98-23458. Tennessee Valley Authority Browns Ferry Nuclear Plant, Units 2 and 3; Environmental Assessment and Finding of no Significant Impact  

  • [Federal Register Volume 63, Number 169 (Tuesday, September 1, 1998)]
    [Notices]
    [Pages 46491-46493]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 98-23458]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    [Docket Nos. 50-260 AND 50-296]
    
    
    Tennessee Valley Authority Browns Ferry Nuclear Plant, Units 2 
    and 3; Environmental Assessment and Finding of no Significant Impact
    
    Introduction
    
        The U.S. Nuclear Regulatory Commission (NRC, or the Commission) is 
    considering issuance of an amendment to Facility Operating License Nos. 
    DPR-52 and DPR-68 issued to the Tennessee Valley Authority (TVA or the 
    licensee) for operation of the Browns Ferry Nuclear Plant (BFN) Units 2 
    and 3, located in Limestone County, Alabama.
    
    Environmental Assessment
    
    Identification of the Proposed Action
    
        The proposed action would allow the licensee to increase allowed 
    core power level by 5 percent, from 3293 megawatt thermal (MWt) to the 
    uprated power level of 3458 MWt.
        The proposed action is in accordance with the licensee's 
    application for amendment dated October 1, 1997, as supplemented 
    October 14, 1997; and March 16 and 20, April 1 and 28, May 1, 20 and 
    22, June 12, 17 and 26, and July 17, 24, and 31, 1998.
    
    The Need for the Proposed Action
    
        The proposed action is needed to allow the licensee to increase the 
    licensed core thermal power and the potential electrical output of each 
    BFN Units 2 and 3 by approximately 55 MWt and thus, providing 
    additional electric power to service TVA's grid. The proposed thermal 
    power uprate project is in accordance with the generic boiling water 
    reactor (BWR) power uprate program established by the General Electric 
    Company and approved by the NRC in a letter dated September 30, 1991. 
    Power uprate has been widely recognized by the industry as a safe and 
    cost-effective method to increase generating capacity. The proposed 
    power uprate will provide the licensee with additional operational 
    flexibility.
    
    Environmental Impacts of the Proposed Action
    
        The Commission has completed its evaluation of the proposed action 
    and concludes that no significant change in the environmental impact 
    can be expected for the proposed increase in power. On September 1, 
    1972, TVA issued a Final Environmental Statement (FES) which is based 
    on a total electrical
    
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    generation name plate rating of 3456 MWt.
    
    Nonradiological Effects
    
        Under normal operation, BFN uses a once-through circulating water 
    system to dissipate heat from the main turbine condensers. Water is 
    drawn from the Tennessee River by the plant intake system and is 
    discharged back to the river. In addition, BFN currently has four 
    mechanical draft cooling towers which can be operated to assist in heat 
    dissipation (helper mode) primarily during summer hot weather periods.
        BFN has a National Pollutant Discharge Elimination System (NPDES) 
    permit issued by the State of Alabama that contains specific 
    requirements applicable to the nonradiological effluents released from 
    BFN. The licensee has evaluated the impact of power uprate on NPDES 
    limitations relating to effluent temperatures, cooling tower usages and 
    effects on biological species. The licensee has evaluated and 
    determined that post-accident effluent temperature from emergency 
    equipment cooling water systems and normal operating condition effluent 
    discharges from other plant systems such as yard drainage, station 
    sumps, and sewage treatment will not change as a result of the power 
    uprate. The licensee indicates that the proposed uprated power level 
    may result in approximately a 1 percent temperature increase of the 
    circulating water leaving the main condenser, a 5 percent increase in 
    the heat rejection to the Tennessee River, and may require additional 
    cooling tower usage during summer periods. The licensee states that as 
    a result of power uprate, cooling tower use would increase 
    approximately 12 percent. However, the impacts of the increase would 
    continue to be bounded by the FES. Based on its evaluation, the 
    licensee has concluded that the changes in discharges to the river as a 
    result of the power uprate will remain within the bounding conditions 
    established in the NPDES permit and no changes to the permit 
    requirements are needed as a result of the power uprate.
        As part of its NPDES permit application in April 1994, the licensee 
    documented its biological monitoring program and the effect of thermal 
    discharge limitations on selected biological species. In that report, 
    the licensee concluded that operation of BFN has not had a significant 
    impact on the reproductive success of yellow perch and sauger, or the 
    overall indigenous community in Wheeler Reservoir. This conclusion is 
    not affected by the power uprate.
        The proposed action would not change the method of generating 
    electricity at BFN Units 2 and 3 nor the methods of handling influents 
    from the environment or effluents to the environment. The licensee 
    indicates that power uprate does not require any plant modifications. 
    Therefore, no changes to land use or impacts to historical areas would 
    result from lay down areas. Therefore, no new or different types of 
    nonradiological environmental impacts are expected. The staff considers 
    that continued compliance with applicable Federal, State, and Local 
    agency requirements relating to environmental protection will preclude 
    any significant increase in nonradiological impacts over those 
    evaluated in the FES.
    
