X96-10605. Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 61, Number 109 (Wednesday, June 5, 1996)]
    [Notices]
    [Pages 28604-28626]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X96-10605]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    Biweekly Notice
    
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from May 11, 1996, through May 23, 1996. The last 
    biweekly notice was published on May 22, 1996 (61 FR 25696).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards onsideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By July 5, 1996, the licensee may file a request for a hearing with 
    respect to issuance of the amendment to the subject facility operating 
    license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also
    
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    provide references to those specific sources and documents of which the 
    petitioner is aware and on which the petitioner intends to rely to 
    establish those facts or expert opinion. Petitioner must provide 
    sufficient information to show that a genuine dispute exists with the 
    applicant on a material issue of law or fact. Contentions shall be 
    limited to matters within the scope of the amendment under 
    consideration. The contention must be one which, if proven, would 
    entitle the petitioner to relief. A petitioner who fails to file such a 
    supplement which satisfies these requirements with respect to at least 
    one contention will not be permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, 
    and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: May 1, 1996
        Description of amendment request: The proposed amendment will 
    relocate the administrative controls related to the quality assurance 
    review and audit requirements of Section 6 from the Pilgrim Station 
    Technical Specifications to the Boston Edison Quality Assurance Manual. 
    This change is in accordance with the guidance contained in NRC 
    Administrative Letter 95-06, ``Relocation of Technical Specification 
    Administrative Controls Related to Quality Assurance.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The change will relocate the administrative controls related to 
    the quality assurance review and audit requirements from the 
    technical specifications to the quality assurance plan. These 
    changes are administrative in nature and do not impact initiators of 
    analyzed events, accident mitigation capabilities, or transient 
    events. The quality assurance program is a logical candidate for 
    such relocation due to the controls imposed by such regulations as 
    Appendix B to 10 CFR [Part] 50, the existence of NRC approved 
    quality assurance plans and commitments to industry quality 
    assurance standards, and the established quality assurance program 
    change control process in 10 CFR 50.54(a). Therefore, the changes do 
    not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The change will relocate the administrative controls related to 
    the quality assurance review and audit requirements from the 
    technical specifications to the quality assurance plan. The quality 
    assurance program is a logical candidate for such relocation due to 
    the controls imposed by such regulations as Appendix B to 10 CFR 
    [Part] 50, the existence of NRC approved quality assurance plans and 
    commitments to industry quality assurance standards, and the 
    established quality assurance program change control process in 10 
    CFR 50.54(a). The proposed changes do not involve a physical 
    alteration of the plant or changes in methods governing plant 
    operation. The changes will not impose or eliminate any new or 
    different requirements. Therefore the changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The change will relocate the administrative controls related to 
    the quality assurance review and audit requirements from the 
    technical specifications to the quality assurance plan. These 
    changes are administrative in nature. The quality assurance program 
    is a logical candidate for such relocation due to the controls 
    imposed by such regulations as Appendix B to 10 CFR [Part] 50, the 
    existence of NRC approved quality assurance plans and commitments to 
    industry quality assurance standards, and the established quality 
    assurance program change control process in 10 CFR 50.54(a). The 
    proposed change will not reduce a margin of safety because it has no 
    impact on any safety analysis assumptions. Therefore, the operation 
    of PNPS [Pilgrim Nuclear Power Station] in accordance with the 
    proposed license amendment will not involve a significant reduction 
    in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Jocelyn A. Mitchell, Acting
    
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    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: May 1, 1996
        Description of amendment request: The proposed amendment will 
    reflect the implementation of 10 CFR Part 50, Appendix J, Option B at 
    the Pilgrim Nuclear Power Station.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The operation of Pilgrim Station in accordance with the 
    proposed amendment will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    The proposed changes do not involve any physical or operational 
    changes to structures, systems or components. The proposed changes 
    provide a mechanism within the TS [Technical Specifications] for 
    implementing a performance-based leakage rate test program which was 
    promulgated by the revision to 10CFR50 to incorporate Option B into 
    Appendix J. The TS Limiting Conditions for Operation (LCO) remain 
    unaffected by these changes. Thus, the safety design basis for the 
    accident mitigation functions of the primary containment is 
    maintained. Therefore, these changes will not increase the 
    probability or consequences of an accident previously evaluated.
        2. The operation of Pilgrim Station in accordance with the 
    proposed amendment will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        Revising surveillance requirement acceptance criteria and 
    frequencies does not physically modify the plant and does not modify 
    the operation of any existing equipment. Further, the TS LCOs remain 
    unaffected by these changes.
        3. The operation of Pilgrim Station in accordance with the 
    proposed amendment will not involve a significant reduction in a 
    margin of safety.
        The proposed changes do not involve a significant reduction in 
    the margin of safety, nor do they affect a safety limit, an LCO, or 
    the manner in which plant equipment is operated. The NRC letter 
    dated November 2, 1995, recognizes that changes similar to the 
    proposed changes are required to implement Option B of 10CFR50, 
    Appendix J. In NUREG-1493, ``Performance-Based Containment Leak-Test 
    Program,'' which forms the basis for the Appendix J revision, the 
    NRC concludes that adoption of performance-based test intervals for 
    Appendix J testing will not significantly reduce the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location:  Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Jocelyn A. Mitchell, Acting
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: May 1, 1996
        Description of amendment request: The proposed amendment would 
    modify the definition of ``Core Alteration,'' and the Limiting 
    Condition for Operation, Surveillance conditions and Bases section 
    associated with Technical Specification (TS) 3.7.C, ``Secondary 
    Containment.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Operation of PNPS [Pilgrim Nuclear Power Station] in accordance 
    with the proposed license amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated because of the following:
        Proposed Change 1: Definition of ``Alteration of the 
    Reactor Core
        The definition, ``Alteration of the Reactor Core'', is being 
    revised so that the term will apply only to those activities that 
    create the potential for a reactivity excursion and, therefore, 
    warrant special precautions or controls in the TS. The proposed 
    definition includes normal control rod movement in the definition, 
    but excludes control rod drive movement (such as rod removal from 
    the core) when all four fuel bundles surrounding a control rod are 
    removed. The proposed change does not increase the probability or 
    consequences of an accident because the proposed definition, by 
    identifying activities with the potential for causing a reactivity 
    excursion, ensures that the additional precautions and controls in 
    the TS are implemented at all appropriate times. In addition, the 
    movement of components excluded by this definition is not assumed in 
    the initiation of any analyzed event. Therefore, the proposed change 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Proposed Change 2: Secondary Containment
        The current specifications are revised to specify more clearly 
    when secondary containment is required, what actions to take if 
    secondary containment is inoperable, and time frames for completing 
    the actions. These revisions enhance the existing specification and 
    serve to make it more definitive by encompassing the conditions 
    currently specified by TS and supplementing them to specify other 
    conditions when secondary containment is required.
        Surveillances 4.7.C.1.a and b were only necessary during initial 
    and Cycle 1 operations. Removing obsolete information from the 
    existing specifications, re-numbering and re-arranging the wording 
    is an administrative change.
        These changes are administrative in nature and do not impact 
    initiators of analyzed events, accident mitigation capabilities, or 
    transient events. Therefore, the changes do not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The operation of PNPS in accordance with the proposed license 
    amendment will not create the possibility of a new or different kind 
    of accident from any accident previously evaluated because of the 
    following:
        Proposed Change 1: Definition of ``Alteration of the 
    Reactor Core
        The definition change specifies more accurately which component 
    movements constitute a ``Core Alteration''. This change does not 
    involve a physical alteration of the plant (no new or different type 
    of equipment will be installed) or changes in methods governing 
    normal plant operation. The proposed changes will allow movement of 
    some components (camera, lights, etc.) during times when ``Core 
    Alterations'' have been halted since these components will not 
    affect core reactivity. Removal of a control rod involves unlatching 
    and withdrawal/insertion from over-vessel handling equipment. These 
    activities necessitate, by design, the removal of the adjacent four 
    fuel assemblies. With this configuration (no fuel in the cell; 
    handling the associated control rod), the proposed change will allow 
    movement of a ``reactivity control component'' while not imposing 
    requirements unique to ``Core Alterations'' (note: other 
    requirements, such as those for handling loads over irradiated fuel, 
    will remain applicable). The reactivity effects of this control rod 
    movement are more than compensated for by the initial removal of the 
    fuel assemblies. Therefore, this change will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        Proposed Change 2: Secondary Containment
        The proposed change does not eliminate or relax any existing TS 
    condition. Rather, it better defines when secondary containment is 
    required, provides action statements for inoperability and removes 
    obsolete
    
    [[Page 28607]]
    
    requirements (from first operating cycle). This change does not 
    involve a physical change to structures, systems or components, and 
    the safety design bases for the accident mitigating function of the 
    secondary containment is maintained. Therefore, these changes will 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The operation of PNPS in accordance with the proposed license 
    amendment will not involve a significant reduction in a margin of 
    safety because of the following:
        Proposed Change 1: Definition of ``Alteration of the 
    Reactor Core
        The proposed definition more accurately identifies those 
    activities with the potential for causing a reactivity excursion. 
    The more accurate identification of ``Core Alterations'' will ensure 
    that when there is a potential for reactivity excursions, 
    appropriate precautions are applied. The components now excluded 
    from the proposed definition are those that do not have the 
    capability for adversely impacting core reactivity. The proposed 
    change has no impact on safety analysis assumptions. Therefore, the 
    change will not involve a significant reduction in a margin of 
    safety.
        Proposed Change 2: Secondary Containment
        The proposed additions of applicability conditions provide a 
    more precise understanding of when secondary containment integrity 
    is required and what actions to take if it becomes inoperable. The 
    change does not eliminate any existing conditions. The deletion of 
    surveillances applicable only for the first operating cycle and re-
    numbering and re-arranging the remaining surveillance wording is an 
    administrative change and has no impact on the operation of the 
    plant or mitigation of accidents. Therefore, the operation of the 
    facility in accordance with this proposed amendment would not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Jocelyn A. Mitchell, Acting
    
    Carolina Power & Light Company, et al., Docket No. 50-325, 
    Brunswick Steam Electric Plant, Unit 1, Brunswick County, North 
    Carolina
    
        Date of amendment request: April 8, 1996
        Description of amendment request: The licensee has proposed to 
    revise the Technical Specifications (TS) to include the following 
    changes: 1. The Minimum Critical Power Ratio (MCPR) Safety Limit 
    specified in TS 2.1.2 from 1.07 to 1.09 for Unit 1 Cycle 11 operation; 
    TS 5.3.1 to reflect the new fuel type (GE13) that will be inserted 
    during Unit 1 Refueling Outage 10; 2. The acceptable range of sodium 
    pentaborate concentration for the standby liquid control system shown 
    in TS Figure 3.1.5-1 to reflect changes to poison material 
    concentration needed to achieve reactor shutdown based on the new GE13 
    fuel type.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Proposed Change 1
        The proposed amendment will allow the loading and use of GE13 
    fuel assemblies in the Brunswick Unit 1 reactor core. The use of 
    GE13 fuel assemblies requires that the safety limit minimum critical 
    power ratio value also be revised. The safety limit minimum critical 
    power ratio is established to maintain fuel cladding integrity 
    during operational transients. The GE13 fuel assembly design has 
    been analyzed using methods that have been previously approved by 
    the Nuclear Regulatory Commission and documented in General Electric 
    Nuclear Energy's reload licensing methodology Topical Report (NEDE-
    24011-P-A-11, ``General Electric Standard Application for Reactor 
    Fuel (GESTAR II)'' dated November 1995).
        The proposed revision of the safety limit minimum critical power 
    ratio does not alter any plant safety-related equipment, safety 
    function, or plant operations that could change the probability of 
    an accident. The change does not affect the design, materials, or 
    construction standards applicable to the fuel bundles in a manner 
    that could change the probability of an accident.
        A methodology that has been previously reviewed and accepted by 
    the Nuclear Regulatory Commission was used to derive both the 
    existing and updated safety limit minimum critical power ratio 
    value. The same methodology and criteria have been applied to derive 
    the existing safety limit minimum critical power ratio of 1.07 as 
    that used to derive the updated safety limit minimum critical power 
    ratio value of 1.09. The updated safety limit minimum critical power 
    ratio assures that fuel cladding protection equivalent to that 
    provided with the existing safety limit minimum critical power ratio 
    value is maintained. This ensures that the consequences of 
    previously evaluated accidents are not significantly increased.
        Proposed Change 2
        The standby liquid control system provides a means of reactivity 
    control that is independent of the normal reactivity control system. 
    The standby liquid control system must be capable of assuring that 
    the reactor core can be placed in a subcritical condition at any 
    time during reactor core life. Technical Specification Figure 3.1.5-
    1 specifies the acceptable range of concentrations and volumes for 
    sodium pentaborate solution used as a neutron absorber (i.e., for 
    reactivity control). The portion of the sodium pentaborate 
    concentration range shown in Technical Specification Figure 3.1.5-1 
    applicable to the lower range of tank volumes is being revised to 
    increase the required concentration of sodium pentaborate solution. 
    This change is needed to account for the additional shutdown 
    reactivity needed based on the planned use of GE13 fuel assemblies 
    as reload fuel for the Unit 1 reactor core. Since the standby liquid 
    control system is independent from the normal means of controlling 
    reactor core reactivity and not used to control core reactivity 
    during normal plant operations, the proposed revision to the sodium 
    pentaborate concentration curve for the standby liquid control 
    system does not alter any plant safety-related equipment, safety 
    function, or plant operations that could change the probability of 
    an accident.
        The current volume-concentration range of sodium pentaborate 
    used in the standby liquid control system will achieve a sufficient 
    concentration of boron in the reactor vessel to ensure reactor 
    shutdown. Based on the increased reactivity of the new GE13 reload 
    fuel assemblies, the required sodium pentaborate volume-
    concentration range is being revised to ensure sufficient neutron 
    absorbing solution is available to achieve reactor shutdown; 
    therefore, the consequences of an accident previously evaluated are 
    not significantly increased.
        2. The proposed amendment would not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        Proposed Change 1
        The GE13 fuel assembly has been designed and complies with the 
    acceptance criteria contained in General Electric Nuclear Energy's 
    standard application for reactor fuel (GESTAR-II), which provides 
    the latest acceptance criteria for new General Electric fuel 
    designs. The GE13 fuel assembly complies with GESTAR-II acceptance 
    criteria that have been previously reviewed and accepted by the 
    Nuclear Regulatory Commission. The similarity of the GE13 fuel 
    design to the previously accepted GE11 fuel design, in conjunction 
    with the increased critical power capability of the GE13 fuel 
    design, ensure that no new mode or condition of plant operation is 
    being authorized by the loading and use of the
    
