X96-30828. Biweekly Notice  

  • [Federal Register Volume 61, Number 168 (Wednesday, August 28, 1996)]
    [Notices]
    [Pages 44353-44368]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X96-30828]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating Licenses 
    Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from August 3, 1996, through August 16, 1996. The 
    last biweekly notice was published on August 14, 1996 (61 FR 42274).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules 
    Review and Directives Branch, Division of Freedom of Information and 
    Publications Services, Office of Administration, U.S. Nuclear 
    Regulatory Commission, Washington, DC 20555-0001, and should cite the 
    publication date and page number of this Federal Register notice. 
    Written comments may also be delivered to Room 6D22, Two White Flint 
    North, 11545 Rockville Pike, Rockville, Maryland from 7:30 a.m. to 4:15 
    p.m. Federal workdays. Copies of written comments received may be 
    examined at the NRC Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC. The filing of requests for a hearing and 
    petitions for leave to intervene is discussed below.
        By September 27, 1996, the licensee may file a request for a 
    hearing with respect to issuance of the amendment to the subject 
    facility operating license and any person whose interest may be 
    affected by this proceeding and who wishes to participate as a party in 
    the proceeding must file a written request for a hearing and a petition 
    for leave to intervene. Requests for a hearing and a petition for leave 
    to intervene shall be filed in accordance with the Commission's ``Rules 
    of Practice for
    
    [[Page 44354]]
    
    Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested persons 
    should consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Docketing and 
    Services Branch, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, 
    and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of amendment request: July 19, 1996
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) Section 3/4.6.2, Containment Spray 
    System, to extend the surveillance interval for performance of an air 
    or smoke flow test through containment spray nozzles from once per 5 
    years to once per 10 years. This change is consistent with the guidance 
    in NRC Generic Letter 93-05, ``Line Item Technical Specifications 
    Improvements to Reduce Surveillance Requirements for Testing During 
    Power Operations,'' and NUREG-1366, ``Improvements To Technical 
    Specifications Surveillance Requirements.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed extended testing frequency of containment spray 
    nozzles will not affect any initiators of any previously evaluated 
    accidents or change the manner of operation for any system or 
    component. The containment spray system serves a mitigating function 
    by removing heat and fission products from a post accident 
    containment atmosphere. Increasing the surveillance test interval 
    will not affect the system's ability to provide this function. 
    Therefore, there would be no increase in the probability or 
    consequences of an accident previously evaluated.
    
    [[Page 44355]]
    
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        Since the proposed change affects only a surveillance frequency, 
    it will not involve any physical alterations to plant equipment or 
    alter the manner in which any safety-related system performs its 
    function. Therefore, the proposed change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        The proposed change does not affect any Final Safety Analysis 
    Report (FSAR) Chapter 15 accident analyses or impact the margin of 
    safety for the containment spray system as defined in the Bases to 
    the Technical Specifications. Therefore, the proposed change does 
    not involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602
        NRC Project Director: Eugene V. Imbro
    
    Commonwealth Edison Company, Docket Nos. 50-254 and 50-265, Quad 
    Cities Nuclear Power Station, Units 1 and 2, Rock Island County, 
    Illinois
    
        Date of amendment request: June 10, 1996
        Description of amendment request: To change the technical 
    specifications to reflect the transition from General Electric Company 
    (GE) to Siemens Power Corporation (SPC) as the fuel supplier for the 
    Quad Cities Nuclear Power Station, Units 1 and 2.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The probability of an evaluated accident is derived from the 
    probabilities of the individual precursors to that accident. The 
    consequences of an evaluated accident are determined by the 
    operability of plant systems designed to mitigate those 
    consequences. Limits will be established consistent with NRC 
    approved methods to ensure that fuel performance during normal, 
    transient, and accident conditions is acceptable. The proposed 
    Technical Specifications amendment reflects previously approved SPC 
    methodology used to analyze normal operations, including anticipated 
    operational occurrences (AOOs), and to determine the potential 
    consequences of accidents.
        Licensing Methods and Models
        The proposed amendment is to support operation with NRC approved 
    fuel and licensing methods supplied from Siemens Power Corporation. 
    In accordance with FSAR Chapter 15, the same accidents and 
    transients will be analyzed with the new fuel and methods as were 
    analyzed by GE for GE fuel. The analysis methods and models are NRC 
    approved. These approved methods and models are used to determine 
    the fuel thermal limits (e.g., LHGR, APLHGR, MCPR). The SPC core 
    monitoring code enables the site to monitor keff as well as rod 
    density to perform the reactivity anomaly surveillance. This is 
    consistent with GE methodology. The support systems for minimizing 
    the consequences of transients and accidents are not affected by the 
    proposed amendment. Therefore, the change in licensing analysis 
    methods and models does not significantly increase the probability 
    of an accident or the consequences of an accident previously 
    identified.
        New Fuel Design
        The use of ATRIUM 9B fuel at Quad Cities does not involve a 
    significant increase in the probability or consequences of any 
    accident previously evaluated in the FSAR. The ATRIUM-9B fuel is 
    generically approved for use as a reload BWR fuel type (Reference: 
    ANF-89-014(P)(A) Rev. 1 Supplement 1, General Mechanical Design for 
    Advanced Nuclear Fuels 9X9-IX and 9X9-9X BWR Reload Fuel). Limiting 
    postulated occurrences and normal operation have been analyzed using 
    NRC-approved methods for the ATRIUM 9B fuel design to ensure that 
    safety limits are protected and that acceptable transient and 
    accident performance is maintained.
        The reload fuel has no adverse impact on the performance of in-
    core neutron flux instrumentation or CRD response. The ATRIUM-9B 
    fuel design will not adversely affect performance of neutron 
    instrumentation nor will it adversely affect the movement of control 
    blades relative to the GE fuel. The exterior dimensions of the 
    ATRIUM-9B fuel have been evaluated by ComEd; the SPC fuel provides 
    adequate clearances relative to the GE10 fuel installed at Quad 
    Cities. Thus, no increased interactions with the adjacent control 
    blade and nuclear instrumentation are created. Additionally, given 
    the above mentioned overall envelope similarities, no problems are 
    anticipated with other station equipment such as the fuel storage 
    racks, the new fuel inspection stand and the spent fuel pool fuel 
    preparation machine. Therefore, the probability of adverse 
    interactions between the Siemens fuel and components in the core and 
    fuel handling equipment is not significantly increased.
        The ATRIUM 9B design is neutronically compatible with the 
    existing fuel types and core components in the Quad Cities core. SPC 
    tests have demonstrated that the ATRIUM-9B fuel design is 
    hydraulically compatible with the GE9/GE10 fuel. The bundle pressure 
    drop characteristics of the ATRIUM 9B bundle are similar to those of 
    the GE9/GE10 fuel design, hence core thermal-hydraulic stability 
    characteristics are not adversely affected by the ATRIUM 9B design. 
    Cycle stability calculations are performed by SPC. Therefore, the 
    probability of thermal hydraulic instability is not significantly 
    increased.
        An evaluation of the Emergency Procedures is being performed to 
    ensure that the use of the ATRIUM-9B fuel at Quad Cities does not 
    alter any assumptions previously made in evaluating the radiological 
    consequences of an accident at Quad Cities Station. Therefore, the 
    radiological consequences of accidents are not significantly 
    increased.
        Methods approved by the NRC are being used in the evaluation of 
    fuel performance during normal and abnormal operating conditions. 
    The ComEd and SPC methods to be used for the cycle specific 
    transient analyses have been previously NRC approved. The proposed 
    methodologies are administrative in nature and do not significantly 
    affect any accident precursors or accident results; as such, the 
    proposed incorporation of the SPC methodologies for Quad Cities does 
    not significantly increase the probability or consequences of any 
    previously evaluated accidents. The description of the fuel is 
    modified to include the water box design of the NRC approved ATRIUM-
    9B fuel. This change is administrative.
        Review of the above concludes that the probability of occurrence 
    and the consequences of an accident previously evaluated in the 
    safety analysis report have not been significantly increased.
        * * * * *
        2) Create the possibility of a new or different kind of accident 
    from any accident previously evaluated:
        Creation of the possibility of a new or different kind of 
    accident would require the creation of one or more new precursors of 
    that accident. New accident precursors may be created by 
    modifications of the plant configuration, including changes in 
    allowable modes of operation.
        Licensing Methods and Models
        The proposed Technical Specification amendment reflects 
    previously approved SPC methodology used to analyze normal 
    operations, including AOOs, and to determine the potential 
    consequences of accidents. In accordance with FSAR Chapter 15, the 
    same accidents and transients will be analyzed with the new fuel and 
    methods as were analyzed by GE for GE fuel. As stated above, the 
    proposed changes do not permit modes of operation which differ from 
    those currently permitted; therefore, the possibility of a new or 
    different kind of accident is not created. Plant support equipment 
    is not affected by the proposed changes; therefore, no new failure 
    modes are created.
        New Fuel Design
        The basic design concept of a 9x9 fuel pin array with an 
    internal water box has been used in various lead assembly programs 
    and in reload quantities in Europe since 1986.
    
