, 1996 (61 FR 
    16651) as corrected April 22, 1996 (61 FR 17735). The additional 
    information contained in the supplemental letter dated May 2, 1996, was 
    clarifying in nature and thus, within the scope of the initial notice 
    and did not affect the staff's proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated May 22, 1996. No 
    significant hazards consideration comments received: No
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy, Center, 
    Linn County, Iowa
    
        Date of application for amendment: July 21, 1995, as supplemented 
    August 8, 1995 and December 15, 1995
        Brief description of amendment: The amendment made administrative 
    changes to various sections of the DAEC Technical Specifications (TS). 
    The amendment replaced the surveillance condition when an Emergency 
    Service Water pump or loop is inoperable with an OPERABILITY 
    verification of the opposite train's Emergency Diesel Generator (EDG). 
    The amendment modified the TS to allow credit for demonstration of EDG 
    OPERABILITY that occurred within the previous 24 hours. The amendment 
    revised the format and language of TS Section 5.5
    
    [[Page 31189]]
    
    to clarify the requirements and state the capacity of the spent fuel 
    pool and vault storage in order to remove ambiguities in the wording 
    and to be more consistent with the Improved Standard TS guidance. The 
    amendment revised the list of Operations Committee responsibilities 
    (Section 6.5.1.6) to eliminate Committee review of procedures 
    implementing Security and Emergency Plans.
        Date of issuance: June 5, 1996
        Effective date: June 5, 1996
        Amendment No.: 214
        Facility Operating License No. DPR-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 27, 1995 (60 
    FR 49938) and February 2, 1996 (61 FR 3953) The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    June 5, 1996. No significant hazards consideration comments received: 
    No.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, S. E., Cedar Rapids, Iowa 52401
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota
    
        Date of application for amendments: May 4, 1995, as supplemented 
    November 27, 1995, and March 1, 1996
        Brief description of amendments: The amendments revise the 
    pressurizer and main steam safety valve lift setting tolerance from 
    plus or minus 1 percent to plus or minus 3 percent (as-found setpoint 
    only), revise the safety limit curves, reformat Section 2, and correct 
    typographical errors.
        Date of issuance: May 21, 1996 Effective date: May 21, 1996, with 
    full implementation within 30 days
        Amendment Nos.: Unit 1 - 123, Unit 2 - 116
        Facility Operating License Nos. DPR-42 and DPR-60. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 13, 1995 (60 
    FR 47621) The November 27, 1995, and March 1, 1996, letters provided 
    clarifying information in response to NRC staff questions. This 
    information was within the scope of the original application and did 
    not change the staff's initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated May 21, 1996. No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of application for amendments: March 13, 1996
        Brief description of amendments: These amendments delete the 
    requirement in Technical Specifications (TS) 4.0.5a for NRC written 
    approval prior to implementation of relief from ASME Code requirements 
    by deleting ``...(g),.except where specific written relief has been 
    granted by the Commission pursuant to 10 CFR 50.55a(g)(6)(i).'' Also, 
    the amendments add the ASME Section XI definition of ``Biennially or 
    every 2 years - At least once per 731 days,'' in TS 4.0.5b.
        Date of issuance: May 28, 1996
        Effective date: May 28, 1996
        Amendment Nos.: Unit 1 - 112; Unit 2 - 110
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 24, 1996 (61 FR 
    18173) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 28, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of application for amendments: April 3, 1996
        Brief description of amendments: These amendments revise the 
    combined Technical Specifications (TS) for the Diablo Canyon Nuclear 
    Power Plant, Unit Nos. 1 and 2 to revise Technical Specifications 3/
    4.7.5, ``Control Room Ventilation System;'' 3/4.7.6, ``Auxiliary 
    Building Safeguards Air Filtration System;'' and 3/4.9.12, ``Fuel 
    Handling Building Ventilation System'' to clarify the testing 
    methodology utilized by PG&E to determine the operability of the 
    charcoal and high efficiency particulate air (HEPA) filters in the 
    engineering safeguards features (ESF) air handling units at the Diablo 
    Canyon Power Plant (DCPP).
        Date of issuance: May 28, 1996
        Effective date: May 28, 1996
        Amendment Nos.: Unit 1 - 113; Unit 2 - 111
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 24, 1996 (61 FR 
    18173) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 28, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. 
    Ginna Nuclear Power Plant, Wayne County, New York
    
        Date of application for amendment: May 8, 1996, as supplemented May 
    10, 1996, and May 29, 1996, and June 3, 1996.
        Brief description of amendment: This amendment modifies the 
    Technical Specifications to correct several typographical errors that 
    were implemented in the Improved Technical Specifications at Ginna 
    Station per Amendment No. 61.
        Date of issuance: June 3, 1996
        Effective date: As of date of issuance.
        Amendment No.: 65
        Facility Operating License No. DPR-18: Amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: Yes (61 FR 24965, dated May 17, 
    1996). That notice provided an opportunity to submit comments on the 
    Commission's proposed no significant hazards consideration 
    determination. No comments have been received. The notice published May 
    17, 1996, also provided for a hearing by June 17, 1996, but indicated 
    that if a Commission makes a final no significant hazards consideration 
    determination, any such hearing would take place after issuance of the 
    amendment. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 3, 1996.
        Local Public Document Room location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610.
    
