X97-10716. Biweekly Notice  

  • [Federal Register Volume 62, Number 136 (Wednesday, July 16, 1997)]
    [Notices]
    [Pages 38130-38146]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X97-10716]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any
    
    [[Page 38131]]
    
    amendments issued, or proposed to be issued, under a new provision of 
    section 189 of the Act. This provision grants the Commission the 
    authority to issue and make immediately effective any amendment to an 
    operating license upon a determination by the Commission that such 
    amendment involves no significant hazards consideration, 
    notwithstanding the pendency before the Commission of a request for a 
    hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from June 23, 1997, through July 3, 1997. The 
    last biweekly notice was published on July 2, 1997 (62 FR 35846).
    
    Notice Of Consideration of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Harards Consideration 
    Determination, And Opportunith For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By August 15, 1997, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no
    
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    significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of amendment request: May 30, 1997, identified as CY-97-006
        Description of amendment request: Changes to the Operating License, 
    DPR-61, and facility Technical Specifications (TS) that reflect the 
    permanently shut down and defueled status of the plant.
        CY-97-006 contains the proposed changes to the license conditions 
    in DPR-61 on Fire Protection, Power Level and Fuel Movement; and 
    submittal of a new set of TS referred to by the licensee as the 
    Defueled TS (DTS). The DTS contain a revised Definitions section, 
    removal of the sections on Safety Limits and Limiting Safety System 
    Settings, Limiting Conditions for Operation and Surveillance 
    Requirements were modified extensively, the Design Features section was 
    revised, and the Administrative Controls section was modified to 
    reflect all the preceding changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Connecticut Yankee Atomic Power Company (CYAPCO) has reviewed 
    the proposed changes to the Operating License and the Technical 
    Specifications in accordance with 10 CFR 50.92 and concluded that 
    the changes do not involve a significant hazards consideration 
    (SHC). The basis for this conclusion is that the three criteria of 
    10 CFR 50.92(c) are not compromised. The proposed changes do not 
    involve an SHC because the changes would not:1. Involve a 
    significant increase in the probability of consequences of an 
    accident previously evaluated.
        Because of the present plant configuration, many of the 
    postulated accidents previously evaluated (i.e., loss or coolant 
    accident, main steam line break, etc.) are no longer possible. The 
    accidents previously evaluated that are still applicable to the 
    plant are fuel handling accidents and gaseous and liquid radioactive 
    releases.
        There is no significant increase in the probability of a fuel 
    handling accident since refueling operations have ceased. In fact, 
    there is more likely a decrease in probability of a fuel handling 
    accident since the need to move/rearrange fuel assemblies is minimal 
    until they are removed from the spent fuel pool (i.e., for dry cask 
    storage or for transferring to U.S. Department of Energy 
    possession).
        The radiological consequences of a gaseous or liquid radioactive 
    release are bounded by the fuel handling accident. With the plant 
    defueled and permanently shutdown, the demands on the radwaste 
    systems is lessened since no new radioisotopes are being generated 
    by irradiation or fission. Therefore, there is no increase in the 
    probability or consequences of a gaseous or liquid radioactive 
    release.
        The changes to the Operating License reflect the permanently 
    defueled condition for power level and fuel movement restrictions 
    and the fire protection regulation which is applicable for a 
    permanently defueled plant.
        With respect to the Service Water System (Specification 3/
    4.7.3), Electrical Power Systems (Specification 3/4.8) and spent 
    fuel pool makeup, the basis for placing appropriate requirements in 
    the Technical Requirements Manual is due to the reduced heat load in 
    the spent fuel pool.
        The plant was shutdown on July 22, 1996 and more than 280 days 
    have passed since the shutdown, thus the heat load on the spent fuel 
    pool cooling system is greatly reduced. Present cooling performance 
    data as well as calculations demonstrate that either the plate or 
    the shell and tube heat exchanger has more than adequate heat 
    removal capacity. In the event of a loss of forced cooling, 
    calculations indicate that the spent fuel pool time to boil is 
    greater than 40 hours based on an initial pool temperature of 
    150 deg.F. The initial pool temperature of 150 deg.F is based on 
    Technical Specification 3/4.9.15 which has a pool temperature limit 
    of 150 deg.F. Even during boiling, the fuel is adequately cooled. 
    Once boiling commences, the operators have in excess of 18 days to 
    provide forced cooling and/or makeup before there is inadequate 
    shielding provided by the water in the pool. This allows sufficient 
    time to provide for alternate forced cooling or makeup to the spent 
    fuel pool in the event of a service water system failure. Therefore, 
    operability of spent fuel pool cooling does not require service 
    water, electrical power, or makeup water to be immediately 
    available.
        Should failure to restore operation of the spent fuel pool 
    cooling system occur before boiling takes place, cooling of the 
    spent fuel can be accomplished by allowing the spent fuel pool to 
    boil and adding makeup water at a rate equal to or greater than the 
    boil-off rate.
        CYAPCO has in place procedures to establish onsite power in the 
    event of a Loss of Normal Power (LNP) and in the event of a loss of 
    cooling to the Spent Fuel Pool. For a LNP, power can be made 
    available within approximately one hour. If onsite power cannot be 
    reestablished, due to equipment failure, at approximately 2 hours 
    into the LNP, limited makeup water could be provided by gravity feed 
    from a tank (available in approximately 30 minutes) or an unlimited 
    supply of water could be provided via the diesel fire pump from the 
    Connecticut River (available in approximately 30 minutes). 
    Therefore, within approximately 2 1/2 hours of the event start, 
    cooling and/or makeup would be reestablished to the spent fuel pool. 
    Historically, the longest LNP the HNP has experienced has been less 
    than 30 minutes.
        The changes to Technical Specification 3.3.3.8, ``Radioactive 
    Gaseous Effluent Monitoring Instrumentation'' and Table 3.3.-10 
    delete the trip function from the main stack noble gas activity 
    monitor. The changes to Technical Specifications 3.11.2.1, Dose 
    Rate, and 3.11.2.3, Dose, delete the requirement to include the 
    radioiodine isotopes in the dose calculations. These changes are 
    based on the following:
        There is no significant increase in the consequences of a fuel 
    handling accident since the accident scenarios assume an assembly 
    with significant amounts of radioactive iodine or noble gas. The 
    plant was shutdown on July 22, 1996. Except for I-125 (half-life 
    =59.5 days), I-129 (half-life = 1.6E7 years), and Kr-85 (half-life 
    =10.8 years), the spent fuel inventory of the dose contributing 
    radioactive iodine and noble gas isotopes has decayed more than 20 
    half-lives since shutdown (i.e., less than 0.0001% of the original 
    amount remains). In addition, the definition for ``Dose Equivalent 
    I-131'' (Standard Technical Specifications, Westinghouse 
    Plants,'' NUREG-1431) does not include I-125 and I-129 in the dose 
    assessment due to their negligible inventory in the spent fuel. 
    Except for Kr-85, the other noble gas nuclides that contribute to a 
    whole
    
