94-16174. Biweekly Notice  

  • [Federal Register Volume 59, Number 128 (Wednesday, July 6, 1994)]
    [Unknown Section]
    [Page 0]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 94-16174]
    
    
    [[Page Unknown]]
    
    [Federal Register: July 6, 1994]
    
    
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    UNITED STATES NUCLEAR REGULATORY COMMISSION
    
     
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating LicensesInvolving 
    No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from June 13, 1994, through June 23, 1994. The 
    last biweekly notice was published on June 22, 1994 (59 FR 32226).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11555 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC 
    20555. The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By August 5, 1994, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC 20555 and at the local 
    public document room for the particular facility involved. If a request 
    for a hearing or petition for leave to intervene is filed by the above 
    date, the Commission or an Atomic Safety and Licensing Board, 
    designated by the Commission or by the Chairman of the Atomic Safety 
    and Licensing Board Panel, will rule on the request and/or petition; 
    and the Secretary or the designated Atomic Safety and Licensing Board 
    will issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to John N. Hannon: petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    room for the particular facility involved.
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of amendment request: June 2, 1994
        Description of amendment request: The proposed amendment would 
    merge Toledo Edison Company into Cleveland Electric Illuminating 
    Company. As described in the application, the company formed from the 
    merger is intended to be renamed. Therefore, the licensee uses the 
    nomenclature ``NEWCO'' as a temporary name of the combined operating 
    company, and will provide the permanent name by supplemental letter. 
    The amendment would (1) replace the Toledo Edison Company and Cleveland 
    Electric Illuminating Company with ``NEWCO'' as a licensee, (2) 
    designate ``NEWCO'' as the owner of the Perry Nuclear Power Plant, Unit 
    1, and (3) make other administrative changes to the license as 
    indicated in the amendment application. Centerior Service Company would 
    be unaffected by the amendment and would remain a licensee.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed changes to the Operating License are administrative 
    and have no effect on any plant systems. All Limiting Conditions for 
    Operation, Limiting Safety Systems Settings and Safety Limits 
    specified in the Technical Specifications remain unchanged. This 
    change meets one of the examples of a change not likely to involve a 
    significant hazards consideration in that it is a purely 
    administrative changes (48 FR 14864).
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes to the Operating License are administrative 
    and have no effect on any plant systems. All Limiting Conditions for 
    Operation, Limiting Safety Systems Settings and Safety Limits 
    specified in the Technical Specifications remain unchanged. This 
    change meets one of the examples of a change not likely to involve a 
    significant hazards consideration in that it is a purely 
    administrative change (48 FR 14864).
        3. The proposed changes do not involve a significant reduction 
    in the margin of safety.
        The proposed changes to the Operating License are administrative 
    and have no effect on any plant systems. All Limiting Conditions for 
    Operation, Limiting Safety Systems Settings and Safety Limits 
    specified in the Technical Specifications remain unchanged. This 
    change meets one of the examples of a change not likely to involve a 
    significant hazards consideration in that it is purely an 
    administrative change (48 FR 14864).
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John N. Hannon
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, IllinoisDocket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of amendment request: May 20, 1994
        Description of amendment request: The proposed amendment would 
    permit the licensee to use an alternate repair criteria (ARC), 
    designated as the F* criteria. Use of the F* criteria would 
    allow tubes with otherwise pluggable indications, to remain in service 
    as long as the indications are below the designated minimum distance of 
    the F* criteria. The F* criteria defines a length of 1.7 
    inches of undegraded expanded tube within the tubesheet as the minimum 
    distance acceptable for implementing this ARC. Below the F* 
    length, a circumferential tube defect can exist and the tube can remain 
    in service. The proposed amendment will change the plugging limit 
    definition and would exclude plugging steam generator tubes with 
    indications that satisfy the F* criteria. The F* criteria 
    maintains the structural integrity of the degraded tube as the primary 
    pressure boundary and allows the tube to remain in service for heat 
    transfer and core cooling.
        This alternate repair criteria qualification is documented in 
    Babcock & Wilcox Nuclear Technologies (BWNT) Topical Report BAW-10196 P 
    Revision 1, ``W-D4 F* Qualification Report'', which is included as 
    part of the licensee's submittal.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        A. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The supporting qualification report for the subject criteria 
    demonstrates that the presence of the tubesheet will enhance the 
    tube integrity in the region of the tube-to-tubesheet roll 
    expansions by precluding tube deformation beyond its initial 
    expanded outside diameter. The resistance to a tube rupture is 
    strengthened by the presence of the tubesheet in that region. The 
    results of hardrolling of the tube into the tubesheet provides a 
    mechanical leak limiting seal between the tube and the tubesheet. A 
    tube rupture cannot occur because the contact between the tube and 
    the tubesheet does not permit sufficient movement of tube material.
        The type of degradation for which the F* criteria has been 
    developed (cracking with a circumferential orientation) can 
    theoretically lead to a postulated tube rupture event provided that 
    the postulated through-wall circumferential crack exists near the 
    top of the tubesheet. An evaluation including analysis and testing 
    has been done to determine the resistive strength of the expanded 
    tubes within the tubesheet. This evaluation provides the basis for 
    the acceptance criteria for tube degradation subject to the F* 
    criteria.
        The F* length of roll expansion is sufficient to preclude 
    tube pullout from tube degradation located below the F* 
    distance, regardless of the extent of the tube degradation. The 
    Technical Specification leakage rate requirements and accident 
    analysis assumptions remain unchanged in the unlikely event that 
    significant leakage from this region does occur. The tube rupture 
    and pullout is fully bounded by the existing steam generator tube 
    rupture analysis included in the UFSAR. The leakage testing of the 
    roll expanded tubes indicates that for tube expansion lengths 
    approximately equal to the F* distance, any postulated primary 
    to secondary leakage from F* tubes would be insignificant. The 
    proposed alternate repair criteria does not adversely impact any 
    other previously evaluated design basis accident.
        The leakage from an F* tube would be limited by the tube-
    to-tubesheet interface since this leak would occur below the 
    secondary face of the tubesheet. Qualification testing and previous 
    experience indicate that normal and faulted leakage is well below 
    Technical Specification and administrative limits creating no 
    increase in the consequences associated with tube rupture type 
    leakages. The UFSAR analyzed accident scenarios are still bounding 
    since the normal and faulted leak rates are well within the normal 
    operating limit of 150 gallons per day. This conclusion is 
    consistent with previous F* programs approved and used at other 
    operating plants.
        All of the design and operating characteristics of the steam 
    generator and connected systems are preserved since the F* 
    criteria utilizes the ``as rolled'' tube configuration that exists 
    as part of the original steam generator design. The F* joint 
    has been analyzed and tested for design, operating, and faulted 
    condition loadings in accordance with Regulatory Guide 1.121 safety 
    factors. The potential for tube rupture is not increased from the 
    original submittal as demonstrated in the qualification analyses and 
    testing completed in the BWNT report.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        B. The proposed changes do not create the possibility of a new 
    or different type of accident from any accident previously 
    evaluated.
        Implementation of the proposed F* criteria does not 
    introduce any significant changes to the plant design basis. Use of 
    the criteria does not provide a mechanism to initiate an accident 
    outside of the region of the expanded portion of the tube. In the 
    unlikely event the failed tube severed completely at a point below 
    the F* region, the remaining F* joint would retain 
    engagement in the tubesheet due to its length of expanded contact 
    within the tubesheet bore. This engagement length would prevent any 
    interaction of the severed tube with neighboring tubes. Any 
    hypothetical accident as a result of any tube degradation in the 
    expanded region of the tube would be bounded by the existing tube 
    rupture accident analysis. Tube bundle structural integrity will be 
    maintained. Tube bundle leak tightness will be maintained such that 
    any postulated accident leakage from F* tubes will be 
    negligible with regard to offsite doses.
        Therefore, there is not a potential for creating the possibility 
    of a new or different type of accident from any accident previously 
    evaluated.
        C. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        The use of the F* criteria has been demonstrated to 
    maintain the integrity of the tube bundle commensurate with the 
    requirements of Reg Guide 1.121 and the primary to secondary 
    pressure boundary under normal and postulated accident conditions. 
    Acceptable tube degradation for the F* criteria is any 
    degradation indication in the tubesheet region, more than the 
    F* distance from the secondary face of the tubesheet or the top 
    of the last hardroll contact point which ever is further into the 
    tubesheet. The safety factors used in the verification of the 
    strength of the degraded tube are consistent with the safety factors 
    in the ASME Boiler and Pressure Vessel Code and Reg Guide 1.121 used 
    in steam generator design. The F* distance has been verified by 
    various testing to be greater than the length of the roll expanded 
    tube-to-tubesheet interface required to preclude both tube pullout 
    and significant leakage during normal and postulated accident 
    conditions. The protective boundaries of the steam generator 
    continue to be maintained with the use of the F* criteria. A 
    tube with the indication of degration previously requiring removal 
    from service can be kept in service through the F* criteria. 
    Since the joint is constrained within the tubesheet bore, there is 
    no additional risk associated with the previously analyzed tube 
    rupture event. The leak testing acceptance criteria are based on the 
    primary to secondary leakage limit in the Technical Specifications 
    and the leakage assumptions used in the UFSAR accident analyses.
        Implementation of the alternate repair criteria will decrease 
    the number of tubes which must be taken out of service with tube 
    plugs or repaired by sleeves. Both plugs and sleeves reduce the RCS 
    flow margin; thus, implementation of the F* criteria will 
    maintain the margin of flow that would otherwise be reduced in the 
    event of increased plugging or sleeving.
        Based on the above, it is concluded that the proposed change 
    does not result in a significant reduction in margin with respect to 
    plant safety as defined in the UFSAR or the Technical Specification 
    Bases.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: For Byron, the Byron Public 
    Library, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; for 
    Braidwood, the Wilmington Township Public Library, 201 S. Kankakee 
    Street, Wilmington, Illinois 60481
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690
        NRC Project Director: Robert A. Capra
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of amendment request: October 22, 1993
        Description of amendment request: The proposed amendment would 
    modify the Reactor Trip System (RTS) and Engineered Safety Feature 
    (ESF) instrumentation surveillance requirements to incorporate the 
    applicable changes specified in NRC-approved WCAP-10271 and related 
    supplements. Four specific changes were approved by the Nuclear 
    Regulatory Commission for the RTS and Engineered Safety Feature 
    Actuation System analog channels. These changes are limited to the 
    specific Reactor Protection System (RPS) channels evaluated in the WCAP 
    (including all supplements) and are subject to the conditions specified 
    by the NRC.
        1. The surveillance or test frequency may be changed from monthly 
    to quarterly.
        2. The time allowed for a channel to be inoperable or out of 
    service in an untripped condition may be changed from 1 hour to 6 
    hours.
        3. The time a channel in a functional group may be bypassed to 
    perform testing may be increased from 2 to 4 hours. This bypass time 
    applies to either an inoperable channel when testing is done in the 
    tripped mode or to the channel in test when testing is done in the 
    bypass mode. The Allowed Outage Time for maintenance of a channel is 12 
    hours.
        4. Routine channel testing may be performed in the bypassed 
