95-22616. Applications and Amendments to Facility Operating LicensesInvolving No Significant Hazards Considerations  

  • [Federal Register Volume 60, Number 177 (Wednesday, September 13, 1995)]
    [Notices]
    [Pages 47613-47630]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 95-22616]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    Biweekly Notice
    
    
    Applications and Amendments to Facility Operating 
    LicensesInvolving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from August 18, 1995, through August 30, 1995. 
    The last biweekly notice was published on Wednesday, August 30, 1995 
    (60 FR 45172). 
    
    [[Page 47614]]
    
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By October 13, 1995, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public 
    
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    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. Where petitions are filed during the last 10 days of 
    the notice period, it is requested that the petitioner promptly so 
    inform the Commission by a toll-free telephone call to Western Union at 
    1-(800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson 
    Steam Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of amendment request: July 17, 1995
        Description of amendment request: The requested change to Technical 
    Specification (TS) section 3.8 would specify that the spent fuel 
    building refueling filter fan and at least one containment purge fan 
    shall be shown to operate within plus or minus 10 percent of the design 
    flow.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:The proposed change to TS is to 
    revise Section 3.8.2.c. This TS section currently states ``All filter 
    system fans shall be shown to operate within [plus or minus] 10% of the 
    design flow.'' The proposed requirements are as follows:
        c.1 The Spent Fuel Building refueling filter fan shall be shown 
    to operate within [plus or minus] 10% of the design flow.
        c.2 At least one Containment purge filter fan shall be shown to 
    operate within [plus or minus] 10% of the design flow and must be 
    operable during core alterations or movement of irradiated fuel 
    assemblies, or at least one automatic containment isolation valve in 
    each line penetrating the containment which provides a direct path 
    from the containment atmosphere to the outside atmosphere shall be 
    securely closed.
        This proposed change does not involve a significant hazards 
    consideration for the following reasons.
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. The proposed change clarifies the operating requirements 
    for the Containment purge and Spent Fuel Building refueling filter 
    systems. This proposed change to the TS specifically delineates the 
    fan filter systems required for refueling operations and does not 
    change the physical operation of the filter systems. The affected 
    systems are not involved in the initiation of any accident. The 
    system response to previously analyzed accidents, including system 
    flows and filter efficiencies will not be altered by the proposed 
    change. These changes are enhancements to clarify existing TS 
    requirements that will not increase the probability or consequences 
    of a previously analyzed accident.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. The proposed change merely clarifies the specific filter 
    systems that are necessary to mitigate a fuel handling accident 
    during core alterations or the movement of irradiated fuel 
    assemblies and is consistent with the accident analysis in Section 
    15.7.4 of the Updated Final Safety Analysis Report (UFSAR). This 
    proposed change does not involve the addition or modification of 
    plant equipment, nor does it alter the design or operation of plant 
    systems. Therefore, operation of the facility in accordance with the 
    proposed TS change will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed change clarifies which filter systems that must 
    be capable of mitigating a design basis fuel handling accident 
    during core alterations or the movement of irradiated fuel 
    assemblies and is consistent with the accident analysis in Section 
    15.7.4 of the UFSAR. The proposed change will not result in an 
    increase in the Control Room or offsite radiation doses. The 
    performance of the filtration systems, including adsorption 
    efficiencies, will not change. Therefore, the proposed change does 
    not involve a reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, SC 29550
        Attorney for licensee: R. E. Jones, General Counsel, Carolina Power 
    & Light Company, Post Office Box 1551, Raleigh, NC 27602
        NRC Project Director: David B. Matthews
    
    Commonwealth Edison Company, Docket Nos. 50-295 and 50-304, Zion 
    Nuclear Power Station, Units 1 and 2, Lake County, Illinois
    