    [[Page 28608]]
    
    GE13 fuel type. The proposed revision of the safety limit minimum 
    critical power ratio from 1.07 to 1.09 does not modify any plant 
    controls or equipment that will change the plant's responses to any 
    accident or transient as given in any current analysis. Therefore, 
    the proposed change to allow the loading and use of the GE13 fuel 
    type and the revision of the safety limit minimum critical power 
    ratio value from 1.07 to 1.09 will not create the possibility for a 
    new or different kind of accident from any accident previously 
    evaluated.
        Proposed Change 2
        As discussed above, the standby liquid control system provides a 
    means of reactivity control that is independent of the normal 
    reactivity control system and is capable of assuring that the 
    reactor core can be placed in a subcritical condition at any time 
    during reactor core life. The proposed revision to the sodium 
    pentaborate concentration range does not modify the standby liquid 
    control system or its controls, does not modify other plant systems 
    and equipment, and does not permit a new or different mode of plant 
    operation. As such, the proposed revision to the minimum pentaborate 
    concentration value does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed license amendment does not involve a significant 
    reduction in a margin of safety.
        Proposed Change 1
        As previously discussed, the GE13 fuel assembly design has been 
    analyzed using methods that have been previously approved by the 
    Nuclear Regulatory Commission and documented in General Electric 
    Nuclear Energy's reload licensing methodology Topical Report (NEDE-
    24011-P-A-11, ``General Electric Standard Application for Reactor 
    Fuel (GESTAR II)'' dated November 1995). The safety limit minimum 
    critical power ratio value is selected to maintain the fuel cladding 
    integrity safety limit (i.e., that 99.9 percent of all fuel rods in 
    the core are expected to avoid boiling transition during operational 
    transients). Appropriate operating limit minimum critical power 
    ratio values are established, based on the safety limit minimum 
    critical power ratio value, to ensure that the fuel cladding 
    integrity safety limit is maintained. The operating limit minimum 
    critical power ratio values are incorporated in the Core Operating 
    limits Report as required by Technical Specification 6.9.3.1. The 
    new GE13 safety limit minimum critical power ratio value of 1.09 is 
    based on the same fuel cladding integrity safety limit criteria [as] 
    that for the GE11 safety limit minimum critical power ratio value of 
    1.07 (i.e., that 99.9 percent of all fuel rods in the core are 
    expected to avoid boiling transition during operational transients); 
    therefore, the proposed change does not result in a significant 
    reduction in the margin of safety.
        Proposed Change 2
        As previously stated, the purpose of the standby liquid control 
    is to inject a neutron absorbing solution into the reactor in the 
    event that a sufficient number of control rods cannot be inserted to 
    maintain subcriticality. Sufficient solution is to be injected such 
    that the reactor will be brought from maximum rated power conditions 
    to subcritical over the entire reactor temperature range from 
    maximum operating to cold shutdown conditions. General Electric 
    methodology establishes a fuel type dependent standby liquid control 
    system shutdown margin to account for calculational uncertainties. 
    General Electric calculations show that an in-vessel concentration 
    of 660 ppm will provide a standby liquid control system minimum 
    shutdown margin in excess of the 3.2%[delta]k value required for the 
    GE13 fuel. To achieve an in-vessel concentration of 660 ppm, the 
    acceptable range of standby liquid control system tank 
    concentrations is being revised for the lower range of tank volumes. 
    Thus, the proposed revision of the standby liquid control system 
    sodium pentaborate volume-concentration range ensures that there 
    will not be a significant reduction in the amount of available 
    shutdown margin and, therefore, not a significant reduction in the 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602
        NRC Project Director: Eugene V. Imbro
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of amendment request: February 27, 1996
        Description of amendment request: The proposed license amendment 
    would modify the Action Statement of Technical Specification (TS) 
    3.7.1.1.1. Currently, the TS action statement requires that with the 
    self actuation function on one or more main steam line code safety 
    valves associated with an operating loop inoperable, the licensee must 
    restore the inoperable valve to operable status within 4 hours. 
    Otherwise, the plant must be in hot standby within the next 6 hours and 
    in hot shutdown within the following 30 hours. The proposed change will 
    allow continued power operation at reduced power levels with main steam 
    safety valves inoperable. The proposed change is consistent with the 
    philosophy of the Westinghouse Standard Technical Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. [The proposed change does not involve] a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change to the Action Statement of LCO [Limiting 
    Condition for Operation] 3.7.1.1.1 will allow indefinite operation 
    at less than or equal to 75% power in the event that the self 
    actuation function of no more than one safety valve per steam 
    generator is inoperable, and allow indefinite operation at less than 
    or equal to 50% power in the event that the self actuation function 
    of no more than two safety valves per steam generator is inoperable. 
    The requirement to reduce power will ensure that there is no 
    increase in the consequences of a loss of load accident. The 
    proposed change is consistent with the methodology in the 
    Westinghouse Standard Technical Specifications. The methodology is 
    conservative, since the PORVs [power operated relief valves] cannot 
    affect the time of reactor trip on high pressurizer pressure. Thus, 
    it is concluded that the change does not increase the consequences 
    of any previously evaluated accident.
        The change only specifies a power reduction in the event that 
    the self actuation function of steam generator safety valves is 
    inoperable. It does not affect the probability of any accident. The 
    change by itself does not affect the likelihood of an inoperable 
    safety valve.
        2. [The proposed change does not create] the possibility of a 
    new or different kind of accident from any previously evaluated.
        The change only specifies a power reduction in the event that 
    the self actuation function of steam generator safety valves is 
    inoperable. This does not create the potential for a new or 
    different kind of accident. The lower power level assures that peak 
    steam generator pressure and RCS [reactor coolant system] pressure 
    will remain below 110% of design. This provides assurance that no 
    equipment failure will occur due to overpressurization. Thus, the 
    change does not create the possibility for a new or different kind 
    of accident.
        3. [The proposed change does not involve] a significant 
    reduction in a margin of safety.
        The allowable power levels have been selected, consistent with 
    the Westinghouse Standard Technical Specifications, to assure that 
    steam generator and RCS pressure will remain below 110% of design. 
    Thus, there is no reduction in a margin of safety for overpressure 
    protection.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the
    
    [[Page 28609]]
    
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of amendment request: March 7, 1996
        Description of amendment request: The licensee will be replacing a 
    locally operated (manual) containment sump suction isolation valve, RH-
    V-808A, with a remote manually operated (motor operated) valve, RH-MOV-
    808A during the upcoming Cycle 19 refueling outage. As a result, 
    changes are being requested to the Haddam Neck Plant Technical 
    Specifications to reflect this design change.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. [The proposed change does not involve] a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed technical specification change to Section 3/4.4.6.2 
    and its bases are the replacement of the designation RH-V-808A with 
    RH-MOV-808A. There are no changes to the requirements of this 
    specification and this change is therefore an administrative change. 
    The changes to Section 3/4.5.1 will make the requirements for RH-
    MOV-808A identical to those of RH-MOV-22. RH-V-808A is being 
    converted to a motor operated valve (MOV). This MOV will make the 
    ability to establish a suction path from the containment to the 
    Residual Heat Removal (RHR) System single failure proof from the 
    control room. Both RH-MOV-22 and RH-MOV-808A will be opened to 
    establish containment sump recirculation post-loss of coolant 
    accident (LOCA). This will provide added assurance that core cooling 
    will be maintained in the switch from injection to containment sump 
    recirculation following a LOCA. The requirement for RH-MOV-808A to 
    be closed and its hand wheel locked can not cause an accident. The 
    credit for operation of RH-MOV-808A to ensure that the establishment 
    of containment sump recirculation is single failure proof is 
    equivalent to the current crediting of RH-V-808A with the only 
    difference being that operation of the valve can now be performed 
    from the control room. Also, since both RH-MOV-22 and RH-MOV-808A 
    will be procedurally opened during establishment of containment sump 
    recirculation, the elimination of the requirement to lock open the 
    breaker for RH-MOV-22 will not affect the consequences of a LOCA. 
    The proposed changes that reflect the conversion of RH-V-808A to a 
    MOV and the proposed changes in how the valve is used do not 
    increase the consequences of a LOCA.
        2. [The proposed change does not create] the possibility of a 
    new or different kind of accident from any previously evaluated.
        The proposed changes will require RH-MOV-808A to be closed with 
    the hand wheel locked. This provides assurance that the valve is in 
    the required position. Also, RH-MOV-808A will be capable of remote 
    manual operation during the monthly surveillance which provides 
    assurance that the valve can be repositioned if necessary. The 
    proposed opening of RH-MOV-808A at the same time as RH-MOV-22 is 
    opened, provides greater assurance that a suction path is available 
    to the RHR pumps as well as lowering the total effective piping 
    resistance from the containment sump to the pump suction. Therefore, 
    the proposed changes do not introduce the possibility of a new or 
    different kind of accident.
        3. [The proposed change does not involve] a significant 
    reduction in a margin of safety.
        The proposed changes make RH-MOV-808A identical to RH-MOV-22 
    with the exception that RH-MOV-808A will not get a closure signal on 
    Safety Injection Actuation. Both RH-MOV-22 and RH-MOV-808A are 
    containment isolation valves in a closed system. For closed systems, 
    the containment isolation requirement is that the valves be either: 
    a) automatic, b) locked closed, or c) capable of remote manual 
    operation. RH-MOV-808A and RH-MOV-22 are both capable of remote 
    manual operation and therefore do not need automatic closure when 
    they are opened as part of the technical specification required 
    surveillance. Therefore, the proposed changes can not cause a 
    significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of amendment request: March 28, 1996
        Description of amendment request: The proposed license amendment 
    will add an additional footnote to Limiting Condition for Operation 
    (LCO) 3.4.2.1 and revise an existing footnote for LCO 3.4.2.2. 
    Currently, the footnote for LCO 3.4.2.2 requires the pressurizer code 
    safety valve as-found lift setting to be within +3 percent and -1 
    percent of the setpoint. The proposed change will relax the negative 
    as-found lift tolerance to -3 percent. The as-left lift tolerance will 
    remain as plus or minus 1 percent. The same footnote will be added to 
    LCO 3.4.2.1.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. [The proposed change does not involve] a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change will relax the pressurizer safety valve 
    negative as-found lift tolerance to -3 percent. The as-left lift 
    tolerance will remain as plus or minus 1 percent. This proposed 
    technical specification change will allow for the full use of the 
    plus or minus 3 percent as-found acceptance criterion for valve 
    testing consistent with 1989 ASME Section XI, Subsection IWV. The 
    relaxing of the as-found lift tolerance can not cause an accident. 
    The relaxing of the tolerance will allow the safety valve setpoint 
    to be closer to the Power Operated Relief Valve (PORV) setpoint and 
    could result in a slightly lower pressure for overheating events. 
    The analysis that takes credit for the increase in pressure to the 
    PORV setpoint is the Loss of Load analysis. The minimum departure 
    from nucleate boiling ratio (DNBR) was reanalyzed without taking any 
    credit for the transient increase in pressure. The minimum DNBR 
    still remains above the acceptance criterion as well as above the 
    limiting minimum DNBR predicted for all Updated Final Safety 
    Analysis Report Chapter 15 accidents. Also, the relaxed tolerance in 
    conjunction with a lower safety valve blowdown, yet still 
    conservative, results in a slightly higher average pressure for a 
    valve lift/reset cycle. This means that pressurizer overfill will 
    not be predicted for the limiting transient, loss of feedwater. 
    Thus, the proposed relaxation of as-found lift tolerance does not 
    increase the probability or consequences of the design basis 
    accidents previously evaluated.
        2. [The proposed change does not create] the possibility of a 
    new or different kind of accident from any previously analyzed.
        The proposed relaxation of the lift tolerance still requires the 
    safety valve lift setpoint to be above both the PORV setpoint and 
    the pressurizer high pressure reactor trip setpoint. In addition, 
    the as-left setpoint is not being changed. The relaxed tolerance in 
    combination with a conservative safety valve blowdown still will 
    preclude the prediction of water relief from the pressurizer. This 
    means that the proposed change does not introduce the possibility of 
    a new or different kind of accident.
    
