99-19133. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 64, Number 144 (Wednesday, July 28, 1999)]
    [Notices]
    [Pages 40903-40914]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 99-19133]
    
    
    -----------------------------------------------------------------------
    
    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Pub. L. 97-415, the U.S. Nuclear Regulatory Commission 
    (the Commission or NRC staff) is publishing this regular biweekly 
    notice. Public Law 97-415 revised section 189 of the Atomic Energy Act 
    of 1954, as amended (the Act), to require the Commission to publish 
    notice of any amendments issued, or proposed to be issued, under a new 
    provision of section 189 of the Act. This provision grants the 
    Commission the authority to issue and make immediately effective any
    
    [[Page 40904]]
    
    amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from July 3, 1999, through July 16, 1999. The 
    last biweekly notice was published on July 14, 1999 (64 FR 38022).
    
    Notice of Consideration of Issuance of Amendments to Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules and 
    Directives Branch, Division of Administration Services, Office of 
    Administration, U.S. Nuclear Regulatory Commission, Washington, DC 
    20555-0001, and should cite the publication date and page number of 
    this Federal Register notice. Written comments may also be delivered to 
    Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville, 
    Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of 
    written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC. The 
    filing of requests for a hearing and petitions for leave to intervene 
    is discussed below.
        By August 27, 1999, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition, and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which much include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
    
    [[Page 40905]]
    
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Carolina Power & Light Company, Docket No. 50-261, H.B. Robinson Stream 
    Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of amendment request: March 26, 1999.
        Description of amendment request: The proposed change provides a 
    Required Action and Completion Time for the Ultimate Heat Sink (UHS) in 
    the event that service water temperature exceeds the current 95 deg.F 
    surveillance limit. It involves an allowance to continue operation for 
    a period of 8 hours with the UHS at a temperature greater than the 
    temperature limits provided in Technical Specification (TS) Limiting 
    Condition of Operation 3.7.8, ``Ultimate Heat Sink (UHS)'' and provides 
    an upper UHS temperature limit beyond which plant shutdown is required.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Carolina Power & Light (CP&L) Company has evaluated the proposed 
    Technical Specification change and has concluded that it does not 
    involve a significant hazards consideration. The conclusion is in 
    accordance with the criteria set forth in 10 CFR 50.92. The bases 
    for the conclusion that the proposed change does not involve a 
    significant hazards consideration are discussed below.
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change does not involve any physical alteration of 
    plant systems, structures or components. The proposed change will 
    allow plant operation for a short period of time when the service 
    water temperature exceeds 95 deg.F. If the service water temperature 
    is restored within the allowed time, a plant shutdown is not 
    required. This minimizes plant transients, which reduces the 
    probability of a reactor trip and the resulting challenges to 
    mitigating systems. A service water temperature of up to 99 deg.F 
    does not increase the failure rate of systems, structures or 
    components because the systems, structures, and components are 
    designed for higher temperatures than at which they operate.
        The Service Water (SW) System temperature is not assumed to be 
    an initiating condition of any accident evaluated in the safety 
    analysis report. Therefore, the allowance of a limited time for 
    service water temperature to be in excess of 95 deg.F does not 
    involve an increase in the probability of an accident previously 
    evaluated in the safety analysis report (SAR). The SW System 
    supports operability of safety related systems used to mitigate the 
    consequences of an accident. The service water temperature is not 
    expected to increase significantly beyond 95 deg.F due to the 
    limited time allowed by the proposed change in conjunction with the 
    generally slow rate of temperature increase experienced from thermal 
    changes in Lake Robinson. The capability of components to perform 
    their safety related function is not affected up to a service water 
    temperature of 99 deg.F with the exception of the Containment Air 
    Recirculation Fan Coolers. The heat removal capacity of the 
    Containment Air Recirculation Fan Coolers is not expected to be 
    significantly reduced by a small increase in service water 
    temperature. If heat removal is not significantly reduced, 
    containment pressure and leakage will not be significantly 
    increased, and the doses from containment leakage will not be 
    significantly increased. Therefore, the proposed change does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated in the SAR.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change does not involve any physical alteration of 
    plant systems, structures or components. A service water temperature 
    of up to 99 deg.F does not introduce new failure mechanisms of 
    systems, structures or components not already considered in the SAR 
    because the systems, structures, and components are designed for 
    higher temperatures than at which they operate. Therefore, the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated is not created.
        3. Does this change involve a significant reduction in a margin 
    of safety?
        The proposed change will allow a small increase in service water 
    temperature above the design basis limit for the SW System and delay 
    by 8 hours the requirement to shutdown the plant when the service 
    water system design limit is exceeded. There are design margins 
    associated with systems, structures and components that are cooled 
    by the service water system that are affected. The capability of 
    components to perform their safety related function is not affected 
    up to a service water temperature 99 deg.F with the exception of the 
    Containment Air Recirculation Fan Coolers. The Containment Air 
    Recirculation Fan Coolers remove heat from containment to mitigate 
    containment pressure and temperature following a MSLB (main 
    streamline break) inside containment or a Large Break LOCA (loss-of-
    coolant accident) inside containment. An increase in service water 
    temperature in excess of the design limit due to hot weather 
    conditions is expected to be small due to the limited time allowed 
    by the proposed change in conjunction with the generally slow rate 
    of temperature increase experienced from thermal changes in Lake 
    Robinson. Therefore, the effect on the Containment Air Recirculation 
    Fan Coolers' heat removal capacity and the resulting containment 
    pressure and temperature is expected to be small. Therefore, there 
    is no significant reduction in margin of safety associated with this 
    change.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550.
        Attorney for licensee: William D. Johnson, Vice President and 
    Corporate Secretary, Carolina Power & Light Company, Post Office Box 
    1551, Raleigh, North Carolina 27602.
        NRC Section Chief: Sheri R. Peterson.
    
