X96-10814. Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 61, Number 158 (Wednesday, August 14, 1996)]
    [Notices]
    [Pages 42274-42290]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X96-10814]
    
    
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    NUCLEAR REGULATORY COMMISSION
    Biweekly Notice
    
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from July 20, 1996, through August 2, 1996. The 
    last biweekly notice was published on July 31, 1996 (61 FR 40013).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that
    
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    failure to act in a timely way would result, for example, in derating 
    or shutdown of the facility, the Commission may issue the license 
    amendment before the expiration of the 30-day notice period, provided 
    that its final determination is that the amendment involves no 
    significant hazards consideration. The final determination will 
    consider all public and State comments received before action is taken. 
    Should the Commission take this action, it will publish in the Federal 
    Register a notice of issuance and provide for opportunity for a hearing 
    after issuance. The Commission expects that the need to take this 
    action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By September 13, 1996, the licensee may file a request for a 
    hearing with respect to issuance of the amendment to the subject 
    facility operating license and any person whose interest may be 
    affected by this proceeding and who wishes to participate as a party in 
    the proceeding must file a written request for a hearing and a petition 
    for leave to intervene. Requests for a hearing and a petition for leave 
    to intervene shall be filed in accordance with the Commission's ``Rules 
    of Practice for Domestic Licensing Proceedings'' in 10 CFR Part 2. 
    Interested persons should consult a current copy of 10 CFR 2.714 which 
    is available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, 
    and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for
    
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    amendment which is available for public inspection at the Commission's 
    Public Document Room, the Gelman Building, 2120 L Street, NW., 
    Washington, DC, and at the local public document room for the 
    particular facility involved.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of amendments request: July 26, 1996
        Description of amendments request: The proposed amendment will 
    revise the appropriate Technical Specifications and their Bases to 
    permit the electrosleeving repair technique developed by Framatome 
    Technologies, Inc. to be used at Calvert Cliffs Nuclear Power Plant 
    (CCNPP). Electrosleeving is a steam generator tube repair method where 
    an ultra-fine grained nickel is electrochemically deposited on the 
    inner surface of a tube to form a structural repair of the degraded 
    tube. The electrodeposition of nickel provides a continuous 
    metallurgical bond that eliminates all leak paths and macro-crevices. 
    The electroformed sleeve provides a structural, leak-tight seal, 
    without deforming or changing the microstructure of the parent tube. 
    Thus, unlike the conventional welded sleeves, electrosleeving does not 
    require a post-installation stress relief.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment would not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The implementation of the proposed steam generator tube 
    electrosleeving has been reviewed for impact on the current CCNPP 
    licensing basis.
        Since the electrosleeve is designed using the applicable 
    American Society of Mechanical Engineers (ASME) Boiler and Pressure 
    Vessel Code as guidance, it meets the objectives of the original 
    steam generator tubing. The applied stresses and fatigue usage for 
    the electrosleeve are bounded by the limits established in the ASME 
    Code. American Society of Mechanical Engineers Code minimum material 
    property values are used for the structural and plugging limit 
    analysis. Mechanical testing has shown that the structural strength 
    of nickel electrosleeves under normal, upset and faulted conditions 
    provides margin to the acceptance limits. These acceptance limits 
    bound the most limiting (three times normal operating pressure 
    differential) burst margin recommended by Regulatory Guide 1.121. 
    Burst testing of electrosleeved tubes has demonstrated that no 
    unacceptable levels of primary-to-secondary leakage are expected 
    during any plant condition.
        As in the original tube, the electrosleeve Technical 
    Specification depth-based plugging limit is determined using the 
    guidance of Regulatory Guide 1.121 and the pressure stress equation 
    of Section III of the ASME Code. A bounding tube wall degradation 
    growth rate per cycle and a nondestructive examination uncertainty 
    has been assumed for determining the electrosleeve plugging limit.
        Evaluation of the proposed electrosleeved tubes indicates no 
    detrimental effects on the electrosleeve or electrosleeve-tube 
    assembly from reactor system flow, primary or secondary coolant 
    chemistries, thermal conditions or transients, or pressure 
    conditions as may be experienced at Calvert Cliffs. Corrosion 
    testing of electrosleeve-tube assemblies indicates no evidence of 
    electrosleeve or tube corrosion considered detrimental under 
    anticipated service conditions.
        The implementation of the proposed electrosleeve has no 
    significant effect on either the configuration of the plant, or the 
    manner in which it is operated. The hypothetical consequences of 
    failure of the electrosleeved tube is bounded by the current steam 
    generator tube rupture analysis described in Section 14.15 of the 
    Calvert Cliffs Updated Final Safety Analysis Report. Due to the 
    slight reduction in diameter caused by the sleeve wall thickness, 
    primary coolant release rates would be slightly less than assumed 
    for the steam generator tube rupture analysis (depending on the 
    break location), and therefore, would result in lower total primary 
    fluid mass release to the secondary system.
        Therefore, BGE [Baltimore Gas and Electric] has concluded that 
    the proposed change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. Would not create the possibility of a new or different kind 
    of accident from any other accident previously evaluated.
        As discussed above, the electrosleeve is designed using the 
    applicable ASME Code as guidance; therefore, it meets the objectives 
    of the original steam generator tubing. As a result, the functions 
    of the steam generators will not be significantly affected by the 
    installation of the proposed electrosleeve. Adhesion and ductility 
    tests performed per ASTM [American Society for Testing and 
    Materials] standards verified that the electrosleeve will not fail 
    by de-bonding or cracking. In addition, the proposed electrosleeve 
    does not interact with any other plant systems. Any accident as a 
    result of potential tube or electrosleeve degradation in the 
    repaired portion of the tube is bounded by the existing tube rupture 
    accident analysis. The continued integrity of the installed 
    electrosleeve is periodically verified by the Technical 
    Specification requirements.
        The implementation of the proposed electrosleeves has no 
    significant effect on either the configuration of the plant, or the 
    manner in which it is operated. Therefore, BGE concludes that this 
    proposed change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. Would not involve a significant reduction in a margin of 
    safety.
        The repair of degraded steam generator tubes via the use of the 
    proposed electrosleeve restores the structural integrity of the 
    faulted tube under normal operating and postulated accident 
    conditions. The design safety factors utilized for the electrosleeve 
    are consistent with the safety factors in the ASME Boiler and 
    Pressure Vessel Code used in the original steam generator design. 
    The repair limit for the proposed electrosleeve is consistent with 
    that established for the steam generator tubes. The portions of the 
    installed electrosleeve assembly which represent the reactor coolant 
    pressure boundary can be monitored for the initiation and 
    progression of electrosleeve/tube wall degradation, thus satisfying 
    the requirements of Regulatory Guide 1.83. Use of the previously 
    identified design criteria and design verification testing assures 
    that the margin to safety with respect to the implementation of the 
    proposed electrosleeve is not significantly different from the 
    original steam generator tubes.
        Therefore, BGE concludes that the proposed changes does not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Jocelyn A. Mitchell, Acting Director
    
    Carolina Power & Light Company, et al., Docket No. 50-325, 
    Brunswick Steam Electric Plant, Unit 1, Brunswick County, North 
    Carolina
    
        Date of amendment request: April 8, 1996, as supplemented on July 
    30, 1996. This notice supersedes the Federal Register notice published 
    on June 5, 1996 (61 FR 28607).
        Description of amendment request: The licensee has proposed to 
    revise the Technical Specifications (TS) to include the following 
    changes: 1. The Minimum Critical Power Ratio (MCPR) Safety Limit 
    specified in TS 2.1.2 from 1.07 to 1.10 for Unit 1 Cycle 11 operation; 
    TS 5.3.1 to reflect the new fuel type (GE13) that will be inserted 
    during Unit 1 Refueling Outage 10; 2. The acceptable range of sodium 
    pentaborate concentration for the standby liquid control system shown 
    in TS Figure
    
