99-20685. Texas Utilities Electric Company; Comanche Peak Steam Electric Station, Units 1 and 2 Environmental Assessment and Finding of No Significant Impact  

  • [Federal Register Volume 64, Number 154 (Wednesday, August 11, 1999)]
    [Notices]
    [Pages 43762-43763]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 99-20685]
    
    
    -----------------------------------------------------------------------
    
    NUCLEAR REGULATORY COMMISSION
    
    [Docket Nos. 50-445 and 50-446]
    
    
    Texas Utilities Electric Company; Comanche Peak Steam Electric 
    Station, Units 1 and 2 Environmental Assessment and Finding of No 
    Significant Impact
    
        The U.S. Nuclear Regulatory Commission (the Commission) is 
    considering issuance of license amendments to Facility Operating 
    License (FOL) Nos. NPF-87 and NPF-89, issued to Texas Utilities 
    Electric Company (TU Electric or the licensee), for operation of the 
    Comanche Peak Steam Electric Station (CPSES), Units 1 and 2, located in 
    Somervell County, Texas.
    
    Environmental Assessment
    
    Identification of the Proposed Action
    
        The proposed license amendments would allow the licensee to 
    increase the licensed thermal power level of CPSES, Unit 2, from 3411 
    to 3445 megawatts thermal (MWt), which represents a 1 percent increase 
    in allowable thermal power. This facility was authorized for power 
    production at 3411 MWt with issuance of the FOL on April 6, 1993.
        The proposed action is in accordance with the licensee's 
    application for license amendment dated December 21, 1998, as 
    supplemented by letters dated April 23 and May 14, 1999. Section V, of 
    Attachment 2, to the licensee's May 14, 1999, supplement, contains the 
    licensee's detailed environmental evaluation of the proposed licensing 
    action.
    
    The Need for the Proposed Action
    
        The proposed action will allow an increase in power generation at 
    CPSES, Unit 2, to provide additional electrical power for distribution 
    to the grid. Power uprate has been widely recognized by the industry as 
    a safe and cost-effective method to increase generating capacity.
    
    Environmental Impacts of the Proposed Action
    
        The Commission has previously evaluated the environmental impact of 
    operation of CPSES, Units 1 and 2, as described in the ``Final 
    Environmental Statement Related to the Operation of Comanche Peak Steam 
    Electric Station, Units 1 and 2,'' NUREG-0775, September 1981. With 
    regard to consequences of postulated accidents, the licensee has 
    reanalyzed the design-basis accident doses for the exclusion area 
    boundary, low population zone, and the control room dose to the 
    operators and determined that there will be a small increase in these 
    doses; however, the analysis presented in NUREG-0775 postulates these 
    doses resulting from releases at 104.5 percent of the currently 
    licensed power level. Thus, the increase in postulated doses due to 
    design-basis accidents is bounded by the previous evaluation presented 
    in NUREG-0775. No increase in the probability of these accidents is 
    expected to occur.
        With regard to normal releases, calculations have been performed 
    that show the potential impact on the radiological effluents from the 
    proposed 1 percent increase in power level of CPSES Unit 2. For the 1 
    percent uprating calculations, the offsite doses from normal effluent 
    releases remain significantly below the bounding limits of Title 10 of 
    the Code of Federal Regulations (10 CFR), Part 50, Appendix I. Normal 
    annual average gaseous release remains limited to a small fraction of 
    10 CFR Part 20 limits for identified mixtures. Solid and liquid waste 
    processing systems are expected
    
    [[Page 43763]]
    
    to operate within their design requirements. More frequent operation of 
    these systems may lead to a slight increase in solid and liquid 
    production.
        The Commission has completed its evaluation of the proposed action 
    and concludes that the proposed action will not increase the 
    probability or consequences of accidents, no changes are being made in 
    the types of any effluents that may be released off site, and there is 
    no significant increase in occupational or public radiation exposure. 
    Therefore, there are no significant radiological environmental impacts 
    associated with the proposed action.
        With regard to potential nonradiological impacts, the proposed 
    action does not involve any historic sites. With regard to thermal 
    discharges to the Squaw Creek Reservoir, a small increase in the 
    circulating water discharge temperature is expect due to the proposed 1 
    percent power uprate. The increase is expected to be approximately .01 
    degree Fahrenheit, and therefore, insignificant. Existing 
    administrative controls ensure the conduct of adequate monitoring such 
    that appropriate actions can be taken to preclude exceeding National 
    Pollution Discharge Elimination System (NPDES) permitted limits. No 
    additional monitoring requirements or other changes relative to the 
    NPDES permit are required as a result of the power uprate.
        Therefore, as described in the preceding discussions, the 1 percent 
    uprate of Unit 2 does not have a significant environmental impact on 
    the Squaw Creek Reservoir.
        No other nonradiological impacts are associated with the proposed 
    action.
        Based upon the above, the Commission concludes that the proposed 
    action does not affect nonradiological plant effluents and has no other 
    environmental impact. Therefore, there are no significant 
    nonradiological environmental impacts associated with the proposed 
    action.
        Accordingly, the Commission concludes that there are no significant 
    environmental impacts associated with the proposed action.
    
    Alternatives to the Proposed Action
    
        As an alternative to the proposed action, the staff considered 
    denial of the proposed action (i.e., the ``no-action'' alternative). 
    Denial of the application would result in no change in current 
    environmental impacts. The environmental impacts of the proposed action 
    and the alternative action are similar.
    
    Alternative Use of Resources
    
        This action does not involve the use of any resources not 
    previously considered in the Final Environmental Statement for the 
    CPSES.
    
    Agencies and Persons Consulted
    
        In accordance with its stated policy, on July 19, 1999, the staff 
    consulted with the Texas State official, Mr. Authur Tate of the Texas 
    Department of Health, Bureau of Radiation Control, regarding the 
    environmental impact of the proposed action. The State official had no 
    comments.
    
    Finding of No Significant Impact
    
        On the basis of the environmental assessment, the Commission 
    concludes that the proposed action will not have a significant effect 
    on the quality of the human environment. Accordingly, the Commission 
    has determined not to prepare an environmental impact statement for the 
    proposed action.
        For further details with respect to the proposed action, see the 
    licensee's application for license amendment December 21, 1998, as 
    supplemented by letters dated April 23 and May 14, 1999, which are 
    available for public inspection at the Commission's Public Document 
    Room, The Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room located at the University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas.
    
        Dated at Rockville, Maryland, this 4th day of August, 1999.
    
        For the Nuclear Regulatory Commission.
    Robert A. Gramm,
    Chief, Section 1, Project Directorate IV & Decommissioning, Division of 
    Licensing Project Management, Office of Nuclear Reactor Regulation.
    [FR Doc. 99-20685 Filed 8-10-99; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
08/11/1999
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
99-20685
Pages:
43762-43763 (2 pages)
Docket Numbers:
Docket Nos. 50-445 and 50-446
PDF File:
99-20685.pdf