95-16249. Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations; Biweekly Notice  

  • [Federal Register Volume 60, Number 128 (Wednesday, July 5, 1995)]
    [Notices]
    [Pages 35058-35091]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 95-16249]
    
    
    
    -----------------------------------------------------------------------
    
    
    NUCLEAR REGULATORY COMMISSION
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations; Biweekly Notice
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from June 10, 1995, through June 22, 1995. The 
    last biweekly notice was published on June 21, 1995 (60 FR 32359).
    
    Notice of Consideration of Issuance of Amendments to Facility Operating 
    Licenses, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. 
    
    [[Page 35059]]
    Under the Commission's regulations in 10 CFR 50.92, this means that 
    operation of the facility in accordance with the proposed amendment 
    would not (1) involve a significant increase in the probability or 
    consequences of an accident previously evaluated; or (2) create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated; or (3) involve a significant reduction in a 
    margin of safety. The basis for this proposed determination for each 
    amendment request is shown below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By August 4, 1995, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the 
    
    [[Page 35060]]
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station, Unit Nos. 
    1, 2, and 3, Maricopa County, Arizona
    
        Date of amendment requests: May 2, 1995.
        Description of amendment requests: The proposed amendment would 
    remove from the technical specifications (TS) plant elevations for the 
    minimum water volume required in the spent fuel pool (SFP) and relocate 
    them to site procedures. This proposed TS amendment also includes two 
    changes to correct administrative errors in the TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis about the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change eliminates the plant elevations from TS 
    Figure 3.1-1, ``Minimum Borated Water Volumes'' for the SFP. The 
    change is administrative in nature and does not involve any 
    modifications to plant equipment or affected plant operation. The 
    required volume of water in the SFP is identified on the figure and 
    will remain unchanged by this amendment. This request relocates the 
    plant elevations to site procedures where they will be controlled in 
    accordance with the provisions of 10 CFR 50.59.
        The removal of the reference to Table 3.8-2 in the Unit 3 TS 
    3.8.4.1 and adding the word ``containment'' to the Unit [2] TS 
    4.6.3.1 are administrative change[s] and do not involve any 
    modifications to plant equipment or affect plant operation. These 
    administrative changes do not affect the scope or intent of any test 
    within the TS.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change eliminates the plant elevations from TS 
    Figure 3.1-1, ``Minimum Borated Water Volumes'' for the SFP. The 
    change is administrative in nature and does not involve any 
    modifications to plant equipment or affect plant operation. The 
    removal of plant elevations from the figure does not cause any 
    change in the method by which any safety-related system performs its 
    function. The required volume of water in the SFP is identified on 
    the figure and will remain unchanged by this amendment.
        The removal of the reference to Table 3.8-2 in the Unit 3 TS 
    3.8.4.1 and adding the word ``containment'' to the Unit 2 TS 4.6.3.1 
    are administrative changes and do not involve any modifications to 
    plant equipment or affect plant operation. These administrative 
    changes do not affect the scope or intent of any test within the TS.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change eliminates the plant elevations from TS 
    Figure 3.1-1, ``Minimum Borated Water Volumes'' for the SFP. The 
    change is administrative in nature and does not involve any 
    modifications to plant equipment or affect plant operation. The 
    required volume of water in the SFP is identified on the figure and 
    will remain unchanged by this amendment.
        The removal of the reference to Table 3.8-2 in the Unit 3 TS 
    3.8.4.1 and adding the word ``containment'' to the Unit 2 TS 4.6.3.1 
    are administrative changes and do not involve any modifications to 
    plant equipment or affect plant operation. These administrative 
    changes do not affect the scope or intent of any test within the TS.
        Therefore, based upon the above, the proposed change does not 
    involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    that review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004.
        Attorney for licensees: Nancy C. Loftin, Esq., Corporate Secretary 
    and Counsel, Arizona Public Service Company, P.O. Box 53999, Mail 
    Station 9068, Phoenix, Arizona 85072-3999.
        NRC Project Director: William H. Bateman.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert County, 
    Maryland
    
        Date of amendments request: June 2, 1995.
        Description of amendments request: The proposed amendments would 
    revise the pressurizer safety valve setpoint tolerance ``as-found'' 
    acceptance criterion to +2%/-1% for the valve with the lower setpoint 
    (RC-200) and plus or minus 2% for the valve with the upper setpoint 
    (RC-201). The ``as-left'' setpoint tolerance will remain plus or minus 
    1% for both valves.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The pressurizer safety valves are used to prevent exceeding the 
    Reactor Coolant System (RCS) pressure safety limit. The proposed 
    change to increase the pressurizer safety valve setpoint tolerance 
    for the ``as-found'' acceptance criteria from [plus or minus]1% to 
    +2%/-1% for the valve with the lower pressure setpoint, and [plus or 
    minus] 2% for the valve with the upper pressure setpoint, does not 
    affect any initiating event. The proposed change does not affect the 
    consequences of the previously evaluated design basis accidents as 
    the new safety valve setpoint tolerances are bounded by the 
    assumptions in the safety analysis. Therefore, the proposed change 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated.
        The proposed change to increase the ``as-found'' setpoint 
    tolerances does not involve any changes in equipment or the function 
    of these safety valves. The proposed change does not represent a 
    change in the configuration or operation of the plant. The test 
    method for the pressurizer safety valves will remain the same. The 
    increase in the setpoint tolerances does not create any new accident 
    initiator. Therefore, the proposed change does not create the 
    possibility of a new or different type of accident from any accident 
    previously evaluated. 
    
    [[Page 35061]]
    
        3. Would not involve a significant reduction in a margin of 
    safety.
        The pressure safety limit for the RCS protects the structural 
    integrity of the system from failure due to overpressurization. The 
    pressurizer safety valves are used to prevent the RCS pressure from 
    exceeding the safety limit. The proposed change to the pressurizer 
    safety valve setpoint tolerances will continue to prevent the RCS 
    pressure from exceeding the design safety limit during any design 
    basis event. Therefore, the proposed change does not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Ledyard B. Marsh.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert County, 
    Maryland
    
        Date of amendments request: June 6, 1995.
        Description of amendments request: The proposed amendments would 
    revise the Calvert Cliffs Nuclear Plant Units 1 and 2 Technical 
    Specifications, extending certain 18-month frequency surveillances to a 
    refueling interval (nominally 24 months, not to exceed 30 months). 
    Systems and equipment affected are the Reactor Protective System (RPS), 
    Engineered Safety Features Actuation System (ESFAS), Power-Operated 
    Relief Valve (PORV) actuation instruments, Low Temperature Overpressure 
    Protection (LTOP)-related instruments, Remote Shutdown Panel 
    instruments, Post-Accident Monitoring (PAM) instruments, Containment 
    Sump Level instruments, and Radiation Monitoring instruments.
        This amendment request would extend the nominal surveillance 
    interval requirement from 18 months to a refueling interval (nominally 
    24 months, not to exceed 30 months) for instrument channel 
    calibrations, RPS and ESFAS total bypass function operability 
    verification, RPS and ESFAS time response tests, ESFAS Manual Trip 
    Button channel functional tests, and ESFAS Automatic Actuation Logic 
    Channel Functional Tests. Calvert Cliffs has been operating on a 24-
    month fuel cycle since July 1987 (Unit 2) and July 1988 (Unit 1), 
    performing some Technical Specification surveillances, such as the ones 
    described here, during mid-cycle outages. The request is the last of a 
    series of proposed license amendments that would eliminate the need for 
    planned mid-cycle outages to perform required surveillances.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The proposed change would extend surveillance intervals for 
    Reactor Protective System (RPS), Engineered Safety Features 
    Actuation System (ESFAS), Power-Operated Relief Valve (PORV), Low 
    Temperature Overpressure Protection (LTOP), Remote Shutdown, Post-
    Accident Monitoring (PAM), Radiation Monitoring, and Containment 
    Sump Level Instruments.
        The purpose of the RPS is to effect a rapid reactor shutdown if 
    any one or a combination of conditions deviates from a pre-selected 
    operating range. The system functions to protect the core and the 
    Reactor Coolant System pressure boundary. The purpose of the ESFAS 
    is to actuate equipment which protects the public and plant 
    personnel from the accidental release of radioactive fission 
    products if an accident occurs, including a loss-of-coolant 
    incident, main steam line break, or loss of feedwater incident. The 
    safety features function to localize, control mitigate, and 
    terminate such incidents in order to minimize radiation exposure to 
    the general public. The Post-Accident Monitoring instruments provide 
    the Control Room operators with primary information necessary to 
    take manual actions, as necessary, in response to design basis 
    events, and to verify proper system response to plant conditions and 
    operator actions. The purpose of the Remote Shutdown System is to 
    provide plant parameter indications to operators on a Remote 
    Shutdown Panel to be used while placing and maintaining the plant in 
    a safe shutdown condition in the event the Control Room is 
    uninhabitable. The indications are used to verify proper system 
    response to plant conditions and operator actions. The LTOP System 
    protects against Reactor Coolant System overpressurization at low 
    temperatures by a combination of administrative controls and 
    hardware. The hardware includes two Power-Operated Relief Valves 
    with variable pressurizer pressure setpoints when operating in the 
    LTOP operating parameter region. The Containment Sump High Level 
    Alarm System provides an alarm in the Control Room for a containment 
    sump to provide one of the available indications of excessive RCS 
    leakage during normal plant operation. The Containment Area High 
    Range Radiation Monitoring System provides an indication of high 
    radiation levels in containment. The Containment Purge System 
    actuates equipment to prevent the release of radioactive material to 
    the environment in the event of a reactor coolant leak, a shielding 
    failure, or a fuel pin failure when the reactor vessel head is 
    removed.
        The instruments in each of the systems described above are 
    designed to be used in response to an accident. Failure of any of 
    these systems is not an initiator for any previously evaluated 
    accident. Therefore, the proposed change would not involve an 
    increase in the probability of an accident previously evaluated.
        Many of the instruments addressed in this license amendment 
    request will have or have recently had a new brand of sensor 
    installed. The effect of the increased surveillance interval with 
    the new sensors was analyzed. The new sensors do not effect the 
    physical design description of the plant, any design or functional 
    requirements, or surveillances. The proposed Technical Specification 
    change extending the surveillance interval from 18 months to a 
    refueling interval (nominally 24 months, not to exceed 30 months) 
    does not physically change the plant, change any design or 
    functional requirements, or effect the surveillances themselves. 
    Analysis has shown that no trip setpoints need to be changed, and 
    operator indications will continue to be accurate for control of 
    plant parameters to effect a safe shutdown. The equipment will 
    continue to perform as designed to mitigate the consequences of 
    accidents. Therefore, the proposed change would not involve a 
    significant increase in the consequences of an accident. [* * *]
        Therefore, the proposed change would not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated.
        The proposed change to increase the interval RPS, ESFAS, PORV, 
    LTOP, Remote Shutdown, PAM, Radiation Monitoring, and Containment 
    Sump Level instrument surveillances from 18 months to a refueling 
    interval (nominally 24 months, not to exceed 30 months) does not 
    involve a significant change in the design or operation of the 
    plant. No hardware is being added to the plant as part of the 
    proposed change. Some detector upgrades in specific plant systems to 
    enhance the performance of those systems have been or will be 
    performed. However, those upgrades were evaluated and deemed 
    acceptable under 10 CFR 50.59 and are not part of this request. The 
    Reactor Protective System, Engineered Safety Features Actuation 
    System, Power-Operated Relief Valve, Low Temperature Overpressure 
    Protection, Containment Sump Level, one Radiation Monitoring 
    actuation setpoints will not be changed. Analysis has shown that the 
    remote shutdown and PAM indications will continue to be accurate. 
    The proposed change will not introduce any new accident initiators. 
    Therefore, this change does not create the possibility of a new or 
    different type of accident from any previously evaluated.
        3. Does operation of the facility in accordance with the 
    proposed amendment 
    
    [[Page 35062]]
    involve a significant reduction in a margin of safety?
        The impact of the surveillance interval extension request was 
    evaluated for each Technical Specification-related safety function 
    for each of the RPS, ESFAS, PORV, LTOP, Remote Shutdown, PAM, 
    Radiation Monitoring, and Containment Sump Level instruments 
    addressed by this submittal. In all cases, parameters specified in 
    the related accident analysis were determined to be unaffected by 
    the surveillance interval extension, and no accident analyses limits 
    required changes. The Reactor Protective System, Engineered Safety 
    Features Actuation System, Power-Operated Relief Valve, Low 
    Temperature Overpressure Protection, Containment Sump Level, and 
    Radiation Monitoring actuation setpoints will not be changed. 
    Analysis has shown that the remote shutdown and PAM indications will 
    continue to be accurate. The methods for detection of degraded 
    instrument operation have not been changed, and remote shutdown and 
    PAM operator indications will continue to provide adequate accuracy. 
    The methods for detection of degraded instrument operation have not 
    been changed, and remote shutdown and PAM operator indications will 
    continue to provide adequate accuracy.
        The proposed change does not affect the operation of the systems 
    involved. The surveillance interval extension will not affect the 
    design of the systems, and methods for detection of degraded 
    instrument operation will continue to identify operation problems 
    between calibrations. Therefore, the proposed change does not 
    involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Ledyard B. Marsh.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert County, 
    Maryland
    
        Date of amendments request: June 9, 1995.
        Description of amendments request: The proposed amendments revise 
    the Calvert Cliffs Nuclear Power Plant Radiological Effluent Technical 
    Specifications (RETS) consistent with Generic Letter (GL), 
    ``Implementation of Programmatic Controls For Radiological Effluent 
    Technical Specifications in the Administrative Controls Section of the 
    Technical Specifications and the Relocation of Procedural Details of 
    RETS to the Offsite Dose Calculation Manual or the Process Control 
    Program (Generic Letter 89-01),'' dated January 31, 1989, and the 
    Improved Standard Technical Specifications for Combustion Engineering 
    Plants published in NUREG-1432, as modified by Mr. W. T. Russell's 
    letter of October 25, 1993, ``Content of Standard Technical 
    Specifications,'' to the Improved Technical Specification Owners Group 
    Chairpersons. Changes for relocating the procedural details of the 
    current RETS to the Offsite Dose Control Manual (ODCM) has been 
    prepared in accordance with the proposed changes to the Administrative 
    Controls section of the Technical Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The proposed change has been evaluated against the standards in 
    10 CFR 50.92 and has been determined to not involve a significant 
    hazards consideration, in that operation of the facility in 
    accordance with the proposed amendments:
        1. Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The proposed changes will provide human factor improvements for 
    the Technical Specifications by relocating existing procedural 
    details of the current Radiological Effluent Technical 
    Specifications to the Offsite Dose Control Manual (ODCM). Procedural 
    details for solid radioactive wastes will be relocated to the 
    Process Control Program. The proposed amendment (1) incorporates 
    programmatic controls in the Administrative Controls section of the 
    Technical Specifications that satisfy the requirements of 10 CFR 
    20.1302, 40 CFR Part 190, 10 CFR 50.36a, 10 CFR Part 50, Appendix I, 
    and our current Technical Specifications; (2) relocates the existing 
    procedural details in current specifications involving radioactive 
    effluent monitoring instrumentation, the control of liquid and 
    gaseous effluents, equipment requirements for liquid and gaseous 
    effluents, radiological environmental monitoring, and radiological 
    reporting details from the Technical Specifications to the ODCM; (3) 
    simplifies the associated reporting requirements; (4) simplifies the 
    administrative controls for changes to the ODCM; and (5) updates the 
    definitions of the ODCM consistent with these changes.
        Relocating existing requirements and eliminating requirements 
    which duplicate regulatory requirements provide Technical 
    Specifications which are easier to use. Because existing 
    requirements are relocated to established programs where changes to 
    those programs are controlled by regulatory requirements, there is 
    no reduction in commitment and adequate control is still maintained. 
    Likewise, the elimination of requirements which duplicate regulatory 
    requirements enhances the usability of the Technical Specifications 
    without reducing commitments. The additional improvements being 
    proposed neither add nor delete requirements, but merely clarify and 
    improve the readability and understanding of the Technical 
    Specifications. Since the requirements remain the same, these 
    changes only affect the method of presentation, and as such, would 
    not affect possible initiating events for accidents previously 
    evaluated or any system functional requirement.
        Furthermore, no safety-related equipment, safety function, or 
    plant operation will be altered as a result of this proposed change. 
    The changes are unrelated to the initiation and mitigation of 
    accidents and equipment malfunctions addressed in the Updated Final 
    Safety Analysis Report.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated.
        Transferring the procedural details of radiological effluent 
    monitoring and reporting from the Technical Specifications to the 
    ODCM has no impact on plant operation or safety. No safety-related 
    equipment, safety function, or plant operation will be altered as a 
    result of this proposed change. No changes to plant components or 
    structures are introduced which could create new accidents or 
    malfunctions not previously evaluated.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. Would not involve a significant reduction in a margin of 
    safety.
        The margin of safety associated with the affected Technical 
    Specifications is to provide assurance that the releases of 
    radioactive materials during actual or potential releases of liquid 
    or gaseous effluents do not exceed the limits of 10 CFR Part 20. 
    This license amendment request relocates the methodology and 
    parameters used to ensure that the 10 CFR Part 20 limits are 
    maintained, but does not change any of these requirements. Thus, no 
    methodology and parameters for controlling radioactive effluent 
    releases will be changed.
        The procedural details of the current Radiological Effluent 
    Technical Specifications will be transferred to the ODCM and 
    replaced with programmatic controls consistent with regulatory 
    requirements, including controls on revisions to the ODCM. Thus, no 
    requirements or controls will be reduced.
        The proposed revisions to the reporting requirements for 
    Radiological Effluent Release Report and the revision from the old 
    10 CFR 20.106 requirements to the new 10 CFR 20.1302 have no impact 
    on plant systems, plant operations or accident precursors. The 
    changes to the effluent 
    
    [[Page 35063]]
    reporting requirements and the updated reference to 10 CFR 20.1302 do 
    not change either the means of controlling radioactive releases or 
    the effluent release limits. Therefore, there will be no change in 
    the types and amounts of effluents that will be released, nor will 
    there be an increase in individual or cumulative radiation exposures 
    to any member of the public.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Ledyard B. Marsh.
    
    Carolina Power & Light Company, Docket No. 50-261, H.B. Robinson Steam 
    Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of amendment request: June 3, 1995.
        Description of amendment request: The requested Technical 
    Specification (TS) change clarifies the definition of operability of 
    the charging pumps by adding a footnote to TS Section 3.2.2.a that 
    states that the connectibility of the emergency power sources is not 
    required for charging pump operability.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        This change request does not involve a significant hazards 
    consideration for the following reasons.
        1. The requested change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The requested change clarifies that the emergency power 
    sources are not required for the operability of the charging pumps. 
    Operation of the charging pumps is not considered in the assumptions 
    for initiation of any analyzed accident and is not credited for 
    accident mitigation in any analyzed accidents in the safety analysis 
    report. Therefore, the availability of emergency power sources to 
    the charging pumps does not affect the probability of occurrence or 
    consequences of an analyzed accident in the safety analysis report.
        2. The requested change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. The requested change clarifies that the emergency power 
    sources are not required for the operability of the charging pumps. 
    The design requirements of the charging pumps to provide reactor 
    coolant inventory and boron inventory control are not changed. The 
    operability of the emergency power source to the charging pumps is 
    not a precursor to any accident scenario. Failure of the charging 
    pumps is bounded by the plant design which strips the charging pumps 
    from the emergency buses under certain conditions. Since the change 
    does not involve changes in the operation of the plant, or physical 
    or equipment changes or involve controls for accident mitigation 
    equipment, the requested change will not create the possibility of 
    new or different kind of accident from any accident previously 
    evaluated.
        3. The requested change clarifies that the emergency power 
    sources are not required for the operability of the charging pumps. 
    Since the charging pumps are stripped from the emergency buses in 
    the event of a loss of power and safety injection, emergency power 
    sources to the charging pumps are not guaranteed to mitigate the 
    consequences of an analyzed accident. As a result, no credit is 
    taken for the charging function in analyzed accidents and the margin 
    of safety as described in the safety analysis report is unchanged. 
    Therefore, the requested change does not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550.
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, North Carolina 27602.
        NRC Project Director: David B. Matthews.
    
    Commonwealth Edison Company, Docket Nos. 50-454 and 50-455, Byron 
    Station, Unit Nos. 1 and 2, Ogle County, Illinois
    
    Docket Nos. 50-456 and 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of amendment request: February 21, 1995.
        Description of amendment request: The proposed amendments would 
    revise Byron and Braidwood technical specifications associated with the 
    reactor coolant system (RCS) resistance temperature detectors (RTDs) 
    used to obtain hot and cold leg temperatures. The amendments are 
    required because of proposed modification that will remove the existing 
    RTDs and their associated piping and valves and replace them with dual 
    element fast response RTDs mounted in the thermowells welded directly 
    in the RCS loop piping.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed modification replaces the existing bypass piping 
    system with thermowell-mounted RTDs. Because the hot leg RTDs are 
    mounted directly in the scoops, temperature measurement inaccuracies 
    caused by imbalances in the flow scoop sample flow are eliminated. 
    The method of measuring coolant temperature with thermowell-mounted 
    fast response RTDs has been analyzed to be at least as effective as 
    the RTD bypass system. With the thermowells welded into the existing 
    RCS hot and cold leg nozzles and the elimination of the bypass 
    piping, the number of pressure boundary welds has been significantly 
    reduced, resulting in a reduced probability of a small break LOCA 
    [Loss of Coolant Accident].
        The RTD response time is incorporated in the safety analyses. In 
    particular, RTD response time is modeled in the OT[DELTA]T [Over 
    Temperature Delta Temperature] and OP[DELTA]T [Over Pressure Delta 
    Temperature] trip functions. The overall response time modeled in 
    the safety analyses for the existing RTD bypass piping system is 8 
    seconds. The overall response time is the elapsed time from the time 
    the temperature change in the RCS exceeds the trip setpoint until 
    the rods are free to fall. More specifically, 6 seconds is modeled 
    as a first order lag term and 2 seconds as pure delay on the reactor 
    trip signal. The 6 second lag term includes such factors as: RTD 
    bypass piping fluid transport delay, RTD bypass piping thermal lag, 
    RTD response time, and RTD electronic filtering. The 2 second delay 
    on reactor trip addresses such factors as electronics delay, trip 
    breakers and gripper release.
        Signal conditioning (filtering) of the individual loop [DELTA]T 
    and Tavg signals is represented by [time constants utilized in 
    the lag compensator for DELTA T] and [time constant utilized in the 
    measured Tavg lag compensator], respectively, in the OT[DELTA]T 
    and OP[DELTA]T equations in Technical Specification Table 2.2-1. 
    With the current bypass manifold system, the filter is not required 
    since the existing RTDs do not respond rapidly to local temperature 
    variances within the reactor coolant loop. The bypass piping and 
    manifold provide adequate mixing of the coolant, eliminating any 
    local temperature variances. Therefore, the values of [time 
    constants utilized in the lag compensator for DELTA T] and [time 
    