    [[Page 44356]]
    
    WNP-2 has loaded reload quantities since 1991. Approximately 650 
    water box assemblies have been irradiated in the United States 
    through 1995, with a substantially higher number being irradiated 
    overseas. The NRC has reviewed and approved the ATRIUM-9B fuel 
    design (Reference: ANF-89-014(P)(A) Rev. 1 Supplement 1, Generic 
    Mechanical Design for Advanced Nuclear Fuels 9X9-IX and 9X9-9X BWR 
    Reload Fuel). The similarities in fuel design and operation between 
    GE and SPC, and the previous Boiling Water Reactor experience with 
    both vendors' fuel indicate there would be no new or different types 
    of accidents for Quad Cities than have been considered for the 
    existing fuel. Therefore, the use of ATRIUM-9B fuel at Quad Cities 
    does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        * * * * *
        3) Involve a significant reduction in the margin of safety for 
    the following reasons:
        The existing margin to safety is provided by the existing 
    acceptance criteria (e.g., 10CFR50.46 limits). The proposed 
    Technical Specification amendment reflects previously approved SPC 
    methodology used to demonstrate that the existing acceptance 
    criteria are satisfied. The revised methodology has been previously 
    reviewed and approved by the USNRC for application to reload cores 
    of GE BWRs. References for the Licensing Topical Reports which 
    document this methodology, and include the Safety Evaluation Reports 
    prepared by the USNRC, are added to the Reference section of the 
    Technical Specifications as part of this amendment.
        Licensing Methods and Models
        The proposed amendment does not involve changes to the existing 
    operability criteria. NRC approved methods and established limits 
    (implemented in the COLR) ensure acceptable margin is maintained. 
    The ComEd and SPC reload methodologies for the ATRIUM-9B reload 
    design are consistent with the Technical Specification Bases. The 
    Limiting Conditions for Operation are taken into consideration while 
    performing the cycle specific and generic reload safety analyses. 
    NRC approved methods are listed in Section 6 of the Technical 
    Specifications.
        Analyses performed with NRC-approved methodology have 
    demonstrated that fuel design and licensing criteria will be met 
    during normal and abnormal operating conditions. The same margins of 
    safety are utilized by SPC as GE (e.g., limits on peak cladding 
    temperature, cladding oxidation, plastic strain). Therefore, there 
    is not a significant reduction in the margin of safety.
        New Fuel Design
        The exterior dimensions of the ATRIUM-9B fuel assembly result in 
    equivalent clearances relative to the GE10B. Thus, no increased 
    interactions with the adjacent control blade and nuclear 
    instrumentation are created. The change does not adversely impact 
    equipment important to safety; therefore,the margin of safety is not 
    significantly reduced.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Dixon Public Library, 221 
    Hennepin Avenue, Dixon, Illinois 61021
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603
        NRC Project Director: Robert A. Capra
    
    Duke Power Company, Docket Nos. 50-269, 270 and 50-287, Oconee 
    Nuclear Station, Units 1, 2 and 3, Oconee County, South Carolina
    
        Date of amendment request: August 12, 1996
        Description of amendment request: The proposed change would 
    implement the performance-based containment leak rate testing 
    provisions of Option B to 10 CFR Part 50 Appendix J for the Type A 
    (containment) testing program.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The following analysis is presented, pursuant to 10 CFR 50.91, 
    to demonstrate that the proposed change will not create a 
    Significant Hazard Consideration.
        1. The proposed change will not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        Containment leak rate testing is not an initiator of any 
    accident; the proposed change does not affect reactor operations or 
    accident analysis, and has no significant radiological consequences. 
    Therefore, this proposed change will not involve an increase in the 
    probability or consequences of any previously-evaluated accident.
        2. The proposed change will not create the possibility of any 
    new accident not previously evaluated.
        The proposed change does not affect normal plant operations or 
    configuration, or change any design basis. The proposed changes will 
    not affect the response of [the] containment during a design basis 
    accident.
        3. There is no significant reduction in a margin of safety.
        The proposed changes are based on NRC-accepted provisions, and 
    maintain necessary levels of reliability of containment integrity. 
    The performance-based approach to leakage rate testing recognizes 
    that historically good results of containment testing provide 
    appropriate assurance of future containment integrity; this supports 
    the conclusion that the impact on the health and safety of the 
    public as a result of extended test intervals is negligible.
        Based on the above, no significant hazards consideration is 
    created by the proposed change.
        The NRC has reviewed the licensee's analysis and, based on 
    thisreview, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691
        Attorney for licensee: J. Michael McGarry, III, Winston and Strawn, 
    1200 17th Street, NW., Washington, DC 20036
        NRC Project Director: Herbert N. Berkow
    
    Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear One, 
    Unit No. 1, Pope County, Arkansas
    
        Date of amendment request: May 31, 1996
        Description of amendment request: The proposed amendment revises 
    the surveillance test interval for the reactor protection system 
    reactor trip breakers, reactor trip modules, and electronic trip relays 
    from 1 month to 6 months. In addition to requesting a change to the 
    Arkansas Nuclear One, Unit 1 Technical Specifications, the request also 
    proposes the same changes to NUREG-1430, Standard Technical 
    Specifications - Babcock and Wilcox Plants.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Criterion 1 - Does Not Involve a Significant Increase in the 
    Probability or Consequences of an Accident Previously Evaluated.
        The accident mitigation features of the plant are not affected 
    by the proposed test interval extension. The results of the B&W 
    Owners Group Topical Report BAW-10167, Supplement 3, ``Justification 
    for increasing The Reactor Trip System On-Line Test Intervals,'' 
    show that the test interval extension of the reactor protection 
    system trip devices is not a significant contributor to trip system 
    unavailability or the risk of core damage.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        Criterion 2. Does Not Create the Possibility of a New or 
    Different Kind of Accident from any Previously Evaluated.
        The reactor trip device surveillance test interval is not, in 
    and of itself, considered to be an accident initiator. Failure of a 
    trip device to function is an analyzed condition and does not 
    constitute a new or different kind of accident.
        Therefore, this change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        Criterion 3. Does Not Involve a Significant Reduction in the 
    Margin of Safety.
        The results of the B&W Owners Group Topical Report BAW-10167, 
    Supplement 3, ``Justification for Increasing The Reactor Trip
    
    [[Page 44357]]
    
    System On-Line Test Intervals,'' show that the test interval 
    extension of the reactor protection system trip devices is not a 
    significant contributor to trip system unavailability or the risk of 
    core damage. In addition, the uncertainty analysis contained in BAW-
    10167 confirms the robustness of the results by demonstrating that 
    even with an order of magnitude change in the failure data, the 
    incremental increase due to an increased test interval is 
    insignificant. Entergy Operations has reviewed BAW-10167 and found 
    it applicable to ANO-1.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations, Inc., Docket Nos. 50-313 and 50-368, Arkansas 
    Nuclear One, Unit Nos. 1 and 2 (ANO-1&2), Pope County, Arkansas
    
        Date of amendment request: May 9, 1996
        Description of amendment request: The proposed amendment changes 
    the name of Arkansas Power and Light Company (AP&L) to Entergy 
    Arkansas, Inc. in both the Operating License and the Technical 
    Specifications. AP&L is licensed to own and possess Arkansas Nuclear 
    One (ANO). The company licensed to operate ANO, Entergy Operations, 
    Inc. is unaffected by this change.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Does Not Involve a Significant Increase in the Probability or 
    Consequences of an Accident Previously Evaluated.
        The proposed change documents changing the legal name of the 
    company. The proposed change will not affect any other obligations. 
    The company will continue to own all of the same assets, will 
    continue to serve the same customers, and will continue to honor all 
    existing obligations and commitments. Therefore, this change does 
    not involve a significant increase in the probability or 
    consequences of any accident previously evaluated.
        2. Does Not Create the Possibility of a New or Different Kind of 
    Accident from any Previously Evaluated.
        The administrative changes in the operating license requirements 
    do not involve any change in the design of the plant. Therefore, 
    this change does not create the possibility of a new or different 
    kind of accident from any previously evaluated.
        3. Does Not Involve a Significant Reduction in the Margin of 
    Safety.
        The proposed change is administrative in nature and does not 
    reduce the margin of safety imposed by any current requirements. 
    Therefore, this change does not involve a significant reduction in 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Dates of amendment request: July 17, 1996
        Description of amendment request: The licensee proposed to change 
    the Turkey Point Units 3 and 4 Technical Specifications (TS) to 
    implement 10 CFR 50, Appendix J, Option B, for containment leakage 
    testing. Changes include relocating the details for containment testing 
    to the ``containment leakage rate testing program'' and adding the 
    requirements of the containment leakage rate testing program to TS 
    6.8.4, which describes facility programs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below.
        (1) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendments do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    because:
        a) These proposed changes are all consistent with NRC 
    requirements and guidance for implementation of 10 CFR 50, Appendix 
    J, Option B.
        b) Based on industry and NRC evaluations performed in support of 
    developing Option B, these changes potentially result in a minor 
    increase in the consequences of an accident previously evaluated due 
    to the expanded testing intervals. However, the proposed changes do 
    not result in an increase in the core damage frequency since the 
    containment system is used for mitigation purposes only.
        c) These changes are expected to result in increased attention 
    to components with poor leakage test history as part of the 
    performance-based nature of Option B, such that the marginally 
    increased consequences from the expanded testing intervals may be 
    further reduced or negated.
        Therefore, these changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendments would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The use of the modified specifications can not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated since the proposed amendments will not change 
    the physical plant or the modes of plant operation defined in the 
    facility operating license. No new failure mode is introduced due to 
    the implementation of a performance-based program for containment 
    leakage rate testing, since the proposed changes do not involve the 
    addition or modification of equipment, nor do they alter the design 
    or operation of affected plant systems, structures, or components.
        (3) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant reduction in a margin of 
    safety.
        The operating limits and functional capabilities of the affected 
    systems, structures, and components are basically unchanged by the 
    proposed amendments due to the following reasons:
        a) The acceptance criteria for total integrated containment 
    leakage of 1.0 La is consistent with the current technical 
    specifications and is within the design basis accident assumptions, 
    and therefore does not reduce the margin of safety.
        b) The increase in intervals between leak-test surveillances 
    will not significantly reduce the margin of safety as shown by 
    findings in NUREG 1493, ``Performance-Based Containment Leak-Test 
    Program'', which was based on implementation of the performance-
    based testing of Option B.
        Therefore these changes do not involve a significant reduction 
    in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied.Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199
        Attorney for licensee: J. R. Newman, Esquire, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036
        NRC Project Director: Frederick J. Hebdon
    
    [[Page 44358]]
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-321 and 50-366, Edwin I. Hatch Nuclear Plant, Units 1 and 2, 
    Appling County, Georgia
    