        Date of amendment request: June 30, 1995
        Description of amendment request: The proposed amendments would 
    modify the emergency diesel generator testing requirements in the 
    Technical Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of occurrence of any accident 
    previously evaluated.
        The proposed changes to the Technical Specifications will change 
    the scope of EDG [Emergency Diesel Generator] testing that is 
    performed on a refueling cycle frequency. The proposed changes will 
    eliminate the requirement to perform sequenced loading of the EDG as 
    part of the hot restart test, and will allow the hot restart test to 
    be initiated from any EDG start signal. The revised requirements 
    will eliminate testing that is redundant, provides no additional 
    meaningful information, significantly constrains scheduling of 
    refueling outage maintenance and testing, and impacts the 
    availability of systems and components important to safety. The 
    proposed testing requirements satisfy the underlying purpose of the 
    EDG hot restart test. The testing in accordance with the proposed 
    requirements will verify the ability of each EDG to complete the 
    start up sequence from an equilibrium temperature immediately 
    following operation at full load for a period of time long enough to 
    stabilize operating temperature.
        A two hour period for operation at full load has been chosen to 
    ensure that full load operating temperature has stabilized prior to 
    shutdown preceding the hot restart test. Momentary transients 
    outside the full load operating band of 3600 to 4000 kW will not 
    invalidate the two hour run since momentary transient will not 
    significantly affect operating temperature. Brief operation 
    subsequent to a momentary transient will normalize operating 
    temperature. Since the proposed changes impact only surveillance 
    requirements used to periodically verify the operability of a 
    required safety system, and since the proposed changes provide an 
    
    [[Page 47616]]
    equivalent level of testing and eliminate redundant testing, the 
    proposed changes will not impact the operability or availability of 
    a required system.
        Operation in accordance with the revised requirements will not 
    increase the likelihood that a transient initiating event will occur 
    since transients are initiated by equipment malfunction and/or 
    catastrophic system failure. The revised requirements affect testing 
    that is performed on a Refueling Cycle frequency. Testing in 
    accordance with the proposed requirements will not increase the 
    probability of failure of the EDGs since the testing will provide an 
    equivalent level of testing to verify the operability of the EDGs. 
    In addition, failure of an EDG to start or failure of an EDG while 
    operating is not assumed to be an initiating event of an accident 
    considered in the Updated Final Safety Analysis Report (UFSAR). 
    Based on the above, operation in accordance with the proposed 
    requirements will not significantly increase the probability of 
    occurrence of any accident previously evaluated.
        The proposed requirements will meet the underlying purposed of 
    the existing testing requirements. The proposed testing will ensure 
    the ability of the EDG to start from a hot condition in the unlikely 
    event of an accident. The proposed changes will eliminate testing 
    requirements that are redundant and unnecessarily challenge the 
    reliability of the EDGs by requiring unnecessary wear and cycling of 
    the diesel engine and auxiliary systems. Since the proposed changes 
    will not adversely affect the operability or availability of the 
    EDGs, the ability of the EDGs to operate and power equipment 
    important to safety will not be impacted and the ability to mitigate 
    the consequences of accidents previously evaluated will not be 
    affected. Based on the preceding discussion, the consequences of 
    accidents previously evaluated will not significantly increase.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes to the Technical Specifications do not 
    involve the addition of any new or different types of safety related 
    equipment, nor do they involve the operation of equipment required 
    for safe operation of the facility in a manner different from those 
    addressed in the UFSAR. No safety related equipment or function will 
    be altered as a result of the proposed changes. Also, the procedures 
    that govern normal operation and recovery from an accident are not 