    Radiological Effects
    
        Gaseous and liquid effluents are produced during both normal 
    operation and abnormal operational events. The licensee has evaluated 
    the radiological effects of the proposed power uprate during both 
    normal operation and postulated accident conditions for gaseous and 
    liquid effluent releases.
        The licensee evaluated the offsite radiation exposure to the 
    maximally exposed individual member of the general public for the 
    proposed uprate. Section 2.4, Table 2.4.3, of the FES dated September 
    1, 1972, projected doses due to radioactive materials released to the 
    environment during routine operations of the BFN units. The estimated 
    radiation exposure of the maximally exposed individual from radioactive 
    material in both liquid and gaseous effluents was 2.2 mrem/year total. 
    The estimated dose based on actual liquid and gaseous effluent releases 
    for the period 1994-1996 was 0.054 mrem/year. Although a 5 percent 
    increase in reactor power does not necessarily result in any increase 
    in effluents, the licensee projected the total body dose would increase 
    to 0.056 mrem/year. This projected dose is about 2 percent of the 
    applicable NRC limits in 10 CFR Part 50, Appendix I. Therefore, the 
    staff concludes that the actual releases at the BFN units will still 
    remain within the FES estimates and are not significantly above current 
    levels.
        With respect to onsite radiation exposure, the licensee stated that 
    in-plant radiation levels will generally increase by no more than the 
    percentage increase in power level. The licensee stated that individual 
    worker exposures will be maintained within the acceptable limits by the 
    site as-low-as-reasonably-achievable program, by procedural controls 
    that compensate for increased radiation levels. The 5-year (1991-1996) 
    average collective dose at Browns Ferry was 202 person-rem per year per 
    reactor and 0.5 person-rem per MWe-year. (See NUREG-0713 Volume 18, 
    Occupational Radiation Exposure at Commercial Nuclear Power Reactors 
    and Other Facilities, 1996). This compares favorably with the average 
    collective dose for all BWRs of 306 person-rem per year per reactor and 
    0.5 person-rem per MWe-year. Considering a potential increase of 5 
    percent, onsite radiation exposure will not be significantly higher 
    than the current operation and will remain within the acceptable limits 
    of 10 CFR 20. Therefore, the staff concludes that operation at the 
    uprated power level will not significantly impact occupational 
    exposures.
        Regarding radioactive waste production, the licensee stated that 
    the total volume of processed waste is not expected to increase 
    appreciably since the only significant increase in processed waste is 
    due to the slightly more frequent backwashes of the condensate 
    demineralizers. Based on this, the licensee concluded that the power 
    uprate would not have an adverse effect on the processing of liquid 
    radwaste. With regard to gaseous waste production, the licensee stated 
    that gaseous effluent releases through building vents are not expected 
    to increase significantly with power uprate, since the releases are 
    maintained within administratively controlled values that are not a 
    function of core power. The noncondensable radioactive gases exhausted 
    from the main condenser and discharged via the off gas system are the 
    major source of radioactive gases. The licensee stated that the 
    operation of the off gas equipment will continue to be within the 
    design parameters for the equipment. The staff concludes that operation 
    at the uprated power will not significantly affect the licensee's 
    ability to process radioactive wastes. Therefore, the staff concludes 
    that operation at the uprated power level will not significantly 
    increase the allowable occupational exposures.
        Technical Specification (TS) 4.3 establishes spent fuel storage 
    design features to ensure that the fuel array in fully loaded fuel 
    racks remains subcritical and to prevent inadvertent draining of the 
    spent fuel pool. No changes to TS 4.3 were necessary for the uprate 
    condition. The design basis for the SFP system remains unchanged during 
    power uprate conditions. Therefore, the proposed action will not 
    significantly increase the probability or consequences of spent fuel 
    storage criticality accidents.
    