    condition instead of the tripped condition.
        In addition, a number of editorial changes are made to improve 
    clarity, and two-loop operating requirements are proposed to be 
    deleted. Also, the surveillance test interval for RTS interlocks is 
    proposed to be changed from monthly to once-per-refueling (about 18 
    months). Although not part of WCAP-10271, this was previously approved 
    generically by NRC.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The determination that the results of the proposed changes are 
    within all acceptable criteria was established in the SER(s) [Safety 
    Evaluation Report(s)] prepared for WCAP-10271, WCAP-10271 Supplement 
    1, WCAP-10271 Supplement 2 and WCAP-10271 Supplement 2, Revision 1 
    issued by letters dated February 21, 1985, February 22, 1989 and 
    April 30, 1990. Implementation of the proposed changes is expected 
    to result in an acceptable increase in total Reactor Protection 
    System yearly unavailability. This increase, which is primarily due 
    to less frequent surveillance, results in an increase of similar 
    magnitude in the probability of an Anticipated Transient Without 
    Scram (ATWS) and in the probability of core melt resulting from an 
    ATWS and also results in a small increase in Core Damage Frequency 
    (CDF) due to Engineered Safety Features Actuation System 
    unavailability.
        Implementation of the proposed changes is expected to result in 
    a significant reduction in the probability of core melt from 
    inadvertent reactor trips. This is a result of a reduction in the 
    number of inadvertent reactor trips (0.5 fewer inadvertent reactor 
    trips per unit per year) occurring during testing of RPS 
    instrumentation. This reduction is primarily attributable to testing 
    in bypass and less frequent surveillance.
        The reduction in [***] core melt frequency is sufficiently large 
    to counter the increase in ATWS core melt probability resulting in 
    an overall reduction in total core melt probability.
        The values determined by the WOG [Westinghouse Owners Group] and 
    presented in the WCAP for the increase in CDF were verified by 
    Brookhaven National Laboratory (BNL) as part of an audit and 
    sensitivity analyses for the NRC Staff. Based on the small value of 
    the increase compared to the range of uncertainty in the CDF, the 
    increase is considered acceptable.
        Changes to Surveillance Test Frequencies for the Reactor Trip 
    System Interlocks do not represent a significant reduction in 
    testing. The currently specified test interval for interlock 
    channels allows the surveillance requirement to be satisfied by 
    verifying that the permissive logic is in its required state using 
    the annunciator status light. The surveillance, as currently 
    required, only verifies the status of the permissive logic and does 
    not address verification of channel setpoint or operability. The 
    setpoint verification and channel operability are verified after a 
    refueling shutdown. The definition of the channel check includes 
    comparison of the channel status with other channels for the same 
    parameter. The requirement to routinely verify permissive status is 
    a different consideration than the availability of trip or actuation 
    channels which are required to change state on the occurrence of an 
    event and for which the function availability is more dependent on 
    the surveillance interval. The change in surveillance requirement to 
    at least once every 18 months does not therefore represent a 
    significant change in channel surveillance and does not involve a 
    significant increase in unavailability of the Reactor Protection 
    System.
        The proposed changes do not result in an increase in the 
    severity or consequences of an accident previously evaluated.
        Implementation of the proposed changes affects the probability 
    of failure of the RPS but does not alter the manner in which 
    protection is afforded nor the manner in which limiting criteria are 
    established.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes do not result in a change in the manner in 
    which the Reactor Protection System provides plant protection. No 
    change is being made which alters the functioning of the Reactor 
    Protection System (other than in a test mode). Rather the likelihood 
    or probability of the Reactor Protection System functioning properly 
    is affected as described above. Therefore,the proposed changes do 
    not create the possibility of a new or different kind of accident 
    nor involve a reduction in a margin of safety as defined in the 
    Safety Analysis Report.
        The proposed changes do not involve hardware changes except 
    those necessary to implement testing in bypass. Some existing 
    instrumentation is designed to be tested in bypass and current 
    technical specifications allow testing in bypass. Testing in bypass 
    is also recognized by IEEE [Institute of Electrical and Electronics 
    Engineers] Standards. Therefore, testing in bypass has been 
    previously approved and implementation of the proposed change for 
    testing in bypass does not create the possibility of a new or 
    different kind of accident from any previously evaluated. 
    Furthermore, since the other proposed changes do not alter the 
    functioning of the RPS, the possibility of a new or different kind 
    of accident from any previously evaluated has not been created.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed changes do not alter the manner in which safety 
    limits, limiting safety system setpoints or limiting conditions for 
    operation are determined. The impact of reduced testing other than 
    as addressed above is to allow a longer time interval over which 
    instrument uncertainties (e.g., drift) may act. Experience has shown 
    that the initial uncertainty assumptions are valid for reduced 
    testing.
        Implementation of the proposed changes is expected to result in 
    an overall improvement in safety by:
        a. Less frequent testing will result in fewer inadvertent 
    reactor trips and fewer actuations of Engineered Safety Feature 
    Actuation System components.
        b. Improvements in the effectiveness of the operating staff in 
    monitoring and controlling plant operation. This is due to less 
    frequent distraction of the operator and shift supervisor to attend 
    to instrumentation testing.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
        Attorney for licensee: Gerald Charnoff, Esquire, Jay E. Silberg, 
    Esquire, Shaw, Pittman, Potts & Trowbridge, 2300 N Street, NW., 
    Washington, DC 20037.
        NRC Project Director: Walter R. Butler
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of amendment request: April 19, 1994
        Description of amendment request: The proposed amendment would 
    modify Specifications 3.4.9.3 and 3.4.11 to incorporate power operated 
    relief valve (PORV) Technical Specification (TS) changes in accordance 
    with the guidance in Generic Letter 90-06 as implemented in NUREG-1431 
    Improved Standard Technical Specifications (ISTS), with some exceptions 
    and modifications to reflect plant specific design features. Certain 
    other TS sections would also be modified to address related TSs.
        The proposed changes involve the details of (a) limiting conditions 
    of operation, and (b) surveillance testing for equipment needed to 
    protect the reactor vessel from overpressure conditions. This equipment 
    includes PORVs and their associated block valves, charging pumps, 
    reactor coolant system (RCS) vent, accumulators, and the overpressure 
    protection system. Numerous administrative changes are also proposed, 
    such as renumbering sections, spelling out mathematical symbols, 
    changes in nomenclature for consistency, and relocating sentences and 
    paragraphs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed changes consolidate the power operated relief valve 
    requirements into Specifications 3.4.9.3 and 3.4.11 which generally 
    adopt the new Improved Standard Technical Specifications of NUREG-
    1431 to address the concerns identified in Generic Letter 90-06 
    except for those changes required to reflect plant specific design 
    features. These changes are proposed to enhance safety and improve 
    the reliability of the PORVs and block valves. Since the proposed 
    changes augment or preserve the requirements contained in the 
    current technical specifications, we have concluded that these 
    changes do not involve a significant increase in the probability or 
    consequences of an accident previously evaluated in the UFSAR 
    [Updated Final Safety Analysis Report].
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes do not involve any physical changes to the 
    PORVs or their setpoints. These changes do not delete any function 
    previously provided by the PORVs nor has the probability of 
    inadvertent opening been increased. Accordingly, no new failure 
    modes have been defined for any plant system or component important 
    to safety nor has any new limiting single failure been identified as 
    a result of these changes. Therefore, these changes will not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated in the UFSAR.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed changes have been incorporated to enhance safety 
    and improve the reliability of the PORVs and block valves to ensure 
    their availability when called upon to perform their function. These 
    changes do not affect the manner by which the facility is operated 
    or involve a change to equipment or features which affect the 
    operational characteristics of the facility. Therefore, operation of 
    the facility in accordance with the proposed amendment would not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis. The staff notes 
    that a significant effort has been made by the NRC and by industry over 
    the last several years to improve and tighten the TS requirements for 
    overpressure protection systems. These efforts are documented in 
    Generic Letter 90-06 and NUREG-1431. The changes proposed by the 
    licensee appear to result in TSs that are significantly more 
    comprehensive and restrictive than those now existing for Beaver Valley 
    Units 1 and 2, and, therefore, should help to reduce the probability of 
    an accident. The staff disagrees with the licensee's claim that the 
    changes do not affect the manner by which the facility is operated 
    (consideration number 3 above). However, the staff believes that the 
    proposed TS changes require more restrictive operation (such as more 
    careful control of the number of charging pumps which can inject into 
    the RCS) and do not involve a significant reduction in a margin of 
    safety. Based on the NRC staff's review, it appears that the three 
    standards of 10 CFR 50.92(c) are satisfied. Therefore, the NRC staff 
    proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
        Attorney for licensee: Gerald Charnoff, Esquire, Jay E. Silberg, 
    Esquire, Shaw, Pittman, Potts & Trowbridge, 2300 N Street, NW., 
    Washington, DC 20037.
        NRC Project Director: Walter R. Butler
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of amendment request: June 9, 1994
        Description of amendment request: The proposed amendment would 
    revise Technical Specification section 4.8.1.1.2 to replace the current 
    qualitative examination of new diesel generator fuel oil for water/
    sediment and particulate contamination with a quantitative examination 
    for the same properties.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    since the diesel generator availability and reliability is not being 
    changed. The quantitative acceptance criteria for new fuel oil is 
    not being changed. Diesel generator performance will therefore not 
    be changed due to the proposed revision to SR [surveillance 
    requirement] 4.8.1[.1].2.d.1.d. The diesel generator will continue 
    to provide sufficient electrical power to ESF [engineered safety 
    feature] systems. The ESF systems will continue to function, as 
    assumed in the safety analyses, to ensure that the fuel, reactor 
    coolant system, and containment
        design limits are not exceeded.
        Therefore, this changes will not increase the probability or 
    consequences of an accident previously evaluated due to the 
    continued availability and reliability of the emergency diesel power 
    source.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed change does not alter the method of operating the 
    plant. This change will continue to ensure that the addition of new 
    fuel oil complies with accepted standards regarding fuel oil 
    quality. Since design requirements continue to be met and the 
    integrity of the reactor coolant system pressure boundary is not 
    challenged, no new failure mode has been created. As a result, an 
    accident which is different than any already evaluated in the 
    Updated Final Safety Analysis Report will not be created due to this 
    change.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The margin of safety is not reduced because the emergency diesel 
    generators will continue to provide sufficient capacity, capability, 
    redundancy, and reliability to ensure availability of necessary 
    power to ESF systems. The ESF systems will continue to function, as 
    assumed in the safety analyses, to ensure that the fuel, reactor 
    coolant systems, and containment design limits are not exceeded. The 
    replacement of the clear and bright qualitative examination with the 
    proposed quantitative test to determine the actual water/sediment 
    and particulates will ensure that new fuel oil meets the required 
    limits for these properties prior to addition to the storage tank, 
    therefore assuring that the quality of the stored fuel is unaffected 
    by the addition of new fuel.
        Therefore, this proposed change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
        Attorney for licensee: Gerald Charnoff, Esquire, Jay E. Silberg, 
    Esquire, Shaw, Pittman, Potts & Trowbridge, 2300 N Street, NW., 
    Washington, DC 20037.
        NRC Project Director: Walter R. Butler
    