    [[Page 28610]]
    
        3. [The proposed change does not involve] a significant 
    reduction in a margin of safety.
        The proposed relaxation of the as-found lift tolerance for valve 
    testing is consistent with 1989 ASME Section XI, Subsection IWV. The 
    as-left lift tolerance will remain plus or minus 1 percent. In 
    addition, the design basis analyses still meet their acceptance 
    criteria with the -3 percent lift tolerance. Therefore, the proposed 
    change can not cause a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of amendment request: April 16, 1996
        Description of amendment request: The licensee is proposing to 
    revise the Technical Specifications to permit the Haddam Neck Plant to 
    remain in Mode 1, 2, 3, or 4 with the average water temperature of the 
    ultimate heat sink (UHS) greater than 90 deg. additional action has 
    been added which would require the plant to be placed in at least Hot 
    Standby within 6 hours and in Cold Shutdown within the following 30 
    hours upon identifying that the average water temperature of the UHS is 
    greater than 95 deg.F. In addition, the licensee is proposing to 
    include a new surveillance requirement for monitoring the average 
    circulating water inlet temperature to be within its limits when the 
    average water temperature of the UHS exceeds 89 deg.F.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. [The proposed change does not] involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed addition to the Action Statement of LCO 3.7.12 of 
    an 8 hour period to monitor the average water temperature of the UHS 
    does not involve an increase in the probability of an accident 
    previously evaluated. The probability of an accident previously 
    evaluated is not increased by a short-term increase in the average 
    water temperature of the UHS. An evaluation of the service water 
    loads associated with the loss-of-offsite power and a coincident 
    worst case single failure of a diesel generator to start (resulting 
    in the loss of two of the four service water pumps) determined that 
    there is adequate margin to accomplish plant cooldown at a service 
    water inlet temperature of 95 deg.F. The recirculation phase of a 
    LOCA [loss-of-coolant accident] was evaluated to verify that 
    adequate flow would be available to the RHR [residual heat removal] 
    heat exchangers. The most limiting assumptions for the recirculation 
    phase are offsite power is available and one RHR heat exchanger 
    service water isolation valve fails to open. The injection phase of 
    a LOCA was evaluated to verify that adequate flow would be available 
    to the CAR [containment air recirculation] fan cooling coils. The 
    most limiting assumption for the injection phase is a loss-of-
    offsite power. The results of these evaluations determined that 
    there is adequate service water flow to accomplish plant cooldown 
    with average water temperature of the UHS up to 95 deg.F. CYAPCO 
    [Connecticut Yankee Atomic Power Company] also proposes to include 
    an additional surveillance requirement to monitor the average water 
    temperature of the UHS at least once per hour if the average water 
    temperature of the UHS exceeds 89 deg.F. This additional 
    surveillance requirement ensures increased operator awareness as the 
    average water temperature of the UHS approaches the 90 deg.F LCO 
    limit. Based on the above, there is no significant increase in the 
    consequences of any accident previously evaluated.
        2. [The proposed change does not] create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed technical specification changes do not create the 
    possibility of a new or different kind of accident from those 
    previously evaluated. The addition of an 8 hour time period to 
    monitor the average water temperature of the UHS increases from 6 to 
    14 hours the amount of time that is allowed before the plant must 
    proceed to Hot Standby should the average water temperature of the 
    UHS increase above 90 deg.F. This extension of the time allowed for 
    the plant to be in Hot Standby does not change the plant 
    configuration. CYAPCO also proposes to include an additional 
    surveillance requirement to monitor the average water temperature of 
    the UHS at least once per hour if the average water temperature of 
    the UHS exceeds 89 deg.F. This additional surveillance requirement 
    ensures increased operator awareness as the average water 
    temperature of the UHS approaches the 90 deg.F LCO limit.
        As such, the changes do not create the possibility of a new or 
    different kind of accident from those previously evaluated.
        3. [The proposed change does not] involve a significant 
    reduction in a margin of safety.
        The proposed technical specification changes do not involve a 
    significant reduction in any margin of safety. The addition of an 8 
    hour time period to monitor the average water temperature of the UHS 
    increases from 6 to 14 hours the time required before the plant must 
    proceed to Hot Standby should the average water temperature of the 
    UHS temperature [exceed] 90 deg.F. An evaluation has been performed 
    to demonstrate that the risk significance associated with the 
    increased action time is very low. In addition, safe shutdown 
    capability has been demonstrated for service water inlet 
    temperatures as high as 95 deg.F. The addition of a surveillance 
    requirement to monitor the average water temperature of the UHS at 
    least once per hour if the average water temperature of the UHS 
    exceeds 89 deg.F is an additional requirement, limitation, or 
    restriction not currently within the technical specifications. 
    Therefore, these changes do not involve a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270
        NRC Project Director: Phillip F. McKee
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of amendment request: April 22, 1996
        Description of amendment request: The proposed amendment will allow 
    the use of the performance-based containment leakage testing 
    requirements described in 10 CFR Part 50, Appendix J, Option B.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        The changes involved in this license amendment request revise 
    the testing criteria for the containment penetrations. The revised 
    criteria will be based on the guidance in Regulatory Guide 1.163, 
    ``Performance-Based Containment Leak-Test Program.'' This guidance 
    allows for the use of relaxed testing frequencies for containment 
    penetrations that have performed satisfactorily on a historical 
    basis. The Containment Leakage Rate Testing Program considers the 
    type of service, the design of the penetration, and the safety 
    impact of the penetration in determining the
    
    [[Page 28611]]
    
    testing interval of each penetration. The NRC Staff has reviewed the 
    potential impact of performance-based testing frequencies for 
    containment penetrations during the development of the Option B 
    regulation. The NRC Staff review is documented in NUREG-1493, 
    ``Performance-Based Containment Leakage-Test Program.'' The review 
    concluded that reducing the frequency of Type A tests (Integrated 
    Leakage Rate Tests) from three per 10 years to one per 10 years 
    leads to an imperceptible increase in risk. For Type B and C testing 
    (Local Leakage Rate Tests), the change in testing frequency should 
    not have significant impact since this leakage contributes less than 
    0.1 percent of the overall risk based on the existing regulations. 
    The use of Option B will allow the extension of testing intervals 
    with a minimal impact on the radiological release rates since most 
    penetration leakage is continually well below the specified limits. 
    In the accident risk evaluation, the NRC Staff noted that the 
    accident risk is relatively insensitive to the containment leakage 
    rate because the accident risk is dominated by accident sequences 
    that result in failure of or bypass of the containment. The use of a 
    performance-based testing program will continue to provide assurance 
    that the accident analysis assumptions remain bounding. Therefore, 
    the proposed change does not involve a significant increase in the 
    probability or consequences of an accident previously analyzed.
        Removal of the surveillance accuracy requirement in Section 
    4.6.1.2.c will not affect the probability of an accident previously 
    analyzed since a similar requirement is contained in ANSI/ANS-56.8-
    1994, ``Containment System Leakage Testing Requirements.'' ANSI/ANS-
    56.8-1994 will be used to develop the technical methods and 
    techniques for the Containment Leakage Rate Test Program as stated 
    in Regulatory Guide 1.163. The technical methods and techniques in 
    ANSI/ANS-56.8-1994 have been determined to be acceptable to the NRC 
    Staff.
        Changes to the Administrative Section describe the containment 
    testing program only and cannot increase the probability or 
    consequences of an accident previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed license amendment does not change the operation or 
    equipment of the plant. The change in the test frequency is 
    dependent on the establishment of a Containment Leakage Test 
    Program. This test program will ensure the performance history of 
    each penetration is satisfactory prior to the changing of any test 
    frequency. Since the performance history of the penetration will be 
    known, there is no possibility of the implementation of the program 
    creating a new or different kind of accident than previously 
    analyzed. Since there is no change to the equipment or the operation 
    of the plant, there is no possibility of creating a new or different 
    kind of accident than previously analyzed. Therefore, the proposed 
    change does not create the possibility of a new or different kind of 
    accident from any previously analyzed.
        Removal of the surveillance accuracy requirement in Section 
    4.6.1.2.c will not create the possibility of a new or different kind 
    of accident from those previously analyzed since a similar 
    requirement is contained in ANSI/ANS-56.8-1994, ``Containment System 
    Leakage Testing Requirements.'' ANSI/ANS-56.8-1994 will be used to 
    develop the technical methods and techniques for the Containment 
    Leakage Rate Test Program as stated in Regulatory Guide 1.163. The 
    technical methods and techniques in ANSI/ANS-56.8-1994 have been 
    determined to be acceptable to the NRC staff.
        Changes to the Administrative Section describe the containment 
    testing program only and cannot create a different accident from any 
    previously analyzed.
        3. Involve a significant reduction in a margin of safety.
        During the development of 10 CFR Part 50, Appendix J, Option B, 
    the NRC staff determined the reduction in safety associated with the 
    implementation of the performance-based testing program. The results 
    of this review are documented in NUREG-1493. The review concluded 
    that reducing the frequency of Type A tests (Integrated Leakage Rate 
    Tests) from three per 10 years to one per 10 years leads to an 
    imperceptible increase in risk. For Type B and C testing (Local 
    Leakage Rate Tests), the increase in testing frequency should not 
    have significant impact since this leakage contributes less than 0.1 
    percent of the overall risk based on the existing regulations. The 
    use of Option B will allow the extension of testing intervals with a 
    minimal impact on the radiological release rates since most 
    penetration leakage is continually well below the specified limits. 
    In the accident risk evaluation, the NRC Staff noted that the 
    accident risk is relatively insensitive to the containment leakage 
    rate because the accident risk is dominated by accident sequences 
    that result in failure of or bypass of the containment. The use of a 
    performance based testing program will continue to provide assurance 
    that the accident analysis assumptions remain bounding. Therefore, 
    this change does not involve a significant reduction in the margin 
    of safety.
        Removal of the surveillance accuracy requirement in Section 
    4.6.1.2.c will not involve a significant reduction in the margin of 
    safety since a similar requirement is contained in ANSI/ANS-56.8-
    1994, ``Containment System Leakage Testing Requirements.'' ANSI/ANS-
    56.8-1994 will be used to develop the technical methods and 
    techniques for the Containment Leakage Rate Test Program as stated 
    in Regulatory Guide 1.163. The technical methods and techniques in 
    ANSI/ANS-56.8-1994 have been determined to be acceptable to the NRC 
    Staff.
        Changes to the Administrative Section describe the containment 
    testing program only and do not reduce the margin of safety.
        Moreover, the Commission has provided guidance concerning the 
    application of standards in 10 CFR 50.92 by providing certain 
    examples (51 FR 7751, March 6, 1986) of amendments that are 
    considered not likely to involve an SHC [significant hazards 
    consideration]. Although the proposed change is not enveloped by a 
    specific example, it has been shown that the proposed change is not 
    an SHC.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270.
        NRC Project Director: Phillip F. McKee
    
    Consumers Power Company, Docket No. 50-255, Palisades Plant, Van 
    Buren County, Michigan
    
        Date of amendment request: February 6, 1996
        Description of amendment request: The proposed amendment would 
    delete the requirement to perform additional operability testing of 
    safety system train components when a required component in the 
    redundant train becomes inoperable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Do the proposed changes involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes remove the requirement for testing which is 
    in addition to the normal surveillance interval. The affected 
    equipment is subject to periodic surveillance testing required by 
    the Technical Specifications. Removing the requirement for 
    additional testing cannot alter any plant operating conditions, 
    operating practices, equipment settings, or equipment capabilities. 
    Therefore, changing an AOT [allowable outage time] or a surveillance 
    interval cannot increase the probability or consequences of an 
    accident previously evaluated.
        2. Do the proposed changes create the possibility of a new or 
    different kind of accident from any previously evaluated?
        The proposed changes remove the requirement for testing which is 
    in addition to the normal surveillance interval. The affected 
    equipment is subject to periodic surveillance testing required by 
    the Technical Specifications. Removing the requirement for 
    additional testing cannot alter any plant operating conditions, 
    operating practices, equipment settings, or equipment capabilities. 
    Therefore, changing an AOT or a surveillance interval cannot create 
    the possibility of a new or different
    
