96-16878. Arizona Public Service Company; Palo Verde Nuclear Generating Station, Unit Nos. 1, 2, and 3; Issuance of Director's Decision Under 10 CFR Sec. 2.206  

  • [Federal Register Volume 61, Number 128 (Tuesday, July 2, 1996)]
    [Notices]
    [Pages 34454-34460]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 96-16878]
    
    
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    NUCLEAR REGULATORY COMMISSION
    [Docket Nos. 50-528, 50-529 and 50-530]
    
    
    Arizona Public Service Company; Palo Verde Nuclear Generating 
    Station, Unit Nos. 1, 2, and 3; Issuance of Director's Decision Under 
    10 CFR Sec. 2.206
    
        Notice is hereby given that the Director, Office of Nuclear Reactor 
    Regulation, has acted on a Petition for action under 10 CFR Sec. 2.206 
    received from Mr. Thomas J. Saporito, Jr., on behalf of Florida Energy 
    Consultants, Inc., dated May 27, 1994, as supplemented on July 8, 1994, 
    for the Palo Verde Nuclear Generating Station, Unit Nos. 1, 2, and 3.
        In a letter dated May 27, 1994, the Petitioner requested that the 
    NRC (1) institute a show-cause proceeding pursuant to 10 CFR Sec. 2.202 
    to modify, suspend, or revoke the operating licenses for Palo Verde; 
    (2) issue a notice of violation against the licensee for continuing to 
    employ The Atlantic Group (TAG) as a labor contractor at Palo Verde; 
    (3) investigate alleged material false statements made by William F. 
    Conway, Executive Vice President at Palo Verde, during his testimony at 
    a Department of Labor hearing (ERA Case No. 92-ERA-030) and, in the 
    interim, require that he be relieved of any authority over operations 
    at Palo Verde; (4) investigate the licensee's statements in a letter of 
    August 10, 1993, from Mr. Conway to the former NRC regional 
    administrator, Mr. Bobby H. Faulkenberry, that Mr. Saporito gave 
    materially false, inaccurate, and incomplete information on his 
    application for unescorted access to Palo Verde and that, as a result, 
    he lacks trustworthiness and reliability for access to Palo Verde; (5) 
    investigate the circumstances surrounding the February 1994 termination 
    of licensee employee Joseph Straub, a former radiation protection 
    technician at Palo Verde, to determine if his employment was illegally 
    terminated by the licensee because he engaged in ``protected activity'' 
    during the course of his employment; (6) require the licensee to 
    respond to a ``chilling effect'' letter regarding the circumstances 
    surrounding Mr. Straub's termination from Palo Verde and to specify 
    whether any measures were taken to ensure that his termination did not 
    have a chilling effect at Palo Verde; and (7) initiate appropriate 
    actions to require the licensee to immediately conduct eddy current 
    testing on all steam generators at Palo Verde because the steam 
    generator tubes were recently found to be subject to cracking.
        In a letter dated July 8, 1994, the Petitioner raised six 
    additional issues. This supplemental Petition asked the NRC to (1) 
    institute a show-cause proceeding pursuant to 10 CFR Sec. 2.202 for the 
    modification, suspension, or revocation of the Palo Verde operating 
    licenses for Units 1, 2, and 3; (2) modify the Palo Verde operating 
    licenses to require operation at 86-percent power or less; (3) require 
    the licensee to submit a No Significant Hazards safety analysis
    
    [[Page 34455]]
    
    to justify operation of those units above 86-percent power; (4) take 
    immediate action (e.g., by confirmatory order) to make the licensee 
    reduce operation to 86-percent power or less; (5) require the licensee 
    to analyze a design-basis steam generator tube rupture (SGTR) event to 
    show that the offsite radiological consequences do not exceed a small 
    fraction of the limits of 10 CFR Part 100; and (6) require the licensee 
    to demonstrate that its emergency operating procedures for SGTR events 
    are adequate and that the plant operators are sufficiently trained in 
    emergency operating procedures.
        The Director of the Office of Nuclear Reactor Regulation has 
    determined that requests 1, 2, 3, 5, and 6 of the July 8, 1994, 
    Petition supplement should be denied for the reasons stated in the 
    ``Director's Decision Under 10 CFR Sec. 2.206'' (DD-96-08), the 
    complete text of which follows this notice and which is available for 
    public inspection at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, N.W., Washington, D.C. 20555, and at the local 
    public document room located at the Phoenix Public Library, 1221 N. 
    Central Avenue, Phoenix, Arizona 85004. The Petitioners' two requests 
    for immediate action (Request 7 of the May 27, 1994 Petition and 
    Request 4 of the July 8, 1994, Petition supplement) were denied in a 
    letter dated July 26, 1994. The remaining requests are under 
    consideration and will be addressed in a separate decision. A 
    Director's Decision (DD-96-04) regarding Requests 1 through 6 in the 
    Petition of May 27, 1994, was issued under separate cover letter on 
    June 3, 1996.
        A copy of this Decision will be filed with the Secretary for the 
    Commission's review in accordance with 10 CFR Sec. 2.206. As provided 
    by the regulation, the Decision will constitute the final action of the 
    Commission 25 days after the date of issuance of the Decision unless 
    the Commission on its own motion institutes a review of the Decision 
    within that time.
    
        Dated at Rockville, Maryland, this 25th day of June 1996.
    
        For the Nuclear Regulatory Commission.
    William T. Russell,
    Director, Office of Nuclear Reactor Regulation.
    