    Duquesne Light Company, et al., Docket No. 50-412, Beaver Valley 
    Power Station, Unit No. 2, Shippingport, Pennsylvania
    
        Date of amendment request: February 16, 1994
        Description of amendment request: The proposed amendment would 
    delete the Appendix B Section 4.2.2 requirement to perform infrared 
    aerial photography every other year.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change will delete from Facility Operating License 
    No. NPF-73 the Appendix B Section 4.2.2 requirement to perform 
    infrared aerial photography every other year. The acceptance limit 
    which forms the licensing basis for this technical specification is 
    related to environmental impact and has no impact on the margin of 
    safety, accident analysis, or other design basis impacting the 
    margin of safety. No increase in adverse environmental impact has 
    been identified over that previously identified in the Final 
    Environmental Statement - Operating License Stage, environmental 
    impact appraisals, or in any decisions of the Atomic Safety and 
    Licensing Board. The Final Environmental Statement concluded, based 
    on a model of combined drift from Units 1 and 2, that no adverse 
    impacts to sensitive species of natural vegetation or to sensitive 
    species of crops were expected. The staff also examined infrared 
    aerial photographs taken from 1975 through 1983 and found no injury 
    to vegetation from cooling tower drift in the vicinity of Unit 1.
        Continued terrestrial monitoring was performed for Beaver Valley 
    Unit 2 by infrared aerial photography in 1986, 1988, 1990, and 1992. 
    The results as provided in the Annual Environmental Reports Non-
    Radiological concluded, ``Based on interpretation of the infrared 
    photographs and field verification, there is no evidence to suggest 
    that the BVPS [Beaver Valley Power Station] cooling towers are 
    causing vegetation stress.''
        Based on the compilation of the infrared aerial photography 
    performed for both BV-1 and BV-2, deletion of this terrestrial 
    monitoring requirement will have no impact on the environment or the 
    operation of the plant. Therefore, the proposed change will not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The Appendix B Section 4.2.2 requirement to perform infrared 
    aerial photography reflects a commitment described in Final 
    Environmental Statement Section 5.14.1. Therein it is stated that 
    the preoperational monitoring studies for BV-2 are based primarily 
    on the BV-1 operational monitoring programs. ``Results of these 
    studies have shown that there were no BV-1 operational impacts on 
    flora, thus, the only terrestrial monitoring planned for BV-2 is 
    continued infrared aerial photography every other year. The 
    photographs will be compared with preoperational photographs of the 
    BV-2 area, nd any signs of injury as a result of salt drift and 
    other sources will be checked. The details of this terrestrial 
    monitoring program will be specified in the Environmental Protection 
    Plan that will be included in Appendix B of the operating license.'' 
    The subject of this concern is the impact of salt and water drift on 
    area vegetation including sensitive agricultural crops. From the 
    standpoint of soil salinization (the effects of the accumulation of 
    salts in the soil), described in the Environmental Report-Operating 
    License Stage Section 5.3.3, no appreciable impact resulting from 
    operation of the natural draft cooling towers is anticipated. This 
    is based on the average rate of precipitation of 36.2 inches 
    annually which greatly reduces the potential for accumulation of 
    salt in the soil. The terrestrial monitoring program has been 
    performed in accordance with the Environmental Protection Plan and 
    has provided additional verification that operation of both cooling 
    towers has not produced any evidence of vegetation stress. The 
    proposed change does not introduce any new mode of plant operation 
    or require any physical modification to the plant, therefore, this 
    change will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        Infrared aerial photography surveillance does not affect safety 
    systems and/or systems important to safety. Terrestrial monitoring 
    is not used in any accident analysis and does not provide a basis 
    for evaluating the radiological consequences of an accident. 
    Deleting the requirement to perform infrared aerial photography will 
    not result in any environmental impact from operation of the cooling 
    tower and will not affect the operation of the cooling tower. The 
    operating history of both the BV-1 and the BV-2 cooling towers has 
    demonstrated that there is no evidence of vegetation stress in 
    accordance with the results obtained from the infrared aerial 
    photography and other associated methods of environmental 
    monitoring. Therefore, based on the above, the proposed change will 
    not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
        Attorney for licensee: Gerald Charnoff, Esquire, Jay E. Silberg, 
    Esquire, Shaw, Pittman, Potts & Trowbridge, 2300 N Street, NW., 
    Washington, DC 20037.
        NRC Project Director: Walter R. Butler
    
    Florida Power and Light Company, et al., Docket No. 50-335, St. 
    Lucie Plant, Unit No. 1, St. Lucie County, Florida
    
        Date of amendment request: May 23, 1994
        Description of amendment request: The amendment will revise 
    Technical Specification (TS) 3.5.2 for Emergency Core Cooling Systems 
    (ECCS) by removing the option that allows High Pressure Safety 
    Injection (HPSI) Pump 1C to be used as an alternative to the preferred 
    pump for subsystem operability. HPSI pump 1C is an installed spare 
    which is not required to be maintained in an operable status, and this 
    change is being requested to upgrade the ECCS operability requirements 
    consistent with actual plant operating needs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed license amendment will remove the option of using 
    High Pressure Safety Injection Pump 1C (HPSI-1C) to satisfy, in 
    part, the Emergency Core Cooling System (ECCS) 
    operabilityrequirements specified in Limiting Condition for 
    Operation (LCO) 3.5.2. HPSI-1C is an installed spare pump that is 
    not required to be operable unless it is being used in place of the 
    preferred B-train ECCS high pressure pump. The required functional 
    response of the ECCS or the required availability of the minimum 
    equipment necessary to accomplish the ECCS safety function will not 
    be changed by removing the spare pump option from the Technical 
    Specifications.
        The calculated cooling performance of the St. Lucie Unit 1 ECCS 
    during postulated accidents conforms to the criteria set forth in 10 
    CFR 50.46 and the ability to achieve this required performance, 
    including considerations of single-failure criteria, is independent 
    from optional use of HPSI-1C. Therefore, operation of the facility 
    in accordance with the proposed amendment will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposed amendment will not change the physical plant or the 
    modes of operation defined in the facility license. Eliminating the 
    option for the licensee to utilize HPSI-1C in place of the preferred 
    B-train ECCS high pressure pump does not involve the addition of new 
    or different types of equipment to the previously analyzed ECCS. 
    Equipment important to safety will continue to perform their safety 
    functions as previously analyzed and will not be affected by this 
    proposed amendment. Therefore, operation of the facility in 
    accordance with the proposed amendment would not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        Removing the option to employ the installed spare HPSI pump 1C 
    in lieu of the preferred B-train pump to determine ECCS operability 
    only removes an operational flexibility that has rarely been used by 
    the licensee. St. Lucie Unit 1 accident analyses do not take credit 
    for an installed spare pump, the minimum complement of safety 
    injection equipment required for safe operation of the facility and 
    that is required by LCO 3.5.2 is not changed, and the results of 
    plant accident and transient analyses are not influenced by this 
    proposed amendment. The proposed change does not alter the bases for 
    any Technical Specification related to the establishment of, or 
    maintenance of, a nuclear safety margin. Therefore, operation of the 
    facility in accordance with the proposed amendment would not involve 
    a significant reduction in a margin of safety.
        Based on the discussion presented above and on the supporting 
    Evaluation of Proposed TS Changes, FPL has concluded that this 
    proposed license amendment involves no significant hazards 
    consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
        Attorney for licensee: Harold F. Reis, Esquire, Newman and 
    Holtzinger, 1615 L Street, NW., Washington, DC 20036
        NRC Project Director: Herbert N. Berkow
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-
    389, St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
    
        Date of amendment request: May 23, 1994
        Description of amendment request: The proposed amendments will 
    relocate the seismic monitoring instrumentation Limiting Conditions for 
    Operation, Surveillance Requirements, and the associated tables 
    contained in Technical Specifications 3.3.3.3, 4.3.3.3.1 and 4.3.3.3.2 
    to the Updated Final Safety Analysis Report. The basis for this request 
    is consistent with NUREG-1432, ``Standard Technical Specifications, 
    Combustion Engineering Plants'' and with the ``Final Policy Statement 
    on Technical Specifications Improvements for Nuclear Power Reactors, 
    ``published in the Federal Register (58 FR 39132) dated July 22, 1993.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed changes are administrative in nature in that the 
    specifications for operation and surveillance of the Seismic 
    Monitoring Instrumentation system will be relocated from Appendix A 
    of the facility operating license to the Updated Final Safety 
    Analysis Report for St. Lucie Unit 1 and Unit 2. Changes to the 
    system will be controlled by 10 CFR 50.59 and the safety analysis 
    report is required to be updated pursuant to 10 CFR 50.71(e). 
    Relocation of these requirements to the UFSAR is consistent with the 
    NRC ``Final Policy Statement on Technical Specifications 
    Improvements for Nuclear Power Reactors'' published in the Federal 
    Register (58 FR 39132) dated July 22, 1993.
        Seismic monitoring instrumentation is not an accident initiator 
    nor a part of the success path(s) which function to mitigate 
    accidents evaluated in the plant safety analyses. The proposed 
    technical specification change does not involve any change to the 
    configuration or method of operation of any plant equipment that is 
    used to mitigate the consequences of an accident, nor do the changes 
    alter any assumptions or conditions in any of the plant accident 
    analyses. Therefore, operation of the facility in accordance with 
    the proposed amendment would not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposed amendment to relocate the existing Technical 
    Specification requirements for Seismic Monitoring Instrumentation to 
    the Updated Final Safety Analysis Report will not change the 
    physical plant or the modes of plant operation defined in the 
    Facility License. The change does not involve the addition or 
    modification of equipment nor does it alter the design or operation 
    of plant systems. Therefore, operation of the facility in accordance 
    with the proposed amendment would not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        The proposed changes are administrative in nature in that 
    operating and surveillance requirements for the Seismic Monitoring 
    Instrumentation system will be relocated from Appendix A of the 
    facility license to the Updated Final Safety Analysis Report for St. 
    Lucie Unit 1 and Unit 2. Seismic monitoring instruments are not used 
    to actuate safety-related equipment, provide interlocks, or 
    otherwise perform plant control functions. The instruments are used 
    to record the magnitude of a seismic event, should it occur. 
    Conditions evaluated in plant accident and transient analyses do not 
    involve seismic instruments. The proposed changes do not alter the 
    basis for any technical specification that is related to the 
    establishment of, or the maintenance of, a nuclear safety margin. 
    Therefore, operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        Based on the above discussion and the supporting Evaluation of 
    Technical Specification changes, FPL has determined that the 
    proposed license amendment involves no significant hazards 
    consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
        Attorney for licensee: Harold F. Reis, Esquire, Newman and 
    Holtzinger, 1615 L Street, NW., Washington, DC 20036
        NRC Project Director: Herbert N. Berkow
    
    Florida Power and Light Company, et al., Docket No. 50-389, St. 
    Lucie Plant, Unit No. 2, St. Lucie County, Florida
    