        Date of amendment request: May 21, 1996
        Description of amendment request: The proposed change to the 
    condensate storage tank (CST) level indication would ensure that the 
    water level is sufficient to provide 50,000 gallons of water for core 
    spray makeup to the reactor pressure vessel.
        Technical Specification (TS) Surveillance Requirement (SR) 
    3.5.2.2.b for ECCS - Shutdown states: ``Condensate storage tank (CST) 
    water level is [greater than or equal to] 12 feet.'' The corresponding 
    Bases state: ''... the CST contains [greater than or equal to] 150,000 
    gallons of water, equivalent to 12 feet, ensures that the CS System can 
    supply at least 50,000 gallons of makeup water to the RPV.''
        Subsequent licensee analyses confirmed that Plant Hatch Units 1 and 
    2 CST configurations are different; that is, for both CSTs, a water 
    level of 12 feet is not equivalent to the required capacity of 150,000 
    gallons of water. Based on these calculations, the correct level for 
    the Unit 1 CST is 13 feet, and the correct level for the Unit 2 CST is 
    15 feet.
        The proposed change would revise Unit 1 and Unit 2 SR 3.5.2.2.b to 
    require a CST water level of greater than or equal to 13 feet and 
    greater than or equal to 15 feet, respectively, to ensure at least 
    50,000 gallons of water are available for core spray (CS) makeup to the 
    reactor pressure vessel (RPV).
        The associated Bases for each unit will be revised accordingly.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration which is presented below:
        1. The proposed TS change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated, because this administrative change to the CST 
    water level does not alter the operation of any plant system or 
    component. The proposed change does not involve a physical 
    modification to any structure, system, or component. The minimum CST 
    water level for each unit is being increased to account for the 
    height of the CS suction standpipe within each CST and the 
    differences in the Unit 1 and
        Unit 2 CST diameters (gallons/ft of water) as follows:
        a. Unit 1 - The proposed minimum water level is calculated as: 
    CS suction standpipe height of 9 ft + (50,000 gallons divided by 
    12,704 gallons/ft) = 12.93 ft or 13 ft.
        b. Unit 2 - The proposed minimum water level is calculated as: 
    CS suction standpipe height of 10 ft + (50,000 gallons divided by 
    11,343 gallons/ft) = 14.4 ft or 15 ft.
        The revised minimum levels ensure at least 50,000 gallons of 
    water are provided above the top of the standpipe in each unit's CST 
    and are available for CS makeup to the RPV, as stated in the 
    applicable Bases. The TS Limiting Conditions for Operation (LCO) 
    remain unaffected by the proposed change.
        2. The proposed TS change does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated. Revising Surveillance Requirement acceptance criteria 
    does not result in any physical modification to the plant or 
    operation of any existing equipment.
        3. The proposed TS change does not involve a significant 
    reduction in a margin of safety, since this administrative change 
    only ensures the existing TS Bases are satisfied by increasing the 
    minimum CST water level requirement to ensure at least 50,000 
    gallons of water are available for CS injection to the RPV. The 
    proposed change does not involve a physical modification to any 
    structure, system or component, and does not modify the operation of 
    any existing equipment.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Herbert N. Berkow
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: July 8, 1996
        Description of amendment request: The proposed amendment would 
    clarify that the component cooling water system surge tank level 
    instrumentation can be demonstrated operable by performing a channel 
    calibration test during any plant mode of operation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change to Technical Specification Surveillance 
    Requirement 4.7.3.b.3 will not effect any accident initiators or 
    precursors and will not alter the design assumptions for the systems 
    or components used to mitigate the consequences of an accident. 
    Calibration is performed on level instrumentation of Component 
    Cooling Water System trains that are out of service for scheduled 
    maintenance. Isolation redundancy is provided by instrumentation 
    associated with the trains that are in service during the 
    calibration. Since the surveillance will continue to be performed at 
    the specified interval, this proposed change will not increase the 
    probability of occurrence of an accident previously evaluated. The 
    surveillance does not differ from those previously performed; 
    therefore, there is no impact on the consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Clarifying the surveillance interval for surge tank level 
    instrumentation does not involve installation or operation of new or 
    different kinds of equipment. There is no change in the procedures 
    as described in the Technical Specifications. The change only 
    clarifies the interval at which the subject calibration will be 
    performed. Therefore, the proposed change does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The specified surveillance will remain as stated in the 
    Technical Specifications. Consequently, there is no reduction in the 
    effectiveness of the surveillance in ensuring equipment operability. 
    Calibration is performed on level instrumentation of Component 
    Cooling Water System trains that are out of service for scheduled 
    maintenance. Isolation redundancy is provided by instrumentation 
    associated with the trains that are in service during the 
    calibration. Consequently, clarifying the interval at which the 
    calibration is performed will have no significant impact on the 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, N.W., Washington, DC 20036-5869
        NRC Project Director: William D. Beckner
    
    [[Page 44359]]
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: August 8, 1996
        Description of amendment request: The proposed amendment would 
    allow the transition from Mode 4 to Mode 3 with the turbine-driven 
    auxiliary feedwater pump inoperable and allow a 72-hour period after 
    the entry into Mode 3 to complete all necessary operability testing.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change will allow entry into Mode 3 with an 
    inoperable Turbine Driven Auxiliary Feedwater pump. Since the 
    operability test on the Turbine Driven Auxiliary Feedwater pump can 
    only be performed once steam pressure is greater than or equal to 
    1000 psig, this change will allow the plant to reach the Mode where 
    steam pressure greater than or equal to 1000 psig is available to 
    perform the operability testing on the Turbine Driven Auxiliary 
    Feedwater pump. The allowance of 72 hours to complete the 
    surveillance testing will make the surveillance requirements 
    consistent with the allowed outage time already established in the 
    Action Statements. The proposed change does not affect the 
    probability of an accident. The Turbine Driven Auxiliary Feedwater 
    pump is not assumed to be an initiator of any analyzed event. The 
    consequences of an accident previously evaluated remain unchanged by 
    allowing the pump to be inoperable until suitable conditions exist 
    to perform the operability testing. The operability testing will 
    continue to demonstrate that the Turbine Driven Auxiliary Feedwater 
    pump will perform as required prior to entry into Mode 2. This 
    change will not alter assumptions relative to the mitigation of an 
    accident or transient event. Therefore, this change will not involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        This change will not physically alter the plant (no new or 
    different type of equipment will be installed). The changes in 
    methods governing normal plant operation are consistent with current 
    safety analysis assumptions. The proposed change will allow entry 
    into Mode 3 with the Turbine Driven Auxiliary Feedwater pump 
    inoperable in order to perform the pump Operability Test on the 
    turbine driven AFW [Auxiliary Feedwater] pump once steam pressure is 
    greater than or equal to 1000 psig. Therefore, this change does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change will allow entry into Mode 3 with the 
    Turbine Driven AFW pump inoperable in order to perform the pump 
    Operability Test on the turbine driven AFW pump once steam pressure 
    is greater than or equal to 1000 psig. This will allow time for the 
    plant to obtain suitable test conditions with steam pressure greater 
    than or equal to 1000 psig. The margin of safety is not affected by 
    this change. The operability testing will continue to maintain 
    assurance that the AFW Pumps will perform as required prior to entry 
    into Mode 2. The safety analysis assumptions will still be 
    maintained, thus, no question of safety exists. Therefore, this 
    change does not involve a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488
        Attorney for licensee: Jack R. Newman, Esq., Morgan, Lewis & 
    Bockius, 1800 M Street, N.W., Washington, DC 20036-5869
        NRC Project Director: William D. Beckner
    
    North Atlantic Energy Service Corporation, Docket No. 50-443, 
    Seabrook Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: June 4, 1996
        Description of amendment request: The proposed amendment would 
    modify the Seabrook Station, Unit No. 1 Technical Specifications to 
    implement Option B to 10 CFR Part 50, Appendix J by referring to 
    Regulatory Guide 1.163, ``Performance-Based Containment Leak-Test 
    Program. The following Technical Specifications would be affected by 
    the proposed amendment:
        1. Definitions: Definition 1.7, Containment Integrity (Item d.) 
    would be revised to reflect that leakage rates would be in accordance 
    with the Containment Leakage Rate Testing Program.
        2. Limiting Conditions for Operation and Surveillance Requirements:
        a. Containment Integrity: Surveillance Requirement 4.6.1.1.c would 
    be deleted because the specific guidance would be contained in the 
    Containment Leakage Rate Testing Program.
        b. Containment Leakage: Limiting Condition for Operation 3.6.1.2.a 
    through 3.6.1.2.c and Surveillance Requirements 4.6.1.2.a through 
    4.6.1.2.h would be revised to replace specific guidance with a 
    reference to the Containment Leakage Rate Testing Program.
        c. Containment Leakage: The Action for Limiting Condition for 
    Operation 3.6.1.2 would be revised to include the equivalent Action as 
    required for Limiting Condition for Operation 3.6.1.1 when the overall 
    integrated containment leak rate exceeds 1.0 La.
        d. Containment Air Locks: Limiting Conditions for Operation 
    3.6.1.3.a and 3.6.1.3.b would be deleted and Surveillance Requirements 
    4.6.1.3.a and 4.6.1.3.b would be revised to replace specific guidance 
    with a reference to the Containment Leakage Rate Testing Program. The 
    footnote addressing the exemption to Appendix J regarding testing the 
    air locks prior to establishing containment integrity would be 
    maintained in the Containment Leakage Rate Testing Program.
        e. Containment Vessel Structural Integrity: Surveillance 
    Requirement 4.6.1.6 would be revised to replace specific guidance with 
    a reference to the Containment Leakage Rate Testing Program.
        f. Containment Ventilation System: Limiting Condition for Operation 
    3.6.1.7, Action b. would be revised to replace specific guidance with a 
    reference to the Containment Leakage Rate Testing Program. Surveillance 
    Requirement 4.6.1.7.1 would be revised to replace specific guidance 
    with a reference to the Containment Leakage Rate Testing Program.
        g. Containment Enclosure Building: Limiting Condition for Operation 
    3.6.5.3 and Surveillance Requirement 4.6.5.3 would be revised to 
    include a reference to the requirements in the Containment Leakage Rate 
    Testing Program.
        3. Bases: Sections 3/4.6.1.2, Containment Leakage; 3/4.6.1.7, 
    Containment Ventilation System; and 3/4.6.5.3, Containment Enclosure 
    Building Structural Integrity, would be revised to reflect the above 
    changes including a reference to the Containment Leakage Rate Testing 
    Program. In addition, a statement would be added to Section 3/4.6.1.2 
    to clarify the operability of containment regarding allowable leakage 
    rates.
        4. Administrative Controls: Section 6.15 would be added to 
    establish a Containment Leakage Rate Testing Program, as specified in 
    Regulatory Guide 1.163, dated September 1995.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the
    