    [[Page 31190]]
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application for amendment: February 9, 1996 as superseded 
    by letter dated March 22, 1996.
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 1.7, 4.6.1.1, 3.6.1.3, 4.6.1.3, 6.8.4 and the 
    associated Bases section to directly reference Regulatory Guide 1.163, 
    ``Performance-Based Containment Leak Test Program,'' as required by 10 
    CFR 50, Appendix J, Option B for the Type A containment integrated leak 
    rate tests and the Type B and C local leak tests.
        Date of issuance: May 28, 1996
        Effective date: May 28, 1996, to be implemented within 30 days from 
    the date of issuance.
        Amendment No.: 111
        Facility Operating License No. NPF-30: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 24, 1996 (61 FR 
    18174) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 28, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 
    50-339, North Anna Power Station, Units No. 1 and No. 2, Louisa 
    County, Virginia
    
        Date of application for amendments: January 30, 1996
        Brief description of amendments: The amendments modify the 
    Technical Specifications to increase the minimal allowable reactor 
    coolant system total flow rate.
        Date of issuance: June 5, 1996
        Effective date: June 5, 1996
        Amendment Nos.: 201 and 182
        Facility Operating License Nos. NPF-4 and NPF-7. Amendments revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: February 28, 1996 (61 
    FR 7559) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 5, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: April 24, as supplemented by 
    letter dated May 29, 1996.
        Brief description of amendment: The amendment would modify the WNP-
    2 technical specifications to support Cycle 12 operation, reflect use 
    of new fuel obtained from ABB/Combustion Engineering, and incorporate 
    staff-approved core reload analysis computer programs (codes). Date of 
    issuance: June 4, 1996 Effective date: June 4, 1996, to be implemented 
    within 30 days of issuance.
        Amendment No.: 146
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 1, 1996 (61 FR 
    19326). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 4, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has
    
    [[Page 31191]]
    
    made a determination based on that assessment, it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By July 19, 1996, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-001, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555-001, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Commonwealth Edison Company, Docket No. 50-249, Dresden Nuclear 
    Power Station, Unit No. 3
    
        Date of application for amendment: May 22, 1996
        Brief description of amendment: The amendment authorizes, on a one- 
    time temporary basis, operation of Dresden, Unit 3, with the structural 
    steel members in the Low Pressure Coolant Injection (LPCI) corner rooms 
    outside the Updated Final Safety Analysis Report (UFSAR) design 
    parameters, but capable of performing their intended safety function. 
    Following a reactor scram on May 15, 1996, Commonwealth Edison Company 
    (ComEd) performed a Safety Evaluation (SE) in accordance with the 
    requirements of 10 CFR 50.59 to determine if the current configuration 
    of the corner room structural steel members had reduced the margin of 
    safety as described in the UFSAR. The SE determined that the 
    configuration does not reduce the margin of safety with respect to the 
    stress allowables for the structural steel if subjected to a Safe 
    Shutdown Earthquake (SSE). An unreviewed safety question was determined 
    to exist because stress allowables for the structural steel subjected 
    to an Operating Basis Earthquake (OBE) were found outside the UFSAR 
    requirements; however, the current configuration of the corner room 
    structural steel members has not
    
    [[Page 31192]]
    
    significantly reduced the margin of safety as described in the UFSAR.
        Date of Issuance: May 31, 1996 Effective date: May 31, 1996
        Amendment No.: 144
        Facility Operating License No. DPR-25. The amendment revised the 
    license.
        Press release issued requesting comments as to proposed no 
    significant hazards consideration: Yes. Joliet Herald News on May 25, 
    1996, and the Morris Daily Herald on May 29, 1996. Comments received: 
    No comments were received on the proposed no significant hazards 
    consideration determination; however, comments were received concerning 
    the licensee's timeliness and decision-making in restoring the UFSAR 
    design margin to the structural steel members installed the LPCI corner 
    rooms at Dresden Unit 3.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, consultation with the State of Illinois and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated May 31, 1996.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690
        Local Public Document Room location: Morris Area Public Library 
    District, 604 Liberty Street, Morris, Illinois 60450.
        NRC Project Director: Robert A. Capra
        Dated at Rockville, Maryland, this 12th day of June 1996.
        For the Nuclear Regulatory Commission
    John A. Zwolinski,
    Deputy Director, Division of Reactor Projects - I/II, Office of Nuclear 
    Reactor Regulation
    [Doc. 96-15398 Filed 6-18-96; 8:45 am]
    BILLING CODE 7590-01-F
    
    

Document Information

Published:
06/19/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X96-10619
Dates:
May 23, 1996, to be implemented for Unit 1 within 30 days of issuance; to be implemented for Unit 2 within 30 days of issuance; to be implemented for Unit 3 within 45 days as of the date of issuance, except for the pressurizer safety valve setpoints change which are effective prior to startup from Unit 3's sixth refueling outage.
Pages:
31171-31192 (22 pages)
PDF File:
x96-10619.pdf