        Date of amendment request: May 23, 1994
        Description of amendment request: The proposed amendment revises 
    Technical Specifications Section 3/4.7.1.1, Turbine Cycle, Safety 
    Valves, to delete a specific reference to the 1974 edition of the ASME 
    Code and refer to testing in accordance with Technical Specification 
    4.0.5, the In-Service Inspection and In-Service Testing Specification.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1)Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendment does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated because the main steam code safety valves will continue to 
    be tested in accordance with current NRC requirements as implemented 
    through 10 CFR 50.55a. The NRC specifies the ASME code requirements 
    for a facility through revisions to 10 CFR 50.55a and through the 
    review and approval of the plant specific in-service testing plan 
    for pumps and valves at the beginning of each in-service inspection 
    interval.
        The probability or consequences of an accident are not increased 
    because testing of the main steam safety valves is in accordance 
    with the appropriate NRC requirements.
        (2) Use of the modified specification would not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        The use of this modified specification can not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated since there is no physical change to the 
    facility or the set points for the main steam safety valves. The 
    valves will be tested in accordance with current requirements. No 
    new failure mode is introduced due to the change because no plant 
    change is being made and main steam safety valve test methods are 
    consistent with the endorsed edition of the ASME Code.
        (3) Use of the modified specification would not involve a 
    significant reduction in a margin of safety.
        The existing technical specification references an outdated 
    version of the ASME Code. This change corrects the reference to 
    Specification 4.0.5 which ensures that in-service testing of ASME 
    Code Class 1, 2, and 3 pumps and valves will be performed in 
    accordance with a periodically updated version of Section XI of the 
    ASME Boiler and Pressure Vessel Code and Addenda as required by 10 
    CFR 50.55a.
        Safety valve setpoints or tolerances are not changed by this 
    proposal. Therefore, the modified specification corrects the ASME 
    Code reference and does not involve a significant reduction in a 
    margin of safety.
        Based on the above, we have determined that the proposed 
    amendment does not (1) involve a significant increase in the 
    probability or consequences of an accident previously evaluated, (2) 
    create the probability of a new or different kind of accident from 
    any previously evaluated, or (3) involve a significant reduction in 
    a margin of safety; and therefore does not involve a significant 
    hazards consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003
        Attorney for licensee: Harold F. Reis, Esquire, Newman and 
    Holtzinger, 1615 L Street, NW., Washington, DC 20036
        NRC Project Director: Herbert N. Berkow
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, 
    Linn County, Iowa
    