    Commonwealth Edison Company, Docket Nos. 50-254 and 50-265, Quad Cities 
    Nuclear Power Station, Units 1 and 2, Rock Island County, Illinois
    
        Date of amendment request: June 29, 1999.
        Description of amendment request: This amendment request proposes 
    to increase the notch testing surveillance interval of partially 
    withdrawn control rods in Technical Specification Surveillance 
    Requirement 3/4.3.C,
    
    [[Page 40906]]
    
    ``Reactivity Control--Control Rod Operability,'' from an interval of 
    once in 7 days to once in 31 days.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Does the change involve a significant increase in the 
    probability of occurrence or consequences of an accident previously 
    evaluated?
        The proposed change extends the Surveillance Frequency for 
    partially withdrawn control rods. The change does not affect 
    equipment design or operation. The affected Surveillance is not 
    considered to be an accident initiator. Therefore, this change will 
    not significantly increase the probability of an accident previously 
    evaluated. Furthermore, extension of the Surveillance Frequency will 
    not impact the ability to perform its function following an 
    accident.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any previously evaluated.
        Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The extension of the Surveillance Frequency does not involve 
    physical modification to the plant and does not introduce a new mode 
    of operation.
        Therefore, the change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Does the change involve a significant reduction in a margin of 
    safety?
        The change in the Surveillance Frequency only provides a minor 
    reduction in the probability of finding an inoperable control rod. 
    Most of the control rods will continue to be tested on the current 
    Frequency. However, if one stuck rod is identified, all rods must be 
    checked promptly.
        Therefore, these changes do not involve a significant reduction 
    in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) 
    are satisfied. Therefore, the NRC staff proposed to determine that 
    the requested amendments involve no significant hazards 
    consideration.
    
        Local Public Document Room location: Dixon Public Library, 221 
    Hennepin Avenue, Dixon, Illinois 61021.
        Attorney for licensee: Ms. Pamela B. Stroebel, Senior Vice 
    President and General Counsel, Commonwealth Edison Company, P.O. Box 
    767, Chicago, Illinois 60690-0767.
        NRC Section Chief: Anthony J. Mendiola.
    
    GPU Nuclear, Inc., et al., Docket No. 50-289, Three Mile Island Nuclear 
    Station, Unit 1, Dauphin County, Pennsylvania
    
        Date of amendment request: April 1, 1999.
        Description of amendment request: The proposed license amendment 
    would modify the Technical Specifications (TSs) to incorporate certain 
    improvements from the Revised Standard Technical Specifications for B&W 
    Plants (NUREG-1430) that would add limiting conditions for operation 
    action statements, make surveillance requirements more consistent with 
    the revised standard TSs, correct conflicts or inconsistencies from 
    earlier TS revisions, correct administrative errors, and revise the 
    spent fuel pool sampling from monthly and after adding chemicals to 
    weekly.
        The staff's proposed no significant hazards determination below 
    does not address the licensee's proposed changes with respect to a high 
    pressure injection system operation in a low temperature overpressure 
    environment.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability of occurrence or consequences of an accident previously 
    evaluated. The proposed amendment makes administrative corrections, 
    adds conditions to the limiting conditions of operation [LCOs], 
    revises selected time clocks and surveillance requirements 
    consistent with NUREG 1430, and adds a time clock to a unique LCO. 
    These changes have no effect on the plant design or operation. The 
    reliability of systems and components relied upon to prevent or 
    mitigate the consequences of accidents previously evaluated is not 
    degraded by proposed changes. Therefore, operation in accordance 
    with the proposed amendment does not involve a significant increase 
    in the probability of occurrence or consequences of an accident 
    previously evaluated.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any previously evaluated, because no new 
    accident initiators would be created.
        3. Operation of the facility in accordance with the proposed 
    amendment will not involve a significant reduction in a margin of 
    safety because no changes to plant operating limits or limiting 
    safety system settings are proposed.
    
        The NRC staff has reviewed the licensee's analysis and based on the 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Law/Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 22037.
        NRC Section Chief: S. Singh Bajwa.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of amendment request: June 4, 1999.
        Description of amendment request: This application for amendment to 
    the Indian Point 3 Technical Specifications (TSS) proposes to revise 
    the definition of operating personnel in section 6.2.2.g to make it 
    consistent with the Standard Technical Specifications and to remove a 
    footnote.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licenses has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated?
        No, these TS changes are administrative in nature. Removing the 
    statement in section 6.2.2.g that defines on shift operating 
    personnel and adding a new paragraph consistent with the Standard 
    Technical Specifications is an administrative line item change that 
    follows NRC guidance. The current statement is not needed because TS 
    Table 6.2.1 defines the minimum operations shift crew composition 
    and commitments to Table B-1 of NUREG-0654 defines the minimum 
    staffing requirements for each function area.
        The change to TS 6.2.2.i is administrative in nature. The 
    statement that reads, ``For the period ending three years after 
    restart from the 1993/1994 Performance Improvement Outage, the 
    Operations Manager will be permitted to have held a SRO [senior 
    reactor operator] license at a Pressurized Water Reactor other than 
    Indian Point Unit 3'', was a relaxation of the requirements of 
    6.2.2i.
        Therefore, these changes will not increase the probability or 
    consequences of an accident previously evaluated, because they are 
    administrative and affect neither accident initiation or mitigation.
        2. Does the proposed license amendment create the possibility of 
    a new or different
    
    [[Page 40907]]
    