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    3.1.5-1 to reflect changes to poison material concentration needed to 
    achieve reactor shutdown based on the new GE13 fuel type.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed license amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Proposed Change 1:
        The proposed license amendment will allow the loading and use of 
    GE13 fuel assemblies in the Brunswick Unit 1 reactor core. The use 
    of GE13 fuel assemblies requires that the safety limit minimum 
    critical power ratio value also be revised. The safety limit minimum 
    critical power ratio is established to maintain fuel cladding 
    integrity during operational transients. The GE13 fuel assembly 
    design has been analyzed using methods that have been previously 
    approved by the Nuclear Regulatory Commission and documented in 
    General Electric Nuclear Energ's reload licensing methodology 
    Topical Report NEDE-24011, ``General Electric Standard Application 
    for Reactor Fuel (GESTAR II).``Based on a cycle-specific calculation 
    performed by General Electric, a safety limit minimum critical power 
    ratio value of 1.10 has been established for the GE13 fuel type for 
    Brunswick Unit 1 Cycle 11 operation. The cycle-specific calculation 
    has been performed in accordance with the methodology in Revision 12 
    of NEDE-24011. This cycle-specific calculation has demonstrated that 
    a safety limit minimum critical power ratio value of 1.10 will 
    ensure that 99.9 percent of the fuel rods avoid boiling transition 
    during a transient event when all uncertainties are considered. The 
    safety limit minimum critical power ratio value of 1.10 assures that 
    fuel cladding protection equivalent to that provided with the 
    existing safety limit minimum critical power ratio value is 
    maintained. This ensures that the consequences of previously 
    evaluated accidents are not significantly increased.
        The proposed revision of the safety limit minimum critical power 
    ratio does not alter any plant safety-related equipment, safety 
    function, or plant operations that could change the probability of 
    an accident. The change does not affect the design, materials, or 
    construction standards applicable to the fuel bundles in a manner 
    that could change the probability of an accident.
        Proposed Change 2:
        The standby liquid control system provides a means of reactivity 
    control that is independent of the normal reactivity control system. 
    The standby liquid control system must be capable of assuring that 
    the reactor core can be placed in a subcritical condition at any 
    time during reactor core life. Technical Specification Figure 3.1.5-
    1 specifies the acceptable range of concentrations and volumes for 
    sodium pentaborate solution used as a neutron absorber (i.e., for 
    reactivity control). The portion of the sodium pentaborate 
    concentration range shown in Technical Specification Figure 3.1.5-1 
    applicable to the lower range of tank volumes is being revised to 
    increase the required concentration of sodium pentaborate solution. 
    This change is needed to account for the additional shutdown 
    reactivity needed based on the planned use of GE13 fuel assemblies 
    as reload fuel for the Unit 1 reactor core. Since the standby liquid 
    control system is independent from the normal means of controlling 
    reactor core reactivity and not used to control core reactivity 
    during normal plant operations, the proposed revision to the sodium 
    pentaborate concentration curve for the standby liquid control 
    system does not alter any plant safety-related equipment, safety 
    function, or plant operations that could change the probability of 
    an accident.
        The current volume-concentration range of sodium pentaborate 
    used in the standby liquid control system will achieve a sufficient 
    concentration of boron in the reactor vessel to ensure reactor 
    shutdown. Based on the increased reactivity of the new GE13 reload 
    fuel assemblies, the required sodium pentaborate volume-
    concentration range is being revised to ensure sufficient neutron 
    absorbing solution is available to achieve reactor shutdown; 
    therefore, the consequences of an accident previously evaluated are 
    not significantly increased.
        2. The proposed amendment would not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        Proposed Change 1:
        The GE13 fuel assembly has been designed and complies with the 
    acceptance criteria contained in General Electric Nuclear Energy's 
    standard application for reactor fuel (GESTAR-II), which provides 
    the latest acceptance criteria for new General Electric fuel 
    designs. The similarity of the GE13 fuel design to the previously 
    accepted GE11 fuel design, in conjunction with the increased 
    critical power capability of the GE13 fuel design, ensure that no 
    new mode or condition of plant operation is being authorized by the 
    loading and use of the GE13 fuel type. The proposed revision of the 
    safety limit minimum critical power ratio from 1.07 to 1.10 does not 
    modify any plant controls or equipment that will change the plant's 
    responses to any accident or transient as given in any current 
    analysis. Therefore, the proposed change to allow the loading and 
    use of the GE13 fuel type and the revision of the safety limit 
    minimum critical power ratio value from 1.07 to 1.10 will not create 
    the possibility for a new or different kind of accident from any 
    accident previously evaluated.
        Proposed Change 2:
        As discussed above, the standby liquid control system provides a 
    means of reactivity control that is independent of the normal 
    reactivity control system and is capable of assuring that the 
    reactor core can be placed in a subcritical condition at any time 
    during reactor core life. The proposed revision to the sodium 
    pentaborate concentration range does not modify the standby liquid 
    control system or its controls, does not modify other plant systems 
    and equipment, and does not permit a new or different mode of plant 
    operation. As such, the proposed revision to the minimum pentaborate 
    concentration value does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed license amendment does not involve a significant 
    reduction in a margin of safety.
        Proposed Change 1:
        As previously discussed, the GE13 fuel assembly design has been 
    analyzed using methods that have been previously approved by the 
    Nuclear Regulatory Commission and documented in General Electric 
    Nuclear Energy's reload licensing methodology Topical Report NEDE-
    24011, ``General Electric Standard Application for Reactor Fuel 
    (GESTAR II).``The safety limit minimum critical power ratio value is 
    selected to maintain the fuel cladding integrity safety limit (i.e., 
    that 99.9 percent of all fuel rods in the core are expected to avoid 
    boiling transition during operational transients). Appropriate 
    operating limit minimum critical power ratio values are established, 
    based on the safety limit minimum critical power ratio value, to 
    ensure that the fuel cladding integrity safety limit is maintained. 
    The operating limit minimum critical power ratio values are 
    incorporated in the Core Operating limits Report as required by 
    Technical Specification 6.9.3.1.
        Based on the cycle-specific calculation performed by General 
    Electric, a safety limit minimum critical power ratio value of 1.10 
    has been established for the GE13 fuel type for Unit 1 Cycle 11 
    operation. This cycle-specific calculation has been performed based 
    on the methodology contained in Revision 12 of NEDE-24011-P-A. The 
    new GE13 safety limit minimum critical power ratio value of 1.10 for 
    Unit 1 Cycle 11 operation is based on the same fuel cladding 
    integrity safety limit criteria as that for the GE11 safety limit 
    minimum critical power ratio (i.e., that 99.9 percent of all fuel 
    rods in the core are expected to avoid boiling transition during 
    operational transients); therefore, the proposed change does not 
    result in a significant reduction in the margin of safety.
        Proposed Change 2:
        As previously stated, the purpose of the standby liquid control 
    is to inject a neutron absorbing solution into the reactor in the 
    event that a sufficient number of control rods cannot be inserted to 
    maintain subcriticality. Sufficient solution is to be injected such 
    that the reactor will be brought from maximum rated power conditions 
    to subcritical over the entire reactor temperature range from 
    maximum operating to cold shutdown conditions. General Electric 
    methodology establishes a fuel type dependent standby liquid control 
    system shutdown margin to account for calculational uncertainties. 
    General Electric calculations show that an in-vessel concentration 
    of 660 ppm will provide a standby liquid control system minimum 
    shutdown margin in excess of the 3.2% delta k value required for the 
    GE13 fuel. To achieve an in-vessel concentration of 660 ppm, the 
    acceptable range of standby liquid control system tank 
    concentrations is being
    
    [[Page 42278]]
    
    revised for the lower range of tank volumes. Thus, the proposed 
    revision of the standby liquid control system sodium pentaborate 
    volume-concentration range ensures that there will not be a 
    significant reduction in the amount of available shutdown margin 
    and, therefore, not a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of North Carolina 
    at Wilmington, William Madison Randall Library, 601 S. College Road, 
    Wilmington, North Carolina 28403-3297.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602
        NRC Project Director: Eugene V. Imbro
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of amendment request: June 21, 1996
        Description of amendment request: The proposed amendments would 
    extend the surveillance interval for TS 4.7.2.b and 4.7.2.d related to 
    testing of the Control Room Emergency Filtration System from 18 months 
    to 24 months. The amendments would also include a one-time extension of 
    the allowed outage time for the Control Room and Auxiliary Electric 
    Equipment Room Emergency Filtration System to allow each subsystem to 
    be inoperable for up to 30 days during modifications to replace the 
    existing deep bed charcoal absorbers with tray-type units.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated because:
        This Technical Specification change does not involve accident 
    initiators or initial accident assumptions. The Control Room and 
    Auxiliary Equipment Room Emergency Filtration System (CREFS) trains 
    A and B are post-accident atmospheric cleanup components that are 
    designed to limit the radiation exposure to personnel occupying the 
    Control Room to 5 rem or less whole body during and following all 
    design basis accident conditions. Therefore, this Technical 
    Specification change does not increase the probability of occurrence 
    of an accident previously evaluated.
        CREFS trains A and B are utilized to control the onsite dose to 
    personnel in the Control Room. This Technical Specification change 
    extends the [Limiting Condition for Operation] LCO duration for 
    allowing each train to be inoperable one at a time from 7 days to 30 
    days total for the current surveillance interval. This change is a 
    one time change to allow for the repair/replacement work associated 
    with the corroded filter unit charcoal retaining screens in the high 
    efficiency charcoal adsorber section of each train. The...normal 
    preventative maintenance and testing [will] be performed on the 
    operable CREFS train just prior to taking the [opposite] filter 
    train out of service for the modification. This action will ensure 
    that the remaining subsystem is operable and ensure maximum 
    reliability of the system. The Technical Specification change will 
    not affect onsite dose if a [design-basis accident] DBA occurs and 
    the operating filter unit does not fail. The operable filter unit 
    will be sufficient to maintain the operating areas habitable. The 
    original LCO allowed 7 day operation with only one operable train 
    and is also susceptible to a single failure during the Allowed 
    Outage Time. The probability that a DBA will occur coupled with the 
    single failure of the operable train during the extended allowed 
    outage time per the Technical Specification change is the same order 
    of magnitude as for the current 7 day allowed outage time. 
    Therefore, this change does not increase the consequences of an 
    accident previously evaluated.
        The extension of the surveillance interval from 18 months to 24 
    months extends the maximum interval between TS surveillances of the 
    filter trains from 22.5 months to 30 months. The equipment that is 
    affected are the CREFS filter trains A and B, which are comprised of 
    HEPA filters, heaters, charcoal adsorbers, and fans. This equipment 
    has a history of satisfactory surveillance testing (in-place testing 
    and laboratory analysis of charcoal), and has had little maintenance 
    problems for the past 5 years. Although the SER Section 6.4.1 and 
    the [Regulatory Guide] RG 1.52 state that the units shall be tested 
    every 18 months, a review of the basis documents for the testing 
    (ANSI N510) shows that the 1975 edition recommended annual testing 
    and later editions (1980 and 1989) state that testing be performed 
    ``at least once every operating cycle''. Therefore the extension of 
    the surveillance intervals from 18 months to 24 months will not 
    increase the consequences of an accident previously evaluated.
        2) Create the possibility of a new or different kind of accident 
    from any accident previously evaluated because:
        This Technical Specification change will allow each train of 
    CREFS to be inoperable one at a time for up to 30 days to repair/
    replace charcoal retaining screens and changes surveillance 
    intervals from 18 months to 24 months. Prior to the extended LCO on 
    a given train, the scheduled monthly surveillance and preventive 
    maintenance will be performed. This Technical Specification change 
    does not involve components that are accident initiators and 
    therefore will not create a new or different kind of accident than 
    those previously analyzed.
        3) Involve a significant reduction in the margin of safety 
    because:
        The purpose of CREFS trains A and B are to control the onsite 
    dose to personnel in the Control Room following an accident that 
    involves a potential radiological release. Redundant filter trains 
    are utilized to ensure that a single active failure will not impact 
    the ability of the system to perform its safety function. Since the 
    probability of an accident occurring during the extended Technical 
    Specification LCO for the inoperable train in conjunction with the 
    probability that the operable CREFS train will fail is the same 
    order of magnitude as for the current LCO, then the proposed 
    Technical Specification change has minimal impact on the safe 
    operation of the plant. The CREFS trains were both determined 
    operable following their last surveillance and no events have 
    occurred at the plant to indicate that they may be inoperable. 
    Normal preventative maintenance and testing will be performed on the 
    operable CREFS train just prior to taking the [opposite] filter 
    train out of service for the modification. This action will ensure 
    that the remaining subsystem is operable and ensure maximum 
    reliability of the system. The change in surveillance intervals from 
    18 months to 24 months will not cause a significant reduction in the 
    margin of safety, because the previous five surveillances have been 
    satisfactory and the equipment/components do not have a tendency to 
    drift over time. Therefore, the proposed amendment will not 
    significantly impact the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603
        NRC Project Director: Robert A. Capra
    