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    body dose have also decayed to a negligible amount. CYAPCO has 
    performed fuel handling and cask drop accident dose calculations 
    which conclude that doses (i.e., whole body and thyroid) at the 
    Exclusion Area Boundary are a small fraction of the 1O CFR 100 dose 
    limits and the EPA PAGS. In fact, due to this decreased radioactive 
    inventory, there is a significant decrease in the consequences of a 
    fuel handling accident.
        Based on the above, the proposed changes to the Operating 
    License and the Technical Specifications do not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        There is no change in how spent fuel is stored or moved in the 
    spent fuel pool. Therefore, the postulated fuel handling accidents 
    are still bounding and are still considered as credible postulated 
    accidents. The bases provided in the CYAPCO analysis of previously 
    evaluated accidents in Section 1, above, also applies to the 
    possibility of new or different accidents herein.
        Based on the analysis in Section 1, above, the changes to 
    Technical Specification related to radioactive iodine and noble gas 
    isotopes do not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        Based on these considerations, the proposed changes to the 
    Operating License and the Technical Specifications do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        With respect to the Service Water System (Specification 3/
    4.7.3), Electrical Power Systems (Specification 3/4.8) and spent 
    fuel pool makeup, the basis for placing appropriate requirements in 
    the Technical Requirements Manual is due to the reduced heat load in 
    the spent fuel pool.
        The Technical Specification basis states that the time to spent 
    fuel pool boiling after a loss of forced cooling following a full 
    core offload is 7 hours.
        In accordance with the analysis set forth above under No. 1, 
    there is no change in how spent fuel is stored or moved in the spent 
    fuel pool.
        Based on the above, the proposed changes to the Operating 
    License and the Technical Specifications do not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270
        NRC Project Director: Marvin M. Mendonca, Acting Director
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of amendment request: May 30, 1997, identified as CY-97-024
        Description of amendment request: CY-97-024 provided the proposed 
    technical specifications (TS) needed to implement the Certified Fuel 
    Handler (CFH) program at the plant. This new position will replace the 
    former licensed operator positions. A copy of the CFH Training Program, 
    ``Nuclear Training Manual NTM-7.083'' was enclosed with the license 
    amendment request for NRC review and approval. However, this manual 
    will be reviewed separately from the proposed TS changes and when the 
    NRC review of the manual is completed a letter of approval will be sent 
    to the licensee.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Connecticut Yankee Atomic Power Company (CYAPCO) has reviewed 
    the proposed changes to the Technical Specifications in accordance 
    with 10 CFR 50.92 and concluded that the changes do not involve a 
    significant hazards consideration (SHC). The basis for this 
    conclusion is that the three criteria of 10 CFR 50.92(c) are not 
    compromised. The proposed changes do not involve an SHC because the 
    changes would not.
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed qualification, staffing and training requirements 
    are appropriate for the present plant conditions.
        The plant has permanently ceased operations, the reactor has 
    been permanently defueled, and the spent fuel stored in the spent 
    fuel pool.
        Because the present plant conditions, many of the postulated 
    accidents previously evaluated (i.e., loss-of-coolant accident, main 
    steam line break, etc.) are no longer possible. The accidents 
    previously evaluated that are still applicable to the plant are fuel 
    handling accidents and gaseous and liquid radioactive releases.
        There is no significant increase in the probability of a fuel 
    handling accident since refueling operations have ceased. In fact, 
    there is more likely a decrease in probability of a fuel handling 
    accident since the need to move/rearrange fuel assemblies is minimal 
    until they are removed from the spent fuel pool (i.e., for dry cask 
    storage or for transferring to U.S. Department of Energy 
    possession).
        There is no significant increase in the consequences of a fuel 
    handling accident since the accident scenarios assume an assembly 
    with significant amounts of radioactive iodine or noble gas. The 
    plant was shutdown on July 22, 1996. Except for I-125 (half-
    life=59.5 days), I-129 (half-life=1.6E7 years), and Kr-85 (half-
    life-10.8 years), the spent fuel inventory of the dose-contributing 
    radioactive iodine and noble gas isotopes has decayed more than 20 
    half-lives since shutdown (i.e., less than 0.0001% of the original 
    amount remains). In addition, the definition for ``Dose Equivalent 
    I-131'' (Standard Technical Specifications, Westinghouse 
    Plants,'' NUREG-1431) does not include I-125 and I-129 in the dose 
    assessment due to their negligible spent fuel inventory. Except for 
    Kr-85, the other noble gas nuclides that contribute to a whole body 
    dose have also decayed to a negligible amount. CYAPCO has performed 
    fuel handling and cask drop accident dose calculations which 
    conclude that doses (i.e., whole body and thyroid) at the Exclusion 
    Area Boundary and the Low Population Zone are a small fraction of 
    the 10 CFR 100 dose limits. In fact, due to this decreased 
    radioactive inventory, there is a significant decrease in the 
    consequences of a fuel handling accident.
        The radiological consequences of a gaseous or liquid radioactive 
    release are bounded by the fuel handling accident. With the plant 
    defueled and permanently shutdown, the demands on the radwaste 
    systems are lessened since no new radioisotopes are being generated 
    by irradiation. Therefore, there is no increase in the consequences 
    of a gaseous or liquid radioactive release.
        Based on the above, the proposed changes to the Technical 
    Specifications do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        There is no change in how spent fuel is stored or moved in the 
    spent fuel pool. Therefore, the postulated fuel handling accidents 
    are still bounding and are still considered as credible postulated 
    accidents.
        Based on the above, the proposed changes to the Technical 
    Specifications do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        There is no change in how spent fuel is stored or moved in the 
    spent fuel pool.
        The plant was shutdown on July 22, 1996. Except for I-125 (half-
    life=59.5 days), I-129 (half-life=1.6E7 years), and Kr-85 (Half-
    life=10.8 years), the spent fuel inventory of the dose-contributing 
    radioactive iodine and noble gas isotopes has decayed more than 20 
    half-lives since shutdown (i.e., less than 0.0001% of the original 
    amount remains). Except for Kr-85, the other noble gas nuclides that 
    contribute to a whole body dose have also decayed to a negligible 
    amount. CYAPCO has performed fuel handling and cask drop accident 
    dose calculations which conclude that doses (i.e, whole body and
    
    [[Page 38134]]
    
    thyroid) at the Exclusion Area Boundary and the Low Population Zone 
    are a small fraction of the 10 CFR 100 dose limits.
        Therefore, there is no significant reduction the margin of 
    safety. In fact, due to this decreased radioactive iodine inventory, 
    there is more likely an increase in the margin of safety.
        Based on the above, the proposed changes to the Technical 
    Specifications do not involve a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270
        NRC Project Director: Marvin M. Mendonca
    
    Detroit Edison Company, Docket No. 50-341, Fermi-2, Monroe County, 
    Michigan
    
        Date of amendment request: June 20, 1997 (NRC-97-0037), as 
    supplemented by letter dated July 3, 1997
        Description of amendment request: The proposed amendment would 
    relocate technical specification surveillance requirement 4.4.1.1.2 for 
    the reactor recirculation system motor-generator (MG) set scoop tube 
    stop setpoints to the Updated Final Safety Analysis Report. In 
    addition, the proposed amendment includes the following changes to the 
    surveillance testing methodology: (1) eliminating any licensing basis 
    requirement for the electrical stops, and (2) revising the periodicity 
    from a calendar basis to a situational basis (i.e., plant conditions 
    that would dictate a change in stop positions).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed change removes from the Fermi 2 Technical 
    Specifications (TS) a Surveillance Requirement (SR 4.4.1.1.2) that 
    is an implementation detail and relocates it to the Updated Final 
    Safety Analysis Report (UFSAR), where it is more adequately and more 
    appropriately controlled in accordance with 10 CFR 50.59. In 
    addition, this proposed change revises the test methodology by: (1) 
    eliminating the requirement for the electrical stops because they 
    are not credited for mitigating any transients or accidents, and (2) 
    revising the periodicity from a calendar basis to a situational 
    basis to coincide with the beginning of each operating cycle or 
    post-maintenance. These changes do not eliminate the necessary 
    testing of the MG set mechanical stops. The MG set mechanical stops 
    will continue to remain operable because the recirculation pump MG 
    set mechanical speed stop settings will continue to be maintained at 
    or below the required limits. The MCPRf [minimum critical 
    power ratio] and MAPLHGRf [maximum average planar linear 
    heat-generation rate] limits, along with the recirculation pump MG 
    set mechanical speed stop settings on which they are based, are 
    specified in the Core Operating Limits Report and operation within 
    these limits is required by Technical Specifications 3.2.1 and 
    3.2.3. The changes described will therefore have no impact on the 
    probability or consequences of an accident previously evaluated.
        2. The changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed Technical Specification change does not result in 
    any changes to the design (equipment/configuration) or operation of 
    the plant and will thus not create a new failure mode or common mode 
    failure. The MG set mechanical stops will continue to operate as 
    intended and as designed. These changes will therefore not create 
    the possibility of a new or different kind of accident, from any 
    accident previously evaluated.
        3. The changes do not involve a significant reduction in the 
    margin of safety.
        Changes in the methodology and frequency of testing will not 
    involve a significant reduction in the margin of safety because the 
    testing necessary to ensure the stops are set correctly will 
    continue to be performed. Additionally, the MCPRf and 
    MAPLHGRf limits, along with the recirculation pump MG set 
    mechanical speed stop setting that they are based on, are specified 
    in the Core Operating Limits Report, and operation within these 
    limits is still required by Technical Specifications 3.2.1 and 
    3.2.3. Therefore, the margin of safety as defined in the bases of 
    any Technical Specification is not reduced by relocating the 
    surveillance requirement from the TS to the UFSAR. In addition to 
    the above, relocation of the TS is consistent with the BWR Improved 
    Standard Technical Specification, NUREG-1433, Rev. 1.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161
        Attorney for licensee: John Flynn, Esq., Detroit Edison Company, 
    2000 Second Avenue, Detroit, Michigan 48226
        NRC Project Director: John N. Hannon
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, 
    Unit No. 2, Pope County, Arkansas
    
        Date of amendment request: April 24, 1997
        Description of amendment request: The requested amendment revises 
    the inservice inspection requirements associated with steam generator 
    tube sleeves.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does Not Involve a Significant Increase in the Probability or 
    Consequences of an Accident Previously Evaluated.
        This change implements a more stringent surveillance requirement 
    than currently exists. It incorporates a requirement to inspect a 
    minimum of 20% of each type of installed sleeve in each steam 
    generator. The 20% inspection criterion is conservative with respect 
    to the existing requirement of a 3% initial inspection of all steam 
    generator tubes. Additionally, since the process for inspections has 
    not changed, the probability or consequences of accidents previously 
    analyzed are not increased as a result of inspection activities. The 
    proposed changes have no impact on any previously analyzed accident 
    in the safety analysis report.
        The administrative changes made to update the technical 
    specifications or to correct inconsistencies introduced in previous 
    amendments do not affect reactor operations or accidental analyses 
    and have no radiological consequences.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        2. Does Not Create the Possibility of a New or Different Kind of 
    Accident from any Previously Evaluated.
        The changes made to increase the initial sample of sleeved tubes 
    inspected during a surveillance, to update the technical 
    specifications and to correct inconsistencies introduced in previous 
    amendments are administrative and do not change the design, 
    configuration or method of operation of the plant nor does it 
    introduce any new possibility for an accident.
        Therefore, this change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        3. Does Not Involve a Significant Reduction in the Margin of 
    Safety.
        As previously discussed, this change implements a more stringent 
    surveillance requirement than currently exists. The existing 
    technical specifications require an initial inspection of 3% of the 
    tubes in each steam generator while the proposed change
    