    kind of accident from any accident previously evaluated?
        No, these TS changes are administrative in nature. Removing the 
    statement in section 6.2.2.g that defines on shift operating 
    personnel and adding a new paragraph consistent with the Standard 
    Technical Specifications is an administrative line item change that 
    follows NRC guidance. The current statement is not needed because TS 
    Table 6.2-1 defines the minimum operations shift crew composition 
    and commitments to Table B-1 of NUREG-0654 defines the minimum 
    staffing requirements for each function area.
        The change to TS 6.2.2.i is administrative in nature. The 
    statement that reads, ``For the period ending three years after 
    restart from the 1993/1994 Performance Improvement Outage, the 
    Operations Manager will be permitted to have held a SRO license at a 
    Pressurized Water Reactor other than Indian Point Unit 3'', was a 
    relaxation of the requirements of 6.2.2.i.
        These changes are administrative, and do not affect how the 
    plant is operated. They also follow the guidance of the Standard 
    Technical Specifications. Therefore, these changes will not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        No, these TS change is administrative in nature. Removing the 
    statement in section 6.2.2.g that defines on shift operating 
    personnel and adding a new paragraph consistent with the Standard 
    Technical Specification is an administrative line item change that 
    follows NRC guidance. The current statement is not needed because TS 
    Table 6.2-1 defines the minimum operations shift new composition and 
    commitments to Table B-1 of NUREG-0654 defines the minimum staffing 
    requirements for each function area.
        The change to TS 6.2.2.i is administrative in nature. The 
    statement that reads, ``For the period ending three years after 
    restart from the 1993/1994 Performance Improvement Outage, the 
    Operations Manager will be permitted to have held a SRO license at a 
    Pressurized Water Reactor other than Indian Point Unit 3'', was a 
    relaxation of the requirements of 6.2.2.i.
        These changes are administrative, and do not affect how the 
    plant is operated. They also follow the guidance of the Standard 
    Technical Specifications. Therefore, these changes do not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposed to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
        Attorney for Licensee; Mr. David E. Blabey, 10 Columbus Circle, New 
    York, New York 10019.
        NRC Section Chief: S. Singh Bajwa.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Units 2 and 3, San Diego 
    County, California
    
        Description of amendment requests: The licensee proposed changes to 
    Technical Specification (TS) 3.3.5 ``ESFAS Instrumentation'' to include 
    restrictions on operation with a channel of the refueling water storage 
    tank level-low input to the recirculation actuation signal (RAS) and 
    the steam generator pressure-low input or steam generator pressure 
    difference-high input to the emergency feedwater actuation signal 
    (EFAS) in the tripped condition. The current TS allows plant operation 
    in this condition indefinitely. The licensee has determined that 
    unacceptable consequences could result from a spurious trip of RAS or 
    EFAS due to operation with a channel in trip condition. The licensee 
    states that the proposed TS changes would improve plant operational 
    safety and, thereby, reduce plant risk.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Will operation of the facility in accordance with this 
    proposed change involve a significant increase in the probability or 
    consequences of an accident previously evaluated?
        Response: No.
        This change provides limits for operating with a channel of the 
    Refueling Water Storage Tank (RWST) Level-Low input in the 
    Recirculation Actuation Signal (RAS) or the Steam Generator (SG) 
    Pressure-Low or SG Pressure Difference (SGPD)-High input to the 
    Emergency Feedwater Actuation Signal (EFAS) in trip.
        As a result of this change, the potential for an inadvertent 
    actuation of either of these two signals is reduced. The proposed 
    Completion Times are based on Probabilistic Risk Assessment (PRA) 
    considerations, and are conservative compared to the current 
    unlimited Completion Times.
        The consequences of an inadvertent actuation of EFAS or RAS are 
    unaffected by this change.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        (2) Will operation of the facility in accordance with this 
    proposed change create the possibility of a new or different kind of 
    accident from any accident previously evaluated?
        Response: No.
        This proposed change provides additional time limits on 
    operation with a channel of the RWST Level-Low input to RAS or the 
    SG Pressure-Lower SGPD-High inputs to EFAS in trip. Operation in 
    this condition is currently allowed indefinitely. The proposed 
    restrictions reduce the possibility of an inadvertent actuation of 
    RAS or EFAS, and do not allow operation in any configuration not 
    currently allowed by the Technical Specifications (TSs).
        Therefore, this proposed change will not create the possibility 
    of a new or different kind of accident from any accident that has 
    been previously evaluated.
        (3) Will operation of the facility in accordance with this 
    proposed change involve a significant reduction in a margin of 
    safety?
        Response: No.
        The proposed change provides additional time limits on operation 
    with a channel of the RWST Level-Low input to RAS or the SG 
    Pressure-Low or SGPD-High inputs to RAS or EFAS in trip. The 
    proposed limits are conservative compared to the current 
    requirements, where the time limit is unrestricted. The overall 
    impact of the change will be [an] increase in the margin of safety.
        Therefore, there will be no significant reduction in a margin of 
    safety as a result of this change.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, Irvine, California 92713.
        Attorney for licensee: Douglas K. Porter, Esquire, Southern 
    California Edison Company, 2244 Walnut Grove Avenue, Rosemead, 
    California 91770.
        NRC Section Chief: Stephen Dembek.
    
    Tennessee Valley Authority, Docket No. 50-328, Sequoyah Nuclear Plant, 
    Unit 2, Hamilton County, Tennessee
    
        Date of application for amendments: June 7, 1999 (TS 99-09).
        Brief description of amendments: The proposed amendment would 
    change the Sequoyah Unit 2 Technical Specification (TS) requirements by 
    adding a new temporary Figure 3.4-1a and temporary footnotes to TS 
    3.4.8, ``Specific Activity,'' Table 4.4-4, and to corresponding Bases 
    in order to raise the reactor coolant specific activity limit to 1.0 
    microcurie per milligram Dose Equivalent iodine-131 for the remainder 
    of Unit 2 Cycle 10 operation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), Tennessee Valley 
    Authority, the licensee, has provided its analysis of the issue of no 
    significant hazards
    
    [[Page 40908]]
    
    consideration, which is presented below:
    
