X94-10622. Biweekly Notice  

  • [Federal Register Volume 59, Number 119 (Wednesday, June 22, 1994)]
    [Unknown Section]
    [Page 0]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X94-10622]
    
    
    [[Page Unknown]]
    
    [Federal Register: June 22, 1994]
    
    
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    UNITED STATES NUCLEAR REGULATORY COMMISSION
    
     
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from May 27, 1994, through June 10, 1994. The 
    last biweekly notice was published on June 8, 1994 (59 FR 29623).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11555 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC 
    20555. The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By July 22, 1994, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC 20555 and at the local 
    public document room for the particular facility involved. If a request 
    for a hearing or petition for leave to intervene is filed by the above 
    date, the Commission or an Atomic Safety and Licensing Board, 
    designated by the Commission or by the Chairman of the Atomic Safety 
    and Licensing Board Panel, will rule on the request and/or petition; 
    and the Secretary or the designated Atomic Safety and Licensing Board 
    will issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    room for the particular facility involved.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of amendment request: April 26, 1994
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications to change the Table 3.5-1 High 
    Containment Pressure ( Hi Level), Safety Injection Setting Limit from 
    less than or equal to 2.0 psig to less than or equal to 5.0 psig.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the High Containment Pressure (Hi Level) 
    actuation setting of [less than or equal to] 2.0 psig be revised to 
    [less than or equal to] 5.0 psig. This additional operating 
    flexibility will decrease the frequency of Containment venting 
    necessary to relieve containment of
        non-condensible gases which build up during normal operation.
        Based upon a statistical analysis of the containment pressure 
    channel uncertainty for a 30 month operating cycle, a margin must be 
    allowed between the Technical Specification limit (plant setting) 
    and the Safety Analysis limit so that the Safety Analysis limit(s) 
    will not be exceeded under the worst circumstances. For a Technical 
    Specification value of [less than or equal to] 5.0 psig, the 
    corresponding Safety Analysis limit must be increased to 10 psig to 
    provide margin for the channel statistical allowance. A safety 
    evaluation performed pursuant to 10 CFR 50.59 is on file which 
    supports a change in the Safety Analysis limit from 7.3 psig 
    (current value) to 10.0 psig. Key conclusions of the Safety 
    Evaluation are that neither the probability nor the consequences of 
    an accident or malfunction of equipment important to safety 
    previously evaluated in the Safety Analysis report would be 
    increased.
        Thus, assurance is provided that appropriate protective actions 
    in accordance with the Technical Specifications will be taken so 
    that Safety Analysis limits are not exceeded.
        2. The possibility of a new or different kind of accident from 
    any previously analyzed has not been created.
        The proposed change in the Technical Specification limit 
    together with the change in the Safety Analysis limit provides 
    adequate margin to accommodate instrument channel uncertainty over a 
    30 month operating cycle. Plant equipment, which would be set at the 
    Technical Specification limit, will therefore provide protective 
    functions to assure that safety analysis limits are not exceeded. 
    This would prevent the possibility of a new or different kind of 
    accident from that previously evaluated from occurring.
        3. There has been no reduction in the margin of safety.
        The proposed change to the Technical Specification limit would 
    decrease the frequency of containment purges necessary to vent the 
    build up of non-condensible gases during normal operation. This 
    would result in a decrease in the amount of radioactivity discharged 
    to the environment (due to decay), decrease the potential for high 
    Containment pressure alarms and increase the margin for an ESF trip. 
    The change to the Safety Analysis limits, justified by a safety 
    Evaluation performed in accordance with 10 CFR 50.59, assures 
    sufficient margin exists to accommodate channel instrument 
    uncertainty over the maximum operating cycle length. This margin is 
    necessary so that safety functions will occur and Safety Analysis 
    limits will be preserved.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
        Attorney for licensee: Brent L. Brandenburg, Esq., 4 Irving Place, 
    New York, New York 10003.
        NRC Project Director: Michael L. Boyle
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: May 24, 1994
        Description of amendment request: The proposed amendments would 
    transfer the boron concentration in Technical Specification (TS) 3.9.1 
    for the reactor coolant system and the refueling canal during MODE 6, 
    and the boron concentration in TS 3.9.12 for the spent fuel pool from 
    the TS to the Core Operating Limits Report (COLR). The application is 
    submitted in response to the guidance in Generic Letter 88-16 which 
    addresses the transfer of fuel cycle-specific parameter limits from the 
    TS to the COLR.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The following analysis, performed pursuant to 10 CFR 50.91, 
    shows that the proposed amendment will not create a significant 
    hazards consideration as defined by the criteria of 10 CFR 50.92.
        1. This amendment will not significantly increase the 
    probability or consequence of any accident previously evaluated.
        No component modification, system realignment, or change in 
    operating procedure will occur which could affect the probability of 
    any accident or transient. The relocation of boron concentration 
    values to the COLR is an adminsitrative change which will have no 
    effect on the probability or consequences of any previously-analyzed 
    accident. The required values of boron concentration will continue 
    to be determined through use of approved methodologies.
        2. This amendment will not create the possibility of any new or 
    different accidents not previously evaluated.
        No component modification or system realignment will occur which 
    could create the possibility of a new event not previously 
    considered. The administrative change of relocating parameters to 
    the COLR, in this case boron concentration, cannot create the 
    probability of an accident.
        3.This amendment will not involve a significant reduction in a 
    margin of safety.
        Required boron concentrations will remain appropriate for each 
    cycle, and will continue to be calculated using approved 
    methodologies. There is no significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: David B. Matthews, Director
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of amendment request: May 12, 1994
        Description of amendment request: The proposed amendment would 
    revise Technical Specification Sections 3.1 and 4.1 for Protective 
    Instrumentation, the associated bases, and tables to increase the 
    surveillance test intervals (STIs) and add allowable out-of-service 
    times (AOTs). All proposed STI and AOT changes are in accordance with 
    General Electric Company Licensing Topical Reports (LTRs) which have 
    been previously reviewed and approved by the NRC staff. Also, AOTs are 
    clarified in accordance with the most recently approved BWR Owners' 
    Group letters which were used in the development of NUREG-1433 
    ``Standard Technical Specifications, General Electric Plants, BWR/4.'' 
    The Technical Specification changes will permit specified Channel Tests 
    to be conducted quarterly rather than weekly or monthly. The amendment 
    will enhance operational safety by reducing 1) the potential for 
    inadvertent plant scrams, 2) excessive test cycles on equipment, and 3) 
    the diversion of plant personnel and resources on unnecessary testing.
        Two additional technical changes are proposed. The first change 
    involves extending the Channel Calibration interval for average power 
    range monitor (APRM) scram instrumentation from weekly to quarterly. 
    GPUN has evaluated the effect of drift on the setpoint over the longer 
    interval for this instrumentation and found it to be acceptable. The 
    second change would add a quarterly Channel Calibration requirement for 
    High Drywell Pressure (for Core Cooling) and Turbine Trip Scram 
    instrumentation. This would be a new requirement not currently 
    incorporated in the Technical Specifications.
        Nineteen editorial changes have been incorporated in 
    Instrumentation Sections 3.1 and 4.1 to provide clarity and 
    consistency. These items are editorial only and do not alter the 
    meaning or intent of any requirements. Examples of editorial changes 
    are: 1) capitalize definitions where used, 2) punctuation and 
    grammatical corrections, 3) ensuring consistency in STI nomenclature, 
    and 4) reformat of tables. A table note and its associated footnote 
    were deleted which involved a 1985 licensing condition which is no 
    longer applicable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analyses of the issue of no significant hazards 
    consideration, which is presented below:
        NO SIGNIFICANT HAZARDS CONSIDERATION EVALUATION OF TECHNICAL 
    CHANGES
        1. The operation of the Oyster Creek Nuclear Generating Station, 
    in accordance with the proposed amendment, will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The generic analysis contained in LTR NEDC-30851P-A assessed the 
    impact of changing RPS [reactor protection system] STIs and adding 
    AOTs on RPS failure frequency, scram frequency and equipment 
    cycling. Specifically, Section 5.7.4, ``Significant Hazards 
    Assessment,'' of NEDC-30851P-A states that:
        Fewer challenges to the safeguards system, due to less frequent 
    testing of the RPS, conservatively results in a decrease of 
    approximately one percent in core damage frequency. This decrease is 
    based upon the following:
        Based on the plant-specific experience presented in Appendix J, 
    the estimated reduction in scram frequency (0.3 scrams/yr) 
    represents a 1 to 2 percent decrease in core damage frequency based 
    on the BWR plant-specific Probabilistic Risk Assessments (PRAs) 
    listed in Table 5-8.
        The increase in core damage frequency due to less frequent 
    testing is less than one percent. This increase is even lower (less 
    than 0.01 percent) when the changes resulting from the 
    implementation of the Anticipated Transients Without Scram (ATWS) 
    rule are considered. Therefore, this increase is more than offset by 
    the decrease in CDF [core damage frequency] due to fewer scrams.
        The effect of reducing unnecessary cycles on RPS equipment, 
    although not easily quantifiable also results in a decrease in core 
    damage frequency.
        The overall impact on core damage frequency of the changes in 
    allowable out-of-service times is negligible.
        The BWR Owners' Group concluded that the proposed changes do not 
    significantly increase the probability or consequences of an 
    accident previously evaluated since the increase in probability of a 
    scram failure due to RPS unavailability is insignificant. The 
    overall probability of an accident is decreased as the time RPS 
    logic operates as designed is increased resulting in less 
    inadvertent scrams during testing and repair. The plant-specific 
    evaluation performed by GPUN and GE demonstrates that while the 
    Oyster Creek RPS differs from the generic model analyzed in the RPS 
    LTR (NEDC-30851P-A), the net effect of the differences do not alter 
    the generic conclusions. The AOTs proposed for RPS instrumentation 
    are based on improved wording developed for use in NUREG 1433, 
    ``Standard Technical Specifications, General Electric Plants, BWR/
    4,'' which ensures a loss of function does not occur. In addition, 
    the change to the APRM Scram Channel Calibration surveillance 
    interval from weekly to quarterly has been evaluated by GPUN to 
    determine the effect on setpoint drift. The results of the 
    evaluation show acceptable performance of this scram parameter 
    ensuring that the safety analysis remains valid. The clarification 
    that a Channel Calibration is not applicable to Turbine Trip Scram 
    instrumentation is appropriate since this trip parameter senses 
    turbine stop valve position via limit switches which are fixed in 
    position and adjusted, as necessary, during valve maintenance. This 
    trip parameter and its switch adjustment methods are similar to the 
    Main Steamline Isolation Valve [MSIV] Scram for which the Technical 
    Specifications require only a Channel Test.
        LTR NEDC-30936P-A (Parts 1 and 2) contains an assessment of the 
    impact of changing STIs and AOTs for BWR ECCS Actuation 
    Instrumentation. Section 4.0, ``Technical Assessment of Changes,'' 
    of NEDC-30963P-A (Part 2) states that:
        The results indicate an insignificant (less than 5E-7 per year) 
    increase in water injection function failure frequency when STIs are 
    increased from 31 days to 92 days, AOTs for repair of the ECCS 
    actuation instrumentation are increased from one hour to 24 hours, 
    and AOTs for surveillance testing are increased from two to six 
    hours. For all four BWR models the increase represents less than 4% 
    increase in failure frequency. However, when other factors which 
    influence the overall plant safety are considered, the net result is 
    judged to be an improvement in plant safety.
        From this generic analysis, the BWR Owners' Group concluded that 
    the proposed changes do not significantly increase the probability 
    or consequences of an accident previously evaluated since the 
    increase in probability of a water injection failure due to ECCS 
    instrumentation unavailability is insignificant and the net result 
    is judged to be an improvement in plant safety. The plant-specific 
    evaluation performed by GPUN and GE demonstrates that while the 
    Oyster Creek ECCS differs from the generic model analyzed in LTR 
    NEDC-30936P-A, the net effect of the plant-specific differences do 
    not alter the generic conclusions. The addition of a quarterly 
    Channel Calibration STI for the High Drywell Pressure ECCS 
    initiation parameter is consistent with the calibration interval 
    requirement for other similar instrumentation at Oyster Creek and 
    ensures the regular performance of calibrations. This is a new 
    requirement not currently contained in the Technical Specifications 
    and experience performing the High Drywell Pressure (Core Cooling) 
    instrument calibration at a quarterly interval has proven adequate 
    for instrument performance monitoring.
        LTRs NEDC-30851P-A, Supplement 2 and NEDC-31677P-A contain 
    generic analyses assessing the impact of changing STIs and AOTs for 
    BWR Isolation Actuation Instrumentation which are common or not 
    common to RPS and ECCS instrumentation. Section 4.0, ``Summary of 
    Results,'' of NEDC-30851P-A, Supplement 2 states that:
        The results indicated that the effects on probability of failure 
    to initiate isolation are very small and the effects on probability 
    or frequency of failure to isolate are negligible in nearly every 
    case. In addition, the results indicated that increasing the AOT to 
    24 hours for tests and repairs has a negligible effect on the 
    probability of failure of the isolation function. These combined 
    with changes to the testing intervals and allowed out-of-service 
    times for RPS and ECCS instrumentation provide a net improvement to 
    plant safety and operations.
        and Section 5.6, ``Assessment of Net Effect of Changes,'' of 
    NEDC-31677P-A states that:
        A reduction in core damage frequency (CDF) of at least as much 
    as estimated in the ECCS instrumentation analysis can be expected 
    when the isolation actuation instrumentation STIs are changed from 
    one month to three months. The chief contributor to this reduction 
    is the channel functional tests for the MSIVs. Inadvertent closure 
    of the MSIVs will cause an unnecessary plant scram. This reduction 
    in CDF more than compensates for any small incremental increase (10% 
    or 1.0E-07/year) in calculated isolation function failure frequency 
    when the STI is extended to three months.
        Based on this generic analysis, the BWR Owners' Group concluded 
    that the proposed changes do not significantly increase the 
    consequences of an accident previously evaluated since the increase 
    in probability of an isolation failure due to isolation 
    instrumentation unavailability is insignificant. The proposed 
    wording of the AOTs is based on the clarifications used in the 
    development of NUREG 1433, ``Standard Technical Specifications, 
    General Electric Plants, BWR/4,'' which ensures a loss of function 
    does not occur where applied to isolation actuation instrumentation.
        LTR NEDC-30851P-A, Supplement 1 contains a generic analysis 
    assessing the impact of changing control rod block STIs on Rod Block 
    failure frequency. Section 5 (Brookhaven National Laboratory 
    Technical Evaluation Report - Attachment 2 to the NRC SER) of NEDC-
    30851P-A, Supplement 1 states that:
        The BWROG proposed changes to the Technical Specifications 
    concerning the test requirements for BWR control rod block 
    instrumentation. The changes consist of increasing the surveillance 
    test intervals form one to three months. These test interval 
    extensions are consistent with the already approved changes to STIs 
    for the reactor protection system. The technical analysis reviewed 
    and verified as documented herein indicates that there will be no 
    significant changes in the availability of the control rod block 
    function if these changes are implemented. In addition, there will 
    be a negligible impact on the plant core melt frequency due to the 
    decreased testing.
        Bases contained in GE Topical Report GENE-770-1-A assessed the 
    impact of changing STIs and AOTs on failure frequency for selected 
    systems. Section 2.0, ``Summary,'' of GENE-770-06-1-A states that:
        Technical bases are provided for selected proposed changes to 
    the instrumentation STIs and AOTs that were identified in the BWROG 
    Improved BWR Technical Specification activity. These STI and AOT 
    changes are consistent with approved changes to the RPS, ECCS, and 
    isolation actuation instrumentation. These proposed changes do not 
    result in a degradation to overall plant safety.
        The BWR Owners' Group concluded from the generic analysis in 
    NEDC-30851P-A, Supplement 1 and the bases in GENE-770-06-1-A that 
    the proposed changes do not significantly increase the probability 
    or consequences of an accident previously evaluated. GPUN's 
    utilization of GENE-770-06-1-A is limited to the identified AOTs for 
    Control Rod Block instrumentation analyzed in NEDC-30851P-A since 
    the Control Rod Block LTR did not explicitly address AOTs.
        2. The operation of Oyster Creek Nuclear Generating Station, in 
    accordance with the proposed amendment, will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The addition of allowable out-of-service times (AOTs) consistent 
    with wording developed for use in Improved Standard Technical 
    Specifications to ensure no loss of function and the revision of 
    surveillance test intervals (STIs) does not alter the function of 
    RPS, ECCS, Isolation or Rod Block instrumentation nor involve any 
    type of plant modification. No new modes of plant operation are 
    involved with the changes.
        Adding a quarterly Channel Calibration STI for High Drywell 
    Pressure instrumentation (for Core Cooling) establishes a 
    requirement in the Technical Specifications which is not currently 
    incorporated. This is an additional requirement beyond that already 
    in place for this instrumentation and will not alter its operation 
    since by their nature STIs ensure proper instrument performance. The 
    clarification that a Channel Calibration is not applicable to 
    Turbine Trip Scram instrumentation is appropriate since this trip 
    parameter senses turbine stop valve position via limit switches 
    which are fixed in position and adjusted during valve maintenance. 
    This trip parameter and its switch adjustment methods are similar to 
    the Main Steamline Isolation Valve Scram for which the Technical 
    Specifications require only a Channel Test. Revising the Channel 
    Calibration STI for APRM Scram instruments from weekly to quarterly 
    allows these instruments to benefit from the Channel Test STI change 
    provided by the generic analysis in the RPS LTR. The benefits 
    include a significant reduction in the number of half-scram states 
    the plant will undergo reducing the potential for inadvertent plant 
    trips. The effect of setpoint drift over the longer interval has 
    been evaluated and found acceptable.
        The proposed changes will not alter the physical characteristics 
    of any plant systems or components and all safety-related systems 
    and components remain within their applicable design limits. Thus, 
    system and component performance is not adversely affected by these 
    changes, thereby assuring that the design capabilities of those 
    systems and components are not challenged in a manner not previously 
    assessed so as to create the possibility of a new or different kind 
    of accident.
        3. The operation of the Oyster Creek Nuclear Generating Station, 
    in accordance with the proposed amendment, will not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed and approved the generic studies 
    contained in the GE Licensing Topical Reports and has concurred with 
    the BWR Owners' Group that the proposed changes do not significantly 
    affect the availability of RPS, ECCS Actuation, Isolation Actuation 
    and Control Rod Block instrumentation. The proposed addition of 
    allowable out-of-service times for instruments addressed by the LTRs 
    provides reasonable times for making repairs and performing tests. 
    The lack of sufficient out-of-service time provided in current 
    Technical Specifications, increases the potential for an inadvertent 
    scram or equipment actuation. The proposed AOTs provide realistic 
    times to complete required actions without increasing overall 
    instrument failure frequency and ensure that no loss of function 
    occurs, therefore, there is no significant reduction in the margin 
    of safety.
        The LTRs demonstrate that extending surveillance test intervals 
    does not result in significant changes in the probability of 
    instrument failure. Where Channel Calibration frequency has not 
    changed, assurance exists that setpoints will not be affected by 
    drift. In the case of the APRM Scram Channel Calibration, the 
    proposed change to quarterly from weekly has been evaluated and 
    found acceptable. Expected instrument performance over the extended 
    interval will assure that applicable safety analyses will continue 
    to be met. In addition, other instrumentation was evaluated for 
    drift effects of setpoints and was found acceptable. The addition of 
    a quarterly Channel Calibration interval for High Drywell Pressure 
    (for Core Cooling) is consistent with Channel Calibration STIs for 
    most other instrumentation at Oyster Creek and has been the interval 
    used to achieve an adequate level of instrument performance 
    monitoring. The clarification that a Channel Calibration is not 
    applicable to Turbine Trip Scram instrumentation ensures consistency 
    in the establishment of surveillance requirements. This trip 
    parameter senses turbine stop valve position via limit switches 
    which are fixed in position and adjusted during valve maintenance. 
    This trip parameter and its switch adjustment methods are similar to 
    the Main Steamline Isolation Valve Scram for which the Technical 
    Specifications require only a Channel Test. These proposed changes, 
    when coupled with the reduced probability of test-induced plant 
    transients and equipment failures, do not result in a reduction in 
    the margin of safety.
        No Significant Hazards Consideration Evaluation For Editorial 
    Changes
        The above nineteen proposed changes are editorial in nature and 
    are typical example I.c.2.e.i in 51FR7744. Therefore, they do not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The editorial changes described above do not change the design 
    or operation of any structure, system or component relied upon to 
    prevent or mitigate the consequences of any accident evaluated. 
    These editorial changes also do not add new structures, systems or 
    components which may have an effect on existing elements of the 
    facility. The changes proposed correct, clarify and/or retain 
    existing requirements.
        2. Create the possibility of a new or different kind of accident 
    form any accident previously evaluated.
        Since neither physical changes to the facility nor changes in 
    its operation are involved in the proposed editorial changes to the 
    Technical Specifications, there is no possibility for creation of a 
    new or different kind of accident.
        3. Involve a significant reduction in the margin of safety.
        Facility configuration and operation are unaffected by the 
    proposed editorial changes. As a result no changes in margin of 
    safety occur.
        The editorial changes described and evaluated above are purely 
    administrative to achieve consistency or correct an error in the 
    Technical Specifications.
        The NRC staff has reviewed the licensee's analyses and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied for both the technical issues and editorial changes. 
    Therefore, the NRC staff proposes to determine that the amendment 
    request involves no significant hazards consideration.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, New Jersey 
    08753
        Attorney for licensee: Ernest L. Blake, Jr., Esquire. Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile 
    Island Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of amendment request: February 10, 1994
        Description of amendment request: The revision proposed by 
    Technical Specification Change Request (TSCR) No. 230 to the Technical 
    Specifications would revise specification 3.7.2.c, ``Unit Electric 
    Power System,'' to eliminate testing of an emergency diesel generator 
    (EDG) when the redundant EDG is inoperable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment serves to assure that an EDG is always 
    available to perform on demand and the lower number of demands for 
    performance reduce the probability of equipment failure. The 
    required action no longer requires a ``test'' be performed. 
    Therefore, the word ``test'' has been deleted from TS 3.7.2.c. The 
    change is administrative. Since the proposed amendment does not 
    affect the design or performance of the diesel generators or their 
    ability to perform their design function, the change will not result 
    in an increase in the consequences or probability of an accident 
    previously analyzed. The proposed change will increase diesel 
    generator reliability, thereby increasing overall plant safety.
        2. Operation of the facility in accordance with the proposed 
    amendment does not create the possibility of a new or different kind 
    of accident from any accident previously evaluated. Accidents 
    involving loss of off-site power and single failure have been 
    previously evaluated. The change does not introduce any new mode of 
    plant operation or new accident precursors, involve any physical 
    alterations to plant configurations, or make any changes to system 
    setpoints which could initiate a new or different kind of accident.
        3. Operation of the facility in accordance with the proposed 
    amendment does not involve a significant reduction in a margin of 
    safety. This change does not result in a reduction in the margin of 
    safety since there is no margin of safety associated with the 
    supplemental immediate and daily testing of the operable EDG. If a 
    margin of safety were presumed to exist, no reduction would result 
    because of the proposed amendment: no physical modification to the 
    plant or change to procedurally prescribed operator actions resulted 
    from the proposed amendment.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, Pennsylvania 17105.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine 
    YankeeAtomic Power Station, Lincoln County, Maine
    