        Date of amendment request: March 27, 1992, as supplemented on 
    January 6, and May 27, 1994.
        Description of amendment request: The proposed amendment would 
    revise the limiting conditions for operation and surveillance 
    requirements for primary containment integrity, secondary containment 
    integrity and other systems and equipment of Technical Specifications 
    Section 3.7.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated because the requested revisions do not affect 
    the FSAR safety analyses involving these system.
        Definitions
        The revisions to Definition 15, ``Primary Containment 
    Integrity'' and Definition 16, ``Secondary Containment Integrity'' 
    agree with the corresponding definitions of the STS. These changes 
    are administrative in nature in that they only clarify the 
    requirements for containment integrity and the appropriate means of 
    isolating penetrations. These changes do not affect the operation or 
    function of the containment isolation systems and, therefore, do not 
    result in a significant increase in the probability or consequences 
    of an accident previously evaluated.
        Primary Containment Integrity
        The revision to TS section 3.7.A, ``Primary Containment 
    Integrity'', only adds a specific requirement to restore primary 
    containment integrity within 1 hour or commence a plant shutdown. 
    These actions are consistent with the actions specified in STS for 
    primary containment integrity. No changes to the primary containment 
    boundary or the requirements for primary containment integrity have 
    been proposed. Therefore, this change does not result in a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        Primary Containment Power Operated Isolation Valves
        The revisions to TS section 3.7.B, ``Primary Containment Power 
    Operated Isolation Valves'' are editorial in nature in that the 
    wording has only been changed to be consistent with the STS 
    requirements for primary containment isolation valves. These changes 
    do not affect the function of the valves, the requirements to 
    isolate a penetration with an inoperable containment isolation valve 
    or the actual methods of isolation. Penetrations are still required 
    to be isolated within 4 hours in a manner that cannot be adversely 
    affected by a single active failure. Therefore, these changes do not 
    result in a significant increase in the probability or consequences 
    of an accident previously evaluated.
        Drywell Average Air Temperature
        The addition of limits, actions, and surveillance requirements 
    for drywell average air temperature are intended to ensure that the 
    initial assumptions in the DAEC Primary Containment Response 
    Analysis to a DBA remain valid. The temperature limit (135 deg.F) 
    corresponds to the initial drywell average temperature assumed for 
    this analysis in the UFSAR. The specified limits, actions and 
    surveillance requirements are consistent with STS. The addition of 
    this limit to the TS will not affect the actual operation or 
    function of any equipment but will ensure that the containment 
    analysis remains valid. Therefore, the addition of this limit will 
    not result in a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Pressure Suppression Chamber-Reactor Building Vacuum Breakers
        The changes to TS section 3/4.7.D only provide additional detail 
    and operability requirements for the pressure suppression chamber-
    reactor building vacuum breakers. These additional details are 
    consistent with the requirements of STS. Specifying separate 
    operability requirements for vacuum breakers inoperable for opening 
    (but known to be closed), or open better reflects the dual functions 
    of these valves (vacuum relief and containment isolation). The 
    additional surveillance requirement will better ensure that the 
    containment isolation function of these valves is maintained. The 
    rewording of existing surveillances only clarifies current 
    requirements. These changes do not affect the actual function, 
    setpoints, or number of valves required to be operable and therefore 
    do not result in a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Drywell-Pressure Suppression Chamber Vacuum Breakers
        The changes to TS section 3/4.7.E, only provide additional 
    detail and operability requirements for the drywell-pressure 
    suppression chamber vacuum breakers. These additional details are 
    consistent with the requirements of STS. Specifying separate 
    operability requirements for vacuum breakers inoperable for opening 
    (but known to be closed) or open better reflects the dual functions 
    of these valves. The additional requirement to verify that each 
    vacuum breaker is closed at least once per week will better ensure 
    that the isolation boundary between the drywell and torus is 
    maintained. The elimination of the requirement to exercise all 
    operable drywell-pressure suppression chamber vacuum breakers upon 
    determination that a vacuum breaker is inoperable for opening will 
    not affect the reliability of these vacuum breakers. The only valid 
    reason to exercise the operable vacuum breakers is if a common mode 
    failure is suspected. We have reviewed the maintenance history of 
    these valves and have not identified any instance of common mode 
    failures. Conditional testing of these changes will not result in a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        Main Steam Isolation Valve Leakage Control System (MSIV-LCS)
        The change to TS Section 3/4.7.F, ``MSIV-LCS'', deletes the 
    unnecessary and potentially non-conservative conditional 
    surveillance testing of the redundant MSIV-LCS subsystems. Although 
    the proposed change will reduce the amount of testing of the MSIV-
    LCS, reliability of these systems would not be decreased and the 
    necessary assurance that the alternate systems/subsystems/components 
    will operate when needed is provided by the ASME Section XI IST 
    Program.
        The possibility of human error will decrease with reduced 
    testing. Human error such as a misalignment of valves after the 
    system is returned to its normal configuration following testing and 
    the misdirection of the operators attention from monitoring and 
    directing plant operations is less likely to occur if this testing 
    is eliminated. Additionally, reducing the scope and frequency of 
    surveillance testing will decrease the probability of equipment 
    failure (due to testing) which could require plant shutdown. 
    Therefore, this change will not increase the probability of 
    occurrence or consequences of an accident previously evaluated.
        Suppression Pool Level and Temperature
        The changes to TS section 3/4.7.F, ``Suppression Pool Level and 
    Temperature'', are intended to clarify these requirements and make 
    them more consistent with STS. The revision to the applicability 
    statement which deletes the requirement for suppression pool level 
    and temperature to be within the specified limits during work which 
    has the potential to drain the vessel is in accordance with STS. 
    Suppression pool level and temperature limits ensure that the 
    suppression pool has the capability of acting as a heat sink for 
    design basis events but are not appropriate or applicable during the 
    refueling or cold shutdown conditions. No changes have been made to 
    the actual suppression pool temperature or level limits and 
    therefore, the assumptions made in the accident and transient 
    analyses remain valid. These limits are consistent with the STS. The 
    revisions to the surveillance requirements are also intended to 
    improve clarity and consistency with STS. The deletion of the 
    requirement to monitor suppression pool water temperature every 5 
    minutes during relief valve operation is appropriate in that plant 
    operating and emergency operating procedures already specify what 
    actions are to be taken when suppression pool average water 
    temperature increases above 95 deg.F including initiation of 
    suppression pool cooling. Monitoring pool temperature every 5 
    minutes during these events is not necessary and is redundant to 
    other actions. Therefore, these changes will not significantly 
    increase the probability of occurrence of the consequences of an 
    accident previously evaluated.
        Containment Atmosphere Dilution
        The revisions to the applicability of TS section 3.7.H, 
    ``Containment Atmosphere Dilution'', requiring the containment 
    atmosphere dilution system to be operable only when the reactor is 
    in power operation and the primary containment is required to be 
    inerted will not significantly increase the probability or 
    consequences of an accident previously evaluated because the CAD 
    system can only function when the containment is inerted. The 
    function of the CAD system is to inject nitrogen into the 
    containment after a LOCA and ensure the containment remains inerted. 
    Drywell inspections performed after plant startup and prior to plant 
    shutdown require that the primary containment be de-inerted for 
    personnel access. Therefore, CAD system operability is not required 
    during these inspections. No changes to the actual function or 
    purpose of the CAD system are proposed.
        Oxygen Concentration
        The changes to TS section 3/4.7.1, ``Oxygen Concentration'' are 
    administrative in that they only clarify the requirement that both 
    the suppression chamber and the drywell must have oxygen 
    concentrations less than 4 [percent] by volume. The revisions to the 
    surveillance requirements are consistent with STS. Decreasing the 
    frequency of verification of oxygen concentration from twice per 
    week to once per week is in accordance with STS and reflects the 
    fact that during power operation, the containment is inerted and 
    slightly pressurized such that air (oxygen) cannot leak into the 
    containment. Therefore, these changes will not significantly 
    increase the probability or consequences of an accident previously 
    evaluated.
        Secondary Containment
        The deletion of the requirement to operate the SGTS immediately 
    after a secondary containment violation is identified will not 
    affect the reliability of the secondary containment in that 
    containment integrity is normally fully restored immediately after a 
    violation is identified. The testing of the SGTS involves insertion 
    of a Group III containment isolation signal and is only appropriate 
    if the restoration of secondary containment involves a temporary or 
    new secondary containment boundary. These modifications to a 
    secondary containment boundary, however, would require that the SGTS 
    be operated as part of post modification testing. Deleting the 
    requirement for the SGTS to be operated after minor secondary 
    containment violations will reduce the possibility of human error 
    (such as misalignment of valves after the system is returned to its 
    normal configuration) due to reduced testing. Operation of the SGTS 
    after a secondary containment violation is not required by STS.
        Revision of the definition of calm wind conditions will not 
    affect the reliability or availability of the secondary containment 
    or SGTS. An engineering evaluation on the effects of wind speed and 
    direction on the ability of the SGTS to maintain 1/4'' vacuum in 
    secondary containment has been performed. The results indicate that 
    while wind effects can be seen on individual instruments, there is 
    minimal effect on the average instrument readings with wind speeds 
    up to 15 mph. A discussion of this evaluation has been added to the 
    Bases of TS section 3.7. Therefore, these changes will not 
    significantly increase the probability or the consequences of an 
    accident previously evaluated.
        Secondary Containment Automatic Isolation Dampers
        The addition of operability requirements, actions and 
    surveillance requirements for secondary containment isolation 
    dampers better ensures the integrity and isolation capability of the 
    secondary containment. The new specifications are consistent with 
    the requirements of the STS. The actual function or operation of the 
    secondary containment isolation valves/dampers will not be affected. 
    The appropriate valves/dampers will be incorporated in plant 
    procedures that are subject to the change control provisions of TS. 
    Therefore, these changes will not increase the probability of 
    occurrence or consequences of an accident previously evaluated in 
    the TS.
        Standby Gas Treatment System
        The change to the output requirements of the inlet heaters for 
    each train of the SGTS from 11 kw to 22 kw better ensures that these 
    heaters (and the SGTS) can perform their design function. The 22 kw 
    output requirement ensures that the inlet air humidity does not 
    exceed the 70 [percent] humidity specified in the UFSAR. This change 
    does not affect the actual operation of the heaters or the SGTS.
        The requirement to demonstrate the HEPA filter uniform air 
    distribution after HEPA filter replacement or after structural 
    maintenance on the filter system housing (rather than annually) will 
    not decrease the reliability of the SGTS. The air flow test will be 
    performed after work or modifications which have the ability to 
    disrupt the system geometry or result in potential flow blockage.
        Revising the shutdown LCO requirement in the various 
    specifications from requiring the plant to be in Cold Shutdown in 24 
    hours to requiring Hot Shutdown in 12 hours and Cold Shutdown (or 
    other condition not requiring equipment operability) in the 
    following 24 hours is consistent with STS and the shutdown 
    requirements in TS section 3.5. This new requirement will allow the 
    reactor to be shutdown in a more controlled manner and will not 
    result in a significant increase in the probability or consequences 
    of an accident previously evaluated.
        The revisions to the Bases are administrative in that they only 
