94-17503. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 59, Number 138 (Wednesday, July 20, 1994)]
    [Unknown Section]
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    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 94-17503]
    
    
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    [Federal Register: July 20, 1994]
    
    
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    NUCLEAR REGULATORY COMMISSION
     
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from June 24, 1994, through July 8, 1994. The 
    last biweekly notice was published on July 6, 1994 (59 FR 34657).
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC 
    20555. The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By August 19, 1994, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC 20555 and at the local 
    public document room for the particular facility involved. If a request 
    for a hearing or petition for leave to intervene is filed by the above 
    date, the Commission or an Atomic Safety and Licensing Board, 
    designated by the Commission or by the Chairman of the Atomic Safety 
    and Licensing Board Panel, will rule on the request and/or petition; 
    and the Secretary or the designated Atomic Safety and Licensing Board 
    will issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1) (i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    room for the particular facility involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station (PVNGS), 
    Unit Nos. 1, 2, and 3, Maricopa County, Arizona
    
        Date of amendment requests: June 17, 1994.
        Description of amendment requests: The proposed changes would 
    enhance the PVNGS technical specifications (TS) by removing five tables 
    of component lists in accordance with NRC Generic Letter (GL) 91-08, 
    ``Removal of Component Lists from Technical Specifications.'' The 
    affected tables are 3.3-9B, 3.3-9C, 3.6-1, 3.8-2, and 3.8-3. The 
    references to these five tables will also be removed from the text of 
    the TS in accordance with the sample TS change amendment provided by 
    the NRC in GL 91-08. These five removed tables will be incorporated 
    into a new document, which will be administratively controlled 
    according to the change controls provisions of the TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensees have 
    provided their analysis about the issue of no significant hazards 
    consideration, which is presented below:
        Standard 1--Involve a significant increase in the probability or 
    consequence of an accident previously evaluated:
        The proposed amendment will remove five tables of component lists 
    from the TS and add them to an administratively controlled document 
    which is subject to the change controls provisions of the TS. The new 
    location of the affected component lists is easily retrievable. The 
    existing TS requirements and those components to which they apply are 
    not altered by this TS amendment. There are no changes to the 
    operations, maintenance, surveillance, and/or qualification of any 
    component on the removed lists. Therefore, the probability of 
    occurrence and the consequences of any previously evaluated accident is 
    [sic] not changed.
        Standard 2--Create the possibility of a new or different kind of 
    accident from any accident previously evaluated:
        The TS requirements and the components to which they apply are not 
    altered by this amendment. The removed component lists are added to a 
    controlled and easily retrievable document. This amendment has no 
    impact on plant operations, maintenance, testing, or component 
    qualification. Therefore, the possibility of a new or different kind of 
    accident is not created by this amendment.
        Standard 3--Involve a significant reduction in a margin of safety:
        The removal of these five component lists from the TS does not 
    alter existing TS requirements or those components to which they apply. 
    These lists will be added to an administratively controlled document 
    which is subject to the controls provisions of the TS. More 
    specifically, there is no impact on safe plant shutdown, maintenance or 
    hot standby, containment isolation capability, containment leakage 
    rate, and/or the operability of safety related valves. Therefore, 
    removal of these five component lists from the TS will not involve a 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensees' analysis and, based on 
    that review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004.
        Attorney for licensees: Nancy C. Loftin, Esq., Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999.
        NRC Project Director: Theodore R. Quay.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert County, 
    Maryland
    
        Date of amendments request: May 27, 1994.
        Description of amendments request: The proposed amendment would 
    revise the Technical Specification surveillance test interval from 
    monthly to quarterly for several channel functional tests for the 
    Reactor Protective System and the Engineered Safety Feature Actuation 
    System (ESFAS). In addition, an administrative change to the ESFAS 
    table would remove an out-of-date footnote concerning the emergency 
    diesel generator logic circuit modifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Would not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The Reactor Protective System (RPS) and the Engineered Safety 
    Features Actuation System (ESFAS) provide the actuation signals to 
    safety equipment necessary to mitigate design basis accidents and 
    transients. The proposed change would increase the surveillance test 
    interval from monthly to quarterly for several of the RPS and ESFAS 
    instrumentation channel functional tests. The RPS/ESFAS instruments are 
    not an initiator in any previously evaluated accidents. Therefore, the 
    proposed changed does not involve an increase in the probability of an 
    accident previously evaluated. The required plant-specific setpoint 
    drift analysis for Calvert Cliffs demonstrated that the observed 
    changes in instrument uncertainties for the extended surveillance test 
    interval do not exceed the current 30-day setpoint assumptions. This 
    provides confidence the 90-day test interval will not impact the 
    ability to detect and monitor system degradation. Therefore, the 
    proposed change will not change the ability of the RPS/ESFAS 
    instrumentation to respond to and mitigate the consequences of any 
    previously evaluated accident. In addition, an obsolete footnote is 
    removed from ESFAS Table 4.3-2.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        2. Would not create the possibility of a new or different type of 
    accident from any accident previously evaluated.
        The proposed extended surveillance test interval for the RPS and 
    ESFAS and the removal of the obsolete footnote does not involve any 
    changes in equipment or the function of these instruments. The proposed 
    change does not represent a change in the configuration or operation of 
    the plant. The RPS and ESFAS setpoints will not be changed as the 
    instrument uncertainties resulting from the proposed surveillance test 
    interval (calculated using actual plant data) are less than the 
    instrument uncertainties assumed for the current surveillance interval. 
    Therefore, the proposed change does not create the possibility of a new 
    or different type of accident from any accident previously evaluated.
        3. Would not involve a significant reduction in a margin of safety.
        The proposed change will not affect the functions of the RPS or the 
    ESFAS instruments. The CEN-327 and CEN-327, Supplement 1, topical 
    reports quantified the corresponding changes in core melt frequency for 
    the representative fault tree models that were developed for Calvert 
    Cliffs. The proposed change has two principal effects with opposing 
    impacts on core melt frequency. The first impact is a slight increase 
    in core melt frequency that results from the increased unavailability 
    of the instrumentation in question. This assumed unavailability results 
    from less frequent testing. The unavailability of the tested 
    instrumentation components represents the potential for the failure of 
    the reactor to trip, an Anticipated Transient Without Scram, or a 
    failure of the appropriate engineered safety features to actuate when 
    required. The opposing impact on core melt risk is the corresponding 
    reduction in core melt frequency that would result due to the reduced 
    exposure of the plant to test-induced transients. The two changes are 
    nearly equal and the net result is no distinguishable effect on plant 
    safety. The NRC issued a Safety Evaluation Report which found that 
    these evaluations were acceptable for justifying the extensions in the 
    surveillance test intervals for the RPS and ESFAS from 30 days to 90 
    days.
        The RPS and ESFAS setpoints will not be changed since the 
    instrument drift resulting from the proposed surveillance test interval 
    is less than the instrument drift presently assumed for the current 
    surveillance interval. This provides confidence the 90-day test 
    interval will not impact the ability to detect and monitor system 
    degradation. The removal of the ESFAS Table footnote only removes 
    obsolete information from the Technical Specifications. The conclusions 
    of the accident analyses in the Calvert Cliffs Updated Safety Analysis 
    Report remain valid and the safety limits continue to be met. 
    Therefore, the proposed change does not involve a significant reduction 
    in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Michael L. Boyle.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert County, 
    Maryland
    
        Date of amendments request: June 8, 1994.
        Description of amendments request: The proposed amendments would 
    revise the Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2 (CC1/
    2), Technical Specifications (TS) 4.6.2.2.b to extend the surveillance 
    interval for the containment fan coolers from 18 months to 24 months. 
    The requested changes have been submitted in accordance with Generic 
    Letter (GL) 91-04, ``Guidance on Preparation of a License Amendment 
    Request for Changes in Surveillance Intervals to Accommodate a 24-Month 
    Fuel Cycle.'' These proposed amendments are part of a series of 
    requests that will eliminate the need for mid-cycle surveillance 
    outages to accommodate the existing 18 month surveillance requirements 
    since CC1-2 is operating on 24-month fuel cycles.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Would not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The purpose of the Containment Air Cooling (CAC) System is to cool 
    the containment atmosphere, and thereby limit containment pressure and 
    temperature, following a Loss of Coolant Accident (LOCA) or Main Stream 
    Line Break in containment. Failure of the CAC System is not an 
    initiator for any previously analyzed accident. Therefore, the proposed 
    change does not involve an increase in the probability of an accident 
    previously evaluated.
        Historical CAC System reliability, monthly surveillances and 
    monitoring of CAC-related plant parameters provide assurance that 
    undetected system degradation will not occur between 24-month 
    surveillances, and the system will continue to perform its safety 
    function. Therefore, there will be no significant increase in the 
    consequences of accidents previously evaluated. Therefore, the proposed 
    Technical Specification change does not increase the probability or 
    consequences of an accident previously evaluated.
        2. Would not create the possibility of a new or different type of 
    accident from any accident previously evaluated.
        This requested revision to increase the interval for a CAC 
    surveillance from 18 to 24 months does not involve a significant change 
    in the design or operation of the plant. No hardware is being added to 
    the plant as part of the proposed change. The proposed change will not 
    introduce any new accident initiators. Therefore, the proposed change 
    would not create the possibility of a new or different type of accident 
    from any accident previously evaluated.
        3. Does operation of the facility in accordance with the proposed 
    amendment involve a significant reduction in a margin of safety.
        The CAC System provides a margin of safety by providing a means by 
    which containment pressure can be limited following a LOCA or Main 
    Steam Line Break. The proposed change does not affect the operation or 
    design of the CAC System. Historical monthly surveillances and Control 
    Room indications give assurance that the reduction in surveillance 
    frequency will not adversely affect our ability to detect degradation 
    in the system. Therefore, the proposed change does not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Michael L. Boyle.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert County, 
    Maryland
    
        Date of amendments request: June 8, 1994.
        Description of amendments request: The proposed amendments would 
    revise the Calvert Cliffs Nuclear Power Plant, Units 1 and 2, Technical 
    Specifications 4.8.1.1.1.b to extend the alternate 69 kV offsite power 
    circuit surveillance frequency from 18 to 24 months.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Would not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The purpose of the 69 kV Southern Maryland Electric Cooperative 
    (SMECO) power source is to act as an independent energy source for 
    achieving and maintaining safe shutdown of the plant if the 500 kV 
    system is not available. Failure of the 69 kV SMECO system is not an 
    initiator for any existing accident. Therefore, the proposed change 
    does not involve an increase in the probability of an accident.
        The 69 kV SMECO system could be used to mitigate the consequences 
    of accidents involving a loss of primary offsite power. However, the 
    accident analyses assume that if the 500 kV circuits were not 
    available, the Emergency Diesel Generators would be used to provide 
    power to maintain the plant in a safe shutdown condition. A historical 
    review of surveillance test results indicates the system has 
    experienced only one significant failure in the last ten years. In 
    addition, the system is routinely used.
        However, the SMECO system is not assumed to function in our 
    accident analysis, so this change will result in no significant 
    increase in the consequences of accidents previously evaluated. 
    Therefore, the proposed Technical Specification change does not 
    increase the probability or consequences of an accident previously 
    evaluated.
        2. Would not create the possibility of a new or different type of 
    accident from any accident previously evaluated?
        This requested increase in the interval for a 69 kV SMECO 
    surveillance from 18 to 24 months does not involve a significant change 
    in the design or operation of the plant. No hardware is being added to 
    the plant of the proposed change. The proposed change will not 
    introduce any new accident initiators. Therefore, the proposed change 
    would not create the possibility of a new or different type of accident 
    from any accident previously evaluated.
        3. Does operation of the facility in accordance with the proposed 
    amendment involve a significant reduction in a margin of safety?
        The 69 kV SMECO system provides a margin of safety by providing an 
    alternate offsite electrical power source. The proposed change does not 
    affect the operation or design of the 69 kV SMECO system. Historical 
    surveillance data and routine use indicates that the reduction in 
    surveillance frequency will not adversely affect our ability to detect 
    degradation in the system. Therefore, the proposed change does not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Michael L. Boyle
    
    Baltimore Gas and Electric Company, Docket No. 50-318, Calvert Cliffs 
    Nuclear Power Plant, Unit No. 2, Calvert County, Maryland
    
        Date of amendment request: May 27, 1994.
        Description of amendment request: This amendment would revise the 
    existing heatup and cooldown curves and rates to increase their 
    applicability to 30 Effective Full-Power Years (EFPY). The fluence 
    value that was used to determine the heatup and cooldown curves was 
    based on the peak fluence and EFPY at the end of Cycle 9 and the peak 
    predicted fluence for Cycles 10 and beyond. In addition, a variable-
    setpoint low-temperature overpressure protection (VLTOP) system is 
    being installed to increase the allowable operating pressure band in 
    the Low-Temperature Overpressure Protection (LTOP) region. The VLTOP 
    system uses a variable power-operated relief valve setpoint to take 
    advantage of increased Appendix G pressure limits at increased reactor 
    coolant system (RCS) temperatures. This system will increase the 
    operating window in which the plant may operate during heatup and 
    cooldown.
        Specifically, this amendment would revise the Unit No. 2 heatup and 
    cooldown curves and rates for the following Technical Specification 
    (TS) sections. TS Section 3.4.9.1.a would be revised to decrease the 
    maximum heatup rate from a fixed value of 75  deg.F/hr to a more 
    conservative variable heatup rate of 30  deg.F to 60  deg.F/hr which 
    varies with RCS temperature range from 70  deg.F to greater than 246 
    deg.F. TS Section 3.4.9.1.b would be revised to increase the RCS 
    temperatures for the maximum allowable cooldown rates. TS Figures 
    3.4.9-1 and 3.4.9-2 would be replaced by new RCS pressure Temperature 
    Limits. The revised curves and rates are based on the predicted fluence 
    value for Cycle 10 and beyond.
        The following TS sections would be revised to support modifications 
    to the LTOP system. TS sections 3.4.9.3.a.1 and 3.4.9.3.a.2 would be 
    changed to ``trip setpoint below the curve in Figure 3.4.9-3*'' to 
    account for the VLTOP system. The footnote, ``When on shutdown cooling, 
    the PORV trip setpoint shall be less than or equal to 443 psia,'' has 
    been added for Shutdown Cooling Operation to maintain an extra setpoint 
    that is independent of RCS temperature and is equal to the lowest 
    variable setpoint. The Minimum Pressure and Temperature (MPT) Enable 
    would be changed from 305  deg.F to 301  deg.F. This change would 
    effect TS sections 3.1.2.1, 3.1.2.3, Table 3.3-3, 3.4.1.2, 3.4.1.3, 
    3.4.3, 3.4.9.3, 4.5.2, and 3.5.3. Due to the lower MPT Enable 
    temperature, the transition region at which the high pressure safety 
    injection pumps are placed under manual control on cooldown and 
    restored to automatic status on heatup would be changed from a 
    temperatue range of 305  deg.F-350  deg.F, to 301  deg.F-325  deg.F. 
    This affects TS 3.5.3 and Table 3.3-3. TS Bases Sections B3/4.4.1, B3/
    4.4.9, and 3/4.5.2 would change to be consistent with the proposed 
    change and to provide additional clarification of some of the existing 
    bases.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Would not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The Low Temperature Overpressure Protection (LTOP) system, 
    including the administrative controls, ensures that the 10 CFR Part 50, 
    Appendix G, Pressure-Temperature (P-T) limits for the reactor pressure 
    vessel will not be violated while operating at low temperatures. The 
    heatup and cooldown curves are conservatively developed in accordance 
    with the fracture toughness requirements of 10 CFR Part 50, Appendix G, 
    as supplemented by the American Society of Mechanical Engineers Boiler 
    and Pressure Vessel Code Section III, Appendix G. The reactor vessel 
    material Adjusted RTNDT values are based on the conservative 
    methodology provided in Regulatory Guide 1.99, Revision 2.
        Analyses show that the proposed use of a variable LTOP system will 
    not result in a significant increase in the probability of an 
    inadvertent opening of a Power-Operated Relief Valve (PORV) causing a 
    small break Loss-of-Coolant-Accident. The proposed heatup and cooldown 
    curves and associated limits continue to provide conservative 
    restrictions on Reactor Coolant System (RCS) pressure to minimize 
    material stresses in the RCS due to normal operating transients, thus 
    minimizing the likelihood of a rapidly propagating fracture due to 
    pressure transients at low temperatures. Because the proposed heatup 
    and cooldown curves and rates are based on conservative Appendix G 
    methods, and because the LTOP controls protect the Appendix G P-T 
    limits, the proposed curves and limits do not involve an increase in 
    the probability of accidents previously evaluated.
        The proposed use of a variable PORV trip setpoint and the increase 
    in the allowable fluence at the reactor vessel wall results in the 
    changes to the heatup and cooldown curves and rates, the Minimum 
    Pressure and Temperature (MPT) Enable temperature, and high pressure 
    safety injection pump manual control transition temperature. These 
    proposed changes continue to provide sufficient margin to accommodate 
    postulated pressurization from mass and energy addition transients. 
    Calculations have been performed that predict the response to such 
    transients. Because the results of the analyses remain well within the 
    conservative acceptance limits of Appendix G, these changes do not 
    increase the consequences of accidents previously evaluated.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        2. Would not create the possibility of a new or different type of 
    accident from any accident previously evaluated.
        The new variable LTOP control system along with the proposed 
    changes to the Technical Specifications will ensure that the Appendix G 
    P-T limits will not be violated during low temperature operations. 
    While setpoints and curves have changed, this proposed change does not 
    introduce any operator actions that are significantly different from 
    current operator actions used at the plant. The variable LTOP system 
    will continue to have redundant channels to ensure that no single 
    equipment failure or operator error will result in violation of the P-T 
    limits. The use of a variable LTOP system does not create a new failure 
    mechanism for the PORV. The failure mechanism for the PORV continues to 
    be an inadvertent opening or the failure to open during a pressure 
    transient which has been previously evaluated. Therefore, the proposed 
    change does not create the possibility of a new or different type of 
    accident from any accident previously evaluated.
        3. Would not involve a significant reduction in a margin of safety.
        This change will ensure that the margin of safety is maintained 
    with respect to energy or mass addition events in that none of the 
    events postulated could challenge the Appendix G limits. The proposed 
    use of a variable PORV trip setpoint and the increase in the allowable 
    fluence at the reactor vessel wall necessitate the changes to the 
    heatup and cooldown curves and rates, the MPT Enable temperature, and 
    high pressure safety injection pump manual control transition 
    temperature. These changes ensure that the margin of safety is 
    maintained by protecting the Appendix G limits for all postulated 
    transients. Therefore, the proposed change does not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Michael L. Boyle.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-324, 
    Brunswick Steam Electric Plant, Units 1 and 2, Brunswick County, North 
    Carolina
    
        Date of amendments request: June 17, 1994.
        Description of amendments request: The proposed amendments would 
    revise the Technical Specifications (TS) to (1) remove the heatup and 
    cooldown curves from TS 3/4.4.6 and relocate them to a newly created 
    Pressure and Temperature Limits Report, and (2) remove the reactor 
    vessel material surveillance program withdrawal schedule from TS Table 
    4.4.6.3-1 and relocate it to the Updated Final Safety Analysis Report.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment [sic] does not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated because the changes are administrative in nature. These 
    changes do not alter the configuration or operation of the facility. 
    The Limiting Safety Systems Settings and Safety Limits specified in the 
    current Technical Specifications remain unchanged.
        2. The proposed amendment [sic] does not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated. The safety analysis of the facility remains complete and 
    accurate. There are no physical changes to the facility and the plant 
    conditions for which the design basis accidents have been evaluated are 
    still valid. The operating procedures and emergency procedures are 
    unaffected.
        3. The proposed amendment [sic] does not involve a significant 
    reduction in the margin of safety because these margins are established 
    through the Limiting Conditions of Operation, Limiting Safety System 
    Settings and Safety Limits specified in the Technical Specifications, 
    and since there are no changes to the physical design or operation of 
    the facility, these margins will not be changed.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602.
        NRC Project Director: William H. Bateman.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station, Units 1 and 2, Lake County, Illinois
    
        Date of amendment request: January 19, 1994.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications by increasing the minimum reactor 
    coolant system temperature required for criticality from 500 degrees 
    Fahrenheit to 530 degrees Fahrenheit.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change does not result in a significant increase in 
    the probability or consequences of accidents previously evaluated. The 
    probability for an accident is independent of the changes being 
    proposed. Reactor criticality at 530 degrees Fahrenheit instead of the 
    nominal no-load Tavg of 547 degrees Fahrenheit does not affect any 
    of the accident initiators in the analyses, but does change one of the 
    initial conditions assumed in the Safety Analysis. However, the change 
    in initial conditions from the nominal no-load temperature of 547 
    degrees Fahrenheit to 530 degrees Fahrenheit does not increase the 
    probability of any of the events considered in the Safety Analysis. The 
    proposed Minimum Temperature for Criticality specification (530 degrees 
    Fahrenheit) will be more restrictive than the current specification 
    which allows reactor criticality at a temperature as low as 500 degrees 
    Fahrenheit. In addition, the Action Statement will require operator 
    response to place the reactor in a subcritical condition (Mode 3) with 
    15 minutes should the temperature drop below the limit for greater than 
    a specified amount of time (15 minutes).
        Likewise, the proposed change does not significantly increase the 
    consequences of an accident previously evaluated. In the reanalysis of 
    the Zero Power accidents (Rod Withdrawal From Subcritical, Rod 
    Ejection, Main Steamline Break, Boron Dilution During Startup, and 
    Feedwater Malfunction) from an initial condition of 530 degrees 
    Fahrenheit, it was concluded that the results and conclusions in the 
    current Safety Analysis remain valid based on the fact that the current 
    analysis results are conservative and bounding for reactor criticality 
    at 530 degrees Fahrenheit. The LOCA transient analyses are unaffected 
    by the proposed change since they are initiated from the limiting 
    condition of 102 percent. Since the full power Tavg value is 
    unchanged by this proposed amendment, the LOCA analyses are unaffected. 
    The proposed change will ensure that plant parameters are within their 
    analyzed ranges prior to reactor criticality and appropriate operator 
    actions are taken should the temperature drop below the temperature 
    limit after reaching criticality.
        The proposed administrative changes delete requirements which are 
    no longer applicable and will have no affect on the probability or 
    consequences of any accident previously evaluated in the analyses.
        The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. The 
    change does not involve the addition of any new or different type of 
    equipment, nor does it involve the operation of equipment required for 
    safe operation of the facility in a manner different from those 
    addressed in the Final Safety Analysis Report. The proposed change will 
    ensure that plant parameters are within their analyzed ranges prior to 
    reactor criticality. The proposed administrative changes delete 
    requirements which are no longer applicable and will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The proposed change does not involve a significant reduction in a 
    margin of safety. The proposed change does not affect any safety 
    related system or component operation or operability, instrument 
    operation, or safety system setpoints, and does not result in increased 
    severity of any of the accidents considered in the analysis. Operator 
    response to a drop in temperature after reaching criticality for a 
    specified period of time (greater than 15 minutes) will place the 
    reactor in a subcritical condition which is inherently more stable than 
    when critical below the Point of Adding Heat. The proposed 
    administrative changes are being made to clarify Technical 
    Specifications with no change of intent. Therefore, the proposed 
    changes do not create a significant reduction in a margin of safety.
        In conclusion, based on the previous considerations, Commonwealth 
    Edison Company believes that the activities associated with this 
    Technical Specification amendment request satisfy the Significant 
    Hazards Consideration standards of 10 CFR 50.92(c) and, accordingly, a 
    finding that this Technical Specification amendment does not represent 
    a Significant Hazards Consideration is justified.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690.
        NRC Project Director: Robert A. Capra.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station, Units 1 and 2, Lake County, Illinois
    