    [[Page 35064]]
    constant utilized in the measured Tavg lag compensator] are 
    currently specified as 0 seconds, effectively turning off the 
    electronic filter. The new fast response RTDs may respond to 
    temperature spikes which are not representative of actual RCS bulk 
    fluid temperature. Signal conditioning may be required to eliminate 
    these temperature spikes. Although, the current Technical 
    Specifications do not provide for any signal conditioning, the 8 
    second total response time used in safety analyses has sufficient 
    margin to account for a typical 2 second time constant for signal 
    conditioning. Industry experience has shown that a 2 second filter 
    is adequate in eliminating the spikes.
        The proposed fast response RTD/thermowell system also has an 
    overall response time of 8 seconds. However, the time distribution 
    for the parameters differ between the existing and proposed designs. 
    The existing design includes a transport time for RCS fluid to reach 
    the RTD, located in the manifold. The RTDs are directly immersed 
    into the coolant, providing a fast response. The new design no 
    longer has the transport delay. However, because the RTDs are 
    mounted in thermowells, the response time of the RTD/thermowell 
    combination will be increased over the existing system.
        The effects of a redistribution of the time responses between 
    the total lag term (pipe transport delay, RTD response and 
    electronic filter delay) and electronics delay term have been 
    evaluated. Westinghouse completed a Safety Evaluation SECL-95-015, 
    ``OT[DELTA]T and OP[DELTA]T Reactor Trip Response Time Safety 
    Evaluation'' to support the revision to the time requirements. The 
    evaluation concludes that, as long as the total response time 
    remains [less than or equal to] 8 seconds, the safety analyses 
    acceptance criteria continue to be met. The OT[DELTA]T and 
    OP[DELTA]T trip functions are unaffected by the change.
        The following Updated Final Safety Analysis Report (UFSAR) 
    Chapter 15 events trip on OT[DELTA]T: Loss of Electric Load/Turbine 
    Trip, Uncontrolled RCCA Bank Withdrawal at Power, CVCS Malfunction 
    that Results in a Decrease in the Boron Concentration in the Reactor 
    Coolant, and Inadvertent Opening of a Pressurizer Safety or Relief 
    Valve. In addition, the following events trip on OP[DELTA]T: 
    Steamline Break at Hot Full Power for Core Response, and Steamline 
    Break Superheat Analysis. These events have been reviewed for a 
    change in the distribution of time responses for OT[DELTA]T and 
    OP[DELTA]T. The review concludes that the time response 
    redistribution did not result in a minimum DNBR lower than the 
    safety analyses limit, did not result in a fuel centerline melt, nor 
    did the superheated steam releases change from those currently 
    existing. Therefore, the radiological consequences for these events 
    do not increase as a result of the less restrictive time response 
    breakdown. Thus, the proposed amendment does not result in an 
    increase in the probability or consequences of a previously 
    evaluated accident.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The OT[DELTA]T and OP[DELTA]T trip functions are unaffected by 
    the change. Electronic filtering of the RTD signal has been 
    included, changing the dynamic compensation term of OT[DELTA]T and 
    OP[DELTA]T setpoint equations. No other changes to the setpoint 
    equation result from the proposed modification.
        The added 7300 hardware is compatible with the existing 7300 
    electronic hardware now used. All changes to the 7300 protection 
    cabinets have been qualified. The proposed system is functionally 
    equivalent to the existing one. The proposed modification has been 
    reviewed for conformance with the Institute of Electrical and 
    Electronics Engineers (IEEE) 279-1971 criteria, associated General 
    Design Criteria, Regulatory Guides, and other applicable industry 
    standards. The single failure criterion is satisfied by the proposed 
    modification, since the independence of redundant protection sets is 
    maintained. The new RTD/thermowell system meets the equipment 
    seismic and environmental qualification requirements of IEEE 
    standards 344-1975 and 323-1974, respectively. The proposed changes 
    do not affect the protection system capabilities to initiate a 
    reactor trip. The 2 of 4 voting coincidence logic of the protection 
    sets is maintained. Therefore, the proposed modification meets all 
    appropriate IEEE criteria, industry standards and other guidelines.
        In addition, the RTD outputs are used for rod control, turbine 
    runback, pressurizer level and other control systems. These control 
    systems receive the signal after it has been processed at the 7300 
    cabinets and are therefore unaffected by the proposed modification.
        The design and installation of the thermowells is in accordance 
    with the American Society of Mechanical Engineers (ASME) Code 
    requirements. However, should a thermowell fail at the RCS pressure 
    boundary, the resulting accident is enveloped by current design 
    basis accident analyses. Thus, implementation of the proposed 
    amendment does not create the possibility of a new or different kind 
    of accident from any of those previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The 7300 protection cabinets calculate individual loop [DELTA]T 
    and Tavg, based on the output of the RTDs. These values are 
    used in the OT[DELTA]T and OP[DELTA]T reactor protection trip 
    signals. Electronic filtering of the RTD signal will be included, 
    changing the dynamic compensation term of OT[DELTA]T and OP[DELTA]T 
    setpoint equations. No other changes to the setpoint equation result 
    from the proposed modification. Although the total response time 
    used as input into the safety analyses is unaffected by the proposed 
    modification, the distribution of response times between the total 
    lag (pipe transport delay, RTD response and electronic filter delay) 
    and the electronic delay has changed. The UFSAR events which rely on 
    OT[DELTA]T and OP[DELTA]T trips have been evaluated. The evaluation 
    concludes that the safety analyses acceptance criteria continue to 
    be met, since the total response time is consistent with the safety 
    analyses. The OT[DELTA]T and OP[DELTA]T trips function in the same 
    manner to terminate DNB-related transients. The reliability of the 
    reactor protection system is unaffected by this change. Thus, the 
    proposed modification does not involve a significant reduction in 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois
    
    Docket Nos. STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 
    and 2, Will County, Illinois
    
        Date of amendment request: May 17, 1995.
        Description of amendment request: The proposed amendment would 
    modify the technical specifications to allow steam generator tubes to 
    be repaired using the tungsten inert gas (TIG) welded sleeve process 
    developed by ABB Combustion Engineering (ABB/CE), remove the ability to 
    repair steam generator tubes using the Babcock & Wilcox Nuclear 
    Technologies (BWNT) kinetically welded sleeve process, and increase the 
    requirement to inspect the number of sleeved tubes from 3 percent of 
    the total number of sleeved tubes in all four steam generators (SGs) or 
    all sleeved tubes in one steam generator to 20 percent of each sleeve 
    design installed. The proposed amendments would also delete the 
    requirement to conduct additional corrosion testing to establish the 
    design life for the BWNT kinetically welded sleeve in the presence of a 
    crevice.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or 
    
    [[Page 35065]]
    consequences of an accident previously evaluated.
        The proposed amendment allows the ABB/CE TIG welded tubesheet 
    sleeves and tube support plate sleeves to be used as an alternate 
    tube repair method for Byron and Braidwood Units 1 and 2 Steam 
    Generators (SGs). The sleeve configuration was designed and analyzed 
    in accordance with the criteria of Regulatory Guide (RG) 1.121 and 
    Section III of the ASME Code. Fatigue and stress analyses of the 
    sleeved tube assemblies produce acceptable results for both types of 
    sleeves as documented in ABB/CE Licensing Report CEN-621-P, Revision 
    00, ``Commonwealth Edison Byron and Braidwood Unit 1 & 2 Steam 
    Generator Tube Repair Using Leak Tight Sleeves, FINAL REPORT,'' 
    April 1995. Mechanical testing has shown that the structural 
    strength of the sleeves under normal, faulted, and upset conditions 
    is within the acceptable limits specified in RG 1.121. Leakage rate 
    testing for the tube sleeves has demonstrated that primary to 
    secondary leakage is not expected during any plant condition. The 
    consequences of leakage through the sleeved region of the tube is 
    fully bounded by the existing steam generator tube rupture (SGTR) 
    analysis included in the Byron and Braidwood Updated Final Safety 
    Analysis Report (UFSAR).
        The current Technical Specification 3.4.6.2.c primary to 
    secondary leakage limit of 150 gallons per day (gpd) through any one 
    SG ensures that SG tube integrity is maintained in the event of main 
    steam line break (MSLB) or loss of coolant accident (LOCA). The RG 
    1.121 criteria for establishing operational leakage rate limits 
    require a plant shutdown based upon a leak-before-break 
    consideration to detect a free span crack before a potential tube 
    rupture. The 150 gpd limit will continue to allow for early leakage 
    detection and require a plant shutdown in the event of the 
    occurrence of an unexpected crack resulting in leakage that exceeds 
    the TS limit.
        The sleeves are designed to allow inservice inspection of the 
    pressure retaining portions of the sleeve and parent tube. Inservice 
    inspection is performed on all sleeves following installation to 
    ensure that each sleeve has been properly installed and is 
    structurally sound. Periodic inspections are performed in subsequent 
    refuel outages to monitor sleeve degradation on a sample basis. The 
    eddy current technique used for inspection will be capable of 
    detecting both axial and circumferential flaws. A 20% sample of the 
    sleeves are inspected each refuel outage. In the event that an 
    imperfection exceeding the repair limit is detected an additional 
    20% sample will be inspected. The inspection scope is expanded to 
    100% of the sleeves should a repairable defect be found in the 
    second sample. Tubes that contain defects in a sleeve, which exceed 
    the repair limit, will be removed from service. This ensures that 
    sleeve and tube structural integrity is maintained.
        The proposed TS change to support the installation of TIG welded 
    sleeves does not adversely impact any previously evaluated design 
    basis accident. The effect of sleeve installation on the performance 
    of the SG was analyzed for heat transfer, flow restriction, and 
    steam generation capacity. The sleeves reduce the risk of primary to 
    secondary leakage in the SG. The installation of ABB/CE sleeve 
    results in a hydraulic flow restriction that is dependent on the 
    number and types of sleeves installed. The reduction in primary 
    system flow rate is a small percentage of the flow rate reduction 
    seen from plugging one tube and is a preferable alternative when 
    considering core margins based on minimum reactor coolant system 
    flow rates. The sleeving installation will result in a resistance to 
    primary coolant flow through the tube for other evaluated accidents. 
    The results of the analyses and testing, as well as industry 
    operating experience, demonstrate that the sleeve assembly is an 
    acceptable means of maintaining tube integrity. In summary, 
    installation of sleeves does not substantially affect the primary 
    system flow rate or the heat transfer capability of the steam 
    generators.
        The sleeve sample size has been increased from 3% of the sleeved 
    tubes in all four steam generators to include an eddy current 
    inspection of a minimum of 20% of each sleeve design installed. 
    Increasing the sample size of the sleeves to be inspected will 
    increase the monitoring of tubes using sleeves for any further 
    degradation while they remain in service. If the sample identifies a 
    sleeve with an imperfection of greater than the repair limit, an 
    additional 20% of the sleeves shall be inspected. The sleeves that 
    have identified imperfections of greater than the repair limit shall 
    be removed from service. Increasing the monitoring of the sleeves 
    will assist in the early detection of a tube or sleeve imperfection 
    and limit the probability of occurrence of an accident previously 
    evaluated in the UFSAR.
        Installation of the sleeves can be used to repair degraded tubes 
    by returning the condition of the tubes to their original design 
    basis condition for tube integrity and leak tightness during all 
    plant conditions. The tube bundle overall structural and leakage 
    integrity will be increased with the installation of the sleeves 
    reducing the risk of primary to secondary leakage in the SG while 
    maintaining acceptable reactor coolant system flow rates. Therefore 
    sleeving will not increase the probability of occurrence of an 
    accident previously evaluated.
        Removal of the BWNT kinetically welded sleeve process as an 
    approved SG tube repair methodology and not completing the 
    additional corrosion testing necessary to establish the design life 
    for the BWNT kinetically welded sleeve in the presence of a crevice 
    will have no affect on plant operations. There are currently no BWNT 
    kinetically welded sleeves installed in the Byron or Braidwood SGs. 
    Had there been, plant operations would have still been bounded by 
    the existing SGTR analysis in the Byron and Braidwood UFSAR.
        Therefore, these proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The implementation of the proposed sleeving process will not 
    introduce significant or adverse changes to the plant design basis. 
    Stress and fatigue analyses of the repair has shown the ASME Code 
    and RG 1.121 allowable values are met. Implementation of TIG welded 
    sleeving maintains overall tube bundle structural and leakage 
    integrity at a level consistent with that of the originally supplied 
    tubing. Leak and mechanical testing of the sleeves support the 
    conclusions that the sleeve retains both structural and leakage 
    integrity during all conditions. Repair of a tube with a sleeve does 
    not provide a mechanism that result in an accident outside of the 
    area affected by the sleeve.
        Any hypothetical accident as a result of potential tube or 
    sleeve degradation in the repaired portion of the tube is bounded by 
    the existing SGTR analysis. The SGTR analysis accounts for the 
    installation of sleeves and the impact on current plugging level 
    analyses. The sleeve design does not affect any other component or 
    location of the tube outside of the immediate area repaired.
        The current Technical Specification 3.4.6.2.c primary to 
    secondary leakage limit of 150 gpd through any one SG ensures that 
    SG tube integrity is maintained in the event of an MSLB or LOCA. The 
    limit will provide for leakage detection and a plant shutdown in the 
    event of the occurrence of an unexpected single crack resulting in 
    excessive tube leakage. The leakage limit also provides for early 
    detection and a plant shutdown prior to a postulated crack reaching 
    critical crack lengths for MSLB conditions.
        Inservice inspections are performed following sleeve 
    installation to ensure proper weld fusion has occurred to maintain 
    structural integrity. The post installation inspection also serves 
    as baseline data to be used for comparison during future 
    inspections. Periodic eddy current inspections monitor the pressure 
    retaining portions of the sleeve and parent tube for degradation. 
    Eddy current techniques will be employed that are sensitive to axial 
    and circumferential degradation.
        Increasing the sample size of tubes repaired using either 
    sleeving process during each scheduled inservice inspection will 
    increase the monitoring of these tubes for any further degradation. 
    The improved monitoring and evaluation of the tube and the sleeves 
    assures tube structural integrity is maintained or the tube is 
    removed for service.
        Corrosion testing of typical sleeve-tube configurations was 
    performed to evaluate local stresses, sleeve life, and resistance to 
    primary and secondary side corrosion. The tests were performed on 
    stress relieved and as-welded (non-stress relieved) sleeve-tube 
    joints. Using the corrosion test data in conjunction with finite 
    element analyses of the local stress, the stress relieved joint life 
    was determined to be in excess of 40 years. The ABB/CE TIG welded 
    sleeve operating experience in the industry has shown no sleeve 
    failures due to service induced degradation in sleeves that were 
    installed with acceptable inspection results. This experience 
    includes the stress relieved and 
    
    [[Page 35066]]
    as-welded sleeve configurations. ComEd will stress relieve all sleeves 
    at Byron and Braidwood as specified in the Technical Report.
        Removal of the BWNT kinetically welded sleeve process as an 
    approved SG tube repair methodology and not completing the 
    additional corrosion testing necessary to establish the design life 
    for the BWNT kinetically welded sleeve in the presence of a crevice 
    will not create the possibility of a new or different type of 
    accident from any accident previously evaluated. Repair of an SG 
    tube with a BWNT kinetically welded sleeve would not have provided a 
    mechanism that resulted in an accident outside of the area affected 
    by the sleeve. Any hypothetical accident as a result of potential 
    tube or sleeve degradation in the repaired portion of the tube would 
    have been bounded by the existing SGTR analysis. The SGTR analysis 
    accounts for the installation of sleeves and the impact on current 
    plugging level analyses. The sleeve design does not affect any other 
    component or location of the tube outside of the immediate area 
    repaired. Furthermore, there are currently no BWNT kinetically 
    welded sleeves installed in the Byron or Braidwood SGs.
        Therefore, the proposed changes do not create the possibility of 
    a new or different type of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The TIG welded sleeving repair of degraded steam generator tubes 
    has been shown by analysis to restore the integrity of the tube 
    bundle to its original design basis condition. The safety factors 
    used in the design of the sleeves for the repair of degraded tubes 
    are consistent with the safety factors in the ASME Boiler and 
    Pressure Vessel Code used in steam generator design. The design of 
    the ABB/CE SG sleeves has been verified by testing to preclude 
    leakage during normal and postulated accident conditions.
        The portions of the installed sleeve assembly which represents 
    the reactor coolant pressure boundary can be monitored for the 
    initiation and progression of sleeve/tube wall degradation, thus 
    satisfying the requirement of RG 1.83. The portion of the SG tube 
    bridged by the sleeve joints is effectively removed from the 
    pressure boundary, and the sleeve then forms the new pressure 
    boundary. The sleeve enhances the safety of the plant by 
    reestablishing the protective boundaries of the steam generator. 
    Keeping the tube in service with the use of a sleeve instead of 
    plugging the tube and removing it from service increases the heat 
    transfer efficiency of the steam generator. During each scheduled 
    inservice inspection, each sleeve inspected and found to have 
    unacceptable degradation shall be removed from service. The effect 
    on the design transients and the accident analyses have been 
    reviewed based on the installation of sleeves equal to the tube 
    plugging level coincident with the minimum reactor coolant flow 
    rate. Evaluation of the installation of sleeves was based on the 
    determination that LOCA evaluations for the licensed minimum reactor 
    coolant flow bound the combined effect of tube plugging and sleeving 
    up to an equivalent of the actual plugging limit. Sleeving results 
    in a fractional amount of the plugging limitation of one tube and is 
    a preferable alternative when considering core margins based on 
    minimum reactor coolant system flow rates. The sleeving installation 
    will result in a resistance to primary coolant flow through the 
    tube. The primary coolant flow through the ruptured tube is reduced 
    by the influence of the installed sleeve, thereby reducing the 
    consequences to the public due to a SGTR event.
        A SG sleeve removes an indication of a possible leak source from 
    the reactor coolant system (RCS) pressure boundary, eliminating the 
    potential of a primary-to-secondary leak. The structural integrity 
    of the tube is maintained by the sleeve and sleeve-to-tube joint.
        Installation of either tube sheet or tube support plate sleeves 
    will increase the protective boundaries of the steam generators and 
    will not reduce the margin of safety.
        Removal of the BWNT kinetically welded sleeve process as an 
    approved SG tube repair methodology and not completing the 
    additional corrosion testing necessary to establish the design life 
    for the BWNT kinetically welded sleeve in the presence of a crevice 
    will not result in a reduction in the margin of safety. There are 
    currently no BWNT kinetically welded sleeves installed in the Byron 
    or Braidwood SGs. SG tube integrity will be maintained by applying 
    an alternate NRC approved repair methodology or removing the SG tube 
    from service by plugging.
        Therefore, the proposed changes do not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of amendment request: April 11, 1995.
        Description of amendment request: The proposed amendments would 
    allow a one-time extension of specific LaSalle, Units 1 and 2, 18 month 
    Technical Specification Surveillance Requirements to allow surveillance 
    testing to coincide with the LaSalle, Unit 1, seventh refueling outage 
    (L1R07). The shutdown for L1R07 has been rescheduled from September 
    1995 until early 1996. The proposed extensions apply to: Calibrations 
    and functional testing of isolation actuation instrumentation, 
    emergency core cooling system actuation instrumentation, and 
    recirculation pump trip actuation instrumentation; leakage testing of 
    reactor coolant system isolation valves; inspection of fire rated 
    seals; functional testing of mechanical snubbers; inspections of 
    emergency diesel generators; and testing of batteries, battery 
    chargers, and other electrical components.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because:
        The proposed change is temporary and allows a one-time extension 
    of specific surveillance requirements for Unit 1 Cycle 7 to allow 
    surveillance testing to coincide with the seventh refueling outage. 
    The proposed surveillance interval extension is short and will not 
    cause a significant reduction in system reliability nor affect the 
    ability of the systems to perform their design function. Current 
    monitoring of plant conditions and continuation of the surveillance 
    testing required during normal plant operation will continue to be 
    performed to ensure conformance with Technical Specification 
    operability requirements. Therefore, this change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        (2) Create the possibility of a new or different kind of 
    accident from any accident previously evaluated because:
        Extending the surveillance interval for the performance of 
    specific testing will not create the possibility of any new or 
    different kind of accidents. No changes are required to any system 
    configurations, plant equipment, or analyses. Therefore, this change 
    will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        (3) Involve a significant reduction in the margin of safety 
    because:
        Surveillance interval extensions will not impact any plant 
    safety analyses since the assumptions used will remain unchanged. 
    The safety limits assumed in the accident analyses and the design 
    function of the equipment required to mitigate the consequences of 
    any postulated accidents will not be changed since only the 
    surveillance test interval is being extended. Historical performance 
    generally indicates a high degree of reliability, and surveillance 
    
    [[Page 35067]]
    testing performed during normal plant operation will continue to be 
    performed to verify continued Operability of affected systems, 
    structures and components. Therefore, the plant will be maintained 
    within the analyzed limits, and the proposed extension will not 
    significantly reduce the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of amendment request: May 19, 1995.
        Description of amendment request: The proposed amendments would 
    revise the technical specification requirement to verify each fire 
    protection valve is in the correct position at least once per 31 days. 
    The proposed change will retain a monthly visual inspection of the fire 
    protection valves that are accessible during plant operation. However, 
    the interval for visual surveillance of those valves considered not 
    accessible during plant operation will be changed to at least once per 
    18 months.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because: The 
    proposed change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated in 
    the UFSAR [Updated Final Safety Analysis Report]. The proposed 
    change only changes the testing frequency for valves that are 
    inaccessible during power operation. A check of the LaSalle LER 
    database for the entire operating lifetime of LaSalle Units 1 and 2 
    was performed, and there has not been any instances in which any 
    Technical Specification related Fire Protection valves have been 
    found out of position. Therefore, the change to the frequency of 
    testing will have no affect on the capability of fire suppression 
    water systems, since all Technical Specification fire protection 
    valves, both accessible and inaccessible at power operation, have a 
    plant history of 100% correct valve lineup during monthly 
    surveillances. Additionally, all fire protection valves that are in 
    the fire suppression water flow path are either locked or seal wired 
    in the required position at all times. The change does not impact 
    the probability of any fire or other accident occurrence. Therefore, 
    the proposed change does not cause an increase in the probability or 
    consequences of an accident previously evaluated.
        (2) Create the possibility of a new or different kind of 
    accident from any accident previously evaluated because:
        The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    in the UFSAR. The proposed change only changes the testing frequency 
    for valves that are inaccessible during power operation. The change 
    to the frequency of testing will have no effect on the capability of 
    fire suppression water systems, since the valves, both accessible 
    and inaccessible at power operation, have a plant lifetime history 
    of 100% correct valve lineup during monthly surveillances. 
    Additionally, these valves are locked or sealed in the required 
    position at all times. The change does not alter the performance of 
    the fire suppression water system, and therefore introduces no new 
    failure modes. With no alteration or degradation to equipment or 
    system operation, the change introduces no new accident or 
    malfunction.
        (3) Involve a significant reduction in the margin of safety 
    because:
        The proposed change does not reduce the margin as defined in the 
    bases for any Technical Specification. The proposed change only 
    changes the testing frequency for all Technical Specification fire 
    protection valves that are inaccessible during power operation. The 
    plant history of 100% correct valve lineup for the Technical 
    Specification fire protection valves, combined with the fact that 
    these valves are always locked or sealed in the required position 
    ensures that the bases' minimum OPERABILITY requirements of the fire 
    suppression systems are met.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station, Units 1 and 2, Lake County, Illinois
    
        Date of amendment request: May 31, 1995.
        Description of amendment request: The proposed amendments would 
    revise the Technical Specifications and incorporate new acceptance 
    criteria for steam generator tubes with degradation in the tubesheet 
    roll expansion region.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed changes do not involve a significant increase in 
    the probability of occurrence or consequences of an accident 
    previously evaluated.
        Application of the F* criteria to degraded steam generator tubes 
    will not affect any of the initiators or precursors of any accident 
    previously evaluated. Application of the proposed change will not 
    increase the likelihood that a transient initiating event will occur 
    because transients are initiated by equipment malfunction and/or 
    catastrophic system failure. The proposed change will allow a new 
    criteria to be applied to disposition steam generator tubes that are 
    degraded in the tubesheet roll transition region. The F* criteria 
    specify a minimum length of tubing which must be free from any 
    indication of degradation. Below the F* length, any type or size of 
    indication, including complete circumferential through wall 
    cracking, will not impact the structural integrity of the tube with 
    respect to pull out forces during normal operation or accident 
    conditions, and does not significantly affect the leakage behavior 
    of the tube. While the Zion UFSAR does not specifically address the 
    Feedwater Line Break (FLB) accident, the FLB event was used as the 
    limiting event in the evaluation of the F* criteria. The FLB 
    pressure differential of 2650 psi maximizes the axial loading on the 
    tube for pull out considerations and is bounding. In addition, the 
    close proximity of the tubesheet to the tube will prevent tube 
    rupture or collapse of the tube in the tubesheet span. Because 
    application of the F* criteria will ensure that degraded tubes will 
    provide the same structural integrity as an original undegraded tube 
    during normal operation and accident and accident conditions, the 
    probability of occurrence of an accident previously evaluated is not 
    significantly increased.
        Application of the F* criteria will not significantly increase 
    the consequences of any accident previously evaluated. The F* 
    criteria ensure that sufficient length of undegraded tube exists to 
    maintain structural integrity and preclude significant leakage. Due 
    to the proximity of the tubesheet to the tube, any leakage from 
    degradations below the F* length would be negligible and would be 
    well below the Technical Specification limits established for steam 
    generator 
    