    Dairyland Power Cooperative (DPC), Docket No. 50-409, LaCrosse 
    Boiling Water Reactor (LACBWR), Vernon County, Wisconsin
    
        Date of amendment request: April 10, 1996
        Description of amendment request: The proposed amendment would 
    update the facility Possession Only License and Technical 
    Specifications to reflect the permanently shutdown and defueled 
    condition of the plant.
    
    [[Page 42279]]
    
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        DPC proposes to modify the LACBWR Technical Specifications to 
    more accurately reflect the permanently shutdown, defueled, 
    possession-only status of the facility.
        Analysis of no significant hazards consideration:
        1. The proposed changes do not create a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed changes delete system requirements that are no 
    longer necessary to prevent, or mitigate the consequences of, a 
    credible SAFSTOR accident as described in our current SAFSTOR 
    Accident Analysis.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes are either administrative in nature or were 
    made based on the analysis of previously evaluated accident 
    scenarios. In no other way do they change the design or operation of 
    the facility and therefore do not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. The proposed changes do not result in a significant reduction 
    in the margin of safety.
        The changes incorporate into the proposed Technical 
    Specifications the margin of safety associated with the current 
    SAFSTOR accident analysis and thus don't involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis, and based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: LaCrosse Public Library, 800 
    Main Street, LaCrosse, Wisconsin 54601.
        Attorney for licensee: Wheeler, Van Sickle and Anderson, Suite 801, 
    25 West Main Street, Madison, Wisconsin 53703-3398
        NRC Project Director: Seymour H. Weiss
    
    Detroit Edison Company, Docket No. 50-341, Fermi-2, Monroe County, 
    Michigan
    
        Date of amendment request: July 25, 1996 (NRC-96-0064)
        Description of amendment request: The proposed amendment would 
    relocate or delete a number of items currently in the Administrative 
    Controls Section (Section 6.0) of the technical specifications (TS). 
    This submittal revises a previous submittal dated December 15, 1994 
    (NRC-94-0107), to modify the proposed TS change to be consistent with 
    NRC Administrative Letter 95-06, ``Relocation of Technical 
    Specifications Administrative Controls Related to Quality Assurance,'' 
    the Improved Standard TS (ISTS), and pending changes to the ISTS. The 
    previous submittal was noticed in the Federal Register on June 6, 1995 
    (60 FR 29873).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    because the proposed changes are administrative in nature. None of 
    the proposed changes involve a physical modification to the plant, a 
    new mode of operation or a change to the UFSAR [Updated Final Safety 
    Analysis Report] transient analyses. No Limiting Condition for 
    Operation, ACTION statement or Surveillance Requirement is affected 
    by any of the proposed changes.
        Also, these proposed changes, in themselves, do not reduce the 
    level of qualification or training such that personnel requirements 
    would be decreased. Therefore, this change is administrative in 
    nature and does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. 
    Further, the proposed changes do not alter the design, function, or 
    operation of any plant component and therefore, do not affect the 
    consequences of any previously evaluated accident.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously evaluated 
    because the proposed changes do not introduce a new mode of plant 
    operation, surveillance requirement or involve a physical 
    modification to the plant. The proposed changes are administrative 
    in nature. The changes propose to revise, delete or relocate the 
    stated administrative control provisions from the TS to the UFSAR, 
    plant procedures or the QA [Quality Assurance] Program whereby, 
    adequate control of information is maintained. Further, as stated 
    above, the proposed changes do not alter the design, function, or 
    operation of any plant components and therefore, no new accident 
    scenarios are created.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety because they are administrative in nature. 
    None of the proposed changes involve a physical modification to the 
    plant, a new mode of operation or a change to the UFSAR transient 
    analyses. No Limiting Condition for Operation, ACTION statement or 
    Surveillance Requirement is affected. The proposed changes do not 
    involve a significant reduction in a margin of safety. Additionally, 
    the proposed change does not alter the scope of equipment currently 
    required to be OPERABLE or subject to surveillance testing nor does 
    the proposed change affect any instrument setpoints or equipment 
    safety functions. Therefore, the change does not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161
        Attorney for licensee: John Flynn, Esq., Detroit Edison Company, 
    2000 Second Avenue, Detroit, Michigan 48226
        NRC Project Director: Mark Reinhart
    
    Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear One, 
    Unit No. 1, Pope County, Arkansas
    
        Date of amendment request: April 29, 1996
        Description of amendment request: The proposed amendment revises 
    the permissible values of the maximum and minimum pressurizer water 
    levels and incorporates a graph to display these values for various 
    operating conditions. The amendment also revises the Bases section of 
    the Technical Specification. The Bases changes revise the acceptable 
    value of the as-found tolerance for the settings of the pressurizer 
    safety valves and change the value of flowrate through the pressurizer 
    safety valves. The moderator temperature coefficient as described in 
    the Bases Section is removed.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does not Involve a Significant Increase in the Probability or 
    Consequences of an Accident Previously Evaluated.
        The startup accident and the rod withdrawal accident have been 
    reanalyzed to justify the proposed increase in pressurizer coder 
    safety value as-found tolerance. The analyses establish more 
    appropriate boundaries and re-analyze the same initiators as are 
    currently found in the ANO-1 Safety Analysis Report. Changing the 
    as-found setpoint tolerance does not change how the pressurizer code 
    safety valve operates as it will continue to be reset to 2500 psig 
    plus or minus 1% prior to reactor startup.
        The acceptance criteria for these analyses are that the reactor 
    coolant system (RCS)
    
    [[Page 42280]]
    
    pressure shall not exceed the safety limit of 2750 psig (110% of 
    design pressure and that the reactor thermal power remains below 
    112% Rated Power. The analyses using the proposed setpoint tolerance 
    have shown that the acceptance criteria were met and that the 
    consequences of the events were essentially the same as those in the 
    ANO-1 SAR. Analyses were performed to determine the pressurizer 
    maximum water level that would prevent the RCS from exceeding the 
    safety limit of 2750 psig in the event of either a startup accident 
    or a rod withdrawal accident. More appropriate pressurizer level 
    requirements have been incorporated in accordance with these 
    analyses.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        2. Does Not Create the Possibility of a New or Different Kind of 
    Accident from any Previously Evaluated.
        The proposed changes introduce no new mode of plant operation. 
    The reanalysis of the startup accident and the rod withdrawal 
    accident were performed using methodologies identical to that 
    employed in the ANO-1 SAR and an improved computer code (RELAP5/
    MOD2). The pressurizer code safety valve setpoint will continue to 
    be reset at 2500 psig plus or minus 1% prior to reactor startup and 
    will continue to function to maintain RCS pressure below the safety 
    limit of 2750 psig. Analyses were performed to determine the 
    pressurizer maximum water level that would prevent the RCS from 
    exceeding the safety limit of 2750 psig in the event of either a 
    startup accident or a rod withdrawal accident. More appropriate 
    pressurizer level requirements have been incorporated in accordance 
    with these analyses.
        Therefore, this change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        3. Does Not Involve a Significant Reduction in the Margin of 
    Safety.
        The safety function of the pressurizer code safety valves is not 
    altered as a result of the proposed change in setpoint tolerance. 
    The reanalysis of the startup accident and rod withdrawal accident 
    have shown that with a plus or minus 3% setpoint tolerance, the 
    pressurizer code safety valves will function to limit RCS pressure 
    below the safety limit of 2750 psig. The sensitivity studies for the 
    startup accident showed the acceptance criteria would still be met 
    even if one pressurizer code safety valve lifted at 5% above 2500 
    psig at startup conditions. Additional analyses were performed to 
    determine the pressurizer maximum water level that would prevent the 
    RCS from exceeding the safety limit of 2750 psig in the event of 
    either a startup accident or a rod withdrawal accident.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location:  Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations, Inc., Docket Nos. 50-313 and 50-368, Arkansas 
    Nuclear One, Unit Nos. 1 and 2 (ANO-1&2), Pope County, Arkansas
    