        Date of amendment request: June 24, 1994.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications by removing the containment 
    recirculation sump level instrumentation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant increase 
    in the probability of occurrence or consequences of any accident 
    previously evaluated.
        This change does not affect the initiators or precursors of any 
    accident previously evaluated. This change will not increase the 
    likelihood that a transient initiating event will occur because 
    transients are initiated by equipment malfunction and/or catastrophic 
    system failure. Since the proposed change does not involve the 
    introduction of new or redesigned plant equipment, failure mechanisms 
    are not impacted. As a result, the probability of occurrence of 
    accidents previously evaluated is not increased.
        The consequences of accidents previously evaluated are not 
    increased. Removal of [containment recirculation sump level] CRSL 
    instrumentation requirements from Technical Specifications does not 
    affect the ability to mitigate the consequences of any accident 
    previously evaluated. The CRSL instrumentation is used to verify that 
    [residual heat removal] RHR pumps have adequate [net positive suction 
    head] NPSH to operate in the recirculation mode following a Loss of 
    Coolant Accident (LOCA).
        As stated in the Zion Updated Final Safety Analysis Report (UFSAR), 
    the changeover from the injection mode to the recirculation mode of 
    emergency core cooling is initiated when the low level alarm on the 
    RWST annunciates. This occurs when the RWST level drops to 13'-7'' 
    (145,600 gallons).
        At this point, sufficient water has been delivered to the 
    containment, from the Containment Spray (CS) system and, by Emergency 
    Core Cooling System (ECCS) injection, through the [reactor coolant 
    system] RCS break, to provide at least one foot of water above the 
    containment floor. One foot of water above the containment floor 
    provides sufficient volume to sustain the required NPSH of the RHR 
    pumps in the recirculation mode of operation. The water level in the 
    Containment Building during the recirculation phase will be 
    approximately 5 feet above the floor elevation (568') based on the 
    volume of the RCS, accumulators, and the minimum required volume of the 
    RWST. Minimum RWST volume of 350,000 gallons is required by Technical 
    Specification 3.8.1.F.
        In summary, RWST level instrumentation, which satisfies Regulatory 
    Guide 1.97 qualification requirements for a Type A, Category 1 
    variable, provides the operator with the primary indication of the 
    appropriate time to initiate switchover to the recirculation mode, as 
    well as indication of adequate NPSH for the RHR pumps. Containment 
    Water Level (wide range) instrumentation which is qualified as a Type B 
    variable provides confirmatory indication of water level in 
    containment.
        The proposed change does not affect the procedures controlling 
    operation of equipment, or systems required to mitigate the accidents 
    considered in the UFSAR. As such, there will be no significant increase 
    in the consequences of any accident previously evaluated.
        2. The proposed amendment does not create the possibility of a new 
    or different kind of accident from any previously analyzed.
        The proposed change does not involve the addition of any new or 
    different types of equipment, nor does it involve the operation of 
    equipment required for safe operation of the facility in a manner 
    different from those addressed in the UFSAR. No safety related 
    equipment or function will be altered as a result of this proposed 
    change. Because no new failure modes are introduced, the proposed 
    amendment does not create a new or different kind of accident from any 
    previously analyzed in the UFSAR. Also, the methods of recovery from 
    accidents described in the UFSAR are not affected.
        Based on the above discussion, the proposed amendment does not 
    create a new or different kind of accident from any previously analyzed 
    in the UFSAR.
        3. The proposed changes do not involve a significant reduction in a 
    margin of safety.
        No design margins are impacted and the newly chosen primary 
    indicator (RWST level) is both consistent with plant emergency 
    procedures and appropriately qualified. The proposed change will not 
    adversely impact the peak clad temperature, amount of fuel damage, or 
    offsite dose projected to occur from the design basis accidents. Thus, 
    the margin of safety is not diminished.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690.
        NRC Project Director: Robert A. Capra.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam Neck 
    Plant, Middlesex County, Connecticut
    
        Date of amendment request: June 16, 1994.
        Description of amendment request: The proposed amendment will 
    remove a footnote applicable for Cycle 18 only regarding the 
    surveillance of the automatic bus transfer (ABT) system and add 
    surveillance requirement 4.8.3.1.2, to test the ABT once per refueling.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes do not involve an SHC [significant hazards 
    consideration] because the changes would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes to delete a note from the limiting condition 
    for operation for the MCC-5 ABT scheme and to add the surveillance 
    requirement has no impact on the probability or consequences of an 
    accident previously evaluated. By removing the requirement to test the 
    scheme on-line, the probability of failure to mitigate an accident 
    while the Haddam Neck Plant is operational is incrementally decreased.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed changes remove the requirements to disable the subject 
    ABT feature for testing, leaving the scheme undisturbed throughout 
    normal plant operation, and therefore does not create the possibility 
    of a new accident or different kind of accident from any previously 
    analyzed.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes require that the MCC-5 ABT feature be tested 
    during a plant shutdown rather than during normal operation. This will 
    place the ABT scheme in a test environment that has no significant 
    reduction in a margin of safety. The plant configuration that is 
    required to perform this test (refueling) would clearly place the 
    Haddam Neck Plant in a state that would be able to accept all possible 
    ABT scheme test outcomes, normal and abnormal. Therefore, these 
    proposed changes do not result in any reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, Connecticut 06457.
        Attorney for licensee: Gerald Garfield, Esquire, Day, Berry & 
    Howard, Counselors at Law, City Place, Hartford, Connecticut 06103-
    3499.
        NRC Project Director: John F. Stolz.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of amendment request: October 29, 1993, as supplemented on 
    March 28, 1994.
        Description of amendment request: This amendment is an additional 
    followup to the amendment request of May 29, 1992, published in the 
    Federal Register (57 FR 30242) on July 8, 1992, which changed the 
    Technical Specifications Section 1.0, Definitions, to accommodate a 24-
    month fuel cycle and which proposed the extension of the test intervals 
    for specific surveillance tests. This amendment proposes extending the 
    surveillance intervals to 24 months for the following additional 
    surveillance tests:
    
    (1) Volume Control Tank Level Transmitter
    (2) Containment High Range Area Radiation Monitors, R-25 and R-26
    (3) Safety Injection System Electrical Loading
    (4) Safety Injection (SI) System
    (5) Reactor Coolant System Sub-Cooling Margin Monitor
    
        The changes requested by the licensee are in accordance with 
    Generic Letter 91-04, ``Changes in Technical Specification Surveillance 
    Intervals to Accommodate a 24-Month Fuel Cycle.''
        The October 29, 1993, submittal included surveillance tests for the 
    Auxiliary Feedwater System which duplicated a previous request which 
    was subsequently approved. The March 28, 1994, submittal withdrew the 
    duplicated request.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazard 
    consideration, which is presented below:
        (1) Volume Control Tank Transmitter:
        The proposed change does not involve a significant hazard 
    consideration since:
        1. A significant increase in the probability or consequences of an 
    accident previously evaluated will not occur.
        It is proposed that the channel calibration frequency for the 
    volume control tank level instrumentation be changed from every 18 
    months (+25%) to every 24 months (+25%).
        A statistical analysis of channel uncertainty for a 30 month 
    operating cycle has been performed. Based upon this analysis it has 
    been concluded that sufficient margin exists between the existing 
    Technical Specification limits and the licensing basis Safety Analysis 
    limits to accommodate the channel statistical error resulting from a 30 
    month operating cycle. The existing margin between the Technical 
    Specification limit and the Safety Analysis limit provides assurance 
    that plant protective actions will occur as required. It is therefore 
    concluded that changing the surveillance interval from 18 months (+25%) 
    to 24 months (+25%) will not result in a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The possibility of a new or different kind of accident from any 
    accident previously evaluated has not been created.
        The proposed change is operating cycle length from a maximum of 
    22.5 months to 30 months resulting from an increased surveillance 
    interval will not result in a channel statistical allowance which 
    exceeds the current margin between the existing Technical Specification 
    limits and the Safety Analysis limits. Plant equipment, which will be 
    set at (or more conservatively than) Technical Specification limits, 
    will therefore provide protective functions to assure that Safety 
    Analysis limits are not exceeded. This will prevent the possibility of 
    any new or different kind of accident from that previously evaluated 
    from occurring.
        3. A significant reduction in a margin of safety is not involved.
        The change in surveillance interval from a maximum of 22.5 months 
    to 30 months resulting from an increased operating cycle will not 
    result in a channel statistical allowance which exceeds the margin 
    which exists between the current Technical Specification limit and the 
    licensing basis Safety Analysis limit. This margin, which is equivalent 
    to the existing margin, is necessary to assure that protective safety 
    functions will occur so that Safety Analysis limits are not exceeded.
        (2) Containment High Range Area Radiation Monitors, R-25 and R-26:
        The proposed change does not involve a significant hazard 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        It is proposed that the calibration frequency for the high-range 
    Containment Radiation Monitors (R-25 and R-26) be revised from every 18 
    months (+25%) to every 24 months (+25%).
        These two monitors are redundant to each other and are used for 
    post accident monitoring purposes. They serve no function during normal 
    plant operation. Furthermore, they serve no purpose in preventing 
    accident initiation or mitigation. They are used for Emergency Planning 
    purposes to indicate a release of radioactivity to containment.
        Review of past test results indicates that the devices have proven 
    reliable during past surveillances and there was no indication that 
    they would not remain operable for an extended operating cycle. In 
    addition, the devices are essentially redundant to each other. Each 
    device would respond to a release of radioactivity to Containment.
        In consideration that the monitors are redundant, and in view of 
    the past test history of the monitors, there would be no significant 
    increase in the probability or consequences of an accident due to an 
    extended operating cycle.
        2. The possibility of a new or different kind of accident from any 
    previously analyzed has not been created.
        The role of R-25 and R-26 is in the assessment of radiological 
    releases to Containment. In this function it is important that one of 
    the instruments, being high range, respond to a radiological release. 
    Indications from the devices are not used in a quantitative manner. 
    Rather they are used for qualitative purposes. Due to redundancy and 
    past test history, continued operability is expected. In addition, the 
    instruments serve no function in preventing accident initiation or 
    accident mitigation. Therefore, it is concluded that an extended 
    operating cycle for these monitors would not result in the possibility 
    of a new or different kind of accident from any previously analyzed.
        3. There has been no significant reduction in the margin of safety.
        Due to the qualitative function served by these two instruments as 
    well as their redundancy and acceptable past test history, no 
    significant reduction in the margin of safety due to an extended 
    operating cycle is expected.
    (3) Safety Injection System Electrical Loading
        The proposed change does not involve a significant hazard 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        The test procedure under consideration is one of the more 
    complicated surveillance procedures accomplished at a refueling 
    interval. Considering the vast number of components that are tested it 
    is highly improbable that some deficiencies will not occur. When such 
    problems are encountered it is important to note whether the failure is 
    time dependent and, in addition, whether the corrective maintenance 
    implemented prevents recurrences in the future. In consideration of the 
    evaluation of past test observations it is important to note that the 
    problems which occurred were not time dependent and that maintenance 
    practices have been effective in precluding future failures of the same 
    type. Equally important is whether the emergency power system would 
    have performed its intended safety function if the situation was not a 
    test but represented an actual demand upon the system. Test acceptance 
    criteria are always more stringent than required by accident scenarios 
    to provide margin. As discussed above the two most significant findings 
    were a failure of a CCW [Component Cooling Water] pump to strip from 
    the bus during the 1989 test and a relay which did not function within 
    its timing sequence. In the first instance, the diesel generator was 
    not overloaded. In the second instance, the relay did function albeit 
    not within the allotted time. In both cases, safety functions would 
    have been performed.
        Thus, it is concluded that an extended period between surveillances 
    will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The possibility of a new or different kind of accident from any 
    previously analyzed has not been created.
        The deficiencies noted in the test data taken during the last 
    several refueling outage surveillances were not substantial in number 
    and would not have impacted the capability of the Safety Injection 
    System and its emergency power supply to perform its intended safety 
    function. The effectiveness of maintenance practices, both preventive 
    and corrective, has been proven in that deficiencies noted in one test 
    are not repeated in subsequent tests. The last refueling surveillance 
    test was completely successful where no new test failures were noted. 
    Because past test deficiencies do not appear to be time dependent, 
    extending the surveillance interval by 7.5 months is not expected to 
    create the possibility of a new or different kind of accident from any 
    accident previously created.
        3. There has been no reduction in the margin of safety.
        Because previous tests indicate that the engineered safety features 
    power supply would have performed its safety function if called upon 
    over the past several years, it is concluded that extending the 
    operating cycle by several months will not involve a significant 
    reduction in a margin of safety.
    (4) Safety Injection System
        The proposed change does not involve a significant hazard 
    consideration since:
        1. There is no significant increase in the probability or 
    consequences of an accident.
        The central safety objective in reactor design and operation is the 
    control of reactor fission products from the fuel. Four methods are 
    used to ensure this objective. Two of these methods are: (1) Retention 
    of fission products in the reactor coolant for whatever leakage occurs; 
    and (2) retention of fission products by the containment for 
    operational and accidental releases beyond the reactor coolant 
    boundary. The engineered safety features are the provisions in the 
    plant that embody these two methods to prevent the occurrence or to 
    ameliorate the effects of serious accidents.
        The engineered safety features systems are the containment system, 
    the safety injection system, the containment spray system, the 
    containment air recirculation cooling and filtration system, the 
    isolation valve seal-water system, and the containment penetration and 
    weld channel pressurization system. Each engineered safety feature 
    provides sufficient performance capability to accommodate any single 
    failure of an active component and still function in a manner to avoid 
    undue risk to the health and safety of the public.
        A comprehensive program of plant testing is formulated for all 
    equipment, systems, and system control vital to the functioning of 
    engineered safety features. The program consists, in part, of 
    integrated tests of the systems as a whole and periodic tests of the 
    actuation circuitry and mechanical components.
        An assessment has been performed of the test results from the last 
    five refueling outages, covering a period in excess of seven years. In 
    reviewing the test results particular attention was directed towards 
    those test anomalies which directly impacted test acceptance criteria 
    and, thus, influence the capability of the safety injection system to 
    perform its intended safety function. Although in each test a problem 
    area was identified, the number of such events were minimal. 
    Furthermore, after corrective action these events were not repeated in 
    subsequent system tests. In all instances the problems were not 
    identified to be time dependent. Furthermore, the consequence from a 
    system safety function perspective was minimal. Thus, it is concluded 
    that extending the surveillance interval by several months will not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The possibility of a new or different kind of accident from any 
    previously analyzed has not been created.
        The number of problem areas in each test have been few and of 
    minimal to nonexistent safety significance. In 1986, a valve failure 
    occurred which would have been detected by alternate means during an 
    extended operating cycle. In another instance, lack of valve movement 
    could not be repeated in a second test, leading to the conclusion that 
    the valve malfunction was not induced by the system but was the result 
    of the test process. In the last problem area, manual SI initiation, no 
    credit is taken within the FSAR [Final Safety Analysis Report] accident 
    analysis for this function. In 1989, a series of containment isolation 
    valves failed to stroke as required. In three instances the valves 
    failed closed, which is the correct position. In the other instances, 
    either the redundant valve did stroke to the correct position or the 
    valve was located in a closed system. In all these events there was 
    minimal impact upon safety. More importantly, after corrective action, 
    these failures were not repeated in the 1991 or 1993 tests. In 1991, 
    one breaker failed to perform within specifications and thus was 
    considered defective. In 1993 there were no major equipment 
    malfunctions, although one containment isolation valve failed to 
    perform as required.
        In summary, although there have been anomalies in all of the tests 
    evaluated, none were deemed serious enough to impact the safety 
    function of the safety injection system or to be considered as having a 
    negative affect upon an increased interval of several months between 
    surveillances. Therefore, it has been concluded that an increased 
    operating cycle will not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        3. There has been no reduction in the margin of safety.
        The results of the previous five cycles of test data have been 
    evaluated. None of the anomalies observed were sufficiently serious to 
    impact the performance of the Safety Injection System or to weigh 
    against an extended operating cycle. As there are no other changes to 
    the safety analysis parameters which are impacted by an extended 
    interval between surveillances, it is concluded that this change will 
    not involve a significant reduction in the margin of safety.
        (5) Reactor Coolant System Sub-Cooling Margin Monitor:
        The proposed change does not involve a significant hazards 
    consideration since:
        1. There is no significant increase in the possibility or 
    consequences of an accident.
        It is proposed that the channel calibration frequency for the 
    volume control tank instrumentation be changed from every 18 months 
    (+25%) to every 24 months (+25%).
        The sub-cooling margin monitoring function is not relied upon 
    during normal operation. There is no reference to its use in the Indian 
    Point Unit 2 standard operating procedures. No credit is taken for this 
    monitoring function within the safety analysis for either the 
    prevention or mitigation of an accident. The increase in ``normal'' 
    operating uncertainty, due to the longer operating cycle, as well as 
    ``adverse'' uncertainties, is being incorporated in the EOPs [Emergency 
    Operating Procedures]. Therefore, the slight increase in uncertainty 
    associated with a longer operating cycle between surveillances will not 
    cause a significant increase in the probability or consequences of an 
    accident.
        2. The possibility of a new or different kind of accident from any 
    previously analyzed has not been created.
        The sub-cooling margin serves no purpose during normal operation 
    for prevention of an accident. No credit is taken within the FSAR 
    Safety Analysis for accident mitigation. The sub-cooling margin monitor 
    is relied upon within the Emergency Operating Procedures. Thus, the 
    normal uncertainty due to a 30 month operating cycle, as supplemented 
    by the instrument loop error due to a post-accident harsh environment, 
    is being factored into the Emergency Operation Procedures in accordance 
    with Emergency Response Guidelines. Thus, it is concluded that the 
    possibility of a new or different kind of accident from any previously 
    analyzed has not been created.
        3. There has been no reduction in the margin of safety.
        Because the sub-cooling margin monitor serves no purpose during 
    normal operation and appropriate measures have been implemented to 
    reflect the additional uncertainty due to a 30 month operating cycle 
    into the EOPs, it is concluded that there will be no significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
        Attorney for licensee: Brent L. Brandenburg, Esq., 4 Irving Place, 
    New York, New York 10003.
        NRC Project Director: Michael L. Boyle, Acting.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of amendment request: June 1, 1994.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications to allow extended Rod Position 
    Indication (RPI) deviation limits and on-line calibration of the RPI 
    channels. Specifically, Section 3.10.6.1 would be changed to allow 
    extended RPI deviation limits, and Section 3.10.4.4 would be changed to 
    allow on-line calibration of the RPI channels. The Basis for Section 10 
    would be changed to reflect the above, and in addition, Section 
    3.10.6.2 would be changed to clarify the operability requirements 
    during calibration. The proposed changes to Sections 3.10.6.1 and 
    3.10.4.4 include power limits to be included in the Core Operating 
    Limit Report (COLR). The use of a COLR for cycle specific core 
    operating limits was proposed by the licensee by submittal of October 
    29, 1993, and is currently under review by the NRC staff.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated?
        Response: Neither the probability nor the consequences of an 
    accident previously analyzed is increased due to the proposed changes. 
    All peaking factors will remain within the limits of the Technical 
    Specifications. Both the shutdown margin and the axial flux difference 
    will be maintained within the limits of the Technical Specifications. 
    There will be no fuel damage due to the changes. All design and safety 
    criteria will be met.
        2. Does the proposed license amendment create the possibility of a 
    new or different kind of accident from any previously evaluated?
        Response: The changes will not create the possibility of a new or 
    different kind of accident. The calibration will be performed using 
    plant procedures that have been reviewed and approved by Con Edison's 
    Safety Committees. It has been shown that even with the new RPI 
    deviation bands and on-line calibration, all power distribution limits 
    will be met.
        3. Does the proposed amendment involve a significant reduction in 
    the margin of safety?
        Response: The proposed amendment does not involve a significant 
    reduction in the margin of safety. There will be no change in the power 
    distribution limits used in the design and safety analyses and the 
    required shutdown margin will be maintained. It has been shown that 
    there is no fuel failure as a result of this change.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
        Attorney for licensee: Brent L. Brandenburg, Esq., 4 Irving Place, 
    New York, New York 10003.
        NRC Project Director: Michael L. Boyle.
    