    [[Page 35068]]
    leakage. Tube rupture as a result of indications below the F* distance 
    is precluded because the tubesheet prevents outward expansion of the 
    tube in response to internal pressure.
        The relationship between the tubesheet region leak rate at the 
    most limiting postulated accident conditions relative to that for 
    normal plant operating conditions has been assessed. For the 
    postulated leak source within the roll expansion, increasing the 
    differential pressure on the tube on the tube wall increases the 
    driving head for the leak; however, it also increases the tube to 
    tubesheet loading.
        For a leak source below the F* Distance, the maximum assumed 
    pressure differential results in an insignificant leak rate relative 
    to that which could be associated with normal plant operation. This 
    is a result of the increased tube to tubesheet loading associated 
    with the increased differential pressure. Thus for a circumferential 
    indication within the roll expansion that is left in service in 
    accordance with F* criteria, any leakage under accident conditions 
    would be less than that experienced under normal operating 
    conditions. Therefore, any leakage under accident conditions would 
    be less than the existing Technical Specification leakage limit, 
    which is consistent with accident analysis assumptions. Steam 
    generator tube integrity must be maintained under the postulated 
    loss of coolant accident condition of secondary-to-primary 
    differential pressure. Based on tube collapse strength 
    characteristics, the constraint provided to the tube by the 
    tubesheet gives a margin between the tube collapse strength and the 
    limiting secondary-to-primary differential pressure condition, even 
    in the presence of circumferential or axial indications. The maximum 
    secondary to primary differential pressure during a postulated LOCA 
    is 1005 psi. This value is significantly below the residual preload 
    between the tubes and the tube sheet. Therefore, no significant 
    secondary to primary leakage would be expected to occur.
        In addition, the proposed changes will not affect the ability to 
    safely shut down the operating unit and mitigate the consequences of 
    an accident because the proposed changes will not necessitate 
    changes to the emergency procedures governing accident conditions or 
    plant recovery.
        Administrative and typographical changes are proposed to correct 
    previous grammatical errors, to eliminate a parenthetical note that 
    could cause confusion when applying the proposed requirements, and 
    to make the terminology used in the Bases section consistent with 
    the definitions provided in Specification 4.3.1. Those proposed 
    changes will not increase the probability of occurrence or 
    consequence of any accident previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes to the Technical Specifications do not 
    involve the addition of any new or different types of safety related 
    equipment nor do they involve the operation of any equipment 
    required for safe operation of the facility in a manner different 
    from those addressed in the UFSAR. No safety related equipment or 
    function will be altered as a result of the proposed changes. Also, 
    the procedures governing normal plant operation and recovery from an 
    accident are not changed by the application of the F* criteria. The 
    F* criteria will allow the use of an alternate method to plugging or 
    sleeving to repair steam generator tubes with degradation in the 
    tubesheet region. The F* criteria ensure that both the structural 
    integrity and leak tight nature of the steam generator tube will be 
    equivalent to the original tube. Since no new failure modes or 
    mechanisms are introduced by the proposed changes, no new or 
    different type of accident is created.
        Administrative and typographical changes are proposed to correct 
    previous grammatical errors, to eliminate a parenthetical note that 
    could cause confusion when applying the proposed requirements, and 
    to make the terminology used in the Bases section consistent with 
    the definitions provided in Specification 4.3.1. Those proposed 
    changes will not create the possibility of a new or different kind 
    of accident from those previously evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        Plant safety margins are established through Limiting Conditions 
    for Operation (LCOs), limiting safety system settings, and safety 
    limits specified in Technical Specifications. There will be no 
    changes to the LCOs, limiting safety system settings, or the safety 
    limits as a result of the proposed changes. Application of the F* 
    criteria will allow degraded steam generator tubes to be repaired by 
    an alternative method to plugging or sleeving. Steam generator tube 
    plugging decreases the total primary reactor coolant flow rate and 
    heat transfer capability of the steam generator. While steam 
    generator tube sleeving only slightly reduces the reactor coolant 
    flow rate, large numbers of sleeves can have a measurable effect on 
    flow rate and can complicate steam generator tube inspection 
    activities.
        Application of the F* criteria will allow a repair method that 
    will restore the integrity of degraded steam generator tubes and 
    will not adversely affect primary system flow rate or heat transfer 
    capability. Application of the F* criteria will preserve the heat 
    transfer capability of the steam generators and will maintain the 
    design margins assumed in the analyses contained in the UFSAR. The 
    alternate repair method will also be less complicated, faster, and 
    will reduce personnel occupational exposure significantly. Based on 
    the above discussion it is concluded that the proposed changes will 
    not significantly reduce a margin of safety.
        Administrative and typographical changes are proposed to correct 
    previous grammatical errors, to eliminate a parenthetical note that 
    could cause confusion when applying the proposed requirements, and 
    to make the terminology used in the Bases section consistent with 
    the definitions provided in Specification 4.3.1. Those proposed 
    changes will not impact any margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Robert A. Capra.
    
    Entergy Operations, Inc., Docket Nos. 50-313 and 50-368, Arkansas 
    Nuclear One, Unit Nos. 1 and 2 (ANO-1&2), Pope County, Arkansas
    
        Date of amendment request: April 4, 1995.
        Description of amendment request: The proposed amendments revise 
    requirements associated with the ventilation system that services both 
    the Unit 1 and Unit 2 control rooms.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    Criterion 1--Does Not Involve a Significant Increase in the Probability 
    or Consequences of an Accident Previously Evaluated.
    
        The control room emergency ventilation and air conditioning 
    systems are not initiators of an accident previously evaluated. 
    Extension of the allowable outage time for one inoperable control 
    room emergency air conditioning system from 7 days to 30 days is 
    acceptable based on the low probability of an event occurring that 
    would require control room isolation and a concurrent or subsequent 
    failure of the remaining operable control room emergency air 
    conditioning system. An evaluation using probabilistic safety 
    assessment techniques has shown the frequency of this event to be at 
    an acceptably low level (4.67E-6/yr). The ANO-1 surveillance 
    requirements for the control room emergency ventilation and air 
    conditioning system has been updated for consistency with the ANO-2 
    requirements and are consistent with RG 1.52, March 1978, Revision 
    2. The relaxation in the ANO-2 Mode of Applicability for the control 
    room radiation monitoring instrumentation is acceptable based on the 
    fuel handling accident analysis dose consequences. The analysis 
    assumes that the control room emergency ventilation system is 
    actuated during a fuel handling accident in the containment 
    building. This analysis also shows that the dose consequences to the 
    control room operators are acceptable in the event of a fuel 
    handling analysis in the 
    
    [[Page 35069]]
    auxiliary building, assuming that the normal control room ventilation 
    system only is in operation. When the unit is in Mode 5 or Mode 6 
    (with no handling of irradiated fuel in the containment building), 
    no accident condition has been identified that would require the 
    control room emergency ventilation system to actuate due to high 
    radiation. The remainder of the changes have been made for 
    consistency between the ANO-1 and ANO-2 TS and are considered to be 
    administrative in nature.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
    
    Criterion 2--Does Not Create the Possibility of a New or Different Kind 
    of Accident from any Previously Evaluated
    
        The control room emergency ventilation and air conditioning 
    systems are not accident initiators. The proposed changes introduce 
    no new mode of plant operation and no new possibility for an 
    accident is introduced by modifying the ANO-1 surveillance testing 
    requirements for the control room emergency ventilation and air 
    conditioning systems.
        Therefore, this change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
    
    Criterion 3--Does Not Involve a Significant Reduction in the Margin of 
    Safety
    
        With the exception of the AOT extension and the relaxation of 
    the ANO-2 Mode of Applicability for the control room radiation 
    monitoring instrumentation, all the ANO-1 and ANO-2 changes are 
    considered administrative or more restrictive and are intended to 
    clarify and make consistent the requirements of the control room 
    emergency habitability equipment. Although the AOT extension does 
    involve an incremental reduction in the margin of safety due to a 
    slight increase in the frequency of an event requiring control room 
    isolation, followed by failure of the operable emergency control 
    room chiller, a probabilistic safety assessment has shown this 
    slight increase in frequency (approximately 3.58E-6/yr) to be 
    acceptably low. The relaxation in the ANO-2 Mode of Applicability 
    for the control room radiation monitoring instrumentation is 
    acceptable based on the fuel handling accident analysis dose 
    consequences. The analysis assumes that the control room emergency 
    ventilation system is actuated during a fuel handling accident in 
    the containment building. This analysis also shows that the dose 
    consequences to the control room operators are acceptable in the 
    event of a fuel handling analysis [sic., accident] in the auxiliary 
    building, assuming that the normal control room ventilation system 
    only is in operation. When the unit is in Mode 5 or Mode 6 (with no 
    handling of irradiated fuel in the containment building), no 
    accident condition has been identified that would require the 
    control room emergency ventilation system to actuate due to high 
    radiation.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: William D. Beckner.
    
    Entergy Operations, Inc., Docket Nos. 50-313 and 50-368, Arkansas 
    Nuclear One, Unit Nos. 1 and 2 (ANO-1&2), Pope County, Arkansas
    
        Date of amendment request: April 4, 1995.
        Description of amendment request: The proposed amendments delete 
    requirements to perform inservice inspections of reactor coolant pump 
    flywheels at both Unit 1 and Unit 2.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    Criterion 1--Does Not Involve a Significant Increase in the Probability 
    or Consequences of an Accident Previously Evaluated.
    
        Missile generation from a reactor coolant pump (RCP) flywheel 
    could damage the reactor coolant system, the containment, or other 
    equipment or systems important to safety. The fracture mechanics 
    analyses conducted to support the change shows that a preexisting 
    crack sized just below detection level will not grow to the flaw 
    size necessary to create flywheel missiles within the life of the 
    plant. This analysis conservatively assumes minimum material 
    properties, maximum flywheel accident speed, location of the flaw in 
    the highest stress area and a number of startup/shutdown cycles 
    eight times greater than expected. Since an existing flaw in the 
    flywheel will not grow to the allowable flaw size under normal 
    operating conditions or to the critical flaw size under LOCA 
    conditions over the life of the plant, elimination of inservice 
    inspections for such cracks during the plant's life will not involve 
    a significant increase in the probability of an accident previously 
    considered.
        The proposed changes do not increase the amount of radioactive 
    material available for release or modify any systems used for 
    mitigation of such releases during accident conditions. Therefore, 
    these changes do not involve a significant increase in the 
    consequences of any accident previously evaluated.
    
    Criterion 2--Does Not Create the Possibility of a New or Different Kind 
    of Accident from any Previously Evaluated
    
        The proposed changes will not change the design, configuration, 
    or method of operation of the plant and therefore, will not create 
    the possibility of a new or different kind of accident from any 
    previously evaluated.
    
    Criterion 3--Does Not Involve a Significant Reduction in the Margin of 
    Safety
    
        Significant conservatisms have been used for calculating the 
    allowable flaw size, critical flaw size and crack growth rate in the 
    RCP flywheels. These include minimum material properties, maximum 
    flywheel accident speed, location of the flaw in the highest stress 
    area and a number of startup/shutdown cycles eight times greater 
    than expected. Since an existing flaw in the flywheel will not grow 
    to the allowable flaw size under normal operating conditions or to 
    the critical flaw size under LOCA conditions over the life of the 
    plant, elimination of inservice inspections for such cracks during 
    the plant's life will not involve a significant reduction in the 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: William D. Beckner.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of amendment request: April 4, 1995.
        Description of amendment request: The proposed amendment revises 
    surveillance requirements associated with the main turbine steam 
    valves.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
    Criterion 1--Does Not Involve a Significant Increase in the Probability 
    or Consequences of an Accident Previously Evaluated.
    
        Modifying the surveillance frequency of the main turbine-
    generator (MTG) overspeed protection system introduces no new 
    failure mechanism for the machine, so the consequences, of a 
    postulated MTG overspeed event are no different than those 
    previously evaluated. 
    
    [[Page 35070]]
    
        As explained in NUREG-1366, ``Improvements to Technical 
    Specifications Surveillance Requirements,'' the present surveillance 
    test frequency requirements were developed for fossil units and 
    carried over to nuclear units due to the similarity in design. 
    However, the particulate concentration, phosphate chemistry and 
    higher steam temperatures present in earlier fossil secondary 
    systems, which were major contributing factors to problems 
    identified by these tests, are not present in the Arkansas Nuclear 
    One-Unit 2 (ANO-2) secondary systems. The operating history of 
    turbine valves at ANO-2 is very good, with no failures identified 
    during the performance of overspeed protection system surveillance 
    testing. Therefore, that change does not involve a significant 
    increase in the probability of any accident previously evaluated.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
    
    Criterion 2--Does Not Create the Possibility of a New or Different Kind 
    of Accident from any Previously Evaluated.
    
        Because the proposed changes do not alter the design, 
    configuration, or method of operation of the plant, they do not 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
    Criterion 3--Does Not Involve a Significant Reduction in the Margin of 
    Safety.
    
        These proposed changes do not alter the acceptance of any 
    surveillance requirements, alter any assumptions used in accident 
    analysis, change any actuation setpoints, nor allow operations in 
    any configuration not previously evaluated. This change in 
    surveillance frequency is based on an operating history of the 
    turbine overspeed protection system which indicates that reducing 
    the test frequency will have no adverse impact on the continued safe 
    operation of the unit.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: William D. Beckner.
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Nuclear Generating Plant, Unit No. 3, Citrus County, Florida
    
        Date of amendment request: May 31, 1995.
        Description of amendment request: The proposed amendment would 
    revise the the Technical Specifications (TS) for the Crystal River Unit 
    3 to facilitate a 24 month operating cycle by changing the surveillance 
    interval for appropriate TS surveillance requirements that are 
    generally performed during a refueling outage. Additionally, the 
    functional description and the ``Allowable Value'' for three Reactor 
    Protection System and one Emergency Feedwater Initiation and Control 
    System setpoints would be revised. The quantitative limits for 
    determining the operational status of the reactor coolant pumps, the 
    main feedwater pumps, and the main turbine would be relocated from the 
    TS to the Final Safety Analysis Report (FSAR). The surveillance 
    associated with the high radiation setpoint for control room isolation 
    would also be changed to reflect that the setpoint is an ``approximate 
    value'' instead of an ``Allowable value''. The current specified 
    surveillance interval for some equipment and systems which were not re-
    evaluated or which could not be justified by the evaluation process 
    would not be changed.
        Specifically:
        1. TS Surveillance Requirements (SR) 3.3.1.6, SR 3.3.5.3, SR 
    3.3.6.1, SR 3.3.9.2, SR 3.3.10.2, SR 3.3.11.3, SR 3.3.17.2, SR 
    3.3.18.2, and SR 3.9.2.2 would be revised to extend the surveillance 
    frequency from 18 to 24 months. Also, in TS SR 3.3.17.2 a note would be 
    added indicating the frequency for Function 12 is 18 months.
        2. In TS Table 3.3.1-1,
        (a) the Function for ``Reactor Coolant Pump Power Monitor (RCPPM)'' 
    would be changed to ``Reactor Coolant Pumps,'' and the ``Allowable 
    Value'' column for this function would be revised to delete the 
    quantitative value and to indicate ``More than one pump tripped'',
        (b) the Function for ``Main Turbine Trip (Control Oil Pressure)'' 
    would be changed to ``Main Turbine,'' and the Allowable Value is 
    changed to ``Turbine Tripped'' and
        (c) the Function for ``Loss of Both Main Feedwater Pumps (Control 
    Oil Pressure)'' would be changed to ``Main Feedwater Pumps,'' and the 
    Allowable Value is changed to ``Both Pumps Tripped''
        3. In TS Table 3.3.11-1, Function 1.a would be changed from ``EFW 
    Initiation--Loss of MFW Pumps (Control Oil Pressure)'' to ``EFW 
    Initiation--Main Feedwater Pumps,'' and the Allowable Value is changed 
    to ``Both Pumps Tripped.''
        4. In TS SR 3.3.16.3, the CHANNEL CALIBRATION setpoint would be 
    changed from an allowable value to an approximate setpoint.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability of occurrence or the consequences of an accident 
    previously evaluated. The proposed amendment extends the interval 
    between successive refueling outage based surveillances to once 
    every 24 months for those surveillances evaluated herein and, 
    maintains the existing surveillance interval restriction for those 
    systems and equipment not evaluated for extension. The reliability 
    of systems and components relied upon to prevent or mitigate the 
    consequences of accidents previously evaluated is not degraded 
    beyond that obtained from the currently defined refueling outage 
    interval. Assurance of system and equipment availability is 
    maintained. This change does not involve any change to system or 
    equipment configuration. Therefore, this change does not increase 
    the probability of occurrence or the consequences of an accident 
    previously evaluated.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated. The 
    proposed amendment extends the interval between successive refueling 
    outage based surveillances to once every 24 months for those 
    surveillances evaluated herein and maintains the existing 
    surveillance interval restriction for those systems and equipment 
    not evaluated for extension. This change does not involve any change 
    to system or equipment configuration. Therefore, this change is 
    unrelated to the possibility of creating a new or different kind of 
    accident from any previously evaluated.
        3. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety. The proposed amendment extends the interval between 
    successive refueling outage based surveillances to once every 24 
    months for the surveillances evaluated herein, and maintains the 
    existing surveillance interval restriction for those systems and 
    equipment not evaluated for extension. The reliability of systems 
    and components is not degraded beyond that obtained from the 
    currently defined refueling outage interval. Assurance of system and 
    equipment availability is maintained.
        Therefore, it is concluded that operation of the facility in 
    accordance with the proposed amendment does not involve a 
    significant reduction in a margin of safety. The proposed extension 
    of the refueling outage interval surveillances to once every 24 
    months does not degrade the reliability of systems and components 
    beyond that obtained from the currently defined refueling outage 
    interval. 
    
    [[Page 35071]]
    Reliable performance of the systems and equipment effected by this 
    change has been demonstrated.
        Implementation of the proposed amendment will maintain the 
    required level of assurance of system and equipment availability. 
    The surveillance interval for systems and equipment that have not 
    been evaluated for extension are excluded from this request. Thus, 
    operation of the facility in accordance with the proposed amendment 
    involves no significant hazards considerations.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 32629.
        Attorney for licensee: A.H. Stephens, General Counsel, Florida 
    Power Corporation, MAC-A5D, P. O. Box 14042, St. Petersburg, Florida 
    33733.
        NRC Project Director: David B. Matthews.
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Nuclear Generating Plant, Unit No. 3, Citrus County, Florida.
    
