X97-10813. Applications and Amendments to Facility Operating LicensesInvolving No Significant Hazards Considerations  

  • [Federal Register Volume 62, Number 156 (Wednesday, August 13, 1997)]
    [Notices]
    [Pages 43365-43381]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X97-10813]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice
    
    
    Applications and Amendments to Facility Operating 
    LicensesInvolving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from July 19, 1997, through August 1, 1997. The 
    last biweekly notice was published on July 30, 1997, (62 FR 40843).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By September 12, 1997, the licensee may file a request for a 
    hearing with respect to issuance of the amendment to the subject 
    facility operating license and any person whose interest may be 
    affected by this proceeding and who wishes to participate as a party in 
    the proceeding must file a written request for a hearing and a petition 
    for leave to intervene. Requests for a hearing and a petition for leave 
    to intervene shall be filed in accordance with the Commission's ``Rules 
    of Practice for Domestic Licensing Proceedings'' in 10 CFR Part 2. 
    Interested persons should consult a current copy of 10 CFR 2.714 which 
    is available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons
    
    [[Page 43366]]
    
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Carolina Power & Light Company, et al., Docket Nos. 50-325 and 50-
    324, Brunswick Steam Electric Plant, Units 1 and 2, Brunswick 
    County, North Carolina
    
        Date of amendments request: July 8, 1997
        Description of amendments request: The proposed amendments remove 
    the suppression chamber water volume band from Technical Specification 
    (TS) 3.6.2.1.a.1 while retaining the equivalent water level band. The 
    values for the suppression chamber water volume corresponding to the 
    low and high suppression chamber water levels will be retained in the 
    Bases section of the TS and will be revised by the proposed amendments 
    to account for the displacement of water due to the planned 
    installation of larger emergency core cooling system suction strainers. 
    The revised relationship between the high and low suppression chamber 
    water levels and suppression chamber water volume will also be 
    described in the Updated Final Safety Analysis Report.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below: 1. The proposed amendments do 
    not involve a significant increase in the probability or consequences 
    of an accident previously evaluated.
        The proposed change revises the values of the minimum and 
    maximum suppression chamber pool water volume limits. The water 
    inventory of the suppression chamber pool is not a precursor of an 
    accident and, therefore, cannot increase the probability of an 
    accident previously evaluated. The pressure suppression chamber 
    water pool mitigates the consequences of loss-of-coolant accidents 
    (LOCAs) transients [sic], and other events by providing a heat sink 
    for reactor primary system energy releases. The proposed minimum and 
    maximum pool water volume values will be consistent with the current 
    suppression chamber pool water level limits. No changes to setpoints 
    will be made as a result of the proposed change. The impact of the 
    proposed change to the minimum and maximum suppression chamber pool 
    volume limits on the suppression chamber pool temperatures and 
    pressures following a design basis LOCA, an Safety/Relief Valve 
    (SRV) blowdown event, an Anticipated Transient Without Scram (ATWS) 
    event, an Appendix R fire event, and a station blackout event has 
    been evaluated and does not cause accident parameters to exceed 
    acceptable values. In addition, the impact the proposed change has 
    on the time to reach cold shutdown when using the alternate Residual 
    Heat Removal (RHR) shutdown cooling function is negligible. The 
    potential impact the proposed change to the suppression chamber pool 
    water volume limits has on SRV line loads, SRV discharge line 
    reflood height, wetwell pressurization, suppression chamber pool 
    swell loads, vent thrust loads, and condensation oscillation and 
    chugging loads was also reviewed. The change to the suppression 
    chamber pool water volume limits has no significant adverse impact 
    on any of these parameters. As delineated above, the capability of 
    the suppression chamber water pool to perform its mitigative 
    functions is not affected by the proposed change. Therefore, the 
    proposed change does not involve a significant increase in the 
    consequences of an accident previously evaluated.
        2. The proposed amendments would not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
    
    [[Page 43367]]
    
        The proposed change revises the values of the minimum and 
    maximum volume of the suppression chamber water pool. The proposed 
    change will not alter any physical mechanism by which the 
    suppression chamber water pool volume is maintained between the 
    minimum and maximum values. The suppression chamber pool water level 
    will continue to be maintained between -27 and -31 inches. The 
    suppression chamber pool water level limits are retained in 
    Technical Specification (TS) 3.6.2.1.a.1, since this is the 
    information available to the operators regarding the suppression 
    chamber pool water volume limits. These level limits are equivalent 
    to the suppression chamber pool water volume limits; therefore, it 
    is only the presentation of the equivalency that is being relocated 
    to the Bases and the Updated Final Safety Analysis Report (UFSAR). 
    As such, the relocated suppression chamber pool water volume limits 
    are not required to be in the TS to provide adequate protection of 
    the public health and safety. As a result of the proposed strainer 
    changes, there are no physical changes to any other suppression 
    chamber components or instrumentation. No new mode of operation is 
    introduced as a result of the proposed change. Analyses have been 
    performed which conclude that the proposed change will not affect 
    the operability of the equipment designed to mitigate the 
    consequences of an accident. Therefore, the proposed change does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed license amendments do not involve a significant 
    reduction in a margin of safety.
        The proposed change revises the values of the minimum and 
    maximum suppression chamber water pool volumes. The pressure 
    suppression chamber water pool mitigates the consequences of several 
    postulated accidents and transients by providing a heat sink for the 
    primary coolant system. These accidents and events are the 
    postulated design basis LOCA, an SRV blowdown event, an ATWS event, 
    an Appendix R fire, and station blackout events. The consequences of 
    the change in the suppression pool water volume limits have been 
    evaluated for these events, and there is no significant reduction in 
    the margin of safety.
        The results of the analyses for the postulated accidents and 
    events indicate the temperature of the suppression chamber pool 
    water could increase slightly as a consequence of the decrease in 
    the minimum suppression chamber pool water volume limit. However, 
    the suppression chamber pool water and containment temperatures 
    remain within acceptable values. The impact of the calculated 
    increase in containment temperature on the available Net Positive 
    Suction Head (NPSH) for the Residual Heat Removal (RHR) and Core 
    Spray pumps has been evaluated for the postulated design basis LOCA 
    and indicate[s] adequate NPSH is maintained throughout the event.
        The potential impact of the proposed change to the suppression 
    chamber pool water volume limits on the SRV line loads, SRV 
    discharge line reflood height, wetwell pressurization, suppression 
    chamber pool swell loads, vent thrust loads, and condensation 
    oscillation and chugging loads was evaluated with the conclusion 
    that there are no adverse impacts on these parameters.
        In addition, a small suppression chamber pool water temperature 
    increase could result due to the reduction in minimum suppression 
    pool volume limit in the event reactor shutdown is conducted through 
    a path utilizing the suppression chamber pool. Such a shutdown path 
    is an alternative to the normal RHR shutdown cooling function, and 
    the small potential increase in temperature results in a negligible 
    increase in the time required to reach cold shutdown conditions. 
    Cold shutdown conditions can still be reached well within the 
    Technical Specification requirements.
        The proposed increase in the suppression pool water volume limit 
    does not adversely impact containment parameters as a result of 
    postulated accidents and events. The potential increase in 
    temperature of the pressure suppression chamber pool water does not 
    significantly decrease the ability to maintain containment 
    parameters within acceptable limits. The potential increase in time 
    to reach cold shutdown conditions utilizing the suppression pool as 
    an alternative to the normal RHR shutdown cooling function is 
    negligible. Therefore, the proposed change to revise the minimum and 
    maximum suppression water pool volumes does not involve a 
    significant reduction in a margin of safety.
        The suppression chamber pool water level limits are retained in 
    TS 3.6.2.1.a.1, since this is the information available to the 
    operators regarding the suppression chamber pool water volume 
    limits. These level limits are equivalent to the suppression chamber 
    pool water volume limits and the equivalency is being relocated to 
    the Bases and the UFSAR. As such, the relocated suppression chamber 
    pool water volume limits are not required to be in the TS to provide 
    adequate protection of the public health and safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602
        NRC Project Director: Gordon E. Edison, Acting
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, 
    Unit No. 2, Pope County, Arkansas
    
        Date of amendment request: July 21, 1997
        Description of amendment request: Technical Specification Change 
    Request Concerning Emergency Feedwater Surveillance Testing. This 
    request is to make several changes to the ANO-2 Technical 
    Specifications including an extension of the emergency feedwater (EFW) 
    pump surveillance testing frequency, a reduction in the minimum steam 
    generator pressure required to perform the surveillance testing on the 
    turbine-driven EFW pump, and a modification to the EFW pump testing 
    requirements.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does not Involve a Significant Increase in the Probability or 
    Consequences of an Accident Previously Evaluated.
        The proposed changes included in this amendment request are 
    being made to the emergency feedwater (EFW) system technical 
    specification (TS) surveillances. These changes include surveillance 
    interval modifications, allowances to perform the turbine driven EFW 
    pump surveillance at a lower steam generator (S/G) pressure, 
    removing the requirements to perform specific EFW surveillance 
    requirements (SRs) during plant shutdowns, bases changes, and 
    various administrative changes. These changes are consistent with 
    the applicable SRs located in NUREG-1432 and have therefore, been 
    previously approved by the NRC.
        These changes do not alter the functional characteristics of any 
    plant component and do not allow any new modes of operation of any 
    component. The accident mitigation features of the plant are not 
    affected by the proposed amendment request. No modifications have 
    been made to the EFW system due to this amendment request. Although 
    the minimum steam generator pressure has been reduced for the 
    turbine driven EFW pump testing, calculations show that significant 
    margin exists between the proposed value and that needed to 
    adequately perform the test. The capability of the EFW pumps to 
    perform their required safety function is not impacted by this 
    change. The addition of the electric driven EFW flow path 
    verification will help [to] assure proper alignment of both trains 
    of EFW following extended outages.
        The accident mitigation features of the plant are not affected 
    by the proposed amendment. No modification has been made to the pump 
    or turbine driver. The capability of the turbine driven EFW pump to 
    perform its required function is not impacted by this change. The 
    EFW pumps will be tested in accordance with the more restrictive of 
    the
    
