98-16746. Southern Nuclear Operating Company, Inc., et al.; Vogtle Electric Generating Plant, Units 1 and 2; Environmental Assessment and Finding of No Significant Impact  

  • [Federal Register Volume 63, Number 121 (Wednesday, June 24, 1998)]
    [Notices]
    [Pages 34491-34493]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 98-16746]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    [Docket Nos. 50-424 and 50-425]
    
    
    Southern Nuclear Operating Company, Inc., et al.; Vogtle Electric 
    Generating Plant, Units 1 and 2; Environmental Assessment and Finding 
    of No Significant Impact
    
        The U.S. Nuclear Regulatory Commission (the Commission) is 
    considering issuance of amendments to Facility Operating License Nos. 
    NPF-68 and NPF-81 issued to Southern Nuclear Operating Company, Inc., 
    et al. (the licensee), for operation of the Vogtle Electric Generating 
    Plant (VEGP), Units 1 and 2, respectively, located in Burke County, 
    Georgia.
    
    Environmental Assessment
    
    Identification of the Proposed Action
    
        The proposed action would change the common VEGP Technical 
    Specifications to allow an increase in the Unit 1 spent fuel storage 
    capacity from 288 to 1476 fuel assemblies. The increase in spent fuel 
    storage capacity is achieved by replacing the existing spent fuel 
    storage racks, a process referred to herein as ``reracking.'' The 
    proposed action is in accordance with the licensee's application for 
    license amendments dated September 4, 1997, as supplemented by letters 
    dated November 20, 1997, May 19 and June 12, 1998.
    
    The Need for the Proposed Action
    
        The VEGP spent fuel pools (SFPs) are operated as a single facility 
    and accept spent fuel from both Units 1 and 2. The VEGP Unit 2 spent 
    fuel pool has a storage capacity of 2098 fuel assemblies. Under current 
    conditions, the SFPs will lose the capacity for a full-core off-load 
    (193 fuel assemblies) in the year 2005. There are no independent 
    commercial spent fuel storage facilities operating in the U.S., nor are 
    there any domestic reprocessing facilities; therefore, the projected 
    loss of storage capacity in the VEGP SFPs would affect the licensee's 
    ability to operate VEGP. The proposed amendments are needed to ensure 
    the capability of full-core off-load until the year 2015.
    
    Environmental Impacts of the Proposed Action
    
    Radiological Impacts
        VEGP has waste treatment systems designed to collect and process 
    waste that may contain radioactive material. The radioactive waste 
    treatment systems were evaluated in the ``Final Environmental Statement 
    Related to the Operation of Vogtle Electric Generating Plant,'' NUREG-
    1087, March 1985. The SFP cooling and purification system is designed 
    to remove the decay heat generated by stored spent fuel assemblies and 
    to clarify and purify the water to permit unencumbered access to the 
    plant fuel storage area and maintain optical clarity of the SFP water.
    Liquid Radioactive Waste
        It is not expected that there will be a significant increase in the 
    liquid release of radionuclides from the plant as a result of the SFP 
    reracking modifications. The SFP cooling and purification system 
    operates as a closed system. The SFP demineralizer resin removes 
    soluble radioactive materials from the SFP water. A small increase in 
    activity on the filters and demineralizers may occur during the 
    installation of the new racks because of the more frequent fuel 
    shuffling and underwater pressure washing of the old racks during 
    removal. However, the amount of radioactivity released to the 
    environment as a result of the proposed reracking is expected to be 
    negligible.
    Solid Radioactive Waste
        The existing spent fuel racks in the VEGP Unit 1 SFP will be 
    removed from the site by a salvage company. After usable material has 
    been salvaged, the remainder will be volume reduced and disposed of at 
    the Barnwell, South Carolina, facility. In a worst-case scenario, with 
    no salvageable material and no volume reduction, the resulting material 
    would represent 44 percent of the expected solid waste volume 
    associated with VEGP Units 1 and 2 for 1998; however, this volume is 
    not significant when viewed over the 40-year operational lifetime of 
    the VEGP facility.
        In addition to the spent fuel assemblies themselves, the only other 
    solid radioactive waste generated by the SFP is the SFP polisher resin, 
    which is used for water clarity. As indicated in the licensee's 
    submittal of September 4, 1997, these resins are replaced approximately 
    once per refueling cycle. No additional spent resins are expected to be 
    generated by the pool cleanup system as a result of the expanded spent 
    fuel storage capability; therefore, no significant increase in the 
    volume of solid radioactive waste associated with these resins is 
    expected with the proposed amendments.
    Radioactive Material Released to the Atmosphere
        The only radioactive gas of significance that could be attributable 
    to storing additional spent fuel assemblies for a longer period of 
    time, made possible as a result of the proposed reracking, would be the 
    noble gas radionuclide krypton-85 (Kr-85). Experience has demonstrated 
    that after spent fuel has decayed 4 to 6 months, there is no longer a 
    significant release of fission products, including Kr-85, from stored 
    spent fuel containing cladding defects. The licensee has stated that in 
    the past 2 years, the Kr-85 concentrations measured from the fuel 
    storage area ventilation release point have been negligible and the 
    licensee expects that enlarging the storage capacity of the SFP will 
    have no effect on the average annual quantities of Kr-85 released to 
    the atmosphere.
        Iodine-131 released from spent fuel assemblies to the SFP water 
    will not be significantly increased as a result of the expansion of the 
    fuel storage capacity since the iodine-131 inventory in the fuel will 
    decay to negligible levels between refuelings.
        Most of the tritium in the SFP water results from activation of 
    boron and lithium in the primary coolant during power operation. A 
    relatively small amount of tritium is produced during reactor operation 
    by the fission process within the reactor fuel. The subsequent 
    diffusion of the tritium through the fuel and cladding represents a 
    small contribution to the total amount of tritium in the SFP water. 
    Tritium releases from the fuel assemblies occur mainly during reactor 
    operation and, to a limited extent, shortly after shutdown. Thus, 
    expanding the SFP capacity will not increase the tritium concentration 
    in the SFP.
        Most airborne releases of tritium and iodine from nuclear power 
    plants result during refuelings from evaporation of reactor coolant, 
    which contains tritium and iodine in higher concentrations than in the 
    SFP. The storage of additional spent fuel assemblies in the SFP is not 
    expected to significantly increase the SFP bulk water temperature, and, 
    therefore, evaporation rates from the SFP are not expected to 
    significantly increase. Consequently, it is not expected that there 
    will be any significant change in the annual release of tritium or 
    iodine as a result of the proposed modifications from that previously 
    evaluated in NUREG-1087.
    