    [[Page 38135]]
    
    requires inspection of a minimum of 20% of each type of installed 
    sleeve. The 20% inspection criterion is conservative with respect to 
    the existing technical specification. Existing technical 
    specification operability and surveillance requirements are not 
    reduced by the proposed change, thus no margins of safety are 
    reduced.
        The other administrative changes do not reduce technical 
    specification operability and surveillance requirements, and 
    therefore, do not reduce any margin of safety.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: June 26, 1997
        Description of amendment request: The proposed amendment will 
    modify Technical Specification (TS) Tables 3.7-1 and 3.7-2. Table 3.7-1 
    will be revised to change the Main Steam Safety Valves (MSSVs) orifice 
    size from 26 square inches to 28.27 square inches and to relocate the 
    orifice size from the TS Table to the TS Bases. The change to correct 
    the orifice size is an editorial change to make the TS consistent with 
    plant design. Table 3.7-2 will be revised by deleting the provision 
    that allows continued plant operation with three MSSVs inoperable. The 
    proposed amendment will also revise TS Bases 3/4.7.1.1 to remove the 
    equation used for determining the reduced maximum allowable linear 
    power level-high reactor trip settings of TS Table 3.7-2.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: No
        In response to the ABB/CE report pursuant to 10CFR21 regarding 
    the omission of Main Steam Safety Valve (MSSV) piping pressure loss 
    in safety analyses, the proposed change will eliminate the ability 
    to operate the plant in accordance with Technical Specification 
    3.7.1.1 Action a with three MSSVs inoperable. The Bases to this 
    Technical Specification will also be revised to state that the 
    acceptability for operation at lower power levels with one or two 
    MSSVs inoperable will be determined from results obtained from a 
    loss of condenser vacuum accident analysis under these conditions. 
    Deleting the allowance for continued operation with three MSSVs 
    inoperable does not increase the probability of an accident. The 
    consequences of an accident will not be increased by these changes. 
    These changes are more restrictive and ensure that the MSSVs 
    maintain their safety function of removing adequate heat from the 
    steam generator in order to maintain peak steam generator pressure 
    and peak pressurizer pressure well below their respective acceptance 
    criteria during normal operation and all anticipated operational 
    occurrences.
        Changing the MSSVs orifice size listed in TS to their actual 
    size and the orifice size utilized in the safety analysis, and 
    relocating the MSSVs orifice size to the Technical Specification 
    Bases does not affect the probability or consequences of an 
    accident. The correct orifice size was used in the safety analysis 
    and it is not subject to change unless a station modification is 
    performed which will require a 10CFR50.59 evaluation and revision of 
    the safety analysis. The MSSVs orifice size can be adequately 
    controlled in the TS Bases which will also require a 10CFR50.59 to 
    be changed.
        Therefore, operation of Waterford 3 in accordance with this 
    proposed change will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different type of 
    accident from any accident previously evaluated?
        Response: No
        The proposed change will eliminate the ability to operate the 
    plant in compliance with Technical Specification 3.7.1.1 Action a 
    with three MSSVs inoperable. The Bases for this Technical
        Specification will also be revised to state that the 
    acceptability for operation at lower power levels with one or two 
    MSSVs inoperable will be determined from results obtained from a 
    loss of condenser vacuum accident under these conditions. The 
    proposed change also revises the MSSVs orifice size to reflect the 
    actual orifice size and the orifice size utilized in the safety 
    analysis, and relocates the orifice size from Technical 
    Specifications to the Technical Specification Bases. The proposed 
    change does not involve any new equipment, components, or 
    modifications and does not create any new system interactions or 
    connections. Therefore, operation of Waterford 3 in accordance with 
    this proposed change will not create the possibility of a new or 
    different type of accident from any accident previously evaluated.
        3. Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: No
        The proposed change will ensure that all appropriate acceptance 
    criteria for the MSSVs are met during normal operation and all 
    anticipated operational occurrences. The Technical Specification 
    Bases 3/4.7.1.1 will be updated to state that the acceptance 
    criteria for operation in accordance with Technical Specification 
    3.7.1.1 Action a will be determined from the results of the limiting 
    loss of condenser vacuum accident. This change ensures that the 
    transient and dynamic effects which occur during accident scenarios 
    are fully evaluated. These changes also ensure that the MSSVs will 
    maintain peak steam generator pressure and peak pressurizer pressure 
    well below their respective acceptance criteria during normal 
    operation, design basis accidents and anticipated operational 
    occurrences.
        The proposed change also revises the MSSVs orifice size to 
    reflect the actual orifice size and the orifice size utilized in the 
    safety analysis, and relocates the orifice size from Technical 
    Specifications to the Technical Specification Bases. This change 
    corrects an editorial error in the Technical Specifications and 
    relocates unsurveilled design details from the Technical 
    Specifications. Adequate control of the orifice size will remain 
    adequate because any changes to the orifice size or the orifice size 
    listed in the Bases will require a station modification and a TS 
    Bases change. Station Modifications and TS Bases changes requires 
    evaluation in accordance with 10CFR50.59.
        Therefore, operation of Waterford 3 in accordance with this 
    proposed change will not involve a significant reduction in the 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: James W. Clifford, Acting
    
    Northeast Nuclear Energy Company (NNECO), et al., Docket No. 50-
    423, Millstone Nuclear Power Station, Unit No. 3, New London 
    County, Connecticut
    
        Date of amendment request: May 5, 1997
        Description of amendment request: The proposed amendment to 
    Technical Specifications 3.9.1.2 and 3.9.13 and
    
    [[Page 38136]]
    
    their Bases would allow crediting soluble boron for maintaining k-
    effective at less than or equal to 0.95 within the spent fuel pool 
    (SFP) rack matrix following a seismic event of a magnitude greater than 
    or equal to an operating basis earthquake (OBE).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed change in accordance with 
    10CFR50.92 and has concluded that the change does not involve a 
    Significant Hazards Consideration (SHC). The bases for this 
    conclusion is that the three criteria of 10CFR50.92(c) are not 
    satisfied. The proposed change does not involve [an] SHC because the 
    change would not:
        1. Involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        There is one Spent Fuel Pool accident condition discussed in 
    Chapter 15 of the FSAR [Final Safety Analysis Report]. The FSAR 
    discusses a fuel handling accident which drops a fuel assembly onto 
    the fuel racks during fuel movement. Degradation of the Boraflex 
    panels in a post-seismic condition will have no effect on the 
    probability of a fuel assembly drop onto the stored fuel, or the 
    fuel racks. Changing the way Boraflex responds to a seismic event 
    will have no impact on the probability of a seismic event. A 
    misplaced fuel assembly can be postulated in the MP3 [Millstone Unit 
    3] fuel pool as a result of either equipment malfunction or operator 
    error. Degradation of the Boraflex panels will have no effect on the 
    probability of a fuel misplacement event. Therefore, the degradation 
    of Boraflex in a post-seismic condition does not involve an increase 
    in the probability of an accident previously evaluated.
        A fuel handling accident could cause a radioactive release of 
    fission gases, resulting in dose consequences. This radioactive 
    release of fission gases is due to the failure of a certain number 
    of fuel pins which are postulated to fail during the fuel handling 
    accident. The number of fuel pins which are postulated to fail in 
    this event is not affected by the degradation of the Boraflex panels 
    in a post-seismic condition. There are no criticality issues with 
    this fuel handling accident for the reasons described next. Should a 
    fuel handling accident occur prior to a seismic event, the existing 
    fuel handling accident/misloading criticality analysis is still 
    valid, such that 800 ppm [parts per million] of soluble boron is 
    sufficient to ensure that K-effective of the SFP is maintained at 
    less than 0.95. Although overly conservative, should a fuel handling 
    accident occur during or after a seismic event, even with no 
    Boraflex credit, the proposed 1750 ppm of soluble boron is 
    sufficient to ensure that K-effective of the SFP is maintained at 
    less than 0.95. Therefore, this proposed change does not involve an 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequence of an accident previously 
    evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The change in the way Boraflex in conjunction with the addition 
    of 1750 ppm boron responds to a seismic event does not create a new 
    accident. The use of soluble boron in the Spent Fuel Pool is safe 
    during and immediately following a seismic event, because the 
    balance of the equipment in the fuel building not connected to the 
    fuel pool which could cause a dilution (firewater, hot water 
    heating, and demineralized water, CCP [component cooling-plant]) are 
    seismic or mounted in such a fashion as to not direct unborated 
    water into the fuel pool should a line rupture. Non borated water 
    sources that are connected to the SFP will be isolated following a 
    seismic event of greater than or equal to [an] OBE to prevent 
    dilution. Therefore there is no possibility of [an] SFP boron 
    dilution accident coincident with a seismic event, and credit for 
    soluble boron is acceptable to meet the K-effective limit of 0.95 
    for the SFP. The crediting of soluble boron in the Spent Fuel Pool 
    to control K-effective following a seismic event does not create a 
    new accident as boron dilution of the pool can be prevented by 
    closing and administratively controlling the opening of dilution 
    paths to the pool and initiating routine sampling requirements on 
    SFP boron. At present the crediting of soluble boron following a 
    fuel misplacement event is allowed for the Millstone 3 Spent Fuel 
    Pool. Analysis has shown that a seismic event of greater than an OBE 
    level earthquake can be more limiting than a fuel misplacement 
    event. As such the minimum boron requirement in the fuel pool will 
    be increased from 800 ppm to 1750 ppm. As such, no new accident has 
    been created because the crediting of boron following a malfunction/
    accident has always been an allowed event.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The margin of safety, as defined by MP3 Technical 
    Specifications, is to ensure that the K-effective of the MP3 SFP is 
    maintained less than or equal to 0.95 at all times. There is no 
    reduction in the margin of safety as the result of the degradation 
    of Boraflex following a greater than an OBE seismic event, because 
    soluble boron can be used to compensate for the loss of Boraflex. A 
    value of 1750 ppm of soluble boron in the SFP at all times ensures 
    that K-effective of the MP3 SFP is maintained less than or equal to 
    0.95 at all times, including this new malfunction of degraded 
    Boraflex following a greater than an OBE seismic event.
        Eliminating the credit for the negative reactivity effect of 
    Boraflex panels in conjunction with the addition of 1750 ppm boron 
    will have no effect on the probability of a seismic event. As the 
    probability of a seismic event has not changed there is no increase 
    in the probability of an accident or malfunction due to a seismic 
    event. Following a seismic event operators are presently required to 
    make inspections of the plant to determine post seismic event plant 
    conditions. As a result of this change, inspections will be required 
    to post seismic event evaluations to review the status of the Spent 
    Fuel Pool and isolate potential dilution paths. These action are 
    consistent with present guidance in the seismic response procedure 
    and do not create an undue burden on the operator. To compensate for 
    the potential
        loss of Boraflex after a seismic event, the SFP is now required 
    to be borated at all times to 1750 ppm to maintain the proper post 
    seismic [K-effective] condition. As such there is no mitigation 
    equipment that has to operate in the Spent Fuel Pool following a 
    seismic event.
        Although the Boraflex in the fuel racks is assumed to fail in a 
    greater than an OBE seismic event, the presence of soluble boron in 
    the fuel pool water will compensate for the loss of Boraflex. 
    Surveillance requirements on SFP boron will ensure that there will 
    be boron present in the SFP and ensure that the SFP is not diluted 
    below the minimum required boron concentration during normal 
    operation.
        As the presence of SFP soluble boron during and after a seismic 
    event maintains [K-effective] less than 0.95 there is no effect on 
    the consequences of any malfunctions evaluated. As there are no new 
    accidents created and there are no changes in the probability or 
    consequences of previously analyzed accidents there is no effect on 
    the consequences of any accident. There is no reduction in the 
    margin of safety as the result of the degradation of Boraflex 
    following a greater than an OBE seismic event, because soluble boron 
    can be used to compensate for the loss of Boraflex to maintain K-
    effective less than 0.95.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
        In conclusion, bases on the information provided, it is 
    determined that the proposed change does not involve an SHC.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270 NRC Deputy Director: Phillip F. McKee
    