    [[Page 28612]]
    
    kind of accident from any previously evaluated.
        3. Do the proposed changes involve a significant reduction in a 
    margin of safety?
        The proposed changes remove the requirement for testing which is 
    in addition to the normal surveillance interval, in effect extending 
    the surveillance interval. An excessive surveillance interval 
    extension could reduce the margin of safety by reducing assurance 
    that required equipment will function as designed; an overly 
    restrictive surveillance interval could also reduce the margin of 
    safety by imposing unnecessary testing wear, equipment 
    manipulations, and system transients on the plant.
        The existing requirements to perform cross-train testing were 
    based on the operating experience available when they were added to 
    the TS. Typically this was done during the initial plant licensing 
    in 1971. The recently published Standard Technical Specifications 
    (NUREG 1432) do not include cross-train testing requirements for the 
    Engineered Safety Features components. It has been judged by the NRC 
    and by the industry, that cross-train testing is unnecessary, and 
    that testing at normal surveillance intervals is adequate to assure 
    equipment operability. This recent judgment is based on a much 
    larger accumulation of operating experience than was available at 
    the time Palisades was licensed. There are no special features of 
    the Palisades plant which would invalidate these more recent 
    judgments of optimal testing requirements. Therefore, operation of 
    the facility in accordance with the proposed changes will not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423
        Attorney for licensee: Judd L. Bacon, Esquire, Consumers Power 
    Company, 212 West Michigan Avenue, Jackson, Michigan 49201
        NRC Project Director: Mark Reinhart
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: December 14, 1995, as supplemented by 
    letter dated May 16, 1996.
        Description of amendment request: The proposed amendments would 
    change the Technical Specifications (TS) to improve the TS Action 
    Statements and Surveillance Requirements for diesel generators in 
    accordance with the recommendations and guidance in Generic Letter 93-
    05, Generic Letter 94-01, NUREG-1366, and NUREG-1431. The proposed 
    amendments would also incorporate technical and administrative changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Criterion 1
        Operation of the facilities in accordance with the requested 
    amendments will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. 
    Improvements to the LCOs [limiting condition for operation] and 
    surveillance requirements for the emergency diesel generators do not 
    affect their capability to provide emergency power to plant vital 
    instruments and safety related equipment. In fact, these 
    improvements make the diesel generators more reliable since they 
    significantly reduce the amount of wear and stress due to excessive 
    and unnecessary testing. The proposed monthly testing of the diesel 
    generator continues to ensure that the system is ready for service 
    when needed. The fast starts and fast loadings continue to ensure 
    that the timing and loading requirements for engineered safety 
    features actuation are met. The proposed changes do not affect any 
    of the design basis accident analyses previously evaluated. 
    Therefore, these proposed changes do not involve any increase in the 
    probability or consequences of any accident previously evaluated. 
    The proposed changes are fully consistent with the recommendations 
    and guidance contained in GL [Generic Letter] 93-05, GL 94-01, 
    NUREG-1366, NUREG-1431, and are compatible with plant operating 
    experience.
        Criterion 2
        Operation of the facilities in accordance with the requested 
    amendments will not create the possibility of a new or different 
    kind of accident from any accident previously evaluated. The 
    proposed changes in fact improve the reliability of the diesel 
    generators by eliminating unnecessary wear and stress. Improved 
    reliability decreases the failure probability which also decreases 
    the probability of an accident not previously evaluated. None of the 
    requested amendments increase the common mode failure probability 
    thus would not increase the chance of both EDG's [emergency diesel 
    generators] for a particular nuclear unit being out of service 
    simultaneously. The proposed changes are fully consistent with the 
    recommendations and guidance contained in GL 93-05, GL 94-01, NUREG-
    1366, NUREG-1431, and are compatible with plant operating 
    experience.
        Criterion 3
        Operation of the facilities in accordance with the requested 
    amendments will not involve a significant reduction in a margin of 
    safety. The proposed monthly testing of the diesel generators 
    continues to ensure that the system is ready for service when 
    needed. The fast starts and fast loadings continue to ensure that 
    the timing and loading requirements for engineered safety features 
    actuation are met. The proposed changes improve the reliability of 
    the diesel generators. Implementation of the Maintenance Rule also 
    ensures continued reliability of the diesel generators. No margin of 
    safety is decreased as a result of these TS changes.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear One, 
    Unit No. 1, Pope County, Arkansas
    
        Date of amendment request: April 29, 1996
        Description of amendment request: The proposed amendment relocates 
    several cycle specific operating parameters from the technical 
    specifications to the Core Operating Limits Report per Generic Letter 
    88-16. The parameters being relocated by this change include the 
    variable low reactor coolant system pressure trip (VLPT) and the 
    variable low reactor coolant system pressure-temperature protective 
    limits.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Criterion 1. Does Not Involve a Significant Increase in the 
    Probability or Consequences of an Accident Previously Evaluated.
        The removal of the cycle-dependent variable low RCS pressure-
    temperature protective limits and the VLPT setpoint from technical 
    speciications and placing them into the COLR has no impact on plant 
    safety and is considered to be administrative in nature. The 
    proposed change does not affect the safety analyses, physical 
    design, or operation of the plant. Technical specifications will 
    continue to require operation within the core protective and 
    operational limits for each reload cycle as calculated by the 
    approved reload design methodologies. The appropriate actions 
    required if limits are violated will remain in the technical 
    specifications. The reload report presents the results of cycle-
    specific evaluations of accident analyses and transients addressed 
    in the ANO-1 Safety Analysis Report. The cycle-specific 10CFR50.59 
    evaluation of the reload
    
    [[Page 28613]]
    
    report demonstrates that changes in fuel cycle design and the 
    corresponding COLR do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        Criterion 2. Does not Create the Possibility of a New or 
    Different Kind of Accident from any Previously Evaluated.
        The proposed change to relocate the variable low RCS pressure-
    temperature protective limits and the VLPT setpoint from the 
    technical specifications to the COLR is administrative in nature. No 
    change to the design configuration or method of operation of the 
    plant is made by this proposed change, and therefore, no new 
    transient initiator has been created. Technical specifications will 
    continue to require operation within the required core protective 
    and operating limits and appropriate actions will be taken if the 
    limits are exceeded. Because plant operation will continue to be 
    limited by the cycle-specific COLR limits that are established using 
    NRC-approved methodologies, these relocations will have no impact on 
    plant safety.
        Therefore, this change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        Criterion 3. Does Not Involve a Significant Reduction in the 
    Margin of Safety.
        Existing technical specification operability and surveillance 
    requirements are not reduced by the proposed change to relocate the 
    variable low RCS pressure-temperature protective limits and the VLPT 
    setpoint to the COLR. The proposed changes are administrative in 
    nature and do not relate to or modify the safety margins defined in 
    and maintained by the technical specifications. The cycle-specific 
    COLR limits for future reload fuel cycles will continue to be 
    developed based on NRC approved methodologies. Each future reload 
    undergoes a 10CFR50.59 evaluation to assure that operation of the 
    plant within the cycle-specific limits will not involve a 
    significant reduction in a margin of safety.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf 
    Nuclear Station, Unit 1, Claiborne County, Mississippi
    
        Date of amendment request: May 6, 1996
        Description of amendment request: The amendment would reflect that 
    the name of Mississippi Power & Light Company (MP&L) has been changed 
    to Entergy Mississippi, Inc. The amendment revises Operating License 
    NPF-29 and Antitrust Conditions for the Grand Gulf Nuclear Station, 
    Unit 1 (GGNS) to (1) add the phrase ``(now renamed Entergy Mississippi, 
    Inc.)'' after the name of Mississippi Power & Light Company (MP&L), (2) 
    replace the name of Mississippi Power & Light Company (MP&L) by the 
    name Entergy Mississippi, Inc., and (3) replace a footnote by the 
    statement: ``Amendment ---- resulted in a name change for Mississippi 
    Power & Light Company (MP&L) to Entergy Mississippi, Inc.''.The 
    proposed amendment involves only a change in company name. It does not 
    involve any changes to the Technical Specifications for GGNS, or to any 
    requirements or limiting conditions for operation on any equipment or 
    any systems in the plant.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Entergy Operations, Inc. proposes to change the current Grand 
    Gulf Nuclear Station Facility Operating License and Antitrust 
    Conditions. The specific proposed change is to reflect that the name 
    of one of the companies owning Grand Gulf Nuclear Station has 
    legally changed from Mississippi Power & Light Company to Entergy 
    Mississippi, Inc.
        The Commission has provided standards for determining whether a 
    no significant hazards consideration exists as stated in 10 CFR 
    50.92(c). A proposed amendment to an operating license involves no 
    significant hazards consideration if operation of the facility in 
    accordance with the proposed amendment would not: (1) involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated; or (3) involve a significant reduction in a margin of 
    safety.
        Entergy Operations, Inc. has evaluated the no significant 
    hazards consideration in its request for this license amendment and 
    determined that no significant hazards consideration results from 
    this change. In accordance with 10 CFR 50.91(a), Entergy Operations, 
    Inc. is providing the analysis of the proposed amendment against the 
    three standards in 10 CFR 50.92(c). A description of the no 
    significant hazards consideration determination follows:
        I. The proposed change does not significantly increase the 
    probability or consequences of an accident previously evaluated.
        The proposed change documents changing the legal name of the 
    company. The proposed change will not affect any other obligations. 
    The company will still own all of the same assets, serve the same 
    customers, and all existing obligations and commitments will 
    continue unaffected.
        [The proposed change does not affect any of the existing 
    requirements or commitments on equipment or systems that are 
    designed for the safe operation of the plant. It does not affect the 
    design or operation of the plant.]
        Therefore, the proposed change does not significantly increase 
    the probability or consequences of an accident previously evaluated.
        II. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The administrative changes to the Operating License [and 
    Antitrust Condition] requirements [to change the name of Mississippi 
    Power & Light] do not involve any change in the design or operation 
    of the plant. The company will still own all of the same assets, 
    serve the same customers, and all existing obligations and 
    commitments will continue unaffected.
        [The proposed changes do not affect equipment or systems that 
    could caused an accident at the plant.]
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        III. The proposed change does not involve a significant 
    reduction in a margin of safety.
        The proposed change [in name] is administrative in nature, as 
    described above; therefore, this change does not reduce the level of 
    safety imposed by any current requirements. [The proposed changes do 
    not affect any equipment or systems at the plant.] The company will 
    still own all of the same assets, serve the same customers, and all 
    existing obligations and commitments will continue unaffected.
        Therefore, the proposed changes do not cause a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. herefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    [[Page 28614]]
    
    Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf 
    Nuclear Station, Unit 1, Claiborne County, Mississippi
    
        Date of amendment request: May 8, 1996
        Description of amendment request: The amendment request would 
    replace the current frequency requirements in Surveillance Requirement 
    (SR) 3.6.1.3.5, on the leakage rate testing for each containment purge 
    valve with resilient seals, in the Technical Specifications for Grand 
    Gulf Nuclear Station, Unit 1 (GGNS). The proposed changes would place 
    these purge valves on a performance-based leakage testing frequency, 
    instead of the current once every 184 days and once within 92 days 
    after opening the valve.The proposed changes do not change the limiting 
    conditions for operation, the required actions for inoperability, or 
    the other surveillance requirements on these primary containment 
    isolation valves.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        In accordance with 10 CFR 50.92, Entergy Operations, Inc. has 
    evaluated the proposed change to the Operating License of GGNS and 
    has determined that the operation of the facility in accordance with 
    the proposed amendment would not involve any significant hazards 
    considerations. In accordance with 10 CFR 50.91(a), Entergy 
    Operations, Inc. is providing the following analysis of the proposed 
    amendment against the three [following] standards of 10 CFR 
    50.92(c):
        1) The proposed change does not significantly increase the 
    probability or consequences of an accident previously evaluated.
        This change deletes the augmented testing requirement for these 
    containment isolation valves and allows the surveillance intervals 
    to be set in accordance with the Appendix J testing program. 
    [Appendix J to 10 CFR Part 50 defines primary containment leakage 
    testing requirements for water-cooled power reactors as GGNS and 
    these requirements include frequency of testing for the primary 
    containment isolation valves.] This change does not affect the 
    system function or design. The purge valves are not an initiator of 
    any previously analyzed accident. Leakage rates do not affect the 
    probability of the occurrence of any accident. Operating history has 
    demonstrated that these valves do not degrade and cause leakage as 
    previously anticipated. Because these valves have been demonstrated 
    to be reliable, these valves can be expected to perform the 
    containment isolation function as assumed in the accident analyses.
        Therefore, there is no significant increase in the consequences 
    of any previously evaluated accident.
        2) The proposed change would not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Extending the test intervals has no influence on, nor does it 
    contribute in any way to, the possibility of a new or different kind 
    of accident or malfunction from those previously analyzed. No change 
    has been made to the design, function or method of performing 
    leakage testing [or to the design and function of these valves]. 
    Leakage acceptance criteria have not changed. No new accident modes 
    are created by extending the testing intervals. No safety-related 
    equipment or safety functions are altered as a result of this 
    change.
        [Therefore, the proposed changes do not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.]
        3) The proposed change does not involve a significant reduction 
    in a margin of safety
        The only margin of safety that has the potential of being 
    impacted by the proposed changes involves the offsite dose 
    consequences of postulated accidents which are directly related to 
    the containment leakage rate. The proposed change does not alter the 
    method of performing the tests nor does it change the leakage 
    acceptance criteria. Sufficient data has been collected to 
    demonstrate that the resilient seals do not degrade at an 
    accelerated rate.
        [Also, the proposed change would test these valves in accordance 
    with the Appendix J testing program at the plant. Appendix J to 10 
    CFR Part 50 defines primary containment leakage testing requirements 
    for water-cooled power reactors as GGNS and these requirements 
    include frequency of testing for the primary containment isolation 
    valves.]
        Because of this demonstrated reliability, this change will 
    provide sufficient surveillance to determine an increase in the 
    unfiltered leakage prior to the leakage exceeding that assumed in 
    the accident analysis.
        Therefore, the proposed change does not result in a significant 
    reduction in a margin of safety.
        Based on the above evaluation, Entergy Operation, Inc. has 
    concluded that operation in accordance with the proposed amendment 
    involves no significant hazards considerations.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf 
    Nuclear Station, Unit 1, Claiborne County, Mississippi
    
        Date of amendment request: May 9, 1996
        Description of amendment request: The amendment request would (1) 
    increase the safety limit minimum critical power ratio (MCPR) for two 
    loop operation and single loop operation to 1.10 and 1.11, 
    respectively, and (2) add a General Electric topical report to the list 
    of documents describing the analytical methods used to determine the 
    core operating limits. The proposed changes are to Section 2.1.1, 
    Reactor Core Safety Limits, and Section 5.6.5, Core Operating Limits 
    Report (COLR), respectively, of the Technical Specifications (TSs).
        The licensee also proposed changes to the Bases of the TSs 
    associated with the above proposed changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Entergy Operations, Inc. proposes to change the current Grand 
    Gulf Nuclear Station [GGNS] Technical Specifications. The specific 
    change is to modify the Minimum Critical Power Ratio (MCPR) safety 
    limits reported in Technical Specification 2.1.1.2, the list of 
    references in Technical Specification 5.6.5, and associated Bases 
    changes. The proposed change is necessary in order to switch reload 
    fuel vendors. [General Electric GE11 fuel is being added to the core 
    in place of Siemens Power Corporation (SPC) fuel.]
        The Commission has provided standards for determining whether no 
    significant hazards considerations exists as stated in 10 CFR 50.92 
    (c). A proposed amendment to an operating license involves no 
    significant hazards if operation of the facility in accordance with 
    the proposed amendment would not: (1) involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated; (2) create the possibility of a new or different kind of 
    accident from any accident previously evaluated; or (3) involve a 
    significant reduction in a margin of safety.
        Entergy Operations, Inc. has evaluated the no significant 
    hazards consideration in its request for this license amendment and 
    determined that no significant hazards considerations result from 
    this change. In accordance with 10 CFR 50.91(a), Entergy Operations, 
    Inc. is providing the analysis of the proposed amendment against the 
    three standards in 10 CFR 50.92(c). A description of the no 
    significant hazards consideration determination follows:
        I. The proposed change does not significantly increase the 
    probability or consequences of an accident previously evaluated.
    