    [[Page 34492]]
    
    Occupational Doses
        The licensee estimates that the increased number of fuel assemblies 
    stored in the Unit 1 SFP may result in a small increase in doses in the 
    areas adjacent to the sides of the SFP, although it will not be enough 
    to change any existing radiation zone designations. To minimize any 
    potential dose rate increases from the increased storage of spent fuel, 
    the licensee plans to control the placement of freshly discharged fuel 
    so that it is not placed in SFP rack positions adjacent to the sides of 
    the SFP. Dose rates on the fuel pool level are primarily due to 
    radionuclides in the pool water. During normal operations, dose rates 
    in this area are generally 2.5 mrem/hr or less. The staff finds these 
    dose rates to be acceptable and in accordance with SFP dose rates at 
    other plants.
        The licensee will constantly monitor the doses to the workers 
    during the reracking operation using electronic personnel dosimetry. 
    Each diver will be monitored using multiple teledosimetry devices. 
    These teledosimetry devices will transmit diver dose and dose rate data 
    that will be continuously monitored adjacent to the SFP. Cameras will 
    be used to monitor the movements of the divers. The licensee will use 
    continuous air samplers when there is a potential for airborne activity 
    in the SFP area during the modifications. In addition, the plant 
    effluent radiation monitoring system will monitor any gaseous releases.
        The total occupational dose to plant workers as a result of the 
    reracking operation is estimated to be approximately 4.3 person-rem. 
    This dose estimate is based on the licensee's detailed review of the 
    anticipated work activities, their duration, and expected dose rates 
    associated with each of the activities related to the SFP reracking. 
    The upcoming reracking operation at Vogtle Unit 1 will follow detailed 
    procedures prepared with full consideration of as low as is reasonably 
    achievable (ALARA) principles. On the basis of its review of the 
    proposed action, the staff concludes that the Vogtle Unit 1 SFP rerack 
    modification can be performed in a manner that will ensure that doses 
    to workers will be maintained ALARA. The estimated dose of 4.3 person-
    rem to perform the proposed SFP rerack is a small fraction of the 
    annual collective dose accrued at Vogtle and, therefore, the staff 
    finds this dose to be acceptable.
    Uranium Fuel Cycle and Transportation
        The environmental impacts on the uranium fuel cycle and 
    transportation resulting from the use of higher enrichment fuel and 
    extended irradiation were published in NUREG/CR-5009, ``Assessment of 
    the Use of Extended Burnup Fuels in Light Water Power Reactors,'' 
    February 1988, and discussed in the staff's Environmental Assessment 
    and Finding of No Significant Impact published in the Federal Register 
    on February 29, 1988 (53 FR 6040). The staff concluded that no 
    significant adverse effects will be generated by increasing the burnup 
    levels as long as the maximum rod-average burnup level of any fuel rod 
    is no greater than 60 Gwd/MtU. The staff also stated that the 
    environmental impacts summarized in Tables S-3 and S-4 for a burnup 
    level of 33 Gwd/MtU are conservative and bound the corresponding 
    impacts for burnup levels up to 60 Gwd/MtU and uranium-235 enrichments 
    up to 5 weight percent. Since the proposed amendment does not involve 
    an increase in the enrichment or burnup of fuel utilized at VEGP, the 
    staff concludes that there is no significant radiological environmental 
    impact associated with the proposed expansion of the spent fuel storage 
    capacity at VEGP Unit 1 or with the uranium fuel cycle or 
    transportation.
    Accident Considerations
        In the Vogtle Final Safety Analysis Report, the licensee evaluated 
    the possible consequences of the following three hypothetical accidents 
    involving fuel in the SFP: a fuel-handling accident in the fuel-
    handling building; a fuel-handling accident in the containment with the 
    airlock closed; and a fuel-handling accident in the containment with 
    the airlock open. The licensee reevaluated these hypothetical accidents 
    to determine the thyroid and whole-body doses at the exclusion area 
    boundary, in the low-population zone, and in the control room.
        On the basis of the review of the licensee's reevaluation, the NRC 
    staff concludes that the proposed reracking of the Vogtle Unit 1 SFP 
    will not result in an increase in the doses from any of these 
    hypothetical accidents.
    Nonradiological Impact
        The proposed amendments do not modify land use at the site; no new 
    facilities or laydown areas are needed to support the rerack or 
    operation after rerack; therefore, the proposed amendments do not 
    affect land use or land with historical or archeological sites.
        The increased spent fuel inventory results in a minor bulk pool 
    temperature increase. This minor increase in temperature results in a 
    minor increase in the pool water evaporation rate. The licensee's 
    submittal of September 4, 1997, indicates that the effects of the 
    increased temperature and evaporation rates are within the capacity of 
    the existing fuel-handling building heating, ventilation, and air 
    conditioning system. The total heat load from spent fuel cooling 
    dissipated to the environment represents 2.5 percent of the total 
    rejected plant heat.
        The proposed action does not affect nonradiological plant 
    effluents, and no changes to the National Pollution Discharge 
    Elimination System permit are needed. The proposed action does not 
    result in any significant changes to land use or water use, or result 
    in any significant changes to the quantity or quality of effluents; no 
    effects on endangered or threatened species or on their habitat are 
    expected.
        The proposed action will not change the method of generating 
    electricity or the method of handling any influents from the 
    environment or nonradiological effluents to the environment. Therefore, 
    no changes or different types of nonradiological environmental impacts 
    are expected as a result of the amendments.
    