    Detroit Edison Company, Docket No. 50-16, Enrico Fermi Power Plant, 
    Unit 1, Monroe County, Michigan
    
        Date of application for amendment: December 9, 1993 (Reference NRC-
    93-0143)
        Brief description of amendment: This Licensee Amendment Request 
    (LAR) proposes to revise the Enrico Fermi Power Plant, Unit 1, 
    Technical Specifications (TS) to bring the TS into conformance with a 
    revision of 10 CFR Part 20 (56 FR 23360).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        a. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes are administrative in nature and do not impact 
    the SAFSTOR status or design of any plant structures, systems or 
    components. As a result, this proposed change cannot increase the 
    probability or the consequences of any accident previously evaluated.
        b. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes do not affect the plant SAFSTOR status as 
    defined. As a result, the proposed changes cannot create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        c. Does the change involve a significant reduction in a margin of 
    safety?
        The proposed changes do not affect the plant SAFSTOR status. The 
    changes will not increase the amounts or change the types of effluents 
    that may be released offsite. These changes only ensure compliance with 
    revised 10 CFR 20. These changes do not alter any of the requirements 
    or responsibilities for protection of the public against radiation 
    hazards. As a result, these changes do not reduce the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161.
        Attorney for licensee: John Flynn, Esq., Detroit Edison Company, 
    2000 Second Avenue, Detroit, Michigan 48226.
        NRC Branch Chief: John H. Austin.
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, Beaver 
    Valley Power Station, Unit Nos. 1 and 2, Shippingport, Pennsylvania
    
        Date of amendment request: September 16, 1992, as superseded 
    February 4, 1994.
        Description of amendment request: The proposed amendment would 
    supersede in its entirety a previous proposed amendment which was 
    submitted by letter dated September 16, 1992. A notice of application 
    and proposed no significant hazards consideration determination for the 
    September 16, 1992, submittal was published in the Federal Register on 
    January 21, 1993 (58 FR 5429); this notice supersedes the January 21, 
    1993, notice in its entirety.
        The proposed amendment would modify the Technical Specifications 
    (TSs) related to containment air locks to make them as close to the 
    Improved Standard TSs in NUREG-1431 as the plant-specific design will 
    permit. The proposed changes in TS 3.6.1.1 and 3.6.1.3 would modify 
    surveillance requirements and limiting conditions of operation and 
    effect numerous administrative and format changes. The changes relate 
    to air lock operability, leak testing, and door interlocks.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The probability of occurrence of a previously evaluated accident is 
    not increased because the containment air locks do not effect the 
    initiation of any design basis accident [DBA]. The consequences of an 
    accident are also not significantly increased because the proposed 
    revisions to the action statements will continue to ensure that at 
    least one door in each air lock is maintained closed. A single door in 
    each air lock is capable of withstanding a pressure in excess of the 
    maximum expected pressure following a DBA. The structural integrity and 
    leak tightness of the containment will not be changed by this proposed 
    revision. For the brief period of time that the operable air lock door 
    is open and the inoperable door is providing the single containment 
    barrier, the consequences of [2an] accident may be increased. However, 
    the probability of an event occurring requiring containment integrity 
    is sufficiently remote to justify limited access when required.
        Therefore, based on the continued ability of the containment air 
    locks to provide a barrier to limit leakage from containment during a 
    DBA, this proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        Air lock operation does not interface with the reactor coolant 
    pressure boundary or any other mechanical or electrical controls which 
    could impact the operations of the reactor or its direct support 
    systems.
        Containment air locks are designed for the purpose of containment 
    entry and exit. During this operation, the air lock maintains 
    containment integrity by providing at least one door which is capable 
    of providing a leak tight barrier during a DBA.
        The proposed changes will continue to ensure that air lock 
    operation is performed as assumed in the original design of the plant. 
    During the period when the operable door is open and the other door 
    inoperable, at least one door is being maintained closed as designed. 
    This condition is ensured due to the subatmospheric conditions that 
    exist during plant operation. The operable air lock door cannot be 
    safely opened unless the inoperable door is closed due to the 
    approximately 5 psi pressure differential that exists. The operable air 
    lock door would only be opened long enough to allow personnel to enter 
    the air lock.
        Therefore, this proposed change does not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin of 
    safety?
        The applicable margin of safety consists of maintaining the primary 
    containment leak rates within the assumptions of the DBA analysis. 
    These leak rates are maintained provided at least one operable air lock 
    door remains closed during the event.
        The proposed revisions will continue to ensure that at least one 
    air lock door is maintained closed. During the brief period of time 
    that an operable air lock door is open and the inoperable door is 
    providing the single containment barrier, the margin of safety is 
    decreased. The inoperable door may not limit containment leak rates 
    within the assumptions of the DBA analysis. However, the probability of 
    an event requiring the inoperable air lock door to limit containment 
    leakage occurring during this time period is sufficiently low and the 
    overall margin of safety would not be decreased by a significant 
    amount. The proposed increase in allowable door seal leakage will not 
    affect the overall ability of the containment air locks to restrict the 
    release of fission products to the environment. The overall air lock 
    leakage limit of less than or equal to .05 La remain unchanged. 
    The amount of leakage which the air lock(s) are permitted to contribute 
    to the combined containment leakage limit of 0.60 La remain 
    unchanged. Therefore, the margin of safety due to increasing the door 
    seal leakage limit remains unchanged.
        Therefore, this proposed change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B.F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
        Attorney for licensee: Gerald Charnoff, Esquire, Jay E. Silberg, 
    Esquire, Shaw, Pittman, Potts & Trowbridge, 2300 N Street, NW., 
    Washington, DC 20037.
        NRC Project Director: Walter R. Butler.
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric 
    Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50-424 and 
    50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County, 
    Georgia
    
        Date of amendment request: March 31, 1994.
        Description of amendment request: The proposed amendments would 
    change Technical Specification 3/4.7.1.1 and its Bases regarding 
    maximum allowed reactor thermal power operation with inoperable main 
    steam safety valves.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    The new power range neutron flux high setpoint values will ensure that 
    the secondary side steam pressure will remain below 110 percent of its 
    design value following a loss of load/turbine trip (LOL/TT) when one or 
    more main steam safety valves (MSSVs) are declared inoperable. 
    Therefore, this transient will remain classified as a Condition II 
    probability event (faults of moderate frequency) per ANSI--N18.2, 1973 
    as discussed in Section 15.0.1 of the VEGP Final Safety Analysis Report 
    (FSAR). Accordingly, since the new power range setpoints will maintain 
    the capability of the MSSVs to perform their pressure relief function 
    associated with a LOL/TT event, there will be no effect on the 
    probability or consequences of an accident previously evaluated.
        2. The proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. The 
    proposed changes do not involve any change to the configuration or 
    method of operation of any plant equipment, and no new failure modes 
    have been defined for any plant system or component. The new power 
    range neutron flux high setpoints will maintain the capability of the 
    MSSVs to perform their pressure relief function to ensure the secondary 
    side steam design pressure is not exceeded following a LOL/TT. 
    Therefore, since the function of the MSSVs is unaffected by the 
    proposed changes, the possibility of a new or different kind of 
    accident from any accident previously evaluated is not created.
        3. The proposed changes do not involve a significant reduction in a 
    margin of safety. The algorithm methodology used to calculate the new 
    power range neutron flux high setpoints is conservative and bounding 
    since it is based on a number of inoperable MSSVs per loop; i.e., if 
    only one MSSV in one loop is out of service, the applicable power range 
    setpoint would be the same as if one MSSV in each loop were out of 
    service. Another conservatism with the algorithm methodology is with 
    the assumed minimum total steam flow rate capability of the operable 
    MSSVs. The assumption is that if one or more MSSVs are inoperable per 
    loop, the inoperable MSSVs are the largest capacity MSSVs, regardless 
    of which capacity MSSVs are actually inoperable. Therefore, since the 
    power range setpoints calculated for the proposed changes using the 
    algorithm methodology are more conservative and ensure the secondary 
    side steam design pressure is not exceeded following a LOL/TT, there 
    will not be a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Burke County Public Library, 
    412 Fourth Street, Waynesboro, Georgia 30830.
        NRC Project Director: David B. Matthews.
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric 
    Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50-424 and 
    50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County, 
    Georgia
    
        Date of amendment request: May 20, 1994.
        Description of amendment request: The proposed amendments would 
    relocate the heat flux hot channel factor penalty of 2 percent in 
    Specification 4.2.2.2.f to the cycle-specific Core Operating Limits 
    Report to allow burnup-dependent values of the penalty in excess of 2 
    percent. The licensee also proposes to revise the reference in 
    Specification 6.8.1.6 to the Westinghouse FQ(Z) surveillance 
    methodology in order to reflect Revision 1 of WCAP-10216-P, 
    ``Relaxation of Constant Axial Offset Control--FQ Surveillance 
    Technical Specification,'' approved by the NRC on November 26, 1993.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change involves only the manner in which the penalty 
    factors for FQ(Z) would be specified (i. e., a burnup-dependent 
    factor specified in the Core Operating Limits Report (COLR) versus a 
    constant factor specified in the TS [Technical Specification]). This is 
    simply used to account for the fact that FQ(Z) may increase 
    between surveillance intervals. These penalty factors are not assumed 
    in any of the initiating events for the accident analyses. Therefore, 
    the proposed change will have no effect on the probability of any 
    accidents previously evaluated. The penalty factors specified in the 
    COLR will be calculated using NRC-approved methodology and will 
    therefore continue to provide an equivalent level of protection as the 
    existing TS requirement. Therefore, the proposed change will not affect 
    the consequences of any accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change does not involve a physical alteration to the 
    plant (no new or different kind of equipment will be installed) or 
    alter the manner in which the plant would be operated. Thus, this 
    change does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Does this change involve a significant reduction in a margin of 
    safety?
        The proposed change will continue to ensure that potential 
    increases in FQ(Z) over a surveillance interval will be properly 
    accounted for. The penalty factors will be calculated using NRC-
    approved methodology. Therefore the proposed change will not involve a 
    reduction in margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Burke County Public Library, 
    412 Fourth Street, Waynesboro, Georgia 30830.
        Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders, 
    NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta, 
    Georgia 30308.
        NRC Project Director: David B. Matthews.
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of amendment request: June 22, 1994.
        Description of amendment request: The proposed amendment changes 
    Technical Specification Sections 1.6, 3.2.A, 3.9.F.5, and 4.2.A which 
    specify the Shutdown Margin (SDM) requirements that ensure the reactor 
    can be made subcritical and can be maintained sufficiently subcritical 
    to preclude inadvertent criticality in any core condition. The 
    amendment also proposes a new definition, Shutdown Margin, Section 
    1.45. The proposed changes address the requirements for SDM 
    demonstration and provide clarification for actions if SDM is not met.
        The amendment also proposes administrative changes to Sections 1.7 
    and 3.2.B.2 (b). The definition, COLD SHUTDOWN CONDITION, was 
    simplified by stating the reactor is in the SHUTDOWN CONDITION which 
    eliminates the need of repeating the requirements for this condition. 
    The note which permitted unlimited reactor startups without the Rod 
    Worth Minimizer during Cycle 11 is no longer applicable. The note and 
    its reference are deleted from the new page 3.2-2. Starting with page 
    3.2-2 in Section 3.2, the pages were renumbered and repaginated to 
    accommodate the changes in text.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        GPU Nuclear has determined that operation of the Oyster Creek 
    Nuclear Generating Station in accordance with the proposed Technical 
    Specifications does not involve a significant hazard. The changes do 
    not:
        1. Involve a significant increase in the probability or the 
    consequence of an accident previously evaluated.
        The proposed SDM Limits are more restrictive and provide adequate 
    shutdown margin for various modes of reactor operation. Since the new 
    SDM limits do not modify any initial conditions for the accidents 
    previously evaluated in the SAR [Safety Analysis Report], the proposed 
    changes do not involve a significant increase in the probability or 
    consequences of these accidents.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        The proposed TS changes do not modify the function of any 
    structure, system or component. The new Shutdown Margin requirements 
    will still meet the basic criterion that the core in its maximum 
    reactivity condition be subcritical with the control rod of highest 
    worth fully withdrawn and all operable rods fully inserted. Based on 
    these facts, the proposed TS changes do not create the possibility of a 
    new or different kind of accident from any previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes do not reduce the margin of safety, because 
    the new SDM limits where the highest worth control rod is determined 
    analytically (0.38% delta k) or by measurement (0.28% delta k) are more 
    restrictive than the current Oyster Creek limit (0.25% delta k).
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, New Jersey 
    08753.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire. Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, Docket 
    Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, Matagorda 
    County, Texas
    
        Date of amendment request: June 6, 1994.
        Description of amendment request: The licensee proposes to modify 
    the South Texas Project, Units 1 and 2, Technical Specification 3/
    4.8.1.1, ``A.C. Sources,'' to revise the action statements and 
    surveillance requirements for testing of the standby diesel generators 
    (SDGs). The proposed amendment would eliminate excessive and 
    unnecessary testing of the SDGs consistent with the guidance provided 
    in NUREG-1366, ``Improvements to Technical Specifications Surveillance 
    Requirements,'' NUREG-1431, ``Standard Technical Specifications for 
    Westinghouse Plants,'' Generic Letter 84-15, ``Proposed Staff Actions 
    to Improve and Maintain Diesel Generator Reliability,'' and Generic 
    Letter 93-05, ``Line-Item Technical Specifications Improvements to 
    Reduce Surveillance Requirements for Testing During Power Operation.'' 
    This request replaces a request for amendment dated November 23, 1993, 
    which was noticed on January 5, 1994 (59 FR 621). This revised 
    amendment request includes elimination of additional identified 
    unnecessary testing discovered since the original submittal. The 
    changes include: (1) eliminating the requirement to demonstrate the 
    operability of an operable SDG whenever an offsite AC power source is 
    determined to be inoperable, or whenever a support system or an 
    independently testable component of another SDG is inoperable, (2) 
    eliminating the requirement to load the diesel in 10 minutes during 
    testing, (3) replacing the minimum required loading for testing with a 
    load band, (4) relocating some surveillance requirements to the Diesel 
    Fuel Oil Testing Program, and (5) eliminating unnecessary loss of 
    offsite power tests.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The Standby Diesel Generators do not initiate any accidents, 
    therefore these changes do not increase the probability or [of] an 
    accident previously evaluated. The proposed changes will permit the 
    elimination of the unnecessary mechanical stress and wear on the diesel 
    engine and generator while ensuring that the diesel generators will 
    perform their designed function. The elimination of this mechanical 
    stress and wear will improve the reliability and availability of the 
    Standby Diesel Generators which will have a positive effect on the 
    ability of the diesel generators to perform their design function. 
    Therefore, the consequences of an accident previously evaluated are not 
    increased. The proposed changes are consistent with NUREG-1366, NUREG-
    1431, Generic Letter 93-05, and Generic Letter 84-15.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        The elimination of these unnecessary tests does not affect the 
    design bases of the SDGs, or any of the accident evaluations involving 
    the SDGs. The SDGs are designed to provide electrical power to the 
    equipment important for safety during all modes and plant conditions 
    following a loss of offsite power. The test schedule established in 
    accordance with GL 84-15 assures that operable SDGs are capable of 
    performing their intended safety function. The proposed changes to the 
    surveillance requirements are consistent with NUREG-1431, NUREG-1366, 
    Generic Letter 93-05, industry operating experience, and South Texas 
    Project operating experience. These changes are intended to improve 
    plant safety, decrease equipment degradation, and remove unnecessary 
    burden on personnel resources by reducing the amount of testing that 
    the Technical Specification requires during power operation. Relocating 
    the diesel fuel oil testing requirement to the STP Fuel Oil Monitoring 
    Program outside of the Technical Specifications is an administrative 
    change consistent with NUREG-1431 and consequently has no effect on 
    accident probability, consequences, or margin. Therefore, this change 
    does not create the possibility of a new or different kind of accident 
    from any previously evaluated.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        The proposed changes extend testing frequency and eliminate 
    unnecessary mechanical stress and wear on the diesel generator in an 
    effort to improve plant reliability and safety. These changes are 
    consistent with NUREG-1431, NUREG-1366, industry operating experience, 
    and STP operating experience and do not adversely affect the design 
    bases, accident analysis, reliability or capability of the SDGs to 
    perform their intended safety function. Relocating the diesel fuel oil 
    testing requirements to the STP Fuel Oil Monitoring Program outside of 
    the Technical Specifications is an administrative change consistent 
    with NUREG-1431 and consequently has no effect on accident probability, 
    consequences, or margin. Therefore the proposed changes do not involve 
    any reduction in a margin to safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involve no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges, Learning Center, 911 Boling Highway, Wharton, Texas 
    77488.
        Attorney for licensee: Jack R. Newman, Esq., Newman & Holtzinger, 
    P.C., 1615 L Street, N.W., Washington, D.C. 20036.
        NRC Project Director: William D. Beckner.
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, Linn 
    County, Iowa
    
        Date of amendment request: June 18, 1993 as supplemented on 
    December 17, 1993 and May 5, 1994.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TS) by clarifying TS wording for 
    the Low Pressure Coolant Injection (LPCI) and Containment Spray modes 
    of the Residual Heat Removal (RHR) system to assure consistency with 
    requirements of the DAEC Updated Final Safety Analysis Report.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) The probability or consequences of a previously-analyzed 
    accident will not be increased by these proposed changes to the LPCI 
    and Containment Spray LCOs and BASES because they merely clarify 
    existing TS requirements and are consistent with the DAEC UFSAR 
    accident analysis. The addition of the footnote clarifying LPCI 
    OPERABILITY during RHR system operation in the Shutdown Cooling mode is 
    consistent with the requirements in the NRC Standard TS (NUREG-1433). 
    No changes in either system design or operating strategies will be made 
    as a result of these changes, thus no opportunity exists to increase 
    the probability or consequences of a previously-analyzed accident.
        (2) The possibility of a new or different kind of accident from 
    those previously analyzed will not be created by these changes to the 
    LPCI and Containment Spray LCOs and BASES because they merely clarify 
    existing requirements. The addition of the footnote clarifying LPCI 
    OPERABILITY during RHR system operation in the Shutdown Cooling mode is 
    consistent with the requirements in the NRC Standard TS (NUREG-1433). 
    No changes in either system design or operating strategies will be made 
    as a result of these changes, thus no possibility exists to introduce a 
    new or different kind of accident.
        (3) The margin of safety will not be decreased as a result of these 
    changes because they merely clarify existing TS requirements and are 
    consistent with the UFSAR accident analysis. The addition of the 
    footnote clarifying LPCI OPERABILITY during RHR system operation in the 
    Shutdown Cooling mode is consistent with the requirements in the NRC 
    Standard TS (NUREG-1433). No changes in either system design or 
    operating strategies will be made as a result of these changes, thus no 
    possibility exists to reduce a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, S.E., Cedar Rapids, Iowa 52401.
        Attorney for licensee: Jack Newman, Esquire, Kathleen H. Shea, 
    Esquire, Newman and Holtzinger, 1615 L Street NW., Washington, DC 
    20036.
        NRC Project Director: John N. Hannon.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile Point 
    Nuclear Station, Unit 2, Oswego County, New York
    
        Date of amendment request: July 1, 1994.
        Description of amendment request: The proposed amendment would 
    revise the drawdown time testing requirement of Technical Specification 
    (TS) 4.6.5.1.c.1 and the secondary containment inleakage testing 
    requirement of TS 4.6.5.1.c.2. These revisions would support a revised 
    design basis radiological analysis which would support an increase in 
    secondary containment drawdown time from 6 to 60 minutes by taking 
    credit for fission product scrubbing and retention in the suppression 
    pool. The current design basis radiological analysis does not take 
    credit for the pressure suppression pool as a fission product cleanup 
    system as permitted in NUREG-0800, Section 6.5.5, ``Pressure 
    Suppression Pool as a Fission Product Cleanup System.'' The proposed 
    amendment would also take credit for additional mixing of primary 
    containment and engineered safety feature systems leakage with 50 
    percent of the secondary containment free air volume prior to the 
    release of radioactivity to the environment. In the revised analysis, 
    mixing is assumed to occur at the onset of a Design Basis Loss-of-
    Coolant Accident as the primary containment and the engineered safety 
    feature systems leak into secondary containment. The current analysis 
    takes credit for mixing within secondary containment only after 
    achieving a -0.25 inch water gauge (WG) pressure in secondary 
    containment with respect to the outside surrounding atmosphere. The 
    licensee's radiological evaluation for this accident, which reflects 
    these proposed changes and an assumed drawdown time of 60 minutes, has 
    determined that the radiological doses remain below 10 CFR Part 100 
    guidelines values and General Design Criterion 19 criteria. The revised 
    radiological doses, as calculated by the licensee, are lower than the 
    doses currently presented in the Updated Safety Analysis Report (USAR).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The operation of the Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Secondary containment and the SGTS [Standby Gas Treatment System] 
    are not initiators or precursors to an accident. Secondary containment 
    provides a pressure boundary, with limited inleakage, for the purpose 
    of establishing a negative pressure to prevent a ground level 
    unfiltered release of radioactivity. SGTS responds to accidents 
    involving a release of radioactivity to the secondary containment by 
    establishing and maintaining a negative pressure inside secondary 
    containment and by providing an elevated filtered release. Therefore, 
    changes to SECONDARY CONTAINMENT INTEGRITY surveillances cannot affect 
    the probability of a previously evaluated accident.
        The suppression pool and secondary containment are largely passive 
    in nature, and the active components are suitably redundant. Therefore, 
    their fission product attenuation functions can be accomplished 
    assuming a single failure.
        Currently, using an assumed drawdown time of 6 minutes, the 
    radiological doses for a DBA-LOCA [Design Bases Accident--Loss-of-
    Coolant Accident] are below the guidelines of 10 CFR Part 100 and GDC 
    [General Design Criterion] 19 criteria. The calculated doses, 
    considering the pressure suppression pool as a fission product cleanup 
    system, additional mixing within secondary containment and an assumed 
    secondary containment drawdown time of 60 minutes, are lower than the 
    previously calculated doses. The new doses are below 10 CFR Part 100 
    guideline values and GDC 19 criteria. The revised radiological analysis 
    follows the source term assumptions of RG [Regulatory Guide] 1.3, with 
    the exception of regulatory position C.1.f as permitted by SRP 
    [Standard Review Plan] Section 6.5.5, and continues to provide a 
    conservative representation of the timing and the composition of the 
    release of radioactivity from secondary containment during a DBA-LOCA.
        The Technical Specification SRs [Surveillance Requirements] will 
    ensure a continued state of readiness for the SGTS, the secondary 
    containment, the suppression pool and the suppression chamber/drywell 
    vacuum breakers. Therefore, the assumptions used in the dose assessment 
    will continue to bound the actual bypass of the suppression pool and 
    the mixing in secondary containment during a DBA-LOCA. The proposed 
    changes to the surveillances provide assurance that the performance of 
    the SGTS and secondary containment supports the radiological analysis. 
    Accordingly, as shown in Table 1, page 14 of 20, [of the July 1, 1994, 
    amendment request] operation with the SGTS and the proposed change to 
    the surveillances for secondary containment will not significantly 
    increase the consequences of an accident previously evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed change to the surveillances ensures that the SGTS and 
    secondary containment will be available to respond to an accident such 
    that the guidelines of 10 CFR Part 100 and the limits of GDC 19 are not 
    exceeded. The proposed change to the surveillances reflect 
    consideration of the pressure suppression pool as a fission product 
    cleanup system and credit for additional mixing in secondary 
    containment. The suppression pool will continue to perform its safety 
    functions as a pressure suppression pool and as a source of water to 
    support emergency core cooling system operation during a DBA-LOCA. In 
    addition, secondary containment will continue to perform its safety 
    function of controlling and minimizing radioactive leakage to the 
    outside atmosphere during a DBA-LOCA. Safety related equipment will 
    continue to be OPERABLE in the radioactive environment of secondary 
    containment to mitigate the consequences of a DBA-LOCA. Accordingly, 
    the proposed Technical Specification change will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        The SGTS exhausts the secondary containment atmosphere to the 
    environment through the filtration system. To verify the SGTS has not 
    degraded, SR 4.6.5.1.c.1 verifies that each SGTS subsystem will 
    establish and maintain a pressure in the secondary containment that is 
    equal to or more negative than -0.25 inch WG within the required time 
    limit. To verify secondary containment is intact, SR 4.6.5.1.c.2 
    demonstrates that one SGTS subsystem can maintain a pressure which is 
    equal to or more negative than -0.25 inch WG for 1 hour at a flow rate 
    less than or equal to the maximum allowed inleakage. The 1 hour test 
    period allows secondary containment to be in thermal equilibrium at 
    steady state conditions. Furthermore, as an interim measure, NMPC 
    [Niagara Mohawk Power Corporation] implemented certain compensatory 
    measures through administrative controls to ensure that the 
    radiological consequences of a DBA-LOCA would remain within regulatory 
    criteria. Together, these tests and the compensatory measures assure 
    SGTS performance and secondary containment boundary integrity.
        The proposed change to these surveillances incorporate changes to 
    the design basis, i.e., credit for fission product scrubbing and 
    retention by the suppression pool and credit for additional mixing 
    within secondary containment. The new inleakage is 2670 cfm which is 
    loss [less] than one change of the secondary containment free air 
    volume per day. The new drawdown time limit reflects consideration of 
    the proposed change in the secondary containment inleakage limit. Due 
    to the effects of service water temperature, inside and outside 
    temperature, flow measurement inaccuracies and actual test pressures, 
    meeting the current SRs does not by itself assure adequate SGTS 
    performance. Therefore, the surveillances' results are adjusted to 
    account for actual test conditions. Compliance with the proposed 
    surveillances assures that the SGTS can achieve and maintain -0.25 inch 
    WG in less than 60 minutes following a postulated DBA-LOCA. Achieving 
    -0.25 inch WG within 60 minutes assures that radiological doses will 
    remain below regulatory limits (see Table 1 [of the July 1, 1994, 
    amendment request]). Therefore, the proposed surveillances, together 
    with the proposed adjustments, provide adequate assurance of SGTS 
    performance and secondary containment boundary integrity. Accordingly, 
    the proposed Technical Specification change will not involve a 
    significant reduction in a margin of safety.
        Therefore, as determined by the analysis above, this proposed 
    amendment involves no significant hazards consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street NW., Washington, DC 20005-3502.
        NRC Project Director: Michael L. Boyle.
    