        Date of amendment request: May 25, 1994
        Description of amendment request: The proposed amendment would 1) 
    allow entry through an operable personnel air lock hatch to perform 
    surveillance testing, repair an inoperable hatch, or perform other 
    necessary activities inside containment, 2) update plant Technical 
    Specifications to reflect a previous change to the list of containment 
    boundary valves, 3) add a new exception to allow quarterly surveillance 
    testing of the excess flow check valves, 4) add a new exception to 
    allow periodic preventive maintenance on control room ventilation 
    lasting up to 30 minutes per calendar quarter without a written report 
    of such inoperability, and 5) make related administrative changes to 
    reflect and clarify items 1 through 4 above.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The staff's analysis is 
    presented below:
        1. The proposed amendment would not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Containment air lock hatch entry, surveillance testing of the 
    excess flow check valves, and preventive maintenance of control room 
    ventilation are of short duration and do not alter any associated 
    remedial action completion times, or the requirements of Technical 
    Specification 3.0.A. If necessary, prompt operator action to restore 
    containment integrity, excess flow check valve position, or control 
    room ventilation is assured by plant operators, or individual(s) 
    procedurally dedicated to perform such restoration. The subject 
    containment boundary valves are manual containment isolation valves, 
    and the current specification allows them to be repositioned under 
    administrative control without compensatory measures to isolate the 
    penetration. The boundary valves to be added remain closed during 
    power operation, and are opened only after the reactor is shut down 
    and cooldown has begun. The boundary valves to be deleted are open 
    only during plant heatup.
        The staff therefore concludes that implementation of the proposed 
    change will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed amendment would not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed change to containment air lock hatch entry, 
    surveillance testing of the excess flow check valves, and preventive 
    maintenance of the control room ventilation system, will not affect 
    equipment reliability when such equipment is required to be 
    operable. The Limiting Conditions for Operation and Remedial Actions 
    for these items remain unchanged to govern operability of the 
    equipment. The containment boundary valves being added are closed 
    when the reactor is at power, and are opened only after the reactor 
    is shut down. The boundary valves being deleted are open only during 
    plant heatup. The subject boundary valves are manual containment 
    isolation valves, and the current specification allows them to be 
    repositioned under administrative control without compensatory 
    measures to isolate the penetration.
        The staff therefore concludes that implementation of the 
    proposed change will not create any new or different kind of 
    accident from any accident previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The proposed change would allow excess flow check valves to be 
    exercised through approximately 1.5 inches of valve travel on a 
    quarterly basis without declaring the valves inoperable or taking 
    compensatory measures. Such testing constitutes approximately 15 
    minutes per calendar quarter, during which time containment 
    isolation can easily be reestablished. Similarly, access through an 
    operable air lock hatch would allow the hatch to be open for only a 
    short period of time and while under control of an individual 
    dedicated to operating the hatch. The proposed change also permits 
    the control room ventilation system to be inoperable for 30 minutes 
    per calendar quarter, without a written report of such 
    inoperability. Because of the short time during which these systems 
    are unavailable, and because operation is easily reestablished, 
    there is no significant reduction in a margin of safety. The 
    containment boundary valves being added are closed when the reactor 
    is at power, and are opened only after the reactor is shut down. The 
    boundary valves being deleted are open only during plant heatup. The 
    subject boundary valves are manual containment isolation valves, and 
    the current specification allows them to be repositioned under 
    administrative control without compensatory measures to isolate the 
    penetration.
        The staff therefore concludes that implementation of the proposed 
    change would not involve a significant reduction in a margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, Maine 04578
        Attorney for licensee: Mary Ann Lynch, Esquire, Maine Yankee Atomic 
    Power Company, 83 Edison Drive, Augusta, Maine 04336
        NRC Project Director: Walter R. Butler
    