    [[Page 43368]]
    
    data points required by the safety analysis or the inservice testing 
    program. Therefore, this change does not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        2. Does Not Create the Possibility of a New or Different Kind of 
    Accident from any Previously Evaluated.
        No new possibility for an accident is introduced by modifying 
    the proposed specifications for the surveillance testing of the EFW 
    pumps. The EFW surveillance requirements will continue to 
    demonstrated the pump's ability to perform its safety function. The 
    modifications to the proposed EFW surveillance requirements are 
    consistent with the current revision of NRC approved NUREG -1432, 
    ``Standard Technical Specifications Combustion Engineering Plants'' 
    (ITS). Therefore, this change does not create the possibility of a 
    new or different kind of accident from any previously evaluated.
        3. Does Not Involve a Significant Reduction in Margin of Safety.
        The safety function of the EFW system is not altered as a result 
    of this change. The capability of the EFW pumps to perform their 
    required function is not impacted by this change. The capability of 
    the EFW pumps is not impacted by this change. The EFW pumps will be 
    tested and proven operable in accordance with the more restrictive 
    of the data points required by the safety analysis of the inservice 
    testing program. The addition of the electric driven EFW flow path 
    verification will help assure [to] proper alignment of both trains 
    of EFW following extended outages. Therefore, this change does not 
    involve a significant reduction in the margin of safety.
        Therefore, based upon the reasoning presented above and the 
    previous discussion of the amendment request, Entergy Operations has 
    determined that the requested change does not involve significant 
    hazards consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502
        NRC Project Director: James Clifford, Acting
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Nuclear Generating Plant, Unit No. 3, Citrus County, Florida
    
        Date of amendment request: June 26, 1997
        Description of amendment request: The proposed amendment would 
    revise the Operating License No. DPR-72, License Condition 2.C.(5) and 
    delete the requirement for installation and testing of flow indicators 
    in the emergency core cooling system to provide indication of 40 
    gallons per minute flow for boron dilution from the license. Approval 
    of this amendment will allow removal of the appropriate flow 
    indicators, DH-45-Fl and DH-46-Fl, from the Crystal River 3 (CR3) Final 
    Safety Analysis Report.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Criterion 1
        The change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        This license amendment removes the requirement for flow 
    indication on the DH drop line and auxiliary pressurizer spray line 
    for boron precipitation mitigation during a LOCA [Loss of Coolant 
    Accident]. The original need for these indicators was to provide 
    flow indication to the operator to aid in decision making relative 
    to an alternate active method for boron precipitation prevention. 
    Alternate active methods have been replaced by the passive flow path 
    through the gaps which exist between the reactor vessel and the 
    reactor vessel internals. Since auxiliary pressurizer spray flow is 
    no longer used, and no other active means is required to be employed 
    by the operator in the event drop line flow is not indicated, the 
    original usefulness of and need for this indication no longer 
    exists. Removal of this requirement from the license condition does 
    not involve a change in the Improved Technical Specifications. The 
    operators do not use the flow indication for decision making in 
    post-accident conditions. Since these instruments are no longer used 
    for boron precipitation mitigation during a LOCA, abandonment or 
    removal of flow indicator DH-45-Fl and DH-46-Fl does not increase 
    the probability of an accident because no previously evaluated 
    accidents at CR-3 are initiated by DH-45-Fl or DH-46-Fl. Those CR-3 
    accidents that are analyzed are contained in the Final Safety 
    Analysis Report (FSAR) and include events such as Loss-of-Coolant 
    Accidents, Main Steam Line Breaks, Station Blackout, Anticipated 
    Transients Without Scram, etc. Since DH-45-Fl and DH-46-Fl are 
    attached to the outside of the DH drop line and auxiliary 
    pressurizer spray line, their removal will not change the design, 
    material, or construction standards applicable to the DH System 
    piping. The removal of the indicator will not affect overall system 
    performance of the ECCS. All of these previously evaluated accidents 
    described in the CR-3 FSAR have dose consequences which remain well 
    within the requirements of 10 CFR Part 100 (25 rem whole body, 300 
    rem thyroid) and GDC [General Design Criterion] 19 (5 rem whole 
    body, or its equivalent to any part of the body). Removal of DH-45-
    Fl and DH-46-Fl will not alter any assumptions made in evaluating 
    the radiological consequences of any accident described in the FSAR 
    nor will it affect any fission product barriers since the ECCS and 
    containment systems will still perform to meet design requirements. 
    Therefore, removal of DH-45-Fl and DH-46-Fl will not alter the 
    consequences of an accident previously evaluated.
        Criterion 2
        The change does not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposed license amendment removes the requirement for 
    indicators which were originally installed to aid the operator in 
    decision making relative to an alternate flow path for boron 
    precipitation mitigation during a LOCA. These indicators no longer 
    serve this purpose, since alternate active flow paths are no longer 
    considered. Evaluations which consider boron precipitation no longer 
    rely on three active methods of mitigation, but rather one active 
    and one passive. Operator action is not required to effect the 
    backup method in the event that the primary method fails due to a 
    single active failure. The flow indicators are external to the DH 
    System piping. They do not penetrate any piping so their removal 
    cannot create the possibility of a new or different kind of 
    accident. The accident mitigation strategies remain the same 
    regardless of whether or not the flow indicators are present. 
    Therefore, the flow indicators serve no purpose in the analyses. The 
    proposed amendment does not affect any of the parameters or 
    conditions that could contribute to the initiation of any accidents.
        Criterion 3
        The change does not involve a significant reduction in the 
    margin of safety.
        Boron precipitation within the reactor vessel during post-LOCA 
    conditions, if it were to occur, would challenge the margin of 
    safety that is provided by assuring compliance with Criterion 5 of 
    10 CFR 50.46. The license amendment does not change the methodology 
    of mitigating the consequences of boron precipitation following a 
    LOCA as described in the current licensing basis. The primary method 
    of flow through the DH drop line and the use of gap flow as the 
    ``backup'' method for prevention of boron precipitation have been 
    analyzed, shown to meet all the criteria of 10 CFR 50.46, and 
    accepted by the NRC. The passive method requires no specific 
    operator action for initiation, in the event that the primary method 
    fails due to a single active failure. Therefore, the indication 
    serves no safety function and does not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 34428
    
    [[Page 43369]]
    
        Attorney for licensee: R. Alexander Glenn, General Counsel, Florida 
    Power Corporation, MAC - A5A, P. O. Box 14042, St. Petersburg, Florida 
    33733-4042
        NRC Project Director: Frederick J. Hebdon
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Nuclear Generating Plant, Unit No. 3, Citrus County, Florida
    
        Date of amendment request: July 18, 1997
        Description of amendment request: The proposed amendment would 
    revise the Crystal River 3 (CR-3) technical specifications (TS) to 
    incorporate a new TS 3.4.11 for a Low Temperature Overpressure 
    Protection (LTOP) System. The proposed changes would be consistent with 
    the recommendations in the NRC Generic Letter 88-11, ``NRC Position on 
    Radiation Embrittlement of Reactor Vessel Materials and Its Impact on 
    Plant Operations.'' TS 3.5.3 and associated TS Bases would also be 
    revised to reflect the proposed change.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does Not Involve a Significant Increase in the Probability or 
    Consequences of an Accident Previously Evaluated.
        This change does not involve a significant increase in the 
    probability or consequences of any accident previously evaluated.
        There are currently no LTOP requirements in the CR-3 Improved 
    Technical Specifications. CR-3 currently implements LTOP features 
    through administrative controls and a lowered PORV [power-operated 
    relief valve] setpoint. The proposed change will establish new LTOP 
    technical specification requirements necessary to preclude an LTOP 
    event from occurring. The proposed LTOP requirements are based on 
    safety analyses that apply ASME [American Society of Mechanical 
    Engineers] Code Case N-514. These requirements will decrease the 
    probability of a low temperature overpressure event by providing 
    protection for all pressure and temperature combinations for which a 
    low temperature overpressure event may be postulated.
        The consequences of a low temperature overpressure accident are 
    not affected by this change. There is no change to the 10 CFR [Code 
    of Federal Regulations] Part 100 dose calculation for a low 
    temperature overpressure accident.
        2. Does Not Create the Possibility of a New or Different Kind of 
    Accident from any Previously Evaluated
        This change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        The new LTOP Technical Specification does not require 
    modification to the plant nor does it create a new mode of plant 
    operation. The LTOP system adds no new accident initiators.
        3. Does Not Involve a Significant Reduction in the Margin of 
    Safety.
        The proposed change does not involve a significant reduction in 
    the margin of safety and will provide added safety benefit gained 
    through the requirements to preclude a low temperature 
    overpressurization event to the RCS [reactor coolant system].
        The margin of safety prior to having an LTOP system was limited 
    due to the informal, administrative method of minimizing the impact 
    of a low temperature overpressure accident. By formalizing these 
    requirements into a technical specification, at the least, margin of 
    safety is retained and perhaps improved due to the elevated 
    significance of required actions.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 34428
        Attorney for licensee: R. Alexander Glenn, General Counsel, Florida 
    Power Corporation, MAC - A5A, P. O. Box 14042, St. Petersburg, Florida 
    33733-4042
        NRC Project Director: Frederick J. Hebdon
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Nuclear Generating Plant, Unit No. 3, Citrus County, Florida
    
        Date of amendment request: July 29, 1997
        Description of amendment request: The proposed amendment would 
    revise the Crystal River Nuclear Generating Unit 3 (CR3) technical 
    specifications (TS) to add subcooling margin and decay heat removal 
    (low pressure injection) flow and correct certain nomenclature in the 
    post-accident monitoring (PAM) instrumentation TS. In addition, the 
    licensee proposes to add emergency diesel generator (EDG) kilowatt (kW) 
    indication to the PAM instrumentation. Specifically, the following TS 
    would be revised:
        A. Table 3.3.17-1, Function 8: The descriptor is changed from 
    ``Containment Pressure (Narrow Range)'' to ``Containment Pressure 
    (Expected Post-Accident Range).''
        B. Table 3.3.17-1, Function 18: The required channels for Core Exit 
    Temperature (Backup) is changed from ``2 sets of 5'' to ``3 per core 
    quadrant.''
        C. Table 3.3.17-1: A new Function 20 is added and designated as 
    ``Low Pressure Injection Flow'', with 2 required channels, and 
    Condition E.
        D. Table 3.3.17-1: A new Function 21 is added and designated as 
    ``Degrees of Subcooling'', with 2 required channels, and Condition E.
        E. Table 3.3.17-1: A new Function 22 is added and designated as 
    ``Emergency Diesel Generator kW Indication'', with 2 required channels, 
    and Condition E. A note clarifying the number of required channels is 
    added: ``(c): one indicator per EDG''.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below. The items A, B, C, D and E 
    corresponds to the specific TS changes described above.
        1. The proposed changes will not significantly increase the 
    probability or consequences of an accident previously evaluated 
    because:
        A/B. The changes in containment pressure and core exit 
    thermocouple nomenclature do not reflect any physical changes to the 
    facility. This would have no impact on accident probability or 
    consequences.
        C/D/E. The addition of low pressure injection flow, degrees of
        subcooling, and EDG kW indication to the Post-Accident 
    Monitoring Instrumentation LCO [Limiting Condition for Operation] is 
    being done to comply with a commitment made during the technical 
    specification improvement program to include in the technical 
    specifications that instrumentation which monitors variables 
    classified as Type A in accordance with Regulatory Guide 1.97. These 
    three variables have been reclassified as Type A. The associated 
    instruments are used in post-accident conditions to prompt the 
    operators to take certain mitigative actions. Therefore, the 
    probability of an accident occurring is unaffected. As part of the 
    re-classification of these variables to Type A and inclusion in 
    technical specifications, the associated monitoring instrumentation 
    will be under more strict surveillance and control, which provides 
    additional assurance that the prescribed manual operator actions 
    will be implemented when necessary. This, in turn, assures the 
    previously evaluated accident consequences remain valid.
        2. The proposed changes will not create the possibility of a new 
    or different kind of accident from any accident previously evaluated 
    because:
        A/B. The changes in containment pressure and core exit
        thermocouple nomenclature do not reflect any physical changes to 
    the facility. The changes provide clarification for the instruments 
    which are required to comply with the LCO. This would not create 
    possibility of a new or different kind of accident.
        C/D/E.The addition of low pressure injection flow, degrees of 
    subcooling, and EDG kW indication to the Post-Accident Monitoring 
    Instrumentation LCO is being
    