    Northern States Power Company, Docket No. 50-263, Monticello Nuclear 
    Generating Plant, Wright County, Minnesota
    
        Date of amendment request: June 8, 1994.
        Description of amendment request: The proposed amendment would 
    revise sections 3.7/4.7, which pertain to the Standby Gas Treatment 
    System (SGTS) and Secondary Containment. The proposed amendment would 
    revise the surveillance requirements for both SGTS and secondary 
    containment and revise the performance requirements for the SGTS 
    filters and process stream electric heaters.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment will not involve a significant increase 
    in the probability or consequences of an accident previously evaluated.
        The function of the SGTS and secondary containment is to mitigate 
    the consequences of a loss of coolant accident and fuel handling 
    accidents. The proposed changes maintain or improve this capability. 
    Therefore, this amendment will not cause a significant increase in the 
    probability or consequences of an accident previously evaluated for the 
    Monticello plant.
        2. The proposed amendment will not create the possibility of a new 
    or different kind of accident from any accident previously analyzed.
        The proposed changes to Technical Specifications for the standby 
    gas treatment system and secondary containment do not alter the 
    function of the systems or its interrelationships with other systems. 
    The proposed changes provide requirements to ensure the systems are 
    capable of performing the required functions or that actions are taken 
    to minimize the potential for its function being required consistent 
    with regulatory guidance; therefore, this amendment will not create the 
    possibility of a new or different kind of accident from any accident 
    previously analyzed.
        3. The proposed amendment will not involve a significant reduction 
    in the margin of safety.
        Improvements in the margin of safety are provided via the permanent 
    elimination of a potential single failure which could adversely affect 
    both standby gas treatment systems by deleting the reference to the 
    standby gas system room heaters in the technical specification bases 
    and providing appropriate surveillance requirements to assure system 
    operability. A review of the performance history of the Standby Gas 
    Treatment System and licensing basis assumptions has determined that 
    the proposed changes do not adversely affect plant safety. Changes to 
    the SGTS performance requirements provide greater assurance of SGTS 
    operability. The proposed change for the completion time to place the 
    plant in a cold shutdown condition if limiting conditions for operation 
    can not be satisfied is consistent with the time frame specified in the 
    current specification and is consistent with Standard Technical 
    Specifications. The proposed amendment will not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW, Washington, DC 20037.
        NRC Project Director: Ledyard B. Marsh.
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station, 
    Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: February 12, 1993, as supplemented by 
    letters dated August 20, 1993 and June 6, 1994.
        Description of amendment request: This amendment request was 
    previously noticed in the Federal Register on April 14, 1993 (58 FR 
    19485). The June 6, 1994, submittal supplements the February 12, 1993, 
    application for amendment, and includes and incorporates the NRC staff 
    comments. The proposed amendment would modify the Technical 
    Specifications (TS) to implement the reactor coolant system (RCS) leak 
    before break (LBB) methodology detection criteria, in accordance with 
    the recommendations listed in Generic Letter (GL) 84-04.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes will require additional leak detection 
    instruments be operable to close Unresolved Safety Issue A-2, 
    ``Asymmetrical Blowdown Loads on Reactor Primary Coolant System,'' for 
    the Fort Calhoun Station. Requiring additional instruments to be 
    operable does not increase the probability or consequences of an 
    accident since the safety function of the instruments is not being 
    altered.
        The proposed changes require at least two different types of RCS 
    leak detection instruments, of diverse monitoring principles, be 
    operable or corrective actions be taken to restore the instrumentation 
    to operable status. Currently the Technical Specifications require only 
    one RCS leak detection instrument to be operable.
        The probability of leaks occurring due to thermal or normal fatigue 
    is not affected as indicated in the fracture mechanics analysis 
    referenced in Generic Letter 84-04. No changes are proposed to primary 
    RCS piping systems or supports as a result of the proposed revision. 
    The proposed changes will ensure that a potential significant failure 
    does not go undetected within the Regulatory Guide 1.45 criteria as 
    noted in Generic Letter 84-04.
        The Loss of Coolant Accident (LOCA) analysis will not be impacted 
    by the proposed change. The results of the current Fort Calhoun LOCA 
    analyses cited in Section 14.15 of the Updated Safety Analysis Report 
    (USAR) will not be impacted as a result of these changes.
        (2) Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        It has been determined that a new or different kind of accident 
    will not be created due to the proposed changes since no new or 
    different modes of operation are created by this change. The existing 
    operating procedures were established to support an enhanced RCS leak 
    detection program. Operation of RCS leak detection instruments will not 
    differ from existing conditions.
        (3) Involve a significant reduction in a margin of safety.
        The margin of safety as defined in the basis for the Technical 
    Specifications is not changed or reduced by this proposed change. 
    Defining adequate RCS LBB monitoring is required to meet 
    recommendations provided in Generic Letter 84-04.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102.
        Attorney for licensee: LeBoeuf, Lamb, Leiby, and MacRae, 1875 
    Connecticut Avenue NW., Washington, DC 20009-5728.
        NRC Project Director: William D. Beckner.
    
    Philadelphia Electric Company, Docket No. 50-352, Limerick Generating 
    Station, Unit 1, Montgomery County, Pennsylvania
    
        Date of amendment request: June 6, 1994.
        Description of amendment request: The amendment would remove the 
    controls for a remote shutdown system control valve and delete the 
    isolation signal for certain primary containment isolation valves from 
    TS Tables 3.3.7.4-1 and 3.6.3-1 respectively, as a result of 
    eliminating the steam condensing mode of the Redidual Heat Removal 
    system.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specifications (TS) changes do not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        The RHR system steam condensing mode is a non-safety related 
    function of the RHR system and has been eliminated at Limerick 
    Generating Station, Unit 1. These proposed changes will not affect any 
    components required to perform the safety-related function of the RHR 
    system.
        The ability of the RHR system to respond to an accident will not be 
    degraded by the proposed changes. Valve HV-51-1F011A is locked closed 
    with the electrical power removed. The valve's handswitch which is part 
    of the remote shutdown panel (RSP) controls, does not perform any 
    function and will be physically removed from the RSP. The deletion of 
    the isolation signal for valves HV-C-51-1F103A and HV-C-51-1F104B will 
    not affect the ability of these valves to function as primary 
    containment isolation valves (PCIVs), since they are locked closed 
    already in their safety-related position, providing containment 
    isolation as manual PCIVs. Therefore, the proposed TS changes do not 
    involve an increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed TS changes do not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        No new failure modes of RHR system are created by the proposed TS 
    changes. All valves associated with the proposed changes are dedicated 
    specifically for the RHR system steam condensing mode, and will not 
    impact the operation of any components or piping required for other 
    modes of operation of the RHR system. These valves are locked-closed in 
    their safety-related position with the electrical power removed. 
    Therefore, the proposed TS changes do not create the possibility of a 
    new or different kind of accident from any previously evaluated.
        3. The proposed TS changes do not involve a significant reduction 
    in a margin of safety.
        The steam condensing mode is a non-safety related function of the 
    RHR system and, therefore, is not addressed in the TS. The controls for 
    remote shutdown system control valve HV-51-1F011A are not being used. 
    Presently, the valve is locked closed with the electrical power removed 
    and the valve's handswitch will be removed from the RSP, since it does 
    not perform any function. The proposed changes will not impact the safe 
    operation of LGS Unit 1. The deletion of the isolation signal for 
    valves HV-C-51-1F103A and HV-C-51-1F104B will not affect the ability of 
    these valves to function as primary containment isolation valves 
    (PCIVs), since they are locked closed already in their safety-related 
    position. Therefore, the proposed TS changes do not involve a reduction 
    in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101.
        NRC Project Director: Charles L. Miller.
    
    Philadelphia Electric Company, Docket No. 50-352, Limerick Generating 
    Station, Unit 1, Montgomery County, Pennsylvania
    
        Date of amendment request: June 10, 1994.
        Description of amendment request: The amendment involves a one-time 
    change affecting the Allowed Outage Time (AOT) for the Emergency 
    Service Water (ESW) System, Residual Heat Removal Service Water (RHRSW) 
    System, Suppression Pool Cooling, Suppression Pool Spray, and Low 
    Pressure Coolant Injection modes of the Residual Heat Removal System, 
    and Core Spray System to be extended from 3 and 7 days to 14 days 
    during the Limerick Generating Station (LGS), Unit 2 third refueling 
    outage scheduled to begin in January 1995. This proposed extended AOT 
    would allow adequate time to install isolation valves and cross-ties on 
    the ESW and RHRSW Systems to facilitate future inspections or 
    maintenance.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specifications changes do not involve a 
    significant increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed one-time TS changes will not increase the probability 
    of an accident since it will only extend the time period that the `B' 
    ESW and RHRSW loops and the affected equipment can be out-of-service. 
    The extension of the time duration that certain equipment is out-of-
    service has no direct physical impact on the plant. The proposed 
    inoperable systems are normally in a standby mode while the unit is in 
    OPCON 1 or 2 and are not directly supporting plant operation. 
    Therefore, they can have no impact on the plant that would make an 
    accident more likely to occur due to their inoperability.
        During transients or events which require these systems to be 
    operating, there is sufficient capacity in the operable loops to 
    support plant operation or shutdown, in-so-much that failures that are 
    accident initiators will not occur more frequently than previously 
    postulated.
        In addition, the consequences of an accident previously evaluated 
    in the SAR will not be increased. With the `B' loops of ESW and RHRSW 
    inoperable, a known quantity of equipment is either inoperable or the 
    equipment is not fully capable of fulfilling its design function under 
    all design conditions due to certain support systems not being 
    operable. Based on the support functions of the ESW and RHRSW systems, 
    a review of the plant was performed to determine the impacts that the 
    inoperable ESW and RHRSW `B' loops would have on other systems. The 
    impacts were identified for each system, as discussed in the preceding 
    Safety Assessment, and it was determined whether there were any adverse 
    [effects] on the systems. It was then determined how the adverse 
    [effects] would impact each system's design basis and overall plant 
    safety. The consequences of any postulated accidents occurring on Unit 
    1 during this AOT extension was found to be bounded by the previous 
    analyses as described in the SAR.
        The existing AOTs limit the amount of time that the plant can 
    operate with certain equipment inoperable, where single failure 
    criteria is still met. The minimum equipment required to mitigate the 
    consequences of an accident and/or safely shutdown the plant will be 
    operable or the plant will be shutdown. Therefore, by extending certain 
    AOTs and extending the assumptions concerning the combinations of 
    events and single failures for the longer duration of each extended 
    AOT, we conclude, based on the evaluations above, that at least the 
    minimum equipment required to mitigate the consequences of an accident 
    and/or safely shutdown the plant will still be operable during the 
    extended AOT. Therefore, the consequences of an accident previously 
    evaluated in the SAR will not be increased.
        Therefore, these proposed one-time TS changes will not result in a 
    significant increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed TS changes do not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The proposed one-time TS changes will not create the possibility of 
    a different type of accident since it will only extend the time period 
    that the `B' ESW and RHRSW loops and the affected equipment can be out-
    of-service. The extension of the time duration that certain equipment 
    is out-of-service has no direct physical impact on the plant and does 
    not create any new accident initiators. The systems involved are either 
    accident mitigation systems, safe shutdown systems or systems that 
    support plant operation. All of the possible impacts that the 
    inoperable equipment may have on its supported systems were previously 
    analyzed in the SAR and are the basis for the present TS ACTION 
    statements and AOTs. The impact of inoperable support systems for a 
    given time duration was previously evaluated and any accident 
    initiators created by the inoperable systems was evaluated. The 
    lengthening of the time duration does not create any additional 
    accident initiators for the plant.
        Therefore, the proposed one-time TS changes will not create the 
    possibility of a new or different type of accident from any accident 
    previously evaluated.
        3. The proposed TS changes do not involve a significant reduction 
    in a margin of safety.
        The ESW and RHRSW systems and their supported systems are designed 
    with sufficient independence and redundancy such that the removal from 
    service of a component/subsystem will not prevent the systems from 
    performing their required safety functions. Since removal of an ESW and 
    a RHRSW loop from service with one unit in operation and the other unit 
    in a refueling outage is allowed by the current Technical 
    Specifications, then the concern is the reduced margin of safety 
    incurred by extending the affected AOTs.
        The present ESW and RHRSW AOT limits were set to ensure that 
    sufficient safety-related equipment is available for response to all 
    accident conditions and that sufficient decay heat removal capability 
    is available for a LOCA/LOOP on one unit and simultaneous safe shutdown 
    of the other unit. A slight reduction in the margin of safety is 
    incurred during the proposed extended AOT due to the increased risk 
    that an event could occur in a fourteen day period versus a three or 
    seven day period. This increased risk is judged to be minimal due to 
    the low probability of an event occurring during the extended AOT and 
    based on the following discussion of minimum ECCS/decay heat removal 
    requirements.
        The reduction in the margin of safety is not significant since the 
    remaining operable ECCS equipment is adequate to mitigate the 
    consequences of any accident. This conclusion is based on the 
    information contained in documents NEDO-24708A and NEDC-30936-A. These 
    documents described the minimum requirements to successfully terminate 
    a transient or LOCA initiating event (with scram), assuming multiple 
    failures with realistic conditions and were used to justify certain TS 
    AOTs per UFSAR sections 6.3.1.1.2.o and 6.3.3.1. The minimum 
    requirements for short term response to an accident would be either one 
    LPCI pump or one Core Spray loop in conjunction with ADS, which would 
    be adequate to re-flood the vessel and maintain core cooling sufficient 
    to preclude fuel damage. For long term response, the minimum 
    requirements would be one loop of RHR for decay heat removal, along 
    with another low pressure ECCS loop. These minimum requirements will be 
    met since implementation of the proposed TS changes will require the 
    operability of HPCI, ADS, two LPCI subsystems (or one LPCI subsystem 
    and one RHR subsystem during decay heat removal) and one Core Spray 
    subsystem be maintained during the 14 day period.
        In addition, measures will be taken prior to or during the proposed 
    extended AOT for those fire regions that rely on one or more safe 
    shutdown methods which would all be unable to safely shutdown the plant 
    with inoperable loops of the ESW and RHRSW systems or the inoperable 
    systems that ESW or RHRSW support. These measures will offset the 
    increased risk of a fire event occurring in the vulnerable areas, 
    during the fourteen day versus three day AOT period. Therefore, the 
    proposed extended AOT does not adversely affect the approved level of 
    fire protection as described in UFSAR Appendix 9A (Fire Protection 
    Evaluation Report).
        A special procedure will be written to administratively control the 
    requirement to maintain the operability of specified components and 
    implementation of any appropriate compensatory measures which are 
    deemed necessary during the proposed AOT. In addition, operations 
    personnel are fully qualified by normal periodic training to respond to 
    and mitigate a Design Basis Accident, including the actions needed to 
    ensure decay heat removal while LGS Unit 1 and Unit 2 are in the 
    operational configurations described within this submittal. 
    Accordingly, procedures are already in place that cover safe plant 
    shutdown and decay heat removal for situations applicable to those in 
    the proposed AOTs.
        A Probabilistic Safety Assessment (PSA) Study was performed for an 
    ESW and RHRSW loop being out-of-service for 14 days on an operating 
    unit. This analysis includes EDG D12 being aligned to `A' ESW and HPCI 
    and RCIC not requiring room cooling. No other deviations from the 
    bounding assumptions used in the base PSA model were made. The Core 
    Damage Frequency (CDF) increased by 2.7x10-6, from 5.11x10-6/
    reactor-year to 7.8x10-6 /reactor-year. In absolute terms, this is 
    not a significant increase in risk. In addition, the modifications to 
    be installed during this proposed extended AOT will allow for future 
    maintenance and inspections to be performed on the ESW and RHRSW loops 
    without removing an entire loop from service, which will reduce risk in 
    the future. For example, if the ESW loop unavailability, due to testing 
    or maintenance, is reduced by half, the CDF will decrease by more than 
    four percent. It will also minimize the potential need for future AOT 
    extensions on these systems.
        Therefore, the implementation of the proposed one-time TS changes 
    will not involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J.W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101.
        NRC Project Director: Charles L. Miller.
    
    Philadelphia Electric Company, Public Service Electric and Gas Company, 
    Delmarva Power and Light Company, and Atlantic City Electric Company, 
    Dockets Nos. 50-277 and 50-278, Peach Bottom Atomic Power Station, 
    Units Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: May 10, 1994.
        Description of amendment request: The licensee is proposing to 
    revise the Technical Specifications (TS) requirements governing the 
    minimum low pressure cooling availability when irradiated fuel is in 
    the reactor vessel and the reactor is in the cold condition. 
    Specifically, the proposed changes are: (1) Revise the TS section 
    titles in the Table of Contents to agree with the TS section titles in 
    the body of the TS. (2) Revise TS Section 3.5.A.1 to provide proper 
    reference to the revised TS Section 3.5.F. (3) Revise TS Section 
    3.5.A.3 to provide proper reference to the revised TS Section 3.5.F. 
    (4) Revise TS Section 3.5.B.1 to delete the reference to TS Section 
    3.5.F.3. (5) Revise TS Section 3.5.F to require the limiting condition 
    for operation (LCO) governing minimum low pressure cooling availability 
    when irradiated fuel is in the reactor vessel and the reactor is in the 
    cold condition to be identical with the corresponding LCO in NUREG-
    1433, ``Standard Technical Specifications General Electric Plants, BWR/
    4.'' (6) Revise TS Section 4.5.F to require the surveillance 
    requirements (SR) governing minimum low pressure cooling availability 
    when irradiated fuel is in the reactor vessel and the reactor is in the 
    cold condition to be identical with the corresponding SR in NUREG-1433. 
    (7) Revise TS BASES 3.5.A to delete the reference to the core spray 
    subsystem as also providing a source for flooding of the core in case 
    of accidental draining because the information is being added to TS 
    BASES 3.5.F. (8) Revise TS BASES 3.5.F to be consistent with the 
    corresponding TS BASES in NUREG-1433. (9) Revise TS BASES 4.5 to be 
    consistent with the corresponding TS BASES in NUREG-1433. (10) Revise 
    TS Section 3.7.A.1 to provide proper reference to the revised TS 
    Section 3.5.F.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        Proposed changes 1, 2, 3, 4, 7, 8, 9 and 10 are administrative in 
    nature and involve no technical changes to the TS. These proposed 
    changes do not impact initiators of analyzed events or the assumed 
    mitigation of accidents or transients events. Therefore, these changes 
    do not involve an increase in the probability or consequences of an 
    accident previously evaluated.
        Proposed changes 5 and 6 will not increase the probability of 
    initiating an analyzed event or alter assumptions relative to 
    mitigation of an accident or transient event. These changes will not 
    alter the operation of process variables or systems, structures, or 
    components (SSC) as described in the safety analyses. These changes do 
    not involve any physical changes to plant SSC. TS requirements that 
    govern Operability or routine testing and verification of plant 
    components and variables are not assumed to be initiators of any 
    analyzed event. The proposed changes will not alter the operation of 
    equipment assumed to be available for the mitigation of accidents or 
    transients by the plant safety analysis or licensing basis. The 
    proposed changes establish or maintain adequate assurance that 
    components are operable when necessary for the prevention or mitigation 
    of accidents or transients and that plant variables are maintained 
    within limits necessary to satisfy the assumptions for initial 
    conditions in the safety analysis. These changes have been confirmed to 
    ensure no previously evaluated accident has been adversely affected. 
    These changes will not allow continuous plant operation with plant 
    conditions during a unit outage such that a single failure will result 
    in a loss of any safety function. Therefore, the changes will not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes do not involve a physical alteration of the 
    plant (no new or different type of equipment will be installed or 
    removed) and will not alter the method used by any system to perform 
    its design function. The proposed changes do not allow plant operation 
    in any mode that is not already evaluated. Therefore, these changes 
    will not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        3. The proposed changes do not involve a significant reduction in a 
    margin of safety.
        Proposed changes 1, 2, 3, 4, 7, 8, 9 and 10 are administrative in 
    nature and will not involve any technical changes. These proposed 
    changes will not reduce a margin of safety because they have no impact 
    on any safety analysis assumptions. Because these changes are 
    administrative in nature, no question of safety is involved. Therefore, 
    these changes do not reduce the margin of safety.
        Proposed changes 5 and 6 add some new requirements and make some 
    existing requirements more restrictive. These changes will not impact 
    any safety analysis assumptions. Adding new requirements and making 
    existing ones more restrictive either increases or does not affect the 
    margin of safety. As such, no question of safety is involved. 
    Therefore, these changes will not involve a significant reduction in a 
    margin of safety.
        Proposed changes 5 and 6 also make three less restrictive changes. 
    The first change deletes the requirements for the containment cooling 
    system when the reactor is in the Cold Condition. The containment 
    cooling system is necessary to maintain primary containment Operable to 
    mitigate the release of radioactive material following a DBA [design 
    basis accident].
        However, primary containment is not required to be Operable with 
    the reactor in the Cold Condition. As a result, the containment cooling 
    system is not needed to maintain the primary containment Operable with 
    the reactor in the Cold Condition. This change does not affect any 
    safety limits, operating limits, or design assumptions. This [change] 
    provides the benefit of allowing maintenance to be performed on the 
    containment cooling systems during a unit outage to ensure their 
    reliability during power operation. Therefore, this change does not 
    involve a significant reduction in a margin of safety.
        The current TS requirement that both core spray systems and the 
    LPCI system be Operable during a refueling outage is being relaxed by 
    the second change to require one core spray subsystem and one LPCI 
    subsystem or two core spray subsystems to be Operable. This [change] 
    does not adversely affect any accident or transient analyses because 
    the change ensures adequate vessel inventory makeup is available in the 
    event of an inadvertent vessel draindown. The long term cooling 
    analysis following a design bases LOCA [loss of coolant accident] 
    demonstrates only one low pressure ECCS [emergency core cooling system] 
    injection/spray subsystem is required, post LOCA, to maintain the peak 
    cladding temperature below the allowable limit. This change will not 
    affect any safety limits, operating limits, or design assumptions. This 
    change provides the benefit of allowing maintenance to be performed on 
    the low pressure ECCS subsystems not required to be operable to ensure 
    their reliability during plant operation. Therefore, this change does 
    not involve a significant reduction in a margin of safety.
        The final less restrictive change will allow low pressure 
    injection/spray subsystems to be inoperable during a refueling outage 
    if the spent fuel storage gates are removed and the water level is at 
    the required height over the top of the reactor pressure vessel flange. 
    This is acceptable because the water level requirement provides 
    sufficient coolant inventory to allow operator action to terminate any 
    inventory loss prior to fuel uncovery in the event of an inadvertent 
    draindown. This change will not affect any safety limits, operating 
    limits, or design assumptions. This change provides the benefit of 
    allowing maintenance to be performed on the low pressure ECCS 
    subsystems to ensure their continued reliability during plant 
    operation. Therefore, this change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
        Attorney for Licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101.
        NRC Project Director: Charles L. Miller.
    