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        As discussed above, the projected dose due to power uprate is about 
    2 percent of the applicable NRC limits in 10 CFR Part 50, Appendix I 
    for offsite exposures, and will remain within the acceptable limits of 
    10 CFR 20 for occupational exposures. The actual releases at the BFN 
    units will also remain within the FES estimates. Thus, the amendment 
    does not significantly effect the amount or type of radiological plant 
    effluents, and has no other environmental impact. Therefore, the staff 
    concludes that continued compliance with applicable Federal, State, and 
    Local agency requirements relating to environmental protection will 
    preclude any significant radiological environmental impacts associated 
    with the proposed uprate. Accordingly, the Commission concludes that 
    there are no significant radiological environmental impacts associated 
    with the proposed action.
    
    Alternatives to the Proposed Action
    
        Since the Commission has concluded there is no significant 
    environmental impact associated with the proposed action, any 
    alternatives with equal or greater environmental impact need not be 
    evaluated. As an alternative to the proposed action, the NRC staff 
    considered denial of the proposed action (no action alternative). 
    Denial of the application would result in no change in current 
    environmental impacts and would reduce operational flexibility.
    
    Alternative Use of Resources
    
        This action does not involve the use of any resources not 
    previously considered in the FES dated September 1, 1972 for BFN Units 
    2 and 3.
    
    Agencies and Persons Consulted
    
        In accordance with its stated policy, on August 26, 1998, the NRC 
    staff consulted with the Alabama State official, Mr. Kirk Whatley of 
    the State Office of Radiation Control, regarding the environmental 
    impact of the proposed action. The State official had no comments.
    
    Finding of no Significant Impact
    
        Based upon the environmental assessment, the Commission concludes 
    that the proposed action will not have a significant effect on the 
    quality of the human environment. Accordingly, the Commission has 
    determined not to prepare an environmental impact statement for the 
    proposed action.
        For further details with respect to this action, see the 
    application for amendment dated October 1, 1997, as supplemented 
    October 14, 1997; and March 16 and 20, April 1 and 28, May 1, 20 and 
    22, June 12, 17 and 26, and July 17, 24, and 31, 1998, which are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street NW., Washington, DC and at the 
    local public document room located at the Athens Public Library, 405 E. 
    South Street, Athens, Alabama.
    
        Dated at Rockville, Maryland, this 26th day of August 1998.
    
        For the Nuclear Regulatory Commission.
    Frederick J. Hebdon,
    Director, Project Directorate II-3, Division of Reactor Projects--I/II, 
    Office of Nuclear Reactor Regulation.
    [FR Doc. 98-23458 Filed 8-31-98; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
09/01/1998
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
98-23458
Pages:
46491-46493 (3 pages)
Docket Numbers:
Docket Nos. 50-260 AND 50-296
PDF File:
98-23458.pdf