        Date of amendment request: June 28, 1996
        Description of amendment request: The proposed amendments would 
    remove the Unit 1 and Unit 2 Technical Specification requirements to 
    secure the containment equipment hatch during core alterations or fuel 
    handling.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Criterion 1 - Does Not Involve a Significant Increase in the 
    Probability or Consequences of an Accident Previously Evaluated.
        The proposed change would allow the containment equipment hatch 
    door to remain open during fuel movement and core alterations. This 
    door is normally closed during this time period in order to prevent 
    the escape of radioactive material in the event of a fuel handling 
    accident. This door is not an initiator of any accident. The 
    probability of a fuel handling accident is unaffected by the 
    position of the containment equipment hatch door. The current fuel 
    handling analysis, which has been approved by the Staff for ANO-2 
    and submitted for ANO-1, calculates maximum offsite doses to be well 
    within the limits of 10 CFR Part 100. The current fuel handling 
    accident analysis results in maximum offsite doses of 63.6 and 41.8 
    Rem to the Thyroid and 0.902 and 0.598 Rem to the whole body (sum of 
    beta and gamma) for ANO-1 and ANO-2, respectively. This analysis 
    assumes the entire release from the damaged fuel is allowed to 
    migrate to the site boundary unobstructed. Therefore, allowing the 
    equipment hatch doors to remain open results in no change in 
    consequences. Also, the calculated doses during a fuel handling 
    accident would be considerably larger than the actual doses since 
    the calculation does not incorporate the closing of the equipment 
    hatch door following evacuation of containment. The proposed change 
    would significantly reduce the dose to workers in the containment in 
    the event of a fuel handling accident by expediting the containment 
    evacuation process. Therefore, this change does not involve a 
    significant increase in the probability or consequences of any 
    accident previously evaluated.
        Criterion 2 - Does Not Create the Possibility of a New or 
    Different Kind of Accident from any Previously Evaluated.
        The proposed change does not involve the addition or 
    modification of any plant equipment. Also, the proposed change would 
    not alter the design, configuration, or method of operation of the 
    plant beyond the standard functional capabilities of the equipment. 
    Therefore, this change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        Criterion 3 - Does Not Involve a Significant Reduction in the 
    Margin of Safety.
        The proposed change does not have the potential for an increased 
    dose at the site boundary due to a fuel handling accident. The 
    margin of safety as defined by 10 CFR Part 100 has not been 
    significantly reduced. Closing the equipment hatch door following an 
    evacuation of containment further reduces the offsite doses in the 
    event of a fuel handling accident and provides additional margin to 
    the calculated offsite doses. Therefore, this change does not 
    involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile 
    Point Nuclear Station Unit No. 1, Oswego County, New York
    
        Date of amendment request: July 12, 1996
        Description of amendment request: The proposed amendment would 
    change Technical Specification (TS) Sections 6.2.2.h and 6.2.2.i. To 
    provide adequate shift coverage without routine heavy use of overtime, 
    TS Section 6.2.2.h specifies an objective to have operating personnel 
    work ``a normal 8-hour day, 40-hour week'' while the facility is 
    operating. The proposed amendment would change the objective to ``an 8 
    to 12 hour day, nominal 40-hour week.''
        TS Section 6.2.2.i currently states, ``The General Supervisor 
    Operations, Supervisor Operations, Station Shift Supervisor Nuclear, 
    and Assistant Station Shift Supervisor Nuclear shall hold senior 
    reactor operator licenses.'' The proposed amendment would change this 
    section to state, ``The
    
    [[Page 42281]]
    
    Manager Operations, Station Shift Supervisor Nuclear and Assistant 
    Station Shift Supervisor Nuclear shall hold senior reactor operator 
    licenses.'' This change is based upon a reorganization that eliminates 
    the positions of General Supervisor Operations and Supervisor 
    Operations from the Unit 1 Operations management structure. The 
    responsibilities of these positions will be assumed by the Manager 
    Operations or delegated to off-shift Senior Reactor Operators. Thus, 
    Senior Reactor Operators will report directly to the Manager 
    Operations.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequence of an accident previously evaluated.
        Establishing operating personnel work hours at, ``an 8 to 12 
    hour day, nominal 40-hour week,'' provides enhanced continuity for 
    normal plant operations. There has been no noticeable increase in 
    safety related problems during the trial period [The facility has 
    been implementing 12-hour operator shifts for over 1 year on a trial 
    basis]. Overtime remains controlled by site administrative 
    procedures in accordance with the NRC Policy Statement of working 
    hours (Generic Letter 82-12). The probability for operating 
    personnel error due to (1) incomplete or insufficient turnover or 
    (2) interruption of in-plant maintenance and testing is reduced. No 
    physical plant modifications are involved, and none of the 
    precursors of previously evaluated accidents are affected. 
    Therefore, this change will not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The assimilation of the responsibilities of the previous 
    positions of General Supervisor Operations and Supervisor Operations 
    into the position of Manager Operations and to off-shift Senior 
    Reactor Operators reflects a restructuring of the operations 
    department, and is essentially a reduction in layers of management. 
    This proposed change does not involve any physical modification to 
    the plant, and does not affect any precursor of a previously 
    evaluated accident. Therefore, this change will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        Establishing operating personnel hours at ``an 8 to 12-hour day, 
    nominal 40-hour week'' provides increased flexibility in scheduling 
    and does not adversely affect their performance. Overtime remains 
    controlled by site administrative procedures in accordance with the 
    NRC Policy Statement on working hours (Generic Letter 82-12). No 
    physical modification of the plant is involved. As such, the change 
    does not introduce any new failure modes or conditions that may 
    create a new or different accident. Therefore, operation in 
    accordance with the proposed amendment will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        The responsibilities of the previous positions of General 
    Supervisor Operations and Supervisor Operations will be assimilated 
    into the positions of the Manager Operations and the off-shift 
    Senior Reactor Operators. There is no physical plant modification. 
    The change does not introduce any new failure modes or conditions 
    that may create a new or different accident. Therefore, the change 
    does not in itself create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        Establishing operating personnel hours at ``an 8 to 12-hour day, 
    nominal 40-hour week,'' provides increased flexibility in scheduling 
    and does not adversely affect their performance. This change also 
    decreases the risk of miscommunication between shifts by reducing 
    the number of turnovers per day and increases operations and 
    maintenance efficiency by promoting continuity in ongoing plant 
    activities. Overtime remains controlled by site administrative 
    procedures in accordance with the NRC Policy Statement on working 
    hours (Generic Letter 82-12) and is consistent with the Improved 
    Standard Technical Specifications. The proposed change involves no 
    physical modification of the plant, or alterations to any accident 
    or transient analysis [...], and the changes are administrative in 
    nature. Therefore, the change does not involve any significant 
    reduction in a margin of safety.
        The assimilation of the responsibilities of the positions of 
    General Supervisor Operations and Supervisor Operations, into the 
    positions of the Manager Operations and the off-shift Senior Reactor 
    Operators, effectively reduces layers of management. The proposed 
    change is consistent with Standard Review Plan (SRP) 13.1.2-13.1.3. 
    This administrative transformation of the operations department 
    management structure involves no physical modification of the plant 
    or alterations to any accident or transient analysis. Therefore, 
    this change in itself does not involve any significant reduction in 
    a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: Jocelyn A. Mitchell, Acting Director
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile 
    Point Nuclear Station Unit No. 2, Oswego County, New York
    
        Date of amendment request: July 12, 1996
        Description of amendment request: The proposed amendment would 
    change Technical Specification (TS) Section 6.2.2.i. To provide 
    adequate shift coverage without routine heavy use of overtime, TS 
    Section 6.2.2.i specifies an objective to have operating personnel work 
    ``a normal 8-hour day, 40-hour week'' while the facility is operating. 
    The proposed amendment would change the objective to ``an 8 to 12 hour 
    day, nominal 40-hour week.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequence of an accident previously evaluated.
        Establishing operating personnel work hours at, ``an 8 to 12 
    hour day, nominal 40-hour week,'' allows normal plant operations to 
    be managed more effectively and with enhanced continuity. There has 
    been no noticeable increase in safety related problems during the 
    trial period [The facility has been implementing 12-hour operator 
    shifts for over 1 year on a trial basis]. Overtime remains 
    controlled by site administrative procedures in accordance with the 
    NRC Policy Statement on working hours (Generic Letter 82-12). The 
    probability for operating personnel error due to (1) incomplete or 
    insufficient turnover or (2) interruption of in-plant maintenance 
    and testing is reduced. No physical plant modifications are 
    involved, and none of the precursors of previously evaluated 
    accidents are affected. Therefore, this change will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        Establishing operating personnel hours at, ``an 8 to 12-hour 
    day, nominal 40-hour week,'' improves the quality of life for 
    operating personnel and does not adversely affect their performance. 
    Overtime remains controlled by site administrative procedures in 
    accordance with the NRC Policy Statement on working hours (Generic 
    Letter 82-12). No physical modification of the plant is
    