    [[Page 43370]]
    
    done to comply with a commitment made during the technical 
    specification improvement program to include in the technical 
    specifications that instrumentation which monitors variables 
    classified as Type A in accordance with Regulatory Guide 1.97. These 
    three variables have recently been reclassified as Type A. The 
    associated instruments are used after an accident occurs to prompt 
    the operators to take certain mitigative actions. Since the 
    instrumentation is used only post-accident, these changes do not 
    create the possibility of a new or different kind of accident.
        3. The proposed change will not involve a significant reduction 
    to the margin of safety because:
        A/B. The changes in containment pressure and core exit 
    thermocouple nomenclature have no affect on the margin of safety. 
    The changes provide clarification of the technical specifications. 
    This reduces the potential for confusion regarding this 
    instrumentation.
        C/D/E. The addition of low pressure injection flow, degrees of
        subcooling, and EDG kW indication to the post-accident 
    monitoring instrumentation table in technical specifications results 
    in added controls on the OPERABILITY of this post-accident 
    monitoring instrumentation and provides greater assurance that it 
    will be available should an accident occur.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 34428
        Attorney for licensee: R. Alexander Glenn, General Counsel, Florida 
    Power Corporation, MAC - A5A, P. O. Box 14042, St. Petersburg, Florida 
    33733-4042
        NRC Project Director: Frederick J. Hebdon
    
    Northeast Nuclear Energy Company (NNECO), et al., Docket No. 50-
    423, Millstone Nuclear Power Station, Unit No. 3, New London 
    County, Connecticut
    
        Date of amendment request: July 18, 1997
        Description of amendment request: The proposed amendment adds a new 
    Technical Specification and associated Bases to address the operability 
    of the steam generator atmospheric relief bypass valves (SGARBVs).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        NNECO has reviewed the proposed revision in accordance with 
    10CFR50.92 and has concluded that the revision does not involve a 
    significant hazards consideration (SHC). The basis for this 
    conclusion is that the three criteria of 10CFR50.92(c) are not 
    satisfied. The proposed revision does not involve an SHC because the 
    revision would not:
        1. Involve a significant increase in the probability or 
    consequence of an accident previously evaluated.
        The operability of the SGARBVs provides a method to recover from 
    a SGTR [steam generator tube rupture] event during which the 
    operator is required to perform a limited cooldown to establish 
    adequate subcooling as a necessary step to limit the primary to 
    secondary break flow into the ruptured steam generator. For other 
    design events, the SGARBVs provide a safety grade method for cooling 
    the unit to residual heat removal entry conditions should the 
    preferred heat sink via the steam bypass system or the steam 
    generator atmospheric relief valves be unavailable. This proposed 
    revision to the Technical Specifications will add a new Technical 
    Specification 3/4.7.1.6 and its associated Bases Section 3/4.7.1.6 
    which were developed bases on the information contained in the 
    Westinghouse Improved Standard Technical Specifications, NUREG 1431, 
    Rev. 1. The proposed specification and bases provide further 
    assurance that the SGARBVs will be available to function as 
    described in the accident analysis.
        Therefore, the proposed revision does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        This proposed revision to the Technical Specifications to add a 
    new specification and bases for the SGARBVs does not cause a change 
    in the operation of any system or component during normal or 
    accident conditions.
        Therefore, the proposed revision does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed new Technical Specification 3/4.7.1.6 and its 
    associated Bases Section 3/4.7.1.6 were developed based on the 
    information contained in the Westinghouse Improved Standard 
    Technical Specifications, NUREG 1431, Rev. 1. The SGARBV's are not 
    currently in the Technical Specifications of Millstone Unit No. 3 
    and are being added to ensure accident mitigation functional 
    capability. The NUREG 1431, Rev. 1 surveillance frequency is 18 
    months. The NUREG 1431, Rev. 1 surveillance frequency bases reads 
    ``operating experience has shown that these components usually pass 
    the surveillance when performed at the 18 month frequency''. The 
    proposed frequency acceptability has been evaluated by reviewing 
    SGARBV AWO's [automated work order's] for the period from Jan. 1990 
    to April 1997 to confirm the absence of excessive work orders which 
    indicate valve functional failures and none were identified. 
    Additionally, each SGARBV line consists of one SGARBV and an 
    associated block valve. These proposed changes are consistent with 
    the design and operation of the SGARBVs. There is no negative affect 
    on the dose consequences from any design basis event or core damage 
    frequency.
        Therefore, the proposed revision does not involve a significant 
    reduction in a margin of safety.
        In conclusion, based on the information provided, it is 
    determined that the proposed revision does not involve an SHC.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270
        NRC Deputy Director: Phillip F. McKee
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota
    
        Date of amendment requests: November 27, 1996
        Description of amendment requests: The proposed amendment[s] would 
    incorporate new steam generator tube sleeve designs and installation 
    and examination techniques into the Prairie Island Technical 
    Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment[s] will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The supporting technical evaluation and safety evaluation for 
    the Combustion Engineering leak tight sleeves demonstrate that the 
    sleeve configuration will provide steam generator tube structural 
    and leakage integrity under normal operating and accident 
    conditions. The sleeve configurations have been designed and 
    analyzed in accordance with the requirements of the ASME [American 
    Society of Mechanical Engineers] Code. Mechanical testing has shown 
    that the sleeve and sleeve joints provide margin above acceptance
    
    [[Page 43371]]
    
    limits. Ultrasonic examination is used to verify the leak tightness 
    of the above the [sic] tubesheet sleeve welds. Testing has 
    demonstrated the leak tightness of the hard roll joint as well as 
    the structural integrity of the hard roll joint. Tube rupture can 
    not occur at the hard roll joint due to the reinforcing effect of 
    the tubesheet. Tests have demonstrated that tube collapse will not 
    occur due to postulated LOCA [loss-of-coolant accident] loadings.
        The existing Technical Specification leakage rate requirements 
    and accident analysis assumptions remain unchanged in the event that 
    significant leakage did occur from the sleeve joints or that a 
    sleeve assembly ruptured. Any leakage through the sleeve assembly is 
    fully bounded by the existing steam generator tube rupture analysis 
    included in the Prairie Island Plant USAR [updated safety analysis 
    report]. The proposed sleeving repair does not adversely impact any 
    other previously evaluated design basis accident.
        The sleeve minimum acceptable wall thickness used for developing 
    the depth based plugging limit for the sleeve is determined using 
    the guidance of draft Regulatory Guide 1.121 [Bases for 
    Plugging Degraded PWR [Pressurized-Water Reactor] Steam Generator 
    Tubes] and the pressure stress equation of Section III of 
    the ASME Code. Evaluation of the minimum acceptable wall thickness 
    for normal, upset, and postulated accident condition loading per the 
    ASME Code finds that the limiting condition is established from 
    normal operating conditions which then bounds the upset and accident 
    condition values. Allowance for non-destructive examination and 
    growth of existing sleeve wall degradation must be made when 
    determining the sleeve plugging limit. The proposed plugging limit 
    is 40% through wall degradation. The sleeve assembly will be 
    examined by state of the art non-destructive examination techniques 
    on a periodic basis to provide early indication of sleeve 
    degradation. The corrosion resistance of the Alloy 690 sleeve has 
    been verified by field experience at Prairie Island. The oldest 
    Alloy 690 sleeves were installed May 1987. No indication of 
    corrosion of the sleeve or the parent tube in the weld joint has 
    been identified by state-of-the-art eddy current examination. These 
    oldest sleeve welds did not receive post weld heat treatment. In 
    addition, 5 sleeves were removed for destructive examination in 
    February, 1996. No corrosion was found in any of these sleeves 
    including those dating from October 1992. The pulled sleeves had 
    received post weld heat treatment. Post weld heat treatment can be 
    optionally applied to the free span sleeve weld joints to reduce the 
    susceptibility of the weld joint and parent tube to stress corrosion 
    cracking. Since the sleeve design meets the requirements of the ASME 
    code and mechanical tests have demonstrated margins above acceptance 
    criteria, the installation of the Combustion Engineering leak tight 
    sleeves will not increase the probability or consequences of an 
    accident previously evaluated.
        2. The proposed amendment[s] will not create the possibility of 
    a new or different kind of accident from any accident previously 
    analyzed.
        Installation of sleeves does not introduce any significant 
    changes to the plant design basis. The use of a sleeve to span a 
    degraded region of steam generator tubing restores the structural 
    and leakage integrity of the tubing to meet the original design 
    bases. Stress and fatigue analysis of the sleeve assembly shows that 
    the requirements for ASME Code are met. Mechanical testing has 
    demonstrated that margin exists above the design criteria. Any 
    hypothetical accident as a result of any degradation in the sleeved 
    tube would be bounded by the existing tube rupture accident 
    analysis.
        3. The proposed amendment[s] will not involve a significant 
    reduction in the margin of safety.
        The use of the sleeves to repair degraded steam generator tubing 
    has been demonstrated to maintain the integrity of the tube bundle 
    commensurate with the requirements of the ASME Code and draft 
    Regulatory Guide 1.121 and to maintain the primary to secondary 
    pressure boundary under normal and postulated accident conditions. 
    The safety factors used in the verification of the strength of the 
    sleeve assembly are consistent with the safety factors in the ASME 
    Boiler and Pressure Vessel Code used in steam generator design. The 
    operational and faulted condition stresses and cumulative fatigue 
    usage are bounded by the ASME Code requirements. The sleeve assembly 
    has been verified by testing to prevent both tube pullout and 
    significant leakage during normal and postulated accident 
    conditions. A test program was conducted to ensure the rolled joint 
    design for the lower joint in the tubesheet sleeve was leak tight 
    and capable of withstanding the designs loads. The primary coolant 
    pressure boundary of the sleeve assembly will be periodically 
    inspected by non-destructive examination to identify sleeve 
    degradation due to operation. Installation of sleeves will decrease 
    the number of tubes which must be taken out of service. There is a 
    small amount of primary coolant flow reduction due to sleeves for 
    which an equivalent plugging sleeve to plug ratio is assigned and is 
    used to assess the final equivalent plugging percentage used as an 
    input to other safety analyses. Because the sleeve maintains the 
    design basis requirements for the steam generator tubing, it is 
    concluded that the proposed change does not result in a significant 
    reduction in margin with respect to plant safety as defined in the 
    USAR or the Technical Specification Bases.
        Based on the evaluation described above, and pursuant to 10 CFR 
    Part 50, Section 50.91, Northern States Power Company has determined 
    that operation of the Prairie Island Nuclear Generating Plant in 
    accordance with the proposed license amendment request does not 
    involve any significant hazards considerations as defined by NRC 
    regulations in 10 CFR Part 50, Section 50.92.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota
    