    Philadelphia Electric Company, Public Service Electric and Gas Company, 
    Delmarva Power and Light Company, and Atlantic City Electric Company, 
    Dockets Nos. 50-277 and 50-278, Peach Bottom Atomic Power Station, 
    Units Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: June 9, 1994.
        Description of amendment request: The licensee proposed the 
    following changes to its Technical Specifications (TS): (1) Revise TS 
    4.3.C.1 to require that each control rod be scram time tested after 
    each refueling outage or after a reactor shutdown that is greater than 
    120 days with reactor steam dome pressure greater than or equal to 800 
    psig prior to exceeding 40% of rated power. Scram time testing is not 
    required for control rods inserted per TS 3.3.B.1. (2) Replace TS 
    4.3.C.2 with the requirement to perform scram time testing with the 
    reactor steam dome pressure greater than or equal to 800 psig prior to 
    exceeding 40% of rated power for only those control rods associated 
    with the core cells affected by any fuel movement within the reactor 
    pressure vessel. (3) Add TS 4.3.C.3 to perform scram time testing for a 
    representative sample of control rods at least once per 120 days of 
    power operation with the reactor steam dome pressure greater than or 
    equal to 800 psig. (4) Add TS 4.3.C.4 to perform scram time testing at 
    any reactor steam dome pressure for individual control rods prior to 
    declaring them operable after work on the control rod or control rod 
    drive system is performed that could affect scram insertion time. (5) 
    Revise TS Bases 3.3.C and 4.3.C to describe: the rational for 
    performing scram time testing with reactor pressure greater than or 
    equal to 800 psig; the rationale for requiring control rods to be scram 
    time tested once per 120 days; what constitutes a representative sample 
    of control rods; examples of work that could affect scram times; and 
    the rational and methods for performing scram time testing following 
    work that could affect the scram insertion times. (6) Add TS 4.3.C.5 to 
    perform scram time testing with the reactor steam dome pressure greater 
    than or equal to 800 psig prior to exceeding 40% of rated power after 
    work on the control rod or control rod drive system that could affect 
    scram insertion time. (7) Revise TS 4.5.K.2 from performing scram time 
    testing of 19 or more control rods on a rotation basis to performing 
    scram time testing of a representative sample of control rods.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed changes will not involve any physical changes to plant 
    systems, structures, or components (SSC). These proposed changes will 
    not alter operation of process variables or SSC as described in the 
    safety analysis. The proposed changes establish or maintain adequate 
    assurance that components are operable when necessary for the 
    prevention or mitigation of accidents or transients and that plant 
    variables are maintained within limits necessary to satisfy the 
    assumptions for initial conditions in the safety analysis. In 
    particular, proposed change 1 is acceptable based on industry 
    experience with control rod scram time testing coupled with the 
    additional requirement in proposed change 4 that scram time testing of 
    any control rod on which work was performed must be satisfactorily 
    completed before that control rod can be declared operable. The 
    proposed changes will not allow continuous plant operation with plant 
    conditions such that a single failure will result in a loss of any 
    safety function. Therefore, the changes will not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        (2) The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes do not alter the plant configuration (no new 
    or different type of equipment will be installed or removed) and will 
    not alter the method used by any system to perform its design function. 
    The proposed changes do not allow plant operation in any mode that is 
    not already evaluated. Therefore, these changes will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        (3) The proposed changes do not involve a significant reduction in 
    a margin of safety.
        Following a refueling outage, control rod scram time testing for 
    all control rods is currently required to be performed during 
    operational hydrostatic testing or during startup prior to 
    synchronizing the main turbine generator. Any control rods not tested 
    during operational hydrostatic testing must be tested at greater than 
    30% power but less than 40% power. Proposed change 1 will require that 
    scram time testing for all control rods be completed prior to exceeding 
    40% Reactor Power. This change is acceptable based on industry 
    experience with control rod scram time testing coupled with the 
    additional requirement in proposed change 4 that scram time testing of 
    any control rod on which work was performed must be satisfactorily 
    completed before that control rod can be declared operable. Proposed 
    changes 2, 3, 4 and 6 add some new requirements and make some existing 
    requirements more restrictive. The margin of safety is not reduced by 
    more restrictive changes. If anything, the margin of safety may 
    increase. Proposed change 5 revises the BASES to provide consistency 
    with the previously discussed SR [surveillance requirements] changes. 
    Proposed change 7 is administrative in nature and does not involve any 
    technical changes. Proposed changes 5 and 7 will not reduce a margin of 
    safety because they have no impact on any safety analysis assumptions. 
    Therefore, these changes will not involve a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
        Attorney for Licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: Charles L. Miller.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of amendment request: June 29, 1994.
        Description of amendment request: The proposed changes would alter 
    the Plant Operating Review Committee's (PORC's) membership requirements 
    and would delegate a portion of PORC's procedure review 
    responsibilities for nuclear safety related procedures and procedure 
    changes to the line organizations. Section 6.5, ``Review and Audit,'' 
    of the Technical Specifications (TSs) would be revised to modify the 
    composition of the PORC and delete review and audit responsibilities 
    for the Emergency and Security Plans from the TSs. The review and audit 
    responsibilities would be relocated to the respective Emergency and 
    Security Plans consistent with Generic Letter 93-07, ``Modification of 
    the Technical Specification Administrative Control Requirements for 
    Emergency and Security Plans.'' The proposed changes would also revise 
    Section 6.5 and Section 6.8, ``Procedures,'' of the TSs to delegate a 
    portion of the PORC's procedure review responsibilities for nuclear 
    safety related procedures to the line organizations. The PORC would 
    continue to perform safety reviews associated with procedures that are 
    of safety significance.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Consistent with the criteria of 10 CFR 50.92, the enclosed 
    application is judged to involve no significant hazards based on the 
    following information:
        1. Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident previously 
    analyzed?
        Response: The proposed changes do not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated since: (1) PORC will continue to review environmental impact 
    and 10 CFR 50.59 safety evaluations associated with procedures and 
    procedure changes; (2) Only personnel knowledgeable in the affected 
    functional areas will review procedures and procedure changes; (3) 
    Review and approval personnel (designated technical reviewers, 
    qualified safety reviewers and responsible procedure owners) will be 
    identified in the appropriate administrative procedures; (4) Designated 
    technical reviewers shall meet or exceed the qualifications described 
    in Section 4 of ANSI N18.1-1971 [* * *] for applicable positions and 
    are designated by the Department Managers; 5) The designated technical 
    reviewers will be responsible for identifying whether additional cross 
    disciplinary reviews are required; (6) The qualified safety reviewers 
    will be responsible for reviewing the procedure changes from a safety 
    perspective; (7) The responsible procedure owners are designated by the 
    Resident Manager; and (8) The responsible procedure owners will be 
    responsible for verifying that procedure reviews are performed in 
    accordance with the administrative procedure governing the procedure 
    review and approval process.
        The proposed changes (1) will add more detailed requirements 
    regarding procedure review and approval to the Technical Specifications 
    which will strengthen the controls over the process, and (2) will free 
    PORC from reviewing items that are outside the charter of a ``safety 
    review'' committee [* * *] [because non-safety significant items can 
    reduce the time that PORC members can spend on matters that are safety 
    significant. The proposed Technical Specification change establishes a 
    highly structured review and approval program for procedures.]
        The proposed change to the PORC membership requirements would not 
    significantly increase the probability or consequences of an accident 
    because it does not adversely affect the level of expertise applied to 
    the PORC review function or its effectiveness. The PORC quorum is 
    currently composed of five members including up to two designated 
    alternates and a Chairman. [* * *] [This composition is not changed by 
    the proposed amendment.]
        The miscellaneous administrative changes not related to the 
    procedure review and approval process or the PORC membership 
    requirements cannot affect the probability or consequences of an 
    accident because they do not affect plant operations[,] [* * *] 
    equipment[, or any safety-related activity.]
        2. Does the proposed license amendment create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated?
        Response: [* * *] [No physical changes to the plant or changes in 
    plant equipment operating procedures are being proposed.] The changes 
    are administrative and will not have any direct effect on equipment 
    important to safety. Changing the process by which procedures are 
    reviewed and approved cannot in itself create the possibility of a new 
    or different kind of accident. Furthermore, a documented safety review, 
    utilizing screening criteria, will be performed for all nuclear safety 
    related procedures and procedure changes. The proposed change 
    establishes detailed controls while allowing PORC to spend more time on 
    safety significant issues.
        The proposed change to the PORC membership requirements would not 
    create the possibility of a new or different kind of accident from any 
    previously evaluated since no physical alterations of plant 
    configuration or changes to setpoints or operating parameters are 
    proposed.
        The miscellaneous administrative changes not related to the 
    procedure review and approval or the PORC Membership requirements 
    cannot create the possibility of an accident because they do not affect 
    plant operations[,] [* * *] equipment [or any safety-related activity.]
        3. Does the proposed amendment involve a significant reduction in a 
    margin of safety?
        Response: The proposed amendment does not involve a significant 
    reduction in the margin of safety because a program controlled by 
    Administrative Procedures using designated technical reviewers approved 
    by the Department Managers will be in place to review new procedures 
    and procedure changes. A 10 CFR 50.59 screening of each new procedure 
    and permanent procedure change will be performed by a qualified safety 
    reviewer, and PORC will continue to review 10 CFR 50.59 Safety and 
    Environmental Impact Evaluations associated with procedures and 
    procedure changes. Cross disciplinary reviews will be conducted as 
    appropriate. Thus, the margin of safety will be maintained by 
    implementing the new procedure review and approval process.
        The proposed change to the PORC membership requirements would not 
    involve a significant reduction in the margin of safety since the level 
    and quality of PORC review will be maintained and there will not be an 
    adverse change to the collective educational background and work 
    experience of PORC. [There will not be an adverse loss of PORC 
    effectiveness as a result of this change.] The PORC quorum is currently 
    composed of five members including up to two designated alternates and 
    a Chairman. [* * *] [This composition is not changed by the proposed 
    changes.]
        The miscellaneous administrative changes not related to the 
    procedure review and approval process or PORC membership program cannot 
    reduce any margin of safety because they do not affect any safety 
    related activity or equipment. These changes increase the probability 
    that the Technical Specifications are correctly interpreted by 
    clarifying information.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
        Attorney for licensee: Mr. Charles M. Pratt, 10 Columbus Circle, 
    New York, New York 10019.
        NRC Project Director: Michael L. Boyle.
    
    Power Authority of the State of New York, Docket No. 50-333, James A. 
    FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of amendment request: June 17, 1994.
        Description of amendment request: The proposed changes would revise 
    Section 6.5, ``Review and Audit,'' of the Technical Specifications 
    (TSs) to modify the composition of the Plant Operating Review Committee 
    (PORC) and delete review and audit responsibilities for the Emergency 
    and Security Plans from the TSs. The review and audit responsibilities 
    would be relocated to the respective Emergency and Security Plans 
    consistent with Generic Letter 93-07, ``Modification of the Technical 
    Specification Administrative Control Requirements for Emergency and 
    Security Plans.'' The proposed changes would also revise Section 6.5 
    and Section 6.8, ``Procedures,'' of the TSs to delegate a portion of 
    the PORC's procedure review responsibilities for nuclear safety related 
    procedures to the line organizations. The PORC would continue to 
    perform safety reviews associated with procedures that are of safety 
    significance.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of the FitzPatrick plant in accordance with the proposed 
    amendment would not involve a significant hazards consideration as 
    defined in 10 CFR 50.92, since the proposed changes would not:
        1. involve a significant increase in the probability of an accident 
    or consequence previously evaluated.
        The proposed changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated since: 
    1) PORC will continue to review environmental impact and 10 CFR 50.59 
    safety evaluations associated with procedures and procedure changes; 2) 
    Only personnel knowledgeable in the affected functional areas will 
    review procedures and procedure changes; 3) Review and approval 
    personnel (designated technical reviewers, and responsible procedure 
    owners) will be identified in the appropriate administrative 
    procedures. Designated technical reviewers shall meet or exceed the 
    qualifications described in section 4 of ANSI N18.1-1971 for applicable 
    positions. Designated technical reviewers are designated by the 
    Department Managers. The responsible procedure owners are designated by 
    the Resident Manager; 4) The designated technical reviewers will be 
    responsible for identifying whether additional cross-disciplinary 
    reviews are required; 5) The qualified safety reviewers will be 
    responsible for reviewing the procedure changes from a safety 
    perspective; and 6) The responsible procedure owners will be 
    responsible for verifying that procedure reviews are performed in 
    accordance with the administrative procedure governing the procedure 
    review and approval process.
        The proposed changes (1) will add more detailed requirements 
    regarding procedure review and approval to the Technical Specifications 
    which will strengthen the controls over the process, and (2) will free 
    PORC from reviewing items that are outside the charter of a ``safety 
    review'' committee because non-safety significant items can reduce the 
    time that PORC members can spend on matters that are safety 
    significant. The proposed Technical Specification change establishes a 
    highly structured review and approval program for procedures.
        The proposed change to the PORC Membership requirements would not 
    significantly increase the probability or consequences of an accident 
    because it does not adversely affect the level of expertise applied to 
    the PORC review function. There will not be an adverse loss of PORC 
    effectiveness as a result of this change. The PORC quorum is currently 
    composed of five members including up to two designated alternates and 
    a Chairman. This composition is not changed by the proposed amendment.
        The miscellaneous administrative changes not related to the 
    procedure review and approval process or the PORC Membership 
    requirements cannot affect the probability or consequences of an 
    accident because they do not affect operations, equipment, or any 
    safety-related activity.
        2. Create the possibility of a new or different kind of accident 
    from those previously evaluated.
        No physical changes to the plant or changes in plant equipment 
    operating procedures are being proposed. The changes are administrative 
    and will not have any direct effect on equipment important to safety. 
    Changing the process by which procedures are reviewed and approved 
    cannot in itself create the possibility of a new or different kind of 
    accident. Furthermore, a documented safety review, utilizing screening 
    criteria, will be performed for all nuclear safety related procedures 
    and procedure changes. The proposed change establishes detailed 
    controls while allowing PORC to spend more time on safety significant 
    issues.
        The proposed change to the PORC Membership requirements would not 
    create the possibility of a new or different kind of accident from any 
    previously evaluated since no physical alterations of plant 
    configuration or changes to setpoints or operating parameters are 
    proposed.
        The miscellaneous administrative changes not related to the 
    procedure review and approval or the PORC Membership requirements 
    cannot create the possibility of an accident because they do not affect 
    operations, equipment or any safety-related activity.
        3. Involve a significant reduction in the margin of safety.
        The proposed amendment does not involve a significant reduction in 
    the margin of safety because a program controlled by Administrative 
    Procedures using designated technical reviewers approved by the 
    Department Managers will be in place to review new procedures and 
    procedure changes. A 10 CFR 50.59 screening of each new procedure and 
    permanent procedure change will be performed by a qualified safety 
    reviewer and PORC will continue to review 10 CFR 50.59 Safety and 
    Environmental Impact Evaluations associated with procedures and 
    procedure changes. Cross-disciplinary reviews will be conducted as 
    appropriate. Thus the margin of safety will be maintained by 
    implementing the new procedure review and approval process.
        The proposed change to the PORC Membership requirements would not 
    involve a significant reduction in the margin of safety since the level 
    and quality of PORC review will be maintained and there will not be an 
    adverse change to the collective educational background and work 
    experience of PORC. There will not be an adverse loss of PORC 
    effectiveness as a result of this change. The PORC quorum is currently 
    composed of five members including up to two designated alternates and 
    a Chairman. This composition is not changed by the proposed changes.
        The miscellaneous administrative changes not related to the 
    procedure review and approval process or PORC Membership program cannot 
    reduce any margin of safety because they do not affect any safety-
    related activity or equipment. These changes increase the probability 
    that the Technical Specifications are correctly interpreted by 
    clarifying information.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mr. Charles M. Pratt, 1633 Broadway, New 
    York, New York 10019.
        NRC Project Director: Michael L. Boyle.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of amendment requests: February 18, 1994, as supplemented by 
    letter dated April 6, 1994 for Salem Unit 1; and March 28, 1994 for 
    Salem Unit 2.
        Description of amendment request: The proposed change to Salem Unit 
    1 Technical Specifications (TS) replaces the main feedwater control and 
    control bypass valves with the main feedwater stop check valves for the 
    Containment Isolation Function. The proposed change to Salem Unit 2 TS 
    adds a footnote to the 21-24 BF22 (main feedwater stop check valves) on 
    Table 3.6-1, ``Containment Isolation valves.'' This note identifies 
    those containment isolation valves that are not subject to 10 CFR 50 
    Appendix J, Type C leakage testing.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below.
        1. Do not involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        The Salem Unit 1 main feedwater stop check valves provide the same 
    isolation function presently accomplished by the main feedwater control 
    and control bypass valves, without reliance on an actuation signal. 
    Positive closure is assured during all postulated accident scenarios, 
    through remote-manual controls in the main control room. These valves 
    satisfy the requirements of GDC 57 for Containment Isolation.
        A previous amendment request for Salem Unit 2 neglected to 
    designate the main feedwater stop check valves as exempt from Type C 
    leakage testing. That request was subsequently approved as Salem Unit 2 
    Amendment 128. The amended Technical Specifications are now 
    inconsistent with the Salem Updated Final Safety Analysis Report, which 
    correctly shows that these valves are exempt from Type C leakage 
    testing. Valve functionality and operation are not affected by this 
    change.
        Therefore, it may be concluded that the proposed changes do not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. Do not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The Salem Unit 1 main feedwater stop check valves were originally 
    intended to perform the Containment Isolation Function. The only 
    changes to the original plant design were the addition of motor 
    operators and the upgrading of associated controls to safety-related. 
    These changes bring the stop check valves into compliances with GDC 57 
    requirements, and ensure positive valve closure during all postulated 
    accident scenarios. As stated above, a previous amendment request for 
    Salem Unit 2 neglected to designate the main feedwater stop check 
    valves as exempt from Type C leakage testing. The Salem Updated Final 
    Safety Analysis Report correctly shows that these valves are exempt 
    from Type C leakage testing. Valve functionality and operation are not 
    affected by these changes.
        The changes do not involve modifications to plant equipment or 
    operation. Therefore, no new or different accident can be created by 
    these changes.
        3. Do not involve a significant reduction in a margin of safety.
        Check valves provide inherent isolation from reverse flow 
    conditions. Stop check valves provide increased safety due to the 
    positive closure feature. Motor operators with remote-manual closure 
    capability, allow positive closure from the main control room during 
    all postulated accident scenarios. These features ensure that an 
    adequate margin of safety is maintained.
        Additionally, feedwater isolation, utilizing the main feedwater 
    control and control bypass valves, occurs through Reactor Trip and/or 
    Engineered Safety Features actuation. This feature is unaffected by the 
    proposed changes and redundant to the stop check valves for Containment 
    Isolation. There are no modifications to plant equipment or operation 
    involved. Feedwater system operation during normal and accident 
    conditions remains the same.
        Therefore, it may be concluded that the proposed changes do not 
    involve a significant reduction in a margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment requests involve no significant hazards 
    consideration.
        Local Public Document Room location: Salem Free Public library, 112 
    West Broadway, Salem, New Jersey 08079.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: Charles L. Miller.
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. Ginna 
    Nuclear Power Plant, Wayne County, New York
    
        Date of amendment request: May 13, 1994, as supplemented June 24, 
    1994.
        Description of amendment request: The proposed amendment would 
    revise the Ginna Station Technical Specifications (TSs) Section 6.0 
    ``Administrative Controls,'' to be consistent with the criteria 
    contained in the NRC Final Policy Statement of Technical Specifications 
    Improvements for Nuclear Power Reactors, and NUREG-1431 ``Standard 
    Technical Specifications, Westinghouse Plants,'' September 1993. The 
    proposed amendment would also relocate to other programs and documents, 
    several TS requirements in accordance with this criteria.
        The May 13, 1994, request supersedes the request of March 23, 1992, 
    published in the Federal Register on November 25, 1992 (57 FR 55589).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated. The changes are 
    consistent with the Final Policy Statement on Technical Specifications 
    Improvements for Nuclear Power Reactors and NUREG-1431 and have 
    therefore, been previously evaluated by the NRC. Implementation of 
    these changes is expected to result in a significant human factors 
    improvement and enable RG&E [Rochester Gas & Electric] and the NRC to 
    focus on the most important requirements without any reduction in 
    safety. The changes which do not duplicate NRC guidance in NUREG-1431 
    are currently addressed by existing technical specifications and 
    regulations, the Ginna Station license, plant procedures, or the QA 
    [Quality Assurance] program.
        2. Operation of Ginna Station in accordance with the proposed 
    changes does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated. The Administrative 
    Controls section contains those requirements that are not covered by 
    other technical specifications which are considered necessary to assure 
    safe operation of the facility. The majority of changes are consistent 
    with the Final Policy Statement on Technical Specifications 
    Improvements for Nuclear Power Reactors and NUREG-1431 and have 
    therefore, been previously evaluated by the NRC. [* * *].
        3. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant reduction in a margin of safety. 
    All requirements removed from technical specifications are relocated to 
    other programs and documents. These alternative programs and documents 
    are controlled by existing regulations which provide a more appropriate 
    vehicle for addressing changes and compliance. There were no 
    administrative control requirements which were removed from technical 
    specifications and not addressed by other regulations. Therefore, there 
    is no significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610.
        Attorney for licensee: Nicholas S. Reynolds, Winston & Strawn, 1400 
    L Street, NW., Washington, DC 20005.
        NRC Project Director: Walter R. Butler.
    