    affected by the proposed changes.
        The proposed changes will eliminate testing requirements that 
    are redundant and provide no additional meaningful information. 
    Testing in accordance with the revised requirements will provide an 
    equivalent level of confidence in the reliability of the EDG systems 
    to complete the start up sequence from a hot condition. The proposed 
    testing requirements satisfy the purpose Regulatory Guide 1.108 in 
    that the testing requirements will ensure EDG operability and 
    reliability. In addition, the proposed changes are consistent with 
    the changes recommended by the NRC in Generic Letter 93-05. Since no 
    new failure modes or mechanisms are introduced by the proposed 
    changes, the possibility of a new or different kind of accident is 
    not created.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        Plant safety margins are established through LCOs, limiting 
    safety system settings, and safety limits specified in the Technical 
    Specifications. There will be no changes to either the physical 
    design of the plant or to any of these settings or limits as a 
    result of the proposed changes. The proposed changes will eliminate 
    testing requirements that are redundant and provide no additional 
    information. Testing in accordance with the revised requirements 
    will verify the ability of the EDGs to complete the start up 
    sequence from a hot condition as is intended by the recommended 
    testing in Regulatory Guide 1.108. In addition, the proposed changes 
    are consistent with the changes recommended by the NRC in Generic 
    Letter 93-05. Since the proposed changes will not impact the 
    availability or operability of the EDGs to perform their intended 
    function and since no LCOs, safety limits, or safety system settings 
    are affected by the proposed changes, there is no significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Waukegan Public Library, 128 
    N. County Street, Waukegan, IL 60085
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, IL 60603
        NRC Project Director: Robert A. Capra
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of amendment request: July 26, 1995.
        Description of amendment request: The licensee proposes to change 
    Turkey Point Units 3 and 4 Technical Specifications to allow rod 
    misalignment of +/- 18 steps at or below 90% of rated thermal power. In 
    addition, a change is proposed to the Limiting Condition for Operation 
    range of rod travel from 228 to ``All Rods Out.'' The introduction of 
    ``All Rods Out'' is consistent with Amendment 167/161 which approved 
    the removal of Technical Specification 3.1.3.6, ``Rod Insertion Limit'' 
    from the Technical Specifications and placement into the Core Operating 
    Limits Report (COLR).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of any accident previously evaluated.
        The proposed limits on rod misalignment do not increase the 
    probability of an accident. The Technical Specifications' allowed 
    increase in peaking factor limits as power is reduced accommodates 
    an increase in rod misalignment of [plus or minus] 18 steps below 
    90% of RTP [rated thermal power]. The initial conditions remain 
    unchanged from that assumed in the Updated Final Safety Analysis 
    Report (UFSAR). Therefore, this proposed change poses no significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        No new accident scenarios, failure mechanisms or limiting single 
    failure are introduced as a result of implementing the proposed rod 
    misalignment criteria. The institution of the proposed rod 
    misalignment criteria will have no adverse effect, nor does it 
    challenge, the performance of any other safety related system. 
    Therefore, the proposed amendment does not in any way create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in the margin of 
    safety.
        Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in the margin of 
    safety. The margin of safety, as defined in the BASES for the 
    Technical Specifications, is not significantly affected by the 
    changes to the rod misalignment limit. The Technical Specifications' 
    allowed increase in peaking factor limits as power is reduced 
    accommodates an increase in rod misalignment of [plus or minus] 18 
    steps below 90% of RTP. The initial conditions remain unchanged from 
    that assumed in the UFSAR. Since the peaking factor limits are not 
    modified, the proposed change does not constitute a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, FL 33199 
    