        A. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed TS change increases the allowed reactor coolant 
    specific activity for iodine-131 and decreases the leakage quantity 
    that would be postulated to occur at the faulted steam generator 
    (SG) during a main steam line break (MSLB) accident. The described 
    changes will return these parameters to the same values under which 
    the plant operated prior to the implementation of TS Change 98-02 
    submitted on June 26, 1998. The June 26, 1998 submittal was a 
    voluntary change that allowed for a greater leakage quantity during 
    an MSLB accident as described in Generic Letter 95-05. Returning 
    these parameters to their previous values does not affect or 
    increase the probability of any accidents previously evaluated.
        An increase in the consequences of an accident would not occur 
    because the proportional increase in reactor coolant specific 
    activity, while proportionally decreasing the allowable primary-to-
    secondary leakage during a postulated MSLB accident to values under 
    which the plant was previously operated, was evaluated in [Topical 
    Report No.] WCAP-13990 during the establishment of the original 
    primary-to-secondary leak limits. No changes to the physical plant, 
    to the plant operation, or maintenance practices have been 
    implemented that would invalidate the limits defined in WCAP-13990.
        The control room dose, the low population zone dose, and the 
    dose at the exclusion area boundary remain bounded by the acceptance 
    criteria of the Updated Final Safety Analysis Report. Therefore, the 
    proposed TS change does not result in an increase in the 
    consequences of an accident previously analyzed.
        B. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed TS change does not alter the configuration of the 
    plant. The changes do not directly affect plant operation. The 
    change will not result in the installation of any new equipment or 
    systems or the modification of any existing equipment or systems. No 
    new operating procedures, conditions, or modes will be created by 
    this proposed change. SG tube structural integrity, as defined in 
    draft Regulatory Guide 1.121, remains unchanged. Therefore, the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated is not created.
        C. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        Raising the allowed reactor coolant specific activity, while 
    decreasing the allowed primary-to-secondary leakage during a 
    postulated MSLB accident, keeps the amount of activity released to 
    the environment unchanged. Design basis and offsite dose calculation 
    assumptions remain satisfied. Therefore, the proposed change does 
    not result in a significant reduction in the margin of safety.
    
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 10H, Knoxville, Tennessee 37902.
        NRC Section Chief: Sheri R. Peterson.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak Steam 
    Electric Station (CPSES), Units 1 and 2, Somervell County, Texas
    
        Date of amendment request: May 24, 1999, as supplemented by letter 
    dated July 9, 1999.
        Brief description of amendments: The proposed license amendments 
    would remove several cycle-specific parameter limits from the Technical 
    Specifications (TSs). These parameter limits would be added to the Core 
    Operating Limits Report (COLR). Appropriate references to the COLR 
    would be inserted in the affected TSs. In addition, the core safety 
    limit curves would be replaced with safety limits more directly 
    applicable to the fuel and fuel cladding fission product barriers. The 
    affected Technical Specifications are: (1) TS 2.0, ``Safety Limits 
    (SLs),'' (2) TS 3.3.1, ``Reactor Trip System Instrumentation 
    Setpoints,'' (3) TS 3.4.1, ``RCS pressure temperature and flow from 
    Nucleate Boiling (DNB) Limits,'' and (4) TS 5.6.5, ``Core Operating 
    Limits Report.'' The May 24, 1999, application was previously noticed 
    and published in the Federal Register on June 30, 1999 (64 FR 53213).
        The July 9, 1999, supplement provided proposed additional 
    information that would: (a) Add the Reactor Core Safety Limit figures 
    to the COLR, (b) clarify that the overpower N-16 setpoint remains in 
    the TSs, and (c) reflect NRC approval of the topical reports used to 
    determine the core operating limits presented in the COLR. The 
    supplemental information is being noticed herein to address the issue 
    of no significant hazards consideration.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Do the proposed changes involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes remove cycle-specific parameter limits from 
    the Technical Specifications, add them to the list of limits 
    contained in the Core Operating Limits Report (COLR), and revise the 
    Administrative Controls section of the Technical Specifications. The 
    proposed changes also insert the original minimum RCS flow limits 
    into the Technical Specifications. The changes do not, by 
    themselves, alter any of the parameter limits. The changes are 
    administrative in nature and have no adverse effect on the 
    probability of an accident or on the consequences of an accident 
    previously evaluated. The removal of parameter limits from the 
    Technical Specifications does not eliminate the requirement to 
    comply with the parameter limits.
        The parameter limits in the COLR may be revised without prior 
    NRC approval. However, [Technical] Specification 5.6.5c continues to 
    ensure that the parameter limits are developed using NRC-approved 
    methodologies and that applicable limits of the safety analyses are 
    met. While future changes to the COLR parameter limits could result 
    in event consequences which are either slightly less or slightly 
    more severe than the consequences for the same event using the 
    present parameter limits, the differences would not be significant 
    and would be bounded by the requirement of specification 5.6.5c to 
    meet the applicable limits of the safety analysis.
        Based on the above, addition of the minimum RCS flow limit into 
    the Technical Specifications, removal of the parameter limits the 
    Technical Specifications and the addition of the described limits in 
    the COLR, thus allowing revision of the parameter limits without 
    prior NRC approval, has no significant effect on the probability or 
    consequences of an accident previously evaluated.
        2. Do the proposed changes create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        The proposed changes add the minimum RCS flow limit into the 
    Technical Specifications, remove certain parameter limits from the 
    Technical Specifications and add these limits to the list of limits 
    in the COLR, thus removing the requirements for prior NRC approval 
    of revisions to those parameters. The changes do not add new 
    hardware or change plant operations and therefore cannot initiate an 
    event nor cause an analyzed event to progress differently. Thus, the 
    possibility of a new or different kind of accident is not created.
        3. Do the proposed changes involved a significant reduction in a 
    margin of safety?
        The margin of safety is the difference between the acceptance 
    criteria and the associated failure values. The proposed changes do 
    not affect the failure values for any parameter. Though the accident 
    analyses, all applicable limits (i.e., relevant event acceptance 
    criteria as described in the NRC-approved analysis methodologies) 
    are shown to be satisfied; therefore, there is no impact
    
    [[Page 40909]]
    
    on event acceptance criteria. Because neither the failure values nor 
    the acceptance criteria are affected, the proposed change has no 
    effect on the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas 76019.
        Attorney for licensee: George L. Edgar, Esq., Morgan, Lewis and 
    Bockius, 1800 M Street, NW., Washington, DC 20036.
        NRC Section Chief: Robert A. Gramm.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont.
    