    [[Page 44360]]
    
    licensee has provided its analysis of the issue of no significant 
    hazards consideration. The NRC staff has reviewed the licensee's 
    analysis against the standards of 10 CFR 50.92(c). The NRC staff's 
    review is presented below.
        A. The changes do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated (10 
    CFR 50.92(c)(1)) because the proposed changes merely revise the 
    testing criteria for containment penetrations. The revised criteria 
    will be based on the guidance in Regulatory Guide 1.163, 
    ``Performance-Based Containment Leak-Test Program.''
        This guidance allows for the use of relaxed testing frequencies 
    for containment penetrations that have performed satisfactorily on a 
    historical basis.
        To support consideration of Option B to Appendix J, the NRC 
    staff reviewed the potential impact of performance-based testing 
    frequencies for containment penetrations. The NRC staff review is 
    documented in NUREG-1493 ``Performance-Based Containment Leak-Test 
    Program.'' One of the staff's conclusions was that reducing the 
    frequency of Type A tests (Integrated Leak Rate Tests) from three 
    per 10 years to one per 10 years leads to a marginal increase in 
    risk. For Type B and C testing (Local Leak Rate Tests), the change 
    in testing frequency will not have significant impact since, under 
    existing requirements, leakage contributes less than 0.1 percent of 
    the overall accident risk. The use of a performance-based testing 
    program will continue to provide assurance that the accident 
    analysis assumptions remain bounding.
        B. The changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated 
    (10 CFR 50.92(c)(2)) because they do not affect the manner by which 
    the facility is operated or involve changes to structures, systems, 
    or components that affect the operational characteristics of the 
    facility. The changes merely revise the testing criteria for the 
    containment penetrations, and establish a Containment Leakage Rate 
    Testing Program to ensure that the performance history of each 
    penetration is satisfactory prior to changing any test frequency. 
    Since there is no change to the facility or the way in which the 
    facility is operated, there is no possibility of creating a new or 
    different kind of accident than previously analyzed.
        C. The changes do not involve a significant reduction in a 
    margin of safety (10 CFR 50.92(c)(3)). During the development of 10 
    CFR Part 50, Appendix J, Option B, the NRC staff determined the 
    reduction in safety associated with the implementation of the 
    performance-based testing program. The staff concluded that reducing 
    the frequency of Type A tests (Integrated Leak Rate Tests) from 
    three per 10 years to one per 10 years would have an imperceptible 
    impact upon risk. For Type B and C testing (Local Leak Rate Tests), 
    the change in testing frequency will not have significant impact 
    since this leakage contributes less than 0.1 percent of the overall 
    risk based on the existing regulations. The use of Option B will 
    have minimal impact on the radiological release rates since most 
    penetration leakage is well below the specified limits. The staff 
    noted that the accident risk is relatively insensitive to 
    containment leakage rate because accident risk is dominated by 
    accident sequences that result in failure of or bypass of the 
    containment. The use of a performance-based testing program will 
    continue to provide assurance that the accident analysis assumptions 
    remain bounding.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, NH 03833
        Attorney for licensee: Lillian M. Cuoco, Esquire, Northeast 
    Utilities Service Company, Post Office Box 270, Hartford CT 06141-0270
        NRC Project Director: Phillip F. McKee
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun 
    Station, Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: May 17, 1996
        Description of amendment request: The proposed amendment would 
    revise the technical specifications (TS) to relocate the operability 
    requirements for shock suppressors (snubbers) from the TS to the 
    Updated Safety Analysis Report (USAR) and incorporate snubber 
    examination and testing requirements into TS 3.3.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change will relocate operability requirements for 
    shock suppressors (snubbers) from the Technical Specifications (TS) 
    to the Updated Safety Analysis Report (USAR) and/or plant 
    procedures. On July 16, 1993, the NRC issued a Final Policy 
    Statement on Technical Specification Improvements for Nuclear Power 
    Reactors. The Final Policy Statement contains four criteria which 
    can be used to determine which constraints on the design and 
    operation of nuclear power plants are appropriate for inclusion in 
    TS. The NRC has incorporated these criteria into 10 CFR 50.36, 
    ``Technical specifications.'' Snubbers do not meet any of the four 
    criteria for inclusion as a Limiting Condition for Operations within 
    the TS, and therefore it is proposed that these requirements be 
    relocated from the TS. The proposed change would not reduce or 
    revise any of the current requirements for snubber operability, only 
    relocate the requirements. Any changes to the requirements contained 
    in the USAR and/or plant procedures can be made without NRC approval 
    only when the changes meet the criteria of 10 CFR 50.59. Changes to 
    the snubber operability requirements that do not meet the criteria 
    of 10 CFR 50.59 must be approved by the NRC by license amendment. 
    Therefore, the relocation of the requirements on snubber operability 
    from the TS to the USAR does not increase the probability or 
    consequences of any accident previously analyzed.
        The proposed change also deletes sections of the TS which are 
    redundant or in conflict with the American Society of Mechanical 
    Engineers (ASME) Boiler and Pressure Vessel Code. Snubbers are 
    required to be examined and tested in accordance with ASME Section 
    XI by 10 CFR 50.55a. The proposed change will ensure that the TS 
    implement ASME Section XI examination and testing requirements for 
    snubbers in accordance with 10 CFR 50.55a. Where differences between 
    the deleted sections of the TS and ASME Section XI requirements 
    exist, the Section XI requirements are similar or more conservative 
    than the TS. For example, although the functional test sample size 
    differs between the methodologies, both ensure that a very high 
    percentage of the snubbers in the plant are operable within 
    acceptance limits. Therefore, the proposed revision does not reduce 
    the effectiveness of snubber examination and testing.
        The proposed change would not reduce the operability 
    requirements, acceptance criteria, or examination and testing of 
    snubbers. Therefore, the proposed change would not increase the 
    probability or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        There will be no physical alterations to the plant 
    configuration, changes to setpoint values, or changes to the 
    implementation of setpoints or limits as a result of this proposed 
    change.
        The proposed change deletes duplicate or conflicting 
    requirements between the TS and the ASME Section XI. In these areas, 
    the proposed deletions would remove the TS requirements and testing 
    would be conducted in accordance with ASME Section XI as directed by 
    10 CFR 50.55a. Although the requirements of ASME Section XI differ 
    from the TS in some cases, the differences do not decrease the 
    effectiveness of testing and examination as compared to the TS 
    requirements. Other areas, such as snubber operability requirements 
    and service life monitoring, which are presently addressed by TS, 
    but are not covered under ASME Section XI, will be maintained in the 
    USAR so that these requirements cannot be deleted without NRC 
    approval.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change does not reduce the operability, 
    examination, or testing requirements for snubbers. Snubbers will 
    still be required to meet the requirements of ASME Section XI and 10 
    CFR 50.55a except where specific written relief has been granted by 
    the NRC. Therefore, the proposed change does not involve a 
    significant reduction in a margin of safety.
    