    Tennessee Valley Authority, Docket No. 50-328, Sequoyah Nuclear Plant, 
    Unit 2, Hamilton County, Tennessee
    
        Date of amendment request: June 28, 1994 (TS 94-09).
        Description of amendment request: The proposed amendment would 
    revise the Sequoyah Nuclear Plant Unit 2 Technical Specifications (TS) 
    surveillance requirements, bases, and a Limiting Condition For 
    Operation to incorporate alternate steam generator tube plugging 
    criteria at tube support plate intersections. The proposed changes 
    would be implemented for Fuel Cycle 7 only and would affect: (1) TS 
    4.4.5.2.c.2 to address bobbin probe inspections; (2) TS 4.4.5.3.d to 
    address future inspections of tubes where the interim criteria is used; 
    (3) TS 4.4.5.4.a.6 to address application of the interim criteria for 
    indications found within the thickness of the tube support plate; (4) 
    TS 4.4.5.4.a.10 to address application of the tube plugging alternate 
    criteria and evaluation of indications; (5) TS 4.4.5.5.d and 4.4.5.5.e 
    to address reporting requirements and information to be reported to the 
    Commission regarding application of the criteria; (6) TS 3.4.6.2.c to 
    reduce the allowable reactor coolant system total primary-to-secondary 
    leakage through all steam generators from 1 gallon per minute to 600 
    gallons per day and from any one steam generator from 500 gallons per 
    day to 150 gallons per day; and (7) Bases 3/4.4.5 and 3/4.4.6.2 to 
    reflect the new primary-to-secondary leakage limits and add a 
    reference.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        TVA has evaluated the proposed TS change and has determined that it 
    does not represent a significant hazards consideration based on 
    criteria established in 10 CFR 50.92(c). Operation of Sequoyah Nuclear 
    Plant (SQN) in accordance with the proposed amendment will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Testing of model boiler specimens for free-span tubing (no tube 
    support plate restraint) at room temperature conditions shows burst 
    pressures in excess of 500 pounds per square inch (psi) for indications 
    of outer-diameter stress corrosion cracking with voltage measurements 
    as high as 19 volts. Burst testing performed on intersections pulled 
    from SQN with up to a 1.9-volt indication shows measured burst pressure 
    in excess of 6,600 psi at room temperature. Burst testing performed on 
    pulled tubes from other plants with up to 7.5-volt indications shows 
    burst pressures in excess of 6,300 psi at room temperatures. Correcting 
    for the effects of temperature on material properties and minimum 
    strength levels (as the burst testing was done at room temperature), 
    tube burst capability significantly exceeds the safety-factor 
    requirements of NRC Regulatory Guide (RG) 1.121.
        Tube burst criteria are inherently satisfied during normal 
    operating conditions because of the proximity of the tube support plate 
    (TSP). Test data indicates that tube burst cannot occur within the TSP, 
    even for tubes that have 100 percent throughwall electrodischarge 
    machining notches, 0.75-inch long, provided that the TSP is adjacent to 
    the notched area. Since tube-to-tube support plate proximity precludes 
    tube burst during normal operating conditions, use of the criteria must 
    retain tube integrity characteristics that maintain a margin of safety 
    of 1.43 times the bounding faulted condition steam line break (SLB) 
    pressure differential. During a postulated SLB, the TSP has the 
    potential to deflect during blowdown following a main SLB, thereby 
    uncovering the TSP intersections.
        Based on the existing database, the RG 1.121 criterion requiring 
    maintenance of a safety factor of 1.43 times the SLB pressure 
    differential on tube burst is satisfied by 7/8-inch-diameter tubing 
    with bobbin coil indications with signal amplitudes less than 8.82 
    volts, regardless of the indicated depth measurement. A 2.0-volt 
    plugging criterion (resulting in a projected end-of-cycle {EOC} 
    voltage) compares favorably with the 8.82-volt structural limit 
    considering the extremely slow apparent voltage growth rates and few 
    numbers of indications at SQN. Using the established methodology of RG 
    1.121, the structural limit is reduced by allowances for uncertainty 
    and growth to develop a beginning of cycle (BOC) repair limit that 
    would preclude indications at EOC conditions that exceed the structural 
    limit. The nondestructive examination (NDE) uncertainty component is 
    20.5 percent, and is based on the Electric Power Research Institute 
    (EPRI) alternate repair criteria (ARC).
        Because of the few number of indications at SQN, the EPRI 
    methodology of applying a growth component of 35 percent per effective 
    full power year (EFPY) will be used. Near-term operating cycles at SQN 
    are expected to be bounded by 1.23 years, therefore, a 43 percent 
    growth component is appropriate. When these allowances are added to the 
    BOC interim plugging criteria of 2.0 volts in a deterministic bounding 
    EOC voltage of approximately 3.26 volts for Cycle 7, operation can be 
    established. A 5.56-volt deterministic safety margin exists (8.82 
    structural limit--3.26-volt EOC equal 5.56-volt margin).
        For the voltage/burst correlation, the EOC structural limit is 
    supported by a voltage of 8.82 volts. Using this structural limit of 
    8.82 volts, a BOC maximum allowable repair limit can be established 
    using the guidance of RG 1.121. The BOC maximum allowable repair limit 
    should not permit the existence of EOC indications that exceed the 
    8.82-volt structural limit. By adding NDE uncertainty allowances and an 
    allowance for crack growth to the repair limit, the structural limit 
    can be validated. Therefore, the maximum allowable BOC repair limit 
    (RL) based on the structural limit of 8.82 volts can be represented by 
    the expression:
    
    RL + (0.205  x  RL) + (0.43  x  RL) = 8.82 volts, or,
    the maximum allowable BOC repair limit can be expressed as,
    RL = 8.82-volt structural limit/1.64 = 5.4 volts.
    
        It is reasonable that this RL (5.4 volts) could be applied for 
    interim plugging criteria (IPC) implementation to repair bobbin 
    indications greater than 2.0 volts independent of rotating pancake coil 
    (RPC) confirmation of the indication. Conservatively, an upper limit of 
    3.6 volts will be used to assess tube integrity for those bobbin 
    indications that are above 2.0 volts but do not have confirming RPC 
    calls. This 3.6-volt upper limit for nonconfirmed RPC calls is 
    consistent with other recently approved IPC programs.
        The conservatism of the growth allowance used to develop the repair 
    limit is shown by the most recent SQN eddy current data. Two tubes 
    plugged in Unit 1 during the last outage had less than one volt of 
    growth over the past five operating cycles. Only one tube in Unit 2 
    required repair because of outer-diameter stress corrosion (ODSCC) at 
    the TSP intersections.
        Relative to the expected leakage during accident condition 
    loadings, it has been previously established that a postulated main SLB 
    outside of containment, but upstream of the main steam isolation valve 
    (MSIV), represents the most limiting radiological condition relative to 
    the IPC. In support of implementation of the IPC, it will determine 
    whether the distribution of cracking indications at the TSP 
    intersections at the end of Cycle 7 for Unit 2 is projected to be such 
    that primary-to-secondary leakage would result in site boundary doses 
    within a small fraction of the 10 CFR 100 guidelines. A separate 
    analysis has determined this allowable SLB leakage limit to be 4.3 
    gallons per minute (gpm) in the faulted loop. This limit uses the TS 
    reactor coolant system (RCS) Iodine-131 activity level of 1.0 
    microcuries per gram dose equivalent Iodine-131 and the recommended 
    Iodine-131 transient spiking values consistent with NUREG-0800. The 
    projected SLB leakage rate calculation methodology prescribed in 
    Section 3.3 of draft NUREG-1477 is used to calculate EOC leakage. 
    Because of the relatively low number of indications at SQN, it is 
    expected that the actual leakage values will be far less than this 
    limit. Additionally, the current Iodine-131 levels at SQN range from 
    about 25 to 100 times less than the TS limit of 1.0.
        Application of the criteria requires the projection of postulated 
    SLB leakage, based on the projected EOC voltage distribution for Cycle 
    7. Projected EOC voltage distribution is developed using the most 
    recent EOC eddy current results and a voltage measurement uncertainty. 
    Data indicates that a threshold voltage of 2.8 volts would result in 
    throughwall cracks long enough to leak at SLB condition. Draft NUREG-
    1477 requires that all indications to which the IPC are applied must be 
    included in the voltage projection. Tube pull results from another 
    plant with 7/8-inch tubing with a substantial voltage growth database 
    have shown that tube wall degradation of greater than 40 percent 
    throughwall was readily detectable either by the bobbin or RPC probe. 
    The tube with the maximum throughwall penetration of 56 percent (42 
    average) had a voltage of 2.02 volts. This indication also was the 
    largest recorded bobbin voltage from the EOC eddy current data. Based 
    on the SQN pulled tube and industry pulled tube data supporting a lower 
    threshold for SLB leakage of 2.8 volts, inclusion of all IPC 
    intersections in the leakage model is quite conservative. The ODSCC 
    occurring at SQN is in its earliest stages of development. The 
    conservative bounding growth estimations to be applied to the expected 
    small number of indications for the upcoming inspection should result 
    in very small levels of predicted SLB leakage. Historically, SQN has 
    not identified ODSCC as a contributor to operational leakage. The 
    current leakage level at SQN is less than 1.0 gallon per day (gpd).
        In order to assess the sensitivity of an indication's BOC voltage 
    to EOC leakage potential, a Monte Carlo simulation was performed for a 
    2.0-volt BOC indication. The maximum EOC voltage (at 99.8 percent 
    cumulative probability) was found to be 4.8 volts. Using NUREG-1477 and 
    EPRI leakage models, the leakage component from an indication of this 
    magnitude is 0.12 and 0.028 gpm, respectively.
        Therefore, as implementation of the 2.0-volt IPC criterion during 
    Cycle 7 in Unit 2 does not adversely affect steam generator (S/G) tube 
    integrity and implementation will be shown to result in acceptable dose 
    consequences, the proposed amendment does not result in any increase in 
    the probability or consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        Implementation of the proposed S/G tube IPC criteria does not 
    introduce any significant changes to the plant design basis. Use of the 
    criteria does not provide a mechanism that could result in an accident 
    outside of the region of the TSP elevations; no ODSCC is occurring 
    outside the thickness of the TSP. Neither a single or multiple tube 
    rupture event would be expected in a S/G in which the plugging criteria 
    have been applied (during all plant conditions).
        TVA will implement a maximum leakage rate limit of 150 gpd per S/G 
    to help preclude the potential for excessive leakage during all plant 
    conditions. The SQN TS limits on primary-to-secondary leakage at 
    operating conditions are to be a maximum of 0.42 gpm (600 gpd) for all 
    S/Gs, or, a maximum of 150 gpd for any one S/G. The RG 1.121 criterion 
    for establishing operational leakage rate limits that require plant 
    shutdown is based upon leak-before-break considerations to detect a 
    free-span crack before potential tube rupture during faulted plant 
    conditions. The 150-gpd limit should provide for leakage detection and 
    plant shutdown in the event of the occurrence of an unexpected single 
    crack resulting in leakage that is associated with the longest 
    permissible crack length. RG 1.121 acceptance criteria for establishing 
    operating leakage limits are based on leak-before-break considerations 
    such that plant shutdown is initiated if the leakage associated with 
    the longest permissible crack is exceeded. The longest permissible 
    crack is the length that provides a factor of safety of 1.43 against 
    bursting at faulted conditions maximum pressure differential. A voltage 
    amplitude of 8.82 volts for typical ODSCC corresponds to meeting this 
    tube burst requirement at a lower 95 percent prediction limit on the 
    burst correlation coupled with 95/95 lower tolerance limit material 
    properties. Alternate crack morphologies can correspond to 8.82 volts 
    so that a unique crack length is not defined by the burst pressure 
    versus voltage correlation. Consequently, typical burst pressure versus 
    through-wall crack length correlations are used below to define the 
    ``longest permissible crack'' for evaluating operating leakage limits.
        The single through-wall crack lengths that result in tube burst at 
    1.42 times the SLB pressure differential and the SLB pressure 
    differential alone are approximately 0.57 inch and 0.84 inch, 
    respectively. A leak rate of 150 gpd will provide for detection of 0.4-
    inch-long cracks at nominal leak rates and 0.6-inch-long cracks at the 
    lower 95 percent confidence level leak rates. Since tube burst is 
    precluded during normal operation because of the proximity of the TSP 
    to the tube and the potential exists for the crevice to become 
    uncovered during SLB conditions, the leakage from the maximum 
    permissible crack must preclude tube burst at SLB conditions. Thus, the 
    150-gpd limit provides for plant shutdown before reaching critical 
    crack lengths for SLB conditions. Additionally, this leak-before-break 
    evaluation assumes that the entire crevice area is uncovered during 
    blowdown. Partial uncover will provide benefit to the burst capacity of 
    the intersection.
        As S/G tube integrity upon implementation of the 2.0-volt IPC 
    continues to be maintained through in-service inspection and primary-
    to-secondary leakage monitoring, the possibility of a new or different 
    kind of accident from any accident previously evaluated is not created.
        3. Involve a significant reduction in a margin of safety. The use 
    of the voltage based bobbin probe interim TSP elevation plugging 
    criteria at SQN is demonstrated to maintain S/G tube integrity 
    commensurate with the criteria of RG 1.121. RG 1.121 describes a method 
    acceptable to the NRC staff for meeting General Design Criteria (GDC) 
    14, 15, 31, and 32 by reducing the probability or the consequences of 
    S/G tube rupture. This is accomplished by determining the limiting 
    conditions of degradation of S/G tubing, as established by in-service 
    inspection, for which tubes with unacceptable cracking should be 
    removed from service. Upon implementation of the criteria, even under 
    the worst-case conditions, the occurrence of ODSCC at the TSP 
    elevations is not expected to lead to a S/G tube rupture event during 
    normal or faulted plant conditions. The EOC distribution of crack 
    indications at the TSP elevations will be confirmed to result in 
    acceptable primary-to-secondary leakage during all plant conditions and 
    that radiological consequences are not adversely impacted.
        In addressing the combined effects of loss-of-coolant accident 
    (LOCA), plus safe shutdown earthquake (SSE) on the S/G component (as 
    required by GDC 2), it has been determined that tube collapse may occur 
    in the S/Gs at some plants. This is the case as the TSP may become 
    deformed as a result of lateral loads at the wedge supports at the 
    periphery of the plate because of the combined effects of the LOCA 
    rarefraction wave and SSE loadings. Then, the resulting pressure 
    differential on the deformed tubes may cause some of the tubes to 
    collapse.
        There are two issues associated with S/G tube collapse. First, the 
    collapse of S/G tubing reduces the RCS flow area through the tubes. The 
    reduction in flow area increases the resistance to flow of steam from 
    the core during a LOCA, which in turn, may potentially increase the 
    peak clad temperature (PCT). Second, there is a potential that partial 
    through-wall cracks in tubes could progress to through-wall cracks 
    during tube deformation or collapse.
        Consequently, since the leak-before-break methodology is applicable 
    to the SQN reactor coolant loop piping, the probability of breaks in 
    the primary loop piping is sufficiently low that they need not be 
    considered in the structural design of the plant. The limiting LOCA 
    event becomes either the accumulator line break or the pressurizer 
    surge line break. LOCA loads for the primary pipe breaks were used to 
    bound the conditions at SQN for smaller breaks. The results of the 
    analysis using the larger break inputs show that the LOCA loads were 
    found to be of insufficient magnitude to result in S/G tube collapse or 
    significant deformation. The LOCA, plus SSE tube collapse evaluation 
    performed for another plant with Series 51 S/Gs using bounding input 
    conditions (large-break loadings), is considered applicable to SQN.
        Addressing RG 1.83 considerations, implementation of the bobbin 
    probe voltage based interim tube plugging criteria of 2.0 volt is 
    supplemented by: (1) enhanced eddy current inspection guidelines to 
    provide consistency in voltage normalization, (2) a 100 percent eddy 
    current inspection sample size at the TSP elevations, and (3) RPC 
    inspection requirements for the larger indications left in service to 
    characterize the principal degradation as ODSCC.
        As noted previously, implementation of the TSP elevation plugging 
    criteria will decrease the number of tubes that must be repaired. The 
    installation of S/G tube plugs reduces the RCS flow margin. Thus, 
    implementation of the alternate plugging criteria will maintain the 
    margin of flow that would otherwise be reduced in the event of 
    increased tube plugging.
        Based on the above, it is concluded that the proposed license 
    amendment request does not result in a significant reduction in margin 
    of safety.
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902.
        NRC Project Director: Frederick J. Hebdon.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak Steam 
    Electric Station, Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: February 14, 1994, as supplemented by 
    letter dated May 17, 1994.
        Brief description of amendments: The proposed changes revise the 
    Technical Specifications to allow power ascension above 50% rated 
    thermal power (RTP) with a quadrant power tilt ratio greater than 1.02 
    provided the assumptions of affected safety analyses are confirmed to 
    be satisfied.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not increase the probability or 
    consequences of a previously evaluated accident.
        The proposed changes affect the Action Statements which are to be 
    taken when it is discovered that the Quadrant Power Tilt Ratio (QPTR) 
    is greater than the value specified in the Limiting Condition for 
    Operation. The frequency for determining QPTR has been reduced. The 
    requirements to reduce power to below 50% RTP and to reduce the power 
    range flux trip setpoints based on QPTR have been replaced by similar 
    requirements based on FQ(Z) and FNH. The 
    requirement to correct the cause prior to increasing power and 
    verifying QPTR hourly is replaced with specific requirements to verify 
    that FQ(Z) and FNH are within their limits, the 
    safety analyses remain valid, and the excore detectors are re-
    normalized to indicate zero quadrant power tilt. If the proposed 
    actions are not met, a requirement to reduce power to 50% 
    RTP within 4 hours was added.
        The only item above that could affect the probability of an 
    accident is the removal of the requirement to reduce the power range 
    neutron flux setpoints. However, because the Protection Cabinets must 
    be entered to make these adjustments, eliminating the requirement to 
    adjust these setpoints actually slightly reduces the probability of an 
    inadvertent plant trip. Thus, the changes do not increase the 
    probability of an accident previously evaluated and may reduce the 
    probability of a plant trip.
        The proposed Action Statements, require that accident analyses be 
    re-evaluated to confirm that the results remain valid within 24 hours. 
    Prior to completion of this confirmation, the plant is not permitted to 
    operate at a power level higher than is permitted under the current 
    specification. If the re-evaluation of accident analyses cannot confirm 
    that the plant is within the accident analyses results, the required 
    actions are similar to the requirements of the current specification. 
    Although higher initial power levels generally increase accident 
    consequences, once the accident analyses are confirmed to be valid, the 
    consequences of any accident will be within analyzed acceptable limits. 
    Thus, the higher plant power levels permitted by the proposed changes 
    do not significantly increase the consequences of any accidents 
    previously evaluated.
        The proposed specification does not require a reduction in Power 
    Range Neutron Flux--High reactor trip setpoints during the time the 
    appropriate peaking factor surveillances are being performed. The 
    interval during which the proposed specification permits operation 
    without reduced setpoints (and unverified peaking factors) is longer 
    than is permitted under the current specification. However, the 
    consequences of any accident which could occur during this interval are 
    the same as for the conditions prior to resetting the trip setpoints in 
    the current specification. Therefore the change does not increase the 
    consequences of any accident which could occur during this interval. 
    The impact of the extended interval is addressed in response to 
    question (3) below.
        Based on the discussions above, the proposed changes do not involve 
    an increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any previously evaluated accident.
        The proposed changes do not involve any hardware changes. System 
    operation has not been changed to create any new system configurations 
    which were not previously allowed. Therefore, the proposed changes do 
    not create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        The limits for the parameters of concern (QPTR, FQ(Z) and 
    FNH) remain unchanged. The acceptance criteria for 
    analyzed events also remain the same. The margin of safety established 
    by the LCOs [Limiting Conditions for Operation] remains unchanged.
        The only impact of the proposed changes is an increase in the 
    allowed duration of operation above 50% RTP without a reduction in the 
    Power Range Neutron Flux--High trip setpoint. This could potentially 
    affect a margin of safety by allowing operation at conditions which are 
    potentially outside the assumptions of the accident analyses for an 
    interval longer than is permitted under the current specification. The 
    impact on safety margin is not considered to be significant, however, 
    because: the allowed interval is still small (24 hours versus the 
    current 6 hours); the likelihood of an accident during the interval is 
    small; and, it is considered unlikely that the peaking factors would be 
    outside their limits without outer indications.
        Thus, it is concluded that the proposed changes do not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 701 South Cooper, P.O. 
    Box 19497, Arlington, Texas 76019.
        Attorney for licensee: George L. Edgar, Esq., Newman and 
    Holtzinger, 1615 L Street, NW., Suite 1000, Washington, DC 20036.
        NRC Project Director: William D. Beckner.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak Steam 
    Electric Station, Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: March 28, 1994.
        Brief description of amendments: The proposed amendment would 
    revise Section 6 of the Technical Specifications (TS) by deleting a 
    reference to a no longer used loss of coolant accident (LOCA) topical 
    report and adding a reference to a new steamline break methodology 
    topical report.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve an increase in the 
    probability or consequences of a previously evaluated accident.
        The NRC assures that appropriate core operating limits are 
    established by requiring that they be determined using NRC approved 
    analytical methods. These approved methods are described in the 
    documents listed in TS Section 6.9.1.6b. TU Electric has developed the 
    analysis capability to evaluate the core operating limits. The 
    methodologies used by TU Electric have been documented in a series of 
    TU Electric submittals which were reviewed and approved by the NRC. 
    This TS revision adds the topical report which describes the TU 
    Electric steamline break analysis methodology to TS Section 6.9.1.6b.
        Also, the Westinghouse report which describes the methodology 
    previously used in the analysis of Unit 1 large break LOCAs is no 
    longer used and is being deleted. Large break LOCA analyses for Unit 1 
    are now performed using NRC approved TU Electric methodology.
        Because the revisions are administrative only, they cannot directly 
    affect the probability or the consequences of any previously evaluated 
    accident. The steamline break analysis methodology is part of a group 
    [of] methodologies which are authorized by the technical specifications 
    to be used to verify that each reload cycle continues to satisfy the 
    core operating limits. The core operating limits are set to assure that 
    relevant plant parameters are maintained such that potential accidents 
    are within the bounds of the accident analyses. Because the applicable 
    limits of the safety analyses will be verified to be satisfied using 
    authorized methodologies, there is no significant impact on the 
    consequences of an accident previously evaluated. In addition, since 
    the core operating limits do not affect any accident initiators, the 
    change has no impact on the probability of any accident previously 
    analyzed.
        2.The proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed changes involve a change in the permissible analysis 
    methodologies for determining core operating limits. As such, the 
    changes play an important role in the analysis of postulated accidents 
    but none of the changes affect plant hardware or the operation of plant 
    systems in a way that could initiate an accident. Therefore, the 
    proposed changes do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        3. The proposed changes do not involve a significant reduction in 
    the margin of safety.
        In reviewing and approving the methods used for safety analyses, 
    the NRC has approved the safety analysis limits which establish the 
    margin of safety to be maintained. Satisfaction of event-specific 
    acceptance criteria ensures that the approved safety analysis limits 
    are met and thus provides the margin of safety. The methodology being 
    added to the TS demonstrates, in a conservative manner, that the event 
    acceptance criteria are satisfied. Therefore, including this method in 
    the TS does not change the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 701 South Cooper, P.O. 
    Box 19497, Arlington, Texas 76019.
        Attorney for licensee: George L. Edgar, Esq., Newman and 
    Holtzinger, 1615 L Street, NW., Suite 1000, Washington, DC 20036.
        NRC Project Director: William D. Beckner.
    