        Date of amendment request: May 26, 1999.
        Description of amendment request: The licensee proposed revising 
    the suppression pool water temperature surveillance requirements to 
    specify monitoring the temperature every 5 minutes when performing 
    testing that adds to the suppression pool. In addition, the licensee 
    proposed revising the requirement to check the suppression chamber 
    water level and temperature from ``once per shift'' to ``daily'' and 
    specify that it is the average temperature that is checked.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided the NCR its analysis of the issue of no significant hazard 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below:
        1. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment, will not involve a significant 
    increase in the probability or consequences of an accident previously 
    evaluated.
        Vermont Yankee has determined that the proposed change will not 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated. The proposed change revises the 
    surveillance frequency for ``once per shift'' suppression pool water 
    level and temperature monitoring. Additionally, the surveillance 
    requirement for suppression pool water temperature monitoring when 
    there are indications of relief valve operation that add heat to the 
    suppression pool is also revised. The proposed change will revise the 
    surveillance wording such that routine suppression pool monitoring will 
    be ``daily'' and an operator will verify pool temperature every 5 
    minutes only during testing that adds heat to the suppression pool. 
    Also clarified, is that the parameter being monitored is ``average'' 
    suppression pool water temperature.
        The consequence of an accident previously evaluated is not 
    significantly increased since the initial suppression pool water 
    temperature limit, which is an input valve for accident analyses, is 
    not changed.
        The proposed change affects only surveillance requirements and does 
    not require any hardware or equipment modification. Equipment 
    operation, plant limiting conditions for operation, and accident 
    analyses will be unchanged. Therefore, the proposed change does not 
    involve a significant increase in the probability or consequences of 
    accidents.
        2. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment, will not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        Vermont Yankee has determined that the proposed change does not 
    create the possibility of a new or different kind of accident from any 
    accident previously evaluated. The proposed change involves revision of 
    Technical Specification surveillance requirements. There are no 
    hardware modifications or equipment changes involved and operation of 
    plant equipment will be unchanged. Thus, no new or different accident 
    precursors will be created by this change.
        3. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment, will not involve a significant 
    reduction in a margin or safety. VY has determined that the proposed 
    change does not involve a significant reduction in a margin of safety. 
    The proposed change involves revision of Technical Specification 
    surveillance requirements. There are no hardware modifications or 
    equipment changes involved and plant operation and accident analyses 
    are unchanged. The initial suppression pool water temperature limit, 
    which is an input value for accident analyses, is not changed. 
    Therefore, the proposed change will not involve a significant reduction 
    in the margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
        Attoney for licensee: Mr. David R. Lewis, Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037-1128.
        NRC Section Chief: James W. Clifford.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of amendment request: June 29, 1999.
        Description of amendment request: The licensee proposed revising 
    the leak rate requirements of Technical Specifications 3.7.A.4 and 
    4.7.A.4 for the main steam line isolation valves. Specifically, a total 
    leakage rate allowable value for the sum of the four main steam lines 
    is proposed that is equal to four times the current individual main 
    steam line isolation valve leakage rate allowable value. The individual 
    main steam line isolation valve leakage rate allowable value is 
    proposed to be one half of the total leakage rate allowable value.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        1. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The proposed change does not involve a change to the plant 
    design or operation. As a result, the proposed change does not 
    affect any of the parameters or conditions that contribute to the 
    initiation of any accidents previously evaluated. Thus, the proposed 
    change cannot increase the probability of any accident previously 
    evaluated.
        The proposed change does not affect the leak-tight integrity of 
    the containment structure that is designed to mitigate the 
    consequences of a loss-of-coolant accident (LOCA). The primary 
    containment must maintain functional integrity during and following 
    the peak transient pressures and temperatures that result from any 
    LOCA, thereby limiting fission product leakage following the 
    accident. Because the proposed change does not alter any of the 
    fission product lead rate assumptions used in the design basis LOCA 
    analysis, the analyzed consequences of the Loss of Coolant Accident 
    are not changed.
        The control room radiological habitability analysis uses as an 
    input assumption main steam line leakage rate at four times the 
    current Technical Specifications limit. An allowable value for total 
    main steam line
    
    [[Page 40910]]
    
    leakage rate equivalent to four times the current Technical 
    Specifications limit for a single main steam line isolation valve is 
    being added by this change. Thus, there is no effect on the main 
    control room radiological habitability calculation.
        Based on the above VY [Vermont Yankee] has concluded that the 
    proposed change will not result in a significant increase in the 
    probability or consequences of any accident previously evaluated.
        2. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The proposed change does not involve a change to the plant 
    design or operation. As a result, the proposed change does not 
    affect any parameters or conditions that could contribute to the 
    initiation of any accident. The methods of performing the tests are 
    not changed. No new accident modes are created. No safety-related 
    equipment or safety functions are altered as a result of this 
    change. Restating the acceptance criteria while maintaining the 
    assumptions of all affected calculations has no influence over nor 
    does it contribute to, the possibility of a new or different kind of 
    accident or malfunction from those previously evaluated.
        Based on the above VY has concluded that the proposed change 
    will not create the possibility of a new or different kind of 
    accident from those previously evaluated.
        3. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment will not involve a 
    significant reduction in a margin of safety.
        Restating the acceptance criteria for the main steam line 
    isolation valve leakage rate while maintaining the assumptions of 
    all affected calculations does not impact the margin of safety. The 
    0.6La maximum and minimum pathway leakage rate acceptance 
    criteria provide the previously analyzed margin of safety. The 
    testing method for determining the leak-tightness of the main steam 
    line isolation valves has not changed. The leak rate test results 
    are presently added to the Types B and C tests summation. The 
    0.6La maximum and minimum pathway leak rate acceptance 
    criteria and the proposed Technical Specifications requirements 
    provide assurance that component degradation does not impact the 
    assumptions used to determine, nor provide a reduction in, and the 
    analyzed margin of safety.
        Based on the above VY has concluded that the proposed change 
    will not cause a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
        Attorney for licensee: Mr. David R. Lewis, Shaw, Pittman, Potts and 
    Trobridge, 2300 N Street, NW., Washington, DC 20037-1128.
        NRC Section Chief: James W. Clifford.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont.
    