    Northeast Nuclear Energy Company (NNECO), Docket No. 50-
    245,Millstone Nuclear Power Station, Unit 1, New London County, 
    Connecticut
    
        Date of amendment request: April 29, 1994
        Description of amendment request: The amendment would change the 
    requirement for reactor operators (RO) in Table 6.2-1 from 2 to 3 for 
    the RUN, STARTUP/HOT STANDBY and HOT SHUTDOWN conditions. In addition, 
    two typographical corrections are made to page 6-4.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed changes in accordance with 
    10CFR50.92 and concluded that the changes do not involve a 
    significant hazards consideration (SHC). The basis for this 
    conclusion is that the three criteria of 10CFR50.92(c) are not 
    compromised. The proposed changes do not involve a significant 
    hazards consideration because the changes would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        Accident analyses for Millstone Unit No. 1 do not require a 
    specific number of operators. Increasing the Technical Specification 
    minimum to require a third RO does not decrease the effectiveness of 
    the shift staff in response to normal or abnormal conditions. In 
    fact, the third RO enhances the ability of the operating crew to 
    mitigate complex transients which could occur during beyond design 
    basis events. The shifts have trained and functioned at the higher 
    staffing level for several years.
        The typographical corrections to page 6-4 provide a clearer 
    representation of the required actions, and do not affect the intent 
    nor implementation of the specification.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of a previously analyzed 
    accident.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The addition of a third RO to the minimum shift-crew composition 
    required by Technical Specification Table 6.2-1 does not affect the 
    operation of the unit, nor does it change any of the operating 
    procedures, off-normal procedures, or EOPs [emergency operating 
    procedures]. Staffing the control room with an additional operator 
    enhances the capability of the operating crew to mitigate 
    transients. Therefore, addition of a third RO to the minimum shift-
    crew composition cannot create the possibility of a new or different 
    accident.
        3. Involve a significant reduction in the margin of safety.
        The proposed addition of a third reactor operator is to ensure 
    that sufficient operating staff is available to respond to complex 
    transients involving multiple equipment failures. Ensuring that 
    sufficient resources are available to cope with beyond design basis 
    event scenarios provides an increase in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, Connecticut 06360.
        Attorney for licensee: Gerald Garfield, Esquire, Day, Berry & 
    Howard, Counselors at Law, City Place, Hartford, Connecticut 06103-
    3499.
        NRC Project Director: John F. Stolz
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut
    
        Date of amendment request: May 6, 1994
        Description of amendment request: The proposed amendment would 
    modify the Limiting Conditions for Operation (LCO) for the Millstone 
    Unit 2 Technical Specifications 3.8.2.3 and 3.8.2.4 and the 
    surveillance requirement of TS 4.8.2.3.2.c.3. These changes relate to 
    the amperage requirements and the charging capability of the DC 
    distribution systems.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes do not involve an SHC [significant hazards 
    consideration] because the changes would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        In 1993, revised battery and battery charger sizing calculations 
    demonstrated that a charger capacity of 400 amperes is sufficient to 
    provide the continuous DC loads, and is capable of recharging a 
    fully discharged station battery in a timely manner consistent with 
    the design basis discussed in Section 8.5.3.1 of the Millstone Unit 
    No. 2 FSAR [Final Safety Analysis Report]. The calculations 
    determined that the largest continuous load was 154 amperes; 
    therefore, 400 amperes of charging capacity could provide 246 
    amperes to recharge a battery.
        The calculations conservatively demonstrated that this charging 
    capacity could recharge a battery in 10.37 hours. This recharging 
    time is well within the 12-hour recharging time discussed in Section 
    8.5.3.1 of the Millstone Unit No. 2 FSAR. Additionally, this 
    recharging time is more conservative than the 24-hour recharging 
    time stated in Section 8.3.2 of the original Safety Evaluation for 
    Millstone Unit No. 2. Therefore, the proposed changes do not involve 
    a significant increase in the probability or consequences of an 
    accident previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed LCO and surveillance changes do not alter the 
    existing DC bus configuration, as described in Section 8.5.3.1 of 
    the Millstone Unit No. 2 FSAR. This bus configuration has been 
    previously analyzed, and was found acceptable. The proposed changes 
    also meet the recharging time specified in the design basis. 
    Therefore, the proposed changes do not create the possibility of a 
    new or different kind of accident from any previously analyzed.
        3. Involve a significant reduction in the margin of safety.
        In 1993, revised battery and battery charger sizing calculations 
    demonstrated that a charger capacity of 400 amperes is sufficient to 
    provide the continuous DC loads, and is capable of recharging a 
    fully discharged station battery in a timely manner consistent with 
    the design basis discussed in Section 8.5.3.1 of the Millstone Unit 
    No. 2 FSAR. The calculations determined that the largest continuous 
    load was 154 amperes; therefore, 400 amperes of charging capacity 
    could provide 246 amperes to recharge a battery. The calculations 
    conservatively demonstrated that this charging capacity could 
    recharge a battery in 10.37 hours. This recharging time is well 
    within the 12-hour recharging time discussed in Section 8.5.3.1 of 
    the Millstone Unit No. 2 FSAR. Additionally, this recharging time is 
    more conservative than the 24-hour recharging time stated in Section 
    8.3.2 of the original Safety Evaluation for Millstone Unit No. 2. 
    Therefore, the proposed changes do not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, Connecticut 06360.
        Attorney for licensee: Gerald Garfield, Esquire, Day, Berry & 
    Howard, City Place, Hartford, Connecticut 06103-3499.
        NRC Project Director: John F. Stolz
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut
    