        Date of amendment request: May 31, 1995.
        Description of amendment request: The proposed amendment would 
    revise the technical specifications (TS) for the Crystal River Nuclear 
    Plant Unit 3 (CR3) relating to the Once Through Steam Generator's 
    (OTSG's) tube inspection acceptance criteria. Currently, the TS specify 
    repair limit for removing steam generator tubes from service based on a 
    structural evaluation of a simplified model of tubes with uniform 
    through wall (T/W) thinning. A recent tube-pull examination at CR3 
    identified a number of low signal-to-noise (S/N) tube eddy current 
    indications. The licensee indicated that these S/N indications are a 
    substantially different morphology from the model used to develop the 
    current TS inspection and acceptance limit. As a result of the small 
    signal amplitude associated with these S/N indications, they cannot be 
    accurately sized by conventional bobbin coil phase angle. Therefore, 
    the licensee proposed an alternate methodology for dispositioning the 
    S/N indications. The proposed criteria would address both wear and 
    Inter-Granular-Attack (IGA) degradation mechanisms. Crack-like eddy 
    current indications are not included within the proposed scope.
        Specifically, the licensee proposed to:
        A. Revise TS 5.6.2.10.2, page 5.0-14, ``The results of each sample 
    inspection shall be classified into one of the following three 
    categories:'' to read: ``The results of each bobbin coil sample 
    inspection shall be classified into one of the following three 
    categories:''
        B. Revise the Note in TS 5.6.2.10.2, page 5.0-14, ``In all 
    inspections, previously degraded tubes whose degradation has not been 
    spanned by a sleeve must exhibit a significant increase in the 
    applicable imperfection size measurement (> +0.5V bobbin coil amplitude 
    increase for S/N indications or >10% further wall penetration for all 
    other imperfections) to be included in the below percentage 
    calculations.''
        C. Revise the sentence in TS 5.6.2.10.4.a.2, page 5.0-16, ``Eddy-
    current* * *as imperfections'' to read: S/N indications with a bobbin 
    coil amplitude < 0.9v="" are="" considered="" imperfections.="" other="" eddy="" current="" testing="" indications="" below="" 20%="" of="" the="" nominal="" tube="" wall="" thickness,="" if="" detectable,="" may="" also="" be="" considered="" as="" imperfections.="" d.="" revise="" ts="" 5.6.2.10.4.a.4,="" page="" 5.0-16,="" to="" read:="" ``degraded="" tube="" means="" a="" tube="" containing="" a="" s/n="" indication="" with="" a="" bobbin="" coil="" amplitude=""> 0.9V or other imperfection 
     20% of the nominal wall thickness caused by degradation 
    except where all such degradation has been spanned by the installation 
    of a sleeve.''
        E. Add TS 5.6.2.10.4.a.7 ``Signal-to-Noise (S/N) indication means 
    an indication whose associated bobbin coil amplitude is < 5="" times="" the="" background="" noise,="" excluding="" indications="" located="" in="" the="" tube="" sheet="" regions="" or="" indications="" determined="" to="" be="" other="" than="" a="" volumetric="" morphology.''="" f.="" renumber="" 5.6.2.10.4.a.7="" to="" 5.6.2.10.4.a.8,="" and="" revise="" to="" read:="" plugging/sleeving="" limit="" means="" the="" imperfection="" depth="" at="" or="" beyond="" which="" the="" tube="" shall="" be="" restored="" to="" serviceability="" by="" the="" installation="" of="" a="" sleeve="" or="" removed="" from="" service="" because="" it="" may="" become="" unserviceable="" prior="" to="" the="" next="" inspection.="" the="" limit="" for="" s/n="" indications="" is="" equal="" to="" a="" bobbin="" coil="" amplitude="" of="" 2.5v,="" an="" axial="" extent="" of="" 0.33="" inches,="" or="" a="" circumferential="" extent="" of="" 0.6="" inches.="" the="" limit="" is="" equal="" to="" 40%="" of="" the="" nominal="" tube="" or="" sleeve="" wall="" thickness="" for="" other="" imperfections.="" no="" more="" than="" 5000="" sleeves="" may="" be="" installed="" in="" each="" otsg.="" g.="" renumber="" 5.6.2.10.4.a.8,="" and="" 9="" to="" 5.6.2.10.4.a.9="" and="" 10.="" h.="" revise="" ts="" 5.7.2.c.2,="" page="" 5.0-29,="" to="" read:="" location,="" bobbin="" coil="" amplitude,="" and="" axial="" and="" circumferential="" extent="" (if="" determined)="" for="" each="" s/n="" indication="" and="" the="" location="" and="" percent="" of="" wall="" thickness="" penetration="" for="" each="" other="" indication="" of="" an="" imperfection,="" and="" basis="" for="" proposed="" no="" significant="" hazards="" consideration="" determination:="" as="" required="" by="" 10="" cfr="" 50.91(a),="" the="" licensee="" has="" provided="" its="" analysis="" of="" the="" issue="" of="" no="" significant="" hazards="" consideration,="" which="" is="" presented="" below:="" 1.="" the="" proposed="" change="" will="" not="" significantly="" increase="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" the="" relevant="" accidents="" are="" excessive="" leakage="" or="" steam="" generator="" tube="" rupture="" (as="" a="" consequence="" of="" mslb="" [main="" steam="" line="" break]="" or="" otherwise).="" rg="" [regulatory="" guide]="" 1.121="" establishes="" a="" standard="" method="" for="" demonstrating="" structural="" integrity="" under="" worse-than-dbe="" [design="" basis="" event]="" conditions.="" the="" existing="" ts="" is="" based="" on="" this="" rg.="" the="" s/="" n="" disposition="" strategy="" continues="" to="" rely="" on="" this="" guidance.="" current="" tw="" sizing="" techniques="" would="" allow="" defects="" greater="" than="" the="" current="" ts="" limit="" of="" 40%="" to="" remain="" in="" service="" since="" these="" techniques="" do="" not="" accurately="" measure="" percent="" wall="" penetration="" for="" small="" volume="" indications.="" the="" proposed="" disposition="" strategy="" is="" based="" in="" measurable="" eddy="" current="" parameters="" of="" voltage,="" axial="" extent,="" and="" circumferential="" extent="" shown="" to="" provide="" a="" higher="" confidence="" that="" unacceptable="" flaws="" are="" removed="" from="" service.="" therefore,="" the="" probability="" of="" a="" steam="" generator="" tube="" rupture="" (sgtr)="" is="" not="" increased="" and="" may="" well="" be="" decreased="" by="" implementation="" of="" this="" s/n="" disposition="" strategy.="" the="" probability="" of="" otsg="" tube="" leakage="" during="" normal="" operation="" or="" accident="" conditions="" is="" not="" adversely="" affected="" by="" the="" proposed="" s/n="" disposition="" strategy.="" operating="" history="" indicates="" essentially="" no="" primary="" to="" secondary="" leakage="" through="" the="" otsg="" tubes="" at="" cr-3.="" growth="" rate="" studies="" imply="" this="" trend="" could="" be="" expected="" to="" continue.="" therefore,="" current="" leakage="" limits="" are="" retained.="" small="" volume="" indications="" which="" might="" leak="" during="" worse-case="" fwlb="" [feedwater="" line="" break]="" conditions="" are="" addressed="" in="" the="" rg="" 1.121="" evaluation.="" the="" disposition="" strategy="" ensure="" these="" indications="" are="" removed="" from="" service="" as="" part="" of="" the="" inservice="" inspection.="" once="" detected,="" the="" proposed="" criteria="" is="" at="" least="" as="" effective="" in="" determining="" those="" indications="" which="" should="" be="" removed="" from="" service="" as="" are="" the="" existing="" ts="" limits.="" the="" s/n="" disposition="" strategy="" is="" an="" integral="" part="" of="" an="" overall="" effort="" to="" better="" address="" these="" and="" similar="" phenomena="" in="" otsgs.="" 2.="" the="" proposed="" change="" will="" not="" create="" the="" possibility="" of="" a="" new="" or="" different="" kind="" of="" accident="" from="" any="" accident="" previously="" evaluated.="" the="" key="" `new="" or="" different'="" accidents="" addressed="" in="" this="" and="" similar="" proposals="" is="" the="" potential="" for="" mslb-induced="" multiple="" sgtr="" or="" excessive="" primary-to-secondary="" leakage="" during="" such="" events.="" while="" these="" events="" are="" addressed="" in="" cr-3="" emergency="" operating="" procedures="" (eops),="" they="" are="" beyond="" those="" licensed="" for="" the="" facility.="" however,="" as="" noted="" above,="" the="" probability="" of="" mslb="" induced="" multiple="" sgtr="" is="" reduced="" by="" more="" effective="" screening="" and="" plugging/="" [[page="" 35072]]="" sleeving="" criteria.="" the="" probability="" of="" detection="" and="" identification="" of="" tubes="" which="" should="" be="" removed="" from="" service="" is="" maintained="" or="" improved="" by="" the="" s/n="" disposition="" strategy.="" the="" likelihood="" of="" adverse="" effects="" from="" plugging="" sound="" tubes="" is="" reduced.="" the="" operation="" of="" the="" otsg="" or="" related="" structures,="" systems="" or="" components="" is="" otherwise="" unaffected.="" 3.="" the="" proposed="" change="" will="" not="" involve="" a="" significant="" reduction="" to="" any="" margin="" of="" safety.="" the="" margins="" of="" safety="" defined="" in="" rg="" 1.121,="" including="" the="" required="" pressure="" used="" in="" the="" structural="" analysis,="" are="" retained.="" the="" probability="" of="" detecting="" degradation="" is="" unchanged="" since="" bobbin="" coil="" methods="" will="" continue="" to="" be="" the="" primary="" means="" of="" initial="" detection.="" the="" probability="" of="" leakage="" remains="" acceptably="" small.="" the="" proposed="" s/="" n="" disposition="" strategy="" is="" an="" enhancement="" to="" the="" inservice="" inspection="" of="" otsg="" tubing="" that="" will="" provide="" a="" higher="" level="" of="" confidence="" that="" tubes="" exceeding="" the="" allowable="" limits="" are="" repaired="" while="" sound="" tubes="" are="" left="" in="" service.="" based="" upon="" results="" of="" the="" various="" growth="" rate="" studies,="" the="" probability="" of="" an="" accident="" at="" the="" end="" of="" cycle="" is="" essentially="" the="" same="" as="" the="" beginning.="" the="" nrc="" staff="" has="" reviewed="" the="" licensee's="" analysis="" and,="" based="" on="" this="" review,="" it="" appears="" that="" the="" three="" standards="" of="" 50.92(c)="" are="" satisfied.="" therefore,="" the="" nrc="" staff="" proposes="" to="" determine="" that="" the="" amendment="" request="" involves="" no="" significant="" hazards="" consideration.="" local="" public="" document="" room="" location:="" coastal="" region="" library,="" 8619="" w.="" crystal="" street,="" crystal="" river,="" florida="" 32629.="" attorney="" for="" licensee:="" a.="" h.="" stephens,="" general="" counsel,="" florida="" power="" corporation,="" mac-a5d,="" p.="" o.="" box="" 14042,="" st.="" petersburg,="" florida="" 33733.="" nrc="" project="" director:="" david="" b.="" matthews.="" florida="" power="" and="" light="" company,="" docket="" nos.="" 50-250="" and="" 50-251,="" turkey="" point="" plant="" units="" 3="" and="" 4,="" dade="" county,="" florida="" date="" of="" amendment="" request:="" june="" 19,="" 1995.="" description="" of="" amendment="" request:="" the="" licensee="" proposes="" to="" change="" turkey="" point="" units="" 3="" and="" 4="" technical="" specifications="" (ts)="" by="" separation="" of="" the="" 24-hour="" emergency="" diesel="" generator="" (edg)="" run="" and="" hot="" restart="" edg="" test="" from="" the="" loss-of-offsite-power="" load="" acceptance="" test.="" the="" licensee="" revised="" the="" original="" amendment="" request="" dated="" march="" 30,="" 1995,="" by="" letters="" dated="" may="" 5,="" 1995,="" and="" june="" 19,="" 1995.="" basis="" for="" proposed="" no="" significant="" hazards="" consideration="" determination:="" as="" required="" by="" 10="" cfr="" 50.91(a),="" the="" licensee="" has="" provided="" its="" analysis="" of="" the="" issue="" of="" no="" significant="" hazards="" consideration,="" which="" was="" previously="" presented="" in="" the="" federal="" register="" (60="" fr="" 27339,="" may="" 23,="" 1995).="" the="" licensee="" concluded="" that="" the="" proposed="" license="" amendments'="" revisions="" do="" not="" alter="" the="" original="" conclusion="" that="" no="" significant="" hazards="" considerations="" exist="" pursuant="" to="" 10="" cfr="" 50.92.="" the="" nrc="" staff="" has="" reviewed="" the="" licensee's="" analysis="" and,="" based="" on="" this="" review,="" it="" appears="" that="" the="" three="" standards="" of="" 50.92(c)="" are="" satisfied.="" therefore,="" the="" nrc="" staff="" proposes="" to="" determine="" that="" the="" amendment="" request="" and="" its="" revisions="" involve="" no="" significant="" hazards="" consideration.="" local="" public="" document="" room="" location:="" florida="" international="" university,="" university="" park,="" miami,="" florida="" 33199.="" attorney="" for="" licensee:="" j.r.="" newman,="" esquire,="" morgan,="" lewis="" &="" bockius,="" 1800="" m="" street,="" nw.,="" washington,="" dc="" 20036.="" nrc="" project="" director:="" david="" b.="" matthews.="" georgia="" power="" company,="" oglethorpe="" power="" corporation,="" municipal="" electric="" authority="" of="" georgia,="" city="" of="" dalton,="" georgia,="" docket="" nos.="" 50-321="" and="" 50-366,="" edwin="" i.="" hatch="" nuclear="" plant,="" units="" 1="" and="" 2,="" appling="" county,="" georgia="" date="" of="" amendment="" request:="" january="" 13,="" 1995,="" as="" supplemented="" by="" letters="" dated="" april="" 5="" and="" june="" 20,="" 1995.="" description="" of="" amendment="" request:="" the="" proposed="" amendments="" would="" change="" the="" facility="" operating="" licenses="" and="" their="" corresponding="" appendices="" a="" which="" contain="" the="" technical="" specifications="" (ts)="" to="" permit="" the="" implementation="" of="" the="" power="" uprate="" program="" at="" the="" edwin="" i.="" hatch="" nuclear="" plant,="" units="" 1="" and="" 2.="" the="" hatch="" units="" are="" currently="" licensed="" for="" operation="" at="" 2436="" megawatts="" thermal="" (mwt).="" the="" proposed="" changes="" would="" redefine="" the="" rated="" thermal="" power="" to="" 2558="" mwt,="" which="" represents="" an="" increase="" of="" 5%="" over="" the="" current="" licensed="" level="" in="" accordance="" with="" the="" generic="" boiling="" water="" reactor="" (bwr)="" power="" uprate="" program="" established="" by="" the="" general="" electric="" company="" (ge)="" and="" approved="" by="" the="" u.s.="" nuclear="" regulatory="" commission="" (nrc)="" staff="" in="" a="" letter="" from="" w.="" t.="" russell,="" nrc,="" to="" p.="" w.="" marriott,="" ge,="" dated="" september="" 30,="" 1991.="" implementation="" of="" the="" proposed="" power="" uprate="" at="" plant="" hatch="" will="" result="" in="" an="" increase="" of="" steam="" flow="" to="" approximately="" 106%="" of="" the="" current="" value="" but="" will="" require="" no="" changes="" to="" the="" basic="" fuel="" design.="" implementation="" of="" this="" proposed="" power="" uprate="" will="" require="" minor="" modifications,="" such="" as="" resetting="" the="" safety="" relief="" setpoints,="" as="" well="" as="" the="" calibration="" of="" plant="" instrumentation="" to="" reflect="" the="" uprated="" power.="" plant="" operating,="" emergency,="" and="" other="" procedure="" changes="" will="" be="" made="" where="" necessary="" to="" support="" uprated="" operation.="" basis="" for="" proposed="" no="" significant="" hazards="" consideration="" determination:="" as="" required="" by="" 10="" cfr="" 50.91(a),="" the="" licensee="" has="" provided="" its="" analysis="" of="" the="" issue="" of="" no="" significant="" hazards="" consideration="" which="" is="" presented="" below:="" 1.="" will="" the="" changes="" involve="" a="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated?="" a.="" rated="" thermal="" power="" is="" increased="" to="" 2558="" mwt="" on="" page="" 3="" of="" the="" unit="" 1="" operating="" license,="" page="" 4="" of="" the="" unit="" 2="" operating="" license,="" and="" in="" section="" 1.1="" (definitions)="" of="" the="" units="" 1="" and="" 2="" technical="" specifications.="" evaluation="" the="" changes="" in="" the="" operating="" licenses="" and="" technical="" specifications="" were="" evaluated="" and="" it="" was="" determined="" that="" the="" probability="" (frequency="" of="" occurrence)="" of="" design="" basis="" accidents="" occurring="" is="" not="" affected="" by="" the="" increased="" power="" level,="" as="" the="" regulatory="" criteria="" established="" for="" plant="" equipment="" (e.g.,="" asme="" code,="" ieee="" standards,="" nema="" standards,="" regulatory="" guide="" criteria)="" will="" still="" be="" complied="" with="" at="" the="" uprated="" power="" level.="" scram="" setpoints="" (equipment="" settings="" that="" initiate="" automatic="" plant="" shutdowns)="" will="" be="" established="" such="" that="" there="" is="" no="" significant="" increase="" in="" scram="" frequency="" due="" to="" uprate.="" no="" new="" challenges="" to="" safety-related="" equipment="" will="" result="" from="" power="" uprate.="" the="" changes="" in="" consequences="" of="" hypothetical="" accidents="" which="" would="" occur="" from="" 102%="" of="" the="" uprated="" power,="" compared="" to="" those="" previously="" evaluated,="" are="" in="" all="" cases="" insignificant,="" because="" the="" power="" uprate="" accident="" evaluations="" will="" not="" result="" in="" exceeding="" any="" nrc-approved="" acceptance="" limits.="" enclosure="" 4="" of="" reference="" 1,="" general="" electric="" report="" nedc-32405p,="" ``power="" uprate="" safety="" analysis="" for="" edwin="" i.="" hatch="" plant="" units="" 1="" and="" 2,''="" december="" 1994,="" investigated="" the="" spectrum="" of="" hypothetical="" accidents="" and="" transients,="" and="" showed="" the="" plant's="" current="" regulatory="" criteria="" are="" satisfied="" at="" power="" uprate.="" for="" example,="" in="" the="" area="" of="" core="" design,="" the="" fuel="" operating="" limits="" will="" still="" be="" met="" at="" the="" uprated="" power="" level,="" and="" fuel="" reload="" analyses="" will="" show="" plant="" transients="" meet="" the="" criteria="" accepted="" by="" the="" nrc="" as="" specified="" in="" nedo-24011,="" ``gestar="" ii.''="" challenges="" to="" fuel="" or="" emergency="" core="" cooling="" system="" (eccs)="" performance="" were="" evaluated="" (section="" 4.2="" of="" nedc-32405p)="" and="" shown="" to="" still="" meet="" the="" criteria="" of="" 10="" [cfr]="" 50.46="" and="" appendix="" k.="" challenges="" to="" the="" containment="" were="" evaluated="" (section="" 4.1="" of="" nedc-32405p)="" and="" shown="" to="" still="" meet="" 10="" cfr="" 50="" appendix="" a,="" criterion="" 38,="" long="" term="" cooling,="" and="" criterion="" 50,="" containment.="" radiological="" release="" events="" were="" evaluated="" (section="" 9.2="" of="" nedc-32405p)="" and="" shown="" to="" meet="" the="" criteria="" of="" 10="" cfr="" 100="" (unit="" 1="" fsar="" chapter="" 14="" and="" unit="" 2="" fsar="" chapter="" 15).="" the="" results="" of="" the="" analyses="" discussed="" above="" demonstrate="" that="" operation="" at="" the="" power="" uprate="" level="" does="" not="" significantly="" increase="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" b.="" the="" surveillance="" test="" discharge="" pressure="" for="" the="" standby="" liquid="" control="" pump="" at="" 41.2="" gpm="" is="" increased="" from="" 1190="" psig="" to="" 1201="" psig.="" this="" value="" appears="" in="" surveillance="" requirement="" (sr)="" 3.1.7.7="" and="" the="" [[page="" 35073]]="" corresponding="" bases="" section="" b="" 3.1.7="" in="" the="" unit="" 1="" and="" unit="" 2="" technical="" specifications.="" evaluation="" power="" uprate="" operation="" will="" result="" in="" a="" 30="" psi="" increase="" in="" reactor="" operating="" pressure.="" as="" will="" be="" discussed="" in="" these="" proposed="" changes,="" several="" pressure-dependent="" setpoints="" (including="" safety="" relief="" valve="" [srv]="" setpoints)="" will="" be="" increased="" to="" preserve="" current="" margins.="" increasing="" the="" pressure="" 11="" psi,="" at="" which="" a="" 41.2="" gpm="" flow="" rate="" is="" developed,="" assures="" continued="" conformance="" to="" anticipated="" transient="" without="" scram="" (atws)="" criteria="" at="" uprated="" conditions.="" the="" surveillance="" test="" pressure="" is="" based="" on="" the="" maximum="" pressure="" for="" an="" atws="" event="" during="" the="" time="" period="" when="" the="" standby="" liquid="" control="" pump="" is="" in="" operation.="" section="" 6.5="" of="" nedc-32405p="" discusses="" the="" capability="" of="" these="" positive="" displacement="" pumps.="" a="" small="" increase="" in="" the="" srv="" setpoints="" will="" have="" no="" effect="" on="" the="" rated="" injection="" flow="" to="" the="" reactor.="" this="" change,="" therefore,="" will="" not="" increase="" the="" probability="" or="" consequences="" of="" a="" previously="" evaluated="" accident.="" c.="" the="" reactor="" vessel="" steam="" dome="" high="" pressure="" allowable="" value="" for="" reactor="" protection="" system="" (rps)="" instrumentation="" is="" increased="" 31="" psi,="" consistent="" with="" the="" nominal="" pressure="" increase="" for="" power="" uprate.="" the="" allowable="" value="" appears="" in="" section="" 3.3.1.1,="" table="" 3.3.1.1-1,="" function="" 3,="" in="" the="" unit="" 1="" and="" unit="" 2="" technical="" specifications.="" evaluation="" the="" reactor="" vessel="" steam="" dome="" high="" pressure="" scram="" limit="" is="" increased="" because="" the="" steam="" dome="" operating="" pressure="" is="" increased.="" operating="" pressure="" for="" uprated="" power="" is="" increased="" to="" assure="" that="" satisfactory="" reactor="" pressure="" control="" is="" maintained.="" the="" operating="" pressure="" was="" chosen="" on="" the="" basis="" of="" steam="" line="" pressure="" drop="" characteristics="" and="" the="" steam="" flow="" capability="" of="" the="" turbine.="" satisfactory="" reactor="" pressure="" control="" requires="" an="" adequate="" flow="" margin="" between="" the="" uprated="" operating="" condition="" and="" the="" steam="" flow="" capability="" of="" the="" turbine="" control="" valves="" at="" their="" maximum="" stroke.="" an="" operating="" dome="" pressure="" of="" 1035="" psig,="" which="" is="" 30="" psi="" higher="" than="" the="" current="" operating="" dome="" pressure,="" is="" expected.="" therefore,="" the="" high="" pressure="" scram="" is="" increased="" approximately="" the="" same="" amount="" to="" preserve="" existing="" margins="" to="" reactor="" trips.="" the="" high="" pressure="" scram="" terminates="" a="" pressurization="" transient="" not="" terminated="" by="" direct="" scram="" or="" high="" neutron="" flux="" scram.="" the="" setting="" is="" maintained="" above="" the="" nominal="" reactor="" vessel="" operating="" pressure="" and="" below="" the="" specified="" analytical="" trip="" limit="" used="" in="" the="" safety="" analyses.="" the="" revised="" high="" pressure="" scram="" setpoint="" will="" preserve="" the="" hierarchy="" of="" pressure="" setpoints.="" this="" means="" that="" the="" high="" pressure="" scram="" setpoint="" will="" remain="" below="" the="" opening="" setpoint="" of="" the="" srvs.="" the="" srv="" nominal="" setpoints="" are="" also="" increased="" 30="" psi,="" as="" discussed="" in="" item="" g="" below.="" this="" hierarchy="" of="" setpoints="" provides="" assurance="" that="" the="" probability="" of="" opening="" more="" than="" one="" srv="" without="" scram="" intervention="" is="" low.="" since="" the="" scram="" function="" and="" the="" current="" margins="" to="" trip="" avoidance="" are="" maintained="" with="" revised="" setpoints,="" there="" is="" no="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" d.="" the="" atws="" reactor="" vessel="" steam="" dome="" high="" pressure="" recirculation="" pump="" trip="" (rpt)="" allowable="" value="" is="" raised="" 80="" psi.="" the="" allowable="" value="" appears="" in="" section="" 3.3.4.2,="" sr="" 3.3.4.2.3,="" in="" the="" unit="" 1="" and="" unit="" 2="" technical="" specifications.="" evaluation="" the="" atws-rpt="" high="" pressure="" setpoint="" initiates="" a="" trip="" of="" the="" recirculation="" pumps,="" thereby="" adding="" negative="" reactivity="" following="" events="" in="" which="" a="" scram="" does="" not="" (but="" should)="" occur.="" section="" 5.1.3.2="" of="" nedc-32405p="" discusses="" this="" function="" in="" detail.="" the="" current="" analytical="" limit="" for="" the="" atws-rpt="" high="" pressure="" trip="" is="" 1150="" psig.="" this="" value="" was="" increased="" 30="" psi="" in="" the="" power="" uprate="" atws="" safety="" evaluations="" to="" account="" for="" the="" 30="" psi="" increase="" in="" vessel="" operating="" pressure,="" srv="" setpoints,="" etc.="" the="" current="" allowable="" value="" in="" the="" technical="" specifications="" is="" 1095="" psig.="" this="" allowable="" value="" was="" not="" set="" by="" the="" current="" analytical="" limit,="" but="" by="" the="" range="" of="" the="" installed="" pressure="" instruments.="" as="" part="" of="" the="" power="" uprate="" plant="" changes,="" these="" pressure="" instruments="" will="" be="" replaced="" to="" accommodate="" higher="" pressure,="" and="" the="" allowable="" value,="" in="" conjunction="" with="" the="" analytical="" limit="" used="" in="" the="" safety="" analysis,="" will="" be="" increased.="" sections="" 5.1="" and="" 9.3="" of="" nedc-32405p="" show="" the="" system="" can="" adequately="" perform="" its="" atws="" function="" with="" the="" new="" setpoint.="" therefore,="" the="" proposed="" change="" does="" not="" cause="" a="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" e.="" the="" low-low="" set="" (lls)="" srv="" arming="" pressure="" allowable="" value="" is="" increased="" 31="" psi,="" consistent="" with="" the="" increase="" in="" operating="" pressure="" and="" high="" pressure="" scram="" allowable="" value.="" the="" lls="" arming="" pressure="" allowable="" value="" appears="" in="" section="" 3.3.6.3,="" table="" 3.3.6.3-1,="" function="" 1,="" in="" the="" unit="" 1="" and="" unit="" 2="" technical="" specifications.="" evaluation="" the="" allowable="" value="" for="" the="" lls="" srv="" high="" pressure="" arming="" setpoint="" is="" increased="" because="" the="" high="" pressure="" scram="" setpoint="" is="" increased.="" no="" changes="" to="" the="" lls="" arming="" logic="" associated="" with="" the="" srv="" tailpipe="" pressure="" switches="" and="" the="" lls="" opening="" and="" closing="" pressure="" setpoints="" are="" proposed.="" the="" lls="" relief="" logic="" mitigates="" the="" postulated="" containment="" loads="" of="" subsequent="" srv="" actuations="" during="" small="" or="" intermediate="" loss="" of="" coolant="" accidents="" (locas)="" by="" extending="" the="" time="" between="" actuations.="" the="" lls="" logic="" requires="" two="" separate="" signals="" to="" arm="" itself="" for="" operation.="" specifically,="" the="" lls="" logic="" arms="" when="" an="" srv="" opens="" (i.e.,="" tailpipe="" pressure="" switch)="" and="" reactor="" pressure="" concurrently="" exceeds="" the="" scram="" setpoint.="" to="" preserve="" the="" hierarchy="" of="" pressure="" setpoints,="" the="" high="" pressure="" input="" to="" the="" lls="" srv="" arming="" logic="" has="" the="" same="" setpoint="" as="" the="" high="" pressure="" scram,="" thus="" minimizing="" the="" potential="" for="" a="" spurious="" srv="" opening="" through="" the="" lls="" logic="" without="" occurrence="" of="" a="" reactor="" scram.="" increasing="" the="" arming="" setpoint="" is="" consistent="" with="" increasing="" the="" high="" pressure="" scram="" setpoint="" and="" will="" not="" increase="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" f.="" lower="" the="" permissible="" rod="" line="" for="" single-loop="" operation="" (slo)="" below="" 45="" percent="" core="" flow="" from="" the="" 80="" percent="" rod="" line="" to="" the="" 76="" percent="" rod="" line.="" this="" technical="" specifications="" limit="" appears="" in="" section="" 3.4.1="" (figure="" 3.4.1-1)="" and="" the="" corresponding="" bases="" section="" b="" 3.4.1="" of="" the="" unit="" 1="" and="" unit="" 2="" technical="" specifications.="" evaluation="" during="" development="" of="" the="" generic="" power="" uprate="" program,="" ge="" and="" the="" nrc="" agreed="" to="" maintain="" the="" current="" exclusion="" region="" in="" the="" power-to-flow="" map="" related="" to="" thermal-hydraulic="" stability.="" the="" current="" limit="" for="" slo="" is="" the="" 80="" percent="" rod="" line.="" power="" uprate="" will="" redefine="" 100="" percent="" rated="" power="" and,="" therefore,="" rated="" rod="" or="" flow="" control="" lines.="" the="" 76="" percent="" rod="" line="" at="" uprated="" conditions="" closely="" corresponds="" on="" an="" absolute,="" rather="" than="" percentage="" basis,="" to="" the="" existing="" 80="" percent="" rod="" line.="" therefore,="" this="" proposed="" technical="" specifications="" change="" ensures="" that="" power="" uprate="" operation="" will="" not="" cause="" a="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" accident="" previously="" evaluated.="" g.="" the="" srv="" lift="" setpoints="" in="" the="" units="" 1="" and="" 2="" technical="" specifications="" sr="" 3.4.3.1="" will="" be="" increased="" 30="" psi.="" evaluation="" the="" srvs="" are="" designed="" to="" prevent="" overpressurization="" of="" the="" reactor="" pressure="" vessel="" during="" abnormal="" operational="" transients.="" the="" srv="" lift="" setpoints="" are="" increased="" to="" accommodate="" the="" increase="" in="" operating="" pressure="" that="" accompanies="" power="" uprate.="" the="" increase="" in="" srv="" setpoints="" ensures="" that="" adequate="" margins="" are="" maintained="" so="" that="" the="" increase="" in="" dome="" pressure="" during="" normal="" operation="" does="" not="" result="" in="" an="" increase="" in="" the="" number="" of="" unnecessary="" srv="" actuations.="" the="" setpoint="" increase="" also="" maintains="" the="" hierarchy="" of="" pressure="" setpoints="" described="" in="" these="" proposed="" changes.="" transient="" evaluations="" include="" a="" +3="" percent="" tolerance="" to="" the="" nominal="" setpoints.="" as="" described="" in="" section="" 3.2="" of="" nedc-32405p,="" peak="" vessel="" pressure="" increases="" by="" 3="" percent,="" but="" remains="" well="" below="" the="" 1375="" psig="" asme="" code="" limit.="" although="" not="" credited="" in="" the="" transient="" analysis,="" gpc="" installed="" a="" pressure="" transmitter="" system="" which="" can="" electronically="" actuate="" the="" srvs="" on="" high="" vessel="" pressure.="" the="" nominal="" trip="" setpoints="" for="" its="" actuation="" correspond="" with="" the="" nominal="" mechanical="" lift="" setpoints="" in="" the="" technical="" specifications.="" the="" srv="" pressure="" transmitter="" system="" nominal="" setpoints="" will="" also="" be="" increased="" 30="" psi.="" general="" electric="" generically="" evaluated="" the="" adequacy="" of="" bwr="" srvs="" to="" operate="" at="" uprated="" temperatures="" and="" pressures.="" the="" reactor="" operating="" pressure="" and="" temperature="" increases="" of="" less="" than="" 40="" psi="" and="" 5="" deg.f,="" respectively,="" used="" in="" that="" evaluation="" bound="" the="" uprated="" hatch="" operating="" conditions.="" the="" impact="" of="" power="" uprate="" on="" the="" hatch="" containment="" dynamic="" loads="" due="" to="" srv="" discharge="" has="" also="" been="" evaluated.="" as="" discussed="" in="" section="" 4.1.2="" of="" nedc-32405p,="" the="" vent="" thrust="" loads="" with="" power="" uprate="" were="" calculated="" to="" be="" less="" than="" the="" loads="" used="" in="" the="" containment="" analysis.="" the="" effects="" of="" power="" uprate="" on="" srv="" air-="" clearing,="" the="" [[page="" 35074]]="" discharge="" line,="" the="" pool="" pressure="" boundary,="" and="" submerged="" structure="" drag="" loads="" are="" discussed="" in="" section="" 4.1.2="" of="" nedc-32405p="" which="" concludes="" that="" the="" small="" increase="" in="" the="" setpoint="" pressure="" is="" well="" within="" the="" margin="" in="" the="" srv="" loads="" defined="" in="" the="" mark="" i="" containment="" long-term="" program.="" therefore,="" power="" uprate="" does="" not="" impact="" the="" hatch="" srv="" load="" definitions="" used="" in="" the="" containment="" analysis,="" and="" no="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated="" is="" caused="" by="" this="" proposed="" change.="" h.="" the="" limiting="" condition="" for="" operation="" (lco)="" and="" srs="" for="" the="" maximum="" reactor="" steam="" dome="" pressure="" will="" be="" increased="" from="" 1020="" psig="" to="" 1058="" psig.="" this="" requirement="" appears="" in="" lco="" 3.4.10,="" sr="" 3.4.10.1,="" and="" the="" corresponding="" bases="" in="" the="" unit="" 1="" and="" unit="" 2="" technical="" specifications.="" evaluation="" as="" discussed="" in="" the="" technical="" specifications="" bases="" and="" nedc-="" 32405p,="" the="" maximum="" reactor="" dome="" pressure="" is="" an="" initial="" condition="" of="" the="" vessel="" overpressure="" protection="" analysis,="" which="" assumes="" a="" fast="" isolation="" of="" all="" four="" main="" steam="" lines="" by="" the="" main="" steam="" isolation="" valves="" (msivs).="" the="" reactor="" scram="" signal="" generated="" directly="" by="" the="" valve="" closure="" is="" assumed="" defeated="" for="" this="" analysis.="" instead,="" the="" scram="" signal="" is="" generated="" by="" high="" neutron="" flux.="" the="" overpressure="" analysis="" for="" power="" uprate="" assumed="" an="" initial="" dome="" pressure="" of="" 1058="" psig,="" which="" represents="" an="" increase="" of="" 38="" psig.="" this="" initial="" pressure="" was="" chosen="" approximately="" 2="" percent="" above="" the="" 1035="" psig="" steam="" dome="" operating="" pressure="" expected="" for="" power="" uprate="" operation.="" the="" analysis="" also="" included="" the="" other="" changes="" (including="" srv="" setpoints)="" discussed="" in="" these="" proposed="" changes.="" therefore,="" there="" is="" no="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" i.="" the="" hpci="" and="" rcic="" surveillance="" test="" pressures="" in="" units="" 1="" and="" 2="" technical="" specifications="" srs="" 3.5.1.8="" and="" 3.5.3.3,="" respectively,="" are="" increased="" 38="" psi.="" evaluation="" the="" allowable="" hpci="" and="" rcic="" surveillance="" test="" pressure="" is="" increased="" to="" correspond="" with="" the="" increase="" in="" normal="" reactor="" operating="" pressure="" and="" lco/sr="" on="" maximum="" reactor="" pressure="" that="" accompanies="" power="" uprate.="" (as="" discussed="" in="" item="" h="" above,="" the="" lco="" on="" reactor="" steam="" dome="" pressure="" is="" increased="" 38="" psi.)="" the="" change="" is="" needed="" to="" ensure="" that="" pressure="" and="" power="" reductions="" are="" not="" required="" to="" perform="" surveillance="" testing.="" the="" requested="" changes="" will="" allow="" the="" quarterly="" demonstration="" of="" the="" hpci="" and="" rcic="" systems'="" capability="" to="" perform="" at="" normal="" reactor="" operating="" pressures,="" which="" meets="" the="" original="" intent="" of="" the="" technical="" specifications.="" the="" hpci="" and="" rcic="" systems="" have="" been="" evaluated="" and="" demonstrated="" to="" be="" capable="" of="" injecting="" design="" flow="" rate="" at="" the="" higher="" reactor="" pressure="" as="" discussed="" in="" sections="" 4.2="" and="" 3.8="" of="" nedc-32405p="" and="" in="" reference="" 2.="" therefore,="" these="" changes="" will="" ensure="" that="" power="" uprate="" operation="" will="" not="" cause="" a="" significant="" increase="" in="" the="" probability="" or="" consequences="" of="" an="" accident="" previously="" evaluated.="" j.="" bases="" changes="" several="" changes="" to="" the="" hatch="" units="" 1="" and="" 2="" technical="" specifications="" bases="" are="" proposed="" for="" consistency="" with="" the="" power="" uprate="" safety="" analyses.="" these="" proposed="" changes="" are="" in="" addition="" to="" the="" bases="" changes="" corresponding="" to="" proposed="" changes="" a="" through="" i.="" i.="" the="" main="" steam="" line="" flow="" differential="" pressure="" setpoints="" (bases="" section="" b="" 3.3.6.1.c)="" and="" the="" hpci/rcic="" high="" flow="" differential="" pressure="" setpoints="" (bases="" section="" b="" 3.3.6.3.a="" and="" b="" 3.3.6.4.a)="" are="" changed="" for="" both="" units.="" the="" allowable="" values="" (in="" percent="" of="" rated)="" will="" not="" change="" for="" power="" uprate="" operation.="" however,="" the="" actual="" differential="" pressure="" will="" change="" due="" to="" the="" increase="" in="" steam="" flow="" and="" pressure.="" ii.="" the="" hpci="" and="" rcic="" upper="" design="" pressure="" in="" bases="" sections="" b="" 3.5.1="" and="" b="" 3.5.3,="" respectively,="" is="" increased="" 34="" psi="" for="" both="" units="" the="" bases="" changes="" support="" the="" design="" of="" these="" high="" pressure="" systems="" to="" pump="" rated="" flow="" from="" approximately="" 150="" psig="" up="" to="" a="" pressure="" associated="" with="" the="" first="" group="" of="" srv="" setpoints.="" this="" proposed="" design="" pressure="" conservatively="" considers="" the="" 30="" psi="" higher="" nominal="" setpoints="" and="" 3="" percent="" setpoint="" drift.="" the="" capability="" of="" the="" hpci="" and="" rcic="" systems="" to="" deliver="" design="" flows="" at="" these="" pressures="" is="" discussed="" in="" reference="" 2,="" and="" was="" reviewed="" by="" ge="" for="" the="" unit="" 1="" and="" unit="" 2="" systems.="" note="" that="" the="" upper="" design="" pressure="" for="" hpci="" and="" rcic="" is="" different="" from="" the="" surveillance="" test="" pressure="" for="" hpci="" and="" rcic="" discussed="" previously="" in="" item="" i.="" the="" maximum="" surveillance="" test="" pressure="" corresponds="" to="" reactor="" operating="" pressure,="" since="" the="" surveillance="" test="" is="" performed="" when="" the="" unit="" is="" operating.="" the="" hpci="" and="" rcic="" upper="" design="" pressure="" reflects="" the="" capability="" to="" inject="" water="" to="" the="" vessel="" following="" a="" reactor="" scram="" and="" isolation.="" iii.="" the="" peak="" post="" accident="" containment="" pressure="">a) is 
    changed to 49.6 psig (Unit 1) and 45.5 psig (Unit 2). These values 
    appear in Bases Sections B 3.6.1.1, B 3.6.1.2, and B 3.6.1.4 in each 
    unit's Technical Specifications.
        Section 4.1.1.3 of NEDC-32405P discusses the peak short-term 
    containment pressure response which was recalculated for power 
    uprate conditions. Containment pressure and temperatures remain 
    below design limits and are essentially unchanged.
        iv. The main condenser offgas gross gamma activity rate limit of 
    240 mci/second will not be changed for power uprate. A statement 
    that the current limit is conservative for power uprate conditions 
    was added to Bases Section 3.7.6 for both units.
        The Bases derive the current 240 mci/second limit using a rated 
    core thermal power limit of 2436 MWt. A slightly higher limit could 
    be justified using the uprated power level. However, adequate margin 
    exists with the current limit.
        v. The inservice hydrostatic and leak testing pressures shown in 
    Bases Section 3.10.1 are increased 33 psi and 30 psi, respectively. 
    This change affects each unit's Bases.
        This change is a direct result of the 30 psi increase in normal 
    operating pressure proposed for power uprate. The leakage test is 
    normally performed at operating pressure and the hydrostatic test at 
    approximately 110 percent of operating pressure.
        The above Bases changes Items i-v have been evaluated and will 
    not increase the probability or consequences of an accident 
    previously evaluated.
        2. Will the changes create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
    