    [[Page 44361]]
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102
        Attorney for licensee: Perry D. Robinson, Winston & Strawn, 1400 L 
    Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William H. Bateman
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun 
    Station, Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: May 20, 1996
        Description of amendment request: The proposed amendment would 
    revise the technical specifications (TS) to clarify surveillance test 
    requirements of TS 3.1, Tables 3-1, 3-2, 3-3, 3-3A, and 3-5.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The changes to the Table of Contents are administrative in 
    nature to reflect the removal of incore instrumentation 
    (Specification 2.10.3) from the TS by Amendment 167 and for 
    consistency. Amendment 169 inadvertently reinserted incore 
    instrumentation back into the Table of Contents.
        The change to Specification 2.1.7(1)b is necessary because the 
    requirement to test the signal to alarm meter relay located in 
    Specification 3.1, Table 3-3, Item 6 is being deleted. The test, 
    which verifies the high and low pressurizer level alarm settings and 
    the pressurizer heater cutout function is unnecessary. Operating 
    experience has shown that a shiftly pressurizer level verification 
    as proposed for Specification 3.1, Table 3-3, Item 6.a is sufficient 
    to detect any level deviation and verify that operation is within 
    safety analyses assumptions. The level alarms serve as early warning 
    devices but do not provide an accident mitigation function. 
    Replacing the monthly test with a channel check is in accordance 
    with NUREG-1432, Combustion Engineering (CE), Standard Technical 
    Specifications (STS), Surveillance Requirement (SR) 3.3.11.1 (post 
    accident monitoring instrumentation). The monthly channel check 
    supplements the shiftly level verification.
        The Basis of Specification 3.1 is revised to clarify 
    expectations regarding a channel check of channels that are normally 
    off scale when the surveillance is required. In this situation, the 
    channel check only verifies that they are off scale in the same 
    direction. Off scale low current loop channels are verified to be 
    reading at the bottom of the range and not failed downscale. These 
    statements are taken from the Bases of CE STS SR 3.3.4.1 Engineered 
    Safety Features Actuation System (ESFAS) Instrumentation (Analog).
        In addition, the Basis of Specification 3.1 is revised to 
    clarify that power operated relief valve (PORV) actuation is not 
    required during the channel functional test of the PORV low 
    temperature setpoint (Table 3-3, Item 18.a). PORV actuation is not 
    required because it could depressurize the reactor coolant system. 
    This clarification is modeled after a similar statement from the 
    Bases of SR 3.4.12.6 (Low Temperature Overpressure Protection (LTOP) 
    System) of the CE STS.
        Changing Specification 3.1, Tables 3-1, 3-2, 3-3, and 3-3A by 
    using defined terms to enable the Surveillance Method to match the 
    Surveillance Function is an administrative change designed to 
    simplify the tables. Removal of the extraneous text does not alter 
    the surveillance because the defined terms are equivalent in meaning 
    to the deleted text.
        The reordering of several items in the tables into a Check-Test-
    Calibrate sequence adds consistency to the tables. Text revisions in 
    the Channel Description or Surveillance Function columns of Tables 
    3-1 and 3-2 add clarity and/or consistency. Footnote No. 1 in Table 
    3-1 concerning the bistable trip tester was deleted because it is 
    unnecessary.
        The Surveillance Function of Table 3-1, Item 1.c (Power Range 
    Safety Channels) is being changed to ``Test'' from ``Calibrate and 
    Test.'' It is not necessary for Item 1.c to require both because 
    Item 1.b already requires the power range safety channel adjustment 
    (calibration) to be performed daily. As stated in the Basis of 
    Specification 3.1, ``The minimum calibration frequencies of once-
    per-day for the power range safety channels, ...are considered 
    adequate.'' To further clarify the issue, the Basis of Specification 
    3.1 is being revised to note that the daily calibration is a heat 
    balance adjustment only.
        Changing Table 3-1, Item 4 (Thermal Margin/Low Pressure (TM/LP)) 
    to use the defined term CHANNEL CALIBRATION will allow OPPD to relax 
    the current TM/LP calibration requirements with a negligible impact 
    on safety. Calibration of the temperature input and pressure input 
    will still require calibration to known standards (i.e., resistance 
    and pressure), but will allow the calibrations to be done separately 
    instead of coincidently. The channel functional test that follows 
    the channel calibration verifies proper function of the TM/LP 
    circuitry.
        Removing the word ``Instruments'' from the Channel Description 
    of Table 3-2, Item 14 makes the Channel Description consistent with 
    the Surveillance Method. Table 3-2, Item 14 is not intended to 
    verify safety injection tank (SIT) instrumentation operability but 
    rather that the parameters level and pressure are within limits. 
    Generic Letter (GL) 93-05, Item 7.4, states that the operability of 
    SIT instrumentation is not directly related to the capability of a 
    SIT to perform its safety function. GL 93-05 concludes that the 
    surveillance should only confirm that the parameters defining SIT 
    operability are within their specified limits.
        Items 22 & 24 are being added to Table 3-2 to clearly state the 
    requirement for testing manual actuation of the Engineered Safety 
    Features (ESF) channels for Off-site Power Low Signal (OPLS) and 
    Auxiliary Feedwater. Although testing manual actuation of these 
    channels is done via the existing Specifications, the requirement to 
    do so is not clearly stated. Reordering Table 3-2, Item 23 into a 
    Check-Test-Calibrate Surveillance Frequency sequence adds clarity 
    and consistency.
        The addition of Footnote No. 7 to Table 3-2 clarifies that the 
    refueling frequency ESF channel functional test pertains to the 
    backup channels such as derived circuits and equipment that cannot 
    be tested when the plant is at power. Operating certain relays 
    during power operation could cause plant transients or equipment 
    damage.
        The revisions to Table 3-3, Item 6, clarify that pressurizer 
    level is the parameter to be verified and not the pressurizer level 
    instruments. The revision to Item 6.a is consistent with CE STS SR 
    3.4.9.1 (pressurizer water level). Reordering Item 6 into a Check-
    Test-Calibrate Surveillance Function sequence makes Item 6 
    consistent with the ordering of the other items in Table 3-3. The 
    requirement to test the signal to alarm meter relay currently 
    located in Specification 3.1, Table 3-3, Item 6.c is unnecessary. 
    Operating experience has shown that a shiftly pressurizer level 
    verification as proposed for Specification 3.1, Table 3-3, Item 6.a 
    is sufficient to detect any level deviation and verify that 
    operation is within safety analyses assumptions. Thus, the monthly 
    ``Test'' requirement will be replaced with a ``Check'' to supplement 
    the less formal but more frequent shiftly level verification of Item 
    6.a.
        Table 3-3, Items 21 (PORV Operation & Acoustic Position 
    Indication Channel) and 23 (Safety Valve Acoustic Position 
    Indication Channel) should be revised to a channel functional test 
    from a channel/circuit check. An oscillator and installed impactors 
    are used to generate noise signals and therefore, this surveillance 
    is more accurately described as a channel functional test rather 
    than a channel check.
        Table 3-3, Items 21 and 22 (PORV Block Valve Operation & 
    Position Indication) should have the requirement to verify operation 
    on the emergency power supply deleted. Permanent Class 1E power 
    supplies the PORV and PORV Block Valve. Therefore, verification of 
    PORV or PORV Block Valve operability while powered from the 
    emergency power supply system provides no additional benefit. 
    (Operability of the emergency power supply system is tested in 
    accordance with Specification 3.7.) The proposed revision is in 
    accordance with the exception for plants with a permanent Class 1E 
    power supply to these valves as stated in CE STS, SR 3.4.11.4.
        Deletion of the requirement of TS 3.2, Table 3-5, Item 15, to 
    test spent fuel pool surveillance coupons for a change in hardness 
    corrects an oversight in the Application for Amendment dated 
    December 7, 1992.
        As stated in the Safety Evaluation Report enclosed with 
    Amendment 155, ``Each
    
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    coupon, upon its removal from the mounting jacket, will be analyzed 
    according to the following tests:
        visual observation and photography
        neutron attenuation
        dimensional measurements (length, width, and thickness)
        weight and specific gravity.''
        The tests listed above are sufficient to detect degradation of 
    the Boral material and do not require that the surveillance coupons 
    be tested for hardness.
        Based on the above discussion, the proposed changes clarify and 
    standardize existing surveillance requirements, remove redundant 
    requirements, correct minor oversights from previous amendment 
    requests or are in accordance with CE STS. Thus, none of the 
    requested changes involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed revisions will not result in any physical 
    alterations to the plant configuration, changes to setpoint values, 
    or changes to the application of setpoints or limits. Therefore, the 
    proposed changes do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed changes clarify existing surveillance requirements, 
    remove redundant requirements, correct minor oversights from 
    previous amendment requests or are in accordance with CE STS. Thus, 
    none of the requested changes involves a significant reduction in a 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: W. Dale Clark Library, 215 
    South 15th Street, Omaha, Nebraska 68102
        Attorney for licensee: Perry D. Robinson, Winston & Strawn, 1400 L 
    Street, N.W., Washington, DC 20005-3502
        NRC Project Director: William H. Bateman
    
    Pennsylvania Power and Light Company, Docket No. 50-388 Susquehanna 
    Steam Electric Station, Unit 2, Luzerne County, Pennsylvania
    
        Date of amendment request: May 20, 1996, as supplemented by letter 
    dated July 25, 1996
        Description of amendment request: This amendment request would 
    modify the Technical Specifications for the unit by: changing the 
    Minimum Critical Power Ratio safety limit values, adding a reference to 
    reflect the use of the ANF-B Critical Power Correlation, and modifying 
    the associated Bases.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The change to the ANFB correlation and corresponding MCPR Safety 
    Limits does not physically change the plant systems, structures, or 
    components. Thus, the probability of an event evaluated in the SAR 
    is not increased. The acceptance criterion for the MCPR Safety Limit 
    (i.e., 99.9% of the fuel rods expected to avoid boiling transition) 
    is not changed. Only the methodology used to demonstrate compliance 
    is changed.
        Therefore, the consequences of anticipated operational 
    occurrences (which must show the Safety Limit is not violated) are 
    not changed. Results of incorporating this change will not 
    significantly increase the probability or consequences of an 
    accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        As stated above, this methodology change does not impact the 
    acceptance criteria for the MCPR Safety Limits and does not 
    physically change the plant systems, structures, or components. 
    Since no changes to the physical plant are being made, this change 
    does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        A cycle specific MCPR Safety Limit analysis was performed by SPC 
    [Siemens Power Corporation]. This analysis used NRC approved methods 
    described in the SPC report: ANF-524(P)(A), Revision 2 and 
    Supplement 1, Revision 2. The MCPR Safety Limit value is calculated 
    such that at least 99.9% of the fuel rods are expected to avoid 
    boiling transition during normal operation or anticipated operation 
    occurrences. Both the existing analysis using XN-3 and the new 
    analysis using ANFB utilize NRC approved methods to accomplish this 
    same objective. Therefore, the change to an ANFB based Safety Limit 
    does not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
        TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche 
    Peak Steam Electric Station (CPSES), Units 1 and 2, Somervell 
    County, Texas
        Date of amendment request: July 31, 1996
        Brief description of amendments: Based on analyses of the core 
    configuration and expected operation for CPSES Unit 1, Cycle 6, the 
    proposed amendments would revise core safety limit curves and 
    Overtemperature N-16 reactor trip setpoints. In addition, the TU 
    Electric Small Break LOCA Topical Report on the Core Operating Limits 
    Report Technical Specification is incorporated. The topical report 
    change is applicable to both Units.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1.a. Revision to the Unit 1 Core Safety Limits
        Analyses of reactor core safety limits are required as part of 
    reload calculations for each cycle. TU Electric has performed the 
    analyses of the Unit 1, Cycle 6 core configuration to determine the 
    reactor core safety limits. The methodologies and safety analysis 
    values result in new operating curves which, in general, permit 
    plant operation over a similar range of acceptable conditions. This 
    change means that if a transient were to occur with the plant 
    operating at the limits of the new curve, a different temperature 
    and power level might be attained than if the plant were operating 
    within the bounds of the old curves. However, since the new curves 
    were developed using NRC approved methodologies which are wholly 
    consistent with and do not represent a change in the Technical 
    Specification BASES for safety limits, all applicable postulated 
    transients will continue to be properly mitigated. As a result, 
    there will be no significant increase in the consequences, as 
    determined by accident analyses, of any accident previously 
    evaluated.
        1.b. Revision to Unit 1 Overtemperature N-16 Reactor Trip 
    Setpoints, Parameters and Coefficients
        As a result of changes discussed, the Overtemperature N-16 
    reactor trip setpoint has been recalculated. These trip setpoints 
    help ensure that the core safety limits are maintained and that all 
    applicable limits of the safety analysis are met.
        Based on the calculations performed, the safety analysis value 
    for Overtemperature N-16 reactor trip setpoint has changed. This 
    essentially means if a transient were to occur, the actual 
    temperature and power level achievable prior to initiating a reactor 
    trip could be slightly higher. However, the analyses performed show 
    that, using the TU Electric methodologies, all applicable limits of 
    the safety analysis are met. This setpoint
    