    [[Page 38137]]
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun 
    Station, Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: March 26, 1997
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TS) to incorporate additional 
    restrictions on the operation of the main steam safety valves (MSSVs).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The Omaha Public Power District (OPPD) proposes to revise the 
    Fort Calhoun Station (FCS) Unit No. 1 Technical Specifications (TS) 
    2.1.6, ``Pressurizer and Main Steam Safety Valves,'' to incorporate 
    additional restrictions on the Main Steam Safety Valves (MSSVs) as a 
    result of recent engineering analyses.
        FCS has two Steam Generators (SG), each with one 2 1/2-inch MSSV 
    and four 6-inch MSSVs. The purpose of the MSSVs is to limit the 
    secondary system pressure to less than or equal to 110% of the 
    design pressure of 1000 lbs. per square inch absolute (psia) when 
    passing 100% of design steam flow.
        The pressure drops in the main steam lines were calculated. The 
    total losses (line losses and valve losses) of 30.5 psid (2 1/2 inch 
    valves) and 33.5 psid (6 inch valves) were compared to the valve 
    blowdown which is adjusted/checked each refueling outage as part of 
    the required surveillance test. The pressure losses are less than 
    the 39 psid and 40 psid blowdown for the 2 1/2 inch and 6 inch valve 
    with the lowest setpoint (respectively). Therefore, the 
    recommendation from the Part 21 to review blowdown settings to 
    preclude valve chatter was conducted and there is no concern at FCS. 
    A review of existing calculations for line losses in the primary 
    system was conducted and was determined to be 39 psid for the inlets 
    to the primary safety valves.
        Analyses were then conducted to determine the impact of the 
    total line losses on previously analyzed accidents documented in the 
    Updated Safety Analysis Report (USAR). The scope of the analyses was 
    to evaluate the pressure drops in the piping run for both the 
    primary and MSSVs to determine the impact on the peak primary and 
    secondary system pressures. The applicable transient for peak 
    primary system pressure is the Loss of Load, and for maximum 
    secondary system pressure is the Loss of Feedwater. All analyses 
    were performed using the NRC-approved CESEC-III transient analysis 
    methodology and computer code.
        The assumptions of the analyses were that the plant is operating 
    at 1535.6 MWt, (100% power + 2% uncertainty + reactor coolant pump 
    heat), the MSSVs lifted at +3% of their nominal setpoints, the 
    primary safety valve setpoints were adjusted to account for line 
    losses and lifting at +1% of their setpoints, and the pressure 
    losses in the main steam line to the SG were added to obtain the 
    maximum secondary system pressure within the SG. Additional cases 
    were evaluated with a +6% primary safety valve drift since this 
    possibility is described in the Bases to TS 2.1.6.
        The results from these analyses confirm that the effective 
    increase in MSSV set pressure caused by the piping pressure losses 
    leading to the primary safeties and MSSVs is below the 1100 psia 
    design limit for the secondary system, and below the 2750 psia 
    design limit for the primary system. This is predicated on the fact 
    that only one (1) MSSV may be inoperable per SG.
        Failure of a MSSV is not an initiator of any previously analyzed 
    accident, and therefore the proposed changes do not increase the 
    probability of an accident previously analyzed. The proposed change 
    to revise TS 2.1.6 to allow only one MSSV per SG to be inoperable 
    has been shown, utilizing NRC approved methodology, to
        limit the design pressure to values below the design limits. An 
    administrative change to revise the TS setpoint value for both the 
    primary safety valves and MSSVs from pounds absolute to pounds gauge 
    is proposed to be consistent with the nameplate values of the valves 
    and has no effect on any analyses. Therefore the proposed changes do 
    not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        There will be no physical alterations to the plant 
    configuration, changes in operating modes, setpoints, or testing 
    methods. The additional restrictions being incorporated into the TS 
    on MSSV operation will ensure that the design basis limits of 110% 
    of design pressure will be met for the primary and secondary systems 
    for analyzed accidents when considering inlet pipe pressure drops. 
    The possibility of valve chatter being caused by the additional 
    pressure losses identified in the Main Steam lines and MSSVs was 
    reviewed and is not a concern. This is due to the valve blowdown 
    (the difference between a valve's opening pressure and closing 
    pressure) being greater than the pressure losses. Therefore, the 
    proposed changes do not create the possibility of a new or different 
    kind of accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change results in a peak primary pressure of 2649 
    psia (with 1% primary safety valve drift as allowed by TS 2.1.6) and 
    peak secondary pressure of 1081 psia for the loss of load event 
    compared to 2632 psia and 1075 psia documented in USAR Section 14.9. 
    The proposed change results in a peak primary pressure of 2562 psia 
    and peak secondary pressure of 1090 psia for the loss of feedwater 
    event compared to 2487 psia and 1052 psia documented in USAR Section 
    14.10. The analyses confirm that the primary and secondary systems 
    will continue to be below their respective design limits of 2750 
    psia and 1100 psia. Therefore, the proposed changes do not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102
        Attorney for licensee: Perry D. Robinson, Winston & Strawn, 1400 L 
    Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William H. Bateman
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: May 31, 1996
        Description of amendment request: This change deletes Technical 
    Specification 4.7.2.d.2, ``Control Room Emergency Outside Air Supply 
    System Surveillance Requirement,'' related to the detection of 
    chlorine.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. This proposal does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Review of the various design basis accidents identified in 
    Chapter 15 of the Susquehanna SES [Steam Electric Station] Final 
    Safety Analyses Report (FSAR) concluded that none of these accidents 
    are affected by deletion of the chlorine detection surveillance 
    requirement from Technical Specifications. With the elimination of 
    bulk quantities of gaseous chlorine from use at Susquehanna SES the 
    probability of control room inhabitability due to a gaseous chlorine 
    release has actually decreased. Therefore, this proposed change does 
    not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. This proposal does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed change involves only the deletion of the chlorine 
    detection system Technical Specifications based upon a plant
    
    [[Page 38138]]
    
    modification to remove gaseous chlorine as a biocide from 
    Susquehanna SES and replace it with an oxidizing biocide with non-
    gaseous/non-volatile properties. The release of chlorine from an 
    off-site source is bounded by Reg. [Regulatory] Guide 1.95 in that 
    manual isolation capability for the control room ventilation system 
    is acceptable. Therefore, the proposed change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. This change does not involve a significant reduction in a 
    margin of safety.
        The proposed change would not alter the margins of safety 
    provided in the existing FSAR analysis (Sections 2.2.3.1.3 and 6.4) 
    for chlorine release events since the basis for the existing margin 
    of safety, which are the Reg. Guide 1.95 requirements, are not 
    altered by the change. As stated above, since gaseous chlorine is no 
    longer used for open cooling water treatment at Susquehanna SES and 
    since the biocide currently used does not pose the same personnel 
    inhalation threat as gaseous chlorine, safety margin has actually 
    increased. Therefore, the proposed change does not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 
    50-364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston 
    County, Alabama
    