    Evaluation
    
        The Operating License changes in power level and the associated 
    Technical Specifications changes discussed previously will not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated, as summarized below.
        Equipment that could be affected by power uprate was evaluated. 
    No new operating mode, safety-related equipment lineup, accident 
    scenario, or equipment failure mode were identified. The full 
    spectrum of accident considerations defined in RG 1.70 was 
    evaluated, and no new or different kind of accident was identified. 
    Uprate uses already-developed technology and applies it within the 
    capabilities of existing plant equipment in accordance with 
    presently existing regulatory criteria to include NRC-approved 
    codes, standards, and methods. GE has designed BWRs of higher power 
    levels than the uprated power of any of the currently operating BWR 
    fleet, and no new power dependent accidents have been identified.
        The Technical Specifications changes required to implement power 
    uprate require only minor modifications to the plant's 
    configuration. All changes were evaluated and found to be 
    acceptable.
        3. Will the changes involve a significant reduction in the 
    margin of safety?
        A. Rated Thermal Power is increased to 2558 MWt on page 3 of the 
    Unit 1 Operating License, page 4 of the Unit 2 Operating License, 
    and in Section 1.1 (Definitions) of the Unit 1 and Unit 2 Technical 
    Specifications.
    
    Evaluation
    
        The events analyzed in the FSAR were re-evaluated to demonstrate 
    that power uprate can be implemented without exceeding any 
    regulatory limit. Because the applicable safety analysis criteria 
    and limits are satisfied for power uprate, the margin of safety 
    associated with the safety limits and other limits identified in the 
    Technical Specifications will be maintained.
        As discussed in NEDC-32405P, the safety margins prescribed by 
    the Code of Federal Regulations are maintained by meeting the 
    appropriate regulatory criteria. Similarly, the margins provided by 
    the application of the ASME design criteria are maintained. Section 
    11.4.2 of NEDC-32405P discusses the effects of power uprate on 
    safety margins for the following:
        Fuel thermal limits Design basis accidents and the challenges to 
    fuel, containment, and radiological releases. Transient analyses. 
    Non-LOCA radiological releases. Environmental consequences.
        These evaluations conclude that applicable safety analysis 
    criteria and limits are 
    
    [[Page 35075]]
    satisfied, and thus, the margin of safety will not be significantly 
    reduced.
        B. The surveillance test discharge pressure for the SLC pump at 
    41.2 gpm is increased from 1190 psig to 1201 psig. This value 
    appears in SR 3.1.7.7 and corresponding Bases Section B 3.1.7 in the 
    Unit 1 and Unit 2 Technical Specifications.
    
    Evaluation
    
        Power uprate operation will result in a 30 psi increase in 
    reactor operating pressure. Several pressure-dependent setpoints 
    (including SRV setpoints) will be increased to preserve current 
    margins. Increasing the pressure 11 psi, at which a 41.2 gpm flow 
    rate is developed, assures continued conformance to ATWS criteria at 
    uprated conditions. The surveillance test pressure is based on the 
    maximum pressure for an ATWS event during the time period when the 
    SLC pump is in operation. Section 6.5 of NEDC-32405P discusses the 
    capability of these positive displacement pumps. A small increase in 
    the SRV setpoints will have no effect on the rated injection flow to 
    the reactor.
        For power uprate, the capability of the SLCS to respond with 
    adequate margin to an ATWS event was confirmed. The results are 
    reported in Section 9.3.1 of NEDC-32405P. The limiting ATWS event 
    was an inadvertent MSIV closure. The event was reanalyzed at uprate 
    conditions with the higher SRV setpoints and ATWS-RPT setpoints. 
    Peak vessel pressure was well below the ASME emergency limit of 1500 
    psig. The effect of power uprate on peak clad temperature and 
    maximum suppression pool temperature was judged to be negligible, 
    because the calculations showed no increase in fuel surface heat 
    flux or integrated SRV flow.
        In summary, all ATWS criteria are satisfied and the SLC pumps 
    are capable of injecting the required amounts of sodium pentaborate 
    at uprated conditions. Therefore, there is no significant decrease 
    in the margin of safety.
        C. The reactor vessel steam dome high pressure allowable value 
    for RPS instrumentation is increased 31 psi, consistent with the 
    nominal pressure increase for power uprate. The allowable value 
    appears in Section 3.3.1.1, Table 3.3.1.1-1, Function 3, in the Unit 
    1 and Unit 2 Technical Specifications.
    
    Evaluation
    
        The reactor vessel steam dome high pressure scram limit is 
    increased because the steam dome operating pressure is increased. 
    Operating pressure for uprated power is increased to assure that 
    satisfactory reactor pressure control is maintained. The operating 
    pressure was chosen on the basis of steam line pressure drop 
    characteristics and the steam flow capability of the turbine. 
    Satisfactory reactor pressure control requires an adequate flow 
    margin between the uprated operating condition and the steam flow 
    capability of the turbine control valves at maximum stroke. An 
    operating dome pressure of 1035 psig, which is 30 psi higher than 
    the current operating dome pressure, is expected. Therefore, the 
    high pressure scram is increased approximately the same amount to 
    preserve existing margins to reactor trips.
        The increases in the steam dome high pressure scram instrument 
    setpoints for uprated power were evaluated by determining whether 
    the high pressure scram, which is used as a backup to other scram 
    signals, provides adequate overpressure protection. The evaluation 
    demonstrates that the backup protection function, with the revised 
    setpoints, continues to provide adequate overpressure protection at 
    uprated power conditions by meeting the applicable ASME Code 
    criteria. Therefore, there is no significant decrease in the margin 
    of safety.
        D. The ATWS reactor vessel steam dome high pressure RPT 
    allowable value is raised 80 psi. The allowable value appears in 
    Section 3.3.4.2, SR 3.3.4.2.3, in the Unit 1 and Unit 2 Technical 
    Specifications.
    
    Evaluation
    
        The ATWS-RPT high pressure setpoint initiates a trip of the 
    recirculation pumps, thereby adding negative reactivity following 
    events in which a scram does not (but should) occur. Section 5.1.3.2 
    of NEDC-32405P discusses this function in detail.
        For power uprate, the capability of the SLCS to respond to a 
    postulated ATWS event with adequate margin was confirmed (Section 
    9.3.1 of NEDC-32405P). By reducing reactor power until the SLCS can 
    inject the required amounts of sodium pentoborate to achieve full 
    shutdown, the RPT also reduces suppression pool temperature for 
    isolation cases (also shown to be acceptable for power uprate 
    conditions in Section 9.3.1 of NEDC-32405P). Therefore, there is no 
    significant decrease in a margin of safety.
        E. The LLS SRV arming pressure allowable value is increased 31 
    psi, consistent with the increase in operating pressure and high 
    pressure scram allowable value. The LLS arming pressure allowable 
    value appears in Section 3.3.6.3, Table 3.3.6.3-1, Function 1, in 
    the Unit 1 and Unit 2 Technical Specifications.
    
    Evaluation
    
        The allowable value for the LLS SRV high pressure arming 
    setpoint is increased, because the high pressure scram setpoint is 
    increased. No changes to the LLS arming logic associated with the 
    SRV tailpipe pressure switches, and the LLS opening and closing 
    pressure setpoints are proposed.
        Since this proposed change only affects one of two arming 
    signals for LLS, the safety analyses are not affected; therefore, 
    there is not a significant change in the margin of safety.
        F. Lower the permissible rod line for SLO below 45 percent core 
    flow from the 80 percent rod line to the 76 percent rod line. This 
    Technical Specifications limit appears in Section 3.4.1 (Figure 
    3.4.1-1) and corresponding Bases Section B 3.4.1 of the Unit 1 and 
    Unit 2 Technical Specifications.
    
    Evaluation
    
        This change to the power versus flow map restricted zone is made 
    to maintain the same operating constraints and stability margin that 
    were established for the current power level. This change avoids any 
    increase in the possibility of occurrence or any increase in the 
    potential effects of power oscillations. Therefore, there is no 
    significant decrease in a margin of safety.
        G. The SRV lift setpoints in Surveillance Requirement 3.4.3.1 
    (both units) will be increased 30 psi.
    
    Evaluation
    
        The SRVs are designed to prevent overpressurization of the 
    reactor pressure vessel during abnormal operational transients. The 
    SRV lift setpoints are increased to accommodate the increase in 
    operating pressure that accompanies power uprate. The increase in 
    SRV setpoints ensures that adequate margins are maintained so that 
    the increase in dome pressure during normal operation does not 
    result in an increase in the number of unnecessary SRV actuations. 
    The setpoint increase also maintains the hierarchy of pressure 
    setpoints described in these proposed changes. Transient evaluations 
    include a + 3 percent tolerance to the nominal setpoints. As 
    described in Section 3.2 of NEDC-32405P, peak vessel pressure 
    increases by 3 percent but remains well below the 1375 psig ASME 
    Code limit. Therefore, there is no significant decrease in the 
    margin of safety.
        H. The Limiting Condition for Operation (LCO) and Surveillance 
    Requirements for the maximum reactor steam dome pressure will be 
    increased from 1020 psig to 1058 psig. This requirement appears in 
    LCO 3.4.10, SR 3.4.10.1, and the corresponding Bases in the Unit 1 
    and Unit 2 Technical Specifications.
    
    Evaluation
    
        As discussed in the Technical Specifications Bases and in 
    Section 3.2 of NEDC-32405P, the maximum reactor dome pressure is an 
    initial condition of the vessel overpressure protection analysis, 
    which assumes a fast isolation of all four main steam lines by the 
    main steam isolation valves. It is also used as a sensitivity study 
    parameter for certain transient and LOCA events.
        With this revised limit, peak vessel pressure remains below ASME 
    Code criteria, transient limits are maintained, and LOCA fuel 
    performance satisfies the requirements of 10 CFR 50.46 and 10 CFR 
    50, Appendix K. Therefore, there is no significant decrease in a 
    margin of safety.
        I. The HPCI and RCIC surveillance test pressures in SRs 3.5.1.8 
    and 3.5.3.3, respectively, (both units) are increased 38 psi.
    
    Evaluation
    
        The allowable HPCI and RCIC surveillance test pressure is 
    increased to correspond with the increase in normal reactor 
    operating pressure and LCO/SR on maximum reactor pressure that 
    accompanies power uprate. (As discussed previously, the LCO on 
    reactor steam dome pressure is increased 38 psi.)
        The purpose of the HPCI and RCIC surveillance test is to provide 
    periodic demonstration of the systems' ability to perform consistent 
    with the requirements of the analyses at the higher operating 
    pressure associated with power uprate conditions. An evaluation of 
    the HPCI and RCIC systems confirmed their ability to operate at 
    slightly higher turbine speed and provide design flow 
    
    [[Page 35076]]
    at power uprate conditions. System performance will be confirmed during 
    the initial power ascension to uprated conditions (and periodically 
    thereafter per the Technical Specifications). Therefore, there is no 
    significant decrease in the margin of safety.
    
