97-17990. Wisconsin Electric Power Company; Point Beach Nuclear Plant; Environmental Assessment and Finding of No Significant Impact  

  • [Federal Register Volume 62, Number 131 (Wednesday, July 9, 1997)]
    [Notices]
    [Pages 36852-36853]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 97-17990]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    [Docket Nos. 50-266 and 50-301]
    
    
    Wisconsin Electric Power Company; Point Beach Nuclear Plant; 
    Environmental Assessment and Finding of No Significant Impact
    
        The U.S. Nuclear Regulatory Commission (the Commission) is 
    considering issuance of amendments to Facility Operating License Nos. 
    DPR-24 and DPR-27, issued to Wisconsin Electric Power Company, (the 
    licensee), for operation of the Point Beach Nuclear Plant, Units 1 and 
    2, located in Manitowoc County, Wisconsin.
    
    Environmental Assessment
    
    Identification of the Proposed Action
    
        The proposed action would revise Technical Specification (TS) 
    15.3.3, ``Emergency Core Cooling System, Auxiliary Cooling Systems, Air 
    Recirculation Fan Coolers, and Containment Spray,'' to change allowed 
    outage times and increase the number of pumps required to be operable 
    for the service water and component cooling water systems; TS 15.3.7, 
    ``Auxiliary Electrical Systems,'' to reflect service water system 
    operability requirements; TS 15.3.12, ``Control Room Emergency 
    Filtration,'' to increase charcoal filtration efficiencies and include 
    a specific testing standard; and TS 15.5.2, ``Containment,'' to change 
    the design heat removal capability of the containment fan coolers.
        The proposed action is in accordance with the licensee's 
    application for amendments dated September 30, 1996 (TSCR-192), as 
    supplemented on November 26 and December 12, 1996, February 13, March 
    5, April 2, April 16, May 9, June 3, June 13 (two letters), and June 
    25, 1997.
    
    The Need for the Proposed Action
    
        The proposed action would allow the licensee to maintain the 
    original design basis requirement to maintain service water as a 
    single-phase fluid in the water-filled cooler portion of the 
    containment air recirculation fan coolers and to modify the design and 
    operation of plant systems to accurately reflect system and component 
    capabilities of Units 1 and 2. The proposed action would change the TS 
    to reflect revised design and operating requirements for the emergency 
    core cooling system, auxiliary cooling systems, air recirculation fan 
    coolers, containment spray system, auxiliary electrical systems, and 
    control room emergency filtration system. The revised design and 
    operating requirements include decreasing service water flow to the air 
    recirculation fan coolers to ensure adequate backpressure is maintained 
    in the air recirculation fan coolers to prevent two-phase flow in the 
    coolers; decreasing the containment heat removal capability of the air 
    recirculation fan coolers because of the decrease in service water 
    flow; limiting the source of water supplied for the containment spray 
    pumps to the available volume of water in the refueling water storage 
    tank, recalculating available volume of water in the refueling water 
    storage tank to address instrument inaccuracies; reducing the volume of 
    water assumed in the containment sump at the start of recirculation 
    initiation; increasing the required number of operable service water 
    pumps to six, increasing the required number of operable component 
    cooling water pumps to two per unit; eliminating the one-unit and two-
    unit conditions for the component cooling water system; modifying the 
    designation of service water loops to define three headers (north, 
    south, and west); revising the limiting conditions for operation of 
    components in the service water system; changing the required actions 
    in case of electrical bus availability to require shutdown of both 
    units; increasing the charcoal filter efficiency based on standardized 
    testing to a minimum of 99 percent methyl iodide removal efficiency, 
    revising the standard for thyroid dose conversion factors; revising the 
    activity limits for the primary and secondary systems; changing the 
    modes of operation of the control room ventilation system; reevaluating 
    components in containment required to be environmentally qualified to 
    revised pressure and temperature limits resulting from a large-break 
    loss-of-coolant accident; and modifying the post-accident sampling 
    system design. Changes resulting from replacing the steam generators 
    for Unit 2 and revising the accident analyses for Units 1 and 2 to 
    incorporate new steam generator setpoints, operating pressures, and 
    instrument inaccuracies were also included in the evaluations to 
    support these amendment applications.
        The changes proposed by the proposed amendments provide the 
    appropriate limiting conditions for operation, action statements, 
    allowable outage times, and design specifications for service water, 
    containment cooling, component cooling water, control room ventilation 
    system, and normal and emergency power supplies. This ensures that the 
    safety systems that protect the reactor and containment will operate as 
    required. The design of the reactor and containment are not affected by 
    these proposed changes. The proposed changes resulted in a revised 
    design basis for both units. The revised design basis was appropriately 
    evaluated to ensure that there was not a significant reduction in the 
    margin of safety. The safety systems and limiting conditions for 
    operation for these safety systems that provide support functions will 
    continue to meet the requirements for accident mitigation for Point 
    Beach Nuclear Plant. The revised accident analyses required 
    reevaluation of the radiological consequences. The limiting design-
    basis accident for dose assessment is the large-break loss-of-coolant 
    accident.
    