        Date of amendment request: May 6, 1994
        Description of amendment request: The proposed amendment would 
    provide additional Technical Specification requirements regarding non-
    Quality Assurance (QA) equipment utilized to achieve feedwater 
    isolation in response to a main steam line break (MSLB) inside 
    containment. Specifically the amendment would incorporate additional 
    sections numbered 3/4.7.1.6, titled ``Plant Systems - Main Feedwater 
    Isolation Components (MFICs);'' 3/4.8.2.1A, titled '' Onsite Power 
    Distribution Systems - A.C. Distribution - Operating;'' and 3/4.8.2.5, 
    titled ``Onsite Power Distribution Systems (Turbine Battery) - D.C. 
    Distribution - Operating.'' In addition, the proposed amendment would 
    modify the Index and the Bases to reflect the additional requirements.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed changes in accordance with 
    10CFR50.90 and has concluded that the changes do not involve a 
    significant hazards consideration (SHC). The basis for this 
    conclusion is that the three criteria of 10CFR50.92(c) are not 
    compromised. The proposed changes do not involve an SHC because the 
    changes would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        Currently, the Millstone Unit No. 2 Technical Specifications 
    contain response time requirements for the feedwater isolation 
    valves to ensure rapid isolation of feedwater to the steam 
    generators and to maintain the peak containment pressure below the 
    containment design pressure of 54 psig. However, clear Action 
    Statements specifying operability requirements for the non-QA 
    equipment associated with feedwater isolation are not included 
    within the Millstone Unit No. 2 Technical Specifications. NNECO's 
    proposal to add sections 3/4.7.1.6, 3/4.8.2.1A, and 3/4.8.2.5 into 
    the Millstone Unit No. 2 Technical Specifications will incorporate 
    additional requirements regarding components that are credited to 
    provide feedwater isolation in the event of an MSLB inside 
    containment. These proposed changes will impose additional 
    limitations, restrictions, and controls not currently in place in 
    the Millstone Unit No. 2 Technical Specifications.
        Additionally, NNECO's proposals to modify the Bases and the 
    Index of the Millstone Unit No. 2 Technical Specifications will: 1) 
    provide personnel with information concerning the additional 
    requirements, and 2) correct an editorial error. These proposed 
    changes to the Bases and the Index do not alter the manner in which 
    equipment is operated, nor do they affect equipment availability.
        Based on the above, the proposed license amendment does not 
    involve a significant increase in the probability or consequences of 
    an accident previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        NNECO's proposal to add section 3/4.7.1.6, 3/4.8.2.1A, and 3/
    4.8.2.5 into the Millstone Unit No. 2 Technical Specifications will 
    incorporate additional requirements regarding components that are 
    credited to provide feedwater isolation in the event of an MSLB 
    inside containment. These proposed changes will impose additional 
    limitations, restrictions, and controls not currently in place in 
    the Millstone Unit No. 2 Technical Specifications.
        Additionally, NNECO's proposals to modify the Bases and the 
    Index of the Millstone Unit No. 2 Technical Specifications will: 1) 
    provide personnel with information concerning the additional 
    requirements, and 2) correct an editorial error. These proposed 
    changes to the Bases an the Index do not alter the manner in which 
    equipment is operated, nor do they affect equipment availability.
        Based on the above, the proposed license amendment cannot create 
    the possibility of a new or different kind of accident from any 
    previously analyzed.
        3. Involve a significant reduction in a margin of safety.
        NNECO's proposal to add sections 3/4.7.1.6, 3/4.8.2.1A, and 3/
    4.8.2.5 into the Millstone Unit No. 2 Technical Specifications will 
    incorporate additional requirements regarding components that are 
    credited to provide feedwater isolation in the event of an MSLB 
    inside containment. These proposed changes will impose additional 
    limitations, restrictions, and controls not currently in place in 
    the Millstone Unit No. 2 Technical Specifications.
        Additionally, NNECO's proposals to modify the Bases and the 
    Index of the Millstone Unit No. 2 Technical Specifications will: 1) 
    provide personnel with information concerning the additional 
    requirements, and 2) correct an editorial error. These proposed 
    changes to the Bases and the Index do not alter the manner in which 
    equipment is operated, nor do they affect equipment availability.
        Therefore, this proposed license amendment does not involve a 
    significant reduction in a margin of safety. In fact. The margin of 
    safety will be increased due to the imposition of restriction on the 
    non-QA equipment credited for feedwater isolation in the event of an 
    MSLB inside containment.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, Connecticut 06360.
        Attorney for licensee: Gerald Garfield, Esquire, Day, Berry & 
    Howard, City Place, Hartford, Connecticut 06103-3499.
        NRC Project Director: John F. Stolz
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of amendment request: May 6, 1994
        Description of amendment request: The proposed amendment modifies 
    the monthly operational test of the reactor trip bypass breakers to 
    monthly staggered, such that each breaker is tested every 62 days.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes do not involve an SHC [significant hazards 
    consideration] because the changes would not:
        1. Involve a significant increase in probability or consequences 
    of an accident previously evaluated.
        Revising the technical specifications to require a staggered 
    monthly surveillance operational test of the reactor trip bypass 
    breakers (such that each breaker is tested every 62 days) will only 
    make operational testing of the reactor trip bypass breakers 
    consistent with operational testing of the trip breakers and the 
    automatic trip and interlock logic. It will also reduce cycling of 
    the reactor trip bypass breakers by eliminating the requirement to 
    test both bypass breakers during the monthly surveillance, thereby 
    reducing maintenance and surveillance time. The proposed changes do 
    not affect any of the design basis accidents nor are there any 
    malfunctions associated with these changes.
        Additionally, this technical specification bases change only 
    clarifies both the meaning of a reactor trip breaker and trip 
    breaker train which have been included for completeness and clarity 
    concerning the reactor trip breaker system.
        2. Create the possibility of a new or different kind of accident 
    previously evaluated.
        Revising the technical specifications to require a staggered 
    monthly surveillance operational test of the reactor trip bypass 
    breakers (such that each breaker is tested every 62 days) will only 
    make operational testing of the reactor trip bypass breakers 
    consistent with operational testing of the reactor trip breakers and 
    the automatic trip and interlock logic. There are no new failure 
    modes associated with the proposed changes. Since the plant will 
    continue to operate as designed, the proposed changes will not 
    modify the plant response to the point where it can be considered a 
    new accident.
        3. Involve a significant reduction in a margin of safety.
        Revising the technical specifications to require a staggered 
    monthly surveillance operational test of the reactor trip bypass 
    breakers (such that each breaker is tested ever 62 days) will only 
    make operational testing of the reactor trip bypass breakers 
    consistent with operational testing of the reactor trip breakers and 
    the automatic trip and interlock logic. It will also reduce cycling 
    of the reactor trip bypass breakers by eliminating the requirement 
    to test both bypass breakers during the monthly surveillance, 
    thereby reducing maintenance and surveillance time. The proposed 
    changes do not have any adverse impact on the protective boundaries 
    nor do they affect the consequences of any accident previously 
    analyzed. The surveillance requirements will still ensure that the 
    reactor trip breakers and the reactor trip bypass breakers are 
    tested and within the limits. Therefore, the proposed changes will 
    not impact the margin of safety as designated in the bases of any 
    technical specification.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, Connecticut 06360.
        Attorney for licensee: Gerald Garfield, Esquire, Day, Berry & 
    Howard, City Place, Hartford, Connecticut 06103-3499.
        NRC Project Director: John F. Stolz
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of amendment request: May 18, 1994
        Description of amendment request: The amendment would change 
    operability requirements for the Fuel Building Exhaust Filter System to 
    require it to be operable whenever irradiated fuel is in the spent fuel 
    pool, which has had less than 60 days of decay time. Surveillance 
    requirements for the Fuel Building Exhaust Filter System would be 
    changed to require that the system be tested and verified operable at 
    no greater than 31 days prior to its required usage.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        ...The proposed change does not involve an SHC [significant 
    hazards consideration] because the change would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed modification will revise the period of time during 
    which the Fuel Building Exhaust Filter System must be operable.
        The propose[d] change will require that the system is operable 
    whenever irradiated fuel, which has decayed less than 60 days, is in 
    the spent fuel pool. Currently, the system is required to be 
    operable whenever a load is moved over the pool or fuel is being 
    moved in the pool.
        The modification has no effect on the probability of a fuel 
    handling accident. The consequences of a fuel handling accident has 
    been evaluated at two intervals. The first time is the minimum decay 
    time. At this time (t=100 hours) with irradiated fuel in the pool, 
    the Fuel Building Exhaust Filter System is required, per the 
    existing and the proposed Technical Specification, to be operable. 
    Therefore, the consequences of an accident are identical to that 
    described in the FSAR [Final Safety Analyses Report]. The second 
    scenario evaluated is when the filters are initially isolated (t=60 
    days). The resultant offsite dose, assuming no filtration and lower 
    core inventory due to decay, are significantly lower than was 
    calculated at t=100 hours. Therefore, the existing accident analysis 
    in FSAR Section 15.7.4 is limiting and the proposed modification 
    will not impact the probability or consequences of an accident.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        The proposed change does not impact any system or component 
    which could cause a fuel handling accident. The Fuel Building 
    Exhaust Filter System is used for accident mitigations. It's failure 
    cannot, in any way, create the possibility of a new or different 
    kind of accident.
        3. Involve a significant reduction in a margin of safety.
        The proposed change to the Fuel Building Exhaust Filter System 
    has been analyzed at the two most critical times. The first analysis 
    was done when the fuel is first placed in the pool, and the second 
    analysis was done when the filtration system is isolated. The first 
    event resulted in no change in assumptions in the analysis presented 
    in the FSAR, ergo no change in dose. The second event has been 
    analyzed and doses have decreased, when compared to the first event. 
    The system will be verified operable per the performance of 
    Surveillance Requirement 4.9.12a prior to fuel or load movement over 
    the pool. Therefore, there is no reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, Connecticut 06360.
        Attorney for licensee: Gerald Garfield, Esquire, Day, Berry & 
    Howard, City Place, Hartford, Connecticut 06103-3499.
        NRC Project Director: John F. Stolz
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: May 13, 1994
        Description of amendment request: This amendment would revise 
    Technical Specifications Surveillance Requirement 4.8.1.1.2e.8, which 
    requires that an emergency diesel generator be retested within 5 
    minutes after completing a 24-hour endurance run.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specifications (TS) change does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The proposed TS change would revise the Emergency Diesel 
    Generator (EDG) surveillance criteria to allow the hot restart test 
    to be performed independent of the Engineered Safety Features (ESF) 
    load sequencing test and the 24 hour endurance run. The proposed 
    surveillance requirements would continue to demonstrate that the 
    objectives of each of these tests are met. Specifically, the EDG's 
    are shown to be capable of starting the ESF loads in the required 
    sequence, operating at full load for an extended period of time, and 
    restarting from a full load temperature condition. Therefore, the 
    proposed changes would not adversely affect the EDG's ability to 
    support mitigation of the consequences of any previously evaluated 
    accident. The proposed changes to the surveillance requirements do 
    not affect the initiation or progression of any accident sequence.
        Therefore, the proposed change does not involve an increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed TS change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        This proposed TS change does not require physical changes to the 
    plant or equipment, and does not impact any design or functional 
    requirements of the Emergency Diesel Generators (EDGs). The proposed 
    change affects surveillance test criteria such that increased 
    scheduling flexibility is allowed while the test objectives 
    associated with demonstrating EDG operability continue to be met. 
    The proposed changes do not allow any plant configurations that are 
    presently prohibited by the Technical Specifications.
        Therefore, the proposed TS change does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. The proposed TS change does not involve a significant 
    reduction in a margin of safety.
        The proposed TS change does not involve a change to the physical 
    design or functional requirements of the Emergency Diesel Generators 
    (EDGs). Surveillance testing in accordance with the proposed 
    Technical Specification will continue to demonstrate the ability of 
    the EDG's to perform their intended function of providing electrical 
    power to ESF systems needed to mitigate design basis transients, 
    consistent with the plant safety analyses. The margin of safety 
    demonstrated by the plant safety analyses is therefore not affected 
    by the proposed change.
        Therefore, the proposed TS change does not involve a reduction 
    in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: Charles L. Miller
    
    Philadelphia Electric Company, Public Service Electric and Gas 
    Company,Delmarva Power and Light Company, and Atlantic City 
    Electric Company,Docket No. 50-277, Peach Bottom Atomic Power 
    Station, Unit No. 2,York County, Pennsylvania
    