    J. Bases Changes
    
        Several changes to the Hatch Units 1 and 2 Technical 
    Specifications Bases are proposed for consistency with the power 
    uprate safety analyses. These proposed changes are in addition to 
    the Bases changes corresponding to proposed changes A through I.
        i. The main steam line flow differential pressure setpoints, as 
    shown in Bases Section B 3.3.6.1.c, and the HPCI/RCIC high flow 
    differential pressure setpoints (Units 1 and 2 Bases Sections B 
    3.3.6.3.a and B 3.3.6.4.a) are changed.
        The allowable values (in percent of rated) will not change for 
    power uprate operation. However, the actual differential pressure 
    will change due to the increase in steam flow and pressure.
        ii. The HPCI and RCIC upper design pressure in Units 1 and 2 
    Bases Sections B 3.5.1 and B 3.5.3, respectively, is increased 34 
    psi.
        The Bases changes support the design of these high pressure 
    systems to pump rated flow from approximately 150 psig up to a 
    pressure associated with the first group of SRV setpoints. This 
    proposed design pressure conservatively considers the 30 psi higher 
    nominal setpoints and 3 percent setpoint drift. The capability of 
    the Unit 1 and Unit 2 HPCI and RCIC systems to deliver design flows 
    at these pressures was reviewed by GE and is discussed in Reference 
    2.
        iii. The peak post accident containment pressure (Pa) is 
    changed to 49.6 psig (Unit 1) and 45.5 psig (Unit 2). These values 
    appear in Units 1 and 2 Bases Sections B 3.6.1.1, B 3.6.1.2, and B 
    3.6.1.4.
        Section 4.1.1.3 of NEDC-32405P discusses the peak short-term 
    containment pressure response which was recalculated for power 
    uprate conditions. Containment pressure and temperatures remain 
    below design limits and are essentially unchanged.
        iv. The main condenser offgas gross gamma activity rate limit of 
    240 mci/second will not be changed for power uprate. A statement 
    that the current limit is conservative for power uprate conditions 
    was added to Units 1 and 2 Bases Section 3.7.6.
        The Bases derive the current 240 mci/second limit using a rated 
    core thermal power limit of 2436 MWt. A slightly higher limit could 
    be justified using the uprated power level. However, adequate margin 
    exists with the current limit.
        v. The inservice hydrostatic and leak testing pressures shown in 
    Units 1 and 2 Bases Section 3.10.1 are increased 33 psi and 30 psi, 
    respectively.
        This change is a direct result of the 30 psi increase in normal 
    operating pressure proposed for power uprate. The leakage test is 
    normally performed at operating pressure and the hydrostatic test at 
    approximately 110 percent of operating pressure.
        The above Bases changes i-v were evaluated, and there is no 
    significant decrease in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC 
    20037.
        NRC Project Director: Herbert N. Berkow.
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric 
    Authority of Georgia, City of Dalton, Georgia, Docket No. 50-366, Edwin 
    I. Hatch Nuclear Plant, Unit 2, Appling County, Georgia
    
        Date of amendment request: April 14, 1995.
        Description of amendment request: The licensee proposes to revise 
    Plant Hatch Unit 2 Technical Specifications (TS) to eliminate selected 
    response time testing requirements from the TS. Specifically, the 
    response time testing to be eliminated includes sensors and specified 
    loop instrumentation for: (1) the Reactor Protection System, (2) the 
    Isolation System, and (3) the Emergency Core Cooling System (ECCS). The 
    deletion of instrumentation from the ECCS response time testing 
    necessitates moving the remaining portion of the test to the ECCS 
    system TS. In addition, the Note for Surveillance Requirement 
    3.3.6.1.7, which reads: ``Radiation detectors may be excluded,'' is 
    being removed since response time testing is not required for any 
    radiation detector that provides a primary containment isolation signal 
    as indicated in Table 3.3.6.1-1.
        Proposed TS Changes 1, 2, and 3 are supported by an analysis 
    performed by the BWR Owners' Group (BWROG), with the licensee's 
    participation. The analysis was submitted to the NRC for approval as 
    Topical Report NEDO-32291, ``System Analyses for the Elimination of 
    Selected Response Time Testing Requirements,'' Boiling Water Reactor 
    Owners' Group, January 1994. The NRC approved the Topical Report by a 
    Safety Evaluation Report (SER) issued on December 28, 1994, 
    ``Evaluation of Boiling Water Reactor Owners' Group Topical Report 
    NEDO-32291, System Analyses for the Elimination of Selected Response 
    Time Testing Requirements.'' The BWROG analysis demonstrates that other 
    periodic tests required by TS, such as channel calibrations, channel 
    checks, channel functional tests, and logic system functional tests, 
    ensure that instrument response times are within acceptable limits. The 
    applicability of the referenced analysis to Plant Hatch has been 
    verified. Proposed Change 4 removes an unnecessary note, since no 
    functions subject to this surveillance include radiation monitors.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
    Basis for Proposed Changes 1, 2, and 3
    
        1. The changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. The 
    purpose of the proposed changes is to eliminate response time 
    testing requirements for selected instrumentation in the RPS 
    [Reactor Protection System], Isolation System], and ECCS. However, 
    because of the continued application of other existing Technical 
    Specifications requirements, such as channel calibrations, channel 
    checks, channel functional tests, and logic system functional tests, 
    the response time of these systems will be maintained within the 
    acceptance limits assumed in plant safety analyses. This will assure 
    successful mitigation of an initiating event. The proposed Technical 
    Specifications changes do not affect the capability of the 
    associated systems to perform their intended function within their 
    required response time.
        The BWR Owners' Group (BWROG) has documented an evaluation in 
    NEDO-32291, ``System Analyses for Elimination of Selected Response 
    Time Testing Requirements,'' which was submitted to the NRC for 
    review and approval as a Topical Report in January 1994 and 
    subsequently approved by an NRC SER in December 1994. This 
    evaluation demonstrates that response time testing is redundant to 
    the other Technical Specifications requirements listed in the 
    preceding paragraph. These other tests are sufficient to identify 
    failure modes or degradation in instrument response time and ensure 
    operation of the associated systems within acceptance limits. There 
    are no known failure modes that can be detected by response time 
    testing that cannot also be detected by the other Technical 
    Specifications tests.
        2. The proposed changes will not create the possibility of a new 
    or different kind of accident from any accident previously analyzed. 
    As discussed above, the proposed Technical Specifications changes do 
    not affect the capability of the associated systems to perform their 
    intended function within the acceptance limits assumed in plant 
    safety analyses.
        3. The proposed changes do not involve a significant reduction 
    in the margin of safety. The current Technical Specifications 
    response times are based on the maximum allowable values assumed in 
    the plant safety 
    
    [[Page 35077]]
    analyses, which conservatively establish the margin of safety. As 
    described above, the proposed Technical Specifications changes do 
    not affect the capability of the associated systems to perform their 
    intended function within the allowed response time used as the basis 
    for the plant safety analyses. Plant and system responses to an 
    initiating event will remain in compliance with the assumptions of 
    the safety analyses; therefore, the margin of safety is not 
    affected.
        Although not explicitly evaluated, the proposed Technical 
    Specifications changes enhance plant safety and operation by:
        a. Reducing the time safety systems are unavailable,
        b. Reducing safety system actuations,
        c. Reducing shutdown risk,
        d. Limiting radiation exposure to plant personnel, and
        e. Eliminating the diversion of key personnel to conduct 
    unnecessary testing.
    Basis for Proposed Change 4
    
        1. The change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. The 
    Note for SR 3.3.6.1.7 indicates that response time testing for 
    radiation detectors that provide primary containment isolation 
    signals as indicated in Table 3.3.6.1-1 is not required. However,
        Table 3.3.6.1-1 does not reference SR 3.3.5.1.7 for any 
    radiation detector that provides primary containment isolation 
    signals. The proposed change eliminates the potential for confusion 
    during instrumentation surveillance testing. Deletion of the note 
    will not prevent the radiation detectors from performing their 
    intended function and will not affect the results of any accident 
    analysis.
        2. The proposed changes will not create the possibility of a new 
    or different kind of accident from any accident previously analyzed. 
    As discussed above, the proposed Technical Specifications change 
    eliminates the potential for confusion during instrumentation 
    surveillance testing. This change does not modify any plant 
    equipment or change any plant procedure that provides instructions 
    for the operation of plant equipment. Therefore, the proposed change 
    will not create the possibility of a new or different kind of 
    accident from any previously analyzed.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety. The Note that is being deleted by the 
    change states that testing is not required for instrument sensors 
    which is not required by the SR. Therefore, the Note is superfluous 
    and could cause confusion during instrumentation surveillance 
    testing. The proposed change eliminates that potential. This change 
    is conservative, since it deletes a statement that was intended to 
    reduce the amount of surveillance testing performed on certain 
    instrumentation. The proposed change does not affect plant 
    equipment, procedures, or radiation release prevention and 
    mitigating functions. Therefore, the proposed change does not 
    involve a significant reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513.
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric 
    Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50-424 and 
    50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County, 
    Georgia
    
        Date of amendment request: March 17, 1995.
        Description of amendment request: The amendments would revise 
    Technical Specification (TS) 3.9.4, Containment Building Penetrations, 
    to allow the personnel airlock to be open during core alterations or 
    movement of irradiated fuel within the containment.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change to the Technical Specifications does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated. The proposed change to 
    Specification 3.9.4 would allow the containment personnel airlock 
    (PAL) to be open during fuel movement and core alterations. The PAL 
    is currently closed during fuel movement and core alterations to 
    prevent the escape of radioactive material in the event of a fuel 
    handling accident. The PAL is not an initiator to any accident. 
    Whether the PAL doors are opened or closed during fuel movement or 
    core alterations has no effect on the probability of any accident 
    previously evaluated.
        Allowing the PAL doors to be open during fuel movement and core 
    alterations does increase the consequences of a fuel handling 
    accident in the containment from essentially no offsite dose release 
    to an estimated release of 65.6 rem to the thyroid and 0.28 rem to 
    the whole body. However, the calculated offsite dose release is 
    lower than the case analyzed in the FSAR [Final Safety Analysis 
    Report] for an accident in the Spent Fuel Pool, with no filtration 
    of the resulting release. In addition, the calculated doses are 
    larger than the expected doses because the calculation does not 
    incorporate the closing of the PAL door after the containment is 
    evacuated. Closing the airlock door within 15 minutes results in a 
    calculated offsite dose of 8.2 rem to the thyroid and 0.025 rem 
    whole body. The projected dose to control room operators was 
    reviewed and the projected dose remained below SRP acceptance limits 
    as long as control room emergency ventilation was established within 
    7 minutes. It was assumed the individual assigned to close the 
    airlock doors remained stationed at the airlock for 15 minutes. A 
    best estimate dose analysis indicated this individual could be 
    expected to receive 5.6 rem to the thyroid and 0.15 rem whole body. 
    The proposed change will significantly reduce the dose to other 
    workers in the containment in the event of a fuel handling accident 
    by speeding the containment evacuation process. The proposed change 
    will also significantly decrease the wear on the PAL doors and, 
    consequently, increase the availability of the PAL doors in the 
    event of an accident.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change to the Technical Specifications does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated because the proposed change 
    affects a previously evaluated accident, e.g., a fuel handling 
    accident. It does not represent a significant change in the 
    configuration or operation of the plant and, therefore, does not 
    create the possibility of a new or different type of accident from 
    any accident previously evaluated.
        3. The proposed change to the Technical Specifications does not 
    involve a significant reduction in a margin of safety. The margin of 
    safety as defined by 10 CFR Part 100 for a fission product release 
    is 300 rem thyroid and 25 rem whole body for an individual exposed 
    at the site boundary for two hours. The analysis shows values that 
    are well below the acceptance limits. In fact, the margin remains 
    essentially the same as previously evaluated by the NRC. There is no 
    increase in calculated offsite dose resulting from a fuel handling 
    accident. Therefore, the proposed change does not involve a 
    significant reduction in a margin of safety.
        Based upon the preceding information, it has been determined 
    that the proposed Technical Specifications addition does not involve 
    a significant hazards consideration as defined by 10 CFR 50.92.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Burke County Public Library, 
    412 Fourth Street, Waynesboro, Georgia 30830.
        Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders, 
    NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta, 
    Georgia 30308.
        NRC Project Director: Herbert N. Berkow.
    
    [[Page 35078]]
    
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric 
    Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50-424 and 
    50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County, 
    Georgia
    
        Date of amendment request: May 12, 1995.
        Description of amendment request: The proposed amendments would 
    revise the Technical Specifications (TS) to support a one-time 
    exemption from the requirement of Section III.D.1(a) of 10 CFR Part 50, 
    Appendix J, and any other future Appendix J exemptions that may be 
    approved by the NRC for Vogtle, Unit 1. Specifically, the TS change 
    would insert the words ``Except as modified by NRC approved 
    exemptions'' at the beginning of the first sentence of TS Surveillance 
    Requirement 4.6.1.2.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. The 
    proposed change does not involve a change to structures, systems, or 
    components which would affect the probability of an accident 
    previously evaluated in the Vogtle Electric Generating Plant (VEGP) 
    Final Safety Analysis Report (FSAR). The change only provides a 
    mechanism for implementing exemptions to 10 CFR 50, Appendix J 
    containment leak rate testing criteria which have been approved by 
    the NRC.
        2. The proposed change will not create the possibility of a new 
    or different kind of accident from any accident previously analyzed. 
    The amendment would not change the design, configuration, or method 
    of plant operation. It only allows exemption to specific 10 CFR 50, 
    Appendix J criteria as previously approved by the NRC.
        3. Operation of VEGP, Unit 1 in accordance with the proposed 
    change will not involve a significant reduction in the margin of 
    safety. The proposed change would not, in itself, change a safety 
    limit, an LCO, or a surveillance requirement on equipment required 
    for plant operation. Before the change could be used an exemption to 
    10 CFR 50, Appendix J would have to be evaluated and approved by the 
    NRC. The change only provides a way to implement NRC approved 
    exemptions without violating the Technical Specifications.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Burke County Public Library, 
    412 Fourth Street, Waynesboro, Georgia 30830.
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile Island 
    Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of amendment request: June 1, 1995.
        Description of amendment request: The proposed license amendment 
    would revise the Technical Specifications (T.S.) for Three Mile Island 
    Nuclear Station, Unit 1 (TMI-1) to delete the remaining portions of the 
    TMI-1 Radiological Effluent Technical Specifications (RETS) and 
    relocate them in accordance with the guidance contained in the Generic 
    Letter 89-01 (GL 89-01) and NUREG-1430. The proposed change would also 
    modify the Radiation Monitoring Systems surveillance requirements to 
    specify only those radiation monitors that have Limiting Conditions for 
    Operation (LCO), and revise some of the calibration frequencies.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
    
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability of occurrence or the consequences of an accident 
    previously evaluated. The proposed amendment allows relocation of 
    the remaining RETS to the ODCM [Offsite Dose Calculation Manual] 
    according to the guidance contained in GL 89-01 and NUREG-1430. This 
    proposal simplifies the RETS, meets the regulatory requirements for 
    radioactive effluent controls and radiological environmental 
    monitoring, and is provided as a line-item improvement of the T.S.
        In addition, this proposed amendment specifies surveillance 
    requirements only for those radiation monitors that have an LCO or 
    specified operability requirements. The radiation monitors that are 
    currently included in the T.S. surveillance program but have no 
    associated LCO or specified operability requirement will be placed 
    in the PM [preventive maintenance] program.
        Finally, the proposed amendment extends the interval between 
    successive calibration surveillances for those radiation monitors 
    evaluated herein. This change does not involve any change to the 
    actual surveillance requirements, nor does it involve any change to 
    the limits or restrictions on plant operations. The reliability of 
    systems and components relied upon to prevent or mitigate the 
    consequences of accidents previously evaluated is not degraded 
    beyond that obtained from the currently defined quarterly interval. 
    Assurance of system and equipment availability is maintained.
        This change does not involve any change to system or equipment 
    configuration. Therefore, this change does not significantly 
    increase the probability of occurrence or the consequences of an 
    accident previously evaluated.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposal in part relocates procedural details, currently 
    included in the T.S., on radioactive effluents to the ODCM. Future 
    changes to these procedural details in the ODCM will be handled 
    under the administrative controls for changes to the ODCM.
        In addition, this proposed amendment specifies surveillance 
    requirements only for those radiation monitors that have an LCO or 
    specified operability requirements. The radiation monitors that are 
    currently included in the T.S. surveillance program but have no 
    associated LCO or specified operability requirement will be placed 
    in the PM program.
        Finally, the proposed amendment extends the interval between 
    successive calibration surveillances for those radiation monitors 
    evaluated herein. This change does not involve any change to the 
    actual surveillance requirements, nor does it involve any change to 
    the limits and restrictions on plant operations. This change does 
    not involve any change to system or equipment configuration.
        Therefore, this change is unrelated to the possibility of 
    creating a new or different kind of accident from any previously 
    evaluated.
        3. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        The procedural details being relocated to the ODCM are 
    consistent with the guidance provided in GL 89-01 and NUREG-1430.
        In addition, this proposed amendment specifies surveillance 
    requirements only for those radiation monitors that have an LCO or 
    specified operability requirements. The radiation monitors that are 
    currently included in the T.S. surveillance program but have no 
    associated LCO or specified operability requirement will be placed 
    in the PM program.
        Finally, the proposed amendment extends the interval between 
    successive calibration surveillances for those radiation monitors 
    evaluated herein. This change does not involve any change to the 
    actual surveillance requirements, nor does it involve any change to 
    the limits and restrictions on plant operations. The reliability of 
    the radiation monitors is not significantly degraded beyond that 
    obtained from the currently defined surveillance interval. Assurance 
    of system availability is maintained.
        Therefore, it is concluded that operation of the facility in 
    accordance with the proposed amendment does not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this 
    
    [[Page 35079]]
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Law/Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Phillip F. McKee.
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, Unit 
    1, West Feliciana Parish, Louisiana
    
        Date of amendment request: May 30, 1995.
        Description of amendment request: The proposed amendment would 
    revise the technical specifications (TS) to increase the surveillance 
    test period for the containment integrated leak rate test (ILRT) from 
    40 plus or minus 10 months to every 10 years based on past performance. 
    The change would also require testing on a more frequent basis if any 
    test failures were to occur and to return to the 10 year period with 
    subsequent performance improvements.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) The proposed change does not involve a change to the plant 
    design or operation. As a result, the proposed change does not 
    affect any of the parameters or conditions that contribute to 
    initiation of any accidents previously evaluated. Thus, the proposed 
    change cannot increase the probability of any accident previously 
    evaluated. The proposed change potentially affects the leak tight 
    integrity of the containment structure designed to mitigate the 
    consequences of a loss of coolant accident (LOCA). The function of 
    the containment is to maintain functional integrity during and 
    following the peak transient pressures and temperatures which result 
    from any loss of coolant accident (LOCA). The containment is 
    designed to limit fission product leakage following the design basis 
    LOCA and analyses demonstrate that these offsite doses are less than 
    those allowed under 10CFR100 design limits of 15 psig and 185 
    deg.F. Because the proposed change does not alter the plant design, 
    only the frequency of measuring containment leakage, the proposed 
    change does not directly result in an increase in containment 
    leakage. However, decreasing the test frequency can increase the 
    probability that a large increase in containment leakage could go 
    undetected for an extended period of time. These leakage paths 
    include potential cracks in the containment structure and various 
    penetrations through the containment structure. Based upon the 
    results of the structural integrity test conducted as part of the 
    preoperational or preservice test program and the periodic 
    containment and drywell structural integrity surveillance tests, 
    additional cracking of the containment is not expected during the 
    remaining life to the plant. Ventilation and piping penetrations are 
    designed with two isolation valves in series with one valve in the 
    drywell and another either outside primary containment or in the 
    wetwell. High energy lines that extend into the wetwell, such as the 
    Main Steam and Feedwater lines, are encapsulated by guard pipes to 
    direct energy to the drywell in case of a piping rupture.
        Electrical penetrations are sealed with a high strength/density 
    material that will prevent leakage as well as provide radiation 
    shielding. The TS ILRT acceptance criterion of 0.75 La [maximum 
    allowable leakage rate at the calculated maximum accident pressure, 
    Pa] provides margin for degradation. Containment performance 
    data to date suggests that containment degradation, even during a 
    ten (10) year interval between tests, will not exceed this margin.
        Based on the above, EOI [Entergy Operations, Inc.] has concluded 
    that the proposed change will not result in a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        (2) The proposed change does not involve a change to the plant 
    design or operation. As a result, the proposed change does not 
    affect any of the parameters or conditions that could contribute to 
    initiation of any accidents. This change involves the reduction in 
    the Integrated Leak Rate Test frequency. The method of performing 
    the test is not changed. No new accident modes are created by 
    extending the testing intervals. No safety-related equipment or 
    safety functions are altered as a result of this change. Extending 
    the test frequency has no influence on, nor does it contribute to, 
    the possibility of a new or different kind of accident or 
    malfunction from those previously analyzed. Based upon the above, 
    EOI has concluded that the proposed change will not create the 
    possibility or a new or different kind of accident previously 
    evaluated.
        (3) The proposed change only affects the frequency of measuring 
    containment leakage and does not change the leakage rate limit. 
    However, the proposed change can increase the probability that a 
    large increase in containment leakage could go undetected for an 
    extended period of time. Operational experience has shown that the 
    leak tightness of the containment has been maintained significantly 
    below the allowable leakage limit. In fact, an analysis was 
    conducted to determine the potential risk to the public from the 
    proposed change. Based on this analysis, under several different 
    accident scenarios, the risk of radioactivity release from 
    containment was found to be negligible.
        The margin of safety that has the potential of being impacted by 
    the proposed change involves the offsite dose consequences of 
    postulated accidents which are directly related to containment 
    leakage rate. The containment isolation system is designed to limit 
    leakage to La which is defined by the RBS Technical 
    Specifications to be 0.26 percent by weight of the containment air 
    per 24 hours at 7.6 psig (Pa). The limitation on containment 
    leakage rate is designed to ensure that total leakage volume will 
    not exceed the value assumed in the accident analyses at the peak 
    accident pressure (Pa) or 7.6 psig.
        To provide additional conservatism, the measured overall 
    integrated leakage rate is further limited to less than or equal to 
    0.75 La during performance of the periodic Integrated Leak Rate 
    Test and to less than or equal to 0.60 La (total combined 
    leakage) for Type B and C leak rate tests. This is done to account 
    for the possible degradation of the containment leakage barriers 
    between tests. These acceptance criteria ensure that an acceptable 
    margin of safety is being maintained and will not be altered by the 
    proposed change. The preservation of this margin will continue to 
    provide for potential degradation of the leakage barriers between 
    tests. RBS [River Bend Station] presently has on docket with the 
    staff a submittal (reference RBG-41133, Rev. 1 to LAR 93-14 dated 
    January 18, 1995) that allows the acceptance criteria, between 
    required leakage rate tests, to be less than or equal to 1.0 La 
    since at less than or equal to 1.0 La, the offsite does 
    consequences are bounded by the assumptions of safety analysis.
        No change in the method of testing is being proposed. The Type A 
    test will continue to be done at full pressure (Pa) or greater. 
    Primary containment penetrations which require Type B or C leak 
    tests will be performed in the same manner as before. Other programs 
    are in place to ensure that proper maintenance and repairs are 
    performed during the service life of the primary containment and 
    systems and components penetrating the primary containment.
        No change in the RBS allowable leakage rate is being proposed. 
    These conservative leakage rates ensure that the containment leakage 
    remains low. As a result, EOI has concluded that the proposed change 
    will not result in a significant reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803.
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    
    [[Page 35080]]
        1400 L Street, N.W., Washington, DC 20005.
        NRC Project Director: William D. Beckner.
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, Unit 
    1, West Feliciana Parish, Louisiana
    
        Date of amendment request: May 30, 1995.
        Description of amendment request: The proposed amendment would 
    revise the technical specifications (TS) to increase the time period 
    for drywell leakage tests from eighteen months to five years based on 
    performance. The new surveillance requirements would also reduce the 
    time period if any failures occur and limit subsequent periods until 
    drywell leakage test performance again improves.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) The proposed change does not involve a change to the plant 
    design or operation. As a result, the proposed change does not 
    affect any of the parameters or conditions that contribute to 
    initiation of any accidents previously evaluated. Thus, the proposed 
    change cannot increase the probability of any accident previously 
    evaluated.
        The proposed change potentially affects the leak tight integrity 
    of the drywell, a structure used to mitigate the consequences of a 
    loss of coolant accident (LOCA). The function of the drywell is to 
    channel the steam released from a LOCA through the suppression pool, 
    limiting the amount of steam released to the primary containment 
    atmosphere. This limits the containment pressurizations due to the 
    LOCA. The leakage of the drywell is limited to ensure that the 
    primary containment does not exceed its design limits of 185 deg.F 
    and 15 psig. Because the proposed change does not alter the plant 
    design, only the frequency of measuring the drywell leakage, the 
    proposed change does not directly result in an increase in drywell 
    leakage. However, decreasing the test frequency can increase the 
    probability that a large increase in drywell bypass leakage could go 
    undetected for an extended period of time. There are several 
    potential sources of steam bypass leakage paths. These include 
    potential cracks in the drywell concrete structure and various 
    penetrations through the drywell structure. Based upon the results 
    of the structural integrity test conducted as part of the 
    preoperational or preservice test program, additional cracking of 
    the drywell is not expected during the remaining life of the plant. 
    Ventilation and piping penetrations are designed with two isolation 
    valves in series with one valve in the drywell and another either 
    outside primary containment or in the wetwell. High energy lines 
    that extend into the wetwell, such as the Main Steam line and 
    Feedwater lines, are encapsulated by guard pipe to direct energy to 
    the drywell in case of a piping rupture. Electrical penetrations are 
    sealed with a high strength/density material that will prevent 
    leakage as well a provide radiation shielding. The TS DBLRT [Drywell 
    Bypass Leakage Rate Tests] acceptance criterion of 10% of the design 
    bypass leakage area parameter provides margin for degradation. 
    Drywell performance data to date suggests that drywell degradation, 
    even during a five year interval between tests, will not exceed this 
    margin. RBS presently has on docket with the staff a submittal 
    (reference EOI letter RBG-41133, Rev. 1 to LAR 93-14 dated January 
    18, 1995) that allows the acceptance criteria, between required 
    leakage rate tests, to be (bypass leakage area parameter) since at 
    (bypass leakage area parameter) the containment temperature and 
    pressurization response are bounded by the assumptions of the safety 
    analysis.
        Based on the above, EOI has concluded that the proposed change 
    will not result in a significant increase in the consequences of any 
    accident previously evaluated.
        (2) The proposed change does not involve a change to the plant 
    design or operation. As a result, the proposed change does not 
    affect any of the parameters or conditions that could contribute to 
    initiation of any accidents. Thus, the proposed change cannot create 
    the possibility of an accident not previously evaluated.
        (3) The proposed change only affects the frequency of measuring 
    the drywell bypass leakage rate and does not change the bypass 
    leakage limit for the drywell. However, the proposed change can 
    increase the probability that a large increase in drywell bypass 
    leakage could go undetected for an extended period of time. 
    Operational experience has shown that the leak tightness of the 
    drywell has been maintained significantly below the allowable 
    leakage limits. In fact, an analysis was conducted to determine the 
    potential risk to the public from the proposed change. Based on this 
    analysis, under several different accident scenarios, the risk of 
    radioactivity release from containment was found to be negligible.
        As a result, EOI has concluded that the proposed change will not 
    result in a significant reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803.
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005.
        NRC Project Director: William D. Beckner.
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald 
    C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, Michigan
    
        Date of amendment requests: May 25, 1995 (AEP:NRC:107IT).
        Description of amendment requests: The proposed amendments would 
    implement a cycle- and burnup-dependent peaking factor penalty to the 
    allowable power level. The Technical Specifications would be changed to 
    refer to the Core Operating Limits Report for this burnup-dependent 
    penalty.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Per 10 CFR 50.92, a proposed amendment will not involve a 
    significant hazards consideration if the proposed amendment does 
    not:
        (1) involve a significant increase in the probability or 
    consequences of an accident previously evaluated,
        (2) create the possibility of a new or different kind of 
    accident from any accident previously evaluated, or
        (3) involve a significant reduction in a margin of safety.
    