    [[Page 28615]]
    
        The Minimum Critical Power Ratio (MCPR) safety limit is defined 
    in the Bases to Technical Specification 2.1.1 as that limit which 
    ``ensures that during normal operation and during Anticipated 
    Operational Occurrences (AOOs), at least 99.9% of the fuel rods in 
    the core do not experience transition boiling.'' The MCPR safety 
    limit is re-evaluated for each reload and, for GGNS [Operating] 
    Cycle 9, the analyses have concluded that a two-loop MCPR safety 
    limit of 1.10 based on the application of the generic GE MCPR 
    methodology is necessary to ensure that this acceptance criterion is 
    satisfied. For single-loop operation, a MCPR safety limit of 1.11 
    based on the generic GE MCPR methodology was determined to be 
    necessary. Core MCPR operating limits are developed to support the 
    Technical Specification 3.2 requirements and ensure these safety 
    limits are maintained in the event of the worst-case transient. 
    Since the MCPR safety limit will be maintained at all times, 
    operation under the proposed changes will ensure at least 99.9% of 
    the fuel rods in the core do not experience transition boiling. 
    Therefore, The Minimum Critical Power Ratio (MCPR) safety limit 
    change does not affect the probability or consequences of an 
    accident.
        The implementation of GE's GESTAR-II approved methodology has no 
    effect on the probability or consequences of any accidents 
    previously evaluated. One exception to GESTAR is that the mis-
    oriented and mis-located bundle events will continue to be analyzed 
    as accidents subject to the acceptance criteria in the current 
    licensing basis. The design of the GE11 fuel bundles is such that 
    the bundles are not likely to be mis-oriented or mis-located and the 
    normal administrative controls will be in effect for assuring proper 
    orientation and location. Therefore, the probability of a fuel 
    loading error is not increased. This analysis ensures that 
    postulated dose releases will not exceed a small fraction (10 
    percent) of 10CFR100 limits.
        Therefore, the consequences of accidents previously evaluated 
    are unchanged.
        II. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The GE11 fuel to be used in [Operating] Cycle 9 is of a design 
    compatible with fuel present in the core and used in the previous 
    cycle. Therefore, the GE11 fuel will not create the possibility of a 
    new or different kind of accident. The proposed changes do not 
    involve any new modes of operation, any changes to setpoints, or any 
    plant modifications. They introduce revised MCPR safety limits that 
    have been proved to be acceptable for Cycle 9 operation. Compliance 
    with the applicable criterion for incipient boiling transition 
    continues to be ensured. The proposed MCPR safety limits do not 
    result in the creation of any new precursors to an accident.
        Therefore, the proposed changes do not create the possibility of 
    a new or different type of accident from any accident previously 
    evaluated.
        III. The proposed change does not involve a significant 
    reduction in a margin of safety.
        The MCPR safety limits have been evaluated to ensure that during 
    normal operation and during AOOs [abnormal operating occurrences], 
    at least 99.9% of the fuel rods in the core do not experience 
    transition boiling. Therefore, the implementation of the proposed 
    changes in the MCPR safety limit ensure there is no reduction in the 
    margin of safety.
        As with the current SPC methodology, GGNS will implement only 
    the NRC-approved revisions to GE's GESTAR methodology. This GE 
    methodology is similar to those SPC reports currently listed in TS 
    5.6.5 and it will be applied in a similar, conservative fashion. One 
    exception to GESTAR is that the mis-oriented and mis-located bundle 
    events will continue to be analyzed as accidents subject to the 
    acceptance criteria in the current licensing basis. This analysis 
    ensures that postulated dose releases will not exceed a small 
    fraction (10 percent) of 10CFR100 limits. On this basis, the 
    implementation of this GE methodology does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: February 6, 1996
        Description of amendment request: The proposed change will amend 
    the Allowable Values of parameters in Table 3.3-4 of Waterford Steam 
    Electric Station, Unit 3, (Waterford 3) Technical Specifications (TSs) 
    to make it consistent with the identical parameters in Table 2.2-1 of 
    TSs for Waterford 3. The proposed change will add Mode 4 to the 
    surveillance requirements of Table 4.3-2, Item 5.c (Safety Injection 
    System Automatic Actuation Logic) that was inadvertently removed. 
    Finally, the proposed change removes a reference to TS 3.3.3.2 in 
    Surveillance Requirements TS 4.10.2.2 and 4.10.4.2 since Incore 
    Detectors has been removed from the TSs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes described herein are administrative changes 
    necessary to correct administrative errors. The proposed changes 
    will have no affect on any design basis accidents nor will these 
    changes affect any material condition of the plant. Therefore, the 
    proposed changes will not involve a significant increase in the 
    probability or consequences of any accident previously evaluated.
        The proposed changes are purely administrative. There are no new 
    system or design changes associated with this proposal. Therefore, 
    the proposed change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed change will have no impact on any protective 
    boundary, safety limit, or margin to safety. The proposed change 
    corrects inconsistencies in the TS and is purely administrative in 
    nature. Therefore, the proposed change will not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: William D. Beckner
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of amendment request: May 7, 1996 (TSCR 247)
        Description of amendment request: The proposed change to the 
    technical specifications would adopt the provisions of the Standard 
    Technical Specifications (STS), NUREG-1433, Rev. 1, which clarify 
    surveillance requirement applicability and allow a maximum period of 24 
    hours to complete a surveillance requirement upon discovery that the 
    surveillance has been missed.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of the facility in accordance with the proposed 
    amendment would not
    
    [[Page 28616]]
    
    involve a significant increase in the probability of occurrence or 
    consequence of an accident previously evaluated. The proposed 
    changes only affect administrative requirements regarding the 
    applicability and performance of surveillances. This change 
    clarifies surveillance requirement applicability and allows a 
    maximum 24 hour delay period for the performance of a surveillance 
    when it is discovered that the surveillance has not been performed 
    within the required frequency, consistent with the STS. There is 
    minimal safety significance associated with a delay of 24 hours in 
    completing the required surveillance, particularly due to the fact 
    that the most probable result of any particular surveillance 
    performed is the successful verification of conformance with the 
    requirements.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any previously evaluated. The proposed changes 
    only affect administrative requirements regarding the applicability 
    of surveillance requirements and the performance of surveillances to 
    allow a maximum 24 hour delay period when it is discovered that a 
    surveillance has been missed. No changes to plant equipment or 
    operation are affected.
        3. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in the margin of 
    safety since the change contained in the proposed amendment does not 
    change any existing safety margins.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753
        Attorney for licensee: Ernest L. Blake, Jr., Esquire. Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    GPU Nuclear Corporation, Docket No. 50-320, Three Mile Island 
    Nuclear Station, Unit No. 2 (TMI-2), Dauphin County, Pennsylvania
    
        Date of amendment request: February 16, 1995
        Description of amendment request: The proposed amendment would 
    revise TMI-2 Operating License No. DPR-73 by modifying sections 4.02, 
    4.04, and 4.1.1.3 of the unit technical specifications. The revisions 
    to sections 4.02 and 4.04 would add flexibility to the scheduling of 
    surveillance activities and would allow for a 24 hour period to perform 
    missed surveillances before declaration of a limiting condition for 
    operation, respectively. These changes would make the TMI-2 technical 
    specifications consistent with the Standard Technical Specifications 
    for B&W Plants (NUREG-1430). The revision to section 4.1.1.3 would 
    allow extension of the time interval for surveillance of the 
    containment airlock doors from quarterly to annually. The proposed 
    changes to the TMI-2 technical specifications section 4.1.1.3 would 
    allow a decrease in worker exposure to radiation while maintaining an 
    adequate level of environmental protection at the facility.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        10 CFR 50.92 provides the criteria which the Commission uses to 
    perform a no significant hazards consideration. 10 CFR 50.92 states 
    that an amendment to a facility license involves no significant 
    hazards if operation of the facility in accordance with the proposed 
    amendment would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated, or
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated, or
        3. Involve a significant reduction in a margin of safety.
        The proposed changes to the technical specifications sections 
    4.02 and 4.04 are administrative and do not involve any physical 
    changes to the facility. No changes are made to operating limits or 
    parameters, nor to any surveillance activities. The changes to 
    section 4.1.1.3 extends the interval between surveillance of the 
    containment airlocks; it does not change the operability 
    requirements, test methodology or acceptance criteria. Based on 
    this, GPU Nuclear has concluded that the proposed changes to 
    sections 4.02 and 4.04 do not:
        1. Involve a significant increase in the probability of 
    occurrence or the consequences of an accident previously evaluated. 
    The changes do not modify any operating parameters or the release of 
    radioactive materials. The clarification of maximum time extensions 
    for surveillance is consistent with the NRC's Standard Technical 
    Specifications for Babcock and Wilcox Plants (NUREG-1430).
        2. Create the possibility of a new or different kind of accident 
    since these change are administrative and no plant configuration or 
    operational changes are involved.
        3. Involve a change in the margin of safety. These changes are 
    administrative in nature, compatible with standard technical 
    specifications, and do not affect any safety settings or operational 
    limits.
        GPU Nuclear has also concluded that the proposed changes to 
    section 4.1.1.3 do not:
        1. Involve a significant increase in the probability of 
    occurrence of or consequences of an accident previously evaluated. 
    The change to this section does not change operating parameters, 
    equipment operability requirements, surveillance test methodology, 
    or acceptance criteria.
        2. Create the possibility of a new or different kind of accident 
    since the change does not affect plant equipment, plant 
    configuration, or plant operating parameters.
        3. Involve a change in the margin of safety since the change 
    does not affect any operational limits.
        Based on the above analysis the licensee concluded that the 
    proposed changes involve no significant safety hazards 
    considerations as defined by 10 CFR 50.92.
        The NRC staff has reviewed the analysis of the licensee and, based 
    on this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, Pennsylvania 17105
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: Seymour H. Weiss
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: May 1, 1996
        Description of amendment request: The proposed amendments would 
    change the Technical Specifications to implement 10 CFR Part 50, 
    Appendix J, Option B, by referring to Regulatory Guide 1.163, 
    ``Performance-Based Containment Leakage-Test Program.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        [South Texas Project] STP has evaluated the proposed Technical 
    Specification Amendment and determined that it does not represent a 
    significant hazards consideration. Based on the criteria for 
    defining a significant hazards consideration established in 10 CFR 
    50.92, operation of STP in accordance with the proposed amendment 
    will not:
        1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because of the 
    following:
        10 CFR [Part] 50, Appendix J has been amended to include 
    provisions regarding
    
    [[Page 28617]]
    