    reflect the changes to the individual specifications described 
    previously in this section or correct minor discrepancies. All 
    changes are consistent with the applicable specifications.
        (2) The proposed amendment will not increase the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated for the following reasons.
        As described in the above response to question 1, none 
    of the proposed changes alters the design of the plant or equipment 
    or the plant's transient response. The changes to the definitions 
    and limiting conditions for operation applicable to TS section 3.7 
    are consistent with STS and better ensure that equipment assumed to 
    be operable in our accident analysis will be operable upon demand. 
    The addition of limiting conditions for operation for drywell 
    average temperature and secondary containment isolation valves will 
    better ensure that the assumptions in our accident analysis remain 
    valid.
        The changes to the surveillance requirements are consistent with 
    the STS. Those systems required to mitigate accidents evaluated in 
    the UFSAR will still be operable and available.
        The reduction in conditional surveillance testing of certain 
    systems and equipment will reduce the probability of equipment 
    failure as a result of excessive testing or due to human error.
        (3) The proposed amendment will not involve a significant 
    reduction in a margin of safety for the following reasons.
        The revisions to the limiting conditions for operation in 
    Chapter 3.7 of the TS will not invalidate the original licensing 
    basis assumptions and will not invalidate any assumptions or input 
    parameters for any DAEC event analysis. These changes provide more 
    specific guidance only and are in accordance with the STS. Extending 
    the time period within which the DAEC must achieve Cold Shutdown 
    conditions will permit increased operator attention and minimal 
    distractions for operators during shutdown, thus minimizing the 
    risks of unexpected operational transients.
        Additional surveillance testing for certain instrumentation and 
    systems will provide additional assurance that these systems will be 
    available when needed.
        Elimination of unnecessary or conditional surveillance testing 
    will not reduce the minimum necessary equipment operability 
    requirements or equipment reliability. Elimination of the redundant 
    testing will reduce equipment failure due to excessive testing or 
    human error.
        In summary, the proposed administrative changes do not change 
    the probability or consequences of an accident previously evaluated, 
    do not create the possibility of a new or different kind of accident 
    and do not involve a reduction in the margin of safety.
        Therefore, the proposed license amendment is judged to involve 
    no significant hazards consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    thisreview, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, S.E., Cedar Rapids, Iowa 52401.
        Attorney for licensee: Jack Newman, Esquire, Kathleen H. Shea, 
    Esquire, Newman and Holtzinger, 1615 L Street, NW., Washington, DC 
    20036
        NRC Project Director: John N. Hannon
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of amendment request: May 27, 1974
        Description of amendment request: The amendment would temporarily 
    allow the Operations Manager to not have a senior reactor operator 
    (SRO) license for Millstone 3, providing other conditions are met.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:...The proposed change does not 
    involve an SHC [significant hazards consideration] because the change 
    would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change affects only an administrative control, 
    which was based on the existing industry guidance in ANSI N18.1-
    1971, that recommended the Operations Manager hold a SRO license. 
    The current guidance in Section 4.2.2 of ANSI/ANS-3.1-1987 
    recommends, as one option, that the Operations Manager have held a 
    license for a similar unit and the Operations Middle Manager hold a 
    SRO license. The Operations Middle Manager position does not exist 
    at NNECO [Northeast Nuclear Energy Company]. Therefore, the proposed 
    change requests an exception to ANSI N18.1-1971 to allow use of 
    ANSI/ANS-3.101987 in a limited circumstance. Specifically, the 
    proposed revision to Technical Specification 6.3.1 would temporarily 
    allow the Operations Manager to have held a SRO at a PWR 
    [pressurized water reactor] other than Millstone Unit No. 3. The 
    proposed revision would be in effect for the period ending three 
    years after the Staff's approval for this request.
        The proposed exception to ANSI N18.1-1971 will allow at least 
    one of the Operations Assistants (instead of a Operations Middle 
    Manager) to hold, and continue to hold, a SRO license, if the 
    Operations Manager does not hold a license. The proposed change 
    includes the requirement if the Operations Manager does not hold a 
    SRO license at Millstone Unit No. 3, he shall have held a license 
    for a similar unit in accordance with Section 4.2.2 of ANSI/ANS-3.1-
    1987. For those areas of knowledge that require a SRO license, at 
    least one of the Operations Assistants hold a SRO license and 
    provides technical guidance normally required by the Operations 
    Manager.
        The proposed change does not alter the design of any system, 
    structure, or component. It does not change the way any plant 
    systems are operated. It does not reduce the knowledge, 
    qualifications, or skills of any operator on watch, and does not 
    affect the way the Operations Department is managed by the 
    Operations Manager in maintaining the effective performance of his 
    personnel and to ensure the plant is operated safely and in 
    accordance with the requirements of the Operating License.
        The proposed change does not detract from the Operations 
    Manager's ability to perform his primary responsibilities. In this 
    case, by having previously held a SRO license for a similar unit, he 
    will have gained the necessary training, skills, and experience to 
    fully understand the operation of plant equipment and the watch 
    requirements for operators.
        The proposed change does not weaken the supervisory chain that 
    presently exists in the Operations Department. All Control Room 
    operators will continue to be supervised by the licensed Shift 
    Supervisor.
        In summary, the proposed change does not affect the ability of 
    the Operations Manager to provide the plant oversight required of 
    his position. In addition, it does not have any [e]ffect on the 
    probability or consequences of any previously evaluated accident.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated.
        The proposed change to Technical Specification 6.3.1 does not 
    affect the design or function of any plant system, structure, or 
    component. It does not affect, in any way, the performance of NRC 
    licensed operators, nor does it change the way any plant equipment 
    is operated. Operation of the plant in conformance with technical 
    specifications and other license requirements will continue to be 
    supervised by personnel who hold an NRC SRO license. The proposed 
    change to Technical Specification 6.3.1 ensures that the Operations 
    Manager will be a knowledgeable and qualified individual. The 
    proposed change does not introduce any new failure modes.
        3. Involve a significant reduction in a margin of safety.
        The proposed change involves only an administrative control 
    which is not related to the margin of safety as defined in the 
    technical specifications. The proposed change does not reduce the 
    level of knowledge or experience required of an individual who fills 
    the Operations Manager position, nor does it affect the conservative 
    manner in which the plant is operated. All Control Room operators 
    will continue to be supervised by personnel who hold a SRO license.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, Connecticut 06360.
        Attorney for licensee: Gerald Garfield, Esquire, Day, Berry & 
    Howard, City Place, Hartford, Connecticut 06103-3499.
        NRC Project Director: John F. Stolz
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: May 31, 1994
        Description of amendment request: This amendment will change the 
    frequency for monitoring the Spray Pond ground water level from once 
    per month to once every six months in Technnical Specification 
    Requirement 4.7.1.3.c for each Susquehanna unit.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        I. This proposal does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed Technical Specification change to extend the 
    monthly surveillance interval for Spray Pond ground water level 
    measurement to biannual does not affect the the probability or 
    consequences of an accident previously evaluated. The safety 
    analysis performed for this change concludes that the ground water 
    level is stable, predictable, and significantly below the acceptance 
    criteria established in the Technical Specifications. Thus, less 
    frequent monitoring of the ground water level does not increase the 
    probability that the Spray Pond will become inoperable due to rising 
    ground water levels or the probability of any accident scenarios 
    associated with Spray Pond inoperability. The Technical 
    Specification change will not impact the function or the method of 
    operation of plant systems, structures, or components. Thus, the 
    consequences of a malfunction of equipment important to safety 
    previously evaluated in the FSAR are not increased by the change.
        II. This proposal does not create the possibility of a new or 
    different kind of accident or from any accident previously 
    evaluated.
        The proposed Technical Specification change to extend the 
    monthly surveillance interval for Spray Pond ground water level 
    measurement to biannual does not create the possibility of a new or 
    different kind of accident or from any accident previously 
    evaluated. The proposed change dies not affect systems, structures, 
    or components (SSCs) or the operation of the SSCs; and therefore 
    does not create the possibility of a new or different kind of 
    accident.
        III. This change does not involve a significant reduction in a 
    margin of safety.
        The proposed Technical Specification change to extend the 
    monthly surveillance frequency to biannual does not reduce the 
    margin of safety. The ground water level in the vicinity of the 
    Spray Pond has been proven to be stable and predictable through 
    twelve years of monthly data collection. This data has shown the 
    highest ground water levels (still considerably lower than the 
    Technical Specification limit) to occur in the months of April and 
    October. Therefore, surveillance of the ground water level at the 
    observation sites during April and October will adequately monitor 
    this aspect of the Spray Pond operability.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: Charles L. Miller
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of amendment request: May 25, 1994
        Description of amendment request: Salem is in the process of 
    upgrading the Radiation Monitoring System. This upgrade will involve a 
    replacement on many of the existing radiation monitors. The proposed 
    change modifies Tables associated with Technical Specifications 3/
    4.3.3.1 Radiation Monitoring Instrumentation, 3/4.3.3.8 Radioactive 
    Liquid Effluent Monitoring Instrumentation, and 3/4.3.3.9 Radioactive 
    Gaseous Effluent Monitoring Instrumentation. The proposed change 
    relocates the Salem specific radiation monitor numbers from the table 
    to a cross reference in the Bases. No required radiation monitoring 
    functions are being changed.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. [This proposal does not involve] a significant increase in 
    the probability or consequences of an accident previously analyzed.
        The proposed change to relocate the Salem specific radiation 
    monitor numbers to the Bases is administrative. There are no 
    modifications or changes in operating conditions associated with the 
    proposed changes. Providing a more accurate description of a 
    referenced radiation monitor in the note is editorial. The proposed 
    changes do not affect the probability of occurrence or the 
    consequences of accidents identified in the UFSAR. No accident 
    precursors are being generated by the proposed changes. Therefore, 
    the proposed changes do not involve a significant increase in the 
    probability or consequences of a previously analyzed accident.
        2. [This proposal does not create] the possibility of a new or 
    different kind of accident.
        The proposed changes to relocate the Salem specific radiation 
    monitor numbers to the Bases are administrative. The change to the 
    note on Table 3.3-6 is editorial to provide a more accurate 
    description of the required radiation monitor. There are no 
    modifications or changes in operating conditions associated with the 
    proposed changes. Therefore, the proposed changes will not increase 
    the possibility of a new or different kind of accident from any 
    accident previously identified.
        3. [These changes do not involve] a significant reduction in a 
    margin of safety.
        The Technical Specification operability requirements for the 
    radiation monitors are not being changed. Relocating the Salem 
    specific radiation monitor numbers to the Bases will not change any 
    requirements for the radiation monitors. The change to the note on 
    Table 3.3-6 is editorial to provide a more accurate description of 
    the required radiation monitor. Therefore, the changes to the 
    surveillance frequencies do not involve a significant reduction in 
    any margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public library, 112 
    West Broadway, Salem, New Jersey 08079
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502
        NRC Project Director: Charles L. Miller
    