    Summary
    
        The Commission has completed its evaluation of the proposed action. 
    The proposed action will not increase the probability or consequences 
    of accidents, no changes are being made in the types of any effluents 
    that may be released off site, and there is no significant increase in 
    the allowable individual or cumulative occupational or offsite 
    radiation exposure. Accordingly, the Commission concludes that there 
    are no significant radiological environmental impacts associated with 
    the proposed action.
        With regard to potential nonradiological impacts, the proposed 
    action does involve features located entirely within the restricted 
    area as defined in 10 CFR Part 20. It does not affect nonradiological 
    plant effluents and has no other environmental impact. Accordingly, the 
    Commission concludes that there are no significant nonradiological 
    environmental impacts associated with the proposed action.
    
    Alternatives to the Proposed Action
    
        Since the Commission has concluded there are no significant 
    environmental impacts associated with the proposed action, any 
    alternatives with equal or greater environmental impact need not be 
    evaluated. As an alternative to the proposed action, the staff 
    considered denial of the proposed action. Denial of
    
    [[Page 34493]]
    
    the application would result in no change in current environmental 
    impacts. The environmental impacts of the proposed action and the 
    alternative action are similar.
    
    Alternative Use of Resources
    
        The proposed action does not involve the use of any resources not 
    previously considered in NUREG-1087.
    
    Agencies and Persons Consulted
    
        In accordance with its stated policy, on May 26, 1998, the staff 
    consulted with the Georgia State official, Mr. J. Setzer of the Georgia 
    Department of Natural Resources, regarding the environmental impact of 
    the proposed action. The State official had no comments.
    
    Finding of No Significant Impact
    
        Based upon the environmental assessment, the Commission concludes 
    that the proposed action will not have a significant effect on the 
    quality of the human environment. Accordingly, the Commission has 
    determined not to prepare an environmental impact statement for the 
    proposed action.
        For further details with respect to the proposed action, see the 
    licensee's letter dated September 4, 1997, as supplemented by letters 
    dated November 20, 1997, May 19 and June 12, 1998, which are available 
    for public inspection at the Commission's Public Document Room, The 
    Gelman Building, 2120 L Street, NW., Washington, DC, and at the local 
    public document room located at the Burke County Library, 412 Fourth 
    Street, Waynesboro, Georgia.
    
        Dated at Rockville, Maryland, this 19th day of June 1998.
    
        For the Nuclear Regulatory Commission.
    Jacob I. Zimmerman,
    Acting Director, Project Directorate II-2, Division of Reactor 
    Projects--I/II, Office of Nuclear Reactor Regulation.
    [FR Doc. 98-16746 Filed 6-23-98; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
06/24/1998
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
98-16746
Pages:
34491-34493 (3 pages)
Docket Numbers:
Docket Nos. 50-424 and 50-425
PDF File:
98-16746.pdf