    [[Page 44363]]
    
    provides a trip function which allows the mitigation of postulated 
    accidents and has no impact on accident initiation. Therefore, the 
    changes in safety analysis values do not involve an increase in the 
    probability of an accident and, based on satisfying all applicable 
    safety analysis limits, there is no significant increase in the 
    consequences of any accident previously evaluated.
        In addition, sufficient operating margin has been maintained in 
    the overtemperature setpoint such that the risk of turbine runbacks 
    or reactor trips due to upper plenum flow anomalies or other 
    operational transients will be minimized, thus reducing potential 
    challenges to the plant safety systems.
        1.c. Incorporation of TU Electric Small Break LOCA Topical 
    Report, RXE-95-0001-P.
        TU Electric has submitted the topical report ``Small Break Loss 
    of Coolant Accident Analysis Methodology,'' RXE-95-001-P and plans 
    to use the report to support Unit 1 Cycle 6. In order to accomplish 
    this activity, it is necessary to include the topical report in the 
    list of NRC-approved methodologies in Technical Specification 
    6.9.1.6b. Use of this topical report is contingent upon NRC 
    approval; therefore, inclusion of this report in Section 6 of the 
    Technical Specifications is administrative in nature and does not 
    change the probability or consequences of an accident.
        2. The proposed changes involve the use of revised safety 
    analysis values and the calculation of new reactor core safety 
    limits and reactor trip setpoints. As such, the changes play an 
    important role in the analysis of postulated accidents but none of 
    the changes effect plant hardware or the operation of plant systems 
    in a way that could initiate an accident. Therefore, the proposed 
    changes do not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. In reviewing and approving the methods used for safety 
    analyses and calculations, the NRC has approved the safety analysis 
    limits which establish the margin of safety to be maintained. While 
    the actual impact on safety is discussed in response to question 1, 
    the impact on margin of safety is discussed below:
        3.a.
        Revision to the Unit 1 Reactor Core Safety Limits
        The TU Electric reload analysis methods have been used to 
    determine new reactor core safety limits. All applicable safety 
    analysis limits have been met. The methods used are wholly 
    consistent with Technical Specification BASES 2.1 which is the bases 
    for the safety limits. In particular, the curves assure that for 
    Unit 1, Cycle 6, the calculated DNBR is no less than the safety 
    analysis limit and the average enthalpy at the vessel exit is less 
    than the enthalpy of saturated liquid. The acceptance criteria 
    remains valid and continues to be satisfied; therefore, no change in 
    a margin of safety occurs.
        3.b. Revision to Unit 1 Overtemperature N-16 Reactor Trip 
    Setpoints, Parameters and Coefficients
        Because the reactor core safety limits for CPSES Unit 1, Cycle 6 
    are recalculated, the Reactor Trip System instrumentation setpoint 
    values for the Overtemperature N-16 reactor trip setpoint which 
    protect the reactor core safety limits must also be recalculated. 
    The Overtemperature N-16 reactor trip setpoint helps prevent the 
    core and Reactor Coolant System from exceeding their safety limits 
    during normal operation and design basis anticipated operational 
    occurrences. The most relevant design basis analysis in Chapter 15 
    of the CPSES Final Safety Analysis Report (FSAR) which is affected 
    by the change in the safety analysis value for the CPSES Unit 1 
    Overtemperature N-16 reactor trip setpoint is the Uncontrolled Rod 
    Cluster Control Assembly Bank Withdrawal at Power (FSAR Section 
    15.4.2). This event has been re-analyzed with the revised safety 
    analysis value for the Overtemperature N-16 reactor trip setpoint to 
    demonstrate compliance with event specific acceptance criteria. 
    Because all event acceptance criteria are satisfied, there is no 
    degradation in a margin of safety.
        The nominal Reactor Trip System instrumentation setpoints values 
    for the Overtemperature N-16 reactor trip setpoint (Technical 
    Specification Table 2.2-1) are determined based on a statistical 
    combination of all of the uncertainties in the channels to arrive at 
    a total uncertainty. The total uncertainty plus additional margin is 
    applied in a conservative direction to the safety analysis trip 
    setpoint value to arrive at the nominal and allowable values 
    presented in Technical Specification Table 2.2-1. Meeting the 
    requirements of Technical Specification Table 2.2-1 assures that the 
    Overtemperature N-16 reactor trip setpoint assumed in the safety 
    analyses remains valid. The CPSES Unit 1, Cycle 6 Overtemperature N-
    16 reactor trip setpoint is different from previous cycles which 
    provides more operational flexibility to withstand mild transients 
    without initiating automatic protective actions. Although the 
    setpoint is different, the Reactor Trip System instrumentation 
    setpoint values for the Overtemperature N-16 reactor trip setpoint 
    are consistent with the safety analysis assumption which has been 
    analytically demonstrated to be adequate to meet the applicable 
    event acceptance criteria. Thus, there is no reduction in a margin 
    of safety.
        3.c. Revise 6.9.1.6b to include Topical Report RXE-95-001-P, 
    ``Small Break Loss of Coolant Accident Methodology''
        TU Electric has submitted the topical report ``Small Break Loss 
    of Coolant Accident Analysis Methodology,'' RXE-95-001-P and plans 
    to use the report to support Unit 1 Cycle 6. In order to accomplish 
    this activity, it is necessary to include the topical report in the 
    list of NRC-approved methodologies in Technical Specification 
    6.9.1.6b. Use of this topical report is contingent upon NRC 
    approval; therefore, inclusion of this report in Section 6 of the 
    Technical Specifications is administrative in nature and does not 
    reduce the margin of safety.
        Using the NRC approved TU Electric methods, the reactor core 
    safety limits are determined such that all applicable limits of the 
    safety analyses are met. Because the applicable event acceptance 
    criteria continue to be met, there is no significant reduction in 
    the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, TX 76019
        Attorney for licensee: George L. Edgar, Esq., Morgan, Lewis and 
    Bockius, 1800 M Street, N.W., Washington, DC 20036
        NRC Project Director: William D. Beckner
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak 
    Steam Electric Station (CPSES), Units 1 and 2, Somervell County, 
    Texas
    
        Date of amendment request: July 31, 1996
        Brief description of amendments: The proposed amendments would 
    revise the Technical Specifications by (1) changing the battery charger 
    ratings; (2) by clarifying the meaning of the term ``associated 
    inverter''; and by (3) deleting the protection channel and the vital 
    bus ratings for the instrument busses identified for Mode 1 through 4. 
    These changes are associated with a plant modification in which the 
    inverters and battery chargers are being replaced and an installed 
    spare inverter is being added for each safety train. These changes are 
    equally applicable to CPSES Units 1 and 2.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. DO THE PROPOSED CHANGES INVOLVE A SIGNIFICANT INCREASE IN THE 
    PROBABILITY OR CONSEQUENCES OF AN ACCIDENT PREVIOUSLY EVALUATED?
        CHANGE TO IDENTIFY BATTERY CHARGER RATINGS
        The first proposed change replaces the test amperes with the 
    design value for the replacement battery charger and allows a 
    voltage range (greater than or equal to 130 volts) instead of a 
    single value. The intent of the surveillance requirement or the 
    surveillance frequency is not changed. The replacement inverters and 
    battery chargers will continue to provide the capacity needed to 
    perform the required safety functions. The revised surveillance will 
    continue to assure that the battery chargers are capable of 
    performing as designed. Therefore this change does not impact the 
    probability or the consequences of an accident previously evaluated.
        CLARIFICATION TO DEFINE ASSOCIATED INVERTER
        The second proposed change adds a foot note to clarify the term 
    ``associated inverter'' by describing it as, ''... the dedicated 
    inverter or installed spare inverter.'' Also the Bases
    
    [[Page 44364]]
    