    performance based leakage testing requirements (Option B). Option B 
    allows plants with satisfactory Integrated Leak Rate Testing (ILRT) 
    performance history to extend the Type A testing interval from three 
    tests in ten years to one test in ten years. For Type B and Type C 
    tests, Option B allows extended testing interval[s] based on the 
    leak rate test history of each component. To be consistent with the 
    requirements of 10 CFR [Part] 50, Appendix J, Option B, STP proposes 
    to include appropriate changes to the Technical Specifications that 
    incorporate the necessary revisions associated with 10 CFR [Part] 
    50, Appendix J, Option B.
        The proposed amendment represents the conversion of current 
    Technical Specification requirements to maintain consistency with 
    those requirements specified by 10 CFR [Part] 50, Appendix J, Option 
    B. The proposed changes are consistent with the current safety 
    analyses. Implementation of these changes will provide continued 
    assurance that specified parameters associated with containment 
    integrity will remain within acceptance limits, and will not 
    significantly increase the probability or consequences of a 
    previously evaluated accident.
        Some proposed changes represent minor relaxations in current 
    Technical Specification requirements, but are based on the 
    requirements specified by Option B of 10 CFR [Part] 50, Appendix J. 
    Changes are consistent with the current safety analyses and 
    determined to represent sufficient requirements for the assurance 
    and reliability of equipment assumed to operate in the safety 
    analyses, and provide continued assurance that specified parameters 
    associated with containment integrity remain within their acceptance 
    limits. These changes will not significantly increase the 
    probability or consequences of a previously evaluated accident.
        The systems affecting containment integrity related to this 
    proposed amendment request are not assumed in any safety analyses to 
    initiate any accident sequence. The probability of any accident 
    previously evaluated is not increased by this proposed amendment. 
    The proposed changes to Technical Specification LCOs or SRs maintain 
    an equivalent level of reliability and availability for all affected 
    systems. The proposed amendment does not increase the consequences 
    of any accident previously evaluated.
        There is no change to the consequences of an accident previously 
    evaluated because maintaining leakage within the analyzed limit 
    assumed for any associated accident analyses does not adversely 
    affect either the on-site or off-site dose consequences resulting 
    from an accident. There is no adverse impact on the probability of 
    accident initiators. There is no significant increase in the 
    probability of any previously analyzed accident. A plant specific 
    risk-based analysis of Appendix J performed for STP indicates the 
    containment penetration leakage dose rate contribution to the total 
    dose rate in person-rem is insignificant.
        2) Create the possibility of a new or different kind of accident 
    from any accident previously evaluated because:
        10 CFR [Part] 50, Appendix J, Option B specifies, in part, that 
    a Type A test which measures both the containment system overall 
    integrated leakage rate at containment pressure and system 
    alignments assumed during a large break LOCA [loss-of-coolant 
    accident], and demonstrates the capability of primary containment to 
    withstand an internal pressure load, may be conducted at an interval 
    based on the performance of the overall containment system. The 
    acceptable leakage rates are specified in the plant's Technical 
    Specifications. For Type B and Type C tests, intervals are proposed 
    based on the performance history of each component. Acceptance 
    criteria for each component is based upon demonstration that the sum 
    leakage rates at design basis pressure conditions for applicable 
    penetrations, is within the limit specified in the Technical 
    Specifications.
        The proposed amendment represents the conversion of current 
    Technical Specification requirements to maintain consistency with 
    those requirements specified in 10 CFR [Part] 50, Appendix J, Option 
    B. The proposed changes are consistent with the current safety 
    analyses. Some minor relaxations in current Technical Specification 
    requirements, associated with containment integrity are based on 
    generic guidance provided in Option B, NEI 94-01 and ANSI/ANS 56.8, 
    1994. These changes do not involve revisions to the design of the 
    station. Some of the changes may involve revision in the testing of 
    components; however, these are in accordance with the STP current 
    safety analyses and provide for appropriate testing or surveillance 
    that are consistent with 10 CFR [Part] 50, Appendix J, Option B. The 
    proposed changes will not introduce new failure mechanisms beyond 
    those already considered in the current safety analyses.
        The proposed amendment has been reviewed for acceptability 
    considering similarity of system or component design affecting 
    containment integrity. No new modes of operation are introduced by 
    the proposed changes. Surveillance requirements are changed to 
    reflect corresponding changes associated with Option B of 10 CFR 
    [Part] 50, Appendix J and improvements in technique or interval of 
    leak rate testing performance. The proposed changes maintain, at 
    minimum, the present level of operability of any system that affects 
    containment integrity. The proposed changes do not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        The associated systems that affect leak rate integrity related 
    to the proposed amendment, are not assumed in any safety analysis to 
    initiate any accident sequence. The proposed surveillance 
    requirements for any affected systems are consistent with the 
    current requirements specified within the Technical Specifications 
    and are consistent with the requirements of Option B of 10 CFR 
    [Part] 50, Appendix J. The proposed surveillance requirements 
    maintain an equivalent level of reliability and availability of all 
    affected systems and therefore, does not increase the consequences 
    of any previously evaluated accident.
        3) Involve a significant reduction in the margin of safety 
    because:
        The provisions specified in Option B of 10 CFR [Part] 50 
    Appendix J allow changes to Type A, Type B, and Type C test 
    intervals based upon the performance of past leak rate tests. The 
    effect of extending containment leakage rate testing intervals has a 
    corresponding increase in the likelihood of containment leakage. The 
    degree to which intervals can be extended is a direct function of 
    the potential effect to existing safety margins and the public 
    health and safety that can occur due to an increased likelihood of 
    containment leakage. 10 CFR [Part] 50 Appendix J, Option B allows 
    longer intervals between leakage tests based on performance trends 
    but does not increase the leakage acceptance criteria. La [maximum 
    allowable leakage rate] is still limited to 0.3 wt%/day. By 
    referencing the Containment Leakage Rate Testing Program in LCO 
    3.6.1.2 ACTION, the point at which ACTION is required is increased 
    from .75 La to 1.0 La. This makes the specification consistent with 
    the intent of having margin between an AS-LEFT leakage of less than 
    or equal to .75 La and maintaining operability with less than or 
    equal to 1.0 La.
        Changing Appendix J test intervals from those currently provided 
    in the Technical Specification to those provided in 10 CFR [Part] 
    50, Appendix J, Option B, slightly increases the risk associated 
    with Type A, Type B, and Type C specified accident sequences. 
    Historical data suggests that increasing the Type C test interval 
    can slightly increase the associated risk; however, this is 
    compensated by the corresponding risk reduction benefits associated 
    with reduction in component cycling, stress, and wear associated 
    with increased test intervals. When considering the total integrated 
    risk which includes all analyzed accident sequences, the risk 
    associated with increasing test intervals is negligible. A plant 
    specific risk-based analysis of Appendix J performed for STP 
    indicates the containment penetration leakage dose rate contribution 
    to total dose rate in person-rem is insignificant.
        STP proposes to revise the Technical Specifications to be 
    consistent with those provisions specified in Option B of 10 CFR, 
    Appendix J. The proposed changes are consistent with the STP current 
    safety analyses. These proposed changes do not involve revisions to 
    the design of the station. The proposed changes will maintain the 
    same level of reliability of equipment associated with containment 
    integrity assumed to operate in the safety analysis, and provide 
    continued assurance that specified parameters affecting plant leak 
    rate integrity will remain within acceptance limits. The proposed 
    changes provide continued assurance of leakage integrity of 
    containment without adversely affecting the public health and safety 
    and will not significantly reduce existing safety margins. Plant 
    specific risk-based analysis indicates sufficient technical 
    justification exists to further extend the limits beyond those 
    allowed by Option B.
        The proposed amendment to the Technical Specifications 
    implements present requirements, or the requirements in accordance 
    with the guidelines set forth in Option B of 10 CFR [Part] 50, 
    Appendix J. NUREG-1493, ``Performance-Based Containment Leak-Test 
    Program,'' served as the technical basis for Option B. STP
    
    [[Page 28618]]
    
    performed a plant specific risk-based analysis of containment 
    penetration leakage dose utilizing the same methodology used in 
    NUREG-1493. The analysis indicates the containment penetration 
    leakage dose rate contribution to the total dose rate in person-rem 
    is insignificant. This plant specific analysis serves to validate 
    the applicability of the proposed changes for STP. The proposed 
    changes have been approved by the NRC, are applicable to STP, 
    maintain necessary levels of system or component reliability 
    affecting containment integrity, and do not involve a significant 
    reduction in the margin of safety.
        The performance-based approach to leakage rate testing concludes 
    the impact on public health and safety due to revised testing 
    intervals is negligible. The proposed amendment will not reduce 
    availability of systems associated with containment integrity when 
    required to mitigate accident conditions; therefore, the proposed 
    changes do not involve a significant reduction in the margin of 
    safety.
        Guidance has been provided in ``Final Procedures and Standards 
    on No Significant Hazards Considerations,'' Final Rule, 51 FR 7744, 
    for the application of standards to license change requests for 
    determination of the existence of significant hazards 
    considerations. This document provides examples of amendments which 
    are and are not considered likely to involve significant hazards 
    considerations.
        This proposed amendment does not involve a significant 
    relaxation of the criteria used to establish safety limits, a 
    significant relaxation of the bases for limiting safety system 
    settings or a significant relaxation of the bases for LCOs. 
    Therefore, based on the guidance provided in the Federal Register 
    and criteria established in 10 CFR 50.92(c), the proposed change 
    does not constitute a significant hazards consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, N.W., Washington, DC 20036-5869
        NRC Project Director: William D. Beckner
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota
    
        Date of amendment requests: December 14, 1995
        Description of amendment requests: The proposed amendments would 
    revise the Administrative Control (Chapter 6) Section and other 
    affected Sections of the Prairie Island Technical Specifications to 
    generally conform with NUREG-1431, Standard Technical Specifications, 
    Westinghouse Plants, Revision 1, dated April 7, 1995.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Operation of the Prairie Island plant in accordance with the 
    proposed changes does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. 
    None of the proposed changes involve a physical modification to the 
    plant, a new mode of operation or a change to the Updated Safety 
    Analysis Report transient analyses. These proposed amendments 
    generally conform to the guidance of NUREG-1431, Revision 1, Section 
    5.0 which was previously reviewed, accepted and issued by the NRC.
        Some Section 5.0 Specifications in NUREG-1431 were not 
    incorporated in this License Amendment Request. These Specifications 
    were not proposed because they 1) specify requirements not currently 
    in the Prairie Island Technical Specifications or otherwise 
    committed to, 2) are addressed elsewhere in the current Technical 
    Specifications, or 3) the current Technical Specifications level of 
    commitment is maintained. In all these instances, the NRC has 
    previously reviewed and approved the proposed level of commitment 
    through the issuance of the current Prairie Island Technical 
    specifications.
        The proposed changes, in themselves, do not reduce the level of 
    qualification or training such that personnel requirements would be 
    decreased.
        In total these changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed amendment will not create the possibility of a 
    new or different kind of accident from any accident previously 
    analyzed.
        The proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated 
    because the proposed changes, in themselves, do not introduce a new 
    mode of plant operation, surveillance requirement or involve a 
    physical modification to the plant. These proposed amendments 
    generally conform to the guidance of NUREG-1431, Revision 1, Section 
    5.0 which was previously reviewed, accepted and issued by the NRC.
        Some Section 5.0 Specifications in NUREG-1431 were not 
    incorporated in this License Amendment Request. These Specifications 
    were not proposed because they 1) specify requirements not currently 
    in the Prairie Island Technical Specifications or otherwise 
    committed to, or 2) are addressed elsewhere in the current Technical 
    Specifications. Other features are not fully implemented but rather, 
    the current Technical Specification level of commitment is 
    maintained. In all these instances, the NRC has previously reviewed 
    and approved the proposed level of commitment through the issuance 
    of the current Prairie Island Technical Specifications.
        In general, the proposed changes are administrative in nature. 
    The changes propose to revise, delete or relocate Specifications 
    within the Technical Specifications or from the Technical 
    Specifications to the Updated Safety Analysis Report, plant 
    procedures or the Operational Quality Assurance Plan through which 
    adequate control is maintained. The proposed changes do not alter 
    the design, function, or operation of any plant components and 
    therefore, no new accident scenarios are created.
        Therefore, the possibility of a new or different kind of 
    accident from any accident previously evaluated would not be created 
    [by] these amendments.
        3. The proposed amendment will not involve a significant 
    reduction in the margin of safety.
        The proposed changes do not involve a significant reduction in a 
    margin of safety because the Current Technical Specifications 
    requirements for safe operation of the Prairie Island plant are 
    maintained or increased. The proposed changes are administrative in 
    nature and do not involve a physical modification to the plant, a 
    new mode of operation or a change to the Updated Safety Analysis 
    Report transient analyses. The proposed changes do not alter the 
    scope of equipment currently required to be operable or subject to 
    surveillance testing nor does the proposed change affect any 
    instrument setpoints or equipment safety functions.
        Therefore, a significant reduction in the margin of safety would 
    not be involved with these amendments.
        Based on the evaluation describe above, and pursuant to 10 CFR 
    Part 50, Section 50.91, Northern States Power Company has determined 
    that operation [of] the Prairie Nuclear Generating Plant in 
    accordance with the proposed license amendment request does not 
    involve any significant hazards considerations as defined by Nuclear 
    Regulatory Commission regulations in 10 CFR Part 50, Section 50.92.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037
    
    [[Page 28619]]
    
        NRC Project Director: Mark Reinhart (Acting Director)
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of amendment requests: February 15, 1996
        Description of amendment requests: The proposed amendments would 
    revise the combined Technical Specifications (TS) for the Diablo Canyon 
    Nuclear Power Plant, Unit Nos. 1 and 2 to revise Technical 
    Specification 3.5.2, ``ECCS Subsystems - Tavg Greater Than or Equal to 
    350 deg.F,'' to change the allowed outage time for any one safety 
    injection pump from 72 hours to 7 days. The specific TS change proposes 
    to add a new footnote that increases the allowed outage time (AOT) for 
    one safety injection (SI) pump from 72 hours to 7 days for performance 
    of non-routine, emergent maintenance and requires review by the Plant 
    Staff Review Committee (PSRC), and requires Plant Manager approval 
    prior to exceeding 72 hours.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed allowed outage time (AOT) extension does not change 
    the operating practices of Diablo Canyon Power Plant (DCPP). 
    Although the proposed change increases the allowed time in which the 
    safety injection (SI) system may be out of service for maintenance 
    or testing, this extended AOT will only be used in emergent 
    circumstances.
        Increasing the AOT for the SI pumps does not involve physical 
    alteration of any plant equipment and does not affect analysis 
    assumptions regarding functioning of required equipment designed to 
    mitigate the consequences of accidents. Further, the severity of 
    postulated accidents and resulting radiological effluent releases 
    will not be affected by the increased AOT.
        Finally, the probabilistic risk assessment determined that the 
    increase in the core damage probability is not considered 
    significant.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed increase to the SI pump AOTs does not change the 
    method by which DCPP operates. Further, the proposed change would 
    not result in any physical alteration to any plant system, and there 
    would not be a change in the method by which any safety related 
    system performs its function.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        There is no safety analysis impact since the extension of the SI 
    pump AOT interval will have no effect on any safety limit, 
    protection system setpoint, or limiting condition of operation. 
    There is no hardware change that would impact existing safety 
    analysis acceptance criteria.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
        Attorney for licensee: Christopher J. Warner, Esq., Pacific Gas and 
    Electric Company, P.O. Box 7442, San Francisco, California 94120
        NRC Project Director: William H. Bateman
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        ]Date of application request: April 17, 1996
        Description of amendment request: The proposed amendment would 
    change Technical Specification (TS) 3/4.3 to support a future 
    modification to replace existing digital portions of the main steam and 
    feedwater isolation system (MSFIS) with digital processor equipment and 
    would authorize revision of the FSAR to include a description of the 
    MSFIS modification. The MSFIS modification is a change to the facility, 
    as described in the safety analysis report, that involves an unreviewed 
    safety question. The modification involves an unreviewed safety 
    questions because: (1) the MSFIS design will use software which could 
    result in a common mode failure, (2) the original NRC review of the 
    MSFIS did not evaluate 2 out of 3 coincidence circuitry, which could 
    introduce new system failure modes, and (3) the MSFIS modification 
    utilizes manual handswitches that could introduce new system failure 
    modes. The NRC will review the modification in accordance with 10 CFR 
    50.59(a)(2) in conjunction with the review of the proposed TS 
    amendment.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The addition of the MSFIS actuation logic and relays to the TS 
    has no adverse impact on the probability of occurrences or the 
    consequences of an accident. The proposed amendment does not change 
    or alter the design assumptions for the systems or components used 
    to mitigate the consequences of an accident and the methodologies 
    used in the accident analysis remain unchanged. The operating limits 
    will not be changed.
        No design basis accidents will be affected by this design change 
    since the logic which currently exists will continue to be 
    performed. Thus, the radiological consequences will not change.
        The system response time is enveloped by the current 5 second 
    valve stroke time. The MSFIS response time will be less than 500 
    msec.
        A common mode software failure could exist if both separation 
    groups have their PLCs [programmable logic controllers] (3 per train 
    - six total) malfunction at the same time. However, a diverse means 
    of isolating the feedwater lines exists given the ability of the 
    Main Feed Control Valves to close on a Feedwater Isolation Signal. 
    The MSIVs [main steam isolation valves] do not have a diverse means 
    of isolating their respective steam lines if a common mode software 
    failure occurs. As a result, this modification provides a means to 
    manually fast close the valves at the MSFIS cabinets. The operators 
    will be alerted of the failure conditions of any PLC logic channel 
    via MCB [main control board] annunciators and indicators. This 
    failure mode has a low probability of occurrence based upon the 
    inherent quality of the design provided by the V&V [verification & 
    validation] process. Therefore, the accident consequences are not 
    increased for this failure mode.
        The test panel in the MSFIS cabinets has been laid out to 
    provide the same functions as the existing test panel, except that 
    PLC status indication and coincidence logic test functions are 
    provided. The Emergency Override Panel, located below the Test 
    Panel, provides the operator with the ability to bypass the FWIS 
    [feedwater isolation signal] signal and manually fast close each 
    MSIV as required by the Emergency Operating Procedures. The MSIV 
    manual FC [fast close] switch operation is necessary for a diverse 
    means of operation for software common mode failures. The FWIS 
    bypass switch will allow main feedwater flow to be re-established to 
    each Steam Generator.
    