        Date of amendment requests: May 15, 1997
        Description of amendment requests: The proposed amendments would 
    change the Technical Specifications (TS) to revise certain limitations 
    on reactor coolant system leakage and steam generator tube 
    surveillance. The proposed changes would implement a voltage-based 
    repair criteria per the requirements of NRC Generic Letter 95-05, 
    ``Voltage-Based Repair Criteria for Westinghouse Steam Generator Tubes 
    Affected by Outside Diameter Stress Corrosion Cracking.'' In addition, 
    a typographical error in TS Section 4.12.c. is being corrected.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment[s] will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The supporting technical evaluation and safety evaluation for 
    the voltage based repair criteria demonstrate that steam generator 
    tube structural and leakage integrity under normal operating and 
    accident conditions will be maintained. Tube burst criteria are 
    inherently satisfied during normal operating conditions due to the 
    proximity of the tube support plate (TSP). Test data referenced in 
    Generic Letter 95-05 indicates that tube burst cannot occur within 
    the TSP, even for tubes which have 100% throughwall electric 
    discharge machining notches, 0.75 inch long, provided that the TSP 
    is adjacent to the notched area. Since tube-to-TSP proximity 
    precludes tube burst during normal operating conditions, use of the 
    criteria must retain tube integrity characteristics which maintain a 
    margin of safety of 1.43 times the bounding faulted condition, main 
    steamline break (MSLB) pressure differential. The Regulatory Guide 
    (RG) 1.121 [Bases for Plugging Degraded PWR [Pressurized-
    Water Reactor] Steam Generator Tubes] criterion requiring 
    maintenance of a safety factor of 1.43 times the MSLB pressure 
    differential on tube burst
    
    [[Page 43372]]
    
    is satisfied by 7/8'' diameter tubing with bobbin coil indications 
    with signal amplitudes less than the current 8.7 volts structural 
    limit, regardless of the indicated depth measurement.
        The upper voltage repair limit (VURL) will be 
    determined prior to each outage using the most recently NRC approved 
    database to determine the tube structural limit (VSL). 
    The structural limit is reduced by allowances for nondestructive 
    examination (NDE) uncertainty (VNDE) and growth 
    (VGR) to establish VURL. Using the Generic 
    Letter (GL) 95-05 NDE and growth allowances for an example, the NDE 
    uncertainty component of 20% and a voltage growth allowance of 30% 
    per full power year can be utilized to establish a VURL 
    of 5.2 volts.
        Relative to the expected leakage during accident condition 
    loadings, it has been previously established that a postulated MSLB 
    outside of containment but upstream of the main steam isolation 
    valve (MSIV) represents the most limiting radiological conditions to 
    the plugging criteria. In support of [the] implementation of the 
    revised plugging limit, analyses will be performed to determine 
    whether the distribution of cracking indications at the tube support 
    plate intersections during future cycles are projected to be such 
    that primary-to secondary leakage would result in postulated off 
    site and control room doses exceeding the limits established for 
    application of the voltage-based repair criteria at Prairie Island. 
    A separate calculation has determined the maximum allowable MSLB 
    leakage limit in a faulted loop. This limit was calculated using the 
    technical specification reactor coolant system (RCS) Iodine-131 
    activity level of 1.0 microcuries per gram dose equivalent Iodine-
    131 and the recommended Iodine-131 transient spiking values 
    consistent with NUREG-0800 [Standard Review 
    Plan]. The projected MSLB leak rate calculation 
    methodology prescribed in Section 2.b of Generic Letter 95-05 will 
    be used to calculate the end-of-cycle (EOC) leakage. Projected EOC 
    voltage distribution will be developed using the most recent EOC 
    eddy current results and considering an appropriate voltage 
    measurement uncertainty and indication growth allowance. The log-
    logistic probability of leakage correlation will be used to 
    establish the MSLB leak rate used for comparison with the faulted 
    loop allowable limit. Therefore, as implementation of the voltage-
    based repair criteria does not adversely affect steam generator tube 
    integrity and implementation will be shown to result in acceptable 
    dose consequences, the proposed amendment[s] [do] not result in any 
    increase in the probability or consequences of an accident 
    previously evaluated in the Updated Safety Analysis Report (USAR).
        2. The proposed amendment[s] will not create the possibility of 
    a new or different kind of accident from any accident previously 
    analyzed.
        Implementation of the proposed steam generator tube voltage-
    based repair criteria does not introduce any significant changes to 
    the plant design basis. Use of the voltage-based repair criteria 
    does not provide a mechanism which could result in an accident 
    outside of the region of the tube support plate elevations since 
    tubes with outside diameter stress corrosion cracking (ODSCC) not 
    occurring inside the thickness of the tube support plates will be 
    plugged or repaired. Neither a single or multiple tube rupture event 
    would be expected during all plant conditions in a steam generator 
    in which the voltage based repair limit has been applied.
        Northern States Power will implement a maximum primary-to-
    secondary leak rate limit of 150 gpd [gallons per day] per steam 
    generator to help preclude the potential for excessive leakage 
    during all plant conditions. The Regulatory Guide 1.121 criterion 
    for establishing operational leak rate limits that require plant 
    shutdown are based upon leak-before-break considerations to detect a 
    free span crack before potential tube rupture during faulted plant 
    conditions. The 150 gpd limit provides for leakage detection and 
    plant shutdown in the event of the occurrence of an unexpected 
    single crack resulting in leakage that is associated with the 
    longest permissible crack length.
        The operational leakage limit will be reduced to 150 gpd limit 
    consistent with Generic Letter 95-05. This limit is expected to 
    provide for plant shutdown prior to reaching critical lengths for 
    MSLB conditions using the lower 95% leak rate data. Additionally, 
    this leak-before-break evaluation assumes that the entire crevice 
    area is uncovered during blowdown. Partial uncover will provide 
    benefit to the burst capacity of the intersection and only a small 
    percentage of the TSPs are deflected greater than the TSP thickness 
    during a postulated MSLB.
        As steam generator tube integrity upon implementation of the 
    voltage-based repair criteria continues to be maintained through 
    inservice inspection and primary-to secondary leakage monitoring, 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated is not created.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed amendment[s] will not involve a significant 
    reduction in the margin of safety.
        The use of the voltage-based repair criteria at Prairie Island 
    maintains steam generator tube integrity commensurate with the 
    criteria of the ASME [American Society of Mechanical Engineers] Code 
    and Regulatory Guide 1.121. Regulatory Guide 1.121 describes a 
    method acceptable to the Commission for meeting GDCs [General Design 
    Criteria] 14, 15, 30, 31, and 32 by reducing the probability or the 
    consequences of steam generator tube rupture. This is accomplished 
    by determining the limiting conditions of degradation of steam 
    generator tubing, as established by inservice inspection, for which 
    tubes with unacceptable cracking should be repaired or removed from 
    service. Upon implementation of the proposed criteria, even under 
    the worst case conditions, the occurrence of ODSCC at the tube 
    support plate elevations is not expected to lead to the steam 
    generator tube rupture event during normal or faulted plant 
    conditions. The EOC distribution of crack indications at the tube 
    support plate elevations will be confirmed to result in acceptable 
    primary-to-secondary leakage during all plant conditions in order to 
    assure that radiological consequences meet the requirements of 
    Generic Letter 95-05.
        Previous evaluations have indicated a potential for tube 
    deformation and collapse during a postulated loss-of-coolant 
    accident (LOCA) plus safe-shutdown-earthquake (SSE) event. The tube 
    collapse potential arises from TSP deformation at the support plate 
    wedges. Evaluation of the Westinghouse umbrella seismic spectra 
    provided in Westinghouse letter NSP-92-152 for Model 51 steam 
    generators shows that Prairie Island is bounded by those spectra and 
    that no tubes will undergo deformation due to the combined effects 
    of LOCA plus SSE. Therefore, no tubes need to be excluded from 
    application of the voltage based criteria due to deformation 
    resulting from combined LOCA plus SSE loadings. Addressing 
    Regulatory Guide 1.83 [Inservice Inspection of 
    Pressurized Water Reactor Steam Generator Tubes] 
    considerations, implementation of the voltage-based repair criteria 
    is supplemented by enhanced eddy current inspection guidelines to 
    provide consistency in voltage normalization, by an extensive bobbin 
    coil inspection which will include 100% of the hot leg TSP 
    intersections and cold leg intersections down to the lowest cold leg 
    TSP with known ODSCC, by the determination of the TSPs having ODSCC 
    using at least 20% random sampling of tubes inspected over their 
    full length, and by rotating pancake coil inspection (or equivalent) 
    requirements for the larger indications left in service to 
    characterize the principal degradation as ODSCC.
        As noted previously, implementation of the tube support plate 
    intersection voltage-based repair criteria will decrease the number 
    of tubes which must be repaired. The installation of steam generator 
    tube plugs or sleeves reduces the RCS flow margin. Thus, 
    implementation of the voltage-based repair criteria will maintain 
    the margin of flow that would otherwise be reduced in the event of 
    increased tube plugging.
        Based on the above, it is concluded that the proposed license 
    amendment request does not result in a significant reduction in 
    margin with respect to plant safety as defined in the USAR or any 
    Bases of the plant Technical Specifications.
        Based on the evaluation described above, and pursuant to 10 CFR 
    Part 50, Section 50.91, Northern States Power Company has determined 
    that operation of the Prairie Island Nuclear Generating Plant in 
    accordance with the proposed license amendment request does not 
    involve any significant hazards considerations as defined by NRC 
    regulations in 10 CFR Part 50, Section 50.92.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. In addition, the proposed correction to a typographical 
    error has no effect on the three standards of 10
    
    [[Page 43373]]
    