        Date of amendment request: July 12, 1999.
        Description of amendment request: The amendment would revise the 
    value for the Safety Limit Minimum Critical Power Ratio (SLMCPR) and 
    delete the wording specifying these as Cycle 20 values.
        Basis for proposed no significant hazards consideration 
    determination: As required by to CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        1. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment, will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The basis of the SLMCPR is to ensure no mechanistic fuel damages 
    is calculated to occur if the limit is not violated. The new SLMCPR 
    values preserve the existing margin to transition boiling and 
    probability of fuel damage is not increased. The derivation of the 
    revised SLMCPR for Vermont Yankee for incorporation into the 
    Technical Specifications, and its use to determine plant and cycle-
    specific thermal limits, have been performed using NRC approved 
    methods. These plant-specific calculations are performing each 
    operating cycle and if necessary, will require future changes to 
    these values based upon revised core designs. The revised SLMCPR 
    values do not change the method of operating the plant and have no 
    effect on the probability of an accident initiating event or 
    transient.
        Based on the above, Vermont Yankee has concluded that the 
    proposed change will not result in a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment, will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The proposed changes result only from a specific analysis for 
    the Vermont Yankee core reload design and deletion of a cycle 
    specific reference for the values. These changes do not involve any 
    new or different method for operating the facility and do not 
    involve any facility modifications. No new initiating events or 
    transients result from these changes.
        Based on the above, Vermont Yankee has concluded that the 
    proposed change will not create the possibility of a new or 
    different kind of accident from those previously evaluated.
        3. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment, will not involve a 
    significant reduction in a margin of safety.
        The new SLMCPR is calculated using NRC approved methods with 
    plant and cycle specific parameters for the current core design. The 
    SLMCPR value remains high enough to ensure that greater than 99.9% 
    of all fuel rods in the core will avoid transition boiling if the 
    limit is not violated, thereby preserving the fuel cladding 
    integrity. The operating MCPR limit is set appropriately above the 
    safety limit value to ensure margin when the cycle specific 
    transients are evaluated.
        As a result, Vermont Yankee has determined that the proposed 
    change will not result in a significant reduction in a margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point 
    Beach Nuclear Plant, Units 1 and 2, Town of Two Creeks, Manitowoc 
    County, Wisconsin
    
        Date of amendment request: June 22, 1999 (TSCR 210).
        Description of amendment request: The proposed amendments reflect 
    changes to the Point Beach Nuclear Plant (PBNP) Units 1 and 2 Technical 
    Specifications (TSs) in order to incorporate the Westinghouse 422V+ 
    fuel assemblies into the PBNP reactor cores. Basis for proposed no 
    significant hazards consideration determination: As required by 10 CFR 
    50.91(a), the licensee has provided its analysis of the issue of no 
    significant hazards consideration which is presented below:
    
        1. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not result in a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The accidents which are potentially affected by the parameters 
    and assumptions associated with this amendment have been evaluated/
    analyzed and all design standards and applicable safety criteria are 
    met. The consideration of these changes does not result in a 
    situation where the design and construction standards that were 
    applicable prior to the change are altered. Therefore, the changed 
    occurring with this amendment will not result in any additional 
    challenges to plant equipment that could increase the probability of 
    any previously evaluated accident.
        The proposed changes associated with this amendment do not 
    affect plant systems such that their function in the control of
    
    [[Page 40911]]
    
    radiological consequences is adversely affected. The safety 
    evaluation (included in Attachment 2 of this submittal) documents 
    that the design standards and applicable safety criteria limits 
    continue to be met and therefore fission barrier integrity is not 
    challenged. The proposed changes have been shown not to adversely 
    affect the response of the plant to postulated accident scenarios. 
    Existing system and component redundancy and operation is not being 
    changed by these proposed changes. These changes will therefore not 
    affect the mitigation of the radiological consequences of any 
    accident described in the FSAR [final safety analysis report].
        In some cases, the results of the revised radiological analyses 
    are greater than those of the current FSAR analysis. In other cases, 
    the new and old analyses are not directly comparable because the 
    radiological bases for the new analyses have been upgraded to meet 
    more current NRC requirements. However, in all cases, the calculated 
    doses are well within the regulatory acceptance criteria and do not 
    constitute an unacceptable significant increase in consequences. 
    Since the actual plant configuration, performance of systems, and 
    initiating event mechanisms are not being changed as a result of 
    this evaluation, the probability or consequences of an accident 
    previously evaluated is not significantly increased.
        2. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The possibility for a new or different type of accident from any 
    accident previously evaluated is not created as a result of this 
    amendment. The changes described in the amendment are supported by 
    the analyses and evaluations described in Attachment 2 (safety 
    evaluation). The evaluation of the effects of the proposed changes 
    indicate that all design standards and applicable safety criteria 
    limits are met. These changes therefore do not cause the initiation 
    of any new or different accident nor create any new failure 
    mechanisms.
        All equipment important to safety will continue to operate as 
    designed. Component integrity is not challenged. The changes do not 
    result in any event previously deemed incredible being made 
    credible. The changes do not result in more adverse conditions or 
    result in any increase in the challenges to safety systems. 
    Therefore, operation of the Point Beach Nuclear Plant in accordance 
    with the proposed amendments will not create the possibility of a 
    new or different type of accident from any accident previously 
    evaluated.
        3. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments does not involve a significant reduction in 
    a margin of safety.
        The proposed changes do not involve a significant reduction in 
    the margin of safety. Existing component redundancy is not being 
    changed by these proposed changes. There are no new or significant 
    changes to the initial conditions contributing to accident severity 
    or consequences. The margin of safety is maintained by assuring 
    compliance with acceptance limits reviewed and approved by the NRC. 
    Since all of the appropriate acceptance criteria for the various 
    analyses and evaluations have been met as discussed in Attachment 2 
    (Safety Evaluation) of this submittal and provided for information 
    in Attachment 4 (PBNP FSAR Chapter 14 ``Safety Analysis'' changes 
    required as a result of the analyses performed for the upgraded 
    fuel) of this submittal, by definition there has not been a 
    significant reduction of any margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Lester Public Library, 
    1001 Adams Street, Two Rivers, Wisconsin 54241.
        Attorney for licensee: John H. O'Neill, Jr., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Section Chief: Claudia M. Craig.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, Point 
    Beach Nuclear Plant, Units 1 and 2, Town of Two Creeks, Manitowoc 
    County, Wisconsin
    