    for this specification is revised to reflect the basis for this 
    change. This change allows use of an installed spare inverter (for 
    each train) having the capability to energize the Instrument Bus for 
    the protection channel or the vital bus. Procedural controls and 
    interlocks ensure that the spare is available to feed only one of 
    the protection channel or vital bus Instrument Bus at a time, in the 
    event the dedicated inverter is not available. Procedural controls 
    and interlocks also ensure that the installed spare inverter is fed 
    from the same power source as that of the dedicated inverter not in 
    service and whose loads are being fed by the spare inverter. This 
    proposed design only allows the spare inverter for a safety train to 
    be manually aligned to replace only one of the four inverters in 
    that train at a time.
        The installation of a spare inverter for each train and the 
    associated design configuration increases the availability of 
    energized Instrument Bus for the protection channel and vital bus. 
    These changes do not involve an increase in the probability or 
    consequences of an accident previously evaluated.
        DELETION OF THE PROTECTION CHANNEL AND VITAL BUS RATINGS FOR 
    INSTRUMENT BUS
        The third proposed change deletes specifying of the protection 
    channel and vital bus KVA ratings for the Instrument Bus. The 
    ratings of inverter that feeds these instrument buses are being 
    described in other Licensing Bases Documents or Design Basis 
    Documents. There is no change proposed to the intent of the action 
    statements.
        This is considered an administrative change and does not impact 
    the probability or consequences of an accident previously evaluated.
        2. DO THE PROPOSED CHANGES CREATE THE POSSIBILITY OF A NEW OR 
    DIFFERENT KIND OF ACCIDENT FROM ANY ACCIDENT PREVIOUSLY EVALUATED?
        CHANGE TO IDENTIFY BATTERY CHARGER RATINGS
        Replacing the inverters and battery chargers and changing the 
    parameters of the battery charger surveillance test to match the 
    replacement chargers does not alter the functional modes of this 
    portion of the design and does not result in any new failure modes. 
    As such, it does not create the possibility of a new or different 
    accident from any previously evaluated.
        CLARIFICATION TO DEFINE ASSOCIATED INVERTER
        The second proposed change allows use of an installed spare 
    inverter for each train to energize the one of the Instrument Bus 
    for the protection channel and vital bus at a time for the 
    respective safety train while its dedicated inverter is not 
    available. The spare inverter is such that it has the capability to 
    support the maximum load for the protection channel or vital bus. 
    Manually aligning the installed inverter to replace on[e] of the 
    dedicated inverters is essentially equivalent to a repair activity 
    which replaces a faulted inverter with a new inverter. In addition, 
    procedural controls and interlocks are provided to ensure the proper 
    alignment of the installed spare when it is used. The proposed 
    changes do not create the possibility of a new or different accident 
    from any previously evaluated.
        DELETION OF THE PROTECTION CHANNEL AND VITAL BUS RATINGS FOR 
    INSTRUMENT BUS
        The third proposed change as discussed earlier does not change 
    intent of the Technical Specifications action statements. This is an 
    administrative change which does not introduce new failure modes and 
    has no new or different accidents from any previously evaluated are 
    created.
        3. DO THE PROPOSED CHANGES INVOLVE A SIGNIFICANT REDUCTION IN 
    MARGIN OF SAFETY?
        The relevant Technical Specification sections proposed for 
    changes: (1) ensure that the battery charger is capable of charging 
    the battery by performing the surveillance at 18 month frequency; 
    (2) establish operability requirements of the Instrument Bus for the 
    protection channel and vital bus in MODES 1 through 6; and (3) 
    identify the actions required for not meeting item 2.
        These proposed changes do not alter the intent of the above 
    requirements; however replacement of the currently installed 
    inverters with inverters which are expected to be more reliable and 
    available and the addition of a spare inverter per safety train to 
    energize Instrument Bus for protection channel and vital bus does 
    increase the reliability of the instrument busses for the train. 
    Allowing credit for this spare inverter in meeting the operability 
    requirements of Instrument Bus for the protection channel and vital 
    bus, minimize potential plant shutdowns due to non-energized 
    instrument from its dedicated inverter. These changes do not involve 
    a significant reduction in margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, TX 76019
        Attorney for licensee: George L. Edgar, Esq., Morgan, Lewis and 
    Bockius, 1800 M Street, N.W., Washington, DC 20036
        NRC Project Director: William D. Beckner
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, 
    Vermont Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of amendment request: August 9, 1996
        Description of amendment request: The proposed amendment would 
    revise the Safety Limits for Minimum Critical Power Ratio (MCPR) based 
    upon a Vermont Yankee plant and cycle specific analysis, performed by 
    General Electric. The revised MCPR Safety Limits are needed to 
    accommodate Vermont Yankee's core design for upcoming refueling cycle 
    number 19. Specifically, the MCPR Safety Limits of 1.07 and 1.08 in the 
    Vermont Yankee Technical Specifications (TS) section 1.1.A are proposed 
    to be increased to 1.10 and 1.12 for two loop and single loop 
    operation, respectively.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) The Safety Limit Minimum Critical Power Ratio (MCPR) is 
    defined to ensure that during normal operation and Anticipated 
    Operational Transients (AOTs), at least 99.9% of the fuel rods in 
    the core do not experience transition boiling. Core MCPR operating 
    limits are developed to ensure these Safety Limits are maintained in 
    the event of the worst case transient. Since the Safety Limit MCPR 
    will be maintained at all times, operation under the proposed 
    changes will ensure at least 99.9% of the fuel rods in the core do 
    not experience transition boiling and no significant radiological 
    release will result. Therefore, this Safety Limit MCPR change does 
    not affect the probability or consequences of a previously evaluated 
    accident.
        (2) The proposed changes do not involve any new modes of 
    operation or any plant modifications. Establishment and monitoring 
    of the operating limits will continue as per established procedure. 
    The proposed changes to these limits do not result in the creation 
    of any new precursors to an accident. Therefore, the proposed change 
    does not create the possibility of a new or a different kind of 
    accident from any previously analyzed.
        (3) The Safety Limit MCPR values were evaluated by General 
    Electric based upon a cycle specific Vermont Yankee analysis, using 
    NRC approved methods. The resulting limits are more conservative 
    than the previous generic limits and will continue to assure that at 
    least 99.9% of the fuel rods in the core do not experience 
    transition boiling during analyzed transients. This acceptance 
    criteria ensures the safety design limit of ``no damage to a nuclear 
    system process barrier shall result from forces associated with 
    AOTs.'' Therefore, the implementation of the proposed change does 
    not involve a significant reduction in [a] margin of safety.
        The NRC staff has reviewed the licensee's analysis. The staff notes 
    that, although the proposed change does not involve a plant 
    modification, the reason for the proposed higher safety limit MCPRs is 
    the cycle-specific core design and the local power distribution in the 
    slightly higher enriched fresh GE-9B fuel bundles. This new fuel will 
    be loaded during the September/October 1996 refueling outage. In 
    conjunction with the proposed safety limit MCPRs and the core operating 
    limits determined in accordance with Vermont Yankee TS 6.7.A.4, the new 
    fuel load will not involve a significant increase in the probability or 
    consequences of an
    
    [[Page 44365]]
    
    accident previously evaluated nor a significant reduction in a margin 
    of safety. In addition, the new fuel load does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated. Based on this review, it appears that the three 
    standards of 50.92(c) are satisfied. Therefore, the NRC staff proposes 
    to determine that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301
        Attorney for licensee: R. K. Gad, III, Ropes and Gray, One 
    International Place, Boston, MA 02110-2624
        NRC Project Director: Jocelyn A. Mitchell, Acting Director
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of application for amendment: May 1, 1996
        Brief description of amendment: The proposed amendment will modify 
    the definition of ``Core Alteration,'' and the limiting condition for 
    operation, Surveillance conditions and Bases section associated with 
    Technical Specification 3.7.C, ``Secondary Containment.''
        Date of issuance: August 12, 1996
        Effective date: August 12, 1996
        Amendment No.: 166
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 5, 1996 (61 FR 
    28606) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 12, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location:  Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson 
    Steam Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of application for amendment: July 17, 1995, as supplemented 
    May 2, 1996, and July 1, 1996.
        Brief description of amendment: The change revises technical 
    specification (TS) section 3.8 to specify that the spent fuel building 
    refueling filter fan and at least one containment purge fan shall be 
    shown to operate within plus or minus 10 percent of the design flow.
        Date of issuance: August 6, 1996
        Effective date: August 6, 1996
        Amendment No. 172
        Facility Operating License No. DPR-23. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: September 13, 1995 (60 
    FR 47615). The May 2, and July 1, 1996, letters provided clarifying 
    information that did not affect the proposed no significant hazards 
    consideration. The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 6, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson 
    Steam Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of application for amendment: June 6, 1996
        Brief description of amendment: The amendment revises technical 
    specifications (TS) Section 4.2.3 to allow the licensee to defer the 
    ultrasonic inspection of the reactor coolant pump flywheel for one 
    operating cycle.
        Date of issuance: August 9, 1996
        Effective date: August 9, 1996
        Amendment No. 173
        Facility Operating License No. DPR-23. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 3, 1996 (61 FR 
    34888) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 9, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of application for amendment: May 31, 1996
        Brief description of amendment: The amendment revises Technical 
    Specifications (TS) Table 3.3-7, Seismic Monitoring Instrumentation, 
    and TS Table 4.3-4, Seismic Monitoring Instrumentation Surveillance 
    Requirements, to correct the location described for one of the three 
    Triaxial Peak Accelerograph recorders.
        Date of issuance: August 7, 1996
        Effective date: August 7, 1996
        Amendment No. 66
        Facility Operating License No. NPF-63. Amendment revises the 
    Technical Specifications
        Date of initial notice in Federal Register: July 3, 1996 (61 FR 
    34888) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 7, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of application for amendments: April 16, 1996
        Brief description of amendments: The amendments revise the 
    Technical
    
    [[Page 44366]]
    
    Specifications (TSs) to eliminate selected response time testing 
    requirements based on analyses performed by the Boiling Water Reactor 
    Owners' Group as documented in NEDO-32291. The affected TS sections are 
    3/4.3.1, ``Reactor Protection System Instrumentation;'' 3/4.3.2, 
    ``Isolation Actuation Instrumentation;'' and 3/4.3.3, ``Emergency Core 
    Cooling System Actuation Instrumentation.''
        Date of issuance: August 14, 1996
        Effective date: Immediately, to be implemented within 60 days.
        Amendment Nos.: 114 and 99
        Facility Operating License Nos. NPF-11 and NPF-18: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 22, 1996 (61 FR 
    25702) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 14, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
    
    Detroit Edison Company, Docket No. 50-341, Fermi-2, Monroe County, 
    Michigan
    
        Date of application for amendment: December 21, 1995
        Brief description of amendment: The amendment revises the Technical 
    Specifications (TS) to implement 10 CFR Part 50, Appendix J - Option B, 
    by referring to Regulatory Guide 1.163, ``Performance-Based Containment 
    Leak-Test Program.'' Specifically, changes have been made to TS Section 
    3/4.6.1.2, ``Primary Containment Leakage,'' TS 3/4.6.1.3, ``Primary 
    Containment Air Locks,'' TS 3/4.6.1.5, ``Primary Containment Structural 
    Integrity,'' TS 6.0, ``Administrative Controls,'' and their associated 
    Bases.
        Date of issuance: August 8, 1996
        Effective date: August 8, 1996, with full implementation within 45 
    days.
        Amendment No.: 108
        Facility Operating License No. NPF-43. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 28, 1996 (61 
    FR 7551) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 8, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Monroe County Library System, 
    3700 South Custer Road, Monroe, Michigan 48161
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: April 19, 1996, and supplements 
    dated May 10 and May 28, 1996.
        Brief description of amendments: The amendment changes the 
    Technical Specifications to address frequency extension on a periodic 
    basis, deletes separate notification requirements for an inoperable 
    startup transformer, and allows the operating residual heat removal 
    loop to be removed from operation, under certain conditions, during 
    refueling.
        Date of Issuance: August 6, 1996
        Effective Date: August 6, 1996
        Amendment Nos.: 189 and 183Facility Operating Licenses Nos. DPR-31 
    and DPR-41: Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: July 3, 1996 (61 FR 
    34892) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 6, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments: July 26, 1995, and supplemented 
    March 13, May 3, and May 9, 1996.
        Brief description of amendments: Change TS 6.9.1.7, Core Operating 
    Limits Report, resulting from a reanalysis of the small break loss-of-
    coolant accident for the Turkey Point Units using the NOTRUMP code 
    including the COSI safety injection (SI) condensation model.
        Date of issuance: August 13, 1996
        Effective date: August 13, 1996
        Amendment Nos. 190 and 184Facility Operating Licenses Nos. DPR-31 
    and DPR-41: Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: September 13, 1995 (60 
    FR 47618). The supplements dated March 13, May 3, and May 9, 1996 
    provided clarifying information that did not change the initial 
    proposed no significant hazards consideration determination. The 
    Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated August 13, 1996. No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Florida International 
    University, University Park, Miami, Florida 33199.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: May 1, 1996
        Brief description of amendments: The amendments changed the 
    technical specifications to implement 10 CFR Part 50, Appendix J, 
    Option B, by referring to Regulatory Guide 1.163, ``Performance-Based 
    Containment Leak-Test Program.'' Part of the requested change, that 
    regarding the frequency of leakage rate testing the normal containment 
    purge valves and the supplementary containment purge valves, was 
    denied.
        Date of issuance: August 13, 1996
        Effective date: August 13, 1996
        Amendment Nos.: 84 and 71
        Facility Operating License Nos. NPF-76 and NPF-80. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 5, 1996 (61 FR 
    28616) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 13, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy, Center, 
    Linn County, Iowa
    