        Date of application for amendment: May 13, 1994
        Description of amendment request: The proposed amendment would 
    extend the Type A test (i.e., Containment Integrated Leak Rate Test) 
    interval on a one-time basis.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specifications (TS) change does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The accidents which are potentially negatively impacted by the 
    proposed change are any Loss of Coolant Accident (LOCA) inside 
    primary containment as described in the PBAPS [Peach Bottom Atomic 
    Power Station], Units 2 and 3 UFSAR [Updated Final Safety Analysis 
    Report].
        The proposed change increases the surveillance interval of the 
    10 CFR [Part] 50, Appendix J Type A test (i.e., Containment 
    Integrated Leakage Rate Test (CILRT)) from 42 months to 66 months. 
    This test is performed to determine that the total leakage from 
    containment does not exceed the maximum allowable primary 
    containment leakage rate (i.e., designated La) at a calculated peak 
    containment internal pressure (Pa), as defined in 10 CFR [Part] 50, 
    Appendix J. The primary containment limits the leakage of 
    radioactive material during and following design bases accidents in 
    order to comply with the offsite dose limits specified in 10 CFR 
    [Part] 100. Accordingly, the primary containment is not an accident 
    initiator, it is an accident mitigator. No physical or operational 
    changes to the containment structure, plant systems, or components 
    would be made as a result of the proposed change. Therefore, the 
    probability of occurrence of an accident previously evaluated is not 
    increased.
        The failure effects that are potentially created by the proposed 
    one-time TS change have been considered. The relevant components 
    important to safety which are potentially affected are the 
    containment structure, plant systems, and containment penetrations. 
    There are no physical or operational changes to any plant equipment 
    associated with the proposed TS change. Therefore, the probability 
    or consequences of a malfunction of equipment important to safety is 
    not increased.
        The proposed change introduces the possibility that primary 
    containment leakage in excess of the allowable value (i.e., La) 
    would remain undetected during the proposed 24 month extension of 
    the interval between the second and third Type A test. The types of 
    mechanisms which could cause degradation of the primary containment 
    can be categorized into two types. These are: 1) degradation due to 
    work which is performed as part of a modification or maintenance 
    activity on a component or system (i.e., activity-based), or; 2) 
    degradation resulting from a time-based failure mechanism.
        A review of activity-based failure mechanisms has determined 
    that the potential from degradation due to activity based mechanisms 
    is minimal.
        Regarding the potential for primary containment degradation due 
    to a time-based mechanism, we have concluded that the PBAPS Local 
    Leak Rate Test (LLRT) program would identify most types of 
    penetration leakage. The LLRT program involves measurement of 
    leakage from Type B and Type C primary containment penetrations as 
    defined in 10 CFR [Part] 50, Appendix J.
        The 10 CFR [Part] 50, Appendix J, Type B tests are intended to 
    detect local leaks and to measure leakage across pressure containing 
    or leakage-limiting boundaries other than valves, such as 
    containment penetrations incorporating resilient seals, gaskets, 
    expansion bellows, flexible seal assemblies, door operating 
    mechanism penetrations that are part of the containment system, 
    doors, and hatches. 10 CFR [Part] 50, Appendix J, Type C testing is 
    intended to measure reactor system primary containment isolation 
    valve leakage rates. The frequency of the Type B and Type C testing 
    is not being altered by the proposed TS change. [However, in an 
    April 18, 1994 letter, the licensee has requested a 60-day extension 
    of the Type B and Type C testing.] The acceptance criterion for Type 
    B and Type C leakage is 0.6 La (i.e., 0.3 % wt/day) which, when 
    compared to the Type A test acceptance criterion of 0.75 La (i.e., 
    0.375 % wt/day), is a significant portion of the Type A test 
    allowable leakage.
        The proposed TS change only extends the interval between two 
    consecutive Type A tests. The Type B and Type C tests will be 
    performed as required. The Type B and Type C tests will continue to 
    be used to confirm that the containment isolation valves and 
    penetrations have not degraded. Containment system components that 
    would not be tested are the containment structure itself and small 
    diameter instrumentation lines. Time-based degradation of any of the 
    instrumentation lines would most likely be identified by faulty 
    instrument indication or during instrument calibrations that will be 
    performed during the PBAPS, Unit 2 refueling outage 10. In examining 
    the potential for a time-based failure mechanism that could cause 
    significant degradation of the containment structure, we concluded 
    that the risk, if any, of such a mechanism is small since the design 
    requirements and fabrication specifications established for the 
    containment structure are in themselves adequate to ensure 
    containment leak tight integrity.
        Based on the above evaluation, we have concluded that the 
    proposed TS change will have a negligible impact on the consequences 
    of any accident previously evaluated. To support this conclusion, a 
    review of the PBAPS, Unit 2 CILRT history was performed. This review 
    identified that the only failure mechanism that has been detected 
    during the past CILRTs is an activity based component failure, and 
    that there is no indication of any time-based degradation that would 
    not be identified during performance of Type B and Type C tests.
        Although this review concluded that the risk of undetected 
    primary containment degradation is not increased, the Individual 
    Plant Examination (IPE) for PBAPS, Units 2 and 3, was also reviewed 
    in order to assess the impact of exceeding the primary containment 
    allowable leakage rate, if a non-mechanistic activity type (i.e., 
    time-based) failure were to occur. The IPE included an evaluation of 
    the effect of various containment leakage sizes under different 
    scenarios. The IPE results showed that a containment leakage rate of 
    35% wt/day would represent less than a 5% increase in risk to the 
    public being exposed to radiation. This evaluation was based on a 
    study performed by Oak Ridge National Laboratory for light water 
    reactors that evaluated the impact of leakage rates on public risk. 
    As stated earlier, the current value of La for PBAPS, Unit 2, is 
    0.5% wt/day, which is significantly less than the 35% wt/day 
    discussed in the IPE evaluation.
        Therefore, the proposed TS change involving a one-time extension 
    of the Type A test interval and performing the third Type A test 
    after the second Appendix J 10-year service period will not involve 
    an increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed TS change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed change is an increase of a surveillance test 
    interval and does not make any physical or operational changes to 
    existing plant systems or components. Primary containment acts as an 
    accident mitigator not initiator. Therefore, the possibility of a 
    different type of accident than any previously evaluated or the 
    possibility of a different type of equipment malfunction is not 
    introduced.
        Therefore, the proposed TS change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed TS change does not involve a significant 
    reduction in a margin of safety.
        The total primary containment leakage rate ensures that the 
    total containment leakage volume will not exceed the value assumed 
    in the safety analyses at the peak accident pressure. As an added 
    conservatism, the measured overall leakage rate is further limited 
    to less than or equal to 0.75 La during performance of periodic 
    tests to account for possible degradation of the containment leakage 
    barriers between leakage tests. There is the potential that 
    containment degradation could remain undetected during the proposed 
    24 month surveillance interval extension and result in the 
    containment leakage exceeding the allowable value assumed in safety 
    analysis. A review of activity-based failure mechanisms has 
    determined that the potential from degradation due to activity based 
    mechanisms is minimal.
        Regarding the potential for primary containment degradation due 
    to a time-based mechanism, we have concluded that the PBAPS Local 
    Leak Rate Test (LLRT) program would identify most types of 
    penetration leakage. The LLRT program involves measurement of 
    leakage from Type B and Type C primary containment penetrations as 
    defined in 10 CFR [Part] 50, Appendix J.
        The 10 CFR [Part] 50, Appendix J, Type B tests are intended to 
    detect local leaks and to measure leakage across pressure containing 
    or leakage-limiting boundaries other than valves, such as 
    containment penetrations incorporating resilient seals, gaskets, 
    expansion bellows, flexible seal assemblies, door operating 
    mechanism penetrations that are part of the containment system, 
    doors, and hatches. 10 CFR [Part] 50, Appendix J, Type C testing is 
    intended to measure reactor system primary containment isolation 
    valve leakage rates. The frequency of the Type B and Type C testing 
    is not being altered by the proposed TS change.
        Finally, a review of the results of previous PBAPS, Unit 2 CILRT 
    results concluded that the only failure mechanism which has been 
    detected during the past CILRTs is activity-based and that there is 
    no indication of time-based failures that would not be identified 
    during performance of Type B and Type C tests. Therefore, we have 
    concluded that the proposed extended test interval would not result 
    in a non-detectable PBAPS, Unit 2 primary containment leakage rate 
    in excess of the allowable value (i.e., 0.5% wt/day) established by 
    the TS and 10 CFR [Part] 50, Appendix J.
        Therefore, the proposed TS change does not involve a reduction 
    in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: Charles L. Miller
    