    Virginia Electric and Power Company, Docket Nos. 50-338 and 50-339, 
    North Anna Power Station, Units No. 1 and No. 2, Louisa County, 
    Virginia
    
        Date of amendment request: June 9, 1994.
        Description of amendment request: The proposed change would revise 
    the Technical Specifications (TS) for the North Anna Power Station, 
    Units No. 1 and No. 2 (NA-1&2). Specifically, the proposed change would 
    relocate the TS tables of the response time limits for the Reactor Trip 
    System (RTS) and the Engineered Safety Feature Actuation System (ESFAS) 
    to station-controlled documents.
        On December 29, 1993, the NRC issued Generic Letter 93-08 titled 
    ``Relocation of Technical Specification Tables of Instrument Response 
    Time Limits.'' This generic letter provides guidance for preparing a 
    proposed license amendment to relocate the tables of response time 
    limits for the RTS and the Engineered ESFAS instruments from TS to 
    station-controlled documents.
        The RTS and the ESFAS provides the signals needed to actuate the 
    safety equipment necessary to mitigate accidents and transients. 
    Consistent with Generic Letter 93-08 the licensee is requesting license 
    amendments for NA-1&2 to relocate the RTS and ESFAS tables of 
    instrument response time limits from TS to station-controlled 
    documents.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Specifically, operation of North Anna Power Station in accordance 
    with the proposed Technical Specification[s] changes will not:
        1. Involve a significant increase in the probability of occurrence 
    or consequences of an accident previously evaluated.
        The Reactor Trip System and the Engineered Safety Features 
    Actuation System provide the signals needed to actuate the safety 
    equipment necessary to mitigate accidents and transients. The proposed 
    changes relocate the RTS and ESFAS instrument response time limits from 
    the Technical Specifications to station controlled documents but will 
    not change the operability or surveillance requirements for these 
    instruments. With these proposed changes, revisions to the response 
    times for these instruments can be made pursuant to 10 CFR 50.59 
    without Nuclear Regulatory Commission approval unless the revision 
    involves an unreviewed safety question.
        The proposed changes will not change any accident initiators or the 
    consequences of any analyzed accident. Therefore, the proposed changes 
    do not involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes relocate the RTS and ESFAS instrument response 
    time limits from the Technical Specifications to station controlled 
    documents but will not change the functions of these instruments. The 
    proposed change does not represent a change in the configuration or 
    operation of the plant. No new hardware is being added to the plant as 
    part of the proposed changes. The Technical Specifications will 
    continue to require the same operability and surveillance requirements 
    to be met for these instruments. Therefore, the proposed changes do not 
    create the possibility of a new or different type of accident from any 
    accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed changes will not affect the functions of the RTS or 
    the ESFAS instruments. Relocating the response time limits will not 
    alter the operability or the surveillance requirements of these 
    instruments. The administrative change control provisions for plant 
    procedures written pursuant to 10 CFR 50.59 are adequate to control 
    revisions to the response time limits. Therefore, the proposed changes 
    do not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: Herbert N. Berkow.
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia
    
        Date of amendment request: June 9, 1994.
        Description of amendment request: The proposed changes to the 
    Technical Specifications include: (1) modification of the high head 
    charging pumps seal cooling subsystem, (2) restructuring of the 
    Chemical and Volume Control System and Safety Injection System 
    Specifications, (3) relocation of certain specification requirements 
    within existing specifications, (4) specification of a minimum boric 
    acid solution temperature in lieu of heat tracing channel operability, 
    and (5) minor wording changes which are administrative in nature for 
    consistency in terminology, capitalization of defined terms and 
    clarification.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Specifically, operation of Surry Power Station in accordance with 
    the proposed Technical Specifications changes will not:
        1. Involve a significant increase in the probability of occurrence 
    or consequences of an accident previously evaluated.
        The modifications to the charging pumps and elimination of the 
    charging pump component cooling subsystem do not increase the 
    probability of occurrence of any accident or malfunction previously 
    evaluated in the safety analysis report. The charging pump 
    modifications utilize a passively designed process flow cooling 
    arrangement to reduce exposure, improve reliability, and improve 
    operability. The charging pump modifications will not decrease the 
    pumps ability or the associated subsystems ability to perform their 
    design function.
        The restructuring of the Chemical and Volume Control System and 
    Safety Injection System specifications on a subsystem basis continues 
    to ensure that the reactor can be made subcritical from any operating 
    condition and provide sufficient shutdown margin to preclude 
    inadvertent criticality when in the shutdown condition. The Safety 
    Injection System subsystems continue to maintain sufficient boration 
    capability to mitigate reactivity transients within the design limits 
    associated with postulated accident conditions. The Safety Injection 
    System subsystems ensure that sufficient emergency core cooling 
    capability will be available in the event of a LOCA [loss-of-coolant 
    accident] assuming the loss of one subsystem through any single failure 
    consideration. Either subsystem operating in conjunction with the 
    accumulators remains capable of supplying sufficient core cooling to 
    limit the peak cladding temperatures within acceptable limits in 
    accordance with the loss-of-coolant accident analyses.
        The Chemical and Volume Control System remains capable of achieving 
    Cold Shutdown of both units during any operating conditions in 
    accordance with the safety analysis with a minimum specified solution 
    temperature of 112 degrees F. Heat tracing is not required for 
    operability of the Safety Injection System nor does it affect the 
    ability of the Safety Injection System to mitigate the consequences of 
    any postulated accident identified in the safety analysis.
        The changes ensure that the refueling water storage tank remains 
    capable of providing a sufficient supply of borated water for injection 
    by the emergency core cooling system in the event of a LOCA. The limits 
    specified for refueling water storage tank volume and boron 
    concentration continue to ensure that sufficient solution is available 
    within containment for recirculation cooling flow to the core, and that 
    the reactor will remain subcritical in Cold Shutdown consistent with 
    the LOCA analyses.
        The specified allowed outage time of 72 hours for an inoperable 
    Chemical and Volume Control System subsystem or Safety Injection System 
    subsystem is reasonable for the repair of affected components and is 
    consistent with NRC Memorandum, ``Recommended Interim Revisions to 
    LCO's for ECCS Components,'' dated December 1, 1975, and NUREG-1431, 
    Standard Technical Specifications for Westinghouse Pressurized Water 
    Reactors. A reliability analysis (reference NRC memo above) has shown 
    that the impact of having one subsystem inoperable is sufficiently 
    small to justify continued operation for 72 hours. Engineering 
    evaluation of the proposed changes determined that they are bounded by 
    existing safety analyses. Furthermore, the proposed changes do not 
    increase the allowed outage times to achieve Cold Shutdown presently 
    specified in the Technical Specifications.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The passively designed once-through process flow cooling 
    arrangement for the charging pumps' seals are recommended by the pump 
    manufacturer with the pump seal manufacturer's concurrence and result 
    in no decrease in the pumps ability to perform their safety function. 
    Our Engineering evaluation has determined that the affected systems 
    ability to mitigate the consequences of any accident as described in 
    the safety analyses is not reduced. The restructuring and relocation of 
    specifications has not reduced any limiting condition for operation or 
    surveillance specification requirements. Changes in allowed outage 
    times are consistent with NUREG-0452, NUREG-1431, or Generic Letter 93-
    05 and our accident analyses. Consequently, the possibility of a new or 
    different kind of accident is not created.
        3. Involve a significant reduction in a margin of safety.
        The modifications to the charging pumps result in improved 
    reliability and improved operability of the CVCS [chemical and volume 
    control system] and SI [safety injection] subsystems. Our Engineering 
    evaluation of the manufacturer's proposed modification and the pump 
    seal manufacturer's concurrence with the modification, have determined 
    this modification to be acceptable with no reduction in the pump's 
    safety-related function. The charging pump modification does not reduce 
    the margin of safety in any part of Technical Specifications or the 
    accident analyses.
        The restructuring of the Chemical and Volume Control System 
    specifications continue to ensure that the reactor can be made 
    subcritical from any operating condition and provide sufficient 
    shutdown margin to preclude inadvertent criticality when in the 
    shutdown condition. The Chemical Volume and Control System remains 
    capable of achieving Cold Shutdown of both units during any operating 
    conditions in accordance with the safety analysis with a minimum 
    specified solution temperature of 112 degrees F. The revised allowed 
    outage times for the Safety Injection System subsystems do not impact 
    the margin of safety * * * in the Technical Specifications bases or the 
    accident analyses.
        The Safety Injection System subsystems continue to maintain 
    sufficient boration capability to mitigate reactivity transients within 
    the design limits associated with postulated accident conditions 
    described within the safety analysis report. The Safety Injection 
    System subsystems ensure that sufficient emergency core cooling 
    capability will be available in the event of a LOCA assuming the loss 
    of one subsystem through any single failure consideration. Either 
    subsystem operating in conjunction with the accumulators remains 
    capable of supplying sufficient core cooling to limit the peak cladding 
    temperatures within acceptable limits in accordance with the loss-of-
    coolant accident analyses.
        The changes ensure that the refueling water storage tank remains 
    capable of providing a sufficient supply of borated water for injection 
    by the emergency core cooling system in the event of a LOCA. The limits 
    specified for refueling water storage tank volume and boron 
    concentration continue to ensure that sufficient solution is available 
    within containment for recirculation cooling flow to the core, and that 
    the reactor will remain subcritical in Cold Shutdown consistent with 
    the LOCA analyses. Consequently, the proposed change to Technical 
    Specifications does not involve a significant reduction [in] the margin 
    of safety within the accident analyses.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
        Attorney for licensee: Michael W. Maupin, Esq., Hunton and 
    Williams, Riverfront Plaza, East Tower, 951 E. Byrd Street, Richmond, 
    Virginia 23219.
        NRC Project Director: Herbert N. Berkow.
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: May 17, 1994.
        Description of amendment request: The proposed amendment would 
    revise Kewaunee Nuclear Power Plant (KNPP) Technical Specification (TS) 
    3.3.c by separating the Internal Containment Spray (ICS) and Spray 
    Additive Systems into two distinct specifications. The proposed 
    amendment would also remove the requirement that for a spray train to 
    be operable, a spray pump suction flow path from the additive tank is 
    needed. In addition, the allowable out of service time for the Spray 
    Additive System would be increased from 48 hours to 72 hours.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        The proposed changes were reviewed in accordance with the 
    provisions of 10 CFR 50.92 to show no significant hazards exist. The 
    proposed changes will not:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The likelihood that an accident will occur is neither increased nor 
    decreased by these TS changes. These TS changes will not impact the 
    function or method of operation of plant equipment. Thus, there is not 
    a significant increase in the probability of a previously analyzed 
    accident due to these changes. No systems, equipment, or components are 
    affected by the proposed changes. Thus, the consequences of the 
    malfunction of equipment important to safety previously evaluated in 
    the Updated Safety Analysis Report (USAR) are not increased by these 
    changes.
        The proposed changes have no impact on accident initiators or plant 
    equipment, and thus, do not affect the probabilities or consequences of 
    an accident.
        (2) Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed TS changes would not create the possibility of a new 
    or different kind of accident from any accident previously evaluated.
        The proposed changes do not involve changes to the physical plant 
    or operations. Since these changes do not contribute to accident 
    initiation, they do not produce a new accident scenario or produce a 
    new type of equipment malfunction. Also, these changes do not alter any 
    existing accident scenarios; they do not affect equipment or its 
    operation, and thus, do not create the possibility of a new or 
    different kind of accident.
        (3) Involve a significant reduction in the margin of safety.
        Operation of the facility in accordance with the proposed TS would 
    not involve a significant reduction in a margin of safety. The proposed 
    changes do not affect plant equipment or operation. Safety limits and 
    limiting safety system settings are not affected by these proposed 
    changes. Extending the time the Spray Additive System may be out of 
    service from 48 hours to 72 hours and removing the requirement to have 
    a spray pump suction flow path from the additive tank for a spray train 
    to be operable is consistent with STS. The STS only require that the 
    spray system be capable of taking suction from the refueling water 
    storage tank and the containment sump.
        The Containment Spray System would still be available and would 
    remove some iodine from the containment atmosphere in the event of a 
    Design Basis Accident. The 72 hour completion time takes into account 
    the Containment Spray System redundant flow path capabilities and the 
    low probability of the worst case Design Basis Accident occurring 
    during this period.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin 
    Library Learning Center, 2420 Nicolet Drive, Green Bay, Wisconsin 
    54301.
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P. O. Box 1497, Madison, Wisconsin 53701-1497.
        NRC Project Director: John N. Hannon.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point 
    Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, Manitowoc 
    County, Wisconsin
    
        Date of amendment request: March 29, 1994.
        Description of amendment request: The proposed amendment would 
    modify Point Beach Nuclear Plant Technical Specification (TS) 15.3.2, 
    ``Chemical and Volume Control System,'' by eliminating the necessity 
    for high concentration boric acid and removing the operability 
    requirements for the associated heat tracing. The basis for Section 
    15.3.2 and applicable surveillances in Table 15.4.1-2 would also be 
    revised to support the above changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. Operation of this facility under the proposed Technical 
    Specifications change will not create a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Reduced boron concentration in the boric acid storage tank (BAST) 
    is offset by increasing the volume of boric acid solution that must be 
    contained in the tanks. The heat tracing requirements are used to 
    ensure that the dissolved boric acid is maintained in solution and 
    available for injection into the RCS to adjust core reactivity 
    throughout core life and to meet GDC requirements. Chemical analyses of 
    boron concentrations of 4.0 weight percent have shown that 
    the boric acid does not crystallize at temperatures above 57 deg.F. 
    Ambient temperatures in the areas of the primary auxiliary building 
    where these components are located will normally remain above this 
    temperature. Hence, heat tracing will no longer be needed for boric 
    acid concentrations with corresponding solubility temperatures less 
    than ambient temperatures. The proposed Technical Specifications 
    requirements for boron concentration, volume, and temperature of the 
    BASTs and boration paths ensure that the capability to inject boric 
    acid is maintained. Since the components (and their function) necessary 
    to achieve a safe shutdown have not been changed or modified, this 
    change does not significantly increase the probability or consequences 
    of any accident previously evaluated.
        The proposed changes to the boric acid system Technical 
    Specifications requirements for the chemical and volume control system 
    (CVCS) do not affect the requirements for the emergency core cooling 
    system (ECCS). The original design of the high head safety injection 
    (SI) system used the BASTs as its initial suction source. Westinghouse 
    WCAP-12602, ``Report For The Reduction of SI System Boron 
    Concentration,'' and a 10 CFR 50.59 Safety Evaluation Report performed 
    by Wisconsin Electric justifies the design change to use the refueling 
    water storage tank (RWST) as the initial suction source of SI fluid 
    rather than the BAST. The affected FSAR Chapter 14 accident analyses 
    include the Loss of Coolant Accident (LOCA) events and the Steamline 
    Break (SLB) events. The LOCA events are affected with respect to the 
    large-break post-LOCA long-term core cooling subcriticality 
    requirement. The SLB events are affected with respect to core 
    integrity. The events were analyzed assuming the elimination of the 
    logic which automatically opened the valves in the flow path from the 
    BASTs to the SI pumps upon the receipt of a safety injection signal. 
    The results show that we remain within the acceptance criteria of the 
    aforementioned FSAR Chapter 14 accident analyses. Therefore, the 
    proposed changes will not create a significant increase in the 
    probability or consequences of a[n] accident previously evaluated.
        2. Operation of this facility under the proposed Technical 
    Specifications change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The reactivity control function of the boron in the CVCS and SI 
    systems is not being changed. Therefore, the proposed changes will not 
    create the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. Operation of this facility under the proposed Technical 
    Specifications change will not create a significant reduction in a 
    margin of safety.
        The intent of the proposed Technical Specifications is to ensure 
    that two independent flow paths from the borated water source(s) (BASTs 
    and/or RWST) to the reactor coolant system are maintained whenever a 
    unit is taken critical. This requires that sufficient quantities of 
    boric acid be stored in the tanks, and that this borated water can be 
    delivered to the reactor coolant system when required. Although we 
    presently require diverse sources of borated water (BAST and RWST), the 
    proposed reduction in diversity will be offset by the significant 
    increase in reliability of the boric acid system due to operation with 
    lower boric acid concentrations and, hence, a much lower probability of 
    boron precipitation and system ``freeze-up.'' Reducing the boric acid 
    concentration in the BASTs has been compensated for by increasing the 
    required volume of boric acid.
        The proposed Technical Specifications requirements for boric acid 
    concentration and volume include the additional specification of 
    minimum temperature that must be maintained to assure boric acid 
    solubility. The minimum temperature requirement is more appropriate 
    than the requirement for heat tracing because it is a more precise 
    means of verifying and assuring solubility. Therefore, the proposed 
    boric acid concentration table, which includes the volume and 
    temperature requirements, is an appropriate substitute for the heat 
    tracing requirements. Although the heat tracing requirement is being 
    eliminated, the boric acid heat tracing system will be available during 
    our transition to the lower boric acid concentration to assist in 
    maintaining boric acid system temperature if necessary. Since our 
    analyses have shown that the existing FSAR Chapter 14 accident analyses 
    remain bounded under the proposed specifications, the margin of safety 
    for the plant is not significantly reduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John N. Hannon.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point 
    Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, Manitowoc 
    County, Wisconsin
    
        Date of amendment request: May 26, 1994.
        Description of amendment request: Point Beach Nuclear Plant is 
    installing two additional emergency diesel generators and reconfigure 
    portions of the 4160 Volt emergency electrical power system. The 
    proposed amendment would revise the Point Beach Nuclear Plant Technical 
    Specifications (TS) to establish the requirements for the electrical 
    systems at Point Beach such that the TS will provide the appropriate 
    guidance for all interim configurations and the final configuration. 
    The majority of changes are incorporated in TS Section 15.3.7, 
    ``Auxiliary Electrical Systems.'' Other Sections modified are 15.3.0, 
    ``General Considerations,'' 15.3.14, ``Fire Protection System,'' and 
    15.4.6, ``Emergency Power System Periodic Tests.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        (1) Operation of this facility under the proposed Technical 
    Specifications will not create a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The Point Beach Nuclear Plant Final Safety Analysis Report (PBNP 
    FSAR) shows that the original emergency diesel generators and the 
    associated support systems and connections do not cause or affect the 
    probability of any accident evaluated in the PBNP FSAR. The additional 
    emergency diesel generators, the associated support systems and 
    connections, and reconfiguration of the emergency AC power system will 
    not change this. The emergency AC power system does not initiate any 
    accident previously evaluated in the PBNP FSAR.
        The limiting conditions for operation and allowable outage times 
    proposed in this license amendment request are consistent with the 
    current requirements in the PBNP Technical Specifications. The proposed 
    change in the required emergency diesel generator (EDG) inspection 
    interval, from annually to the time as recommended by the EDG 
    manufacturer, will continue to maintain the operability and reliability 
    of the EDGs. Therefore, the probability of occurrence of an accident 
    previously evaluated in the FSAR is not increased by the proposed 
    Technical Specifications.
        The consequences of the accidents previously evaluated in the PBNP 
    FSAR are determined by the results of analyses that are based on 
    initial conditions of the plant, the type of accident, transient 
    response of the plant, and the operation and failure of equipment and 
    systems. The new emergency diesel generator installation will meet the 
    requirements for emergency power sources for PBNP.
        General Design Criterion (GDC) 39 as described in the PBNP FSAR, 
    states, ``An emergency power source shall be provided and designed with 
    adequate independency, redundancy, capacity, and testability to permit 
    the functioning of the engineered safety features and protection 
    systems required to avoid undue risk to the health and safety of the 
    public. This power source shall provide this capacity assuming a 
    failure of a single component.''
        The limiting conditions for operation and allowable outage times 
    proposed in this license amendment request are consistent with the 
    requirements in GDC-39 and the current Technical Specifications for 
    PBNP. Therefore, this proposed license amendment does not affect the 
    consequences of any accident previously evaluated in the PBNP FSAR, 
    because the factors that are used to determine the consequences of 
    accidents are not being changed.
        (2) Operation of this facility under the proposed Technical 
    Specifications change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The PBNP FSAR shows that the original emergency diesel generators 
    and the associated support systems and connections do not cause any 
    accident evaluated in the PBNP FSAR. The additional emergency diesel 
    generators, the associated support systems and connections, and 
    reconfiguration of the emergency AC power system will not change this, 
    because the new emergency diesel generators will meet the requirements 
    for emergency power sources for PBNP. Additionally, these changes do 
    not introduce any type of system or component malfunction that would 
    create the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        The limiting conditions for operation and allowable outage times 
    proposed in this license amendment request are consistent with the 
    requirements in GDC-39 and the current Technical Specifications for 
    PBNP. The proposed change in the required EDG inspection interval, from 
    annually to the time as recommended by the EDG manufacturer, will 
    continue to maintain the operability and reliability of the EDGs.
        Therefore, the proposed Technical Specification changes for the 
    addition of two diesel generators and changing the required EDG 
    inspection interval do not create the possibility of an accident of a 
    different type than any previously evaluated in the FSAR.
        (3) Operation of this facility under the proposed Technical 
    Specifications change will not create a significant reduction in a 
    margin of safety.
        The new diesel generator and emergency AC power system 
    reconfiguration design and installation are being and have been 
    performed to meet or exceed the original system design requirements. 
    The emergency diesel generators provide power to the safety equipment 
    that operates to maintain the margins of safety. The new diesel 
    generators and emergency AC power configuration will continue to 
    satisfy this requirement.
        The limiting conditions for operation and allowable outage times 
    proposed in this license amendment request are consistent with the 
    requirements in GDC-39 and the current Technical Specifications for 
    PBNP. The proposed change in the required EDG inspection interval, from 
    annually to the time as recommended by the EDG manufacturer, will 
    continue to maintain the operability and reliability of the EDGs.
        Therefore, the proposed Technical Specification changes for the 
    addition of two diesel generators and changing the required EDG 
    inspection interval do not reduce the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John N. Hannon.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point 
    Beach Nuclear Power Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of amendment request: May 26, 1994.
        Description of amendment request: The proposed amendment would 
    revise the Point Beach Nuclear Plant Technical Specifications (TSs) by 
    extending the operation of both units with the current heatup and 
    cooldown limit curves to 23.6 effective full power years (EFPY). The 
    proposal also would revise the bases for TS Section 15.3.1.B, 
    ``Pressure/Temperature Limits,'' to reflect the methodology for the 
    curve compilation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        We have evaluated these proposed amendments in accordance with the 
    requirements of 10 CFR 50.91(a), against the standards of 10 CFR 50.92, 
    and have determined that these modifications will not result in a 
    significant hazards consideration. A proposed amendment will not 
    involve a significant hazards consideration if it does not (1) involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated, (2) create the possibility of a new or 
    different kind of accident from any accident previously evaluated, or 
    (3) involve a significant reduction in a margin of safety.
        The proposed heatup and cooldown curves are identical to the 
    current heatup and cooldown curves except for their projected 
    expiration. The curves were calculated using the most limiting weld and 
    fluence information from either unit as input to the acceptable 
    methodology of Regulatory Guide 1.99, Revision 2. The consequences or 
    probability of a previously evaluated accident will, therefore, not 
    significantly be increased or a margin of safety reduced.
        The underlying purpose of these curves is to define an acceptable 
    operating range of pressures and temperatures to protect the reactor 
    vessels against non-ductile failure. Since this purpose remains 
    unchanged, a new or different kind of accident cannot be created.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Joseph P. Mann Library, 1516 
    Sixteenth Street, Two Rivers, Wisconsin 54241.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John N. Hannon.
    