    CFR 50.92(c). Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    PECO Energy Company, Public Service Electric and Gas Company, 
    Delmarva Power and Light Company, and Atlantic City Electric 
    Company, Dockets Nos. 50-277 and 50-278, Peach Bottom Atomic Power 
    Station, Units Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: June 4, 1997
        Description of amendment request: The proposed Technical 
    Specifications (TSs) amendment revises TS Surveillance Requirement 
    3.8.2.1 to no longer require that automatic emergency diesel generator 
    (EDG) auto-start and trip bypass features must be functional when the 
    emergency core cooling system (ECCS) is not required to be operable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change to the facility does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The proposed change will eliminate an inconsistency between 
    Technical Specifications 3.3.5.1, 3.5.2, and 3.8.2 by clarifying 
    that the EDG auto-start and EDG trip bypass on ECCS initiation 
    capability is not required during periods in which ECCS is not 
    required to be OPERABLE. No physical changes to the facility will be 
    made per this change. The systems, structures, and components 
    affected by this change are considered to be accident mitigators and 
    not accident initiators. The affected systems, structures, and 
    components will continue to operate within the current design 
    parameters. The ability of the EDGs to auto-start on a loss of 
    offsite power or degraded voltage will remain unchanged. No new 
    failure modes or conditions adverse to safety will be created as a 
    result of this change. Therefore, the proposed change does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. The proposed change to the facility does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The proposed change will eliminate an inconsistency between 
    Technical Specifications 3.3.5.1, 3.5.2, and 3.8.2 by clarifying 
    that the EDG auto-start and EDG trip bypass on ECCS initiation 
    capability is not required during periods in which ECCS is not 
    required to be OPERABLE. No physical changes to the facility will be 
    made per this change. The systems, structures and components 
    affected are considered to be accident mitigators not accident 
    initiators. The affected systems, structures and components will 
    continue to operate within the current design parameters. No new 
    failure modes or conditions adverse to safety will be created as a 
    result of this change. The plant conditions which do not require any 
    ECCS to be OPERABLE, (i.e., the plant in MODE 5, the spent fuel 
    storage pool gates are removed, water level is greater than or equal 
    to 458 inches above reactor pressure vessel instrument zero, and 
    there are no OPDRVs [operations with the potential of draining the 
    reactor vessel] in progress) ensure sufficient coolant inventory to 
    allow operator action to prevent uncovering the fuel. The ability of 
    the EDGs to auto-start on a loss of offsite power or degraded 
    voltage will remain unchanged. Therefore, the proposed change does 
    not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        3. The proposed change to the facility does not involve a 
    significant reduction in a margin of safety.
        The proposed change will eliminate an inconsistency between 
    Technical Specifications 3.3.5.1, 3.5.2, and 3.8.2 by clarifying 
    that the EDG auto-start and EDG trip bypass on ECCS initiation 
    capability is not required during periods in which ECCS is not 
    required to be OPERABLE. The ECCS and EDGs capability to perform the 
    required safety functions as described/required in the bases of the 
    current plant Technical Specifications will be maintained. 
    Therefore, the proposed change to the facility does not result in a 
    significant reduction in any margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    PA 17105
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, PECO Energy Company, 2301 Market Street, Philadelphia, 
    PA 19101
        NRC Project Director: John F. Stolz
    
    PECO Energy Company, Public Service Electric and Gas Company, 
    Delmarva Power and Light Company, and Atlantic City Electric 
    Company, Docket No. 50-278, Peach Bottom Atomic Power Station, Unit 
    No. 3, YorkCounty, Pennsylvania
    
        Date of application for amendment: June 30, 1997
        Description of amendment request: The proposed amendment would 
    revise the Technical Specification (TS) 2.1.1.2 safety limit minimum 
    critical power ratios (SLMCPRs) to be consistent with the use of GE 13 
    fuel in the Unit 3 core for operating cycle 12.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed TS changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The derivation of the cycle-specific SLMCPRs for incorporation 
    into the TS, and its use to determine cycle-specific thermal limits, 
    have been performed using the methodology discussed in ``General 
    Electric Standard Application for Reactor Fuel,'' NEDE-24011-P-A-13, 
    and U.S. Supplement, NEDE-24011-P-A-13-US, August, 1996, and the 
    ``Proposed Amendment 25 to GE Licensing Topical Report NEDE-24011-P-
    A (GESTAR II) on Cycle Specific Safety Limit MCPR.'' Amendment 25 
    was submitted by GENE to the U.S. Nuclear Regulatory Commission 
    (USNRC) on December 13, 1996. This change in SLMCPRs cannot increase 
    the probability or severity of an accident.
        The basis of the SLMCPR calculation is to ensure that greater 
    than 99.9% of all fuel rods in the core avoid transition boiling if 
    the limit is not violated. The new SLMCPRs preserve the existing 
    margin to transition boiling and fuel damage in the event of a 
    postulated accident. The fuel licensing acceptance criteria for the 
    SLMCPR calculation apply to PBAPS, Unit 3, Cycle 12 in the same 
    manner as they have applied previously. The probability of fuel 
    damage is not increased. Therefore, the proposed TS changes do not 
    involve an increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The SLMCPR is a TS numerical value, designed to ensure that 
    transition boiling does not occur in 99.9% of all fuel rods in the 
    core during the limiting postulated accident. It cannot create the 
    possibility of any new type of accident. The new SLMCPRs are 
    calculated using methodology discussed in ``General Electric 
    Standard Application for Reactor Fuel,'' NEDE-24011-P-A-13, and U.S. 
    Supplement, NEDE-24011-P-A-13-US, August, 1996, and the ``Proposed
    
    [[Page 43374]]
    
    Amendment 25 to GE Licensing Topical Report NEDE-24011-P-A (GESTAR 
    II) on Cycle Specific Safety Limit MCPR.'' Amendment 25 was 
    submitted by GENE to the U.S. Nuclear Regulatory Commission (USNRC) 
    on December 13, 1996.
        Therefore, the proposed TS changes do not create the possibility 
    of a new or different kind of accident, from any accident previously 
    evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The margin of safety as defined in the TS Bases will remain the 
    same. The new SLMCPRs are calculated using methodology discussed in 
    ``General Electric Standard Application for Reactor Fuel,'' NEDE-
    24011-P-A-13, and U.S. Supplement, NEDE-24011-P-A-13-US, August, 
    1996, and the ``Proposed Amendment 25 to GE Licensing Topical Report 
    NEDE-24011-P-A (GESTAR II) on Cycle Specific Safety Limit MCPR.'' 
    Amendment 25 was submitted by GENE to the U.S. Nuclear Regulatory 
    Commission (USNRC) on December 13, 1996. The fuel licensing 
    acceptance criteria for the calculation of the SLMCPR apply to PBAPS 
    [Peach Bottom Atomic Power Station], Unit 3 Cycle 12 in the same 
    manner as they have applied previously. The SLMCPRs ensure that 
    greater than 99.9% of all fuel rods in the core will avoid 
    transition boiling if the limit is not violated, thereby preserving 
    the fuel cladding integrity. Therefore, the proposed TS changes do 
    not involve a reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    PA 17105
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, PECO Energy Company, 2301 Market Street, Philadelphia, 
    PA 19101
        NRC Project Director: John F. Stolz
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of amendment request: April 14, 1997
        Description of amendment request: The proposed amendment revises 
    Appendix A, Section 6 of the Technical Specifications. The changes will 
    enable Safety Review Committee (SRC) to review plant staff performance 
    by deleting the plant staff performance requirement from Section 
    6.5.2.9.b and incorporating a plant staff review requirement in Section 
    6.5.2.8. The amendment also replaces the position title of Vice 
    President (VP) Regulatory Affairs and Special Projects (RASP) with 
    Director of Regulatory Affairs and Special Projects.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously analyzed?
        Response:
        This amendment application does not involve a significant 
    increase in the probability or consequences of an accident 
    previously analyzed. The proposed changes allow the SRC to perform a 
    review, rather than an audit, of plant staff performance. This 
    change does not diminish the SRC's effectiveness. A review of the 
    1995 QA [quality assurance] audit of plant staff performance shows 
    that no findings related to plant staff performance were issued. 
    This indicates that the other review mechanisms currently in place 
    are sufficient to ensure that plant staff performance is monitored.
        The position title change of VP-RASP to Director-RASP is an 
    administrative change as all previously performed functions are 
    being maintained. Therefore, the proposed changes do not affect the 
    probability or consequences of any previously analyzed accident.
        (2) Does the proposed license amendment create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated?
        Response:
        This amendment application does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. The proposed changes affect an SRC audit requirement and 
    a management position title. These changes do not affect plant 
    equipment or the way the plant operates. Therefore, they cannot 
    create a new or different kind of accident.
        (3) Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        Response:
        This amendment application does not involve a significant 
    reduction in a margin of safety. The requested Technical 
    Specification revisions require the SRC to review rather than audit 
    facility staff performance and will not diminish the effectiveness 
    of the SRC. A review of the 1995 audit confirms that performance of 
    the annual audit is redundant as no findings or recommendations 
    concerning plant staff performance were made. The QA/ORG quarterly 
    trend reports and SRC review of facility staff performance are 
    adequate to ensure that plant staff performance is properly 
    monitored.
        The position title change (VP-RASP to Director-RASP) is an 
    administrative change as all previously performed functions are 
    being maintained. Therefore, the proposed changes do not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposed to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mr. Charles M. Pratt, 1633 Broadway, New 
    York, New York 10019
        NRC Project Director: Alexander W. Dromerick, Acting Project 
    Director
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of amendment request: March 31, 1997, as supplemented by 
    letter dated July 16, 1997. The July 16, 1997, supplement supersedes 
    the March 31, 1997 application.
        Description of amendment request: The proposed amendment would 
    provide changes to Technical Specification (TS) 2.1.2, ``THERMAL POWER, 
    High Pressure and High Flow,'' ACTION a.1.c for TS 3.4.1.1, 
    ``Recirculation Loops,'' and the Bases for TS 2.1, ``Safety Limits.'' 
    These changes are being made to implement an appropriately conservative 
    Safety Limit Minimum Critical Power Ratio, to include Cycle 8 specific 
    analyses, for all Hope Creek core and fuel designs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The derivation of the revised SLMCPRs for Hope Creek for 
    incorporation into the Technical Specifications, and its use to 
    determine cyclespecific thermal limits, have been performed using 
    NRC approved methods. Additionally, interim implementing procedures 
    which incorporate cyclespecific parameters have been used which 
    result in a more restrictive value for SLMCPR. These calculations do 
    not change the method of operating the plant and have no effect on 
    the probability of an accident initiating event or transient.
        There are no significant increases in the consequences of an 
    accident previously evaluated. The basis of the MCPR Safety Limit is 
    to ensure that no mechanistic fuel damage is calculated to occur if 
    the limit is not violated. The new SLMCPRs preserve the
    