    [[Page 47617]]
    
        Attorney for licensee: J. R. Newman, Esquire, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036
        NRC Project Director: David B. Matthews
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of amendment request: July 26, 1995.
        Description of amendment request: The licensee proposes to change 
    Turkey Point Units 3 and 4 Technical Specifications to delete the 
    requirement to adjust the Nuclear Instrumentation System (NIS) downward 
    when operating at less than 70% of rated thermal power (RTP).
        At reduced power levels (i.e., less than 70% of RTP), calorimetric 
    power measurement uncertainties are most influenced by the feedwater 
    flow measurements, which have the potential for large flow 
    uncertainties under low flow conditions. These calorimetric 
    uncertainties create the potential for a non-conservative gain 
    adjustment of the NIS when the NIS is adjusted downward to match 
    calorimetric power at reduced power levels, and may result in a non-
    conservative NIS power level indication when operating at higher power 
    levels. Inappropriate gain adjustments could cause the NIS Power Range 
    High Neutron Flux trip to occur at power levels beyond that assumed in 
    the plant safety analyses. The proposed changes would correct this 
    situation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed change does not involve any physical changes to the 
    NIS. Implementation of the proposed change does not affect the 
    probability of failure of the NIS and does not alter the method in 
    which protection is afforded by the NIS for the reactor and primary 
    system. Therefore, the proposed change does not result in an 
    increase in the severity or consequences of any accident previously 
    evaluated.
        The proposed change in Technical Specifications to remove the 
    requirement which could result in non-conservative gain adjustments 
    of the NIS at reduced power levels (below 70% of RTP), will have no 
    significant effect on the probability or consequences of licensing 
    basis events; and the probability or consequences of an accident 
    previously evaluated for Turkey Point has not been significantly 
    increased. Therefore, operation of the facility in accordance with 
    the proposed amendments would not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposed change does not result in a change in the method in 
    which the NIS provides plant protection. No change is being made 
    which alters the function of the NIS. Therefore, the proposed change 
    does not create the possibility of a new or different kind of 
    accident nor involve a reduction in a margin of safety as defined in 
    the Safety Analysis Report.
        The change in Technical Specifications associated with the 
    removal of the requirement which could result in non-conservative 
    gain adjustments of the NIS at reduced power levels (below 70% of 
    RTP) will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in the margin of 
    safety.
        This change in Technical Specifications only affects the removal 
    of the requirement which has the potential for non-conservative gain 
    adjustments of the NIS at reduced power levels (below 70% of RTP); 
    these changes do not alter the manner in which protection is 
    afforded for the reactor and primary system. In addition, the 
    fundamental process for implementation of the calorimetric power/NIS 
    comparison remains the same.
        The changes in Technical Specifications associated with the 
    removal of the requirement, which could lead to non-conservative 
    gain adjustments of the NIS at reduced power levels (below 70% of 
    RTP), will not involve a significant reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, FL 33199
        Attorney for licensee: J. R. Newman, Esquire, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036
        NRC Project Director: David B. Matthews
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of amendment request: July 26, 1995.
        Description of amendment request: The licensee proposes to change 
    Turkey Point Units 3 and 4 Technical Specifications (TS) to incorporate 
    certain changes which are consistent with guidance provided by NUREG-
    1366 and NRC Generic Letter (GL) 93-05, ``Line-Item Technical 
    Specification Improvements to Reduce Surveillance Requirements for 
    Testing During Power Operation.'' The following proposed changes are 
    requested:
        (1) TS SR 4.1.3.1.2: Change the frequency interval for control rod 
    movement test from monthly to quarterly.
        (2) TS SR 4.6.5.1: Change the hydrogen monitor calibration from 
    quarterly to each refueling interval, and the analog channel 
    operational test from monthly to quarterly.
        (3) TS SR Table 4.3-3: Change the analog channel functional test 
    from monthly to quarterly for radiation monitors. Correct spelling of 
    'Radioactivity' in Item 1.a.
        (4) TS SR 4.4.6.2.2: Increase the time allowed in COLD SHUTDOWN 
    before leak testing the Reactor Coolant System (RCS) isolation valves 
    is required, from 72 hours to 7 days.
        (5) TS SR 4.10.1.2: Changes the requirement for a rod drop test 
    prior to reducing SHUTDOWN MARGIN from ``within 24 hours'' to ``within 
    7 days''.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendments do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    because the proposed amendments conform to the guidance given in 
    Enclosure 1 of the NRC Generic Letter 93-05. The overall functional 
    capabilities of the rod control system, RCS pressure isolation 
    valves, the hydrogen monitoring system, and the radiation monitoring 
    systems will not be modified by the proposed change. These 
    amendments will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated for 
    the following reasons:
        (1) Increasing the interval of control rod movement testing will 
    reduce the possibility of testing-related reactor trips and dropped 
    rods, and result in fewer challenges to safety systems and plant 
    transients.
        (2) Increasing the interval of hydrogen monitor calibration and 
    operational tests will result in a reduction in equipment 
    degradation and reduce a burdensome task on personnel resources.
    
    [[Page 47618]]
    