    I. Introduction
    
        On May 27, 1994, Florida Energy Consultants, Inc. (FEC), by and 
    through Thomas J. Saporito, Jr. (Petitioners), submitted a Petition 
    pursuant to 10 CFR Sec. 2.206 to the U.S. Nuclear Regulatory Commission 
    (NRC). The Petition requested that the NRC (1) institute a show-cause 
    proceeding pursuant to 10 CFR Sec. 2.202 to modify, suspend, or revoke 
    the operating licenses of Arizona Public Service Company (licensee or 
    APS) for Palo Verde Nuclear Generating Station (PVNGS or Palo Verde); 
    (2) issue a notice of violation against the licensee for continuing to 
    employ The Atlantic Group (TAG) as a labor contractor at Palo Verde; 
    (3) investigate alleged material false statements made by William F. 
    Conway, Executive Vice President at Palo Verde, during his testimony at 
    a Department of Labor hearing (ERA Case No. 92-ERA-030) and, in the 
    interim, require that he be relieved of any authority over operations 
    at Palo Verde; (4) investigate the licensee's statements in a letter 
    dated August 10, 1993, from Mr. Conway to the former NRC regional 
    administrator, Mr. Bobby H. Faulkenberry, that Mr. Saporito gave 
    materially false, inaccurate, and incomplete information on his 
    application for unescorted access to Palo Verde and that, as a result, 
    Mr. Saporito lacks trustworthiness and reliability for access to Palo 
    Verde; (5) investigate the circumstances surrounding the February 1994 
    termination of licensee employee Joseph Straub, a former radiation 
    protection technician at Palo Verde, to determine if his employment was 
    illegally terminated by the licensee because he engaged in ``protected 
    activity'' during the course of his employment; (6) require the 
    licensee to respond to a ``chilling effect'' letter regarding the 
    circumstances surrounding Mr. Straub's termination from Palo Verde and 
    specify whether any measures were taken to ensure that his termination 
    did not have a chilling effect at Palo Verde; and (7) initiate 
    appropriate actions to require the licensee to immediately conduct eddy 
    current testing (ECT) on all steam generators (SGs) at Palo Verde 
    because the SG tubes were recently found to be subject to cracking.
        As the bases for these requests, the Petitioners allege that (1) a 
    show-cause proceeding is necessary (a) because the public health and 
    safety concerns alleged are significant and (b) to permit public 
    participation to provide NRC with new and relevant information; (2) 
    past practices of TAG demonstrate that employees of TAG were retaliated 
    against for having raised safety concerns while employed at Palo Verde; 
    (3) citations to testimony from transcripts and newspaper articles 
    (appended as exhibits to the Petition) demonstrate that Mr. Conway's 
    testimony is not credible; (4) statements in the letter of August 10, 
    1993, are inaccurate and materially false and characterize Mr. Saporito 
    as an individual lacking trustworthiness and reliability for access to 
    Palo Verde, and that such negative characterizations have caused the 
    nuclear industry to blacklist him from continued employment, all in 
    retaliation for his raising safety concerns about operations at Palo 
    Verde; thus, the Petitioners ask that these statements be rescinded; 
    (5) an investigation into the termination of Mr. Straub is warranted in 
    view of the fact that the licensee has engaged in similar illegal 
    conduct in the past for which the NRC has required the licensee to pay 
    fines; (6) Mr. Straub is entitled to reinstatement with pay and 
    benefits pending the NRC's investigation into his termination to offset 
    the chilling effect his termination had on the Palo Verde workforce; 
    and (7) in addition to cooling tower problems, the stress-corrosion and 
    cracking in the SGs is a recurring problem of which the licensee is 
    aware and has failed to properly correct, so that the NRC should be 
    concerned about proper maintenance of safety systems and equipment at 
    Palo Verde.
        On July 8, 1994, the Petitioners filed a supplemental Petition 
    (Petition supplement) raising six additional issues. The Petitioners 
    requested that the NRC (1) institute a show-cause proceeding pursuant 
    to 10 CFR Sec. 2.202 for the modification, suspension, or revocation of 
    the Palo Verde operating licenses for Units 1, 2, and 3; (2) modify the 
    Palo Verde operating licenses to require operation at 86-percent power 
    or less; (3) require the licensee to submit a No Significant Hazards 
    safety analysis 1 to justify operation of those units above 86-
    percent power; (4) take immediate action (e.g., by confirmatory order) 
    to require the licensee to reduce operation to 86-percent power or 
    less; (5) require the licensee to analyze a design-basis steam 
    generator tube rupture (SGTR) event to show that the offsite 
    radiological consequences do not exceed a small fraction of the limits 
    of 10 CFR Part 100; and (6) require the licensee to demonstrate that 
    its emergency operating procedures (EOPs) for steam generator (SG) tube 
    rupture events are adequate and the plant operators are sufficiently 
    trained in EOPs.
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        \1\  Section 50.91 of the Commission's regulations provides that 
    at the time a licensee requests an amendment it must provide the NRC 
    its analysis of the issue of no significant hazards consideration, 
    using the standards of Section 50.92.
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        As bases for these requests, the Petitioners allege that (1) the 
    licensee experienced an SGTR in the free-span area on Unit 2 on March 
    14, 1993; (2) during a January 1994 inspection on
    
    [[Page 34456]]
    