    [[Page 43375]]
    
    existing margin to transition boiling and the probability of fuel 
    damage is not increased. Therefore, the proposed change does not 
    involve an increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes contained in this submittal result from an 
    analysis of the Cycle 7 and Cycle 8 core reloads using the same fuel 
    types as previous cycles. These changes do not involve any new 
    method for operating the facility and do not involve any facility 
    modifications. No new initiating events or transients result from 
    these changes. Therefore, the proposed Technical Specification 
    changes do not create the possibility of a new or different kind of 
    accident, from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The margin of safety as defined in the Technical Specification 
    bases will remain the same. The new SLMCPRs are calculated using NRC 
    approved methods which are in accordance with the current fuel 
    design and licensing criteria. Additionally, interim implementing 
    procedures, which incorporate cyclespecific parameters, have been 
    used. The MCPR Safety Limit remains high enough to ensure that 
    greater than 99.9% of all fuel rods in the core will avoid 
    transition boiling if the limit is not violated, thereby preserving 
    the fuel cladding integrity. Therefore, the proposed Technical 
    Specification changes do not involve a reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070
        Attorney for licensee: J. J. Keenan, Esquire, Nuclear Business Unit 
    - N21, P.O. Box 236, Hancocks Bridge, NJ 08038
        NRC Project Director: John F. Stolz
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of amendment request: April 1, 1997, as supplemented by letter 
    dated May 30, 1997
        Description of amendment request: The proposed amendment would 
    provide changes to Technical Specifications (TSs) 4.6.1.1, ``Primary 
    Containment Integrity,'' 3/4.6.1.2, ``Primary Containment Leakage,'' 3/
    4.6.1.3, ``Primary Containment Air Locks,'' 4.6.1.5.1, ``Primary 
    Containment Structural Integrity,'' and 4.6.1.8.2, ``Drywell and 
    Suppression Chamber Purge System.'' The amendment would also change the 
    Bases for 3/4.6.1.2, ``Primary Containment Leakage,'' 3/4.6.1.3, 
    ``Primary Containment Air Locks,'' 3.4.6.1.5, ``Primary Containment 
    Structural Integrity,'' Section 6, ``Administrative Controls,'' and 
    License Condition 2.D of Facility Operating License NPF-57. A new TS, 
    6.8.4.e, ``Primary Containment Leakage Rate Testing Program,'' would be 
    added. These changes modify the TSs and the Facility Operating License 
    to adopt the performance based containment leak rate testing 
    requirements (Option B) of 10 CFR Part 50, Appendix J.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        Containment leak rate testing is not an initiator of any 
    accident. The proposed changes do not make any physical changes to 
    the containment and do not affect reactor operations or the accident 
    analyses. Therefore, the proposed changes do not involve a 
    significant increase in the probability of any previously evaluated 
    accident.
        Since the allowable leakage rate is not being changed and since 
    the analysis documented in NUREG-1493, ``Performance-Based 
    Containment Leak-Test Program'' concludes that the impact on public 
    health and safety due to extended intervals is negligible, the 
    proposed changes will not involve a significant increase in the 
    consequences of any previously evaluated accident.
        Therefore, adoption of a performance-based leakage testing 
    requirements will provide an equivalent level of safety and does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        No physical changes are being made to the plant, nor are there 
    any changes being made to the operation of the plant as a result of 
    the proposed changes. In addition, no new failure modes of plant 
    equipment previously evaluated are being introduced.
        Therefore, the proposed amendment will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes are based on NRC-accepted provisions and 
    maintain adequate levels of reliability of containment integrity. 
    The performance-based approach to leakage rate testing recognizes 
    that historically good results of containment testing provide 
    appropriate assurance of future containment integrity. This supports 
    the conclusion that the impact on the health and safety of the 
    public as a result of extended test intervals is negligible. Since 
    the analysis documented in NUREG-1493 confirms that the performance 
    based schedule continues to maintain a minimal impact on public 
    risk, it can be concluded that the margin of safety is not 
    significantly affected by the proposed changes.
        Therefore, the proposed amendment will not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
        Attorney for licensee: Jeffrie J. Keenan, Esquire, Nuclear Business 
    Unit - N21, P. O. Box 236, Hancocks Bridge, New Jersey 08038
        NRC Project Director: John F. Stolz
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of amendment request: July 3, 1997
        Description of amendment request: The proposed amendment would 
    change Technical Specification Table 3.6.3-1, ``Primary Containment 
    Isolation Valves'' to add valves to the list, therein.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The accidents previously evaluated in the UFSAR [Updated Final 
    Safety Analysis Report] that could be possibly affected by this 
    proposal are those involving loss of coolant scenarios such as a 
    piping or instrument line break. The proposed relief valves, 
    associated piping and the affected portions of containment 
    penetration piping are not initiators of those accidents evaluated 
    in the UFSAR. The proposed relief valves limit the post-accident 
    maximum expected pressures of the affected piping segments within 
    ASME [American Society of Mechanical Engineers] code allowables and 
    system design pressures. The modification does not cause any system 
    or component to be operated outside of their design rating
    
    [[Page 43376]]
    
    allowed by applicable codes. The proposed relief valves will be 
    safety-related and Seismic Category I components (except for the 
    relief valve discharge piping, which will be non-safety related and 
    seismically analyzed, and will meet the design, material and 
    construction standards applicable to the affected piping 
    segments[)].
        The proposed modifications do not jeopardize the capability of 
    the containment isolation valves in the affected penetrations to 
    close on the receipt of a containment isolation signal or to 
    mitigate the consequences of design basis accidents evaluated in the 
    UFSAR. Although the modifications will result in system pressures to 
    be above their currently established design values, the new peak 
    operating pressures of the affected piping segments will be limited 
    to within the requirements of the ASME code. The modification will 
    not alter any assumptions previously made or change, degrade, or 
    prevent actions described in or assumed in evaluating the 
    radiological consequences of the postulated design basis accidents. 
    Containment structure temperature and pressure limits will not be 
    exceeded with this modification and the offsite dose consequences 
    will not be affected.
        Therefore these changes will not significantly increase the 
    probability of an accident previously evaluated, nor involve a 
    significant increase in the consequences of an accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Accidents or malfunctions of equipment important to safety 
    previously evaluated in the UFSAR relating to the proposed 
    modification involve the single active failure of a containment 
    isolation valve to close upon receipt of a containment isolation 
    signal or its failure to limit the containment bypass leakage 
    following its closure. The proposed modification: 1) does not impact 
    the automatic closure times of the containment isolation valves; 2) 
    does not impact their capability to maintain leak tightness during a 
    postulated design basis accident; and 3) does not adversely impact 
    the manner in which any system is operated. The proposed 
    modification does not compromise the UFSAR accident analysis 
    assumptions and/or limits. The licensing basis safety analysis 
    limits for all systems important to safety continue to be met. 
    Furthermore, there is no change in plant testing proposed in this 
    change request which could initiate an event. Therefore, these 
    changes will not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed modifications and Technical Specification changes 
    do not change the design limits, acceptance criteria or accident 
    analysis assumptions pertaining to the containment isolation valves, 
    their associated piping or any other safety-related systems, 
    structures or components. The proposed modification does not impact 
    the automatic closure times of the containment isolation valves, nor 
    does it impact their capability to maintain leak tightness during a 
    postulated design basis accident. For the systems affected by these 
    penetration modifications, there is no change in system function or 
    structural integrity introduced with these proposed changes. 
    Therefore, the changes contained in this request do not result in a 
    significant reduction in a margin of safety for the containment 
    isolation capability of Hope Creek.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070
        Attorney for licensee: J. J. Keenan, Esquire, Nuclear Business Unit 
    - N21, P.O. Box 236, Hancocks Bridge, NJ 08038
        NRC Project Director: John F. Stolz
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of amendment request: July 7, 1997
        Description of amendment request: The proposed amendment would 
    change Technical Specification (TS) 3/4.8.4.2, ``Motor Operated Valves 
    - Thermal Overload Protection (BYPASSED),'' to relocate the list of 
    applicable valves (TS Table 3.8.4.2-1) to the Hope Creek (HC) 
    Generating Station Updated Final Safety Analysis Report (UFSAR).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed TS revisions involve: 1) no hardware changes; 2) no 
    changes to the operation of any systems or components in normal or 
    accident operating conditions; and 3) no changes to existing 
    structures, systems or components. The relocation of Technical 
    Specification Table 3.8.4.2-1 to the UFSAR and existing surveillance 
    procedures will continue to ensure that safety-related motor-
    operated valves (MOVs) are capable of performing their intended 
    safety functions. Therefore these changes will not significantly 
    increase the probability of an accident previously evaluated. To the 
    extent practicable, these proposed changes were developed consistent 
    with the changes approved by the NRC when developing NUREG-1433, 
    ``Standard Technical Specifications, General Electric Plants, BWR/
    4'', with the intent of having this relocated information controlled 
    in other plant documents subject to 10CFR50.59 provisions. Since the 
    plant systems associated with these proposed changes will still be 
    capable of: 1) meeting all applicable design basis requirements; and 
    2) retain the capability to mitigate the consequences of accidents 
    described in the HC UFSAR, the proposed changes were determined to 
    be justified. Therefore, these changes will not involve a 
    significant increase in the consequences of an accident previously 
    evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Relocation of Technical Specification Table 3.8.4.2-1 to the 
    UFSAR will not adversely impact the operation of any safety related 
    component or equipment. Since the proposed changes involve: 1) no 
    hardware changes; 2) no changes to the operation of any systems or 
    components; and 3) no changes to existing structures, systems or 
    components, there can be no impact on the occurrence of any 
    accident. To the extent practicable, these proposed changes were 
    developed consistent with the changes approved by the NRC when 
    developing NUREG-1433, ``Standard Technical Specifications, General 
    Electric Plants, BWR/4'', with the intent of having this relocated 
    information controlled in other plant documents subject to 
    10CFR50.59 provisions. Furthermore, there is no change in plant 
    testing proposed in this change request which could initiate an 
    event. Therefore, these changes will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Relocation of Technical Specification Table 3.8.4.2-1 to the 
    UFSAR is consistent, to the extent practicable, with the changes 
    approved by the NRC when developing NUREG-1433, ``Standard Technical 
    Specifications, General Electric Plants, BWR/4''. The MOV thermal 
    overload protection table will reside in the UFSAR and will ensure 
    that the associated MOVs will be capable of performing their 
    intended safety functions. Any changes to this UFSAR table will be 
    subject to the provisions of 10CFR50.59 and a separate safety 
    evaluation would be developed to support any proposed changes that 
    would subsequently be made. Therefore, the changes contained in this 
    request do not result in a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070
        Attorney for licensee: J. J. Keenan, Esquire, Nuclear Business Unit 
    - N21,
    
    [[Page 43377]]
    
    P.O. Box 236, Hancocks Bridge, NJ 08038
        NRC Project Director: John F. Stolz
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260 and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2 and 3, Limestone County, 
    Alabama
    