        Date of application for amendment: November 30, 1995
        Brief description of amendment: The amendment implements the Option 
    I-D long-term stability solution and removes the existing SIL-380 Rev. 
    1-based specifications. In addition, the amendment requires a plant 
    scram be initiated should the plant enter natural circulation 
    conditions and prohibits restarting a recirculation pump while in 
    natural circulation. Finally, this amendment deletes Technical 
    Specification (TS) actions and surveillance requirements related to 
    core plate differential pressure noise while in single recirculation 
    pump operation (SLO).
        Date of issuance: August 7, 1996
        Effective date: August 7, 1996
        Amendment No.: 215
        Facility Operating License No. DPR-49: Amendment revised the 
    Technical Specifications.
    
    [[Page 44367]]
    
        Date of initial notice in Federal Register: March 13, 1996 (61 FR 
    10394) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 7, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, S. E., Cedar Rapids, Iowa 52401
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy, Center, 
    Linn County, Iowa
    
        Date of application for amendment: November 15, 1995, as 
    supplemented April 9, 1996
        Brief description of amendment: The amendment revises the 
    requirements for the End of Cycle Recirculation Pump Trip logic to 
    match more closely the assumptions applicable to the turbine trip 
    events for which it was installed. The surveillance requirements are 
    also revised, based on those same assumptions.
        Date of issuance: August 8, 1996
        Effective date: August 8, 1996
        Amendment No.: 216
        Facility Operating License No. DPR-49: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 22, 1996 (61 FR 
    1629) The April 9, 1996, submittal was clarifying in nature and did not 
    affect the no significant hazards determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated August 8, 1996. No significant hazards consideration comments 
    received: No.
        Local Public Document Room location:  Cedar Rapids Public Library, 
    500 First Street, S. E., Cedar Rapids, Iowa 52401
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy, Center, 
    Linn County, Iowa
    
        Date of application for amendment: January 18, 1996
        Brief description of amendment: The amendment revises the setpoint 
    at which the Reactor Water Cleanup (RWCU) system isolates, based on 
    reactor vessel water level. In particular, the amendment changes the 
    Group 5 isolation from isolating on ``reactor water level low'' to 
    ``reactor water level low-low.''
        Date of issuance: August 8, 1996
        Effective date: August 8, 1996, and shall be implemented prior to 
    startup from RFO 14.
        Amendment No.: 217
        Facility Operating License No. DPR-49: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 14, 1996 (61 
    FR 5814) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 8, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, S. E., Cedar Rapids, Iowa 52401
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments: January 12, 1996 (AEP:NRC:1233)
        Brief description of amendments: The amendments modify the 
    Technical Specifications to delete the surveillance requirement 
    demonstrating operability of the emergency power supply for the 
    pressurizer power operated relief valves and block valves.
        Date of issuance: August 15, 1996
        Effective date: August 15, 1996, with full implementation within 45 
    days
        Amendment Nos.: 211 and 196
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 28, 1996 (61 
    FR 7554) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 15, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  Maud Preston Palenske 
    Memorial Library, 500 Market Street, St. Joseph, Michigan 49085
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile 
    Point Nuclear Station, Unit 2, Oswego County, New York
    
        Date of application for amendment: February 7, 1996, as 
    supplemented July 26, 1996.
        Brief description of amendment: The amendment revises the operating 
    license, TSs and associated Bases to implement Option B ``Performance-
    Based Requirements'' of Appendix J to 10 CFR Part 50 for Type A, B, and 
    C leakage rate testing.
        Date of issuance: August 13, 1996
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 74
        Facility Operating License No. NPF-69: Amendment revises the 
    Technical Specifications and operating license.
        Date of initial notice in Federal Register: May 8, 1996 (61 FR 
    20849) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 13, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London County, 
    Connecticut
    
        Date of application for amendment: July 3, 1996
        Brief description of amendment: The amendment removes, on a one-
    time basis during the cycle 13 mid-cycle offload/reload activities, the 
    Technical Specification (TS) requirement that the boron concentration 
    in all filled portions of the reactor coolant system be ``uniform.'' 
    The requested change also adds a footnote indicating that it is 
    acceptable for the boron concentration of the water volumes in the 
    steam generators and the connecting piping to be as low as 1300 parts 
    per million. The TS Bases are also updated to reflect the one-time TS 
    change.
        Date of issuance: August 12, 1996
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment No.: 201
        Facility Operating License No. DPR-65. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 11, 1996 (61 FR 
    36583) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 12, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360, and Waterford Library, ATTN: Vince Juliano, 49 Rope 
    Ferry Road, Waterford, CT 06385
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: February 29, 1996
        Brief description of amendments: These amendments relocate 
    Specification 3/4.9.6, ``Refueling Platform,'' to the Susquehanna Steam 
    Electric Station Technical Requirements Manual, a document which is 
    controlled under the requirements of 10 CFR 50.59.
        Date of issuance: August 13, 1996
        Effective date: August 13, 1996
        Amendment Nos.: 159 and 130
    
    [[Page 44368]]
    
        Facility Operating License Nos. NPF-14 and NPF-22. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 10, 1996 (61 FR 
    15992) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 13, 1996. No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701.
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260, and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2, and 3, Limestone County, 
    Alabama
    
        Date of application for amendments: May 20, 1996 (TS 373)
        Brief description of amendment: The amendments incorpore the 
    guidance of Generic Letter 87-09 in the technical specifications, 
    allowing a 24-hour delay in implementing action requirements due to a 
    missed surveillance requirement.
        Date of issuance: August 5, 1996
        Effective Date: August 5, 1996
        Amendment Nos.: 230, 245 and 205
        Facility Operating License Nos. DPR-33, DPR-52 and DPR-68: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: June 19, 1996 (61 FR 
    31185) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 5, 1996. No significant 
    hazards consideration comments received: None
        Local Public Document Room location: Athens Public library, South 
    Street, Athens, Alabama 35611
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application for amendment: May 29, 1996
        Brief description of amendment: The amendment authorizes revision 
    of the Final Safety Analysis Report (FSAR) to incorporate a 
    modification to the facility that will reduce the single failure trip 
    potential for the main feedwater and bypass valves.
        Date of issuance: August 13, 1996
        Effective date: August 13, 1996
        Amendment No.: 115
        Facility Operating License No. NPF-30: The amendment revised the 
    Final Safety Analysis Report.
        Date of initial notice in Federal Register: July 3, 1996 (61 FR 
    34900) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 13, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Callaway County Public 
    Library, 710 Court Street, Fulton, Missouri 65251.
    
    Wisconsin Public Service Corporation, Docket No. 50-305, Kewaunee 
    Nuclear Power Plant, Kewaunee County, Wisconsin
    
        Date of application for amendment: June 4, 1996
        Brief description of amendment: The amendment revises the Technical 
    Specifications by reducing the surveillance test frequencies for the 
    radiation monitoring system (Table TS 4.1-1) and the control rods 
    (Table TS 4.1-3) in accordance with the guidance of Generic Letter 93-
    05, ``Line-Item Technical Specifications Improvements to Reduce 
    Surveillance Requirements for Testing During Power Operation,'' dated 
    September 27, 1993.
        Date of issuance: August 7, 1996
        Effective date: August 7, 1996
        Amendment No.: 125
        Facility Operating License No. DPR-43: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 3, 1996 (61 FR 
    34901) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 7, 1996. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: University of Wisconsin, 
    Cofrin Library, 2420 Nicolet Drive, Green Bay, Wisconsin 54311-7001
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: July 29, 1994, as superseded by letter 
    dated September 15, 1995, and subsequently supplemented by letters 
    dated March 8, 1996, April 18, 1996, June 14, 1996, and July 12, 1996.
        Brief description of amendment: The amendment revises TS 3/4.8.1, 
    ``Electric Power Systems - A.C. Sources,'' and its associated Bases to 
    achieve an overall improvement in emergency diesel generator 
    reliability and availability.
        Date of issuance: August 9, 1996
        Effective date: August 9, 1996, to be implemented within 90 days of 
    the date of issuance.
        Amendment No.: 101
        Facility Operating License No. NPF-42. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 22, 1996 (61 FR 
    25716) The June 14, 1996, and July 12, 1996, supplemental letters 
    provided Bases page changes and did not change the initial no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated August 9, 1996. No significant hazards consideration comments 
    received: No.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Dated at Rockville, Maryland, this 21st day of August 1996.
        For the Nuclear Regulatory Commission
    Steven A. Varga,
    Director, Division of Reactor Projects - I/II Office of Nuclear Reactor 
    Regulation
    [Doc. 96-21813 Filed 8-27-96; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Effective Date:
8/12/1996
Published:
08/28/1996
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X96-30828
Dates:
August 12, 1996
Pages:
44353-44368 (16 pages)
PDF File:
x96-30828.pdf