    South Carolina Electric & Gas Company, South Carolina Public 
    ServiceAuthority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of amendment request: March 11, 1994
        Description of amendment request: The proposed amendment would 
    reduce the allowed outage time for the residual heat removal (RHR) 
    suction relief valves (SRVs) in accordance with the guidance of Generic 
    Letter (GL) 90-06.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. The probability or consequences of an accident previously 
    evaluated is not significantly increased.
        This change decreases the allowed outage time of a Low 
    Temperature Overpressure Protection (LTOP) system. There is no 
    hardware, software, or operating methodology change, so there is no 
    increase in probability or consequences. Since the time allowed for 
    one train of this equipment to be inoperable is shorter, the 
    probability of an overpressure event not being mitigated has also 
    been reduced. The consequences will not change unless the system or 
    operation of the system changes.
        2. [The proposed change will not] [c]reate the possibility of a 
    new or different kind of accident from any previously analyzed.
        As this proposed change will not involve any changes to 
    hardware, software, or operating practices, it cannot create any 
    possibility of new or different kinds of accidents from those 
    previously analyzed. The RHR SRVs are intended to provide protection 
    against a rupture of a pressure boundary from an over-pressure 
    condition which has the potential to result in core uncovery. The 
    original design basis of the plant complies with the requirements of 
    10 CFR 50 Appendix G and uses the RHR SRVs to meet the fracture 
    toughness requirements of 10 CFR 50 Appendix G. This change only 
    increases the availability of this protection and does not create 
    any new or different kinds of accidents.
        3. [The proposed amendment does not] [i]nvolve a significant 
    reduction in a margin of safety.
        SCE&G already has administrative controls in place to minimize 
    the possibility of an overpressure event occurring as well as to 
    assure that there are two trains of LTOP equipment operable during 
    the modes when the potential exists for this event. There are 
    controls to preclude the inadvertent start-up of a Reactor Coolant 
    Pump or Charging Pump and controls to ensure that both RHR Suction 
    Isolation Valves for each train are open and remain open except for 
    testing and maintenance. This alignment is maintained until the RHR 
    System is realigned for its ECCS function. These controls are 
    proceduralized in plant operating procedures.
        This change does not involve a significant reduction in a margin 
    of safety as nothing is changed which affects the margin in a 
    negative direction. The decrease in AOT actually increases the 
    margin since the allowed time for one train to be inoperable has 
    been reduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Fairfield County Library, 
    Garden and Washington Streets, Winnsboro, South Carolina 29180
        Attorney for licensee: Randolph R. Mahan, South Carolina Electric & 
    Gas Company, Post Office Box 764, Columbia, South Carolina 29218
        NRC Project Director: William H. Bateman
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of amendment request: May 16, 1994 (TS 94-03)
        Description of amendment request: The proposed change would remove 
    Table 3.3-2, ``Reactor Trip System Instrumentation Response Times,'' 
    and Table 3.3-5, ``Engineered Safety Features Response Times,'' from 
    the technical specifications and incorporate the limits into the 
    Updated Final Safety Analysis Report. In addition, references to these 
    tables in Specifications 3.3.1.1, 3.3.2.1, and 4.3.1.1.3 (for Unit 1) 
    and 3.3.1, 3.3.2, and 4.3.1.1.3 (for Unit 2) would be removed. A 
    footnote would be added to Specification 4.3.1.1.3 indicating that 
    neutron detectors are exempt from response time testing. These changes 
    have been proposed in accordance with Generic Letter 93-08. A change to 
    the Bases would indicate that the response time limits would be 
    maintained in the Updated Final Safety Analysis Report.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        TVA has evaluated the proposed technical specification (TS) 
    change and has determined that it does not represent a significant 
    hazards consideration based on criteria established in 10 CFR 
    50.92(c). Operation of Sequoyah Nuclear Plant (SQN) in accordance 
    with the proposed amendment will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change does not alter the response time limit 
    requirements for the reactor trip or engineered safety feature 
    actuation systems or surveillance testing and frequency. Placing 
    these limits in the Updated Final Safety Analysis Report (UFSAR) 
    will ensure the plant design basis is maintained in accordance with 
    10 CFR 50.59. Since no actual changes to response time limits or 
    surveillance requirements are involved, the probability or 
    consequences of an accident are not increased.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed changes does not affect any plant equipment, 
    functions, or setpoint by relocating response time limits to the 
    UFSAR. Therefore, the possibility of a new or different kind of 
    accident is not created.
        3. Involve a significant reduction in a margin of safety.
        The proposed change will continue to require SQN to maintain the 
    plant functions at the required setpoints necessary for the design 
    basis and to support the accident analysis. The margin of safety is 
    not reduced because there is no change to plant functions and the 10 
    CFR 50.59 process will continue to ensure the plant design basis is 
    appropriately maintained.
        The NRC has reviewed the licensee's analysis and, based on 
    thisreview, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of amendment request: May 18, 1994 (TS 94-05)
        Description of amendment request: The proposed change would add a 
    note to the action statement for Limiting Condition for Operation 
    3.7.7, ``Control Room Emergency Ventilation System,'' indicating that 
    the provisions of TS 3.0.3 are not applicable while performing actions 
    associated with a tornado warning.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        TVA has evaluated the proposed technical specification (TS) 
    change and has determined that it does not represent a significant 
    hazards consideration based on criteria established in 10 CFR 
    50.92(c). Operation of Sequoyah Nuclear Plant (SQN) in accordance 
    with the proposed amendment will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The control room emergency ventilation system (CREVS) was 
    designed to ensure control room habitability during accident 
    conditions. The design basis of SQN does not include an accident 
    creating a contaminated air condition concurrent with a tornado. The 
    ability of the CREVS to perform its design function has not been 
    affected by this change. The proposed change will not increase the 
    possibility or consequences of an accident.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        An accident involving a contaminated air condition and a tornado 
    have been analyzed as part of the SQN design basis. Both accidents 
    are assumed to occur independently. This change does not create a 
    new or different accident not previously analyzed.
        3. Involve a significant reduction in a margin of safety.
        The design basis of the CREVS is not impacted by this TS change. 
    There is no change in any assumptions made in the Final Safety 
    Analysis Report. Therefore, there is no reduction in the margin of 
    safety as a result of this change.
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of amendment request: March 19, 1994; superseded May 16, 1994 
    (TS 93-04)
        Description of amendment request: The proposed change would clarify 
    and consolidate the technical specifications (TS) regarding the dual 
    function of the containment vacuum relief system (i.e., the vacuum 
    relief and containment isolation functions). The proposed changes would 
    revise TS 3/4.6.6, ``Vacuum Relief Valves,'' to indicate the actions 
    that would be required should one or more vacuum relief (VR) lines be 
    incapable of performing its containment isolation function or incapable 
    of performing its VR function. In addition, the testing requirements 
    would be revised to add specific requirements and reflect the inservice 
    test (IST) program by relocating the testing requirements from TS 
    4.6.3.2.d and Table 3.6-2 to the new TS 4.6.6 (and to Sequoyah's IST 
    program). Other proposed changes affect Bases 3/4.6.6 section and TS 
    index pages to reflect the proposed changes indicated above. This 
    proposed change was originally noticed on May 12, 1993 (58 FR 28060), 
    which is superseded by this notice.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        TVA has evaluated the proposed technical specification (TS) 
    change and has determined that it does not represent a significant 
    hazards consideration based on criteria established in 10 CFR 
    50.92(c). Operation of Sequoyah Nuclear Plant (SQN) in accordance 
    with the proposed amendment will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        TVA's proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    The proposed change does not increase the probability of an accident 
    since the proposed change does not affect any plant systems, 
    equipment, or components. The dual design functions of SQN's 
    containment vacuum relief (VR) system (i.e., provide containment VR 
    and containment isolation) are not affected. The consequences of an 
    event are not significantly increased by the proposed increase in 
    allowed outage time from 4 hours to 72 hours for returning an 
    inoperable VR system to operable status. The probability of an event 
    during the relatively short duration of the TS completion times, in 
    conjunction with the redundancy provided in the design of the 
    system, provide sufficient assurance that the VR lines are available 
    for mitigating an accident or abnormal event.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        No physical modification is being made to any plant hardware or 
    plant operating setpoints, limits, or operating procedures as a 
    result of this change. TVA's proposed change provides a TS 
    improvement that clarifies the TS requirements associated with the 
    dual design function of SQN's VR system. The proposed change removes 
    the potential for creating a conflict between Specification 3/4.6.3, 
    ``Containment Isolation Valves,'' and Specification 3/4.6.6, 
    ``Vacuum Relief Valves.''
        The proposed change does not alter any accident analysis or any 
    assumptions used to support the accident analyses. The containment 
    leakage assumptions used to determine offsite dose limits for 
    compliance with 10 CFR 100 are not affected. The analysis that 
    supports the containment VR system also remains unchanged. The 
    proposed 72-hour and 1-hour completion times for returning an 
    inoperable VR line to operable status are consistent with the NUREG-
    1431 and NUREG-1433. Consequently, the proposed change does not 
    create the possibility of a new or different kind of accident from 
    any previously analyzed.
        3. Involve a significant reduction in a margin of safety.
        The margin of safety provided by the design of SQN's containment 
    VR system remains unchanged. TVA's proposed change does not affect 
    the VR function or the containment isolation function that currently 
    exists in SQN TSs. The proposed change eliminates the potential for 
    conflicting requirements within SQN TSs and ensures that the proper 
    action is taken to preserve these dual design functions while the 
    plant is in Modes 1, 2, 3, or 4. TVA's proposed change provides a TS 
    improvement that combines these functional requirements into a 
    single specification. Both VR and containment isolation requirements 
    will continue to be provided. Accordingly, the proposed change does 
    not involve a reduction in the margin of safety.
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library,1101 Broad Street, Chattanooga, Tennessee 37402
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: February 14, 1993
        Brief description of amendments: The proposed amendments would 
    revise the Comanche Peak Steam Electric Station (CPSES), Units 1 and 2, 
    technical specifications (TS) by (1) changing the allowable value for 
    Unit 2 overtemperature N-16 and pressurizer pressure-low setpoints, (2) 
    deleting Equation 2.2-1 from TS 2.2.1, and (3) administrative changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of a previously evaluated 
    accident.
        Overtemperature N-16, Unit 2
        Incorporation of the increased temperature uncertainties 
    reported by Rosemount will change the Allowable Value of the 
    Overtemperature N-16 trip function. The change does not affect the 
    Safety Analysis Limits assumed in the accident analysis. Because the 
    change only impacts the Allowable Value for a setpoint and does not 
    affect any system designs or operations, the change does not 
    increase the probability of an accident. Although the Allowable 
    Value is changed in the conservative direction, the change assures 
    that, considering the newly identified transmitter uncertainty, the 
    trip actuates prior to the conditions assumed in the accident 
    analyses. As such, there is no impact on the consequences of any 
    accidents previously evaluated.
        Pressurizer Pressure - Low, Unit 2
        The added uncertainties change the Allowable Value of the Unit 2 
    Pressurizer Pressure-Low Reactor Trip function. The change does not 
    affect the Safety Analysis Limits assumed in the accident analysis. 
    Because the change only impacts the Allowable Value for a setpoint 
    and does not affect the system design or operations, the change does 
    not increase the probability of an accident. Although the Allowable 
    Value is changed in the conservative direction, the change assures 
    that, considering the newly identified transmitter uncertainty, the 
    trip actuates prior to the conditions assumed for the accident 
    analyses. As such, there is no impact on the consequences of any 
    accidents previously evaluated.
        Equation 2.2-1
        The changes to Specifications 2.2.1 and 3.3.2, to Tables 2.2-1 
    and 3.3-3, and to the bases sections will require recalibration of 
    the channel and removal of any accumulated errors in any function 
    whose ``as found'' setpoint is found to be less conservative than 
    its allowable value. These changes delete a potentially less 
    conservative option and will result in actual channel operation 
    closer to the nominal setpoint and within the allowable value band. 
    These changes will in effect validate one of the assumptions made in 
    the accident analysis and will not increase the probability or 
    consequences of any accident evaluated in the Safety Analysis 
    Report.
        Administrative Changes
        The changes to combine the Unit 1 and Unit 2 line items into a 
    dual Unit line if the Trip Setpoint and Allowable Value values are 
    the same is administrative and meant as a human factors improvement 
    for operator convenience. The change does not affect the operation 
    of any equipment, the operating point of any equipment, nor any 
    equipment hardware and thus does not increase the probability or 
    consequences of any accident evaluated in the Safety Analysis 
    Report.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously analyzed accident.
        Overtemperature N-16 and Pressurizer Pressure - Low, Unit 2
        As the proposed amendment changes only the Unit 2 Allowable 
    Values of the Overtemperature N-16 reactor trip and the Pressurizer 
    Pressure-Low reactor trip and does not have any physical effect on 
    the transmitter or circuitry, there are no new or different types of 
    accident introduced.
        Equation 2.2-1
        Deletion of this equation and its associated action statements, 
    definitions and values does not introduce any physical changes to 
    any systems, structures, or components. The change merely assures 
    that setpoints which are less conservative than their Allowable 
    Value are recalibrated prior to being declared operable. These 
    changes do not introduce any new credible failure modes which may 
    create the possibility of a new or different accident.
        Administrative Changes
        Combining line items for Unit 1 and Unit 2 into a dual Unit 
    entry for administrative purposes does not introduce any new 
    credible failure modes which may create the possibility of a new or 
    different accident.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety.
        Overtemperature N-16 and Pressurizer Pressure - Low, Unit 2
        Incorporation of the added temperature uncertainties of the 
    Rosemount transmitters assures that the safety analysis limits 
    assumed in the accident analyses for Overtemperature N-16 and 
    Pressurizer Pressure-Low reactor trip functions for Unit 2 are met. 
    There is no change in the acceptance criteria or the results of 
    these analyses due to this change. Thus there is no effect on the 
    margin of safety.
        Equation 2.2-1
        Deletion of Equation 2.2-1, related actions and associated 
    definitions and values, merely eliminates one option to assure that 
    the safety analysis assumptions are met. This option is not 
    presently in use and the accident analyses assumptions have been and 
    will continue to be met using the other option (to re-calibrate 
    channels prior to restoring operability). Thus the margin of safety 
    is unaffected.
        Administrative Changes
        Combining the Unit 1 and Unit 2 line items of Table 2.2-1 for 
    RTS [Reactor Trip Systems] functions and of Table 3.3-3 for ESFAS 
    [Engineered Safety Features Actuation System] functions into dual 
    unit entries does not change the Trip Setpoint or the Allowable 
    Value for the functions. The margin of safety is unaffected.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 701 South Cooper, P.O. 
    Box 19497, Arlington, Texas 76019
        Attorney for licensee: George L. Edgar, Esq., Newman and 
    Holtzinger, 1615 L Street, N.W., Suite 1000, Washington, D.C. 20036
        NRC Project Director: William D. Beckner
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: April 19, 1994
        Description of amendment request: The proposed amendment revises 
    Technical Specification 6.2.2.g to reflect a title designation change 
    within the Wolf Creek Nuclear Operating Corporation (WCNOC) 
    organization. The title of Supervisor Operations is being changed to 
    Assistant Manager Operations. The title change does not represent any 
    change in reporting relationships, job responsibilities, or overall 
    organizational commitments.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    This change involves an administrative change to the WCNOC 
    organization and to the position title and as such has no effect on 
    plant equipment or the technical qualification of plant personnel.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        The proposed change does not create the possibility of a new or 
    different kind of accident from any previously evaluated. This 
    change is administrative in nature and does not involve any change 
    to installed plant systems or the overall operating philosophy of 
    Wolf Creek Generating Station.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety.
        The proposed change does not involve a significant reduction in 
    a margin of safety. This change does not involve any changes in 
    overall organizational commitments. A position title change alone 
    does not reduce any margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: Theodore R. Quay
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: April 19, 1994
        Description of amendment request: The proposed amendment revises 
    Technical Specification Table 3.6-1, ``Containment Isolation Valves,'' 
    by deleting reference to two (2) valves. The Technical Specification 
    change reflects a planned modification which removes the essential 
    service water (ESW) containment air cooler return line isolation valve 
    bypass valves and associated piping.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        After the design modification is completed the ESW Containment 
    Penetrations will be provided with stainless steel isolation valves, 
    which will be provided with automatic SIS [safety injection signal] 
    actuation signals to open automatically to provide required cooling 
    water flow to the Containment Air Coolers following a LOCA [loss-of-
    coolant accident] or MSLB [main steamline break]. Replacement of the 
    current carbon steel isolation valves with stainless steel valves 
    and removing the unnecessary bypass lines and bypass isolation 
    valves will reduce the amount of seat leakage currently experienced 
    with these valves.
        The probability of occurrence of a previously evaluated accident 
    is not increased because this modification does not introduce any 
    new potential accident initiating conditions. The consequences of an 
    accident previously evaluated is not increased because the ability 
    of containment to restrict the release of any fission product 
    radioactivity to the environment will not be degraded by this 
    modification.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        The proposed modification will reduce the number of containment 
    isolation valves and replace several carbon steel isolation valves 
    with stainless steel valves, which will be less susceptible to 
    erosion and corrosion. Thus, potential system leakage will be 
    reduced by this modification, while valve reliability will be 
    enhanced. The new valves are designed to the original ESW System 
    requirements, and removal of the bypass lines and bypass isolation 
    valves will not result in a malfunction of any other plant 
    equipment. Therefore, this proposed modification will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety.
        The removal of the bypass lines and bypass isolation valves will 
    not adversely affect containment isolation capability for credible 
    accident scenarios. Due to a previous design change, the bypass 
    lines are no longer required to ensure adequate cooling flow to the 
    Containment Air Coolers. In addition, the operability and 
    reliability of the remaining isolation valves will be enhanced by 
    replacing the current carbon steel valves with stainless steel 
    valves.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: Theodore R. Quay
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of amendment request: May 11, 1994
        Brief description of amendment request: The amendment would allow 
    reduced power operation as a function of reactor coolant system (RCS) 
    total flow rate for flow rate reductions of up to 5 percent below the 
    currently specified flow rate. Operation will be allowed at total flow 
    rates slightly lower than (293,540 gpm X (1.0 plus C1)) if rated 
    thermal power (RTP) is reduced by 1.5 percent for each one percent that 
    RCS total flow is less than this rate. This change would provide for 
    needed operational margin and flexibility without the unnecessary 
    penalty of a large power reduction.
        Date of publication of individual notice in Federal Register: May 
    25, 1994 (59 FR 27079)
        Expiration date of individual notice: June 24, 1994
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Northeast Nuclear Energy Company, Docket No. 50-245, Millstone 
    NuclearPower Station, Unit 1, New London County, Connecticut
    
        Date of amendment request: May 27, 1994
        Description of amendment request: The amendment would add a new 
    section to Technical Specification Section 6.17 and would require that 
    procedures be in place to provide for monitoring and sampling of 
    emergency service water (ESW) discharge flow during accident conditions 
    when a positive differential pressure cannot be maintained between ESW 
    and low pressure coolant injection (LPCI) in the LPCI heat exchangers.
        Date of publication of individual notice in Federal Register: June 
    7, 1994 (59 FR 29448)
        Expiration date of individual notice: July 7, 1994
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, Connecticut 06360.
    