        Date of amendment request: June 2, 1997 (TS 387)
        Description of amendment request: The proposed amendment allows 
    continued plant operation with a single reactor recirculation loop in 
    service. The Nuclear Regulatory Commission has previously determined 
    single loop operation is generically acceptable as set forth in Generic 
    Letter 86-09, ``Technical Resolution of Generic Issue B-59-(N-1) Loop 
    Operation in BWRs [boiling water reactors] and PWRs [pressurized-water 
    reactors].'' Single loop operation is also recognized as a standard 
    mode of operation in the BWR/4 Improved Standard TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        An analysis of the limiting operational transients has been 
    performed by GE [General Electric] for BFN as documented in NEDO-
    24236 to demonstrate adequate margin to the Safety Limit Minimum 
    Critical Power Ratio (SLMCPR). In addition, SLO [single loop 
    operation] has been specified as a operating option for the 
    transient and accident evaluations performed as part of the cycle-
    specific core reload analyses for Units 2 and 3 which ensure that 
    operating limit Minimum Critical Power Ratios (OLMCPRs) for the 
    current fuel types are established that maintain required margin to 
    the fuel cladding safety limit. A cycle-specific analysis with SLO 
    will be performed for Unit 1 prior to restart and experience 
    indicates similar results are expected as those for Units 2 and 3.
        A review of the values used in the statistical analysis used in 
    the basis of the fuel cladding safety limit determined that, due to 
    increased uncertainties in total core flow readings and Traversing 
    In-Core Probe (TIP) readings during SLO, an increase in the SLMCPR 
    of .02 is bounding when in SLO. Therefore, while operating in 
    single-loop mode, an additional .02 is added to the OLMCPR which 
    maintains the same margin to the fuel cladding safety limit as that 
    established for two-loop operation. This is a conservative approach 
    because the two-loop transients have been shown to be more severe 
    than the equivalent single-loop events and, therefore, the OLMCPRs 
    established for two-loop operation would always be bounding. Thus, 
    the margin of safety for fuel clad integrity is assured and the 
    probability or consequences associated with reactor transients is 
    not increased for SLO.
        SLO results in backflow through the jet pumps in the inactive 
    recirculation loop which perturbs the relationship between the core 
    flow and recirculation drive flow on which the flow biased Average 
    Power Range Monitor (APRM) and Rod Block Monitor (RBM) setpoint 
    equations are based. To compensate, the proposed TS [Technical 
    Specification] changes modify the setpoint equations to correct for 
    one-loop operation. With this adjustment, the setpoint equations 
    preserve the original relationship between the setpoints and the 
    effective recirculation drive flow such that the consequences of a 
    RWE [rod withdrawal event] in SLO are bounded by the cycle-specific 
    RWE analyses. Therefore, these changes do not increase the 
    probability or consequences of the RWE transient previously 
    evaluated.
        Average Planar Linear Heat Generation Rate (APLHGR) limits are 
    established to ensure the acceptance criteria for fuel and Emergency 
    Core Cooling Systems established in 10 CFR 50.46 are met. A SLO Loss 
    of Coolant Accident (LOCA) analysis was performed using the SAFER/
    GESTR computer code as documented in NEDC-32484P, Revision 1, 
    ``Browns Ferry Nuclear Plant, Units 1, 2, and 3, SAFER/GESTR-LOCA, 
    Loss-of-Coolant Accident Analysis.''
        The LOCA [loss of cooling accident] results for SLO using SAFER/
    GESTR showed that, with the application of an APLHGR multiplier as 
    proposed in the TS change, the LOCA peak clad temperature for SLO 
    will always be lower than that for limiting design basis pipe break 
    for two-loop operation. An APLHGR multiplier of 0.9 is applicable 
    for all current fuel types being used. This multiplier is documented 
    in each cycle-specific reload analysis and included in the COLR 
    [core operating limits report]. NEDC-32484P Revision 1 also 
    concludes that the design basis accident (large breaks) are more 
    affected than small break sequences and, therefore, the large break 
    results are bounding for SLO.
        The Recirculation Pump Seizure event in SLO was evaluated in 
    NEDO-24236 and shown to be a non-limiting event. This conclusion is 
    also supported by GE analyses on other BWRs.
        In summary, based on the above discussion, the proposed changes 
    for SLO do not increase the probability or consequences of an 
    accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        Although the proposed change allows extended operation in a 
    configuration that was previously allowed for a limited period, 
    analysis has shown (as described in item A above), that operation 
    with one recirculation pump out-of-service is within existing 
    analyses based on the proposed TS requirements. Therefore, the 
    proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The proposed change to operate in single-loop recirculation mode 
    has been analyzed in accordance with established transient and 
    accident methodologies, and margins of safety for the design basis 
    accidents and transients analyzed in Chapter 14 of the BFN UFSAR 
    [updated final safety analysis report] have not been significantly 
    reduced. The basis for this conclusion is outlined in item A above. 
    Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Athens Public Library, 405 E. 
    South Street, Athens, Alabama 35611
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET l0H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, 
    Vermont Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of amendment request: June 9, 1997
        Description of amendment request: The amendment proposes to update 
    the Technical Specifications, Section 6.0, to add a reference to NRC-
    approved methodologies which will be used to validate or generate the 
    operating limits in the Vermont Yankee Core Operating Limits Report.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. The proposed change will not involve any significant increase 
    in the probability or consequences of an accident. The change 
    updates the Technical Specifications to include [an] NRC approved 
    method reference to allow calculation of thermal hydraulic stability 
    limits. It does not affect plant operation and will not weaken or 
    degrade the facility.
        2. The proposed change will not create the possibility of a new 
    or different kind of accident since the change is administrative. No 
    physical alterations of the plant, setpoint changes, or operating 
    conditions are proposed.
        3. The proposed change will not involve a significant reduction 
    in a margin of safety. The change involves an update to the 
    Administrative Controls in Section 6.0 of the Technical 
    Specifications by adding a reference to NRC approved methods. This 
    administrative change does not alter plant safety margins.
    
    [[Page 43378]]
    
        The NRC staff has reviewed the licensee's analysis and, based 
    onthis review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to 
    determine that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301
        Attorney for licensee: R. K. Gad, III, Ropes and Gray, One 
    International Place, Boston, MA 02110-2624
        NRC Project Director: Ronald B. Eaton, Acting
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of amendment request: June 9, 1997
        Description of amendment request: The proposed amendments authorize 
    a revision to the realistic dose values for the process gas system 
    rupture in Section 15.0 of the Byron/Braidwood (B/B) Updated Final 
    Safety Analysis Report (UFSAR). During preparation of a UFSAR change 
    package, ComEd discovered that the Final Safety Analysis Report (FSAR) 
    had not been updated to correct an error from the previous revision of 
    the dose calculation. Since the correct dose value is greater than that 
    previously reported, the consequences of the accident had increased, 
    and an unreviewed safety question resulted.
        Date of publication of individual notice in Federal Register: July 
    10, 1997 (62 FR 37079).
        Expiration date of individual notice: August 11, 1997 (as corrected 
    (62 FR 39282)).
        Local Public Document Room location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: June 27, 1997, as supplemented by letter 
    dated July 2, 1997 The supplemental letter provided clarifying 
    information and did not change the initial proposed no significant 
    hazards consideration determination.
        Brief description of amendment request: These amendments clarify, 
    in the technical specifications (TSs) for each unit, the methodology 
    used to satisfy surveillance requirements for the laboratory analysis 
    of activated carbon (charcoal) samples from the standby gas treatment 
    system (SGTS) and the control room emergency outside air supply system 
    (CREOASS). The specific changes are made to Sections 4.6.5.3.b.2 and 
    4.6.5.3.c for the SGTS and to Sections 4.7.b.2 and 4.7.2.c for the 
    CREOASS, to include a reference to American Society for Testing 
    Materials (ASTM), ``Radioiodine Testing of Nuclear-Grade Gas Phase 
    Adsorbents,'' ASTM D3803-79. Date of publication of individual notice 
    in Federal Register: July 8, 1997 (62 FR 36580)
        Expiration date of individual notice: August 7, 1997
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of application for amendments: April 14, 1997
        Brief description of amendments: The amendments revise Technical 
    Specification (TS) 3/4.3.8, ``Feedwater/Main Turbine Trip System 
    Actuation Instrumentation'' by changing the minimum channels required 
    from three to four. This change reflects a modification that is being 
    installed to add an auxiliary contact to the trip system logic. In 
    addition, the amendments revise the TS action statement for inoperable 
    channels to be consistent with the Improved Standard Technical 
    Specifications and to account for the additional channel.
        Date of issuance: July 29, 1997
        Effective date: Immediately, to be implemented within 60 days.
        Amendment Nos.: 119 and 104
        Facility Operating License Nos. NPF-11 and NPF-18: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 18, 1997 (62 FR 
    33120). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 29, 1997. No significant 
    hazards consideration comments received: No.
    
    [[Page 43379]]
    
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348
    
    Consumers Energy Company, Docket No. 50-255, Palisades Plant, Van 
    Buren County, Michigan
    
        Date of application for amendment: March 27, 1997, as supplemented 
    July 7, 1997
        Brief description of amendment: The amendment revises the Palisades 
    Plant license and technical specifications to reflect the licensee's 
    name change from ``Consumers Power Company'' to ``Consumers Energy 
    Company.''
        Date of issuance: July 21, 1997
        Effective date: July 21, 1997
        Amendment No.: 176
        Facility Operating License No. DPR-20: Amendment revised the 
    license and the technical specifications.
        Date of initial notice in Federal Register: April 23, 1997 (62 FR 
    19828) The July 7, 1997, letter provided supplementary information 
    within the scope of the original application and did not change the NRC 
    staff's initial proposed no significant hazards considerations 
    determination. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 21, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: May 27, 1997
        Brief description of amendments: The amendments delete Section 
    4.7.13.3.a.2 of each unit's Technical Specifications, regarding the 
    minimum volume and boron concentration of borated water available to 
    the Standby Makeup Pump of the Standby Shutdown System.
        Date of issuance: July 21, 1997
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 160 and 152
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 18, 1997 (62 FR 
    33121) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 21, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Unit No. 3 Nuclear Generating Plant, Citrus County, Florida
    
        Date of application for amendment: February 17, 1997, as revised 
    May 1, 1997.
        Brief description of amendment: Changes to Technical Specification 
    (TS) to implement 10 CFR 50, Appendix J Option B relating to 
    containment leakage tests.
        Date of issuance: July 24, 1997
        Effective date: July 24, 1997
        Amendment No.: 156
        Facility Operating License No. DPR-72: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 28, 1997 (62 
    FR 9214), as superseded June 4, 1997 (62 FR 30632) The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated July 24, 1997. No significant hazards consideration comments 
    received: No.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 32629
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: April 28, 1997
        Brief description of amendment: Technical Specification (TS) 3.7.6 
    requires that flood protection be provided for the service water pump 
    cubicles and components when the water level exceeds a specific value. 
    The amendment (1) adds the closing of the service water pump cubicle 
    sump drain valves to the TS, (2) revises the wording of the action 
    statement to be consistent with the limiting condition for operation, 
    and (3) revises the associated Bases section.
        Date of issuance: July 28, 1997
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment No.: 144
        Facility Operating License No. NPF-49: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 4, 1997 (62 FR 
    30636) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 28, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut 06360, and the Waterford Library, ATTN: Vince 
    Juliano, 49 Rope Ferry Road, Waterford, Connecticut 06385
    