        Date of amendment request: July 1, 1999 (TSCR 214).
        Description of amendment request: The proposed amendments reflect a 
    change to Point Beach Nuclear Plant (PBNP) Units 1 and 2 Technical 
    Specification (TS) Section 15.5.4. The amendment request proposes to 
    remove one of the two separate methods for verifying the acceptability 
    of reactor fuel for placement and storage in the spent fuel pool.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        1. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not create a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed changes are administrative only in that they remove 
    the ability to use the reference Koo method for 
    determining the acceptability of fuel for placement and storage in 
    the spent fuel pool and new fuel storage vault at the Point Beach 
    Nuclear Plant. Use of the remaining approved method and requirements 
    ensure that fuel placed or stored in the spent fuel pool and new 
    fuel storage vault continues to be in accordance with their 
    respective design and licensing basis. That is, fuel in the storage 
    array will continue to meet the design basis requirement that 
    Keff remain less than 0.95. No modifications are being 
    made to the spent fuel pool and its cooling system or to the new or 
    spent fuel storage racks. Since the design basis of the fuel and 
    storage racks continue to be met, operation in accordance with the 
    proposed amendments cannot create a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        No physical modifications are being made to the spent fuel pool 
    and cooling system or to the new or spent fuel storage racks. All 
    design basis requirements for ensuring the safe storage of fuel in 
    the spent fuel pool continue to be met. Therefore, operation in 
    accordance with the proposed amendments cannot create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. Operation of the Point Beach Nuclear Plant in accordance with 
    the proposed amendments does not create a significant reduction in a 
    margin of safety.
        Technical Specification requirements for placing and storing 
    fuel in the spent fuel pool continue to ensure that the design basis 
    requirement, Keff for the fuel array in the spent fuel 
    pool and new fuel storage remains less than 0.95, is maintained. The 
    existing margin of safety established by this design requirement is 
    maintained. Therefore, operation in accordance with the proposed 
    amendments cannot create a reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: The Lester Public Library, 
    1001 Adams Street, Two Rivers, Wisconsin 54241.
        Attorney for license: John H. O'Neill, Jr., Shaw, Pittman, Potts, 
    and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Section Chief: Claudia M. Craig.
    
    Previously Published Notice of Consideration of Issuance of 
    Amendments to Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, and Opportunity for a Hearing
    
    Texas Utilities Electric Company, Docket Nos. 50-445 and 50-446, 
    Comanche Peak Steam Electric Station, Unit Nos. 1 and 2, Somervell 
    County, Texas
    
        Date of amendment request: May 27, 1999, as supplemented by letter 
    dated May 28, 1999
    
    [[Page 40912]]
    
        Description of amendment request: The proposed amendments would add 
    a footnote to Technical Specification (TS) 4.8.2.1e, ``D.C. Sources-
    Operating,'' which would, on a one-time basis for Unit 1 Battery 
    BT1ED2, allow the licensee to substitute a performance discharge test 
    ``*  *  * in lieu of the battery service test required by Specification 
    4.8.2.1d, twice within a 60 month interval.''
        Date of publication of individual notice in Federal Register: June 
    14, 1999. (64 FR 31881).
        Expiration date of individual notice: July 14, 1999.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter 1, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of application for amendment: December 21, 1998, as 
    supplemented on January 28, February 18, April 2, April 15, and April 
    16, 1999.
        Brief description of amendment: This amendment makes changes to 
    Facility Operating License No. DPR-35, the Technical Specifications, 
    and Materials License No. 20-07626-04 to reflect the transfer of the 
    licenses from Boston Edison Company to Entergy Nuclear Generation 
    Company.
        Date of issuance: July 13, 1999.
        Effective date; As of the date of issuance, and shall be 
    implemented within 30 days.
        Amendment No.: 181.
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications and License.
        Date of initial notice in Federal Register: January 26, 1999 (64 FR 
    3984). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated April 29, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of application for amendment: March 3, 1999.
        Brief description of amendment: The amendment modified Technical 
    Specification Table 4.6-3, ``Reactor Vessel Material Surveillance 
    Program Withdrawal Schedule.'' The amendment changed the withdrawal 
    schedule for the upcoming reactor vessel surveillance capsule pull from 
    approximately 15 effective full power years to approximately 18 
    effective full power years.
        Date of issuance: July 15, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days.
        Amendment No.: 182.
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 19, 1999 (64 FR 
    27316). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 15, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-389, 
    St. Lucie Plant, Unit Nos. 1 and 2, St Lucie County, Florida
    
        Date of application for amendments: December 1, 1997, supplemented 
    August 26, 1998.
        Brief description of amendments: Revised the Technical 
    Specifications (TS), Appendix B, Environmental Protection Plan (Non-
    Radiological), to implement the terms and conditions of the incidental 
    Take Statement included in the Biological Opinion issued by the 
    National Marine Fisheries Service, regarding endangered sea turtles.
        Date of Issuance: July 2, 1999.
        Effective Date: July 2, 1999.
        Amendment Nos.: 162 and 103.
        Facility Operating License Nos. DPR-67 and NPF-16: Amendments 
    revised the TS.
        Date of initial notice in Federal Register: December 31, 1997 (62 
    FR 68305). The supplemental letter dated August 26, 1998, provided 
    clarifying information that did not change the original no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated July 2, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New Location County, Connecticut
    
        Date of application for amendment: June 5, 1998, as supplemented 
    January 13, 1999.
        Brief description of amendment: The proposed revision to the 
    Millstone Unit 3 licensing basis would address a recent steam generator 
    tube rupture (SGTR) analysis that was determined to be an unreviewed 
    safety question. The SGTR analyses described in the Final Safety 
    Analysis Report (FSAR) include an offside dose analysis and a margin to 
    overfill analysis. Both of the analyses have been updated. The offsite 
    dose analysis was updated to reflect a larger capacity for the steam 
    generator atmospheric dump valve (ADV) and a decrease in the operator 
    response time to close the ADV block valve. The
    