    Rochester Gas and Electric Corporation, Docket No. 50-244, R. E. 
    Ginna Nuclear Power Plant, Wayne County, New York
    
        Date of amendment request: May 23, 1994, as supplemented June 15, 
    1994
        Description of amendment request: The proposed amendment would 
    revise the Ginna Station Technical Specification (TS) 3.1.4 regarding 
    allowable primary coolant levels of specific activity. The limit for I-
    131 dose equivalent of iodine activity in the reactor coolant would be 
    increased from 0.2 to 1.0 micro Ci/gm. The limit for total specific 
    activity of the reactor coolant would be increased from 84 to 100/E 
    micro Ci/gm, where E is the average beta and gamma energies per 
    disintegration in Mev. Both increased allowable levels are consistent 
    with NUREG-1431 ``Standard Technical Specifications, Westinghouse 
    Plants, September 1992,'' and NUREG-0800 ``Standard Review Plan for the 
    Review of Safety Analysis Reports for Nuclear Power Plants'' (Section 
    15.6.3).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The proposed changes do not affect any accident initiators and 
    therefore the probability of any accident is not increased. 
    Consequences of the changes are analyzed and shown acceptable in the 
    [Westinghouse LOFTTR2 Analysis of Potential Radiological 
    Consequences Following a Steam Generator Tube Rupture at the R.E. 
    Ginna Nuclear Power Plant] analysis, WCAP-11668, Section III.
        2. Operation of Ginna Station in accordance with the proposed 
    changes does not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        The proposed changes involve no physical modifications to the 
    plant; therefore, no new accident can be postulated.
        3. Operation of Ginna Station in accordance with the proposed 
    changes does not involve a significant reduction in a margin of 
    safety, as no margin of safety is reduced by the proposed changes, 
    as shown in WCAP-11668.
        Based upon the above information, it has been determined that 
    the proposed changes to the Ginna Station Technical Specifications 
    do not involve a significant increase in the probability or 
    consequences of an accident previously evaluated, does not create 
    the possibility of a new or different kind of accident previously 
    evaluated, and does not involve a significant reduction in a margin 
    of safety. Therefore, it is concluded that the proposed changes meet 
    the requirements of 10 CFR 50.92(c) and do not involve a significant 
    hazards consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Rochester Public Library, 115 
    South Avenue, Rochester, New York 14610
        Attorney for licensee: Nicholas S. Reynolds, Winston & Strawn, 1400 
    L Street, NW., Washington, DC 20005
        NRC Project Director: Walter R. Butler
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of amendment request: June 6, 1994
        Description of amendment request: The proposed amendment would 
    merge Toledo Edison Company into Cleveland Electric Illuminating 
    Company. As described in the application, the company formed from the 
    merger is intended to be renamed. Therefore, the licensee uses the 
    nomenclature ``NEWCO'' as a temporary name of the combined operating 
    company, and will provide the permanent name by supplemental letter. 
    The amendment would (1) replace the Toledo Edison Company and Cleveland 
    Electric Illuminating Company with ``NEWCO'' as a licensee, (2) 
    designate ``NEWCO'' as the owner of the Davis-Besse Nuclear Power 
    Station, Unit 1, and (3) make other associated changes to the license 
    as indicated in the amendment application. Centerior Service Company 
    would be unaffected by the amendment and would remain a licensee.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below, indicating that the proposed 
    changes would:
        1a. Not involve a significant increase in the probability of an 
    accident previously evaluated because no accident initiators or 
    assumptions are affected. The proposed changes are administrative 
    and have no direct affect on any plant systems. All Limiting 
    Conditions for Operation, Limiting Safety System Settings and Safety 
    Limits specified in the Technical Specifications will remain 
    unchanged.
        1b. Not involve a significant increase in the consequences of an 
    accident previously evaluated because no accident conditions or 
    assumptions are affected. The proposed changes do not alter the 
    source term, containment isolation, or allowable radiological 
    consequences. The proposed changes are administrative and have no 
    direct effect on any plant systems.
        2a. Not create the possibility of a new kind of accident from 
    any accident previously evaluated because no new accident initiators 
    are created. The proposed changes are administrative and have no 
    direct effect on any plant systems. The changes do not affect the 
    reactor coolant system pressure boundary and do not affect any 
    system functional requirements, plant maintenance, or operability 
    requirements.
        2b. Not create the possibility of a different kind of accident 
    from any accident previously evaluated because no different accident 
    initiators are created. The proposed changes are administrative and 
    have no direct effect on any plant systems. The changes do not 
    affect the reactor coolant system pressure boundary and do not 
    affect any system functional requirements, plant maintenance, or 
    operability requirements.
        3. Not involve a significant reduction in the margin of safety 
    because the proposed changes do not involve new or significant 
    changes to the initial conditions contributing to accident severity 
    or consequences. The proposed changes are administrative and have no 
    direct affect on any plant systems.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John N. Hannon
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, 
    Vermont Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of amendment request: May 20, 1994
        Description of amendment request: The proposed amendment would 
    remove Core Spray (CS) High Sparger Pressure Instrumentation from the 
    Vermont Yankee Technical Specifications for Emergency Core Cooling 
    System (ECCS) Actuation Instrumentation. In addition, an unrelated 
    administrative change is also proposed.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change to remove the Core Spray High Sparger 
    Pressure Instrumentation from the Technical Specifications for ECCS 
    Actuation Instrumentation is consistent with NRC requirements 
    concerning this instrumentation. This instrumentation is considered 
    NNS [nonnuclear safety] and performs a local monitoring and alarm 
    function only. In addition, the NRC has recently approved the 
    removal of Core Spray Sparger Break Detection Instrumentation from 
    the Technical Specifications of another BWR [boiling water reactor] 
    with a similar situation.
        The CS Sparger Piping is inspected every refueling outage to 
    verify its integrity. No cracks in the CS Sparger piping have been 
    identified since the first inspection in 1980. CS Sparger Piping 
    integrity is still assured. The instrumentation systems to be 
    removed from the ECCS Actuation Instrumentation Technical 
    Specifications do not perform any automatic control or trip 
    function. In addition, this instrumentation does not provide 
    information that is required to permit the control room operator to 
    take manual actions that are required for safety systems to 
    accomplish their safety functions for design basis accident events.
        The proposed change does not result in any system hardware 
    modification, function change or new plant configuration. The 
    requested change to ECCS Actuation Instrumentation does not impact 
    any FSAR [Final Safety Analysis Report] safety analysis involving 
    the ECCS or Protection Systems. These monitoring functions are not 
    contributors to the initiation of accidents.
        The administrative changes to correct typographical errors on 
    Tables 3.2.1 and 4.2.1 will have no affect on plant hardware, plant 
    design, safety limit setting or plant system operation and 
    therefore, do not modify or add any initiating parameters that would 
    significantly increase the probability or consequences of any 
    previously analyzed accident.
        Therefore, it is concluded that there is not a significant 
    increase in the probability or consequence of an accident previously 
    evaluated.
        2. The function of the Core Spray High Sparger Pressure 
    Instrumentation to be removed from the Technical Specifications is 
    for local indication and alarm only. These functions are not 
    necessary for operators to accomplish any safety functions.
        The proposed change does not involve any change in hardware, 
    function, Technical Specification trip setpoints, plant operation, 
    redundancy, protective function or design basis of the plant. There 
    is no impact on any existing safety analysis or safety design 
    limits. Core Spray High Sparger Pressure Instrumentation functions 
    do not initiate nuclear system parameter variations which are 
    considered potential initiating causes of threats to the fuel and 
    the nuclear system process barrier.
        As discussed above, the proposed administrative change only 
    corrects typographical errors concerning equipment identification 
    numbers. This change doe not affect any equipment and it does not 
    involve any potential initiating events that would create any new or 
    different kind of accident.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change to remove the Core Spray High Sparger 
    Pressure Instrumentation from the Technical Specifications for ECCS 
    Actuation Instrumentation does not affect any existing safety 
    margins. This equipment is NNS and performs a local indication and 
    alarming function only. The original intent of this detection system 
    was because the first BWR plants had only the CS System for long-
    term core cooling. Later, plants like VY [Vermont Yankee] were 
    provided with Low Pressure Coolant Injection (LPCI) Systems in 
    addition to CS.
        Existing Technical Specification requirements for automatic trip 
    functions are unaffected. Failure of the Core Spray High Sparger 
    Pressure Instrumentation does not preclude the ability of the CS 
    System to perform its safety function to mitigate the consequences 
    of accidents or of any other safety system to accomplish its safety 
    functions. Proper ECCS functioning post-accident is not relied upon 
    by NNS alarming functions but by such systems as safety related 
    reactor level indication.
        The CS Sparger Piping is inspected every refueling outage to 
    verify its integrity. No cracks in the CS Sparger piping have been 
    identified since the first inspection in 1980. The removal from the 
    Technical Specifications has no affect on the bases of Protective 
    Instrumentation which is to operate to initiate required system 
    protective actions. The Core Spray High Sparger Pressure 
    Instrumentation does not perform any safety function.
        As discussed above, the proposed administrative change which 
    corrects typographical errors does not affect any equipment involved 
    in potential initiating events or safety limits. [***].
        Based upon the above, it is concluded that the proposed changes 
    do not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, Vermont 05301
        Attorney for licensee: John A. Ritsher, Esquire, Ropes and Gray, 
    One International Place, Boston, Massachusetts 02110-2624
        NRC Project Director: Walter R. Butler
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of amendment request: March 18, 1992, modifications submitted 
    June 25 and July 28, 1992, and December 6, 1993
        Description of amendment request: On December 6, 1993, the licensee 
    submitted a significant modification to its original request of March 
    18, 1992 (April 19, 1992 (57 FR 12349)). The modified request would 
    amend the Technical Specifications (TS) to provide two surveillance 
    tests to determine the operability of the catalyst beds in the 
    containment atmospheric control (CAC) system. One test compares 
    hydrogen content in the influent to the hydrogen content in effluent 
    process streams to assure the catalyst is operating. The second test 
    measures the temperature profile in the catalyst bed to ensure that 
    sufficient catalyst remains available for the recombination process 
    during postulated accident conditions. Since the original proposal has 
    been significantly changed, the staff is issuing a new notice and 
    proposed no significant hazards consideration determination.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The staff's review is 
    presented below:
        1. Does the amendment involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change does not involve any changes in the design 
    or operation of the hydrogen recombiners, which are accident 
    mitigation systems. The proposed change revises surveillance 
    requirements to ensure that existing equipment will perform as 
    designed in response to postulated events. The proposed change does 
    not, therefore, involve an increase in the probability or 
    consequences of an accident previously evaluated.
        2. Does the amendment create the possibility of a new or 
    different kind of accident from any accident previously evaluated?
        The proposed change does not involve any changes in the design 
    or operation of existing equipment, and does not, therefore, create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. Does the amendment involve a significant reduction in a 
    margin of safety?
        The proposed change increases surveillance requirements for 
    existing equipment to ensure that the equipment will perform as 
    designed. With equipment performing as designed in response to 
    postulated accidents, the proposed change does not affect any 
    existing margins of safety.
        Based on the licensee's analysis and the staff's analysis, it 
    appears that the three standards of 10 CFR 50.92(c) are satisfied. 
    Therefore, the NRC staff proposes to determine that the amendment 
    request involves no significant hazards consideration.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
        Attorney for licensee: Nicholas S. Reynolds, Esq., Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502
        NRC Project Director: Theodore R. Quay
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: March 31, 1994
        Description of amendment request: The proposed amendment would 
    revise the Kewaunee Nuclear Power Plant Technical Specifications (TS) 
    by incorporating operability and surveillance requirements for the 
    recently installed Auxiliary Feedwater Pump Low Discharge Pressure Trip 
    instrumentation. Proposed surveillance requirements would be added to 
    Table TS 4.1-1, ``Minimum Frequencies for Checks, Calibrations and Test 
    of Instrument Channels.'' TS 3.4, ``Steam and Power Conversions 
    System,'' would be revised to explicitly link operability of the 
    associated Auxiliary Feedwater Pump Low Discharge Pressure Trip channel 
    to operability of the associated auxiliary feedwater pump. In addition, 
    minor format inconsistencies in TS 3.4.b.1.A and 3.4.b.1.B would be 
    corrected.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (a) Table TS 4.1-1
        The proposed changes were reviewed in accordance with the 
    provisions of 10 CFR 50.92 to show no significant hazards exist. The 
    proposed changes will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change defines the necessary surveillance 
    requirements for the recently installed Auxiliary Feedwater Pump Low 
    Discharge Pressure Trip channels. The intent of adding surveillance 
    requirements to the TS's is to ensure the availability and 
    reliability of the components. The proposed change is an additional 
    restriction not presently included in the TS's. Therefore, it will 
    not increase the probability or consequences of an accident 
    previously evaluated in the USAR.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed change adds surveillance requirements to the TS for 
    the Auxiliary Feedwater Low Discharge Pressure Trip channels. It 
    does not alter the plant configuration or overall plant performance. 
    Therefore, it does not create the possibility of a new or different 
    kind of accident.
        3. Involve a significant reduction in the margin of safety.
        This proposed revision is an additional requirement in the TS's 
    to ensure the availability and reliability of the Auxiliary 
    Feedwater Pump Low Discharge Pressure Trip channels. It does not 
    alter the input or assumptions of the safety analysis, and is an 
    enhancement from an overall safety standpoint. Therefore, it will 
    not involve a reduction in the margin of safety.
        (b) TS 3.4
        The proposed changes were reviewed in accordance with the 
    provision of 10 CFR 50.92 to show no significant hazards exist. The 
    proposed changes will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change defines the necessary operability 
    requirements for the recently installed Auxiliary Feedwater Pump Low 
    Discharge Pressure Trip channels. Installation of this protection 
    was recommended and approved by the NRC prior to their installation. 
    The proposed change requires that the reactor not be heated 
     350 deg.F unless both motor driven Auxiliary Feedwater 
    Pumps and their associated low discharge pressure trip channels are 
    operable. Also, the reactor shall not be heated  
    350 deg.F unless the turbine driven auxiliary feedwater pump and its 
    associated low discharge pressure trip channel are operable, or if 
    not demonstrated operable prior to  350  deg.F, they 
    shall be declared inoperable when 350 deg.F is exceeded. 
    Furthermore, when the reactor is  350 deg.F, an auxiliary 
    feedwater pump low discharge pressure trip channel may be inoperable 
    for a period not to exceed 4 hours. If this time is exceeded, the 
    associated auxiliary feedwater pump shall be declared inoperable and 
    the appropriate limiting condition for operation of TS 3.4.b.2 
    entered. The intent of adding these operability requirements to the 
    TS's is to ensure the availability of the components. The proposed 
    change is an additional restriction not presently included in the 
    TS's. Therefore, it will not increase the probability or 
    consequences of an accident previously evaluated in the USAR.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed change adds operability requirements to the TS for 
    the Auxiliary Feedwater Pump Low Discharge Pressure Trip channels. 
    It does not alter the plant configuration or overall plant 
    performance. Therefore, it does not create the possibility of a new 
    or different kind of accident.
        3. Involve a significant reduction in the margin of safety.
        This proposed revision is an additional requirement in the TS's 
    to ensure the operability of the Auxiliary Feedwater Pump Low 
    Discharge Pressure Trip channels. It does not alter the input or 
    assumptions of the safety analysis, and is an enhancement from an 
    overall safety standpoint. Therefore it will not involve a reduction 
    in the margin of safety
        (c) Administrative changes to TS 3.4.b.1.A and TS 3.4.b.1.B
        The proposed changes were reviewed in accordance with the 
    provision of 10 CFR 50.92 to show no significant hazards exist. The 
    proposed changes will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated, or
        2. Create the possibility of a new or different kind of accident 
    from an accident previously evaluated, or
        3. Involve a significant reduction in the margin of safety.
        The proposed changes are administrative in nature and do not 
    alter the intent of interpretation of the TS. Therefore, no 
    significant hazards exist.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin 
    Library Learning Center, 2420 Nicolet Drive, Green Bay, Wisconsin 
    54301.
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P. O. Box 1497, Madison, Wisconsin 53701-1497.
        NRC Project Director: John N. Hannon
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: May 24, 1994
        Description of amendment request: The amendment request proposes to 
    revise the Technical Specifications (TS) to implement the NRC's Final 
    Policy Statement on Technical Specification Improvements for Nuclear 
    Power Reactors (58 FR 39132). These improvements involve focusing the 
    Technical Specifications on those requirements that are of controlling 
    importance to operational safety by screening each TS in Section 3/4.1 
    through 3/4.11 using the criteria provided in the policy statement. The 
    purpose of the proposed amendment request is to relocate the 
    specifications that do not meet any of the four policy statement 
    criteria. The relocated specifications will be moved to Updated Final 
    Safety Analysis (USAR) Chapter 16. Based on the screening, all or part 
    of 38 technical specifications were identified as not meeting any of 
    the criteria and, therefore, as candidates for relocation. The licensee 
    has categorized the TS changes as (1) specifications relocated intact 
    to USAR Chapter 16, (2) specifications relocated with portions retained 
    in TS, (3) specifications relocated with programmatic requirements 
    referenced in Section 6 of TS, (4) modifications to retained 
    specifications to accomodate relocation of other specifications, and 
    (5) new specification requirements incorporated into the TS. The last 
    category is used to effect the retention of portions of relocated 
    specifications and accomodate the policy statement recommendation to 
    incorporate industry experience in the determination of TS content.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed Technical Specification changes involve relocating 
    requirements that are not conditions or limitations on reactor 
    operation necessary to obviate the possibility of an abnormal 
    situation or event giving rise to an immediate threat to the public 
    health and safety. The proposed changes were identified through the 
    application of criteria designed to cull those requirements that are 
    not important to operational safety from the Technical 
    Specifications. In this process, selected provisions of the 
    Technical Specifications identified for relocation were retained if 
    necessary to support a Technical Specification that was to be 
    retained. Thus, only specification requirements that have little or 
    no operational safety significance are proposed for relocation. In 
    addition, those requirements that would be relocated will be 
    included in the Updated Final Safety Analysis Report (USAR) and, 
    therefore, will be controlled and implemented as NRC commitments. In 
    this manner, those requirements that have no operational safety 
    significance but involve maintaining the plant in its as-designed 
    state (for example, through surveillance programs) would be 
    controlled.
        In addition, the criteria for identifying requirements to be 
    retained in the Technical Specifications specifically call out, for 
    retention, those structures, systems, or components that are 
    required to mitigate accidents previously evaluated.
        Based on the above, the proposed changes do not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed changes do not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        The proposed changes involve relocating Technical Specification 
    requirements to another licensee-controlled document. No changes or 
    physical alterations of the plant are involved. Also, no changes to 
    the operation of the plant or equipment are involved. Therefore, the 
    proposed changes do not create the possibility of a new or different 
    kind of accident from any previously evaluated.
        3. Do the proposed changes involve a significant reduction in 
    the margin of safety.
        The proposed changes involve relocating Technical Specification 
    requirements to the USAR. The requirements to be relocated were 
    identified by applying the criteria endorsed in the Commission's 
    Policy Statement. Thus, those specifications that would be relocated 
    do not impose constraints on design and operation of the plant that 
    are derived form the plant safety analysis report or from 
    probabilistic safety assessment (PSA) information and do not belong 
    in the Technical Specifications in accordance with 10 CFR 50.36 and 
    the purpose of the Technical Specifications stated in the Policy 
    Statement. Therefore, relocation of these requirements does not 
    involve a significant reduction in the margin of safety.
        In addition, revisions to the USAR will be evaluated in 
    accordance with the 10 CFR 50.59 process which considers the 
    reduction in safety margin. Therefore, any future revisions to the 
    provisions in the USAR will consider reductions in the margin of 
    safety using the criteria for identifying an unreviewed safety 
    question.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Theodore T. Quay
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: June 7, 1994
        Description of amendment request: The proposed amendment revises 
    Technical Specification Table 2.2-1, Reactor Trip System 
    Instrumentation Setpoints, to change the over-temperature-delta-
    temperature (OTDT) axial flux difference (AFD) limits to reflect 
    results of the Cycle 8 core maneuvering analysis.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The probability of occurrence and the consequences of an 
    accident evaluated previously in the Updated Safety Analysis Report 
    (USAR) are not increased due to the proposed technical specification 
    change. Operation at 3565 MWt does not affect any of the mechanisms 
    postulated in the USAR to cause LOCA or non-LOCA design basis 
    events. Analyses, evaluations and minimum DNBR [departure from 
    nucleate boiling ratio] calculations confirm that the USAR 
    conclusions remain valid for the proposed changes. On these bases it 
    is concluded that the probability and consequences of the accidents 
    previously evaluated in the USAR are not increased.
        2. The proposed change does not create the possiblity of a new 
    or different kind of accident from any previously evaluated.
        There is no new type of accident or malfunction being created. 
    The proposed change provides revised operating limits necessary to 
    support Cycle 8, and does not change the method and manner of plant 
    operation. The safety design bases in the USAR have not been 
    altered. Thus, this change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in the margin of safety.
        The proposed changes do not change the plant configuration in a 
    way that introduces a new potential hazard to the plant and do not 
    involve a significant reduction in the margin of safety. The 
    analyses and evaluations discussed in the safety evaluation 
    demonstrate that all applicable safety analysis acceptance criteria 
    continue to be met for the proposed operating conditions. Items not 
    specifically cited in this safety evaluation have been reviewed and 
    have been found to be bounded by the evaluations performed for 
    Reference 1 [Wolf Creek Generating Station Technical 
    Specifications]. Therefore, it is concluded that the margin of 
    safety, as described in the bases to any technical specification, is 
    not reduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Theodore. R. Quay
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenberg County, North Carolina
    