        Date of amendments request: June 13, 1997
        Description of amendments request: The proposed amendments would 
    change Technical Specification (TS) 3/4.9.13, ``Storage Pool 
    Ventilation (Fuel Movement),'' by adding a note in the TSs to 
    specifically indicate that the normal emergency power source may be 
    inoperable in MODE 5 or 6 provided that the requirements of TS 3.8.1.2 
    are satisfied and extend the TS 3.9.13 completion time allowed for 
    returning one out-of-service penetration room filtration system from 48 
    hours to 7 days. The Bases will also be modified to provide additional 
    detail concerning these changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) The proposed changes do not significantly increase the 
    probability or consequences of an accident previously evaluated in 
    the FSAR [Final Safety Analysis Report]. The proposed changes have 
    no impact on the probability of an accident. The storage pool 
    ventilation system will continue to ensure that radioactive material 
    released as a result of a fuel handling accident in the spent fuel 
    pool room will be filtered through the HEPA [high efficiency 
    particulate air] filters and charcoal absorbers prior to discharge 
    to the atmosphere. There is no change in the FNP [Farley Nuclear 
    Plant] design basis as a result of this change and, as a result, 
    does not involve a significant increase in the consequences of an 
    accident previously evaluated.
        (2) The proposed changes to the TSs do not increase the 
    possibility of a new or different kind of accident than any accident 
    already evaluated in the FSAR. No new limiting single failure or 
    accident scenario has been created or identified due to the proposed 
    changes. Safety-related systems will continue to perform as 
    designed. The proposed changes do not create the possibility of a 
    new or different kind of accident from any previously evaluated.
        (3) The proposed changes do not involve a significant reduction 
    in the margin of safety. As a result of these proposed changes, the 
    penetration room filtration system, when it is aligned to the spent 
    fuel pool room, will continue to require verification of 
    operability. There is no impact in the accident analyses. These 
    proposed changes are technically consistent with the requirements of 
    NUREG-1431, Revision 1 which has already received the requisite 
    review and approval of the NRC staff. Thus the proposed changes do 
    not involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302
        Attorney for licensee: M. Stanford Blanton, Esq., Balch and 
    Bingham, Post Office Box 306, 1710 Sixth Avenue North, Birmingham, 
    Alabama 35201
        NRC Project Director: Herbert N. Berkow
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of 
    Georgia, City of Dalton, Georgia, Docket No. 50-321, Edwin I. Hatch 
    Nuclear Plant, Unit 1, Appling County, Georgia
    
        Date of amendment request: April 29, 1997, as supplemented by 
    letter dated May 28, 1997
        Description of amendment request: The amendment would revise the 
    Unit 1 reactor vessel pressure and temperature limits to reflect data 
    collected from the material sample recovered during the March 1996 Unit 
    1 outage.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        Pressure and Temperature (P/T) limits for the reactor pressure 
    vessel are established to the requirements of 10 CFR [Part] 50, 
    Appendix G to ensure brittle fracture of the vessel does not occur.
        This revision changes the P/T curves in the Unit 1 Technical 
    Specifications to reflect the material capsule surveillance results 
    from the sample removed during the [s]pring outage of 1996.
        The RPV [reactor pressure vessel] surveillance capsule contained 
    flux wires for neutron flux monitoring and Charpy V notch impact and 
    tensile test specimens. The irradiated material properties were 
    compared to available unirradiated properties to determine the 
    effect of irradiation on material toughness for the base and weld 
    materials through Charpy testing. Irradiated tensile testing results 
    are compared with unirradiated data to determine the effect of 
    irradiation on the stress-strain relationship of the materials.
        The P/T curves are modified to reflect the results of the above 
    examination. These curves and their operating limits were evaluated 
    using the approved methodologies of 10 CFR [Part] 50 Appendix G and 
    ASME [American Society of Mechanical Engineers] Code Appendix G. The 
    new curves therefore represent the latest information available on 
    the state of the reactor vessel materials. The P/T curves are 
    generated for reactor vessel protection against brittle fracture, 
    they do not affect the recirculation piping. Accordingly, the 
    probability of occurrence of a design basis Loss of Coolant Accident 
    (LOCA) is not increased. Likewise, no other previously evaluated 
    accident and transients, as defined in Chapter 14 of the Final 
    Safety Analysis Report (FSAR) are affected by this proposed change 
    to the Unit 1 P/T curves. Additionally, this proposed revision does 
    not affect the design, operation, or maintenance of any safety 
    related system designed for the mitigation or prevention of 
    previously analyzed events.
    
    [[Page 38139]]
    
        Since no previously evaluated accidents or transients are being 
    affected by this change, their probability of occurrence is not 
    increased and their consequences are not made worse.
        2. Do the proposed changes create the possibility of a new or 
    different type of accident from any previously evaluated?
        Implementing the proposed P/T curves into the Unit 1 Technical 
    Specifications does not alter the design or operation of any system 
    or piece of equipment designed for the prevention or mitigation of 
    accidents and transients. As a result, no new operating modes are 
    introduced from which a new type accident becomes possible. Existing 
    systems will continue to be operated per present design basis 
    assumptions.
        The proposed P/T limits were generated from the evaluation of 
    the material capsule removed during the [s]pring Unit 1 outage of 
    1996. As a result, these limits include the latest available 
    information on the reactor vessel materials. Furthermore, they will 
    continue to be monitored per the requirements of the Technical 
    Specifications and 10 CFR [Part] 50 Appendices G and H. For the 
    above reasons, the changes do not create the possibility of a new 
    type of accident.
        3. Do the proposed changes involve a significant reduction in 
    the margin of safety?
        The purpose of the P/T limits is to avoid a brittle fracture of 
    the reactor vessel. As such, material capsules are removed 
    periodically to determine the effects of neutron irradiation on 
    reactor vessel materials. This change to the Unit 1 P/T curves is 
    proposed to incorporate the evaluation results of the latest capsule 
    removed during the [s]pring Unit 1 outage of 1996. Accordingly, 
    these curves represent the latest information available on the 
    reactor vessel materials. Also, the curves were generated using the 
    approved methodologies of 10 CFR [Part] 50 Appendix G.
        The pressure test curve (Figure 3.4.9-1) is also being revised 
    to reflect exposure dependencies. These curves were generated for 
    exposures of 16, 18, 20, 24, 28, and 32 EFPY [effective full-power 
    year]. As previously described, each of these curves were generated 
    using approved methodologies and all reflect the results of this 
    latest material capsule report.
        The proposed change does not affect the evaluation of any FSAR 
    Unit 1 Chapter 14 transient and accident. Furthermore, the proposed 
    change does not affect the operation of systems or equipment 
    important to safety.
        The Limiting Condition for Operation of Specification 3.4.9 will 
    not change. Also, no Technical Specification surveillances or 
    surveillance frequencies are revised as a result of this Technical 
    Specification submittal, besides the fact that the P/T surveillances 
    will now refer to the revised curves. Procedures regarding the 
    monitoring of the P/T limits during reactor startup, cooldown, and 
    leakage testing will not change as a result of this proposed 
    Technical Specification change with respect to frequency of the 
    surveillance or the methods used to perform the surveillances. Thus, 
    the P/T limits will continue to be surveilled as before per the same 
    procedures and the same frequencies.
        No other Technical Specifications are affected by the proposed 
    revision. The margin of safety to any Technical Specifications 
    safety limit therefore is not reduced.
        For the above reasons the new curves do not represent a 
    significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Herbert N. Berkow
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of 
    Georgia, City of Dalton, Georgia, Docket Nos. 50-321 and 50-366, 
    Edwin I. Hatch Nuclear Plant, Units 1 and 2, Appling County, 
    Georgia
    
        Date of amendment request: May 30, 1997
        Description of amendment request: The proposed amendments would 
    revise power sources to valves associated with low pressure coolant 
    injection (LPCI) mode of residual heat removal (RHR) system.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    The LPCI valves operate to establish and maintain adequate core 
    cooling following a LOCA [loss-of-coolant accident]. The proposed 
    changes do not alter the function or mode of operation of the LPCI 
    valves. Therefore, the probability of the LOCA accident is not 
    increased. An analysis which considered the consequences of the 
    various transients and accidents with the proposed change in power 
    supply of the LPCI valves indicates the consequences are not 
    increased.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously analyzed. 
    The change in power supply to the LPCI valves maintains the original 
    design criteria that a power supply independent of the remaining RHR 
    subsystem be utilized for single-failure criteria. The function of 
    the LPCI valves and any other existing equipment is not altered. 
    Operation of the valves in the proposed configuration was analyzed, 
    and no new failure modes exist. An analysis of the impact on the 
    operation and design of other systems and components indicates no 
    new failure modes are introduced. Therefore, these changes do not 
    contribute to a new or different type of accident.
        3. The proposed changes do not involve a significant reduction 
    in the margin of safety. The change in power supply to the LPCI 
    valves was evaluated relative to RHR and electrical distribution 
    system function during normal and accident conditions. The proposed 
    change does not alter the performance of any system safety 
    functions. The results of the SAFER-GESTR LOCA analysis reconfirm 
    the large margins existing in fuel peak cladding temperature under 
    the proposed configuration. Therefore, there is no significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Herbert N. Berkow
    