    Unit 2, 85 axial indications were identified, the longest indication 
    being 7.5 inches; (3) as of May 1994, 28 axial indications were found 
    at Unit 2 and 9 axial indications were found at Unit 1 (more extensive 
    testing will confirm the existence of circumferential crack indications 
    in the expansion and transition areas); (4) in May 1994, SG sludge from 
    Units 1 and 2 indicated a lead content of 4,000 to 6,000 ppm, which is 
    unusually high, accelerates the crevice corrosion process, and is 
    believed to be caused by a feedwater source deficiency; (5) in eight 
    instances, the licensee failed to properly implement operational 
    procedures during the SGTR event on March 14, 1993; (6) the licensee's 
    failure to comply with approved procedures in the above-mentioned event 
    is indicative of a problem plant that warrants further NRC action; (7) 
    in four instances, the NRC is aware of additional licensee weaknesses 
    regarding the SGTR event; (8) the licensee cannot ensure that the 
    radiation dose limits are satisfied for applicable postulated 
    accidents; (9) the licensee is not maintaining an adequate level of 
    public protection in that the offsite dose limits will be exceeded 
    during an SGTR; (10) the licensee cannot demonstrate that a Palo Verde 
    unit can safely be shut down and depressurized to stop SG tube leakage 
    before a loss of reactor water storage tank inventory; (11) SG tubes 
    are an integral part of the reactor coolant boundary and tube failures 
    could lead to containment bypass and the escape of radioactive fission 
    products directly into the environment and, therefore, must be 
    carefully considered by NRC and the licensee; (12) the licensee cannot 
    demonstrate compliance with 10 CFR Part 50, Appendix A, which 
    establishes the fundamental requirements for SG tube integrity; (13) 
    the licensee has failed to comply with NRC recommendations under NUREG-
    0800 to show that in the case of an SGTR event, ``the offsite 
    conditions and single failure do not exceed a small fraction of the 
    limits of 10 CFR Part 100''; and (14) the licensee has posed an 
    unacceptable risk to public health and safety by raising power on all 
    three Palo Verde units above 86 percent, considering the severe 
    degradation of the SG tubes.
        In a letter dated July 26, 1994, I acknowledged receipt of the 
    Petition of May 27, 1994, and the Petition supplement of July 8, 1994, 
    and denied the Petitioners' two requests for immediate action. The 
    Petitioners requested the initiation of actions to require the licensee 
    to immediately conduct ECT on all SGs at Palo Verde (Request 7 of the 
    May 27, 1994, Petition) and immediate action to cause the licensee to 
    reduce operation to 86-percent power or less (Request 4 of the July 8, 
    1994, Petition supplement). Although these two requests for immediate 
    action were denied, the concerns raised by the Petitioners regarding 
    their requests for ECT and reduced power operation are addressed in 
    this Decision.
        The staff informed the Petitioners that the remaining requests were 
    being evaluated under 10 CFR Sec. 2.206 of the Commission's regulations 
    and that a response would be forthcoming. This Decision addresses the 
    Petitioners' concerns about ECT (Request 7 of the May 27, 1994, 
    Petition), steam generator tube integrity, and emergency operating 
    procedures for SGTR events and the remaining requests (Requests 1, 2, 
    3, 5, and 6) of the July 8, 1994, supplement. The staff has completed 
    its review of the remaining issues in your supplemental Petition. A 
    Director's Decision (DD-96-04) regarding Requests 1 through 6 in the 
    Petition of May 27, 1994, was issued under separate cover letter on 
    June 3, 1996. A discussion of the Director's Decision follows.
    
    II. Background
    
        The Petitioners' concerns addressed in this Decision appear to be 
    based largely on the March 1993 SGTR event and the NRC staff findings 
    concerning that event set forth in the NRC Augmented Inspection Team 
    (AIT) 2 report. Palo Verde Unit 2 experienced an SGTR event in SG 
    No. 2 on March 14, 1993. At the time, the unit was at about 98-percent 
    power. The plant operators manually tripped the reactor, declared an 
    Unusual Event,3 which was subsequently upgraded to an Alert,4 
    and entered the PVNGS Functional Recovery Procedure 5 to mitigate 
    the event. The plant was cooled down and depressurized, and the event 
    was terminated when Mode 5 6 was achieved on March 15, 1993.
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        \2\ An AIT is an NRC inspection team composed of experts from 
    the responsible NRC Regional Office augmented by personnel from NRC 
    Headquarters and others Regions with special technical 
    qualifications. The purpose of an AIT is to determine the causes, 
    conditions, and circumstances relevant to an event and to 
    communicate its findings, safety concerns, and recommendations to 
    NRC management.
        \3\ The lowest level of emergency classification as delineated 
    in 10 C.F.R Part 50, Appendix E.
        \4\ The second lowest level of emergency classification as 
    delineated in 10 C.F.R. Part 50, Appendix E.
        \5\ PVNGS Procedures providing operators' actions for responding 
    to design basis events.
        \6\ The operational mode defined as cold shutdown in plant 
    technical specifications.
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        During the period March 17-25, 1993, an NRC AIT conducted an 
    inspection at PVNGS Unit 2. Overall, the AIT concluded that the 
    response to the SGTR succeeded in bringing the unit safely to a cold-
    shutdown condition and limiting the release of radioactivity so that 
    there was no threat to public health and safety. However, the AIT 
    identified weaknesses in the licensee's implementation of emergency 
    plan actions, including event classification, activation of the 
    emergency response facilities, and prompt assignment of tasks to onsite 
    personnel. Weaknesses were also found in the procedures, equipment, and 
    training associated with responding to an SGTR event. The AIT 
    inspection was documented in NRC Inspection Report No. 50-529/93-14, 
    issued on April 16, 1993.
        Enforcement action resulted from the AIT inspection in several 
    areas (e.g., emergency preparedness, chemistry and radiation 
    monitoring, and emergency operating procedures). All violations were 
    issued as Severity Level IV.7
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        \7\ See EA 93-119 (issued July 1, 1993) and EA 93-039 (issued 
    April 27, 1993). At the time, violations were categorized in terms 
    of five levels of severity. Severity Level I and II violations were 
    of very significant regulatory concern. Severity III violations were 
    cause for significant regulatory concern. Severity Level IV 
    violations were less serious but were of more than minor concern. 
    Severity Level V were of minor safety or environmental concern. 
    General Statement of Policy and Procedure for NRC Enforcement 
    Actions, 10 CFR Part 2, Appendix C, Section IV. Effective June 30, 
    1995, the NRC's Enforcement Policy, as published in the Federal 
    Register (60 FR 34381), is set forth in NUREG-1600.
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        The NRC issued a confirmatory action letter 8 (CAL) to the 
    licensee on June 4, 1993, for Unit 2. The NRC issued a safety 
    evaluation by letter dated August 19, 1993, concluding that Unit 2 
    could safely resume operation for 6 months, the interval between steam 
    generator tube inspections. This safety evaluation closed the CAL.
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        \8\  This CAL set forth commitments made by the licensee to the 
    NRC staff on June 2, 1993, regarding the SGTR event on Unit 2. In 
    the CAL, the staff confirmed the licensee's commitment (1) to notify 
    the NRC prior to completion of ECT on the Unit 2 SGs; (2) to include 
    the proposed operating interval to the next SG tube inspection in 
    its safety analysis; and (3) not to restart Unit 2 until the NRC 
    concurs with the restart of the facility.
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        The NRC issued a second CAL 9 on October 4, 1993, for Unit 3 
    (amended on
    