    [[Page 42282]]
    
    involved. As such, the change does not introduce any new failure 
    modes or conditions that may create a new or different accident. 
    Therefore, operation in accordance with the proposed amendment will 
    not create the possibility of a new or different kind of accident 
    from any previously evaluated.
        The operation of Nine Mile Point Unit 2, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        Establishing operating personnel hours at, ``an 8 to 12-hour 
    day, nominal 40-hour week,'' improves the quality of life for 
    operating personnel and does not adversely affect their performance. 
    This change also decreases the risk of miscommunication between 
    shifts and increases operations and maintenance efficiency by 
    promoting continuity in ongoing plant activities. Overtime remains 
    controlled by site administrative procedures in accordance with the 
    NRC Policy Statement on working hours (Generic Letter 82-12) and is 
    consistent with the Improved Standard Technical Specifications. The 
    proposed change involves no physical modification of the plant, or 
    alterations to any accident or transient analysis [...], and the 
    changes are administrative in nature. Therefore, the change does not 
    involve any significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Project Director: Jocelyn A. Mitchell, Acting Director
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: February 2, 1996
        Description of amendment request: This request would change 
    Technical Specification (TS) 3.6.1.2 for each unit to permit primary 
    containment leakage testing of the main steam isolation valves (MSIVs) 
    at either 22.5 psig or 45 psig according to the type of test to be 
    conducted. Currently the TS only specifies 22.5 psig for the MSIVs' 
    test pressure.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        I. This proposal does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed change to the allowable test pressure for MSIV leak 
    testing was reviewed from two perspectives. First is the potential 
    for the change in testing pressure, and test methodology, to impact 
    testing results. The second perspective is the potential for a 
    failure of the testing configuration to result in undesirable 
    consequences.
        Under the proposed change, an increased test pressure of 45.0 
    psig (Pa) in the accident direction will be used to perform 
    Technical Specification required MSIV leak testing. However, the 
    acceptance criteria for testing is maintained consistent with 
    current Technical Specifications. Therefore, the proposed change to 
    allow a test pressure of Pa will not affect the validity of 
    leak test results. The existing Technical Specification required 
    leak integrity of the MSIVs will be maintained under the proposed 
    test methodology and thus the ability of the MSIVs to act as a 
    containment isolation valves is not affected.
        The proposed test pressure of Pa will be applied in the 
    accident direction, and will result in a back pressure being applied 
    to the Main Steam Line (MSL) Plugs. The potential for MSL Plug 
    ejection has been reviewed and adequate precautions have been taken 
    to ensure that fuel damage would not result from [local leak rate 
    test] LLRT induced MSL Plug ejection. The MSL Plugs are installed 
    using a restraint ring which prevents inadvertent ejection. 
    [Pennsylvania Power and Light Company] PP&L procedures require that 
    the restraint ring be installed as a prerequisite for LLRT testing 
    of the MSIVs at Pa. However, in the unlikely event that the MSL 
    Plug and restraint ring were installed improperly and then subjected 
    to back pressurization at Pa, ejection could occur. If this 
    event did occur, the MSL Plug could hit the fuel which is an 
    accident bounded by the fuel assembly handling accident analysis 
    addressed in [Final Safety Analysis Report] FSAR Section 15.7.4. The 
    MSL Plugs, MSL Plug Restraint Ring, and MSL Plug Insert and Remove 
    Tool meet the requirements of NUREG 0612 and PP&L's Heavy Loads 
    Program.
        Therefore, the proposal to allow an alternative test pressure, 
    Pa, does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        II. This proposal does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        All components within the test volume have been evaluated for 
    structural integrity under the proposed test pressures. In addition, 
    pressurization of the Main Steam Line Plugs during testing will be 
    below the evaluated pressure. The acceptance criteria for the test 
    will be maintained, thus verification of the leak integrity of the 
    MSIVs will not be impacted. Therefore, the proposed change to allow 
    for an alternative test pressure of (Pa) does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        III. This change does not involve a significant reduction in a 
    margin of safety.
        The proposed change does not affect the acceptance criteria for 
    the MSIV LLRT. As a result, testing at Pa in the accident 
    direction will provide an equivalent test to that which is performed 
    at Pa. No change in the leak integrity of the MSIVs is 
    anticipated as a result of performing the testing at the alternative 
    pressure. The potential for MSL Plug ejection during MSIV LLRT at 
    Pa has been evaluated and found to be bounded by existing 
    accident analysis. Therefore the proposed change to allow an 
    alternative test pressure, Pa, does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of amendment request: July 12, 1996
        Description of amendment request: The proposed amendment would 
    revise the Indian Point 3 (IP3) Technical Specifications (TSs) by 
    changing the surveillance frequency requirements in Table 4.1-1, 
    ``Minimum Frequencies for Checks, Calibrations, and Tests of Instrument 
    Channels'' to accommodate a 24-month operating cycle.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Does the proposed license amendment involve a significant 
    increase in the probability or consequences of an accident 
    previously analyzed?
        Response:
        The proposed changes do not involve a significant increase in 
    the probability or consequence of any accident previously evaluated. 
    The proposed changes are being made to extend surveillance 
    frequencies from 18 months to 24 months for:
    
    [[Page 42283]]
    
        Vapor Containment High Radiation Monitors
        Reactor Coolant System Subcooling Margin Monitor (SMM),
        Overpressure Protection System (OPS), and
        Reactor Vessel Level Indication System (RVLIS).
        These proposed changes are being made using the guidance 
    provided by Generic Letter 91-04 to accommodate a 24-month fuel 
    cycle. The containment radiation monitors, SMM, and RVLIS are used 
    to provide operator information during post-accident conditions and 
    have no effect on event initiators associated with previously 
    analyzed accidents. The OPS is used only when the plant is shutdown, 
    with RCS [reactor coolant system] temperature below a low 
    temperature limit, and the RCS is not vented. The function of the 
    OPS is to protect the RCS from Low Temperature Overpressurization 
    (LTOP) transients and has no effect on accident initiators. No 
    credit is taken in the IP3 safety analyses for accident mitigation 
    effects that might result from use of these instrument channels. 
    Updated calculations and evaluations to assess the proposed increase 
    in the surveillance intervals demonstrate that the effectiveness of 
    these instrument channels in fulfilling their respective functions 
    is not reduced. The containment high radiation monitors are used for 
    post accident monitoring purposes to provide operators with an 
    indication of adverse conditions in containment based on releases of 
    radioactivity from the RCS to the containment atmosphere. These 
    monitors provide no signals to plant control systems or automatic 
    safety systems used for accident mitigation and have no role as an 
    accident initiator.
        Use of the subcooling margin monitor and core exit thermocouples 
    by plant operators is specified in the Indian Point 3 Emergency 
    Operating Procedures (EOPs) to assess post accident cooling 
    conditions in the RCS. Changes to the EOPs will be made to reflect 
    the results of the updated loop accuracy calculations for this 
    instrumentation. These changes will ensure that safety analysis 
    input assumptions associated with subcooling margin, for small break 
    LOCA [loss-of-coolant accident], steam generator tube rupture, and 
    steamline break, remain valid, and that the response strategies 
    outlined in the Westinghouse Owners Group Emergency Response 
    Guidelines are maintained. Core exit thermocouple readings are not 
    used for input to plant safety analyses.
        The OPS provides a protective function to prevent RCS pressure 
    limits from being exceeded while the plant is shutdown and the RCS 
    is being maintained at a low temperature and not vented. Failure of 
    the OPS is not assumed to be an accident initiator in the plant 
    safety analyses.
        The change to the RVLIS calibration interval does not affect 
    design or operation of plant systems and will not affect the 
    probability of accidents. Revised loop accuracy calculations have 
    demonstrated that operator actions for responding to postulated 
    accidents using RVLIS in conjunction with the Indian Point 3 EOPs 
    will remain consistent with the accuracy requirements RVLIS. The 
    consequences of a previously evaluated accident will not be 
    affected.
        Equipment and system design requirements and safety analysis 
    acceptance criteria continue to be met with the proposed new 
    surveillance intervals. Based on the above information it is 
    concluded that the proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously analyzed.
        (2) Does the proposed license amendment create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated?
        Response:
        The proposed changes to extend the surveillance frequencies for 
    the above listed instrument channel do not create the possibility of 
    a new or different kind of accident from any previously evaluated. 
    The increased surveillance frequencies were evaluated based on past 
    equipment performance and do not require any plant hardware changes 
    or changes in system operation. There are no new failure modes 
    introduced as a result of extending these surveillance intervals, 
    which could lead to the creation of new or different kinds of 
    accident.
        (3) Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        Response:
        The proposed changes do not involve a significant reduction in a 
    margin of safety. [A decreased] surveillance frequency for the 
    Containment High Radiation Monitor, SMM, OPS, and RVLIS does not 
    adversely affect the performance of safety-related systems, 
    equipment, or instruments and does not result in increased severity 
    of accidents evaluated. The radiation monitor, SMM, and RVLIS are 
    not used to support margins of safety identified in the Technical 
    Specifications. OPS provides an equipment protection function to 
    prevent inadvertent overpressurization of the RCS at shutdown 
    conditions. The Low Temperature Overpressurization (LTOP) curve in 
    the Technical Specifications represents material stress limits based 
    on fracture toughness requirements for ferritic steel. Analysis of 
    the proposed change to the OPS surveillance frequency verified 
    sufficient margin to the LTOP curve and therefore does not involve a 
    significant reduction in margin to the material stress limits.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
        Attorney for licensee: Mr. Charles M. Pratt, 10 Columbus Circle, 
    New York, New York 10019.
        NRC Project Director: Jocelyn A. Mitchell, Acting Director
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of amendment request: July 12, 1996
        Description of amendment request: The proposed amendment would 
    change the Indian Point 3 (IP3) Technical Specifications (TS) relating 
    to minimum reactor coolant system (RCS) flow and maximum RCS average 
    temperature to make these parameters consistent with an assumption of 
    100% helium release from the boron coating of the integral fuel 
    burnable absorber (IFBA) rods.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Does the proposed license amendment involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated?
        The proposed changes to the RCS minimum flow and maximum 
    Tavg requirements will not increase the probability or 
    consequences of an accident previously evaluated. Reference 2 [SECL-
    96-046, ``IFBA Helium Release Evaluation for Cycle 9 Restart,'' 
    Westinghouse Electric Corporation, dated July 8, 1996] states that, 
    for the remainder of Cycle 9, all pertinent licensing basis 
    acceptance criteria have been met, and the margin of safety as 
    defined in the Technical Specification Bases is not reduced in any 
    of the licensing basis accident analyses for the assumption of a 
    100% helium release from the IFBA rods. Reference 3 [Westinghouse 
    letter, ``Technical Specification Value for T-Average,'' INT-96-557, 
    dated July 3, 1996] states that a reduction of maximum allowable 
    indicated Tavg from 578.3 deg.F to 571.5 deg.F specifications 
    consistent with the more limiting containment integrity analyses. 
    The associated plant and technical specification changes do not 
    affect any of the mechanisms postulated in the FSAR [Final Safety 
    Analysis Report] to cause licensing basis events. Therefore, the 
    probability of an accident previously evaluated has not increased. 
    Because design limitations continue to be met, and the integrity of 
    the RCS pressure boundary is not challenged, the assumptions 
    employed in the calculation of the offsite radiological doses remain 
    valid. Therefore, the consequences of an accident previously 
    evaluated will not be increased.
        (2) Does the proposed license amendment create the possibility 
    of a new or different kind of accident from any previously 
    evaluated?
        The proposed changes to the RCS minimum flow and maximum 
    Tavg requirements do not create the possibility of a new or 
    different kind of accident from any previously evaluated. Reference 
    2 states that, for the remainder of Cycle 9, all pertinent
    