    Southern Nuclear Operating Company, Inc., Georgia Power Company, 
    Oglethorpe Power Corporation, Municipal Electric Authority of 
    Georgia, City of Dalton, Georgia, Docket Nos. 50-424 and 50-425, 
    Vogtle Electric Generating Plant, Units 1 and 2, Burke County, 
    Georgia
    
        Date of amendment request: June 13, 1997
        Description of amendment request: The proposed amendments would 
    revise the Technical Specification Limiting Condition for Operation 
    3.4.10 Pressurizer Safety Valves. Specifically, the change would reduce 
    the nominal set pressure by 1 percent to 2460 pounds per square inch 
    gauge (psig) and increase the tolerance to plus or minus 2 percent.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    [[Page 38140]]
    
        1. Does the proposed change involve a significant increase in 
    the probability or consequences of an accident previously evaluated?
        The increase in the PSV [pressurizer safety valve] tolerance 
    from [plus or minus] 1% with a setpoint of 2485 psig to [plus or 
    minus] 2% and reduction in the nominal setpoint from 2485 psig to 
    2460 psig has the net effect of reducing the minimum lift setting 
    allowed by the TS [technical specifications] from 2460 psig to 2410 
    psig. The effects of this change have been evaluated for its impact 
    on the assumed frequency of safety valve challenges and failures to 
    reclose, and the proposed change was found to have a negligible 
    impact. In other words, reducing the minimum lift setting does not 
    significantly increase the probability of an inadvertent actuation 
    of a safety valve during normal operation. Reducing the minimum lift 
    setting does increase the potential that the PSVs may open during an 
    event, but this change has been evaluated and does not adversely 
    impact the consequences of any accident previously evaluated. No 
    change to any equipment response or accident mitigation scenario has 
    resulted, and there are no additional challenges to fission product 
    barrier integrity. Therefore, the proposed change does not 
    significantly increase the probability or consequences of any 
    accident previously evaluated.
        2. Does the proposed change create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        The increase in the PSV tolerance from [plus or minus] 1% with a 
    setpoint of 2485 psig to [plus or minus] 2% and reduction in the 
    nominal setpoint from 2485 psig to 2460 psig does not create the 
    possibility of a new or different kind of accident than any accident 
    previously evaluated. No new accident scenarios, failure mechanisms, 
    or limiting single failures are introduced as a result of this 
    proposed change. The proposed revision to Technical Specification 
    3.4.10 does not challenge the performance or integrity of any 
    safety-related systems. Therefore, the possibility of a new or 
    different kind of accident is not created.
        3. Does the proposed change involve a significant reduction in a 
    margin of safety.
        The proposed change to Technical Specification 3.4.10 does not 
    involve a significant reduction in a margin of safety. The 
    modification will have no affect on the availability, operability or 
    performance of the safety-related systems and components. The 
    increased PSV set pressure tolerance has been reviewed with respect 
    to the accident analysis assumptions and requirements and evaluated 
    or analyzed, as required. These evaluations and analyses determined 
    that all applicable acceptance criteria continue to be met, thus the 
    proposed increase in the PSV set pressure tolerance will not result 
    in a significant reduction in the margin of safety associated with 
    the acceptance criteria for the accident analyses.
        The Bases of the Technical Specifications rely in part on the 
    ability of the regulatory criteria being satisfied assuming the 
    limiting conditions for operation for various systems. Conformance 
    to the regulatory criteria for operation with the increased PSV set 
    pressure tolerance is demonstrated, and the regulatory limits are 
    not exceeded. Hence, the margin of safety as defined in the Bases 
    for the Technical Specifications is not significantly reduced.
        Therefore, there is no significant reduction in any margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Burke County Public Library, 
    412 Fourth Street, Waynesboro, Georgia 30830
        Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders, 
    NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta, 
    Georgia 30308
        NRC Project Director: Herbert N. Berkow
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station, Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: May 16, 1997 (TXX-97119)
        Brief description of amendments: The licensee has proposed revised 
    core safety limit curves and Overtemperature N-16 reactor trip 
    setpoints based on analyses of the core configuration for CPSES Unit 2, 
    Cycle 4. These changes apply equally to CPSES Units 1 and 2 licenses 
    since the Technical Specifications are combined.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Do the proposed changes involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        A. Revision to the Unit 2 Core Safety Limits
        Analyses of reactor core safety limits are required as part of 
    reload calculations for each cycle. TU Electric has performed the 
    analyses of the Unit 2, Cycle 4 core configuration to determine the 
    reactor core safety limits. The methodologies and safety analysis 
    values result in new operating curves which, in general, permit 
    plant operation over a similar range of acceptable conditions. This 
    change means that if a transient were to occur with the plant 
    operating at the limits of the new curve, a different temperature 
    and power level might be attained
        than if the plant were operating within the bounds of the old 
    curves. However, since the new curves were developed using NRC 
    approved methodologies which are wholly consistent with and do not 
    represent a change in the Technical Specification BASES for safety 
    limits, all applicable postulated transients will continue to be 
    properly mitigated. As a result, there will be no significant 
    increase in the consequences, as determined by accident analyses, of 
    any accident previously evaluated.
        B. Revision to Unit 2 Overtemperature N-16 Reactor Trip 
    Setpoints
        As a result of changes discussed, the Overtemperature reactor 
    trip setpoint has been recalculated. These trip setpoints help 
    ensure that the core safety limits are protected and that all 
    applicable limits of the safety analysis are met.
        Based on the calculations performed, no significant changes to 
    the safety analysis values for Overtemperature reactor trip setpoint 
    were required. The f(delta I) trip reset function was revised due to 
    more top-skewed axial power distributions predicted for this cycle. 
    The analyses performed show that, using the TU Electric 
    methodologies, all applicable limits of the safety analysis are met. 
    This setpoint provides a trip function which allows the mitigation 
    of postulated accidents and has no impact on accident initiation. 
    Therefore, the changes in safety analysis values do not involve an 
    increase in the probability of an accident and, based on satisfying 
    all applicable safety analysis limits, there is no significant 
    increase in the consequences of any accident previously evaluated.
        In addition, sufficient operating margin has been maintained in 
    the overtemperature setpoint such that the risk of turbine runbacks 
    or reactor trips due to upper plenum flow anomalies or other 
    operational transients will be minimized, thus reducing potential 
    challenges to the plant safety systems.
        SUMMARY
        The changes in the amendment request applies NRC approved 
    methodologies to changes in safety analysis values, new core safety 
    limits and new N-16 setpoint and parameter values to assure that all 
    applicable safety analysis limits have been met. The potential for 
    an operational transient to occur has not been affected and there 
    has been no significant impact on the consequences of any accident 
    previously evaluated.
        2. Do the proposed changes create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        The proposed changes involve the calculation of new reactor core 
    safety limits and overtemperature reactor trip setpoint resets. As 
    such, the changes play an important role in the analysis of 
    postulated accidents but none of the changes effect plant hardware 
    or the operation of plant systems in a way that could initiate an 
    accident. Therefore, the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. Do the proposed changes involve a significant reduction in a 
    margin of safety?
    
    [[Page 38141]]
    
        In reviewing and approving the methods used for safety analyses 
    and calculations, the NRC has approved the safety analysis limits 
    which establish the margin of safety to be maintained. While the 
    actual impact on safety is discussed in response to question 1, the 
    impact on margin of safety is discussed below:
        A. Revision to the Unit 2 Reactor Core Safety Limits
        The TU Electric reload analysis methods have been used to 
    determine new reactor core safety limits. All applicable safety 
    analysis limits have been met. The methods used are wholly 
    consistent with Technical Specification BASES 2.1 which is the bases 
    for the safety limits. In particular, the curves assure that for 
    Unit 2, Cycle 4, the calculated DNBR is no less than the safety 
    analysis limit and the average enthalpy at the vessel exit is less 
    than the enthalpy of saturated liquid. The acceptance criteria 
    remains valid and continues to be satisfied; therefore, no change in 
    a margin of safety occurs.
        B. Revision to Unit 2 Overtemperature N-16 Reactor Trip 
    Setpoints
        Because the reactor core safety limits for CPSES Unit 2, Cycle 4 
    are recalculated, the Reactor Trip System instrumentation setpoint 
    values for the Overtemperature N-16 reactor trip setpoint which 
    protect the reactor core safety limits must also be recalculated. 
    The Overtemperature N-16 reactor trip setpoint helps prevent the 
    core and Reactor Coolant System from exceeding their safety limits 
    during normal operation and design basis anticipated operational 
    occurrences. However, it was shown in these calculations that the 
    current Unit 2 overtemperature reactor trip setpoint (presented in 
    the current Technical Specifications and excluding the f(delta I) 
    trip reset function) remains valid. The most relevant design basis 
    analysis in Chapter 15 of the CPSES Final Safety Analysis Report 
    (FSAR) which is affected by the Overtemperature reactor trip 
    setpoint is the Uncontrolled Rod Cluster Control Assembly Bank 
    Withdrawal at Power (FSAR Section 15.4.2). This event has been 
    analyzed with the new safety analysis value for the Overtemperature 
    reactor trip setpoint to demonstrate compliance with event specific 
    acceptance criteria. Because all event acceptance criteria are 
    satisfied, there is no degradation in a margin of safety.
        The nominal Reactor Trip System instrumentation setpoints values 
    for the Overtemperature N-16 reactor trip setpoint (Technical 
    Specification Table 2.2-1) are determined based on a statistical 
    combination of all of the uncertainties in the channels to arrive at 
    a total uncertainty. The total uncertainty plus additional margin is 
    applied in a conservative direction to the safety analysis trip 
    setpoint value to arrive at the nominal and allowable values 
    presented in Technical Specification Table 2.2-1. Meeting the 
    requirements of Technical Specification Table 2.2-1 assures that the 
    Overtemperature reactor trip setpoint assumed in the safety analyses 
    remains valid. The CPSES Unit 2, Cycle 4 Overtemperature reactor 
    trip setpoint is not significantly different from the previous 
    cycle, and thus provides operational flexibility to withstand mild 
    transients without initiating automatic protective actions. Although 
    the value of the f(delta I) trip reset function setpoint is 
    different, the Reactor Trip System instrumentation setpoint values 
    for the Overtemperature N-16 reactor trip setpoint are consistent 
    with the safety analysis assumptions which have been analytically 
    demonstrated to be adequate to meet the applicable event acceptance 
    criteria. Thus, there is no reduction in a margin of safety.
        Using the NRC approved TU Electric methods, the reactor core 
    safety limits are determined such that all applicable limits of the 
    safety analyses are met. Because the applicable event acceptance 
    criteria continue to be met, there is no significant reduction in 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, TX 76019
        Attorney for licensee: George L. Edgar, Esq., Morgan, Lewis and 
    Bockius, 1800 M Street, N.W., Washington, DC 20036
        NRC Project Director: James W. Clifford, Acting
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Commonwealth Edison Company, Docket No. STN 50-455, Byron Station, 
    Unit No. 2, Ogle County, Illinois Docket No. STN 50-457, Braidwood 
    Station, Unit No. 2, Will County, Illinois
    