        Date of amendment request: May 5, 1994, as supplemented June 16, 
    1994.
        Description of amendment request: The proposed amendments would 
    change the Technical Specifications to increase Main Steam and 
    Pressurizer Code Safety Valve Setpoint Tolerances.
        Date of publication of individual notice in Federal Register: June 
    21, 1994 (59 FR 32029).
        Expiration date of individual notice: July 21, 1994
        Local Public Document Room location:
        Atkins Library, University of North Carolina, Charlotte (UNCC 
    Station), North Carolina 28223.
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    rooms for the particular facilities involved.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of application for amendments: September 29, 1992, as 
    supplemented on October 22, 1993, and November 11, 1993.
        Brief description of amendments: The amendments revise the Site 
    Boundary Map and the Low Population Zone Map.
        Date of issuance: June 22, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 190 and 167
        Facility Operating License Nos. DPR-53 and DPR-69: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: October 28, 1992 (57 FR 
    48813) The Commission prepared an Environmental Assessment and Finding 
    of No Significant Impact which was published in the Federal Register on 
    May 13, 1994 (59 FR 25129). The Commission's related evaluation of 
    these amendments is contained in a Safety Evaluation dated June 22, 
    1994.No significant hazards consideration comments received: No
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station,Plymouth County, Massachusetts
        Date of application for amendment: February 11, 1993, as 
    supplemented December 2, 1993, January 5, February 22, March 1, April 
    15, and May 16, 1994.
        Brief description of amendment: This amendment increases the 
    allowed fuel assembly storage cells from 2320 to 3859, changes the 
    maximum loads allowed to travel over the spent fuel assemblies from 
    1050 to 2000 lbs., and changes the limiting characteristics of 
    assemblies to be stored in the spent fuel from a maximum KINIFITY 
    less than or equal to 1.35 to a Maximum KINIFITY less than or 
    equal to 1.32 and a maximum lattice average uranium enrichment of less 
    than or equal to 4.6% by weight.
        Date of issuance: June 22, 1994
        Effective date: June 22, 1994
        Amendment No.: 155
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 30, 1993 (58 FR 
    26171) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 22, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, IllinoisDocket 
    Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, Units 1 
    and 2, Rock Island County, IllinoisDate of application for 
    amendments: March 26, 1993
    
        Brief description of amendments: The amendments revise Technical 
    Specification 3/4.6 for Dresden and Quad Cities Stations to allow 
    Single Loop Operation (SLO) with the recirculation loop suction and 
    discharge valves open. The amendments also delete outdated and 
    unnecessary portions of Technical Specification 3.6.H for Dresden Units 
    2 and 3 and provide more consistency to the BWR Standard Technical 
    Specifications (NUREG-0123, Revision 4).
        Date of issuance: June 16, 1994
        Effective date: June 16, 1994
        Amendment Nos.: 127, 121, 147, and 143
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29 and DPR-30: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: April 13, 1994 (59 FR 
    17594) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 16, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: For Dresden, Morris Public 
    Library, 604 Liberty Street, Morris, Illinois 60450; for Quad Cities, 
    Dixon Public Library, 221 Hennepin Avenue, Dixon, Illinois 61021.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South CarolinaDate of 
    application for amendments: March 24, 1994, as supplemented April 
    11 and May 31, 1994
    
        Brief description of amendments: The amendments revise the 
    Technical Specification (TS) to increase boron concentration for the 
    spent fuel storage pool during Modes 1-3 operation and for the 
    refueling canal during Mode 6 operation; include two reload related 
    topical reports in TS 6.9.1.9; and correct errors in nomenclature and 
    remove obsolete footnotes.
        Date of issuance: June 13, 1994
        Effective date: June 13, 1994
        Amendment Nos.: 120 and 114
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 28, 1994 (59 FR 
    22006) The April 11 and May 31, 1994, letters provided clarifying and 
    additional information that did not change the scope of the March 24, 
    1994, application and the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated June 13, 1994.No 
    significant hazards consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    ConnecticutDate of application for amendment: December 17, 1993, as 
    supplemented April 12, 1994.
    
        Brief description of amendment: The amendment changes the action 
    statements for the limiting conditions for operation associated with 
    the electrical power sources (Technical Specification 3.8.1.1).
        Date of issuance: June 14, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 177
        Facility Operating License No. DPR-65. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 2, 1994(59 FR 
    4943). The April 12, 1994, letter provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated June 14, 1994.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resource Center, 
    Three Rivers Community-Technical College, Thames Valley Campus, 574 New 
    London Turnpike, Norwich, Connecticut 06360.
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New YorkDate of 
    application for amendment: December 28, 1993
    
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) Section 6.9(A)1.a. to permit startup reports for 
    cycles subsequent to the initial fuel cycle to address only those 
    startup tests that are actually performed. The amendment also revises 
    TS Section 6.9(A) to clarify requirements for the submission of routine 
    reports. These changes are consistent with the guidance provided in 
    NUREG-1433, ``Standard Technical Specifications - General Electric 
    Plants, BWR/4.''
        Date of issuance: June 16, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 212
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 2, 1994 (59 FR 
    4945) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 16, 1994.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: December 29, 1993
        Brief description of amendment: The amendment revises Appendix B of 
    the Technical Specifications (TSs), the Radiological Effluent TSs. 
    Specifically, the amendment revises Appendix B Surveillance Requirement 
    3.1.a. and Table 3.10-2 to provide surveillance requirements for data 
    recorders associated with the gaseous effluent monitoring system. The 
    amendment also makes an editorial change to Appendix B Limiting 
    Condition for Operation 3.1.a. to improve consistency and clarity.
        Date of issuance: June 16, 1994Effective date: As of the date of 
    issuance to be implemented within 30 days.
        Amendment No.: 213
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 2, 1994 (59 FR 
    4946) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 16, 1994.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Southern Nuclear Operating Company, Inc., Docket Nos. 50-348 and 
    50-364, Joseph M. Farley Nuclear Plant, Units 1 and 2, Houston 
    County, Alabama.
    
        Date of amendments request: May 13, 1991, as supplemented October 
    13, 1992.
        Brief description of amendments: The amendments modify the TS for 
    the overpressure protection systems. The allowable outage time (AOT) 
    for one inoperable residual heat removal (RHR) relief valve with one or 
    more of the reactor coolant system cold leg temperatures less than or 
    equal to 310 degrees Fahrenheit is being decreased from 7 days to 24 
    hours for water-solid conditions. The required AOT for low temperature 
    conditions, other than water-solid, will remain at 7 days with one RHR 
    relief valve inoperable, provided the pressurizer level is less than or 
    equal to 30 percent and a dedicated operator is assigned to monitor and 
    control the reactor coolant system pressure.
        Date of issuance: June 16, 1994
        Effective date: June 16, 1994
        Amendment Nos.: 108 and 100
        Facility Operating License Nos. NPF-2 and NPF-8. Amendments revise 
    the Technical Specifications.
        Date of initial notice in Federal Register: July 22, 1992 (57 FR 
    32577) and February 17, 1993 (58 FR 8787)The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    June 16, 1994.No significant hazards consideration comments received: 
    No
        Local Public Document Room location: Houston-Love Memorial Library, 
    212 W. Burdeshaw Street, Post Office Box 1369, Dothan, Alabama 36302
        Tennessee Valley Authority, Docket Nos. 50-259 and 50-296, Browns 
    Ferry Nuclear Plant, Units 1 and 3, Limestone County, Alabama
        Date of application for amendment: April 1, 1992 (TS 302)
        Brief description of amendments: The amendments add requirements to 
    the Browns Ferry Units 1 and 3 Technical Specifications to provide 
    administrative controls for a post-accident sampling system, which were 
    requested by Generic Letter 83-36, ``NUREG-0737 Technical 
    Specifications.''
        Date of issuance: June 21, 1994
        Effective date: June 21, 1994
        Amendment Nos.:207 and 180
        Facility Operating License Nos. DPR-33 and DPR-68:
        Date of initial notice in Federal Register: May 27, 1992 (57 FR 
    22269) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated June 21, 1994. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Athens Public Library, South 
    Street, Athens, Alabama 35611
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse 
    Nuclear Power Station, Unit No. 1, Ottawa County, Ohio
    
        Date of application for amendment: December 23, 1992, as 
    supplemented on March 18, 1994.
        Brief description of amendment: This amendment revises TS 3/4 3.3.5 
    for transfer switches used to meet 10 CFR Part 50, Appendix R (Fire 
    Protection) requirements, and specifies a new special report 
    requirement for TS 6.9.2.
        Date of issuance: June 14, 1994
        Effective date: June 14, 1994
        Amendment No. 187
        Facility Operating License No. NPF-3. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 2, 1994 (59 FR 
    10016) The supplemental information submitted on March 18, 1994, did 
    not change the initial proposed finding of no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated June 14, 1994.No 
    significant hazards consideration comments received: No
        Local Public Document Room location: University of Toledo Library, 
    Documents Department, 2801 Bancroft Avenue, Toledo, Ohio 43606.
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: December 20, 1993, as amended 
    March 25 and April 25, 1994
        Brief description of amendment: The amendment modifies the 
    technical specifications (TS) to address new containment purge and vent 
    valves to be installed in the 1994 refueling outage. The amendment 
    changes the containment purge and vent valve TS as follows: (1) removes 
    the requirement ensuring that valve position remains at less than or 
    equal to 70 degrees, (2) changes the containment leak testing 
    requirements for the metal-to-metal seated valves from 6 months to 2 
    years since they have improved seat designs, and (3) makes 
    administrative changes to delete an out-of-date note, to relocate an 
    action statement requirement from the TS surveillance section to the TS 
    action statement section, and to change a related TS reference to this 
    surveillance section. Valve opening position does not need to be 
    limited to less than or equal to 70 degrees. The resiliently-seated 
    valves have a permanently installed mechanical stop to limit the open 
    position to ensure adequate closure times. The metal-to-metal seated 
    valves are designed to close from the 90-degree open position.
        Date of issuance: June 15, 1994
        Effective date: 15 days from the date of issuance
        Amendment No.:  124
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 30, 1994 (59 FR 
    14901) The additional information contained in the March 25 and April 
    25, 1994, letters was clarifying in nature, is within the scope of the 
    initial notice, and did not affect the NRC staff's proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated June 15, 1994.Public comments on proposed no significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: February 8, 1994, as 
    supplemented March 25, 1994
        Brief description of amendment: The amendment revises the WNP-2 
    Technical Specifications. Specifically, the amendment increases the 
    stroke time, as specified in Table 3.6.3-1, for reactor core isolation 
    cooling (RCIC) valve RCIC-V-8 from 13 seconds to 26 seconds and deletes 
    the Note (j) reference from RCIC-V-8 and RCIC-V-63. Note (j) indicates 
    that the stroke time specified in the table reflects the requirement 
    for containment isolation only.
        Date of issuance: June 17, 1994
        Effective date: June 17, 1994
        Amendment No.: 125
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 12, 1994 (59 FR 
    24754) The additional information contained in the March 25, 1994, 
    letter was clarifying in nature, was within the scope of the initial 
    notice, and did not affect the NRC staff's proposed no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendment is contained in a Safety Evaluation dated 
    June 17, 1994.No significant hazards consideration comments received: 
    No.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352]
        Dated at Rockville, Maryland, this 28th day of June 1994.
        FOR THE NUCLEAR REGULATORY COMMISSION
    Jack W. Roe,
    Director, Division of Reactor Projects - III/IVOffice of Nuclear 
    Reactor Regulation
    [Doc 94-16174 Filed 7-5-94 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Published:
07/06/1994
Department:
Nuclear Regulatory Commission
Entry Type:
Uncategorized Document
Document Number:
94-16174
Dates:
As of the date of issuance to be implemented within 30 days.
Pages:
0-0 (1 pages)
Docket Numbers:
Federal Register: July 6, 1994