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    November 8 and 23, 1993), confirming the commitments made by the 
    licensee in its September 29, 1993, letter. By letter dated December 3, 
    1993, the licensee reported that it had completed the actions discussed 
    in the CAL. Satisfied that the licensee had completed the conditions of 
    the CAL, the staff closed the CAL by letter dated April 1, 1994.
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        \9\  In this CAL, the staff confirmed the licensee's commitment 
    to (1) shut down Unit 3 for ECT inspection of both SGs; (2) continue 
    the review of Unit 3 ECT data to identify indications that were not 
    identified in refueling outage 3R3 by bobbin coil ECT and to provide 
    a written summary of the review; (3) continue to implement the Unit 
    1 SG inspection plan (SGIP); (4) implement changes to emergency 
    operating procedures (EOPs), operator training, and leakage 
    monitoring; and (5) continue to operate Unit 3 to take advantage of 
    some of the preventive measures that can be taken to reduce outside-
    diameter stress corrosion cracking (ODSCC) rates.
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        The licensee voluntarily reduced power to approximately 86-percent 
    power in the fall of 1993 to minimize steam generator degradation. The 
    licensee evaluated and implemented several improvements to the 
    operation of its steam generators, one of which was a reduction in the 
    reactor coolant system hot-leg temperature. The units were all returned 
    to 100-percent power by the fall of 1994.
        Following a midcycle outage on Unit 2 and midcycle and refueling 
    outages on Unit 3, the NRC issued a safety evaluation on June 22, 1994, 
    which concluded that both Unit 2 and 3 could safely operate for 6 
    months between steam generator tube inspections. Since that time, there 
    have been additional midcycle outages on Units 2 and 3 and a refueling 
    outage on all three units. Eddy current inspection results and outage 
    planning for the Units currently support the following operating 
    intervals between inspections: Unit 1, 16 months; Unit 2, 12 months; 
    and Unit 3, 11 months.
    
    III. Discussion
    
    A. Eddy Current Testing on All Steam Generators at Palo Verde
    
        Item 7 of the Petitioners' letter of May 27, 1994, requested the 
    NRC to require the licensee to conduct immediate ECT on all SGs at Palo 
    Verde to ascertain the integrity and life expectancy of the SG tubes. 
    Although, as indicated above, this request for immediate action has 
    been denied, the Petitioners' concerns regarding ECT are addressed 
    below.
        The Petitioners assert as a basis (Petition Basis 7) for their 
    request concerning ECT that the licensee's SGs have recently developed 
    cracks in the free-span portion of their internal structure, that tube 
    stress corrosion and cracking is a recurring problem in SGs, and that 
    there is a risk the emergency cooling system will be unable to prevent 
    the melting of the fuel because of tube ruptures.10
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        \10\  The Petitioner also mentioned cooling tower problems in 
    this basis, stating that ``the NRC should be concerned about proper 
    maintenance of safety systems and equipment there.'' The cooling 
    towers at Palo Verde are not safety-related systems. If the cooling 
    towers of a unit were incapacitated, the unit might operate less 
    efficiently, but that would be an economic penalty, rather than a 
    safety problem. The Petitioners did not provide any specific 
    examples of problems with the cooling towers, though the staff is 
    aware of the general maintenance problems the licensee has had with 
    the cooling towers. This issue was the subject of a previous 
    Director's Decision, Arizona Public Service Company, (Palo Verde 
    Nuclear Generating Station, Units 1, 2, and 3, DD-92-1, 35 NRC 133, 
    137 (1992), which found no substantial nuclear safety concern with 
    the condition of the cooling towers.
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        The licensee has completed at least two eddy current inspections on 
    each of the Palo Verde units since the SGTR event in March 1993. The 
    staff issued safety evaluations (SEs) that addressed Unit 2 and 3 
    operating intervals by letters dated August 19, 1993, and June 22, 
    1994.11 These SEs were based on the results of the licensee's eddy 
    current inspections of Unit 1 in October 1993, of Unit 2 in May 1993 
    and January 1994, and of Unit 3 in December 1993 and May 1994. In 
    summary, the staff concluded that Units 2 and 3 could be safely 
    operated for up to 6 months between SG eddy current inspections. The 
    licensee conducted five of these ``minicycles'' 12 (three on Unit 
    2 and two on Unit 3), thereby obtaining extensive SG eddy current data, 
    which it used to validate models used for analysis. In May 1995, the 
    licensee submitted a report supporting a cycle length of up to 11 
    months on Unit 3. Unit 1 completed a 16-month operating cycle in June 
    1995. After meeting with the licensee, the staff approved a Unit 3 
    cycle length of 11 months in a meeting summary dated August 22, 1995. 
    During a September 20, 1995, meeting with the staff, the licensee 
    presented its submittal and arguments to support a 12-month cycle for 
    Unit 2. The staff incorporated data from the most recent Unit 3 steam 
    generator inspection in its evaluation of the licensee's conclusion 
    regarding a 12-month operating cycle on Unit 2. The staff approved the 
    12-month operating cycle by letter dated March 5, 1996.
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        \11\ Unit 1 was not directly addressed in the SEs because no 
    free span axial indications were identified on Unit 1 at the time.
        \12\ The Palo Verde operating cycle is normally 16-18 months.
    ---------------------------------------------------------------------------
    
        In summary, the licensee performed the necessary eddy current 
    inspections, and the staff extensively reviewed and approved Palo Verde 
    SG eddy current inspection results and continues to review additional 
    information regarding the integrity of the SG tubes. On the basis of 
    its review of ECT, the staff has concluded that the Petitioners' 
    concerns regarding the need for ECT have been satisfactorily addressed 
    by the licensee and that no further action by the NRC staff is 
    warranted.
    