        (3) Increasing the interval of radiation monitor functional 
    tests will result in less equipment degradation as well as reducing 
    the potential for testing-related isolations of the control room, 
    fuel handling building, auxiliary buildings, and various process 
    lines.
        (4) Increasing the time allowed in COLD SHUTDOWN prior to leak 
    testing RCS isolation valves will permit plant personnel to focus on 
    short notice outage recovery and minimize personnel radiation 
    exposure. Since the methods and the acceptance criteria used for the 
    leak test are not altered, increasing the time from 72 hours to 7 
    days will not significantly alter the associated risk.
        (5) Increasing the time required to perform rod tests prior to 
    reducing the SHUTDOWN MARGIN will result in only one rod drop test 
    vice two following a refueling outage, which will in turn reduce 
    plant transients and personnel resource requirements.
        (2) Operation of the facility in accordance with the proposed 
    amendments would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The use of the proposed changes to the TS can not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated since the proposed amendments will not change 
    the physical plant or the modes of plant operation defined in the 
    facility operating license. No new failure mode is introduced due to 
    the surveillance interval changes and clarifications, since the 
    proposed changes do not involve the addition or modification of 
    equipment nor do they alter the design or operation of affected 
    plant systems.
        (3) Operation of the facility in accordance with the proposed 
    amendments would not involve a significant reduction in a margin of 
    safety.
        The operating limits and functional capabilities of the affected 
    systems are unchanged by the proposed amendments. The proposed 
    changes to the TS which establish new or clarify old surveillance 
    intervals consistent with the NRC Generic Letter 93-05 line-item 
    improvement guidance do not significantly reduce any of the margins 
    of safety even though the number of surveillances is decreased. 
    These requested amendments are justified by the following reasoning 
    from NUREG-1366:
        (1) The surveillances could lead to plant transients which would 
    challenge safety systems unnecessarily as in the cases of control 
    rod movement tests and post-refueling rod drop tests.
        (2) The surveillances result in the unnecessary wear to 
    equipment as in the cases of the hydrogen and radiation monitor 
    surveillances.
        (3) The surveillance result in radiation exposure to plant 
    personnel which is not justified by the safety significance of the 
    surveillances as in the case of the time requirement for leak-
    testing RCS isolation valves when in COLD SHUTDOWN.
        (4) The surveillances place an unnecessary burden on plant 
    personnel because the time required is not justified by the safety 
    significance of the surveillance, i.e. hydrogen monitor and post-
    refueling rod drop tests.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, FL 33199
        Attorney for licensee: J. R. Newman, Esquire, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036
        NRC Project Director: David B. Matthews
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of amendment request: July 26, 1995.
        Description of amendment request: The licensee proposes to change 
    Turkey Point Units 3 and 4 Technical Specification Administrative 
    Controls Section 6.9.1.7 to reflect the use of the Westinghouse NOTRUMP 
    model in the Small Break Loss-of-Coolant Accident (SBLOCA) analysis 
    used in determining the K(z) curve contained in the Core Operating 
    Limits Report (COLR). The following references would be added to 
    Section 6.9.1.7 (COLR) of the Administrative Controls section of Turkey 
    Point Units 3 and 4 TS: WCAP-10054-P-A, (proprietary) and 
    WCAP-10081-NP-A, (non-proprietary), ``Westinghouse Small Break ECCS 
    Evaluation Model Using the NOTRUMP Code'', October, 1985.'' WCAP-10054-
    P-A Addendum 2, (proprietary), ``Addendum to the Westinghouse Small 
    Break ECCS Evaluation Model Using the NOTRUMP Code: Safety Injection 
    into the Broken Loop and COSI Condensation Model'', August, 1994.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The modification to the current Section 6.9.1.7 of the 
    Administrative Controls section of the Turkey Point Technical 
    Specifications to include the references to WCAP-10054-P-A, ``Small 
    Break ECCS Evaluation Model Using the NOTRUMP Code'', and WCAP-
    10054-P-A Addendum 2 for the COSI model, does not involve an 
    increase in the probability or consequences of an accident 
    previously evaluated. This modification to the Technical 
    Specification does not change the probability of occurrence 
    previously evaluated.
        This change does not affect the integrity of the fission product 
    barriers utilized for mitigation of radiological dose consequences 
    as a result of an accident. The addition of the new methodology used 
    for Turkey Point uprating analysis does not change, degrade, or 
    prevent the response of safety related mitigation systems to 
    accident scenarios, as described in the Updated Final Safety 
    Analysis Report (UFSAR) Chapter 14. Therefore, the licensee 
    concluded that the probability or consequences of an accident 
    previously evaluated are not increased.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The modification to the current Section 6.9.1.7 of the 
    Administrative Controls section of the Turkey Point Technical 
    Specifications to include the references to WCAP-10054-P-A, ``Small 
    Break ECCS Evaluation Model Using the NOTRUMP Code'', and WCAP-
    10054-P-A Addendum 2 for the COSI model, will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated. No new operating configuration is being 
    imposed by the addition of the references to the Technical 
    Specification. Therefore, no new failure modes or limiting single 
    failures have been identified. The licensee concludes that no new or 
    different kind of accidents from those previously evaluated have 
    been created as a result of this revision.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in the margin of 
    safety.
        The modification to the current Section 6.9.1.7 of the 
    Administrative Controls section of the Turkey Point Technical 
    Specifications to include the references for the Small Break ECCS 
    Evaluation Model Using the NOTRUMP Code will not involve a reduction 
    in the margin of safety. The SBLOCA analysis results show that the 
    limits of 10 CFR 50.46 are maintained as follows. The new calculated 
    value of worst-case PCT will be 1688 deg.F, which is less than the 
    limit of 2200 deg.F. There is significant margin in the current 
    SBLOCA analysis such that the total cladding oxidation limit of 17 
    percent will not be challenged. Further, the calculated total amount 
    of hydrogen generated has been determined to remain less than 1 
    percent. The SBLOCA hydraulic forces are not affected by the K(z) 
    curve and the licensee concludes that the core will remain amenable 
    to cooling. Additionally, post-LOCA long term core cooling and hot 
    leg switchover evaluations are not impacted by the K(z) curve. 
    Therefore, there is no significant reduction in the margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request 
    