        Date of amendment request: May 24, 1997
        Description of amendment request: The amendments revise the 
    technical specifications related to venting of the emergency core 
    cooling system pumps and associated piping. The application originally 
    included Byron, Unit 1. However, on May 31, 1997, ComEd supplemented 
    the application to request an emergency license amendment for Byron, 
    Unit 1. Amendment No. 90 was issued on June 1, 1997.
        Date of publication of individual notice in Federal Register: June 
    10, 1997 (62 FR 31633)
        Expiration date of individual notice: July 10, 1997
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile 
    Point Nuclear Station, Unit No. 1, Oswego County, New York
    
        Date of application for amendment: May 16, 1997
        Brief description of amendment: The proposed amendment would make 
    an administrative change to add a supervisory position to the list of 
    personnel who may be required to hold a senior reactor operator 
    license. Date of publication of individual notice in Federal Register: 
    June 4, 1997 (62 FR 30625)
        Expiration date of individual notice: July 7, 1997
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
    
    [[Page 38142]]
    
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of application for amendment: January 20, 1997, with the 
    proposed no significant hazards consideration submitted by letter dated 
    January 30, 1997, as supplemented February 27, April 11, May 14, and 
    June 20 (2 letters), 1997
        Brief description of amendment: The amendment authorizes Boston 
    Edison Company (BECo) to change the UHS administrative limit from 
    68 deg.F to 75  deg.F, and change the Updated Final Safety Analysis 
    Report (UFSAR) to reflect the use of containment pressure to compensate 
    for the deficiency in NPSH following a design basis accident and 
    increase the accident analysis design UHS temperature from 65 deg.F to 
    75 deg.F. As part of this amendment, BECo has proposed to submit a 
    Technical Specification amendment for the UHS temperature by the first 
    quarter of 1998. In addition, within 180 days of issuance of this 
    amendment, BECo has committed to complete the containment analysis 
    using the ANS 5.1-1979 Decay Heat Curve with a 2-sigma uncertainty 
    added. The staff considers BECo's commitments acceptable and has 
    conditioned the amendment accordingly.
        Date of issuance: July 3, 1997
        Effective date: July 3, 1997
        Amendment No.: 173
        Facility Operating License No. DPR-35: Amendment revised the 
    Updated Final Safety Analysis Report.
        Date of initial notice in Federal Register: February 26, 1997 (62 
    FR 8792) The February 27, April 11, May 14, and June 20 (2 letters), 
    1997, letters provided clarifying information that did not change the 
    initial proposed no significant hazards consideration determination as 
    submitted by letter dated January 30, 1997. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    July 3, 1997. No significant hazards consideration comments received: 
    No.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of application for amendment: March 14, 1997, as supplemented 
    May 16, and June 17, 1997
        Brief description of amendment: The amendment approves changes to 
    the Final Safety Analysis Report to reflect new analysis of the 
    radiological consequences of dropping a fuel cask.
        Date of issuance: June 26, 1997
        Effective date: June 26, 1997
        Amendment No. 73
        Facility Operating License No. NPF-63. Amendment revises the Final 
    Safety Analysis Report.
        Date of initial notice in Federal Register: April 9, 1997 (62 FR 
    17226). The May 16, and June 17, 1997 supplemental information did not 
    change the original no significant hazards consideration determination. 
    The Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated June 26, 1997. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: April 11, 1997
        Brief description of amendment: The amendment changes the Waterford 
    steam Electric Station, Unit 3, Technical Specifications (TSs) by 
    revising TS 3.6.2.2 and Surveillance Requirement 4.6.2.2 for the 
    Containment Cooling System. Also, a Surveillance Requirement is added 
    to verify that valves actuate on a Safety Injection Actuation Signal. 
    To support this addition, Technical Specification Bases 3/4.3.6.2.2 is 
    also included.
        Date of issuance: July 3, 1997
        Effective date: July 3, 1997, to be implemented within 60 days.
        Amendment No.: 131
        Facility Operating License No. NPF-38: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 22, 1997 (62 FR 
    19626) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 3, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: April 17, 1997
        Brief description of amendment: The amendment modifies Technical 
    Specification 3.7.14 by clarifying the actions to be taken when an area 
    temperature exceeds its temperature limit.
        Date of issuance: June 24, 1997
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 141
        Facility Operating License No. NPF-49: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: (62 FR 27798 May 21, 
    1997) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 24, 1997. No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut 06360, and the Waterford Library, ATTN: Vince 
    Juliano, 49 Rope Ferry Road, Waterford, Connecticut 06385
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: April 15, 1997
        Brief description of amendment: The amendment makes changes to 
    Technical Specification (TS) Sections 4.3.3.6 and 4.6.4.1, which 
    require that the hydrogen monitors be periodically tested. 
    Specifically, the changes increase the testing interval of the 
    monitor's hydrogen sensor, correct inconsistencies
    
    [[Page 38143]]
    
    between the TS surveillances, and make changes to the Bases of the 
    surveillances.
        Date of issuance: June 24, 1997
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 142
        Facility Operating License No. NPF-49: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 21, 1997 (62 FR 
    27797) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 24, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut 06360, and the Waterford Library, ATTN: Vince 
    Juliano, 49 Rope Ferry Road, Waterford, Connecticut 06385
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: April 11, 1997
        Brief description of amendments: These amendments revise Technical 
    Specification (TS) 3/4.6.2.3, ``Containment Cooling System,'' and its 
    associated Bases section to ensure that the TSs properly test the 
    containment fan cooling units' post-accident mode of operation.
        Date of issuance: June 24, 1997
        Effective date: Both units, as of the date of issuance, to be 
    implemented within 60 days.
        Amendment Nos. 197 and 180
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 21, 1997 (62 FR 
    27799) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 24, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: March 13, 1997, as supplemented 
    on June 26, 1997 (TS 97-01)
        Brief description of amendments: The amendments change the 
    Technical Specifications by raising the allowable U-235 enrichment, as 
    specified in Section 5.6.1.2, of fuel stored in the new fuel pit 
    storage racks from 4.5 to 5.0 weight percent.
        Date of issuance: July 1, 1997
        Effective date: July 1, 1997
        Amendment Nos.: 225 and 216
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: May 21, 1997 (62 FR 
    27802). The June 26, 1997 supplement provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in an environmental assessment dated June 16, 
    1997, and a Safety Evaluation dated July 1, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, 
    Vermont Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: August 27, 1993, as supplemented 
    by letters dated November 9, 1993, April 26, 1996, and September 25, 
    1996
        Brief description of amendment: The amendment revises the Technical 
    Specifications to incorporate the revised 10 CFR Part 20, Standards for 
    Protection Against Radiation.
        Date of issuance: June 19, 1997
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 151
        Facility Operating License No. DPR-28. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 4, 1995 (60 FR 
    507) The November 9, 1993, April 26, 1996, and September 25, 1996, 
    submittals did not change the initial proposed no significant hazards 
    consideration. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 19, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of application for amendments: June 4, 1996 (TSCR 188 and 
    189), as supplemented August 5, September 26, October 21, November 13, 
    November 20, and December 2, 1996, and January 16, March 20, and April 
    2, 1997
        Brief description of amendments: These amendments revise Technical 
    Specifications (TS) 15.1, ``Definitions;'' TS 15.2.1, ``Safety Limit, 
    Reactor Core;'' TS 15.2.3, ``Limiting Safety System Settings, 
    Protective Instrumentation;'' TS 15.3.1, ``Reactor Coolant System,'' 
    Section C, ``Maximum Coolant Activity,'' and Section G, ``Operational 
    Limitations;'' TS 15.3.4, ``Steam and Power Conversion System;'' TS 
    15.3.5, ``Instrumentation System;'' TS 15.4.1, ``Operational Safety 
    Review;'' TS 15.5.3, ``Design Features-Reactor;'' and TS 15.6.9, 
    ``Plant Reporting Requirements'' to reflect parameters associated with 
    new steam generators in Unit 2 and changes in analyses that affect both 
    Units 1 and 2.
        Date of issuance: July 1, 1997
        Effective date: July 1, 1997. The TS shall be implemented within 45 
    days from the date of issuance and the Final Safety Analysis Report 
    changes shall be implemented by June 30, 1998. Implementation of these 
    amendments includes incorporation of accident analyses submitted in 
    support of this amendment into the Final Safety Analysis Report in 
    sufficient detail to support future evaluations performed in accordance 
    with 10 CFR 50.59 and as described in the licensee's applications dated 
    June 4, 1996, as supplemented on August 5, September 26, October 21, 
    November 13, November 20, and December 2, 1996, and January 16, March 
    20, and April 2, 1997, and evaluated in the staff's safety evaluation 
    dated July 1, 1997.
        Amendment Nos.: 173, 177
        Facility Operating License Nos. DPR-24 and DPR-27: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 3, 1996 (61 FR 
    34903 and 61 FR 34904) and April 9, 1997 (62 FR 17243) The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated July 1, 1997. No significant hazards consideration 
    comments received: No.
        Local Public Document Room location: The Lester Public Library, 
    1001 Adams Street, Two Rivers, Wisconsin 54241
    