    B. Operation Above 86-Percent Power
    
        Requests 1, 2, 3, and 4 of the Petition supplement, in essence, 
    request actions requiring the Palo Verde licenses to be modified to 
    require operation at 86-percent power or less.13
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        \13\ The specific request for immediate action to make the 
    licensee reduce operation to 86-percent power or less (Request 4) 
    was denied by letter of July 26, 1994. With regard to the request 
    (Request 3) to require the licensee to submit a No Significant 
    Hazards safety analysis to justify operation of the units above 86-
    percent power, the licensee is not required by the NRC regulations 
    to submit a no significant hazards analysis, since a TS change was 
    not required to resume operation above 86-percent power. The staff 
    did, however, review a no significant hazards analysis related to 
    operation of the Units at 100-percent power with a reduced hot-leg 
    temperature. These TS changes were submitted by the licensee on 
    February 18, 1994, for Units 1 and 3; and on July 1, 1994, for Unit 
    2. The NRC staff review of these TS changes and support for 
    operation at a power level of 100 percent is discussed at page 17, 
    infra.
    ---------------------------------------------------------------------------
    
        As bases for these requests, the Petitioners assert that on March 
    14, 1993, Palo Verde Unit 2 had an SGTR in the free-span section 
    between the tube supports and that in January 1994, an inspection of 
    Palo Verde's Unit 2 SGs found 85 axial indications (longest indication, 
    7.5 inches) (Petition supplement, Basis 2); and that as of May 1994, 28 
    axial indications were found at Unit 2 and 9 axial indications found at 
    Unit 1. The Petitioners believe that more extensive testing will 
    confirm the existence of circumferential crack indications in the 
    expansion-transition area (Petition supplement, Basis 3). The 
    Petitioners also assert that in May 1994, Units 1 and 2 SG sludge 
    indicated a lead content of 4,000-6,000 ppm, which would accelerate the 
    crevice corrosion cracking process (Petition supplement, Basis 4). The 
    Petitioners also stated that the operation of Palo Verde units at above 
    86-percent power is unacceptable due to severe degradation of the SG 
    tubes (Petition supplement, Basis 14).
    Axial and Circumferential Steam Generator Tube Indications
        With regard to the Petitioners' concern about identifiable axial 
    indications (Petition supplement Basis 2), it is correct that 85 axial 
    indications in the free-span area (longest indication, 7.5 inches) were 
    discovered on SG tubes at Palo Verde Unit 2 during the January 1994 
    inspection. However, this number was apparently based on preliminary 
    information from the licensee's eddy current inspection during the 
    January 1994 eddy current inspection. The licensee's report of March 8, 
    1994, stated that actually 330 free-span axial indications were 
    discovered during the Unit 2 first midcycle outage: 22 in SG 1 of Unit 
    2 (SG 21) and 308 in SG 2 of
    
    [[Page 34458]]
    
    Unit 2 (SG 22). Although a number of axial indications were detected by 
    the licensee, it is not the number of indications that is of a safety 
    concern but rather the severity of the indications (i.e., severity in 
    terms of whether the tube indication had adequate structural and 
    leakage integrity). As noted in the Petition supplement, the longest 
    indication was 7.5 inches long. The safety significance of this 
    indication, as with any eddy current indication, depends not only on 
    the length of the indication but also on the depth of the indication. 
    To assess the safety significance and/or severity of an indication, 
    licensees size the indications in terms of length, depth, and/or 
    voltage.14 However, eddy current testing methods have not been 
    qualified for determining the depth of stress corrosion cracks. Where 
    qualified eddy current methods do not exist, licensees may pursue 
    alternative methods such as in situ pressure testing 15 to further 
    confirm or assess the condition of the tube (i.e., to confirm that the 
    tube indication could withstand the required pressure loadings; thereby 
    demonstrating that the tube had adequate structural integrity). The 
    licensee did select nine tubes for in situ pressure testing during the 
    outage. The 7.5 inch long indication did not meet the licensee's 
    screening criteria for selecting the more severe indications. The 
    screening criteria, discussed in the NRC staff's SE of June 22, 1994, 
    considered the length, depth, and/or voltage of the indication. All 
    nine tubes satisfactorily passed the in situ pressure test thereby 
    providing reasonable assurance that the tube indications had adequate 
    structural integrity. Furthermore, all tubes with axial free span 
    indications were plugged before Unit 2 was returned to operation.
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        \14\  Voltage is electrical force or potential difference. 
    Voltage measurements can be used to estimate the severity of an 
    indication.
        \15\  In situ pressure tests were conducted to determine whether 
    the tubes could withstand the pressure loading specified in NRC 
    Regulatory Guide 1.121 (i.e., whether the SG tubes have adequate 
    structural integrity).
    ---------------------------------------------------------------------------
    
        The Petitioners also assert as of May 1994, 28 axial indications 
    were found on Unit 2 and 9 axial indications found at Unit 1 and that 
    more extensive testing would confirm the existence of circumferential 
    crack indications in the expansion transition areas (Petition 
    supplement, Basis 3). These numbers are incorrect. Neither Unit 1 nor 
    Unit 2 was in an outage conducting eddy current examinations in May 
    1994. Unit 1 had no axial indications identified as of this date. The 
    Unit 2 data is described above. Unit 3 was in an outage at this time 
    and identified a total of 20 axial indications. Regarding the 
    performance of more extensive testing to confirm the existence of 
    circumferential crack indications at the expansion transition area, the 
    licensee has performed inspections in this region. In general, the 
    licensee's steam generator tube inspection program consists of an 
    initial inspection sample which is expanded, if necessary, based on the 
    initial inspection sample results. The licensee has been examining the 
    expansion transition locations with a motorized rotating pancake coil 
    (MRPC) probe since, at least, 1993. These examinations permit the 
    licensee to detect circumferential crack indications. In its SEs and 
    meeting summaries, the NRC staff has reviewed the licensee's results 
    from its MRPC inspections and found them acceptable.16 To date, 
    Palo Verde Units 2 and 3 have each exhibited a small number of 
    circumferential crack indications per Unit. Unit 1 has exhibited the 
    most extensive circumferential cracking both in terms of number of 
    indications and the severity of the indications when compared to Units 
    2 and 3. Nonetheless, the staff concluded in a meeting summary dated 
    October 19, 1994, that operating Unit 1 to the end of the operating 
    cycle (April 1995) did not pose an undue risk to public health and 
    safety in view of (1) the absence of detectable axial free-span cracks 
    during the previous refueling outage inspection; (2) the improved 
    secondary water chemistry performance at Palo Verde; (3) the reduced 
    hot-leg temperature, which is expected to reduce crack growth rates; 
    and (4) the implementation of enhanced MRPC inspection techniques at 
    the expansion transition locations. The licensee will continue to 
    perform extensive SG inspections at the end of each operating cycle to 
    ensure continued safe operation of SGs.
    ---------------------------------------------------------------------------
    