    Previously Published Notices of Consideration of Issuance of Amendments 
    to Facility Operating Licenses, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket No. 
    50-461, Clinton Power Station, Unit No. 1, DeWitt County, Illinois
    
        Date of amendment request: June 20, 1994.
        Brief description of amendment request: The proposed amendment 
    would modify Technical Specification 3/4.4.3.1, ``Reactor Coolant 
    Leakage--Leakage Detection Systems,'' to permit continued plant 
    operation with inoperable drywell floor drain sump flow rate monitoring 
    instrumentation. Continued plant operation would be permitted until the 
    first time the plant is required to be brought to COLD SHUTDOWN after 
    July 10, 1994.
        Date of publication of individual notice in Federal Register: June 
    22, 1994 (59 FR 32247).
        Expiration date of individual notice: July 22, 1994.
        Local Public Document Room location: Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    rooms for the particular facilities involved.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of application for amendment: October 19, 1993.
        Brief description of amendment: This amendment removes the scram 
    and Group I isolation valve closure functions associated with the main 
    steamline radiation monitors.
        Date of issuance: June 21, 1994.
        Effective date: June 21, 1994.
        Amendment No.:  154.
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 24, 1993 (58 
    FR 62151).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 21, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois; Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, Will 
    County, Illinois
    
        Date of application for amendments: March 7, 1994, as superseded by 
    your submittal dated March 24, 1994.
        Brief description of amendments: The amendments change Technical 
    Specification (TS) 4.6.1.2, ``Containment Leakage,'' by removing the 
    specific requirement that containment Type A leak testing be performed 
    at 40 10 month intervals. The revised TS now references 
    Appendix J to 10 CFR 50 as governing the performance of Type A testing.
        Date of issuance: June 30, 1994.
        Effective date: June 30, 1994.
        Amendment Nos.:  62, 62, 52, and 52.
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: April 28, 1994 (59 FR 
    22002).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated June 30, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: For Byron, the Byron Public 
    Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for 
    Braidwood, the Wilmington Township Public Library, 201 S. Kankakee 
    Street, Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois Docket 
    Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, Units 1 and 
    2, Rock Island County, Illinois
    
        Date of application for amendments: March 11, 1994.
        Brief description of amendments: The proposed amendments revise 
    Technical Specification 3/4.7.D, ``Primary Containment Isolation 
    Valves'' by adding check valves installed in the reference leg 
    instrumentation line to the Limiting Condition for Operation (LCO) 
    statement of the Technical Specifications. The valves have been 
    installed as part of the modifications required to meet NRC Bulletin 
    93-03, ``Resolution of Issues Related to Reactor Vessel Water Level 
    Instrumentation in BWRs,'' dated May 28, 1993.
        Date of issuance: July 6, 1994.
        Effective date: For Dresden, Unit 2: the license amendment is 
    effective as of the date of its issuance; to be implemented when the 
    modifications are complete and prior to restart from any cold shutdown 
    after June 30, 1994, or restart from the 14th refuel outage, which ever 
    is first. For Dresden, Unit 3: the license amendment is effective as of 
    the date of its issuance; to be implemented within 30 days. For Quad 
    Cities, Unit 1: the license amendment is effective as of the date of 
    its issuance; to be implemented within 30 days. For Quad Cities, Unit 
    2: the license amendment is effective as of the date of its issuance; 
    to be implemented prior to restart following the 13th refueling outage.
        Amendment Nos.:  For Dresden, Unit 2: Amendment No. 128; for 
    Dresden, Unit 3: Amendment No. 122; for Quad Cities, Unit 1: Amendment 
    No. 148; for Quad Cities, Unit 2: Amendment No. 144.
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29 and DPR-30. 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: April 13, 1994 (59 FR 
    17593).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated July 6, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: For Dresden, the Morris Public 
    Library, 604 Liberty Street, Morris, Illinois 60450; for Quad Cities, 
    the Dixon Public Library, 221 Hennepin Avenue, Dixon, Illinois 61021.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam Neck 
    Plant, Middlesex County, Connecticut
    
        Date of application for amendment: January 28, 1994.
        Brief description of amendment: The amendment modifies Surveillance 
    Requirement 4.6.1.2.d, regarding the Appendix J testing requirements 
    for the purge supply and exhaust valves, and removes surveillance 
    requirement 4.6.1.2.f regarding the purge and exhaust valves.
        Date of issuance: June 27, 1994.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.:  173.
        Facility Operating License No. DPR-61. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27051).
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated June 27, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, Connecticut 06457.
    
    Consolidated Edison Company of New York, Docket No. 50-003 and Docket 
    No. 50-247, Indian Point Nuclear Generating Unit Nos. 1 and 2, 
    Westchester County, New York
    
        Date of application for amendments: September 29, 1993.
        Brief description of amendments: The amendments revise the 
    Technical Specifications (TSs) Administrative sections dealing with the 
    administrative control of keys for doors preventing unauthorized access 
    to High Radiation Areas in which the intensity of radiation exceeds 
    1000 mrem/hr. Specifically, the amendments revise TS Section 4.1.8.1.b 
    for Indian Point Generating Unit No. 1 and TS Section 6.12.1.b for 
    Indian Point Generating Unit No. 2 to add the Radiation Protection 
    Manager as one of the two positions which can administratively control 
    the keys.
        Date of issuance: July 7, 1994.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.:  43 and 171.
        Facility Operating License Nos. DPR-5 and DRP-26: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 24, 1993 (58 
    FR 62153).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated July 7, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Detroit Edison Company, Docket No. 50-341, Fermi-2, Monroe County, 
    Michigan
    
        Date of application for amendment: March 29, 1994, as corrected 
    April 26, 1994.
        Brief description of amendment: The amendment revises the 
    surveillance requirements for scram discharge volume vent and drain 
    valves and isolation actuation instrumentation and modifies the 
    required actions and surveillance requirements for the emergency diesel 
    generators to reduce testing during power operation. These changes are 
    in accordance with guidance contained in Generic Letter (GL) 93-05, 
    ``Line-Item Technical Specifications Improvements to Reduce 
    Surveillance Requirements for Testing During Power Operation,'' dated 
    September 27, 1993.
        Date of issuance: June 28, 1994.
        Effective date: June 28, 1994, with full implementation within 45 
    days.
        Amendment No.:  99.
        Facility Operating License No. NPF-43. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27053).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 28, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161.
    
    Detroit Edison Company, Docket No. 50-341, Fermi-2, Monroe County, 
    Michigan
    
        Date of application for amendment: April 26, 1994.
        Brief description of amendment: The amendment revises the limiting 
    conditions for operation and surveillance requirements in the Technical 
    Specifications (TS) to delete reference to instrument response time 
    limit tables for the reactor protection system, instrument actuation 
    system and emergency core cooling system. These tables are also being 
    moved from the TS to the updated final safety analysis report.
        Date of issuance: June 29, 1994.
        Effective date: June 29, 1994, with full implementation within 60 
    days.
        Amendment No.:  100.
        Facility Operating License No. NPF-43. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27053).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 29, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: March 30, 1994.
        Brief description of amendments: The amendments revise Technical 
    Specification Table 4.3-3 to allow the analog channel operational test 
    interval for radiation monitoring instrumentation to be increased from 
    monthly to quarterly and are consistent with the guidance in Generic 
    Letter 93-05, ``Line-Item Technical Specifications Improvements to 
    Reduce Surveillance Requirements for Testing During Power Operation.''
        Date of issuance: July 5, 1994.
        Effective date: July 5, 1994.
        Amendment Nos.:  121/115.
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27054).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated July 5, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, Turkey 
    Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: April 19, 1994.
        Brief description of amendments: These amendments change the 
    surveillance interval specified for air or smoke flow test through the 
    containment spray header from once per 5 years to once per 10 years.
        Date of issuance: June 28, 1994.
        Effective date: June 28, 1994.
        Amendment Nos. 165 and 159.
        Facility Operating Licenses Nos. DPR-31 and DPR-41: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27055).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated June 28, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, Turkey 
    Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: November 25, 1992 as 
    supplemented by letter dated March 4, 1994.
        Brief description of amendments: These amendments implement Generic 
    Letter 90-06, ``Resolution of Generic Issue 70, `Power-Operated Relief 
    Valve and Block Valve Reliability,' and Generic Issue 94, `Additional 
    Low-Temperature Overpressure Protection for Light-Water Reactors,' 
    Pursuant to 10 CFR 50.54(f).''
        Date of issuance: June 28, 1994.
        Effective date: June 28, 1994.
        Amendment Nos. 166 and 160.
        Facility Operating Licenses Nos. DPR-31 and DPR-41: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 14, 1993 (58 FR 
    19478).
        The licensee's letter of March 4, 1994 did not change the no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated June 28, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile Island 
    Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of application for amendment: June 12, 1991.
        Brief description of amendment: The amendment revises the plant 
    Technical Specifications to clarify the setpoint ranges for the 
    pressurizer power-operated relief valve and provides action statements 
    to be satisfied when setpoint ranges are not met.
        Date of issuance: June 30, 1994.
        Effective date: As of its date of issuance to be implemented within 
    60 days.
        Amendment No.: 186.
        Facility Operating License No. DPR-50. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 10, 1991 (56 FR 
    31435).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 30, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, Pennsylvania 17105.
    
    Illinois Power Company and Soyland Power Cooperative, Inc., Docket No. 
    50-461, Clinton Power Station, Unit No. 1, DeWitt County, Illinois
    
        Date of application for amendment: June 20, 1994.
        Brief description of amendment: The amendment revised the Technical 
    Specifications by modifying a footnote to Technical Specification 3/
    4.4.3.1, ``Reactor Coolant System Leakage--Leakage Detection Systems,'' 
    to permit continued plant operations with inoperable drywell floor 
    drain sump flow monitoring instrumentation until the first time the 
    plant is required to be brought to cold shutdown after July 10, 1994.
        Date of issuance: July 8, 1994.
        Effective date: July 8, 1994.
        Amendment No.: 90.
        Facility Operating License No. NPF-62. The amendment revised the 
    Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration: Yes (59 FR 32247 dated June 22, 1994). That notice 
    provided an opportunity to submit comments on the Commission's proposed 
    no significant hazards consideration determination. No comments have 
    been received. The notice also provided for an opportunity to request a 
    hearing by July 22, 1994, but indicated that if the Commission makes a 
    final no significant hazards consideration determination any such 
    hearing would take place after issuance of the amendment.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, and final determination of no significant 
    hazards consideration are contained in a Safety Evaluation dated July 
    8, 1994.
        Local Public Document Room location: The Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, Illinois 61727.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of application for amendment: February 10, 1992, as 
    supplemented April 14, 1994.
        Brief description of amendment: The amendment removes two tables 
    from the Technical Specifications which list reactor trip system 
    instrumentation response times and engineered safety features actuation 
    system instrumentation response times. These tables will be placed in 
    the Millstone 3 Technical Requirements Manual.
        Date of issuance: June 28, 1994.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 91.
        Facility Operating License No. NPF-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27058).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 28, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, Connecticut 06360.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of application for amendment: March 23, 1994.
        Brief description of amendment: The amendment modifies Technical 
    Specification Table 3.7-6, ``Area Temperature Monitoring,'' by creating 
    two zones for the main steam valve building (MSVB) and increasing the 
    maximum normal excursion temperature limit for this area from 120 deg.F 
    to 140 deg.F. Technical Specification Table 3.7-6 currently identifies 
    the entire MSVB with a temperature limit of 120 deg.F.
        Date of issuance: June 29, 1994.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 92.
        Facility Operating License No. NPF-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 28, 1994 (59 FR 
    22009).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 29, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Community-Technical College, Thames Valley Campus, 574 New London 
    Turnpike, Norwich, Connecticut 06360.
    
    Northern States Power Company, Docket No. 50-263, Monticello Nuclear 
    Generating Plant, Wright County, Minnesota
    
        Date of application for amendment: January 4, 1994, as supplemented 
    March 28, 1994.
        Brief description of amendment: The amendment modifies Section 
    3.11, Reactor Fuel Assemblies, by removing information concerning the 
    analytical method to determine average planar linear heat generation 
    rate and adding a reference to the Core Operating Limits Report. In 
    Section 6.7, Reporting Requirements, the listing of approved analytical 
    methods for developing the Core Operating Limits Report is revised and 
    the specific version of the analytical methods used to develop the 
    report is identified. Also, the Bases for Section 3.11 concerning the 
    calculational methodology for minimum critical power ratio was revised.
        Date of issuance: June 30, 1994.
        Effective date: June 30, 1994.
        Amendment No.: 88.
        Facility Operating License No. DPR-22. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 2, 1994 (59 FR 
    10011).
        The March 28, 1994, letter provided clarifying information that was 
    within the scope of the March 2, 1994, notice. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    June 30, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401.
    
    Pacific Gas and Electric Company, Docket No. 50-133, Humboldt Bay Power 
    Plant, Unit 3, Humboldt County, California
    
        Date of application for amendment: July 7, 1993. (Reference HBL-93-
    041)
        Brief description of amendment: This amendment modified the 
    Technical Specifications incorporated in Facility Operating License No. 
    DPR-7 as Appendix A by revising technical specification VII.H.3, 
    ``Semiannual Radioactive Effluent Release Report,'' to extend the 
    reporting period from semiannually to annually and to change the report 
    submission date from 60 days after January 1 and July 1 of each year to 
    before April 1 of each year.
        Date of issuance: June 30, 1994.
        Effective date: This license amendment is effective as of the date 
    of its issuance and must be fully implemented no later than 30 days 
    from the date of issuance.
        Amendment No.: 26.
        Facility Operating License No. DPR-7: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 19, 1994 (59 FR 
    2869).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 30, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Humboldt County Library, 636 F 
    Street, Eureka, California 95501.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of application for amendments: September 1, 1992 and October 
    15, 1992 as supplemented by letters dated October 30, 1992, March 16, 
    1993, June 10, 1993, July 28, 1993, September 10, 1993, April 29, 1994, 
    June 2, 1994, June 9, 1994, and June 15, 1994.
        Brief description of amendments: The amendments extend the interval 
    for certain Technical Specifications surveillance requirements to 24 
    months with an additional 25-percent grace period.
        Date of issuance: June 28, 1994.
        Effective date: As of 30 days after the date of issuance.
        Amendment Nos.:  71 and 34.
        Facility Operating License Nos. NPF-39 and NPF-85: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: September 16, 1992 (57 
    FR 42778) and October 28, 1992 (57 FR 48823).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated June 28, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket No. 50-352, Limerick Generating 
    Station, Unit 1, Montgomery County, Pennsylvania
    
        Date of application for amendment: May 6, 1994, as supplemented by 
    letter dated June 3, 1994.
        Brief description of amendment: This amendment revised TS Section 
    5.5.3, ``Capacity,'' to facilitate an interim increase in the Unit 1 
    Spent Fuel Pool from 2040 fuel assemblies to 2500 fuel assemblies.
        Date of issuance: June 30, 1994.
        Effective date: June 30, 1994.
        Amendment No.:  72.
        Facility Operating License No. NPF-39. This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27063).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 30, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Power Authority of the State of New York, Docket No. 50-333, James A. 
    FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: December 22, 1993.
        Brief description of amendment: The amendment removes the reference 
    to American Society for Testing and Materials (ASTM) Standard D 270-65 
    from Technical Specification Surveillance Requirement 4.12A.1.i. ASTM D 
    270-65, which specifies procedures to draw a representative fuel oil 
    sample, has been superseded and is no longer in effect. The amendment 
    will allow ASTM D 4057-88 or subsequent industry standards to be used 
    for the sampling of diesel fire pump fuel oil.
        Date of issuance: June 27, 1994.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.:  214.
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 2, 1994 (59 FR 
    4944).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 27, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Power Authority of the State of New York, Docket No. 50-333, James A. 
    FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: January 31, 1994.
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 3.8, ``Miscellaneous Radioactive Materials 
    Sources,'' to adopt the Limiting Conditions for Operation of Section 3/
    4.7.6, ``Sealed Source Contamination,'' in NUREG-0123, ``Standard 
    Technical Specifications for General Electric Boiling Water Reactors 
    (BWR/5).'' The amendment also reformats TSs 3.8 and 4.8 to make them 
    consistent with the remainder of the TSs.
        Date of issuance: June 27, 1994.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 215.
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 2, 1994 (59 FR 
    10014).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 27, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260, and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2, and 3, Limestone County, 
    Alabama
    
        Dates of application for amendments: July 19, 1993 (TS-334).
        Brief description of amendments: The amendments remove the 
    Technical Specifications (TS) addressing reactor coolant chemistry 
    limits and associated sampling requirements that are applicable when 
    the reactor is defueled. The TS requirements being removed have been 
    conservatively incorporated into the BFN chemistry program as elements 
    of a licensee-controlled procedure. Any future changes to these 
    chemistry requirements must be evaluated in accordance with 10 CFR 
    50.59 to determine whether the changes involve an unreviewed safety 
    question. A change involving an unreviewed safety question would 
    require a license amendment and NRC review and approval prior to 
    implementation. In addition, changes to the reactor coolant chemistry 
    TS, applicable when fuel is in the reactor, are included in these 
    amendments to provide clarification and to ensure consistency in 
    requirements among units.
        Date of issuance: June 28, 1994.
        Effective date: June 28, 1994.
        Amendment Nos.:  208, 224 and 181.
        Facility Operating License Nos. DPR-33, DPR-52, and DPR-68: 
    Amendments revised the Technical Specifications.
        Dates of initial notice in Federal Register: November 10, 1993 (58 
    FR 59756).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 28, 1994.
        No significant hazards consideration comments received: None
        Local Public Document Room location: Athens Public Library, South 
    Street, Athens, Alabama 35611.
    
    Tennessee Valley Authority, Docket Nos. 50-259 and 50-296, Browns Ferry 
    Nuclear Plant, Units 1 and 3, Limestone County, Alabama
    
        Date of application for amendment: July 2, 1992 (TS 314)
        Brief description of amendments: The amendments revise requirements 
    associated with Residual Heat Removal valve pressure switches in the 
    Browns Ferry Units 1 and 3 Technical Specifications.
        Date of issuance: June 30, 1994.
        Effective date: June 30, 1994.
        Amendment Nos.:  209 and 182.
        Facility Operating License Nos. DPR-33 and DPR-68: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 28, 1992 (57 FR 
    48826).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 30, 1994.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Athens Public Library, South 
    Street, Athens, Alabama 35611.
    
    The Cleveland Electric Illuminating Company, Centerior Service Company, 
    Duquesne Light Company, Ohio Edison Company, Pennsylvania Power 
    Company, Toledo Edison Company, Docket No. 50-440, Perry Nuclear Power 
    Plant, Unit No. 1, Lake County, Ohio
    
        Date of application for amendment: February 28, 1992.
        Brief description of amendment: The amendment revises Technical 
    Specification Table 3.3.7.1-1 and Table 4.3.7.1-1 to remove the area 
    criticality monitors for the fuel preparation pool, spent fuel pool, 
    and the upper containment pools and their associated action statements, 
    notes, and surveillance requirements. Editorial changes were made as 
    required in the tables.
        Date of issuance: June 28, 1994.
        Effective date: June 28, 1994.
        Amendment No. 62.
        Facility Operating License No. NPF-58 This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 24, 1992 (57 FR 
    28205).
        The Commission's related evaluation of the amendment is contained 
    in an Environmental Assessment dated June 13, 1994, and in a Safety 
    Evaluation dated June 28, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse Nuclear 
    Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: January 31, 1994.
        Brief description of amendment: This amendment revises TS 3/4.1.1.2 
    to permit the reduction of boron concentration of water within the 
    reactor coolant system (RCS), subject to certain restrictions, when the 
    reactor is in Mode 5 and RCS flow is less than 2800 gpm. This amendment 
    is related to Amendment No. 176, which was issued by the NRC on 
    December 8, 1992, and incorporated a similar revision for Mode 6 
    operation.
        Date of issuance: June 28, 1994.
        Effective date: June 28, 1994.
        Amendment No. 188.
        Facility Operating License No. NPF-3: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 16, 1994 (59 FR 
    12369).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 28, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak Steam 
    Electric Station, Unit Nos. 1 and 2, Somervell County, Texas
    
        Date of amendment request: February 14, 1994.
        Brief description of amendments: The amendments revise the 
    technical specifications by replacing the requirements for reporting 
    radiological effluents from semiannual to annual, and the report due 
    dates from 60 days after January 1 and July 1 to prior to May 1. The 
    changes are consistent with the requirements for reporting radioactive 
    effluent releases specified in 10 CFR 50.36a.
        Date of issuance: June 1, 1994.
        Effective date: June 1, 1994, to be implemented within 30 days of 
    issuance.
        Amendment Nos.:  Unit 1--Amendment No. 25; Unit 2--Amendment No. 
    11.
        Facility Operating License Nos. NPF-87 and NPF-89. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 28, 1994 (59 FR 
    22016).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated June 1, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 701 South Cooper, P.O. 
    Box 19497, Arlington, Texas 76019.
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: February 17, 1994.
        Brief description of amendment: The amendment modifies the 
    administrative section of the technical specifications (TS) to reflect 
    management and organizational changes at the Washington Public Power 
    Supply System (the licensee) for operation of the WNP-2 facility. The 
    proposed changes would (1) modify the reporting responsibility of the 
    quality assurance organization from the Managing Director to the 
    Assistant Managing Director, Operations (AMDO), and (2) modify the 
    appointment authority for the Corporate Nuclear Safety Review Board 
    (CNSRB) from the Managing Director to the AMDO. These changes are 
    proposed to reflect the current designation of the AMDO as the 
    licensee's designated official with corporate responsibility for 
    overall plant nuclear safety and as the direct report for the CNSRB.
        In addition, the proposed change would (1) delete the specific 
    requirement for health physics/chemistry program procedures, (2) modify 
    the titles of two positions on the Plant Operations Committee (POC) to 
    reflect revised organizational titles, and (3) delete the requirement 
    that the CNSRB Executive Secretary be designated from the CNSRB 
    membership.
        The staff denies the licensee's request to change CNSRB membership 
    requirements from nine personnel to a minimum of nine personnel.
        Date of issuance: June 28, 1994.
        Effective date: 5 days after the date of issuance.
        Amendment No.: 126.
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 13, 1994 (59 FR 
    17609).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 28, 1994.
        Public comments on proposed no significant hazards consideration 
    comments received: No.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352.
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: May 5, 1994.
        Brief description of amendment: The amendment changes equipment 
    numbering on three primary containment isolation valves.
        Date of issuance: June 28, 1994.
        Effective date: June 28, 1994.
        Amendment No.: 127.
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 12, 1994 (59 FR 
    24762).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 28, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek 
    Generating Station, Coffey County, Kansas.
    
        Date of amendment request: February 24, 1994.
        Brief description of amendment: The amendment revises Technical 
    Specification 3.9.4, Containment Building Penetrations, to allow the 
    use of temporary alternate closure methods for the emergency personnel 
    escape lock and containment wall penetrations, during core alterations 
    or movement of irradiated fuel within the containment.
        Date of issuance: July 7, 1994.
        Effective date: July 7, 1994, to be implemented within 30 days of 
    issuance.
        Amendment No.: 74.
        Facility Operating License No. NPF-42. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 13, 1994 (59 FR 
    17610).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated July 7, 1994.
        No significant hazards consideration comments received: No.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621.
    
        Dated at Rockville, Maryland, this 13th day of July 1994.
    
        For the Nuclear Regulatory Commission.
    John A. Zwolinski,
    Acting Director, Division of Reactor Projects--III/IV, Office of 
    Nuclear Reactor Regulation.
    [FR Doc. 94-17503 Filed 7-19-94; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
07/20/1994
Department:
Nuclear Regulatory Commission
Entry Type:
Uncategorized Document
Document Number:
94-17503
Dates:
June 21, 1994.
Pages:
0-0 (1 pages)
Docket Numbers:
Federal Register: July 20, 1994