    Environmental Impacts of the Proposed Action
    
        Title 10, Code of Federal Regulations, part 100, specifies 
    guidelines for radiation exposure at the exclusion area boundary and 
    the low population zone. The Point Beach Nuclear Plant, Units 1 and 2, 
    were licensed based on not exceeding a total radiation dose to the 
    whole body in excess of 25 rem and a total radiation dose in excess of 
    300 rem to the thyroid from iodine exposure for an individual located 
    at any point on the exclusion area boundary (EAB) for 2 hours 
    immediately following onset of the postulated fission product release 
    and not exceeding a total radiation dose to the whole body in excess of 
    25 rem
    
    [[Page 36853]]
    
    or a total radiation dose in excess of 300 rem to the thyroid from 
    iodine exposure for an individual located at any point on outer 
    boundary of the low population zone (LPZ) who is exposed to the 
    radioactive cloud resulting from the postulated fission product release 
    (during its entire passage which is conservatively assumed to occur 
    over a 30-day period following the radioactive release). The values 
    given in the original safety evaluation report issued in 1970 listed 
    staff determined values of 4 rem whole body and 240 rem thyroid for an 
    individual located at the EAB for a 2-hour period following an accident 
    and less than 1 rem whole body and 45 rem thyroid for an individual 
    located at any point on the outer boundary of the LPZ. The licensee's 
    evaluation of the dose received to the whole body at both the EAB and 
    LPZ was not significantly changed from the original licensing safety 
    evaluation. The licensee's evaluation of the thyroid dose received by 
    an individual at the EAB based on the proposed changes indicate no 
    increase in dose as compared to the dose presented in the original 
    licensing safety evaluation. The licensee's evaluation of the thyroid 
    dose received by an individual in the LPZ indicates an approximately 5 
    percent increase in thyroid dose as compared to the dose presented in 
    the original licensing safety evaluation. However, the dose still 
    represents only 20 percent of the reference values specified in 10 CFR 
    Part 100 and the change is not considered a significant increase based 
    on the exceedingly low probability of occurrence of a large-break loss-
    of-coolant accident and low risk of public exposure to radiation. The 
    licensee concluded that the occupational exposure of the control room 
    operators is within the 30 rem thyroid dose guidelines of 10 CFR Part 
    50, Appendix A, General Design Criterion 19, based on the use of 
    potassium iodide tablets. The reliance on potassium iodide tablets was 
    previously approved in the safety evaluation for closure of NUREG-0737, 
    Item III.D.3.4, ``Control Room Habitability.'' The calculated thyroid 
    dose was previously 23.7 rem and the revised dose is 29.3 rem. The 
    revised dose is still within GDC 19 dose limits. Thus the thyroid dose 
    to control room operators is not considered significant. The licensee 
    has provided commitments to upgrade the design, operation, and analyses 
    to achieve a control room operator thyroid dose based on specific 
    occupancy factors without reliance on potassium iodide. The licensee's 
    changes in dose values are primarily the result of changes in 
    assumptions, methodology, and calculational techniques.
        The Commission has completed its evaluation of the proposed action 
    and concludes that the proposed amendments will not increase the 
    probability or consequences of accidents, no changes are being made in 
    the types of any effluents that may be released offsite, and there is 
    no significant increase in the allowable individual or cumulative 
    occupational radiation exposure. Accordingly, the Commission concludes 
    that there are no significant radiological environmental impacts 
    associated with the proposed action.
        With regard to potential nonradiological impacts, the proposed 
    action does involve features located entirely within the restricted 
    area as defined in 10 CFR part 20. It does not affect nonradiological 
    plant effluents and has no other environmental impact. Accordingly, the 
    Commission concludes that there are no significant nonradiological 
    environmental impacts associated with the proposed action.
    
    Alternatives to the Proposed Action
    
        Since the Commission has concluded there is no measurable 
    environmental impact associated with the proposed action, any 
    alternatives with equal or greater environmental impact need not be 
    evaluated. As an alternative to the proposed action, the staff 
    considered denial of the proposed action. Denial of the application 
    would result in no change in current environmental impacts. The 
    environmental impacts of the proposed action and the alternative action 
    are similar.
    
    Alternative Use of Resources
    
        This action does not involve the use of any resources not 
    previously considered in the Final Environmental Statement for the 
    Point Beach Nuclear Plant, Units 1 and 2.
    
    Agencies and Persons Consulted
    
        In accordance with its stated policy, on July 2, 1997, the staff 
    consulted with the Wisconsin State official, Jeff Kitzenbuel, of the 
    Wisconsin Public Service Commission regarding the environmental impact 
    of the proposed action. The State official had no comments.
    
    Finding of No Significant Impact
    
        Based upon the environmental assessment, the Commission concludes 
    that the proposed action will not have a significant effect on the 
    quality of the human environment. Accordingly, the Commission has 
    determined not to prepare an environmental impact statement for the 
    proposed action.
        For further details with respect to the proposed action, see the 
    licensee's letter dated September 30, 1996, as supplemented on November 
    26 and December 12, 1996, February 13, March 5, April 2, April 16, May 
    9, June 3, June 13 (two), and June 25, 1997, which are available for 
    public inspection at the Commission's Public Document Room, The Gelman 
    Building, 2120 L Street, NW., Washington, DC, and at the local public 
    document room located at The Lester Public Library, 1001 Adams Street, 
    Two Rivers, WI 54241.
    
        Dated at Rockville, Maryland, this 2nd day of July 1997.
    
        For the Nuclear Regulatory Commission.
    Linda L. Gundrum,
    Project Manager, Project Directorate III-1, Division of Reactor 
    Projects--III/IV, Office of Nuclear Reactor Regulation.
    [FR Doc. 97-17990 Filed 7-3-97; 4:20 pm]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
07/09/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
97-17990
Pages:
36852-36853 (2 pages)
Docket Numbers:
Docket Nos. 50-266 and 50-301
PDF File:
97-17990.pdf