    Criterion 1
    
        The proposed changes will not involve a significant increase in 
    the probability of an accident previously evaluated because the 
    changes will not result in a change to any of the process variables 
    that might initiate an accident. There are no physical changes to 
    the plant associated with this T/S change. The consequences of an 
    accident previously evaluated will not be increased because the 
    changes increase the penalty applied to FQ when it is measured 
    to be increasing. FQ and allowable power level (APL) T/S 
    surveillance requirements are not being changed. Furthermore, 
    allowing a cycle and burnup dependent FQ penalty to be located 
    in the COLR was accepted by the NRC in a [November 26, 1993] safety 
    evaluation on WCAP-10216-P, Rev. 1 [``Relaxation of Constant Axial 
    Offset Control- FQ Surveillance Technical Specification''].
    
    Criterion 2
    
        The proposed changes will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated 
    because the changes will involve no physical changes to the plant 
    nor any changes in plant operations. Furthermore, the FQ and 
    APL T/S surveillance requirements are not being changed, and the 
    change to the FQ penalty is conservative.
    
    Criterion 3
    
        The proposed amendment[s] will not involve a significant 
    reduction in a margin of safety. When the increased FQ penalty 
    is applied, it reduces the allowable power level, thus increasing 
    the margin of safety.
    
    
    [[Page 35081]]
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        NRC Project Director: Cynthia A. Carpenter, Acting.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald 
    C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, Michigan
    
        Date of amendment requests: May 25, 1995 (AEP:NRC:1124B).
        Description of amendment requests: The proposed amendments would 
    modify the Technical Specifications (TS) to allow fuel reconstitution. 
    The proposed change is a TS line item improvement per NRC Generic 
    Letter 90-02, supplement 1, ``Alternative Requirements for Fuel 
    Assemblies in the Design Features Section of Technical 
    Specifications.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Per 10 CFR 50.92, a proposed change does not involve significant 
    hazards consideration if the change does not:
        1. Involve a significant increase in the probability or 
    consequence of an accident previously evaluated,
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated, or
        3. Involve a significant reduction in a margin of safety.
    
    Criterion 1
    
        The proposed changes only modify the T/Ss such that 
    reconstitution is recognized as acceptable under very limited 
    circumstances. Reconstitution is limited to substitution of 
    zirconium alloy or stainless steel filler rods, and must be in 
    accordance with approved applications of fuel rod configurations. 
    Although these changes permit reconstitution to occur without the 
    need for a specific T/S change, an approved methodology is required 
    prior to its application. Since the changes will allow substitution 
    of filler rods for leaking or potentially leaking rods, the changes 
    may actually reduce the radiological consequences of an accident. It 
    is noted that the specific changes requested in this letter have 
    previously been found acceptable by the NRC in GL 90-02 supplement 
    1. For these reasons, we conclude that the changes will not involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated.
    
    Criterion 2
    
        The proposed changes will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated 
    because they will only affect the assembly configuration and can 
    only be implemented in accordance with an NRC-approved methodology. 
    The other aspects of plant design, operation limitations, and 
    responses to events will remain unchanged. It is noted that the 
    changes have previously been determined acceptable by the NRC in GL 
    90-02 supplement 1.
    
    Criterion 3
    
        The proposed amendment will not involve a significant reduction 
    in a margin of safety because the changes can only be implemented in 
    accordance with an NRC-approved methodology. It is noted that the 
    changes have previously been determined acceptable by the NRC in GL 
    90-02 supplement 1.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        NRC Project Director: Cynthia A. Carpenter, Acting.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald 
    C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, Michigan
    
        Date of amendment requests: May 25, 1995 (AEP:NRC:1200B).
        Description of amendment requests: The proposed amendments would 
    modify the Technical Specifications to change the surveillance 
    frequency of the manual actuation function for main steam line 
    isolation. This change is consistent with the testing requirements for 
    associated valves as specified in the American Society of Mechanical 
    Engineers (ASME) Code Section XI inservice testing program at Cook.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Per 10 CFR 50.92, a proposed change does not involve significant 
    hazards consideration if the change does not:
        1. Involve a significant increase in the probability or 
    consequence of an accident previously evaluated,
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated, or
        3. Involve a significant reduction in a margin of safety.
    
    Criterion 1
    
        This change will reduce the frequency of the surveillance 
    testing on the MSIV [main steamline isolation valve] manual 
    actuation circuitry from monthly to quarterly. Because of the risks 
    involved in testing the dump valves, the reduction in test frequency 
    may reduce the probability of an accidental unit trip and valve seat 
    failure due to repeated cycling. Our review of the surveillance test 
    history has shown that the system is highly reliable, and gives us 
    confidence that the change in test frequency will not endanger 
    public health and safety. Furthermore, the change to a quarterly 
    surveillance interval is consistent with the testing performed for 
    the dump valves per ASME Section XI. For these reasons, it is our 
    belief that the proposed changes do not involve a significant 
    increase in the probability or consequences of a previously 
    evaluated accident.
    
    Criterion 2
    
        The changes will not introduce any new modes of plant operation, 
    nor will any physical changes to the plant be required. Thus, the 
    changes should not create the possibility of a new or different kind 
    of accident from any accident previously analyzed or evaluated.
    
    Criterion 3
    
        This change will reduce the frequency of the surveillance 
    testing on the MSIV manual actuation circuitry from monthly to 
    quarterly. Our review of the surveillance test history has shown 
    that the system is highly reliable, and gives us confidence that the 
    change in test frequency will not endanger public health and safety. 
    Furthermore, the change to quarterly surveillance is consistent with 
    the testing performed for the dump valves per ASME Section XI. For 
    these reasons, it is our belief that the proposed changes do not 
    involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        NRC Project Director: Cynthia A. Carpenter, Acting. 
    
    [[Page 35082]]
    
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald 
    C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, Michigan
    
        Date of amendment requests: May 26, 1995 (AEP:NRC:1210).
        Description of amendment requests: The proposed amendments would 
    modify the Reactor Trip System Instrumentation and Engineered Safety 
    Feature Actuation System Instrumentation sections of the Technical 
    Specifications (TS) to relocate the tables of response time limits to 
    the Updated Final Safety Analysis Report (UFSAR). These changes are a 
    line item improvement of the TS in accordance with NRC Generic Letter 
    93-08, ``Relocation of Technical Specification Tables of Instrument 
    Response Time Limits.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Per 10 CFR 50.92, a proposed amendment will not involve a 
    significant hazards consideration if the proposed amendment does 
    not:
        (1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated,
        (2) Create the possibility of a new or different kind of 
    accident from any accident previously evaluated, or
        (3) Involve a significant reduction in a margin of safety.
    
    Criterion 1
    
        The proposed changes will not involve a significant increase in 
    the probability of an accident previously evaluated because the 
    changes will not result in a change to any of the process variables 
    that might initiate an accident. There are no physical changes to 
    the plant associated with the T/S change. The consequences of an 
    accident previously evaluated will not be increased because the 
    changes simply allow relocation of response time limits to the 
    UFSAR. Time response testing will continue to be required by the T/
    Ss. Any changes to the response time values will be made in 
    accordance with the requirements of 10 CFR 50.59. It is noted that 
    these T/S changes have previously been determined acceptable by the 
    NRC in GL 93-08.
    
    Criterion 2
    
        The proposed changes will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated 
    because the changes will involve no physical changes to the plant 
    nor any changes in plant operations. Time response testing will 
    continue to be required by the T/Ss. Any changes to the time 
    response values will be made in accordance with the requirements of 
    10 CFR 50.59. It is noted that these changes have previously been 
    determined acceptable by the NRC in GL 93-08.
    
    Criterion 3
    
        The proposed amendment will not involve a significant reduction 
    in a margin of safety because time response testing will continue to 
    be required by the T/Ss. Any changes to the response time values 
    will be made in accordance with the requirements of 10 CFR 50.59. It 
    is noted that these changes have previously been determined 
    acceptable by the NRC in GL 93-08.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085.
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        NRC Project Director: Cynthia A. Carpenter, Acting.
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, Seabrook 
    Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: May 30, 1995.
        Description of amendment request: The proposed amendment would 
    change the upper limit for the moderator temperature coefficient (MTC) 
    for certain operating conditions. Specifically, the upper limit 
    specified in Technical Specification 3.1.1.3 for the MTC would be 
    changed to +0.5 x 10-4 delta k/k/ deg.F for all rods out at the 
    beginning of cycle for power levels up to 70% rated thermal power with 
    a linear ramp to 0 delta k/k/ deg.F at 100% rated thermal power. The 
    currently specified upper limit for all operating conditions is 0 delta 
    k/k/ deg.F.
        A paragraph would be added to the Basis to Technical Specification 
    3.1.1.3 providing a commitment to comply with the ATWS Rule and the 
    basis for the Rule by assuring ATWS core damage frequency will remain 
    below the Commission established target of 1.0 x 10-5 per reactor 
    year. The commitment would be implemented by determining a more 
    restrictive, cycle-specific upper MTC limit and placing it in the Core 
    Operating Limits Report (COLR).
        Additionally, a reference for the analytical method used to 
    determine the cycle-specific MTC upper limit would be added to TS 
    6.8.1.6.b.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below.
        A. The changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated (10 CFR 
    50.92(c)(1)). The proposed changes do not affect the manner by which 
    the facility is operated and do not change any facility design feature 
    or equipment which influences the initiation of an accident, therefore, 
    there is no change in the probability of any accident previously 
    analyzed. Each accident or transient, with the exception of the 
    Anticipated Transient Without SCRAM (ATWS), has been analyzed for the 
    proposed changes and has been approved previously by the Commission 
    with the issuance of Amendment 33 (December 6, 1994) to the Facility 
    Operating License. The proposed cycle-specific MTC to be included in 
    the COLR will assure that the consequences of an ATWS will remain 
    bounded by the analysis previously documented. Therefore, the 
    consequences of previously evaluated accidents, including ATWS, will 
    not be significantly increased by the proposed changes.
        B. The changes do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated (10 CFR 
    50.92(c)(2)) because the changes proposed merely involve changes in the 
    upper limits of MTC imposed by the Technical Specifications and COLR. 
    No changes are made to the design or manner of operation of any 
    structure, system or component and no new failure mechanisms are 
    introduced.
        C. The changes do not involve a significant reduction in a margin 
    of safety (10 CFR 50.92(c)(3)). The analyses of each accident or 
    transient previously presented to support the issuance of Amendment 33 
    were performed using the proposed upper MTC limit, and the results 
    demonstrated that the acceptance criteria specified for each event are 
    met. The cycle-specific MTC limit in the COLR will be adjusted to 
    assure that the acceptance criteria for a postulated ATWS event are met 
    thereby preserving the margin of safety.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration. 
    
    [[Page 35083]]
    
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, NH 03833.
        Attorney for licensee: Thomas Dignan, Esquire, Ropes & Gray, One 
    International Place, Boston MA 02110-2624.
        NRC Project Director: Phillip F. McKee.
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun Station, 
    Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: May 31, 1995.
        Description of amendment request: The amendment would provide 
    additional restrictions on the operation of the component cooling water 
    (CCW) system heat exchangers to ensure that the CCW system temperature 
    is maintained within its analyzed design basis.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        In preparation for, and in response to a service water system 
    operational performance self assessment, the heat loads in the 
    Component Cooling Water (CCW) system were reevaluated to determine 
    the peak temperatures on the system and components cooled by the CCW 
    system. It was determined that if all of the containment coolers 
    were operating, the return temperature of the CCW system could 
    exceed the 120 deg.F stated in the Updated Safety Analysis Report 
    (USAR) as the maximum temperature of the system.
        During a Large Break Loss of Coolant Accident (LBLOCA) or a Main 
    Steam Line Break Inside Containment (MSLB/IC), the containment air 
    cooling units and containment air cooling and filtering units will 
    automatically start to remove heat from the containment atmosphere. 
    The heat sink for the containment air coolers is the CCW system. The 
    heat removed from the containment atmosphere is transferred to the 
    Raw Water (RW) system via the component cooling heat exchangers AC-
    1A, B, C, and D. The heat is then ultimately rejected to the 
    Missouri River by the RW system.
        Calculations indicate that the CCW return temperature (i.e., 
    mixed exit temperature) from the component cooling heat exchangers 
    could exceed 160 deg.F after a LBLOCA or MSLB/IC with the present TS 
    minimum requirements for the heat exchangers. Further evaluation 
    indicated that the CCW system (and components cooled by CCW) could 
    withstand temperatures above the 120 deg.F temperature stated in the 
    USAR, but a return temperature above 158 deg.F would require 
    additional evaluation of thermal-induced stresses on the CCW return 
    side pipe supports. In order to maintain the peak CCW return 
    temperature to less than or equal to 158 deg.F, additional 
    restrictions must be placed on the number of component cooling heat 
    exchangers required to be operable.
        The current minimum requirements for component cooling heat 
    exchangers are contained in Technical Specification (TS) 2.3, 
    ``Emergency Core Cooling System,'' and require that three of the 
    four heat exchangers be operable when the plant is in operating 
    Modes 1 and 2. Analyses show that three in service heat exchangers 
    will maintain the CCW temperatures in an analyzed range following a 
    DBA. In order to ensure that three heat exchangers are available, in 
    conjunction with an assumed single failure, four are required to be 
    operable. The proposed change would place additional restrictions on 
    the operation of the CCW heat exchangers by requiring four heat 
    exchangers to be operable in Modes 1 and 2, and if only three are 
    operable then provide 14 days to restore the system to four operable 
    heat exchangers.
        The proposed change does not involve a significant increase in 
    the probability of an accident previously evaluated. The proposed 
    change does not impact systems, structures, or components that are 
    initiators of any analyzed accidents.
        The proposed change does not involve a significant increase in 
    the consequences of an accident previously evaluated. The proposed 
    change ensures that the CCW system and safety-related components 
    cooled by the CCW will perform their safety functions in response to 
    previously evaluated accidents. The proposed change was evaluated 
    utilizing the probabilistic risk analysis model of the FCS 
    Individual Plant Examination. The IPE concluded that the routine 
    testing and maintenance activities, for the RW and CCW systems 
    (e.g., inoperability of components for testing and maintenance) are 
    not significant contributors to severe accident risk.
        Therefore, the proposed change would not increase the 
    probability or consequences of an accident previously evaluated.
        (2) The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change does not create an initiator for a new or 
    different kind of accident from those previously evaluated. The 
    proposed change places additional restrictions on the operation of 
    equipment to ensure that the CCW system and safety-related 
    components cooled by the CCW will perform their safety functions. 
    The additional restrictions were evaluated in combination with 
    existing allowances on RW and CCW pump inoperability, to confirm 
    that the peak CCW return temperature would be in an analyzed range, 
    and will not adversely impact the operability of the CCW system or 
    safety-related components cooled by CCW. These restrictions are 
    valid up to and including a river temperature of 90 deg.F, which is 
    the upper bound currently cited in the USAR.
        Various single active failures were postulated to determine the 
    most limiting failure in conjunction with the maximum heat load from 
    the containment air coolers. It was determined that with the river 
    temperature less than 70  deg.F, a single failure of a RW valve to 
    open on a component cooling heat exchanger would not raise the CCW 
    return temperature to an unanalyzed level, but with the river 
    temperature greater than or equal to 70  deg.F, the CCW return 
    temperature could be at an unanalyzed level. Therefore, it is 
    proposed that when the river temperature is greater than or equal to 
    70  deg.F four heat exchangers have RW in service (i.e., RW valves 
    open). Having RW in service eliminates the potential failure of a RW 
    valve to auto-open as a credible single active failure.
        The proposed change ensures that the CCW system and safety-
    related components cooled by the CCW will perform their safety 
    functions. Therefore, the proposed change does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        (3) The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change provides additional restrictions on the CCW 
    system and ensures that the CCW system will perform its design 
    safety function. These additional restrictions ensure that the CCW 
    system will be capable of removing the maximum heat load from the 
    containment cooling system following a DBA and thereby ensures that 
    the containment pressure remains below its limit as assumed in the 
    USAR. Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102.
        Attorney for licensee: James R. Curtiss, Winston & Strawn, 1400 L 
    Street, N.W., Washington, DC 20005-3502.
        NRC Project Director: William H. Bateman.
    
    Pennsylvania Power and Light Company, Docket No. 50-387, Susquehanna 
    Steam Electric Station, Unit 1, Luzerne County, Pennsylvania
    
        Date of amendment request: May 5, 1995.
        Description of amendment request: This amendment would remove from 
    the Susquehanna Steam Electric Station Unit 2 Technical Specifications, 
    the listing of three residual heat removal (RHR) system valves in Table 
    3.6.3-1, ``Primary Containment Isolation Valves'' These valves are no 
    longer needed to support the steam condensing mode of the RHR system 
    and are being removed from the plant during the Unit 2 seventh 
    
    [[Page 35084]]
    refueling and inspection outage in September of this year.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        With the prior deletion of the steam condensing mode of RHR and 
    the isolation of the high and low pressure interfaces, the three 
    pressure relief valves that are being removed from the plant have no 
    active function. Their passive function of maintaining system or 
    containment integrity will be fulfilled by blind flanges on 
    equilvent. Also, the RHR and RCIC piping are provided with 
    overpressure protection from other pressure relief valves. 
    Therefore, the removal of these pressure relief valves does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The pressure relief valves that are being removed had two 
    primary functions. First, they provided overpressure protection for 
    the RHR and RCIC piping during the steam condensing mode of RHR. 
    Since the steam condensing mode has been deleted from the plant, 
    these valves no longer have that function. Also, overpressure 
    protection of the RHR and RCIC piping is provided by other existing 
    pressure relief valves. Second, these valves maintained system or 
    containment integrity. When the pressure relief valves are removed 
    from the plant, they will be replaced with blind flanges or 
    equivalent that will maintain system or containment integrity. 
    Therefore, the removal of the three pressure relief valves does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        Since the steam condensing mode of RHR has been eliminated, the 
    three pressure relief valves have no active function. Their passive 
    function of maintaining system or containment integrity will be 
    fulfilled by blind flanges or equivalent. Also, overpressure 
    protection of RHR and RCIC piping is provided by other existing 
    pressure relief valves. Therefore, the removal of the three pressure 
    relief valves does not involve a significant reduction in a margin 
    of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701.
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of amendment request: May 19, 1995.
        Description of amendment request: The proposed Technical 
    Specifications (TS) change would revise TS Table 3.3.3-3, ``Emergency 
    Core Cooling System Response Times'' to reflect the value of 60 seconds 
    for the High Pressure Coolant Injection system response time instead of 
    30 seconds as currently specified.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed Technical Specifications (TS) change does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The proposed TS change will increase the High Pressure Coolant 
    Injection (HPCI) system response time from 30 seconds to 60 seconds. 
    The proposed TS change does not involve any physical change in the 
    plant configuration which may cause an accident, or affect safety-
    related equipment performance or cause its failure. There is no 
    increase in the consequences of an accident, because the HPCI 
    response time increase does not affect the licensing basis Peak 
    Cladding Temperature (PCT), which remains below the regulatory limit 
    of 2200  deg.F.
        The Loss of Feedwater Flow (LOFW) event was evaluated for being 
    potentially affected by the increased HPCI system response time. The 
    HPCI system is one of the systems which provides reactor vessel 
    water makeup inventory, and is initiated automatically on a low 
    reactor water level (Level 2) signal. The LOFW analysis shows that 
    Level 1 is not reached and that the top of the active fuel will 
    remain covered throughout the event. Therefore, adequate core 
    cooling will be maintained and no fuel damage will result. The 
    probability of fuel failure will not be increased by this proposed 
    TS change.
        Therefore, the proposed TS change does not involve an increase 
    in the probability or consequences of an accident previously 
    evaluated.
        2. The proposed TS change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed TS change will increase the High Pressure Coolant 
    Injection (HPCI) system response time from 30 seconds to 60 seconds. 
    This proposed change is bounded by the current Emergency Core 
    Cooling System (ECCS)--Loss-of-Coolant Accident (LOCA) analysis for 
    Limerick Generating Station (LGS) Units 1 and 2. The change in HPCI 
    system response time does not involve any physical modifications to 
    the plant systems or equipment, nor does it introduce a new 
    operational/failure mode, which might cause a different type of 
    accident. In case of a Loss of Feedwater Flow (LOFW) event, the HPCI 
    system will operate as designed, maintaining adequate core cooling.
        Therefore, the proposed TS change does not create the 
    possibility of a new or different kind of accident, from any 
    accident previously evaluated.
        3. The proposed TS change does not involve a significant 
    reduction in a margin of safety.
        The following TS Bases were reviewed for potential reduction in 
    the margin of safety:
    
    3/4.5  Emergency Core Cooling System
    2.1.4  Reactor Vessel Water Level
    
        The TS Bases do not discuss the High Pressure Coolant Injection 
    (HPCI) system start time. The margin of safety, as defined in the TS 
    Bases, will remain the same. The proposed TS change is in accordance 
    with the current licensing basis Emergency Core Cooling System 
    (ECCS)--Loss of Coolant Accident (LOCA) analysis for LGS Units 1 and 
    2, and does not impact any safety limits of the plant. The HPCI 
    system will operate as designed during the LOFW event, maintaining 
    adequate core cooling.
        Therefore, the proposed TS change does not involve a reduction 
    in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101.
        NRC Project Director: John F. Stolz.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    
    
    [[Page 35085]]
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 50-
    529, and STN 50-530, Palo Verde Nuclear Generating Station, Units 1, 2, 
    and 3, Maricopa County, Arizona
    
        Date of application for amendments: December 7, 1994.
        Brief description of amendments: These amendments revise the Bases 
    of TS 3/4.7.5, ``Ultimate Heat Sink'' (UHS), to describe the UHS as 
    containing a 26-day supply of cooling water, instead of a 27-day 
    supply. In addition, the reference to Regulatory Guide 1.27 in the 
    bases of this TS would be revised to reference the January 1976 
    revision rather than the March 1974 revision.
        Date of issuance: June 14, 1995.
        Effective date: June 14, 1995.
        Amendment Nos.: Unit 1--Amendment No. 93; Unit 2--Amendment No. 81; 
    Unit 3--Amendment No. 64.
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the associated Bases of the Technical 
    Specifications.
        Date of initial notice in Federal Register: March 1, 1995 (60 FR 
    11127) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 14, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of application for amendment: February 9, 1995.
        Brief description of amendment: This amendment revises the reactor 
    high water level trip level setting for the Group 1 isolation. The 
    change will allow an increase to the main steam isolation valve high 
    water level isolation setpoint.
        Date of issuance: June 15, 1995.
        Effective date: As of the date of issuance to be implemented within 
    90 days.
        Amendment No.: 164.
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 15, 1995 (60 FR 
    14017) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 15, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois
    
    Docket Nos. STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 
    and 2, Will County, Illinois
    
        Date of application for amendments: May 20, 1994, as revised on 
    February 2, 1995, and supplemented December 2, 1994, and March 14, 
    1995.
        Brief description of amendments: The amendments revised the 
    Technical Specifications (TS) as they apply to Byron, Unit 1, and 
    Braidwood, Unit 1, to incorporate an alternative repair criteria for 
    defects found in the portion of the expanded steam generator tubes 
    within the tubesheet.
        Date of issuance: June 22, 1995.
        Effective date: June 22, 1995.
        Amendment Nos.: 72, 72, 63, and 63.
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: July 6, 1994 (59 FR 
    34659) and March 29, 1995 (60 FR 16184). The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    June 22, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois
    
    Docket Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, Units 
    1 and 2, Rock Island County, Illinois
    
        Date of application for amendments: September 15, 1992, as 
    supplemented April 21, 1995.
        Brief description of amendments: This application upgrades the 
    current custom Technical Specifications (TS) for Dresden and Quad 
    Cities to the Standard Technical Specifications contained in NUREG-
    0123, ``Standard Technical Specification General Electric Plants BWR/
    4.'' This application upgrades only Sections 2.0 (Safety Limits and 
    Limiting Safety System Settings), 3/4.11 (Power Distribution Limits), 
    and 3/4.12 (Special Test Exceptions).
        Date of issuance: June 13, 1995.
        Effective date: Immediately, to be implemented no later than 
    December 31, 1995, for Dresden Station and June 30, 1996, for Quad 
    Cities Station.
        Amendment Nos.: 134, 128, 155, and 151.
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29 and DPR-30. 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: May 10, 1995 (60 FR 
    24906) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 13, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: for Dresden, Morris Area 
    Public Library District, 604 Liberty Street, Morris, Illinois 60450; 
    for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon, 
    Illinois 61021. 
    