    [[Page 42284]]
    
    licensing basis acceptance criteria have been met, and the margin of 
    safety as defined in the Technical Specification Bases is not 
    reduced in any of the licensing basis accident analyses for the 
    assumption of a 100% helium release from the IFBA. Reference 3 
    provides clarifications of the assumptions made in the design basis 
    and restricts DNB temperature limits to be consistent with non-DNB 
    analyses. The associated plant and technical specification changes 
    do not change the plant configuration in a way which introduces a 
    new potential hazard to the plant (i.e., no new failure mode has 
    been created). Therefore, an accident which is different than any 
    previously evaluated will not be created.
        (3) Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        The proposed changes to the RCS minimum flow and maximum 
    Tavg requirements do not involve a significant reduction in a 
    margin of safety. Reference 2 demonstrates that, for the remainder 
    of Cycle 9, all pertinent licensing basis acceptance criteria have 
    been met, and the margin of safety as defined in the Technical 
    Specification Bases is not reduced in any of the licensing basis 
    accident analyses for the assumption of a 100% helium release from 
    the IFBA. Reference 3 maintains the margin of safety by restricting 
    a DNB limit to bound other analyses. Since References 2 and 3 
    demonstrate that all applicable acceptance criteria continue to be 
    met, the subject operating conditions will not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
        Attorney for licensee: Mr. Charles M. Pratt, 10 Columbus Circle, 
    New York, New York 10019.
        NRC Project Director: Jocelyn A. Mitchell, Acting
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260 and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2 and 3, Limestone County, 
    Alabama
    
        Date of amendment request: May 3, 1996 (TS 352)
        Description of amendment request: The proposed amendment requests 
    administrative changes to the Browns Ferry Nuclear Plant (BFN) Units 1, 
    2, and 3 technical specifications. The proposed amendment consists of 
    three parts, designated by the licensee as A, B, and C. Part A deletes 
    technical specification requirements associated with BFN Unit 2 
    Amendment 219, issued November 12, 1993, to permit modification of 
    reactor vessel water level instrumentation requested by NRC Bulletin 
    93-03. Part B deletes technical specification requirements associated 
    with Amendment 228, issued on December 7, 1994, which provided a 
    temporary change to permit upgrade of electrical equipment. The 
    modifications associated with Parts A and C are complete. Part C 
    provides other administrative changes to clarify requirements and to 
    implement rule changes.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Part A: The proposed Technical Specification change to remove 
    the temporary revisions, which were in place to modify the reactor 
    vessel water level instrumentation requested by NRC Bulletin 93-03, 
    is administrative. The temporary limiting condition for the minimum 
    number of trip systems operable will no longer be accurate and the 
    minimum number operable per trip system will be the same as they 
    were prior to November 12, 1993. Therefore, the proposed changes 
    will not significantly increase the consequences of an accident 
    previously evaluated.
        Part B: The proposed Technical Specification change to remove 
    the temporary revisions, which were in place to replace the 250 volt 
    shutdown board batteries is administrative. The LCO to extend the 
    allowed outage time (AOT) from a five-day to a 45-day AOT will no 
    longer be accurate and the five day AOT will be the same as it was 
    prior to Unit 2, Cycle 7. Therefore, the proposed changes will not 
    significantly increase the consequences of an accident previously 
    evaluated.
        Part C: The proposed Technical Specifications change revises 
    items 1 through 5 above (Section I, Description of the Proposed 
    Change, Part C), and is administrative. TVA has evaluated the 
    proposed technical specification changes and has determined that the 
    proposed changes are administrative in nature. Further, it provides 
    a revision based on an NRC Code of Federal Regulations rule change. 
    Also, the proposed changes provide correction of administrative 
    errors from previous technical specifications. For example, the Main 
    Steamline High Radiation remarks in Table 3.2.A, 1.b., should have 
    been deleted from the TS as part of TS-322. It also clarifies some 
    requirements to ensure consistent application throughout the 
    specifications. These changes do not affect any of the design basis 
    accidents. They do not involve an increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        Part A: The proposed Technical Specification change to remove 
    the temporary revisions, which were in place to modify the reactor 
    vessel water level instrumentation requested by NRC Bulletin 93-03, 
    is administrative. The temporary limiting condition for the minimum 
    number of trip systems operable will no longer be accurate and the 
    minimum number operable per trip system will be the same as they 
    were prior to November 12, 1993. No modifications to any plant 
    equipment are involved. There are no effects on system interactions 
    made by these changes. They do not create the possibility of a new 
    or different kind of accident from an accident previously evaluated.
        Part B: The proposed Technical Specification change to remove 
    the temporary revisions, which were in place to replace the 250 volt 
    shutdown board batteries is administrative. The LCO to extend the 
    allowed outage time (AOT) from a five day to a 45-day AOT will no 
    longer be accurate and the five day AOT will be the same as it was 
    prior to Unit 2, Cycle 7. No modifications to any plant equipment 
    are involved. There are no effects on system interactions made by 
    these changes. They do not create the possibility of a new or 
    different kind of accident from an accident previously evaluated.
        Part C: The proposed Technical Specifications change revises 
    items 1 through 5 above (Section I, Description of the Proposed 
    Change, Part C), and is administrative. TVA has evaluated the 
    proposed changes and has determined that they are administrative in 
    nature. Further, it provides revisions based on an NRC Code of 
    Federal Regulations rule change. It also provides correction of 
    administrative errors in previous technical specification changes. 
    For example, the Main Steamline High Radiation remarks in Table 
    3.2.A, 1.b., should have been deleted from the TS as part of TS-322. 
    It also clarifies some requirements to ensure consistent application 
    throughout the specifications. These changes do not affect any of 
    the design basis accidents. No modifications to any plant equipment 
    are involved. There are no effects on system interactions made by 
    these changes. They do not create the possibility of a new or 
    different kind of accident from an accident previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The proposed change is administrative in nature for Parts A, B, 
    and C. The proposed change includes the deletion of temporary 
    changes as a result of modifications to systems and clarification of 
    some requirements to ensure consistent application throughout the 
    specifications. Further, the proposed change corrects errors in 
    previous TS submittals. No safety margins are affected by these 
    changes.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff
    
    [[Page 42285]]
    
    proposes to determine that the amendment request involves no 
    significant hazards consideration.
        Local Public Document Room location: Athens Public Library, South 
    Street,Athens, Alabama 35611
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET l0H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
        Local Public Document Room location:  Athens Public Library, South 
    Street,Athens, Alabama 35611
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET l0H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260 and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2 and 3, Limestone County, 
    Alabama
    
        Date of amendment request: June 21, 1996 (TS 377)
        Description of amendment request: The proposed amendment provides a 
    new minimum critical power ratio safety limit to replace the current 
    non-conservative value. The amendment also updates the technical 
    specification bases to clarify the usage of the residual heat removal 
    supplemental spent fuel pool cooling mode.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed change in the Safety Limit Minimum Critical Power 
    Ratio (SLMCPR) does not increase the frequency of the precursors to 
    design basis events or operational transients analyzed in the Browns 
    Ferry Final Safety Analysis Report. Therefore, the probability of an 
    accident previously evaluated is not significantly increased.
        The proposed change in the SLMCPR ensures that 99.9 percent of 
    the fuel rods in the core are expected to avoid boiling transition 
    during the most limiting anticipated operational occurrence, which 
    is the design and licensing basis for the analysis of accidents and 
    transients described in the Browns Ferry Updated Final Safety 
    Analysis Report (UFSAR). It does not change the nuclear safety 
    characteristics of any safety system or containment system. 
    Therefore, the consequences of an accident, operator error, or 
    malfunction of equipment important to safety previously evaluated in 
    the UFSAR has not been increased.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed change to the Technical Specification requirements 
    for the safety limit minimum critical power ratio does not involve a 
    modification to plant equipment. No new failure modes are 
    introduced. There is no effect on the function of any plant system 
    and no new system interactions are introduced by this change. 
    Therefore, the proposed amendment does not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The proposed change will ensure that during any anticipated 
    operational transient, at least 99.9% of the fuel rods would be 
    expected to avoid boiling transition which is consistent with the 
    licensing basis. Since the margin [of] safety is being increased 
    with this change, the proposed amendment does not involve a 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Athens Public Library, South 
    Street, Athens, Alabama 35611
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET llH, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application request: July 18, 1996
        Description of amendment request: The amendment adopts ASTM D-3803-
    1989 as the laboratory testing standard for charcoal samples from the 
    charcoal adsorbers in the auxiliary/fuel building emergency exhaust 
    system.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The requested change to the charcoal sample surveillance 
    acceptance criteria for the fuel building and auxiliary building 
    emergency exhaust system will not affect the method of operation of 
    the system. The testing of the charcoal filter samples will continue 
    to be performed in accordance with NRC-accepted methods and 
    acceptance criteria, and the new test protocol will still ensure 
    filter efficiency is maintained equal to or greater than 90%. There 
    are no changes to the emergency exhaust system and it will continue 
    to function in a manner consistent with the safety analysis 
    assumptions and the plant design basis. There will be no degradation 
    in the performance of or an increase in the number of challenges to 
    equipment assumed to function during an accident. Therefore, the 
    proposed changes will not increase the probability or consequences 
    of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The changes to the surveillance requirements are being made to 
    adopt current NRC-accepted methods of testing charcoal samples. 
    These changes will not affect the method of operation of the 
    applicable systems and the laboratory testing will continue to 
    demonstrate the required adsorber performance after a design-basis 
    LOCA [loss-of-coolant accident] or fuel handling accident. No new or 
    different kind of accident from any previously evaluated will be 
    created.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The new charcoal adsorber sample laboratory testing protocol is 
    more stringent than the current testing practice and meets current 
    NRC-approved test methods. The new testing criteria will continue to 
    demonstrate the required adsorber performance after a design-basis 
    LOCA or fuel handling accident and will not affect the filter system 
    performance. Therefore, this change will not reduce the margin of 
    safety of the emergency exhaust system filter operation.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    & Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: William H. Bateman
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of amendment request: July 18, 1996
        Description of amendment request: The proposed amendment would 
    revise
    