        \16\ The Staff's reviews are documented in SEs dated August 19, 
    1993, and June 22, 1994, and also in meeting summaries dated August 
    22, 1995, March 22, 1994, October 19, 1994, August 22, 1995, and 
    September 20, 1995.
    ---------------------------------------------------------------------------
    
    Lead Content in Steam Generator Tube Sludge
        The Petitioners assert without providing any supporting basis that 
    the SG sludge of Units 1 and 2 has a lead content of 4,000-6,000 ppm 
    (Petition supplement, Basis 4). The licensee performed sludge analyses 
    during two consecutive Unit 1 outages. The data, which were reported in 
    a letter from the licensee dated November 2, 1993, indicate a lead 
    content of 78 ppm (from Unit 1, Refueling 3) and 98 ppm (Unit 1, 
    Refueling 4).17 Sludge samples were obtained from both Unit 2 SGs 
    after the March 1993 SGTR event. The data were documented in the 
    licensee's report, ``Equipment Root Cause of Failure.'' Both the 
    licensee and outside contractors analyzed the samples; all analyses 
    indicated a lead content of 100 ppm or less.
    ---------------------------------------------------------------------------
    
        \17\ During the Unit 2 midcycle outage in early 1994, the SGs 
    were chemically cleaned before sludge lancing; therefore, the 
    composition of the sludge was not tested.
    ---------------------------------------------------------------------------
    
        The NRC staff conducted two Palo Verde chemistry inspections 
    (Inspection Reports 94-15 and 94-27 on Units 50-528/50-529/50-530). The 
    staff reviewed films and sludge for their lead content, and the data 
    were consistent with the licensee's reports. Inspection Report 50-528/
    50-529/50-530/94-15 specifically referred to the inspector's 
    determination to note ``whether lead was detected, because of recent 
    work which indicated it may have a deleterious effect.'' In referring 
    to examinations of the burst region 18 of pulled tubes, the report 
    stated that insignificant levels of lead were found in the sludge and 
    in the films examined.
    ---------------------------------------------------------------------------
    
        \18\ Burst region refers to the section of the crack in a pulled 
    tube that is exposed as the result of a burst or rupture due to an 
    applied pressure either during plant operation or laboratory 
    testing.
    ---------------------------------------------------------------------------
    
        Inspection Report 50-528/50-529/50-530/94-15 also reviewed the 
    licensee's secondary water chemistry control program.19 The NRC 
    inspection team found that the program requirements had fully conformed 
    to the EPRI guidelines throughout Palo Verde's operating history with 
    respect to chemical parameters, analytical frequency, limits for 
    critical parameters, and required actions when critical parameters were 
    exceeded. In summary, the Petitioners' assertions regarding lead 
    content have not been substantiated and do not agree with available 
    data. The licensee has verified 20 that lead content in both Units 
    1 and 2 SGs is 100 ppm or less, not 4,000-6,000 ppm as asserted by the 
    Petitioners. Additionally, NRC Inspection Reports 94-15 and 94-27 on 
    Units 50-528/50-529/50-530 have not
    
    [[Page 34459]]
    
    revealed any information about elevated lead content.
    ---------------------------------------------------------------------------
    
        \19\ The NRC inspection team compared Electric Power Research 
    Institue (EPRI) NP-6239, ``PWR Secondary Water Chemistry 
    Guidelines,'' Revisions 1 through 2, and EPRI TR-101230, ``Interim 
    PWR Secondary Water Chemistry Recommendations for IGA/IGSCC 
    Control,'' with the licensee's secondary water chemistry control 
    program for PVNGS.
        \20\ PVNGS performed its own inspections and also utilized 
    contractors, ABB-Combustion Engineering (ABB-CE) and Babcock and 
    Wilcox Nuclear Technologies (BWNT), to perform metallurgical 
    examinations. The inspections revealed minor quantities of lead in 
    surface deposits and films. See NRC Inspection Report 50-528/50-529/
    50-530/94-15, dated June 23, 1994.
    ---------------------------------------------------------------------------
    
    Steam Generator Tube Degradation and Operation at a Reduced Power Level
        The Petitioners also assert that the operation of Palo Verde units 
    at above 86-percent power is unacceptable due to severe degradation of 
    SG tubes (Petition supplement, Basis 14). In December 1993, the 
    licensee volunteered to reduce power in all three units to 
    approximately 86 percent as an interim measure to curtail steam 
    generator degradation. The primary purpose of this administrative power 
    limit was to operate with a lower reactor coolant system hot-leg 
    temperature in order to reduce tube degradation. This specific power 
    level had been selected because it provided for a Thot that 
    approximated the value that would be implemented if the licensee's 
    proposed TS changes for operating at 100% power with a reduced 
    Thot were approved by the NRC. Additionally, the licensee's 
    thermal-hydraulic analysis indicated that, at this reduced power level, 
    the potential for freespan tube degradation from corrosion is reduced. 
    The licensee took this action voluntarily to minimize further 
    degradation of the SGs until corrective, mitigative, and preventive 
    actions could be implemented to reduce steam generator tube 
    degradation.
        On June 7, 1994, the NRC issued a TS change for Units 1 and 3 that 
    permitted the licensee to operate at full power with a lower Thot 
    temperature.21 The Unit 2 TS change was reviewed separately 
    because the licensee was continuing to perform analyses arising from 
    the SG tube plugging in Unit 2. The staff issued this TS change on 
    August 12, 1994.22 These TS changes permitted operation at a power 
    level of 100 percent as did the staff's post-March 1993 SGTR SEs dated 
    August 19, 1993, and June 22, 1994, regarding the length of operating 
    cycles of the Palo Verde units. Furthermore, as stated above, the staff 
    did not impose any power restrictions or limits on the licensee.
    ---------------------------------------------------------------------------
    
        \21\ Noticed in the Federal Register on June 22, 1994 (59 Fed. 
    Reg. 32240).
        \22\ Noticed in the Federal Register on August 31, 1994 (59 Fed. 
    Reg. 45038).
    ---------------------------------------------------------------------------
    
        In summary, the Petitioners' concerns regarding operation of the 
    Palo Verde units above 86-percent power (including bases relating to 
    the March 1993 SGTR event, identification of axial and circumferential 
    steam generator tube indications, alleged elevated lead contents in 
    steam generator sludge) have been satisfactorily addressed, and do not 
    warrant any further action by the NRC staff.
    