    [[Page 28620]]
    
        The replacement system is functionally the same as the current 
    system since it performs the same logic, receives the same inputs, 
    and produces the same outputs. However, the system is more reliable 
    and possesses triple redundant logic. Therefore, the probability of 
    malfunction will not be increased.
        The electrical load of the A-B PLC equipment and existing 48 VDC 
    [volts direct current] actuation relays is less than that of the 
    existing equipment so the system will not require any additional 
    cooling over the existing equipment. Proper grounding is provided 
    for the PLC 5 VDC and actuation relay 48 VDC power supplies, which 
    are electrically isolated from each other.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The addition of the MSFIS actuation logic and relays to the TS 
    will not create a new type of accident or malfunction than any 
    previously evaluated in the Safety Analysis Report. The safety 
    functions of the system are not changed in any manner, nor is the 
    reliability of any structure, system or component reduced. All 
    design and performance criteria continue to be met. Since the safety 
    functions and reliability are not adversely affected, the proposed 
    change does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The operator's ability to adequately respond to an accident is 
    not hindered by the man-machine interface added as a result of this 
    modification since the operator interface is similar to the current 
    system and the MCB controls will not change. The operators will be 
    alerted to system malfunctions through annunciation. The current 
    system has a status output for each MSIV and FIV [feedwater 
    isolation valve] valve on the Engineered Safety Feature Status 
    Panel, which will be maintained. In addition, an isolated plant 
    annunciator interface will provide a MSFIS Channel Failure plant 
    annunciator window for both trains. Training will be provided to the 
    technicians, engineers, and operators on the new features of the 
    system prior to installation. Therefore, this modification does not 
    increase the consequential effects due to the man-machine interface.
        The system is compatible with the normal and accident 
    environments and will be seismically qualified in accordance with 
    the SNUPPS [standardized nuclear unit power plant system] seismic 
    spectra profile. The equipment will be qualified for Electromagnetic 
    Interference concerns in accordance with EPRI [Electric Power 
    Research Institute] document TR-102323-EPRI Guideline and will meet 
    the EPRI EMI [electromagnetic interference] limiting practices.
        The system has the same failure mode upon loss of power as the 
    current system and behaves similarly upon power restoration. A loss 
    of power will not result in a MSFIS actuation.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The addition of the MSFIS actuation logic and relays to the TS 
    will not affect or change a safety limit or affect plant operations. 
    This change will not reduce the margin of safety assumed in the 
    accident analysis nor reduce any margin of safety as defined in the 
    basis for any TS.
        The system response time for any given valve will not exceed the 
    required valve stroke time. Since the MSFIS does not contain any 
    analog channels, no channel trip accuracies are impacted.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    & Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339, 
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of amendment request: October 25, 1995
        Description of amendment request: The proposed changes would 
    provide an allowed outage time of 14 days for the pressurizer power-
    operated relief valve (PORV) nitrogen accumulators, as well as provide 
    separate action statements for the PORV depending on the reason for the 
    PORV inoperability during plant operation in power Modes 1, 2, or 3.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
        Specifically, operation of North Anna Power Station in 
    accordance with the proposed Technical Specifications changes will 
    not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The PORVs are assumed to mitigate the consequences of a steam 
    generator tube rupture as described in the North Anna UFSAR [Updated 
    Final Safety Analysis Report] as well as to limit the undesired 
    opening of the pressurizer safety valves for a primary overpressure 
    event. The proposed action statements ensure that the steam 
    generator tube rupture accident analysis requirements are met. The 
    proposed Technical Specification changes require the backup nitrogen 
    supply be available for the PORVs to be consideredoperable and add 
    action statements and surveillance requirements for the nitrogen 
    supply commensurate with its significance. The proposed action 
    statements enhance the availability of the automatic actuation of 
    the PORVs by not requiring the block valves to be closed when the 
    backup nitrogen supplies are inoperable. The proposed surveillance 
    requirements enhance the reliability of the backup nitrogen supply 
    to the PORVs by verifying that there is sufficient nitrogen pressure 
    in the accumulators for the PORVs to perform their design function. 
    The proposed Technical Specification changes do not change any 
    accident analyses, therefore, the probability of any accident and 
    its resulting consequences are not increased.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed Technical Specification changes do not involve any 
    physical modification to the plant or result in a change in a method 
    of operation. The backup nitrogen supply continues to be required 
    for PORV operability. The proposed Technical Specification changes 
    provide operational flexibility and ensure the availability of the 
    PORVs using the normal supply of instrument air while the backup 
    nitrogen supply is being restored. This also prevents undesirable 
    challenges to the pressurizer safety valves. The new surveillance 
    requirements verify that there is sufficient nitrogen pressure in 
    the accumulators for the PORVs to perform their design functions.
        3. Involve a significant reduction in a margin of safety.
        The proposed Technical Specification changes do not affect any 
    safety limits or limiting safety system settings. The availability 
    of the PORVs will be maintained as required in Generic Letter 90-06. 
    The proposed Technical Specifications will continue to ensure that 
    the PORVs will be capable of performing their intended functions.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219
        NRC Project Director: Eugene V. Imbro
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Power Plant, Unit Nos. 1 and 2, Town of Two 
    Creeks, Manitowoc County, Wisconsin
    
        Date of amendment request: April 24, 1996
    
    [[Page 28621]]
    
        Description of amendment request: The proposed amendments would 
    revise Technical Specification (TS) Section 15.7, ``Radiological 
    Effluent Technical Specifications (RETS).'' Portions of the RETS would 
    be moved to licensee-controlled documents consistent with Nuclear 
    Regulatory Commission guidance on TS improvements. Changes to other 
    sections of the TSs are also proposed consistent with the removal of 
    portions of the RETS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed amendment simplifies the RETS and implements the 
    recommendations of GL 89-01 and of GL 95-10. The proposed change 
    relocates the operational requirements of RETS but keeps the 
    programmatic controls for these requirements in the Technical 
    Specifications. Therefore, the proposed changes are administrative 
    in nature and do not affect plant operations. Hence, the proposed 
    amendment does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated because no 
    safety-related equipment, safety function, or plant operation will 
    be altered as a result of this proposed change. Also, the changes 
    are unrelated to the initiation and mitigation of accidents and 
    equipment malfunctions addressed in the Final Safety Analysis 
    Report.
        2. Does the proposed amendment create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated?
        As stated above, the proposed action is the relocation of the 
    RETS procedural details to various manuals while retaining the 
    administrative controls in RETS. The relocation is consistent with 
    the intent of the guidance of GL 89-01 and of GL 95-10. It is 
    administrative and has no impact on plant operation or safety. No 
    safety-related equipment, safety function, or plant operation will 
    be altered as a result of this proposed change. No changes to plant 
    components or structures are introduced which could create new 
    accidents or malfunctions not previously evaluated.
        Therefore, the proposed changes will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated because no new accident scenario is created and no 
    previously evaluated accident scenario is changed by the relocation 
    of the procedural details of RETS from one controlled document to 
    another.
        3. Does the proposed amendment involve a significant reduction 
    in the margin of safety?
        The proposed change does not include a change to any plant 
    structure, system, component, or operation. The proposed changes do 
    not alter the basic regulatory requirements and do not affect any 
    safety analyses. The proposed change is administrative. The 
    procedural details of the current RETS are relocated while the 
    programmatic controls consistent with regulatory requirements, 
    including controls on revisions to the manuals receiving the RETS 
    procedural details, the Environmental Manual (EM), Radiological 
    Effluent Control Program Manual (RECM), Offsite Dose Calculation 
    Manual (ODCM), and Process Control Program (PCP), remain in RETS.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Gail H. Marcus
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Power Plant, Unit Nos. 1 and 2, Town of Two 
    Creeks, Manitowoc County, Wisconsin
    
        Date of amendment request: April 29, 1996
        Description of amendment request: The proposed amendments would 
    revise Technical Specification (TS) Section 15.3.14, ``Fire Protection 
    System,'' and Section 15.4.15, ``Fire Protection System.'' These 
    specifications would be relocated to other licensee-controlled 
    documents in accordance with Nuclear Regulatory Commission generic 
    guidance. Additional administrative changes consistent with the 
    relocation are also proposed.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. Operation of this facility under the proposed Technical 
    Specifications change will not increase the probability or 
    consequences of an accident previously evaluated.
        This change request proposes to remove certain fire protection 
    program requirements from the Point Beach Technical Specifications 
    and incorporate them into the Final Safety Analysis Report (FSAR) 
    and the Fire Protection Evaluation Report (FPER). No requirements 
    are eliminated, modified, or de-emphasized by this change. The 
    proposed amendment ensures that any future changes to the fire 
    protection program will be subject to an appropriate evaluation in 
    accordance with NRC regulations to ensure that there are no 
    unreviewed safety questions.
        Therefore, these proposed changes are administrative in nature. 
    There are no proposed changes to the physical plant or the processes 
    which ensure the plant's capability to mitigate fires and achieve 
    safe shutdown. Therefore, there is no potential effect on the 
    probability or consequences of previously evaluated accidents.
        2. Operation of this facility under the proposed Technical 
    Specifications change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        New or different accidents can only be created by new or 
    different accident initiators or sequences. Because there are no 
    proposed changes to the physical plant or the processes which ensure 
    the plant's fire protection capability, new or different kinds of 
    accident initiators will not be introduced by this change. The 
    proposed changes are administrative in nature.
        3. Operation of this facility under the proposed Technical 
    Specifications change will not create a significant reduction in a 
    margin of safety.
        The margins of safety for Point Beach are based on the design 
    and operation of the reactor and containment and the safety systems 
    that provide their protection. Because there are no proposed changes 
    to the physical plant or the processes which ensure the plant's fire 
    protection capability, there will be no effect on the reactor, 
    reactor containment, or the safety systems which provide their 
    protection. Therefore, the proposed changes will not create a 
    reduction in a margin of safety. The proposed changes are 
    administrative in nature.
        Additionally, the proposed revision to Point Beach's operating 
    license will not allow Wisconsin Electric to make changes to the 
    approved fire protection program without prior approval of the 
    Nuclear Regulatory Commission should these proposed changes 
    adversely affect the ability to achieve and maintain safe shutdown 
    in the event of a fire. In accordance with NRC Generic Letter 86-10, 
    any proposed change to the approved fire protection program requires 
    the performance of a 10 CFR 50.59 evaluation and a fire hazards 
    analysis. Should these evaluations indicate that the ability to 
    reach and maintain safe shutdown has been adversely affected, prior 
    NRC review and approval will be obtained prior to effecting the 
    changes. Thus, a significant reduction in a margin of safety cannot 
    occur.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Joseph P. Mann Library, 1516
    
    [[Page 28622]]
    