    [[Page 35086]]
    
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois
    
    Docket Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, Units 
    1 and 2, Rock Island County, Illinois
    
        Date of application for amendments: December 15, 1993, as 
    supplemented April 21, 1995.
        Brief description of amendments: These amendments upgrade the 
    current custom Technical Specifications (TS) for Dresden and Quad 
    Cities to the Standard Technical Specifications contained in NUREG-
    0123, ``Standard Technical Specifications General Electric Plants BWR/
    4.'' These amendments upgrade only Section 5.0 (Design Features). The 
    amendments include the relocation of some requirements from the TS to 
    licensee-controlled documents.
        Date of issuance: June 14, 1995.
        Effective date: Immediately, to be implemented no later than 
    December 31, 1995, for Dresden Station and June 30, 1996, for Quad 
    Cities Station.
        Amendment Nos.: 135, 129, 156, and 152
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29 and DPR-30. 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: May 10, 1995 (60 FR 
    24909) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 14, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: for Dresden, Morris Area 
    Public Library District, 604 Liberty Street, Morris, Illinois 60450; 
    for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon, 
    Illinois 61021.
    
    Consumers Power Company, Docket No. 50-255, Palisades Plant, Van Buren 
    County, Michigan
    
        Date of application for amendment: December 13, 1994, as 
    supplemented May 3, 1995.
        Brief description of amendment: This amendment revises the 
    Technical Specifications to add a high thermal performance (HTP) 
    departure from nucleate boiling correlation to Safety Limit 2.1. The 
    HTP correlation is used for HTP fuel loaded during recent fuel cycles.
        Date of issuance: June 13, 1995.
        Effective date: June 13, 1995.
        Amendment No.: 168.
        Facility Operating License No. DPR-20. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 10, 1995 (60 FR 
    24910) The May 3, 1995, submittal provided clarifying information which 
    was within the scope of the initial application and did not affect the 
    staff's initial proposed no significant hazards considerations 
    findings.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 13, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423.
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, Beaver 
    Valley Power Station, Unit Nos. 1 and 2, Shippingport, Pennsylvania
    
        Date of application for amendments: June 17, 1993, as supplemented 
    October 20, 1993, and May 23, 1995.
        Brief description of amendments: These amendments revise the 
    Appendix A technical specifications (TSs) for Unit 1 and Unit 2 by 
    relocating the requirements of the radiological effluent technical 
    specifications (RETS) and the solid radioactive wastes TSs from the 
    Appendix A TSs to the offsite dose calculation manual (ODCM) or to the 
    process control program (PCP) in accordance with the guidance provided 
    in NRC Generic Letter 89-01 and NRC Report NUREG-1301. Programmatic 
    controls are also being incorporated into the Administrative Controls 
    section of the TSs. Additionally, editorial and definition changes are 
    being made to facilitate the relocation of these requirements.
        Date of issuance: June 12, 1995.
        Effective date: June 12, 1995.
        Amendment Nos.: 188 and 70.
        Facility Operating License Nos. DPR-66 and NPF-73: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 4, 1993 (58 FR 
    41504). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 12, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
    
    Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear One Unit 
    No. 1, Pope County, Arkansas
    
        Date of amendment request: May 15, 1995, as supplemented by letters 
    dated May 19 and June 7, 1995.
        Brief description of amendment: The amendment was processed as an 
    exigent amendment following issuance of a notice of enforcement 
    discretion (NOED) by NRC letter dated May 17, 1995. The NOED and 
    exigent technical specification (TS) amendment authorized the licensee 
    to continue operating the reactor at power while the service water flow 
    to the reactor building emergency coolers is less than the TS 
    surveillance criteria.
        Date of issuance: June 9, 1995.
        Effective date: June 9, 1995.
        Amendment No.: 182.
        Facility Operating License No. DPR-51. Amendment revised the 
    Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration: Yes (60 FR 27144, dated May 22, 1995). The notice 
    provided an opportunity to submit comments on the Commission's proposed 
    no significant hazards consideration determination. No comments have 
    been received. The notice also provided for an opportunity to request a 
    hearing by June 21, 1995, but stated that any such hearing would take 
    place after issuance of the amendment. The Commission's related 
    evaluation of the amendments, finding of exigent circumstances, and 
    final determination of no significant hazards consideration is 
    contained in a Safety Evaluation dated June 9, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam Electric 
    Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: January 27, 1995.
        Brief description of amendment: The amendment changed the Appendix 
    A Technical Specifications by increasing the allowable maximum 
    enrichment for the spent fuel pool and containment temporary storage 
    rack from 4.1 to 4.9 weight percent U-235 when fuel assemblies contain 
    fixed poisons.
        Date of issuance: June 14, 1995.
        Effective date: June 14, 1995.
        Amendment No.: 108.
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 15, 1995 (60 FR 
    14021)
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 14, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, Louisiana 70122.
    
    [[Page 35087]]
    
    
    Florida Power and Light Company, et al., Docket No. 50-389, St. Lucie 
    Plant, Unit No. 2, St. Lucie County, Florida
    
        Date of application for amendment: February 27, 1995.
        Brief description of amendment: This amendment will modify 
    surveillance requirement (SR) 4.9.8.1 and 4.9.8.2 to allow a reduction 
    in the required minimum shutdown cooling flow rate under certain 
    conditions during operational MODE 6. In addition, the format of the SR 
    will be changed to clarify the intent of the stated surveillances.
        Date of Issuance: June 14, 1995.
        Effective Date: June 14, 1995.
        Amendment No.: 76.
        Facility Operating License No. NPF-16: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 29, 1995 (60 FR 
    16187) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 14, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-389, 
    St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
    
        Date of application for amendments: February 22, 1995.
        Brief description of amendments: The proposed changes eliminate 
    reference to an automatic containment air lock tester from technical 
    specification 4.6.1.3. The automatic air lock tester is no longer being 
    used.
        Date of Issuance: June 22, 1995.
        Effective Date: June 22, 1995.
        Amendment Nos.: 137 and 77.
        Facility Operating License Nos. DPR-67 and NPF-16: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 29, 1995 (60 FR 
    16186) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 22, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, Turkey 
    Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: January 17, 1995.
        Brief description of amendments: These amendments concern 
    implementation of Florida Power and Light nuclear physics methodology 
    for calculations of the core operating limits report parameters.
        Date of issuance: June 9, 1995.
        Effective date: June 9, 1995.
        Amendment Nos. 174 and 168.
        Facility Operating Licenses Nos. DPR-31 and DPR-41: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 1, 1995 (60 FR 
    11133) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 9, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal Electric 
    Authority of Georgia, City of Dalton, Georgia, Docket Nos. 50-424 and 
    50-425, Vogtle Electric Generating Plant, Units 1 and 2, Burke County, 
    Georgia
    
        Date of application for amendments: October 3, 1994, as 
    supplemented by letter dated March 1, 1995.
        Brief description of amendments: The amendments revise Technical 
    Specification 3/4.4.9, Pressure/Temperature Limits, and its associated 
    Bases, to provide new reactor coolant system heatup and cooldown 
    limitations and new power-operated relief valve setpoints for the low 
    temperature overpressure protection system.
        Date of issuance: June 8, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 87 and 65.
        Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 21, 1994 (59 
    FR 65814) The March 1, 1995, letter provided supporting technical data 
    that did not change the scope of the October 1, 1994, application and 
    initial proposed no significant hazards consideration determination. 
    The Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated June 8, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Burke County Library, 412 
    Fourth Street, Waynesboro, Georgia 30830.
    
    GPU Nuclear Corporation, Docket No. 50-320, Three Mile Island Nuclear 
    Station, Unit No. 2, (TMI-2), Dauphin County, Pennsylvania
    
        Date of application for amendment: October 9, 1991.
        Brief description of amendment: This amendment extends the 
    expiration date of the license from November 9, 2009 to April 19, 2014.
        Date of issuance: June 21, 1995.
        Effective date: June 21, 1995.
        Amendment No.: 49.
        Possession-Only License No. DPR-73: The amendment extends the 
    license expiration date.
        Date of initial notice in Federal Register: August 3, 1994 (59 FR 
    39591). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 21, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, Walnut Street and Commonwealth 
    Avenue, Box 1601, Harrisburg, Pennsylvania 17105.
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, and 
    Energy Operations, Inc., Docket No. 50-458, River Bend Station, Unit 1, 
    West Feliciana Parish, Louisiana
    
        Date of amendment request: February 22, 1994, as supplemented May 
    19, 1995.
        Brief description of amendment: The amendment revised Technical 
    Specifications 3.6.1.5, ``Main Steam--Positive Leakage Control 
    System,'' and 3.6.1.10, ``Penetration Valve Leakage Control System,'' 
    to add an allowed outage time of 7 days with both trains of each system 
    inoperable. In addition, the allowed outage time for one train of the 
    Penetration Valve Leakage Control System inoperable is increased from 7 
    days to 10 days.
        Date of issuance: June 19, 1995.
        Effective date: June 19, 1995.
        Amendment No.: 80.
        Facility Operating License No. NPF-47. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 10, 1994 (59 FR 
    11331) The additional information contained in the supplemental letter 
    dated May 19, 1995, was clarifying in nature and thus, within the scope 
    of the initial notice and did not affect the staff's proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated June 19, 1995. 
    
    [[Page 35088]]
    
        No significant hazards consideration comments received. No.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, Louisiana 70803.
    
    PECO Energy Company, Public Service Electric and Gas Company, Delmarva 
    Power and Light Company, and Atlantic City Electric Company, Docket 
    Nos. 50-277 and 50-278, Peach Bottom Atomic Power Station, Unit Nos. 2 
    and 3, York County, Pennsylvania
    
        Date of application for amendments: November 17, 1994 as 
    supplemented March 30, 1995.
        Brief description of amendments: The amendments change equipment 
    designations, instrument range descriptions, instrument setpoints and 
    surveillance requirements in the Peach Bottom Technical Specifications 
    to reflect planned modifications to the main stack and vent stack 
    radiation monitoring systems.
        Date of issuance: June 13, 1995.
        Effective date: June 13, 1995.
        Amendments Nos.: 204 and 207.
        Facility Operating License Nos. DPR-44 and DPR-56: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 15, 1995 (60 FR 
    14027) The March 30, 1995, submittal provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated June 13, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
    PECO Energy Company, Public Service Electric and Gas Company, Delmarva 
    Power and Light Company, and Atlantic City Electric Company, Docket 
    Nos. 50-277 and 50-278, Peach Bottom Atomic Power Station, Unit Nos. 2 
    and 3, York County, Pennsylvania
    
        Date of application for amendments: March 16, 1995.
        Brief description of amendments: These amendments change the 
    existing Technical Specification requirements for source range neutron 
    monitoring equipment while in the refueling mode to requirements based 
    on NUREG-1433, ``Standard Technical Specifications General Electric 
    Plants, BWR/4.''
        Date of issuance: June 13, 1995.
        Effective date: June 13, 1995.
        Amendments Nos.: 205 and 208.
        Facility Operating License Nos. DPR-44 and DPR-56: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 10, 1995 (60 FR 
    24913) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 13, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
    PECO Energy Company, Public Service Electric and Gas Company, Delmarva 
    Power and Light Company, and Atlantic City Electric Company, Docket No. 
    50-277, Peach Bottom Atomic Power Station, Unit No. 2, York County, 
    Pennsylvania
    
        Date of application for amendment: March 30, 1995, as supplemented 
    by letter dated May 26, 1995.
        Brief description of amendment: The proposed amendment revises 
    Technical Specification Section 4.7.D.1.b(1) by adding a footnote to 
    exempt the High Pressure Coolant Injection motor-operated valve MO-2-
    23-015 from quarterly stroke testing requirements until refueling 
    outage 2RO11.
        Date of issuance: June 13, 1995.
        Effective date: June 13, 1995.
        Amendment No.: 206.
        Facility Operating License No. DPR-44: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 10, 1995 (60 FR 
    24912) The May 26, 1995, submittal provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 13, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
    PECO Energy Company, Public Service Electric and Gas Company, Delmarva 
    Power and Light Company, and Atlantic City Electric Company, Docket 
    Nos. 50-277 and 50-278, Peach Bottom Atomic Power Station, Unit Nos. 2 
    and 3, York County, Pennsylvania
    
        Date of application for amendments: March 22, 1995.
        Brief description of amendments: These amendments reduce the local 
    leak rate test hold time specified in the Technical Specification 
    Tables 3.7.2 through 3.7.4 from one hour to 20 minutes.
        Date of issuance: June 19, 1995.
        Effective date: June 19, 1995.
        Amendments Nos.: 207 and 209.
        Facility Operating License Nos. DPR-44 and DPR-56: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 10, 1995 (60 FR 
    24913). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 19, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: October 28, 1994, as 
    supplemented by letter dated April 18, 1995.
        Brief description of amendments: These amendments delete, from the 
    Technical Specifications, the surveillance and operability requirements 
    for chlorine detection and the associated Bases as a result of the 
    removal of bulk quantities of gaseous chlorine from the site.
        Date of issuance: June 19, 1995.
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment Nos.: 147 and 117.
        Facility Operating License Nos. NPF-14 and NPF-22. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 21, 1994 (59 
    FR 65821). The April 18, 1995, letter provided clarifying information 
    that did not change the initial proposed no significant hazards 
    consideration determination. 
    
    [[Page 35089]]
    
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated June 19, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of application for amendments: August 31, 1994.
        Brief description of amendments: This amendment revises the 
    Technical Specifications to permit the operability requirement for the 
    Feedwater/Main Turbine Trip System Actuation Instrumentation to be 
    Operational Condition 1 greater than or equal to 25% Rated Thermal 
    Power.
        Date of issuance: June 13, 1995.
        Effective date: June 13, 1995.
        Amendment Nos. 91 and 55.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 9, 1994 (59 FR 
    55884) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 13, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of application for amendments: August 23, 1994.
        Brief description of amendments: Remove the 125/250 Vdc Class 1E 
    Battery Load Cycle Table from the technical specifications (TS) and 
    rephrase the surveillance requirements to be consistent with NUREG-
    1433, ``Standard Technical Specifications'', and correct Amendments 71 
    and 34, dated June 28, 1994, to change certain surveillance requirement 
    intervals from 24 months to 18 months.
        Date of issuance: June 19, 1995.
        Effective date: June 19, 1995.
        Amendment Nos. 92 and 56.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 12, 1994 (59 FR 
    51624) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 19, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of application for amendments: August 31, 1994.
        Brief description of amendments: These amendments relocate the 
    requirements of TS 3/4.8.4.1, ``Primary Containment Penetration 
    Conductor Overcurrent Protective Devices,'' to the Updated Final Safety 
    Analysis Report and plant procedures.
        Date of issuance: June 22, 1995.
        Effective date: June 22, 1995.
        Amendment Nos. 93 and 57.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 9, 1994 (59 FR 
    55884) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 22, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of application for amendments: August 12, 1994, as 
    supplemented by letter dated March 29, 1995.
        Brief description of amendments: These amendments revise the action 
    statements regarding emergency core cooling systems to allow continued 
    operation in the event that the high pressure coolant injection system, 
    one core spray subsystem and/or one low pressure coolant injection 
    subsystem are inoperable.
        Date of issuance: June 22, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos. 94 and 58.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 12, 1994 (59 FR 
    51623). The March 29, 1995, letter provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 22, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, Limerick 
    Generating Station, Units 1 and 2, Montgomery County, Pennsylvania
    
        Date of application for amendments: August 31, 1994.
        Brief description of amendments: The amendments permit the 
    operability of one Low Pressure Coolant Injection subsystem of Residual 
    Heat Removal while the subsystem is aligned and operating in the 
    Shutdown Cooling Mode during Operational Conditions (OPCONs) 4 and 5.
        Date of issuance: June 22, 1995.
        Effective date: June 22, 1995.
        Amendment Nos. 95 and 59.
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 9, 1994 (59 FR 
    55884). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 22, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of application for amendments: November 18, 1994.
        Brief description of amendments: The amendments revise the 
    Reactivity Control System Technical Specification Limiting Conditions 
    for Operation for boration flow paths and charging pumps by reducing 
    the number of operable charging pumps required for boron addition in 
    Mode 4 from two to one.
        Date of issuance: June 12, 1995.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment Nos. 169 and 151.
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications. 
    
    [[Page 35090]]
    
        Date of initial notice in Federal Register: January 4, 1995 (60 FR 
    505). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 12, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of application for amendments: June 29, 1994, as supplemented 
    August 8, 1994, and May 2, 1995.
        Brief description of amendments: The amendments increase the 
    Technical Specification minimum volume of emergency diesel generator 
    fuel oil contained in the Diesel Fuel Oil Storage Tanks at both units 
    of the Salem station.
        Date of issuance: June 20, 1995.
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment Nos. 170 and 152.
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 17, 1994 (59 FR 
    42346). The August 8, 1994, and May 2, 1995, letters provided 
    clarifying information that did not change the initial proposed no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated June 20, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079.
    
    South Carolina Electric & Gas Company, South Carolina Public Service 
    Authority, Docket No. 50-395, Virgil C. Summer Nuclear Station, Unit 
    No. 1, Fairfield County, South Carolina
    
        Date of application for amendment: March 6, 1995, as supplemented 
    on May 5, 1995 and June 6, 1995.
        Brief description of amendment: The amendment deletes a license 
    condition that required the licensee to maintain a seismic monitoring 
    network around the Monticello Reservoir.
        Date of issuance: June 13, 1995.
        Effective date: June 13, 1995.
        Amendment No.: 124.
        Facility Operating License No. NPF-12. Amendment revises the 
    operating license.
        Date of initial notice in Federal Register: March 29, 1995 (60 FR 
    16201). The May 5, 1995 and June 6, 1995 submittals provided 
    supplemental information that did not change the initial proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated June 13, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180.
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260 and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2 and 3, Limestone County, Alabama
    
        Date of application for amendments: November 15, 1994; superseded 
    March 7, 1995 (TS 350).
        Brief Description of amendment: The amendments remove the 
    frequencies specified in the Technical Specifications for performing 
    audits and delete the requirement to perform the Radiological Emergency 
    Plan, Physical Security Plan, and Safeguard Contingency Plan reviews.
        Date of issuance: June 19, 1995.
        Effective Date: June 19, 1995.
        Amendment Nos.: 221, 236 and 195.
        Facility Operating License Nos. DPR-33, DRP-52 and DPR-68: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: December 21, 1994 (59 
    FR 65823); superseded March 29, 1995 (60 FR 16202). The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated June 19, 1995.
        No significant hazards consideration comments received: None.
        Local Public Document Room Location: Athens Public Library, South 
    Street, Athens, Alabama 35611.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: April 6, 1995 (TS 95-02).
        Brief description of amendments: The amendments add a limiting 
    condition for operation that allows equipment to be returned to service 
    under administrative control to perform operability testing and 
    establishes the time interval to place an inoperable channel in the 
    bypass condition.
        Date of issuance: June 13, 1995.
        Effective date: June 13, 1995.
        Amendment Nos.: 202 and 192.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: April 26, 1995 (60 FR 
    20530). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 13, 1995.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: April 6, 1995 (TS 95-05).
        Brief description of amendments: The amendments revise the 
    technical specifications by deleting Tables 3.6-1, 3.6-2, and 3.8-2 and 
    referenced to them, incorporating related guidance and justification, 
    and modifying the specification related to electrical equipment 
    protective devices in accordance with Generic Letter 91-08.
        Date of issuance: June 13, 1995.
        Effective date: June 13, 1995.
        Amendment Nos.: 203 and 193.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: May 10, 1995 (60 FR 
    24919). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 13, 1995.
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: April 6, 1995 (TS 95-06).
        Brief description of amendments: The amendments remove the 
    technical specification requirements related to crane travel over the 
    spent fuel pool.
        Date of issuance: June 14, 1995.
        Effective date: June 14, 1995.
        Amendment Nos.: 204 and 194.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: April 26, 1995 (60 FR 
    20529). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 14, 1995. 
    
    [[Page 35091]]
    
        No significant hazards consideration comments received: None.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: October 28, 1994.
        Brief description of amendment: The amendment removes the Neutron 
    Monitoring System and Control Rod Position instrumentation from the 
    Vermont Yankee Technical Specifications for post-accident monitoring 
    and incorporates administrative changes.
        Date of issuance: June 20, 1995.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 145.
        Facility Operating License No. DPR-28. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 10, 1995 (60 FR 
    24922). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 20, 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia.
    
        Date of application for amendments: June 9, 1994.
        Brief description of amendments: These amendments modify the 
    Chemical and Volume Control System and Safety Injection System 
    Technical Specifications.
        Date of issuance: May 31, 1995.
        Effective date: May 31, 1995.
        Amendment Nos. 199 and 199.
        Facility Operating License Nos. DPR-32 and DPR-37: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37089). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated May 31. 1995.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
    
        Dated at Rockville, Maryland, this 27th day of June 1995.
    
        For the Nuclear Regulatory Commission.
    Jack W. Roe,
    Director, Division of Reactor Projects--III/IV, Office of Nuclear 
    Reactor Regulation.
    [FR Doc. 95-16249 Filed 7-3-95; 8:45 am]
    BILLING CODE 7590-01-P
    
    

Document Information

Effective Date:
6/14/1995
Published:
07/05/1995
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
95-16249
Dates:
June 14, 1995.
Pages:
35058-35091 (34 pages)
PDF File:
95-16249.pdf