    [[Page 38144]]
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: March 21, 1997, as supplemented by 
    letter dated April 15, 1997
        Brief description of amendment: The amendment revises Technical 
    Specification 6.8.5.b to provide an exception to the examination 
    requirements of Regulatory Guide 1.14, Revision 1, ``Reactor Coolant 
    Pump Flywheel Integrity'' and delays the inspection of the ``D'' 
    reactor coolant pump flywheel to the Fall 1997 refueling outage. A 
    typographical error in TS 6.8.5.c is corrected.
        Date of issuance: June 24, 1997
        Effective date: June 24, 1997, to be implemented within 30 days of 
    issuance.
        Amendment No.: 106
        Facility Operating License No. NPF-42. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 21, 1997 (62 FR 
    27803) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 24, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration and 
    opportunity for a hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By August 15, 1997, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be
    
    [[Page 38145]]
    
    made a party to the proceeding; (2) the nature and extent of the 
    petitioner's property, financial, or other interest in the proceeding; 
    and (3) the possible effect of any order which may be entered in the 
    proceeding on the petitioner's interest. The petition should also 
    identify the specific aspect(s) of the subject matter of the proceeding 
    as to which petitioner wishes to intervene. Any person who has filed a 
    petition for leave to intervene or who has been admitted as a party may 
    amend the petition without requesting leave of the Board up to 15 days 
    prior to the first prehearing conference scheduled in the proceeding, 
    but such an amended petition must satisfy the specificity requirements 
    described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-001, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. A copy of the petition should also be sent to the Office of the 
    General Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 
    20555-001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: December 11, 1996, as 
    supplemented March 27, 1997, April 17, 1997, and June 17, 1997
        Brief description of amendment: The amendment revises Technical 
    Specifications to allow extended rod position indicator deviation 
    limits, on-line calibration of the rod position indication and to 
    clarify the operability requirements during calibration.
        Date of issuance: June 27, 1997
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 194
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: No. The NRC published a public 
    notice of the proposed amendment, issued a proposed finding of no 
    significant hazards consideration and requested that any comments on 
    the proposed no significant hazards consideration be provided to the 
    staff by the close of business on June 25, 1997. The notice was 
    published in the Peekskill Evening Star on June 20-25, 1997.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, consultation with the State of New York and 
    final no significant hazards consideration determination are contained 
    in a Safety Evaluation dated June 27, 1997.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610
    
    North Atlantic Energy Service Corporation, Dockets Nos. 50-443, 
    Seabrook Station, Unit 1, Seabrook, Massachusetts
    
        Date of amendment request: June 19, 1997
        Brief description of amendment: The amendment revised Technical 
    Specification 6.8.1.6.b. to include a reference to the NRC-approved 
    Westinghouse Topical Report WCAP-12610-P-A, ``VANTAGE+ Fuel Assembly 
    Reference Core Report,'' dated April 1995.
        Date of issuance: June 24, 1997
        Effective date: As of the date of issuance, and to be implemented 
    before transition into Operational Mode 2 during startup from Refueling 
    Outage 5.
        Amendment No.: 52
        Facility Operating License No. NPF-86: Amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: No. The Commission's related 
    evaluation of the amendment, finding of emergency circumstances, 
    consultation with the States of New Hampshire and Massachusetts, and 
    final no significant hazards considerations determination are contained 
    in the safety evaluation dated June 24, 1997.
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, New Hampshire 03833
        Attorney for licensee: Lillian M. Cuoco, Esquire, Northeast 
    Utilities Service Company, Post Office Box 270, Hartford CT 06141-0270 
    Acting
        NRC Project Director: Patrick D. Milano
    
    North Atlantic Energy Service Corporation, Dockets Nos. 50-443, 
    Seabrook Station, Unit 1, Seabrook, Massachusetts
    
        Date of amendment request: May 29, 1997
        Brief description of amendment: The amendment modifies Technical 
    Specification 5.3.1 by replacing the current term ``zircaloy'' with 
    terminology that explicitly identifies the NRC-approved Westinghouse 
    fuel assembly design in use at the Seabrook Station consisting of 
    assemblies with either ZIRLO or Zircaloy-4 fuel cladding material.
        Date of issuance: June 24, 1997
        Effective date: As of the date of issuance, and to be implemented 
    before transition into Operational Mode 2 during startup from Refueling 
    Outage 5.
    
    [[Page 38146]]
    
        Amendment No.: 53
        Facility Operating License No. NPF-86: Amendment revised the 
    Technical Specifications. Public comments requested as to proposed no 
    significant hazards consideration: Yes. The NRC published a public 
    notice of the proposed amendment, issued a proposed finding of no 
    significant hazards consideration, and requested that any comments on 
    the proposed no significant hazards consideration be provided to the 
    staff by the close of business on June 10, 1997. The notice was 
    published in Foster's Daily Democrat and in the Portsmouth Herald on 
    June 4, 1997. Public comments were received, and they have been 
    addressed in the staff's safety evaluation.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, consultation with the States of New Hampshire 
    and Massachusetts, and final no significant hazards determination are 
    contained in a safety evaluation dated June 24, 1997.
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, New Hampshire 03833
        Attorney for licensee: Lillian M. Cuoco, Esquire, Northeast 
    Utilities Service Company, Post Office Box 270, Hartford CT 06141-0270 
    Acting
        NRC Project Director: Patrick D. Milano
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: March 22, 1997, as supplemented 
    by letters dated April 2, April 3, April 9, April 15, and May 14, 1997. 
    Additional information was also received by telefax on May 19, 1997.
        Brief description of amendment: The amendment revises Surveillance 
    Requirement (SR) 3.3.1.1.15, Reactor Protection System (RPS) Response 
    Time functions 3 and 4 and SR 3.3.6.1.7, Primary Containment Isolation 
    System Response Time, functions 1.a, 1.b, and 1.c, adding a note to 
    indicate that the sensor is excluded from response time testing when 
    verifying that the response time is within limits. The amendment also 
    revises SR 3.3.5.1.7, Emergency Core Cooling System (ECCS) Response 
    Time by relocating the requirements to SR 3.5.1.8, ECCS Operating, and 
    adding a note to SR 3.5.1.8 to indicate that no actuation 
    instrumentation response time measurement is required. Additionally, SR 
    3.5.1.8 requires that the SR be met in MODES 1, 2, and 3, whereas the 
    previous SR 3.3.5.1.7 was required to be met in MODES 1, 2, 3, 4, and 
    5.
        Date of Issuance: June 11, 1997
        Effective date: June 11, 1997
        Amendment No.: 150
        Facility Operating License No. NPF-21. The amendment revised the 
    Technical Specifications. Press release issued requesting comments as 
    to proposed no significant hazards consideration: Yes. April 11, 1997. 
    Tri-City Herald (Washington). Comments received: No. The Commission's 
    related evaluation of the amendments, finding of exigent circumstances, 
    consultation with the State of Washington and final determination of no 
    significant hazards consideration are contained in a Safety Evaluation 
    dated June 11, 1997.
        Attorney for licensee: Perry D. Robinson, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005-3502
        Local Public Document Room location:  Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
        NRC Project Director: William H. Bateman
        Dated at Rockville, Maryland, this 9th day of July 1997.
        For the Nuclear Regulatory Commission
    Elinor G. Adensam,
    Deputy Director, Division of Reactor Projects III/IV, Office of Nuclear 
    Reactor Regulation
    [Doc. 97-18513 Filed 7-15-97; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Effective Date:
7/3/1997
Published:
07/16/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X97-10716
Dates:
July 3, 1997
Pages:
38130-38146 (17 pages)
PDF File:
x97-10716.pdf