    Notice Of Issuance Of Amendments To Facility Operating LIcenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    rooms for the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units 1, 2, and 3, Maricopa County, Arizona
    
        Date of application for amendments: February 18, 1994, as 
    supplemented by letter dated May 16, 1994
        Brief description of amendments: These amendments modify Technical 
    Specification (TS) Figure 3.2-1, ``REACTOR COOLANT COLD LEG vs CORE 
    POWER LEVEL,'' of TS 3/4.2.6, ``REACTOR COOLANT COLD LEG TEMPERATURE,'' 
    for Units 1 and 3 to include the cold leg temperature between 552 deg.F 
    and 562 deg.F at core power levels between 90 percent and 100 percent 
    within the AREA OF ACCEPTABLE OPERATION. Also, the proposed amendments 
    modify TS 3/4.1.1.4, ``MINIMUM TEMPERATURE FOR CRITICALITY,'' and BASES 
    3/4.1.1.4, ``MINIMUM TEMPERATURE FOR CRITICALITY,'' to allow the 
    minimum temperature for criticality to be established at 545 deg.F, 
    rather than the current value of 552 deg.F, to establish the 
    surveillance temperature at 552 deg.F, rather than the current 
    557 deg.F, and to clarify the BASES for this TS.
        Date of issuance: June 7, 1994
        Effective date: NPF-41 and NPF-51, prior to startup from the next 
    refueling outage; NPF-74, no later than 45 days from the date of 
    issuance.
        Amendment Nos.: 77, 63, and 49
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: March 30, 1994 (59 FR 
    14886) The additional information contained in the May 16, 1994, letter 
    was clarifying in nature, was within the scope of the initial notice, 
    and did not affect the NRC staff's proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated June 7, 1994.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick 
    County,North Carolina
    
        Date of application for amendments: April 14, 1994, as supplemented 
    on May 16, 1994.
        Brief description of amendments: The amendments change the 
    Technical Specifications (TS) to relocate the Instrument Response Time 
    Tables to the Updated Final Safety Analysis Report in accordance with 
    NRC Generic Letter 93-08.
        Date of issuance: May 31, 1994
        Effective date: May 31, 1994
        Amendment Nos.: 171 and 202
        Facility Operating License Nos. DPR-71 and DPR-62. Amendments 
    revise the Technical Specifications.
        Date of initial notice in Federal Register: April 26, 1994 (59 FR 
    21785) The May 16, 1994, letter provided clarifying information that 
    did not change the initial no significant hazards consideration 
    determination.The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 31, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of application for amendments: August 20, 1993, as 
    supplemented by letters dated December 27, 1993, March 22, 1994, and 
    May 31, 1994.
        Brief description of amendments: The amendments delete Technical 
    Specification Section 3/4.6.1.5, ``Primary Containment Structural 
    Integrity'' which includes Surveillance Requirements for the Primary 
    Containment Tendons and adds a Technical Specification requirement to 
    establish, implement, and maintain a comprehensive containment tendon 
    program. The containment tendon program is based on Regulatory Guide 
    1.35, Rev. 3, and is titled ``Inservice Inspection Program for Post 
    Tensioning Tendons.'' The new program will allow the Unit 1 and 2 
    containments to be tested as twin containments.
        Date of issuance: June 3, 1994
        Effective date: June 3, 1994
        Amendment Nos.: 100 and 84
        Facility Operating License Nos. NPF-11 and NPF-18. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 10, 1993 (58 
    FR 59746) The supplemental information submitted December 27, 1993, 
    March 22, 1994, and May 31, 1994, contained clarifying information 
    related to the original request, and did not change the no significant 
    hazards finding. The Commission's related evaluation of the amendments 
    is contained in a Safety Evaluation dated June 3, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Public Library of Illinois 
    Valley Community College, Rural Route No. 1, Oglesby, Illinois 61348.
    
    Commonwealth Edison Company, Docket Nos. 50-254 and 50-265, Quad 
    Cities Nuclear Power Station, Units 1 and 2, Rock Island County, 
    Illinois
    
        Date of application for amendments: December 20, 1993
        Brief description of amendments: The amendments increase the 
    minimum critical power ratio (MCPR) from 1.06 to 1.07 for Quad Cities, 
    Units 1 and 2, as a result of the planned implementation of GE 8x8NB-3 
    fuel for Cycle 14 of each unit.
        Date of issuance: June 10, 1994
        Effective date: June 10, 1994
        Amendment Nos.: 146 and 142
        Facility Operating License Nos. DPR-29 and DPR-30. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 17, 1994 (59 
    FR 10003) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 10, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Dixon Public Library, 221 
    Hennepin Avenue, Dixon, Illinois 61021.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of application for amendment: February 25, 1994
        Brief description of amendment: The amendment adds a new Technical 
    Specification 3/4.7.12, ``Ultimate Heat Sink'' and its associated Bases 
    Section 3/4.7.12.
        Date of Issuance: May 31, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 172
        Facility Operating License No. DPR-61. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 13, 1994 (59 FR 
    17596) The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated May 31, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, Connecticut 06457.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    PointNuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: December 6, 1993
        Brief description of amendment: The amendment revises the Technical 
    Specifications (TSs) to provide several temporary one-time changes that 
    are necessary to support the fuel out, chemical decontamination program 
    that is currently scheduled for the upcoming 1995 refueling outage. 
    Specifically, the amendment revises the definition of the cold shutdown 
    condition in TS 1.2.1 by changing the upper limit of Tavg for the 
    cold shutdown condition from 200 deg.F to 250 deg.F. The amendment also 
    revises the definition of the hot shutdown condition in TS 1.2.2 by 
    changing the lower limit of Tavg for the hot shutdown condition 
    from greater than 200 deg.F to greater than 250 deg.F.
        Date of issuance: June 9, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 170
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 16, 1994 (59 
    FR 7687) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 9, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: January 27, 1994
        Brief description of amendments: The amendments would eliminate the 
    humidity control functions of the containment purge (VP) system 
    humidistats by deleting the surveillance requirement (SR) for periodic 
    verification of automatic isolation of the VP system on a high relative 
    humidity (RH) test signal and heater failure from the existing SR for 
    Catawba Units 1 and 2.
        Date of issuance: May 25, 1994
        Effective date: May 25, 1994
        Amendment Nos.: 118 and 112
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 2, 1994 (59 FR 
    10005) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 25, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: April 29, 1993, as supplemented 
    May 16, 1994
        Brief description of amendments: The amendments delete License 
    Condition 2.C.(20) from Facility Operating License NPF-35 for Unit 1, 
    and License Condition 2.C.(11) from Facility Operating License NPF-52 
    for Unit 2. These conditions address engine teardown and inspection 
    required following the crankshaft failure of an Enterprise emergency 
    diesel generator at the Shoreham Nuclear Plant.
        Date of issuance: June 2, 1994
        Effective date: June 2, 1994
        Amendment Nos.: 119/113
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 26, 1993 (58 FR 
    30192) The May 16, 1994, letter provided additional information that 
    did not change the scope of the April 29, 1993, application and 
    proposed initial no significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated June 2, 1994.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: January 13, 1993, as 
    supplemented January 28, February 17, and April 26, 1993.
        Brief description of amendments: The amendments revise Technical 
    Specification Table 2.2.1, Sections 3/4.1.2.5, 3/4.1.2.6, 3/4.5.1.1, 3/
    4.5.5, and their associated Bases, and Technical Specification 6.9.1.9, 
    to relocate the values of certain cycle-dependent limits from the 
    Technical Specifications to the Core Operating Limits Report.
        Date of issuance: May 31, 1994
        Effective date: May 31, 1994
        Amendment Nos.: 143 and 125
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 4, 1993 (58 FR 
    41503) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 31, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223.
    
    Duke Power Company, Docket Nos. 50-269, 50-270, and 50-287, Oconee 
    Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
    
        Date of application of amendments: March 23, 1994, as supplemented 
    April 14, May 11, and May 17 (two letters) 1994.
        Brief description of amendments: The amendments relating to the 
    March 23, 1994, application revise Technical Specification (TS) 6.9.2, 
    ``Core Operating Limits Report,'' (COLR) to include a reference to a 
    Duke Power Company Topical Report describing an analytical method for 
    determining the core operating limits. Specifically, the amendments 
    add: ``(4) DPC-NE-1004A, Nuclear Design Methodology Using CASMO-3/
    SIMULATE-3P,'' to TS 6.9.2.
        The May 11, 1994, letter added a statement to TS 6.9.2 that the 
    approved methods used to determine the core operating limits given in 
    TS 6.9.1 are specified in the COLR. The May 11 and 17, 1994, letters 
    provided information regarding Duke Power's transition from the EPRI-
    NODE-P based methodology to the simulate methodology. Revision 1 to the 
    COLR for Oconee 1 Cycle 16 was submitted by letter dated May 17, 1994.
        The April 14, 1994, letter revised the TS Table of Contents to 
    delete reference to Table 4.4-1. This table was removed from the TS by 
    an amendment issued on September 16, 1993.
        Date of Issuance: June 8, 1994
        Effective date: June 8, 1994
        Amendment Nos.:  206, 206, and 203
        Facility Operating License Nos. DPR-38, DPR-47, and DPR-55: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: April 28, 1994 (59 FR 
    22007) The April 14, May 11, and May 17 (two letters), 1994, letters 
    provided additional information that did not change the scope of the 
    March 23, 1994, application and the initial proposed no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    June 8, 1994. No significant hazards consideration comments received: 
    No
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    ElectricStation, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: December 23, 1993
        Brief description of amendment: The amendment revised the Technical 
    Specifications in accordance with Generic Letter 93-05, ``Line Item 
    Technical Specification Improvements To Reduce Surveillance 
    Requirements For Testing During Power Operation'' for radiation 
    monitors, pressurizer heaters, reactor coolant isolation valves, and 
    auxiliary feedwater pumps.
        Date of issuance: June 6, 1994
        Effective date: June 6, 1994
        Amendment No.:  96
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 16, 1994 (59 
    FR 7689) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 6, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122.
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-424 and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, 
    Burke County, Georgia
    
        Date of application for amendments: December 30, 1993
        Brief description of amendments: The proposed change would allow a 
    one time extension of the allowable outage time for each residual heat 
    removal (RHR) pump from 3 to 7 days to allow modifications to the RHR 
    system while the plant is in Mode 1.
        Date of issuance: May 31, 1994
        Effective date: May 31, 1994
        Amendment Nos.: 72 and 51
        Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 2, 1994 (59 FR 
    10007) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 31, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Burke County Library, 412 
    Fourth Street, Waynesboro, Georgia 30830
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-424 and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, 
    Burke County, Georgia
    