    [[Page 42286]]
    
    Kewaunee Nuclear Power Plant (KNPP) Technical Specification (TS) 3.8, 
    ``Refueling Operations,'' and its associated Basis, by allowing the 
    containment personnel air lock doors to remain open during refueling 
    operations as long as at least one door is capable of being closed in 
    30 minutes or less.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed changes were reviewed in accordance with the 
    provisions of 10 CFR 50.92 to determine that no significant hazards 
    exist. The proposed changes will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Maintaining the doors of the personnel air lock open during 
    REFUELING OPERATIONS does not adversely affect the probability or 
    consequences of accidents previously evaluated. The only applicable 
    accident is a fuel handling accident described in [Updated Safety 
    Analysis Report] USAR Section 14.2.1. The fuel handling accident 
    evaluated in the USAR Section 14.2.1 assumes the accident to be in 
    the spent fuel pool in the Auxiliary Building. The accident assumes 
    a sudden release of the gaseous fission products held in the voids 
    between the pellets and cladding of all of the rods in the highest 
    rated fuel assembly at 100 hours following reactor shutdown. The 
    accident activity is assumed to discharge from the spent fuel pool 
    directly to the atmosphere at ground level. No credit is taken for 
    existing building structures, ventilation, or filtration systems. A 
    fuel handling accident in containment is bounded by this evaluation. 
    Furthermore, any release from a fuel handling accident in 
    containment can still be terminated by closing one of the personnel 
    air lock doors following containment evacuation.
        The containment personnel air lock doors are components integral 
    to the containment structure. They are not accident initiators. 
    Therefore, the proposed amendment does not increase the probability 
    of any previously evaluated accident.
        The control room operator immersion and inhalation doses were 
    reviewed as part of the updated Control Habitability Evaluation 
    Report. The report states that thyroid and whole body doses received 
    by control room operators in each of the other design basis 
    accidents discussed in KNPP USAR Section 14.2 are less than the 
    [loss of coolant accident] LOCA dose. This amendment does not change 
    the results of the Control Room Habitability Evaluation Report, 
    since the fuel handling accident evaluated in KNPP USAR Section 
    14.2.1 assumes a release directly to the atmosphere. This change 
    does not significantly increase the consequences of an accident 
    previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The accident evaluated in USAR section 14.2.1 bounds a fuel 
    handling accident in containment with the personnel air lock doors 
    open. The fuel handling accident evaluated in USAR section 14.2.1 
    assumes activity is discharged directly to the atmosphere at ground 
    level. Since no credit is taken for building structures, ventilation 
    systems or filtration systems, the position of the doors does not 
    affect the analysis of record. Furthermore, one of the air lock 
    doors can still be closed following containment evacuation to 
    terminate the release.
        The containment personnel air lock doors are components integral 
    to the containment structure. They are not accident initiators. The 
    proposed amendment does not create the possibility of any new or 
    different kind of accident [from any accident] previously evaluated.
        3. Involve a significant reduction in the margin of safety.
        Maintaining the containment personnel air lock doors open during 
    REFUELING OPERATIONS does not involve a significant reduction in the 
    margin of safety. A fuel handling accident in containment is bounded 
    by a fuel handling accident in the spent fuel pool. The spent fuel 
    pool fuel handling accident is assumed to have a sudden release of 
    the gaseous fission products held in the voids between the pellets 
    and cladding of all of the rods in the highest rated fuel assembly, 
    100 hours following reactor shutdown. The accident activity leaving 
    the spent fuel pool is assumed to discharge directly to the 
    atmosphere at ground level. No credit is taken for existing building 
    structures, ventilation, and filtration systems. Therefore, there is 
    no reduction in the current margin of safety. Furthermore, the 
    release caused by a fuel handling accident in containment can be 
    terminated by closing one of the personnel air lock doors following 
    containment evacuation.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, Wisconsin 54311-7001
        Attorney for licensee: Bradley D. Jackson, Esq., Foley and Lardner, 
    P. O. Box 1497, Madison, Wisconsin 53701-1497
        NRC Project Director: Gail H. Marcus
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of amendment request: July 12, 1996
        Brief description of amendment request: The amendment would change 
    Technical Specification 3.3.2.1, ``Engineered Safety Feature Actuation 
    System Instrumentation,'' to reflect a revised setpoint for the 
    interlock designated P-12.
        Date of publication of individual notice in Federal Register: July 
    23, 1996 (61 FR 38229)
        Expiration date of individual notice: August 22, 1996
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment
    
    [[Page 42287]]
    
    under the special circumstances provision in 10 CFR 51.12(b) and has 
    made a determination based on that assessment, it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson 
    Steam Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of application for amendment: January 29, 1996, as 
    supplemented June 17, 1996.
        Brief description of amendment: The amendment revises the technical 
    specifications (TS) table 4.1-3, item 4 to change the frequency of main 
    steam safety valve (MSSV) testing to that specified in NUREG-1431, the 
    improved ``Standard Technical Specifications, Westinghouse Plants'' and 
    adds the MSSV test acceptance requirements.
        Date of issuance: August 1, 1996
        Effective date: August 1, 1996
        Amendment No.: 171
        Facility Operating License No. DPR-23. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 28, 1996 (61 
    FR 7545). The June 17, 1996, submittal provided supplemental 
    information that was not outside the scope of the February 28, 1996, 
    notice. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 1, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of application for amendment: March 20, 1996
        Brief description of amendment: To relocate Technical Specification 
    3.3.3.2, Movable Incore Detectors, to plant procedures.
        Date of issuance: July 24, 1996
        Effective date: July 24, 1996
        Amendment No.: 65
        Facility Operating License No. NPF-63. Amendment revises the 
    Technical Specifications
        Date of initial notice in Federal Register: April 24, 1996 (61 FR 
    18164) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 24, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County and Northeast Nuclear Energy Company, 
    et al., Docket Nos. 50-245, 50-336, and 50-423, Millstone Nuclear 
    Power Station, Units 1, 2, and 3, New London County, Connecticut
    
        Date of application for amendments: November 22, 1995
        Brief description of amendments: The amendments replace the title-
    specific designation of members representing specific functional areas 
    on the Plant Operating Review Committee (PORC) for the Haddam Neck 
    Plant and Millstone Units 1, 2, and 3 with a functional area-specific 
    designation that stipulates membership qualification and experience 
    requirements. The amendments also clarify the composition of the Site 
    Operations Review Committee (SORC) at Millstone.
        Date of issuance: July 16, 1996
        Effective date: As of the date of issuance, to be implemented 
    within 60 days.
        Amendment Nos.: 190, 95, 200, 130
        Facility Operating License Nos. DPR-61, DPR-21, DPR-65, AND NPF-49: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: February 28, 1996 (61 
    FR 7549) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 16, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street Middletown, Connecticut 06457, for the Haddam Neck Plant, and 
    the Learning Resources Center, Three Rivers Community-Technical 
    College, 574 New London Turnpike, Norwich, Connecticut 06360, and 
    Waterford Library, ATTN: Vince Juliano, 49 Rope Ferry Road, Waterford, 
    Connecticut 06385, for Millstone 1, 2, and 3.
    