    C. Need To Reanalyze the Design-Basis SGTR Event
    
        Request 5 (of the Petition supplement) is that the NRC require the 
    licensee to analyze a design-basis SGTR event to show that the offsite 
    radiological consequences do not exceed a small fraction of the limits 
    of 10 CFR Part 100. The staff requires an analysis such as this to be 
    completed for all pressurized-water reactors (PWRs) and documented in a 
    final safety analysis report (FSAR) before plant operation. The 
    licensee complied with this requirement.23
    ---------------------------------------------------------------------------
    
        \23\ Updated Final Safety Analysis Report (UFSAR) Section 
    15.6.3.1.3.2 describes the radiological consequences of an SGTR, and 
    the results are shown in UFSAR Table 15.6.3-5. The staff initially 
    reviewed PVNGS's UFSAR in November 1981.
    ---------------------------------------------------------------------------
    
        The Petitioners assert in the basis (Petition supplement, Bases 8, 
    9, 10, 11 and 13) that the licensee cannot ensure the dose limits are 
    satisfied for applicable postulated SGTR events; the offsite dose 
    limits would be exceeded during an SGTR event and adequate protection 
    to the public would not be maintained; the licensee cannot demonstrate 
    that the plant can be safely shut down and depressurized to stop SG 
    tube leakage before reactor water storage tank inventory is lost; the 
    NRC and the licensee must carefully consider SGTR; and ``the licensee 
    has failed to comply with NRC requirements under NUREG-0800 insofar as 
    the licensee is required to analyze the consequences of a design basis 
    SGTR event to show that the offsite conditions and single failure do 
    not exceed a small fraction of limits of 10 CFR Part 100.''
        The AIT report documents findings regarding the Unit 2 SGTR event 
    of March 1993. The report stated that the plant was safely brought to 
    cold shutdown and no radioactivity was released off site. Additionally, 
    the staff's SE, dated August 19, 1993, assessed a single SGTR event and 
    single and multiple tube ruptures induced by a major secondary-side 
    rapid depressurization and concluded that the radiological consequences 
    were within applicable limits.24 Finally, in a memorandum dated 
    January 26, 1996, the staff performed a confirmatory review of the 
    licensee's updated SGTR event analysis, submitted with Revision 6 to 
    the FSAR (March 10, 1994), and concluded that the results are 
    acceptable. The Petitioners also assert in the basis (Petition 
    supplement, Basis 12) that the licensee cannot demonstrate compliance 
    with certain criteria of Appendix A to 10 CFR Part 50,25 which 
    establishes the fundamental requirements for steam generator tube 
    integrity. However, the Petitioners have failed to provide any details 
    or support for this assertion.
    ---------------------------------------------------------------------------
    
        \24\ In 10 CFR Part 100, acceptance criteria are specified for 
    the dose analyzed during initial plant licensing at the exclusion 
    area boundary (EAB) and low population zone (LPZ) for design-basis 
    accidents. The dose in 2 hours at the EAB is not to exceed 25 rem to 
    the whole body or 300 rem to the thyroid. The dose in 30 days at the 
    boundary of the LPZ is not to exceed 25 rem to the whole body or 300 
    rem to the thyroid. The staff reviewed the licensee's Unit 2 steam 
    generator tube rupture analysis, submitted by letter dated July 18, 
    1993, and concluded that the methods used by the licensee were 
    acceptable. See the NRC staff's safety evaluation dated August 19, 
    1993.
        The Petitioners assert that the licensee has failed to comply 
    with NUREG-0800 requirements regarding consequences of a design 
    basis SGTR event. However, NUREG-0800 does not set forth 
    requirements; rather it sets forth acceptable approaches to 
    satisfying NRC requirements.
        \25\ The Petitioners reference portions of General Design 
    Criteria (GDC) 14, 15, 30, and 31 of Appendix A to 10 CFR Part 50.
    ---------------------------------------------------------------------------
    
        In summary, on the basis of the NRC staff's review of the 
    licensee's design-basis SGTR event and more recent confirmatory review, 
    the staff has concluded that the Petitioners have not presented a basis 
    for further NRC action.
    
    D. Adequacy of Training and Procedures for an SGTR Event
    
        Regarding Request 6 of the Petition supplement, that the NRC 
    require the licensee to demonstrate that its emergency operating 
    procedures (EOPs) for SGTR events are adequate and the plant operators 
    are sufficiently trained in EOPs, the staff has already taken 
    sufficient action. The Petitioners allege (Petition supplement, Bases 
    5, 6, and 7, respectively) that the licensee failed to properly 
    implement operational procedures regarding the SGTR event of March 14, 
    1993, citing eight instances in Basis 5 26; that the licensee's 
    failure to comply with approved procedures in this event is indicative 
    of a problem plant that warrants further NRC attention (Basis 6); and 
    that the NRC is aware of additional licensee weaknesses regarding the 
    SGTR event, citing four instances in Basis 7.27 These bases
    