    Sixteenth Street, Two Rivers, Wisconsin 54241
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Gail H. Marcus
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: May 16, 1996. This supersedes the 
    October 24, 1995, request published in the Federal Register on November 
    27, 1995 (60 FR 58409).
        Description of amendment request: This license amendment request 
    proposes to revise Surveillance Requirement 4.7.6.e.4 to reflect a 
    proposed design change to the output rating, from 15kW to 5kW, of the 
    charcoal filter adsorber unit heater in the pressurization system 
    portion of the control room emergency ventilation system (CREVS). 
    Surveillance Requirements 4.7.6.c.2, 4.7.6.d, and 4.9.13.b and c, are 
    also being revised to reflect a proposed change to the acceptance 
    criteria for the testing of carbon samples from the CREVS charcoal 
    adsorbers and the auxiliary/fuel building emergency exhaust system 
    charcoal adsorbers. Surveillance Requirement 4.7.7.a for the auxiliary 
    building portion of the auxiliary/fuel building emergency exhaust 
    system is also affected by this proposed change. However, since 
    Surveillance Requirement 4.7.7.a refers to Surveillance Requirements 
    4.9.13.b and c, no changes to 4.7.7.a are required.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The design function of the filter adsorber unit heater in the 
    pressurization system portion of CREVS is to reduce the relative 
    humidity of the air entering the charcoal filter beds to 70% 
    relative humidity. Although the original design specified a heater 
    with a rating of 15 kW, review of the design basis calculation for 
    this system indicates that only about 3.13 kW is actually required 
    (including applicable margins to allow for voltage variations). The 
    proposed change to the CREVS heaters output rating from 15 kW to 5 
    kW will not affect the method of operation of the system, and the 
    new heater capacity will still exceed filter operational 
    requirements and safety margin. Neither the heater change nor the 
    charcoal testing protocol changes will affect system operation or 
    performance, nor do they affect the probability of any event 
    initiators. These changes do not affect any Engineered Safety 
    Features actuation setpoints or accident mitigation capabilities. 
    Therefore, the proposed changes will not significantly increase the 
    consequences of an accident or malfunction of equipment important to 
    safety previously evaluated in the USAR [Updated Safety Analysis 
    Report].
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The requested change to the CREVS heaters' output rating and the 
    changes to the charcoal sample testing protocol will not affect the 
    method of operation of the systems, and the new heater capacity will 
    still exceed filter operational requirements and safety margin by a 
    significant amount. The proposed changes only affect the heater size 
    in the system and the testing criteria for the charcoal samples. No 
    new or different accident scenarios, transient precursors, failure 
    mechanisms, or limiting single failures will be introduced as a 
    result of these changes. Therefore, the possibility of a new or 
    different kind of accident other than those already evaluated will 
    not be created by this change.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The requested change to the CREVS heaters' output rating will 
    reduce the heater output of the system, but the new heater output 
    will still exceed filter operational requirements and safety margin 
    by a significant amount. In addition, the reduction in heat load 
    output from the heater will increase the design margin between the 
    cooling capacity of the system air conditioning units and the 
    building heat load. The new charcoal adsorber sample laboratory 
    testing protocol is more stringent than the current testing practice 
    and more accurately demonstrates the required performance of the 
    adsorbers following a design basis LOCA [loss-of-coolant accident]. 
    Therefore, these changes will not reduce the margin of safety of the 
    HVAC [heating, ventilation, and air conditioning] systems' 
    operation.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: January 12, 1996, as 
    supplemented March 4, April 3 and April 10, 1996.
        Brief description of amendments: The amendments revise the 
    Technical Specification so that the containment integrated leak rate 
    Type A testing will now be performed consistent with the revised 10 CFR 
    Part 50, Appendix J, Option B, by referring to Regulatory Guide 1.163, 
    ``Performance-Based Containment Leak-Test Program.'' No
    
    [[Page 28623]]
    
    changes to implement Option B for the Type B and Type C tests were 
    requested by the licensee at this time.
        Date of issuance: May 13, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 144 and 138
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 21, 1996 (61 FR 
    3498); and April 10, 1996 (61 FR 15988) The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    May 13, 1996.No significant hazards consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: March 5, 1996
        Brief description of amendments: These amendments delete the 
    requirement to perform a pressurizer heater surveillance test and 
    change the requirement for containment visual inspection to prevent 
    sump clogging. These changes are in accordance with selected line items 
    from NRC Generic Letter 93-05, ``Line-Item Technical Specification 
    Improvements to Reduce Surveillance Requirements for Testing During 
    Power Operation.''
        Date of issuance: May 13, 1996
        Effective date: May 13, 1996
        Amendment Nos. 184 and 178Facility Operating Licenses Nos. DPR-31 
    and DPR-41: Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: April 10, 1996 (61 
    FR15989) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 13, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498, South Texas Project, Unit 1, Matagorda County, 
    Texas
    
        Date of amendment request: January 22, 1996, as supplemented by 
    letter dated April 18, 1996.
        Brief description of amendment: The amendment modified the steam 
    generator tube plugging criteria in Technical Specification 3/4.4.5, 
    Steam Generators, and the associated Bases, to allow the implementation 
    of alternate steam generator tube plugging criteria for the tube-to-
    tubesheet joints (known in the industry as F*) for Unit 1.
        Date of issuance: May 14, 1996Effective date: May 14, 1996
        Amendment No.: 82
        Facility Operating License No. NPF-76: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 28, 1996 (61 
    FR 7553) The additional information contained in the supplemental 
    letter dated April 18, 1996, was clarifying in nature and thus, within 
    the scope of the initial notice and did not affect the staff's proposed 
    no significant hazards consideration determination.The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated May 14, 1996. No significant hazards consideration 
    comments received: No
        Local Public Document Room location:  Wharton County Junior 
    College, J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 
    77488
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. 
    Ginna Nuclear Power Plant, Wayne County, New York
    
        Date of application for amendment: February 9, 1996, as 
    supplementedMarch 15, 1996, and April 22, 1996.
        Brief description of amendment: The amendment revised the 
    Administrative Controls Section 5.6.6 of the Ginna Technical 
    Specifications to incorporate a reference to the methodology for 
    determining pressure/temperature and low-temperature overpressure 
    protection limits.
        Date of issuance: May 23, 1996
        Effective date: May 23, 1996
        Amendment No.: 64
        Facility Operating License No. DPR-18: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 28, 1996 (61 
    FR 7557) The March 15, 1996, and April 22, 1996, letters provided 
    clarifying information that did not change the initial proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated May 23, 1996.No significant hazards consideration comments 
    received: No
        Local Public Document Room location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610.
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. 
    Ginna Nuclear Power Plant, Wayne County, New York
    
        Date of application for amendment: February 9, 1996
        Brief description of amendment: This amendment changes the 
    setpoints for the steam generator water level-high feedwater isolation 
    function.Date of issuance: May 20, 1996
        Effective date: May 20, 1996
        Amendment No.: 63
        Facility Operating License No. DPR-18: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 28, 1996 (61 
    FR 7558) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 20, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610.
    
    Saxton Nuclear Experimental Corporation (SNEC), Docket No. 50-146, 
    Saxton Nuclear Reactor Facility (SNEF)
    
        Date of application for amendment: November 21, 1995, as 
    supplemented on March 13, 1996.
        Brief description of amendment: The amendment adds GPU Nuclear 
    Corporation as a licensee for the SNEF along with SNEC and transfers 
    all management-related responsibilities for the SNEF from SNEC to GPU 
    Nuclear Corporation.
        Date of issuance: May 10, 1996
        Effective date: May 10, 1996
        Amendment No.: 13Amended Facility License No. DPR-4: Amendment 
    changed the Technical Specifications.
        Date of initial notice in Federal Register: January 31, 1996 (61 FR 
    3502). The Commission also published a notice of consideration of 
    transfer of control of license pursuant to 10 CFR 50.80 on March 19, 
    1996 (61 FR 11231). The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated May 10, 1996.o 
    significant hazards consideration comments received: No
        Local Public Document Room Location: Saxton Community Library, 911 
    Church Street, Saxton, Pennsylvania 16678
    
    [[Page 28624]]
    
    South Carolina Electric & Gas Company, South Carolina Public 
    Service Authority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of application for amendment: December 8, 1995
        Brief description of amendment: The amendment revises the Technical 
    Specifications (TS) to: 1) add a new surveillance requirement to 
    4.1.2.2, 2) delete 3.1.2.3 and 3.1.2.4, revise 3.4.9.3 to assure that 
    only one charging pump is capable of injecting water into the primary 
    coolant whenthe reactor is in a shutdown mode, 4) add a new 
    surveillance requirement to 4.4.9.3, 5) revise the Emergency Core 
    Cooling Water System pump testing acceptance criteria, and 6) revise 
    the BASES supporting the above changes.
        Date of issuance: May 10, 1996
        Effective date: 30 days after issuance
        Amendment No.: 134
        Facility Operating License No. NPF-12: Amendment revises the TS.
        Date of initial notice in Federal Register: January 22, 1996 (61 FR 
    1635) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated May 10, 1996.No significant hazards 
    consideration comments received: No
        Local Public Document Room location:  Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 
    50-364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston 
    County, Alabama.
    
        Date of amendments request: December 19, 1995, as supplemented by 
    letters dated January 5, 1996 and May 3, 1996.
        Brief description of amendments: The amendments replace the 
    requirements associated with the control room emergency ventilation 
    system contained in Technical Specification Section 3/4.7.7 with 
    requirements related to the operation of the control room emergency 
    filtration/pressurization system and the control room air conditioning 
    system. In addition, a one-time extension to the allowable outage time 
    for the control room recirculation filtration system is included to 
    facilitate implementation of design modifications.
        Date of issuance: May 21, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 119 and 111
        Facility Operating License Nos. NPF-2 and NPF-8. Amendments revise 
    the Technical Specifications.
        Date of initial notice in Federal Register: January 22, 1996 (61 FR 
    1637) The January 5, 1996 and May 3, 1996 letters provided clarifying 
    information that did not change the scope of the December 19, 1995, 
    application and initial proposed no significant hazards consideration 
    determination. The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated May 21, 1996.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302
    
    Southern Nuclear Operating Company, Inc., Docket No. 50-364, Joseph 
    M. Farley Nuclear Plant, Unit 2, Houston County, Alabama
    
        Date of amendment request: April 23, 1996
        Brief description of amendment: The amendment would allow steam 
    generator tubes to remain in service with bands of axial degradation in 
    the tube sheet region, for the remainder of Cycle 11, provided 
    sufficient undegraded tubing remains to satisfy the L*-type 
    criteria restrictions established by the licensee.
        Date of issuance: May 20, 1996
        Effective date: May 20, 1996
        Amendment No.: 110
        Facility Operating License No. NPF-8. The amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: Yes (61 FR 19092). The notice 
    provided an opportunity to submit comments on the Commission's proposed 
    no significant hazards consideration determination. No comments have 
    been received. The notice also provided for an opportunity to request a 
    hearing by May 30, 1996, but indicated that if the Commission makes a 
    final no significant hazards consideration determination, any such 
    hearing would take place after issuance of the amendment.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, and final determination of no significant 
    hazards consideration are contained in a Safety Evaluation dated May 
    20, 1996.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an
    
    [[Page 28625]]
    
    opportunity for public comment. If comments have been requested, it is 
    so stated. In either event, the State has been consulted by telephone 
    whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By July 5, 1996, the licensee 
    may file a request for a hearing with respect to issuance of the 
    amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order. As required by 10 CFR 2.714, a petition for leave 
    to intervene shall set forth with particularity the interest of the 
    petitioner in the proceeding, and how that interest may be affected by 
    the results of the proceeding. The petition should specifically explain 
    the reasons why intervention should be permitted with particular 
    reference to the following factors: (1) the nature of the petitioner's 
    right under the Act to be made a party to the proceeding; (2) the 
    nature and extent of the petitioner's property, financial, or other 
    interest in the proceeding; and (3) the possible effect of any order 
    which may be entered in the proceeding on the petitioner's interest. 
    The petition should also identify the specific aspect(s) of the subject 
    matter of the proceeding as to which petitioner wishes to intervene. 
    Any person who has filed a petition for leave to intervene or who has 
    been admitted as a party may amend the petition without requesting 
    leave of the Board up to 15 days prior to the first prehearing 
    conference scheduled in the proceeding, but such an amended petition 
    must satisfy the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-001, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555-001, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    [[Page 28626]]
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units Nos. 1, 2, and 3, Maricopa County, Arizona
    
        Date of application for amendments: May 15, 1996
        Brief description of amendments: The amendment revised Surveillance 
    Requirement (SR) 4.5.2.d.2 in Technical Specification 3/4 5.2 to state 
    that the trisodium phosphate (TSP) contained in the storage baskets in 
    containment is in the form of anhydrous TSP, rather than dodecahydrate 
    TSP, as currently specified.
        Date of issuance: May 15, 1996
        Effective date: May 15, 1996
        Amendment Nos.: Unit 1 - 107; Unit 2 - 99; Unit 3 - 79
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendment revised the Technical Specifications.Public comments 
    requested as to proposed no significant hazards consideration: No.The 
    Commission's related evaluation of the amendments, finding of emergency 
    circumstances, and final determination of no significant hazards 
    consideration are contained in a Safety Evaluation dated May 15, 1996.
        Local Public Document Room location: Phoenix Public Library, 1221 
    N. Central Avenue, Phoenix, Arizona 85004
        Attorney for licensee: Nancy C. Loftin, Esq., Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999
        NRC Project Director: William H. Bateman
        Dated at Rockville, Maryland, this 29th day of May 1996.
        For the Nuclear Regulatory Commission
    Steven A. Varga,
    Director, Division of Reactor Projects - I/II, Office of Nuclear 
    Reactor Regulation
    [Doc. 96-13878 Filed 6-4-96; 8:45 am]
    BILLING CODE 7590-01-9
    
    

Document Information

Published:
06/05/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X96-10605
Dates:
As of the date of issuance to be implemented within 30 days
Pages:
28604-28626 (23 pages)
PDF File:
x96-10605.pdf