    Duke Power Company, et al., Docket No. 50-413, Catawba Nuclear 
    Station, Unit 1, York County, South Carolina
    
        Date of application for amendment: January 26, 1996, as 
    supplemented May 6, May 20, and June 5, 1996
        Brief description of amendment: The amendment revises the Technical 
    Specifications to permit a one-time operation of the containment purge 
    ventilation system during Mode 3 and 4 after the steam generator 
    replacement outage.
        Date of issuance: July 30, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment No.: 150
        Facility Operating License No. NPF-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 24, 1996 (61 FR 
    18165) The supplemental submittals provided clarifying information that 
    did not change the scope of the January 26, 1996, application for 
    amendment nor the initial proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated July 30, 1996. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: March 4, 1996
        Brief description of amendments: The amendments delete Flow 
    Monitoring System from Technical Specification 3.4.6.1 and associated 
    surveillance requirements.
        Date of issuance: July 29, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 168 and 150
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 24, 1996 (61 FR 
    18166) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 29, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223
    
    [[Page 42288]]
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: March 4, 1996
        Brief description of amendments: The amendments consist of changes 
    to the Final Safety Analysis Report for McGuire Units 1 and 2 to delete 
    the seismic qualification requirement for the Containment Atmosphere 
    Particulate Radiation Monitors.
        Date of issuance: July 30, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 169 and 151
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Final Safety Analysis Report.
        Date of initial notice in Federal Register: May 8, 1996 (61 FR 
    20845) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 30, 1996, and an 
    Environmental Assessment dated July 22, 1996. No significant hazards 
    consideration comments received: No.
        Local Public Document Room location:  Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223
    
    Entergy Gulf States, Inc., Cajun Electric Power Cooperative, and 
    Entergy Operations, Inc., Docket No. 50-458, River Bend Station, 
    Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: May 20, 1996
        Brief description of amendment: The amendment revised the Facility 
    Operating License and Appendix C to the license to reflect the name 
    change from Gulf States Utilities Company to Entergy Gulf States, Inc.
        Date of issuance: July 30, 1996
        Effective date: July 30, 1996
        Amendment No.: 88
        Facility Operating License No. NPF-47: The amendment revised the 
    operating license and Appendix C to the license.
        Date of initial notice in Federal Register: June 19, 1996 (61 FR 
    31183) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 30, 1996. No significant 
    hazards consideration comments received. No
        Local Public Document Room location:  Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803
    
    Entergy Operations, Inc., System Energy Resources, Inc., South 
    Mississippi Electric Power Association, and Entergy Mississippi, 
    Inc., Docket No. 50-416, Grand Gulf Nuclear Station, Unit 1, 
    Claiborne County, Mississippi
    
        Date of application for amendment: November 20, 1995, as 
    supplemented by letter dated December 15, 1995
        Brief description of amendment: The amendment revised and deleted 
    surveillance requirements, notes, and action statements involved with 
    the requirements for the drywell leak rate testing, and the air lock 
    leakage and interlock testing in Subsections 3.6.5.1 (Drywell), 3.6.5.2 
    (Drywell Air Lock), and 3.6.5.3 (Drywell Isolation Valves) of the 
    technical specifications.
        Date of issuance: August 1, 1996
        Effective date: August 1, 1996
        Amendment No: 126
        Facility Operating License No. NPF-29: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 22, 1996 (61 FR 
    25704) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 1, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, MS 39120.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: March 21, 1996 as supplemented 
    May 13, 1996.
        Brief description of amendments: Relocate requirements for 
    Radiological Effluent Controls from Technical Specifications (TS) to 
    the Offsite Dose Calculation Manual or the Process Control Program. New 
    programmatic controls for radioactive effluent and radiological 
    environmental controls will be incorporated into the TS. Also, 
    requirements for Gas Decay tanks and Explosive Gas Mixture will be 
    placed in a different area of the TS.
        Date of issuance: July 31, 1996
        Effective date: July 31, 1996
        Amendment Nos.: 188 and 182Facility Operating Licenses Nos. DPR-31 
    and DPR-41: Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: June 19, 1966 (61 FR 
    31180) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 31, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: May 28, 1996
        Brief description of amendments: Amendment changes Technical 
    Specification 6.2.2.i, ``Administrative Controls,'' regarding 
    Operations Manager qualifications.
        Date of issuance: July 22, 1996
        Effective date: July 22, 1996
        Amendment Nos.: 187 and 181Facility Operating Licenses Nos. DPR-31 
    and DPR-41: Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: June 19, 1996 (61 FR 
    31181) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 22, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    GPU Nuclear Corporation and Saxton Nuclear Experimental (SNEC) 
    Corporation, Docket No. 50-146, Saxton Nuclear Experimental 
    Facility (SNEF)
    
        Date of application for amendment: February 2, 1996, as 
    supplemented on February 28, April 24, and May 24, 1996.
        Brief description of amendment: The proposed amendment would (1) 
    increase the scope of work permitted at SNEF to include asbestos 
    removal, removal of defunct plant electrical services, and installation 
    of decommissioning support facilities and systems; (2) eliminate areas 
    within the containment vessel requiring administrative access controls; 
    and (3) revise the facility layout diagram to allow the exclusion area 
    to consist of, at a minimum, the containment vessel and, at a maximum, 
    to extend to the SNEF outer security fence and to include on the 
    diagram the footprint of the proposed decommissioning support 
    facilities.
        Date of issuance: July 23, 1996
        Effective date: July 23, 1996
        Amendment No.: 14
        Amended Facility License No. DPR-4: Amendment changed the Technical 
    Specifications.
        Date of initial notice in Federal Register: June 19, 1996 (61 FR 
    31182).
    
    [[Page 42289]]
    
    The Commission's related evaluation of the amendment is contained in a 
    safety evaluation dated July 23, 1996. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Saxton Community Library, 911 
    Church Street, Saxton, Pennsylvania 16678
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun 
    Station, Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: February 1, 1996
        Brief description of amendment: The amendment revised Technical 
    Specifications to allow an increase in the initial nominal Uranium-235 
    enrichment limit for fuel assemblies which may be stored in the spent 
    fuel pool.
        Date of issuance: July 30, 1996
        Effective date: July 30, 1996
        Amendment No.: 174
        Facility Operating License No. DPR-40. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 13, 1996 (61 FR 
    10396) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 30, 1996 . No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of application for amendments: May 9, 1996
        Brief description of amendments: The amendments revised the 
    combined Technical Specifications (TS) for the Diablo Canyon Nuclear 
    Power Plant (DCPP), Unit Nos. 1 and 2 by revising Technical 
    Specifications (TS) 3/4.3.2, ``Engineered Safety Features Actuation 
    System Instrumentation,'' and 3/4.6.2, ``Containment Spray System.'' 
    The changes clarified the description of the initiation signal required 
    for operation of the containment spray system at DCPP and correctly 
    incorporated changes made in previous license amendments. All of the 
    changes are administrative in nature.
        Date of issuance: August 1, 1996
        Effective date: August 1, 1996
        Amendment Nos.: Unit 1 - 114; Unit 2 - 112
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 19, 1996 (61 FR 
    31184) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 1, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of application for amendments: June 3, 1996, as superseded by 
    application dated June 25, 1996.
        Brief description of amendments: These amendments revise Improved 
    Technical Specification (TS) 3.3.11, ``Post Accident Monitoring 
    Instrumentation (PAMI),'' and Improved TS 5.5.2.13, ``Diesel Fuel Oil 
    Testing Program.'' Specifically, the number of instruments required to 
    measure reactor coolant inlet temperature (TCold), and reactor 
    coolant outlet temperature (THot), will be revised from two per 
    loop to two (with one cold leg indication and one hot leg indication 
    per steam generator). These changes to the Improved TS reinstate 
    provisions of the current San Onofre Nuclear Generating Station 
    (SONGS), Unit Nos. 2 and 3 TS revised as part of NRC Amendment Nos. 127 
    and 116 for SONGS Units 2 and 3 (referred to as the Improved TS).
        Date of issuance: August 1, 1996
        Effective date: August 1, 1996, to be implemented by August 9, 
    1996.
        Amendment Nos.: Unit 2 - 130; Unit 3 - 119
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 2, 1996 (61 FR 
    34452) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 1, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 
    50-339, North Anna Power Station, Units No. 1 and No. 2, Louisa 
    County, Virginia
    
        Date of application for amendments: July 26, 1995, as supplemented 
    April 25, 1996. The April 25, 1996, letter provided clarifying 
    information that did not change the scope of the July 26, 1995, 
    application and initial proposed no significant hazards consideration 
    determination.
        Brief description of amendments: The amendments clarify the 
    Technical Specifications to allow switching of charging and low-head 
    safety injection pumps during unit shutdown conditions. These 
    amendments also allow additional methods of rendering these same pumps 
    incapable of injecting into the reactor coolant system when required 
    for low-temperature conditions.
        Date of issuance: July 24, 1996
        Effective date: July 24, 1996
        Amendment Nos.: 202 and 183
        Facility Operating License Nos. NPF-4 and NPF-7. Amendments revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: August 30, 1995 (60 FR 
    45190) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 24, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of application for amendment: May 8, 1996
        Brief description of amendment: The amendment revises Kewaunee 
    Nuclear Power Plant Technical Specification (TS) 5.3, ``Reactor,'' and 
    TS 5.4, ``Fuel Storage,'' by removing the enrichment limit for reload 
    fuel and imposing fuel storage restrictions on the spent fuel storage 
    racks and the new fuel storage racks. The revised TS are structured 
    consistent with the Westinghouse Standard Technical Specifications and 
    the fuel storage restrictions are based on the criticality analyses 
    used to support Amendment No. 92 dated March 7, 1991.
        Date of issuance: July 23, 1996
        Effective date: July 23, 1996
        Amendment No.: 124
        Facility Operating License No. DPR-43: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 19, 1996 (61 FR 
    31185) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 23, 1996. No significant 
    hazards consideration comments received: No.
    
    [[Page 42290]]
    
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, Wisconsin 54311-7001
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: May 1, 1995
        Brief description of amendment: This amendment revises TS Section 
    6.0, throughout, to reflect an organization change in which the 
    position of Vice President Plant Operations has been eliminated and the 
    positions of Chief Operating Officer and Plant Manager were created. 
    This change assigns certain management responsibilities to the Chief 
    Operating Officer and Plant Manager.
        Date of issuance: August 1, 1996
        Effective date: August 1, 1996, to be implemented within 30 days of 
    issuance.
        Amendment No.: 100
        Facility Operating License No. NPF-42. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 22, 1996 (61 FR 
    25716) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 1, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Dated at Rockville, Maryland, this 7th day of August 1966.
        For the Nuclear Regulatory Commission
    Steven A. Varga, Director,
    Division of Reactor Projects - I/II, Office of Nuclear Reactor 
    Regulation
    [Doc. 96-20586 Filed 8-13-96; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Effective Date:
8/1/1996
Published:
08/14/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X96-10814
Dates:
August 1, 1996
Pages:
42274-42290 (17 pages)
PDF File:
x96-10814.pdf