    [[Page 40913]]
    
    margin to overfill analysis was updated to reflect a new single 
    failure.
        Date of issuance: July 2, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 60 days from the date of issuance.
        Amendment No.: 172.
        Facility Operating License Nos. DPR-49: Amendments authorizes 
    revisions to the FSAR,
        Date of initial notice in Federal Register: July 1, 1998 (63 FR 
    35992).
        The January 13, 1999, supplemental letter provided clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated July 2, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-335, Millstone 
    Nuclear Power Station, Unit No. 2, New Location County, Connecticut
    
        Date of application for amendment: March 19, 1999.
        Brief description of amendment: The amendment relocated Technical 
    Specifications Sections 3.3.3.2, ``Instrumentation, Incore Detectors,'' 
    3.3.3.3, ``Instrumentation, Seismic Instrumentation,'' and 3.3.3.4, 
    ``Instrumentation, Meteorological Instrumentation,'' to the Millstone, 
    Unit No. 2, Technical Requirements Manual. Index page V and TS Bases 
    have been revised to reflect the above relocations.
        Dated of issuance: July 13, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 60 days from the date of issuance.
        Amendment No.: 237.
        Facility Operating License Nos. DPR-65: Amendment Revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 21, 1998 (64 FR 
    19560).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated July 13, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
    
    PP&L, Inc., Docket Nos. 50-387 and 50-388, Susquehanna Steam Electric 
    Station, Units 1 and 2, Luzerne County, Pennsylvania
    
        Date of application for amendment: November 26, 1999, which was 
    superseded by letter dated June 1, 1998, as supplemented by letters 
    dated October 30, 1998, March 29, 1999, April 20, 1999, and May 28, 
    1999.
        Brief description of amendment: These amendment would replace the 
    current ultimate heat sink average water temperature limit for all 
    combination of plant operations.
        Dated of issuance: July 6, 1999.
        Effective date: Both units, effective as of date of issuance and 
    shall be implemented within 30 days.
        Amendment Nos.: 182 and 156.
        Facility Operating License Nos. NPF-14 and NPF-22: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 20, 1998 (63 FR 
    27764). The October 30, 1998, March 29, 1999, April 20, 1999, and May 
    28, 1999, letters provided clarifying information that did not change 
    the initial proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated July 6, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilker-Barre, PA 18701.
    
    PP&L, Inc., Docket Nos. 50-387 and 50-388, Susquehanna Steam Electric 
    Station, Units 1 and 2, Luzerne County, Pennsylvania
    
        Date of application for amendment: November 23, 1999.
        Brief description of amendments: The amendments modified the 
    Susquehanna Steam Electric Station, Units 1 and 2, Technical 
    Specifications limiting condition for operation, 3.8.3, and 
    surveillance requirements, 3.8.3.1, to increase the minimum fuel oil 
    storage tank volume ranges.
        Dated of issuance: July 7, 1999.
        Effective date: Units 1 and 2, as of date of issuance and shall be 
    implemented within 30 days.
        Amendment Nos.: 183 and 157.
        Facility Operating License Nos. NPF-14 and NPF-22: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 27, 1999 (64 FR 
    4160).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated July 7, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Osterhout Free Library, 
    Reference, Department, 71 South Franklin Street, Wikes-Barre, PA 18701.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Units 2 and 3, San Diego 
    County, California
    
        Date of application for amendments: October 17, 1997, as 
    supplemented March 2 and November 28, 1998.
        Brief description of amendments: These amendments authorize changes 
    to the updated Final Safety Analysis Report (FSAR) to permit 
    installation of digital radiation monitors for both the containment 
    purge isolation and the control room isolation signals.
        Date of issuance: July 12, 1999.
        Effective date: July 12, 1999; implementation shall include 
    submission by the licensee of the revised description authorized by 
    these amendments with the next update of the FSAR in accordance with 10 
    CFR 50.71(e).
        Amendment Nos.: Unit 2-154; Unit 3-145.
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the FSAR.
        Date of initial notice in Federal Register: January 28, 1998 (63 FR 
    4324).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated July 12, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P.O. Box 19557, Irvine, California 92713.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf Creek 
    Generating Station, Coffey County, Kansas
    
        Date of application for amendments: January 12,1999, as 
    supplemented by letters dated May 11, and June 30, 1999.
        Brief description of amendments: The amendment revised Technical 
    Specification 3/4.7.5, Ultimate Heat Sink, by adding a new action 
    statement to be used in the event the plant inlet water temperature 
    exceeds 90 deg. F. The amendment is effective only through September 
    30, 1999, and is only for the current TSs. The amendment is also 
    limited to a maximum plant inlet water temperature of 94 deg. F. The 
    proposal to raise this temperature to 95 deg. F will be addressed in a 
    future letter.
    
    [[Page 40914]]
    
        Date of issuance: July 8, 1999.
        Effective date: July 8, 1999, shall be implemented within 30 days 
    of the date of issuance.
        Amendment No.: 125.
        Facility Operating License No. NPF-42: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 24, 1999 ( 64 
    FR 9203). The May 11 and June 30, 1999, supplemental letters provided 
    additional clarifying information, did not expand the scope of the 
    application as originally noticed and did not change the staff's 
    original proposed no significant hazards consideration determination, 
    except that the licensee proposed a maximum plant inlet water 
    temperature of 95 deg. F. where the letters of January and May 11, 
    1999, proposed only 94 deg. F. The amendment is limited to a maximum 
    temperature of 94 deg. F.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated July 8, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621.
    
        Dated at Rockville, Maryland, this 21st day of July 1999.
    
        For the Nuclear Regulatory Commission.
    John A. Zwolinski,
    Director, Division of Licensing Project Management Office of Nuclear 
    Reactor Regulation.
    [FR Doc. 99-19133 Filed 7-27-99; 8:45 am]
    BILLING CODE 7590-01-M
    
    
    

Document Information

Published:
07/28/1999
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
99-19133
Dates:
As of the date of issuance and shall be implemented within 30 days.
Pages:
40903-40914 (12 pages)
PDF File:
99-19133.pdf