    [[Page 34460]]
    
    largely concern areas the staff reviewed after the SGTR event on March 
    14, 1993. Specifically, the Petitioners repeated several of the 
    procedural and operator weaknesses that were described and evaluated in 
    the staff's AIT report (Inspection Report 50-529/93-14, dated April 16, 
    1993).28 Specifically, the AIT report stated that the use of a 
    diagnostic logic tree caused the operators to misdiagnose the SGTR 
    event twice and subsequently enter a Functional Recovery Procedure, 
    contributing substantially to the delay in isolating the faulted steam 
    generator. The staff concluded in its safety evaluation of August 19, 
    1993, that the licensee's modifications to the EOPs and the subsequent 
    operator training provide sufficient enhancement for both diagnosis and 
    mitigation of various SGTR scenarios.
    ---------------------------------------------------------------------------
    
        \26\ The Petitioners assert (Petition supplement, Basis 5) that 
    the licensee (a) failed to classify the event in accordance with the 
    EOPs, (b) failed to actuate the Emergency Operations Facility for 
    the 1-hour time, (c) failed to activate the Emergency Response Data 
    System, (d) violated 10 CFR Sec. 50.72 requirements, activation of 
    the Emergency Response Data System, (e) failed to take prompt 
    corrective actions to repair the condenser vacuum pump exhaust 
    radiation monitor, (f) failed to obtain required approvals for alarm 
    setpoint change on waste gas area combined ventilation exhaust 
    monitor, (g) failed to fully implement an alarm response procedure 
    and, (h) failed to check the owner-controlled area.
        \27\ The Petitioners assert (Petition supplement, Basis 7) that 
    the licensee's (a) alert and alarm setpoints for condenser vacuum 
    pump exhaust and main steam line radiation monitor limits appear to 
    be based on offsite dose limits rather on an SGTR event, (b) 
    simulator alarms occur within 2-3 minutes of an SGTR event, contrary 
    to control room indications, (c) plant staff failed to fully respond 
    to assembly notification, (d) plant staff failed to perform a formal 
    evaluation of the safety significance of an abnormal crack growth in 
    the Unit 2 SG.
        \28\ The licensee addressed the issues raised in the AIT report 
    by implementing the necessary procedural changes and providing 
    training. For example, with regard to the AIT finding (summarized by 
    the Petitioners) regarding differences between alarm response on the 
    simulator and in the control room, the staff's safety evaluation of 
    August 19, 1993, stated that ``the simulator has been modified to 
    more realistically model the plant, particularly the response of the 
    radiation monitoring system to an SGTR.''
    ---------------------------------------------------------------------------
    
        Additionally, the licensee recently revised its EOPs to make them 
    consistent with Combustion Engineering Owners Group (CEOG) guidance 
    (CEN 0152, Rev. 3 29). NRC Inspection Report 50-528/50-529/50-530/
    95-12, dated July 27, 1995, documents the staff's observations on the 
    ``high intensity team'' training conducted for each crew in preparation 
    for implementing the EOPs. In the inspection report, the staff stated 
    that the EOPs enhanced crew performance and allowed for greater 
    flexibility in responding to events. As an example, during the 
    simulator-based SGTR scenario, the crew was able to isolate the faulted 
    SG within 14 minutes of the start of the event. In contrast, during the 
    March 1993 Unit 2 SGTR event, operators took about 3 hours to isolate 
    the faulted SG, partly because of restrictions in the EOPs in use at 
    the time. The staff will further evaluate the effectiveness of EOPs 
    during future licensed operator examinations.
    ---------------------------------------------------------------------------
    
        \29\ A letter from the NRC to Combustion Engineering dated 
    August 2, 1988, stated that, ``pending NRC final review and 
    approval, CE facilities may base their plant-specific emergency 
    operating procedures on Revision 3 of CEN-152. Should future NRC 
    review reveal modifications to Revision 3 to be necessary, CE 
    facilities would be expected to update their procedures to reflect 
    the identified changes. Schedules for such changes should be based 
    on perceived safety significance of the changes.'' The objective of 
    the CEN-152 report is to describe the CEOG emergency procedure 
    guidelines system. The report contains the methodology used to 
    develop and validate the licensee's emergency procedure guidelines 
    and information on the implementation of guidelines.
    ---------------------------------------------------------------------------
    
        On the basis of its review of the Petitioners' request that the 
    licensee demonstrate that its EOPs for SGTR events are adequate and 
    that plant operators are sufficiently trained in EOPs, the staff has 
    concluded that the Petitioners have not presented a basis for further 
    NRC action.
    
    III. Conclusion
    
        The institution of proceedings in response to a request pursuant to 
    Section 2.206 is appropriate only when substantial health or safety 
    issues have been raised. See Consolidated Edison Co. of New York 
    (Indian Point, Units 1, 2, and 3), CLI-75-8, 2 NRC 173, 176 (1975), and 
    Washington Public Power Supply System (WPPSS Nuclear Project No. 2), 
    DD-84-7, 19 NRC 899, 923 (1984). This standard has been applied to the 
    concerns raised by the Petitioners to determine whether the actions 
    requested by the Petitioners are warranted. With regard to the specific 
    requests made by the Petitioners discussed herein, the NRC staff finds 
    no basis for taking additional actions beyond those described above. 
    Accordingly, the Petitioners' requests for additional actions pursuant 
    to Section 2.206, specifically Requests 1, 2, 3, 5, and 6 submitted in 
    the Petitioners' supplement dated July 8, 1994, are denied. 
    Accordingly, no action pursuant to Section 2.206 is being taken in this 
    matter.
        A copy of this Decision will be filed with the Secretary of the 
    Commission for Commission review in accordance with 10 CFR 
    Sec. 2.206(c) of the Commission's regulations. As provided by this 
    regulation, the Decision will constitute the final action of the 
    Commission 25 days after issuance, unless the Commission, on its own 
    motion, institutes a review of the Decision within that time.
    
        Dated at Rockville, Maryland, this 25th day of June 1996.
    
        For the Nuclear Regulatory Commission.
    William T. Russell,
    Director, Office of Nuclear Reactor Regulation.
    [FR Doc. 96-16878 Filed 7-1-96; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
07/02/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
96-16878
Pages:
34454-34460 (7 pages)
Docket Numbers:
Docket Nos. 50-528, 50-529 and 50-530
PDF File:
96-16878.pdf