        Date of application for amendments: November 19, 1993
        Brief description of amendments: The amendments modify Technical 
    Specification Table 3.3-2, Engineered Safety Features Actuation System 
    Instrumentation, modifying the Mode for which Item 6.e, ``Trip of All 
    Main Feedwater Pumps, Start Motor-Driven Pumps,'' is required to be 
    operable.
        Date of issuance: June 1, 1994
        Effective date: June 1, 1994
        Amendment Nos.: 73 and 52
        Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 22, 1993 (58 
    FR 67847) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June, 1, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Burke County Library, 412 
    Fourth Street, Waynesboro, Georgia 30830
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-424 and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, 
    Burke County, Georgia
    
        Date of application for amendments: March 1, 1994
        Brief description of amendments: The amendments modify Technical 
    Specification (TS) 3.2.4, ``Quadrant Power Tilt Ratio,'' by adding an 
    exception to the requirements of TS 3.0.4.
        Date of issuance: June 1, 1994
        Effective date: June 1, 1994
        Amendment Nos.: 74 and 53
        Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 13, 1994 (59 FR 
    17599) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 1, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Burke County Library, 412 
    Fourth Street, Waynesboro, Georgia 30830
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile 
    Island Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of application for amendment: February 7, 1994
        Brief description of amendment: The amendment revises the plant 
    Technical Specifications (TS) to require the Three Mile Island, Unit 1 
    (TMI-1) annual radioactive effluent release report for the previous 
    calendar year be submitted by May 1 of each year. The current TS 
    requires the TMI-1 report be submitted within 60 days after January 1 
    of each year. Changing the TMI-1 due date to May 1 enables the licensee 
    to combine the reports for TMI-1 and TMI-2 into a single report with a 
    common due date.
        Date of Issuance: June 10, 1994
        Effective date: As of its date of issuance to be implemented within 
    30 days.
        Amendment No.: 185
        Facility Operating License No. DPR-50. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 13, 1994 (59 FR 
    17600) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 10, 1994. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, Pennsylvania 17105.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: May 27, 1993, as supplemented by letter 
    dated April 18, 1994.
        Brief description of amendments: The amendments upgrade the fuel 
    used in the South Texas Project reactors to Westinghouse VANTAGE 5 
    Hybrid (V5H) design and implement several analytical and operational 
    upgrades into the South Texas Project Updated Final Safety Analysis 
    Report. The amendments modify related setpoints, limiting conditions 
    for operation, surveillance requirements, design features information, 
    and associated bases in the following specifications: TS Table 2.2-1, 
    ``Reactor Trip System Instrumentation Trip Setpoints,'' TS Figure 3.1-
    1, ``Required Shutdown Margin for Modes 1 and 2,'' TS Figure 3.1-2, 
    ``Required Shutdown Margin for Mode 5,'' TS Figure 3.1-2a, ``MTC versus 
    Power Level,'' TS 3/4.2.5, ``Power Distribution Limits - DNB 
    Parameter,'' TS Table 3.3-4, ``Engineered Safety Features Actuation 
    System Instrumentation Trip Setpoints,'' TS 3/4.6.1.1, ``Primary 
    Containment - Containment Integrity,'' TS 3/4.6.1.2, ``Containment 
    Systems - Containment Leakage,'' TS 3/4.6.1.3, ``Containment Systems - 
    Containment Air Locks,'' TS 3/4.6.1.5, ``Containment Systems - Air 
    Temperature,'' TS 3/4.7.1.2, ``Plant Systems - Auxiliary Feedwater 
    System,'' TS 5.2.1, ``Containment - Configuration,'' TS 5.3.1, 
    ``Reactor Core - Fuel Assemblies,'' TS 5.6.1, ``Fuel Storage - 
    Criticality,'' and adds TS Figure 5.6-7, ``Minimum IFBA Content for In-
    Containment Rack Fuel Storage.''
        Date of issuance: May 27, 1994
        Effective date: May 27, 1994, to be implemented prior to completion 
    of Unit 1 REO5
        Amendment Nos.:  Unit 1 - Amendment No. 61; Unit 2 - Amendment No. 
    50
        Facility Operating License Nos. NPF-76 and NPF-80: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 7, 1993 (58 FR 
    36436) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 27, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488
    
    Indiana Michigan Power Company, Docket No. 50-316, Donald C. Cook, 
    Nuclear Plant, Unit No. 2, Berrien County, Michigan
    
        Date of application for amendment: March 9, 1994, as supplemented 
    April 13, 1994.
        Brief description of amendment: The amendment revises the Technical 
    Specifications to allow a one-time extension for Type B and C leak rate 
    tests. The Commission had previously granted a one-time schedular 
    exemption from the requirements in 10 CFR Part 50, Appendix J, 
    paragraphs III.D.2.(a) and III.D.3. The exemption extends the maximum 
    allowable time between tests by 150 days.
        Date of issuance: June 1, 1994
        Effective date: June 1, 1994
        Amendment No.: 162
        Facility Operating License No. DPR-74. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 28, 1994 (59 FR 
    22009). The April 13, 1994, supplemental letter provided clarifying 
    information that was within the scope of the April 28, 1994, notice. 
    The Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated June 1, 1994.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
    
    Tennessee Valley Authority, Docket Nos. 50-259 and 50-296, Browns 
    Ferry Nuclear Plant, Units 1 and 3, Limestone County, Alabama
    
        Date of application for amendment: January 14, 1992 (TS 300)
        Brief description of amendments: The amendments add requirements to 
    the Browns Ferry Units 1 and 3 Technical Specifications to ensure 
    thermal-hydraulic stability, consistent with guidance provided by NRC 
    Bulletin 88-07 ``Power Oscillations in Boiling Water Reactors,'' and 
    Supplement 1 to that Bulletin.
        Date of issuance: May 31, 1994
        Effective date: May 31, 1994
        Amendment Nos.: 206 and 179
        Facility Operating License Nos. DPR-33 and DPR-68:
        Date of initial notice in Federal Register: April 15, 1992 (57 FR 
    13138) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 31, 1994.No significant 
    hazards consideration comments received: None
        Local Public Document Room location: Athens Public Library, South 
    Street, Athens, Alabama 35611
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: February 8, 1994 (TS 93-14)
        Brief description of amendments: The amendments increase the 
    pressure setpoint for the motor driven auxiliary feedwater pumps 
    switchover from the condensate storage tank to the essential raw 
    cooling water supply.
        Date of issuance: May 27,1994
        Effective date: May 27, 1994
        Amendment Nos.: 183 and 175
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: March 16, 1994 (59 FR 
    12368) The Commission's related evaluation of the amendments are 
    contained in a Safety Evaluation dated May 27, 1994.No significant 
    hazards consideration comments received: None
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, 
    Vermont Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: July 14, 1993
        Brief description of amendment: This amendment revises Sections 3.6 
    and 4.6 of the Technical Specifications to incorporate reactor coolant 
    system leakage detection requirements to address Generic Letter 88-01 
    ``NRC Position on Intergranular Stress Corrosion Cracking (IGSCC) in 
    BWR Austenitic Stainless Steel Piping.''
        Date of issuance: June 1, 1994
        Effective date: June 1, 1994
        Amendment No.: 139
        Facility Operating License No. DPR-28. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 16, 1994 (59 FR 
    12370) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 1, 1994 No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, Vermont 05301.
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC 20555, 
    and at the local public document room for the particular facility 
    involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By July 22, 1994, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC 20555 and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Commonwealth Edison Company, Docket No. STN 50-456, Braidwood 
    Station, Unit No. 1, Will County, Illinois
    
        Date of application for amendments: April 25, 1994, as supplemented 
    April 28, 1994, April 30, 1994, May 2, 1994, May 4, 1994, and May 6, 
    1994.
        Brief description of amendments: The amendment revises Braidwood, 
    Unit 1, technical specifications (TSs) in Appendix A to the operating 
    license by adding additional surveillance and operating requirements to 
    Section 4.4.5.2, ``Steam Generator Tube Sample Selection and 
    Inspection; Section 4.4.5.4, ``Acceptance 
    Criteria; Section 4.4.5.5, ``Reports; and Section 
    3.4.6.2. This amendment is applicable only for 100 calendar days from 
    the date of issuance, not counting any time when the Thot 
    temperature is below 500 deg.F. These changes revise the existing steam 
    generator tube repair criteria to allow usage of the voltage-based 
    criteria identified by the staff in draft NUREG-1477 as the interim 
    plugging criteria (IPC). Additionally, a footnote is added to TS 3.4.8 
    to limit the dose equivalent iodine-131 concentration to 0.35 
    microcuries per gram of coolant for the limited time period cited 
    above. The Unit 1 Bases are revised to be consistent with the changes 
    cited above.
        Date of issuance: May 7, 1994
        Effective date: May 7, 1994
        Amendment No.: 50
        Facility Operating License No. NPF-72. The amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: Yes. The NRC published a public 
    notice of the proposed amendment, issued a proposed finding of no 
    significant hazards consideration and requested that any comments on 
    the proposed no significant hazards consideration be provided to the 
    staff by the close of business on May 5, 1994. The notice was published 
    in the Herald News and the Morris Daily Herald on May 3, 1994. The 
    Commission's related evaluation of the amendment, finding of emergency 
    circumstances, and final determination of no significant hazards 
    consideration are contained in a Safety Evaluation dated May 7, 1994.
        Attorney for the licensee: Michael I. Miller, Esquire, Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690
        Local Public Document Room location: Wilmington Township Public 
    Library, 201 S. Kankakee Street, Wilmington, Illinois 60481.
        NRC Project Director: James E. Dyer
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Unit No. 3 Nuclear Generating Plant, Citrus County, Florida
    
        Date of application for amendment: May 19, 1994
        Brief description of amendment: The amendment revises the 
    surveillance requirements in TS 3.3.9.3 and 3.3.10.3, to change the 
    neutron power limits i.e., 105 neutron counts per second (cps) and 
    1E-6 amperes (amps) indications on the source and intermediate range 
    instruments, respectively, for verifying overlap between them.
        Date of issuance: May 27, 1994
        Effective date: May 27, 1994
        Amendment No.: 150
        Facility Operating License No. DPR-72. Amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: No. The Commission's related 
    evaluation of the amendment and the final determination of no 
    significant hazards consideration comments are contained in a Safety 
    Evaluation dated May 27, 1994.
        Attorney for the Licensee: Harold F. Reis, Esquire, Newman and 
    Holtzer, P.C., 1615 L Street, NW., Washington DC 20036
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 32629
        NRC Project Director: Herbert N. Berkow
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    MillstoneNuclear Power Station, Unit No. 2, New London County, 
    Connecticut
    
        Date of application for amendment: May 27, 1994, as supplemented 
    June 1, 1994.
        Brief description of amendment: The amendment revises the Technical 
    Specifications (TS) by adding a footnote to Tables 3.3-3, 3.3-4 and 
    3.3-5 of the Millstone Unit No. 2 TS denoting that the operability of 
    the automatic initiation logic for the auxiliary feedwater system will 
    rely on operator action for the remainder of Cycle 12.
        Date of issuance: June 7, 1994
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment No.: 176
        Facility Operating License No. NPF-49. Amendment revised the 
    Technical Specifications.Public comments requested as to proposed no 
    significant hazards consideration: No. The Commission's related 
    evaluation of the amendment, finding of emergency circumstances, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated June 7, 1994.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, Connecticut 06360.
        Attorney for licensee: Gerald Garfield, Esquire, Day, Berry & 
    Howard, Counselors at Law, City Place, Hartford, Connecticut 06103-
    3499.
        NRC Project Director: John F. Stolz
        Dated at Rockville, Maryland, this 15th day of June 1994.
        For the Nuclear Regulatory Commission
    Steven A. Varga,
    Director, Division of Reactor Projects - I/IIOffice of Nuclear Reactor 
    Regulation
    [Doc. 94-15025 Filed 6-21-94 8:45 am]
    BILLING CODE 7590-01F
    
    
    

Document Information

Published:
06/22/1994
Department:
Nuclear Regulatory Commission
Entry Type:
Uncategorized Document
Document Number:
X94-10622
Dates:
NPF-41 and NPF-51, prior to startup from the next refueling outage; NPF-74, no later than 45 days from the date of issuance.
Pages:
0-0 (1 pages)
Docket Numbers:
Federal Register: June 22, 1994