    Northern States Power Company, Docket No. 50-263, Monticello 
    Nuclear Generating Plant, Wright County, Minnesota
    
        Date of application for amendment: January 23, 1997, as 
    supplemented January 28, March 4, June 19, July 2, July 16 (2 letters), 
    July 21, and July 25, 1997
        Brief description of amendment: The amendment documents the staff's 
    review and approval of the apparent unreviewed safety questions (USQs) 
    associated with (1) the updated analysis of the design-basis accident 
    (DBA) containment temperature and pressure response, and (2) the 
    reliance on containment pressure to compensate for the potential 
    deficiency in net positive suction head (NPSH) for the emergency core 
    cooling system (ECCS) pumps during a DBA with the worst case scenario 
    assumptions. The amendment also authorizes the licensee to change the 
    Technical Specification bases and the Updated Safety Analysis Report, 
    to reflect the reliance of containment pressure to compensate for the 
    potential deficiency in NPSH for the ECCS pumps following a DBA.
        Date of issuance: July 25, 1997
        Effective date: July 25, 1997. Implementation shall be as specified 
    in Appendix C to the license.
        Amendment No.: 98
        Facility Operating License No. DPR-22: Amendment revised the 
    license and the licensee's updated safety analysis report.
        Date of initial notice in Federal Register: February 12, 1997 (62 
    FR 6576) The June 19, 1997, submittal, expanded the scope of the 
    initial submittal dated January 23, 1997, and therefore, another notice 
    was issued in Federal Register on June 24, 1997 (62 FR 34086). The July 
    2, July 16 (2 letters), July 21, and July 25, 1997, submittals provided 
    additional clarifying information within the scope of the application 
    and did not change the NRC staff's proposed no significant hazards 
    considerations determination that was based on the June 19, 1997, 
    submittal. Therefore, renoticing was not warranted. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated July 25, 1997. No significant hazards consideration comments 
    received: No.
        Local Public Document Room location: Minneapolis Public Library,
    
    [[Page 43380]]
    
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: June 27, 1997, as supplemented 
    by letter dated July 2, 1997 The supplemental letter provided 
    clarifying information and did not change the initial proposed no 
    significant hazards consideration determination.
        Brief description of amendments: These amendments clarify, in the 
    technical specifications (TSs) for each unit, the methodology used to 
    satisfy surveillance requirements for the laboratory analysis of 
    activated carbon (charcoal) samples from the standby gas treatment 
    system (SGTS) and the control room emergency outside air supply system 
    (CREOASS). The specific changes are made to Sections 4.6.5.3.b.2 and 
    4.6.5.3.c for the SGTS and to Sections 4.7.b.2 and 4.7.2.c for the 
    CREOASS, to include a reference to American Society for Testing 
    Materials (ASTM), ``Radioiodine Testing of Nuclear-Grade Gas Phase 
    Adsorbents,'' ASTM D3803-79.
        Date of issuance: July 30, 1997
        Effective date: Both units, as of date of issuance, to be 
    implemented within 30 days.
        Amendment Nos.: 167 and 141
        Facility Operating License Nos. NPF-14 and NPF-22: The amendments 
    revised the Technical Specifications. Public comments requested as to 
    proposed no significant hazards consideration: Yes (62 FR 36580). That 
    notice provided an opportunity to submit comments on the Commission's 
    proposed no significant hazards consideration determination by July 22, 
    1997. No comments have been received. The notice also provided an 
    opportunity to request a hearing by August 7, 1997, but indicated that 
    if the Commission makes a final no significant hazards consideration 
    determination, any such hearing would take place after issuance of the 
    amendment. On July 9, 1997, the NRC staff issued a Notice of 
    Enforcement Discretion in order to delay enforcement of the current, 
    subject, TS requirements until the NRC could take formal action on the 
    July 2, 1997, application. The Commission's related evaluation of the 
    amendments, finding of exigent circumstances, consultation with the 
    State of Pennsylvania, and final no significant hazards consideration 
    determination are contained in a Safety Evaluation dated July 30, 1997.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: February 11, 1997.
        Brief description of amendment: This amendment changes the Hope 
    Creek Technical Specification (TS) Sections 3/4.8.1, ``A.C. Sources,'' 
    6.8, ``Procedures and Programs,'' and the Bases for Section 3/4.8, 
    ``Electrical Power Systems,'' to include: 1) the relocation of existing 
    surveillance requirements related to diesel fuel oil chemistry; 2) the 
    introduction of a new program under TS 6.8.4.e, ``Diesel Fuel Oil 
    Testing Program; 3) revisions to the TS Bases for Section 3/
    4.8 to incorporate information associated with the TS changes; and 4) 
    editorial changes to implement required corrections.
        Date of issuance: July 24, 1997
        Effective date: As of date of issuance, to be implemented within 60 
    days.
        Amendment No.: 100
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 26, 1997 (62 FR 
    14469) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 24, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: March 3, 1997, as supplemented 
    by letter dated May 5, 1997
        Brief description of amendment: This amendment changes Hope Creek 
    TSs as follows: (1) TS 3/4.3.1, ``Reactor Protection System 
    Instrumentation,'' TS 3/4.3.2, ``Isolation Actuation Instrumentation,'' 
    and TS 3/4.3.3, ``Emergency Core Cooling System Actuation 
    Instrumentation,'' to include additional information concerning 
    response time testing; (2) TS 4.0.5 to reference inservice inspection 
    and test requirements; (3) TS 3/4.6.1, ``Primary Containment,'' and 
    associated Bases to reflect a design modification; (4) TS 3/4.7.7, 
    ``Main Turbine Bypass System,'' to specify a new operability 
    requirement; and (5) the Bases for TS 3/4.8, ``Electrical Power 
    Systems.''
        Date of issuance: July 24, 1997
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment No.: 101
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 18, 1997 (62 FR 
    33131) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 24, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: February 11, 1997, as 
    supplemented on May 1, June 12, and July 23, 1997
        Brief description of amendments: The amendments add a new Technical 
    Specification, 3/4.7.10, ``Chilled Water System - Auxiliary Building 
    Subsystem,'' and an associated Bases section to address the support 
    function this system provides to other necessary safety systems.
        Date of issuance: July 29, 1997
        Effective date: Unit 1 to be implemented prior to entering Mode 6 
    from the current unit outage; Unit 2 as of its date of issuance, to be 
    implemented within 10 days of issuance.
        Amendment Nos.: 199 and 182
        Facility Operating License Nos. DPR-70 and DPR-75.: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 12, 1997 (62 FR 
    11497) The licensee's supplemental letters provided additional 
    information that did not affect the staff's proposed no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    July 29, 1997. No significant hazards consideration comments received: 
    No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079
    
    Tennessee Valley Authority, Docket No. 50-390 Watts Bar Nuclear 
    Plant, Unit 1, Rhea County, Tennessee
    
        Date of application for amendment: October 23, 1996, as 
    supplemented
    
    [[Page 43381]]
    
    December 11, 1996, January 31, February 10 and 24, March 11, April 4 
    and 11, May 28, June 26, and July 15, 1997.
        Brief description of amendment: The amendment changes the Watts Bar 
    Nuclear Plant, Unit 1, Technical Specifications (TS) to increase the 
    spent fuel storage capacity from 484 fuel assemblies to 1610 fuel 
    assemblies and to increase the initial enrichment of the fuel to be 
    stored in the spent fuel storage racks from 3.5 weight percent (wt%) to 
    5.0 wt%. This modification also changes the center-to-center spacing of 
    stored fuel assemblies and reflects the use of burnup credit rack 
    modules to be installed peripherally along the pool walls.
        The amendment, as proposed by the licensee, would also involve the 
    installation of spent fuel racks in the spent fuel cask pit for 225 
    storage spaces thus increasing the total WBN spent fuel storage 
    capacity to 1835 spent fuel assemblies. The licensee proposed to 
    provide an impact shield that would be placed over the fuel in the cask 
    pit when heavy loads are moved near or across the cask pit area. The 
    staff is continuing its review of this aspect of the licensee's 
    proposal. Accordingly, this amendment authorizes the reracking and 
    usage of the main spent fuel pool, as proposed for a total of 1610 
    spent fuel spaces. However, it does not authorize the installation of 
    storage racks or storage of spent fuel in the spent fuel cask pit. The 
    staff's review of that aspect of the licensee's application will be 
    addressed by further correspondence.
        Date of issuance: July 28, 1997
        Effective date: July 28, 1997
        Amendment No.: 6
        Facility Operating License No. NPF-90: Amendment revises the TS.
        Date of initial notice in Federal Register: April 2, 1997 (62 FR 
    15733) The April 4, and 11, May 28, June 26 and July 15, 1997 letters 
    provided clarifying informaion that did not change the initial proposed 
    no significant hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in an environmental assessment dated April 7, 1997, and a Safety 
    Evaluation dated July 28, 1997. No significant hazards consideration 
    comments received: None
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, TN 37402
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 
    50-339, North Anna Power Station, Units No. 1 and No. 2, Louisa 
    County, Virginia
    
        Date of application for amendments: November 9, 1987, as 
    supplemented March 31, 1988, June 8, 1992, and February 4, 1997
        Brief description of amendments: These amendments reformat the 
    operability and surveillance requirements for the intermediate range 
    channels.
        Date of issuance: July 30, 1997
        Effective date: July 30, 1997
        Amendment Nos.: 206 and 187
        Facility Operating License Nos. NPF-4 and NPF-7: Amendments revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: June 18, 1997 (62 FR 
    33136) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 30, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: February 17, 1997
        Brief description of amendment: The amendment revises the technical 
    specifications to move Table 3.6-1, ``Containment Isolation Valves'' to 
    Wolf Creek Generating Station procedures. In addition, the technical 
    specifications have been modified to remove all references to Table 
    3.6-1. This change is in accordance with the guidance provided in 
    Generic Letter 91-08, ``Removal of Component Lists from Technical 
    Specifications,'' dated May 6, 1991.
        Date of issuance: July 23, 1997
        Effective date: July 23, 1997, to be implemented within 30 days 
    from the date of issuance.
        Amendment No.: 108
        Facility Operating License No. NPF-42: The amendment revised the 
    Technical Specifications and the Operating License.
        Date of initial notice in Federal Register: April 23, 1997 (62 FR 
    19838) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 23, 1997. No significant 
    hazards consideration comments received: No.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Dated at Rockville, Maryland, this 6th day of August, 1997.
        For the Nuclear Regulatory Commission
    Jack W. Roe,
    Director, Division of Reactor Projects III/IV, Office of Nuclear 
    Reactor Regulation.
    [Doc. 97-21244 Filed 8-12-97; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Published:
08/13/1997
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X97-10813
Dates:
Immediately, to be implemented within 60 days.
Pages:
43365-43381 (17 pages)
PDF File:
x97-10813.pdf