    [[Page 47619]]
    involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, FL 33199
        Attorney for licensee: J. R. Newman, Esquire, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036
        NRC Project Director: David B. Matthews
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of amendment request: July 26, 1995.
        Description of amendment request: The licensee proposes to change 
    Turkey Point Units 3 and 4 Technical Specifications to achieve 
    consistency throughout these documents by (a) removing outdated 
    material, (b) incorporating administrative clarifications and 
    corrections, and (c) correcting typographical errors.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendments do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    because the proposed amendments are purely administrative in nature. 
    These amendments will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated 
    because they do not affect assumptions contained in plant safety 
    analyses, the physical design and/or operation of the plant, nor do 
    they affect Technical Specifications that preserve safety analysis 
    assumptions. Therefore, the proposed changes do not affect the 
    probability or consequences of accidents previously analyzed.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The use of the modified specifications can not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated since the proposed amendments will not change 
    the physical plant or the modes of plant operation defined in the 
    facility operating license. No new failure mode is introduced due to 
    the administrative changes and clarifications, since the proposed 
    changes do not involve the addition or modification of equipment nor 
    do they alter the design or operation of affected plant systems, 
    structures, or components.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in the margin of 
    safety.
        The operating limits and functional capabilities of the affected 
    systems, structures, and components are unchanged by the proposed 
    amendments. The modified specifications which correct administrative 
    errors and clarify existing Technical Specification requirements do 
    not significantly reduce any of the margins of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Florida International 
    University, University Park, Miami, FL 33199
        Attorney for licensee: J. R. Newman, Esquire, Morgan, Lewis & 
    Bockius, 1800 M Street, NW., Washington, DC 20036
        NRC Project Director: David B. Matthews
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, 
    and Entergy Operations, Inc., Docket No. 50-458, River Bend 
    Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: August 17, 1995
        Description of amendment request: The proposed amendment would 
    allow the containment to be opened after about 11 days following 
    shutdown during refueling and would redefine the operability 
    requirements for selected engineered safety feature systems such that 
    these systems are only required to be operable during the calculated 
    decay period. The proposed changes will not remove requirements for 
    systems to mitigate potential vessel draindown events, will not remove 
    requirements for systems required for decay heat removal, and will 
    continue to require high water level over the vessel during fuel 
    movement. Programs are in place to close the containment, if needed, to 
    address shutdown risk concerns.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed limits on recently irradiated fuel is used to 
    establish operational conditions where specific activities represent 
    situations where significant radioactive releases can be postulated. 
    These operational conditions are consistent with the design basis 
    analysis. Because the equipment affected by the revised operational 
    conditions is not considered an initiator to any previously analyzed 
    accident, inoperability of the equipment cannot increase the 
    probability of any previously evaluated accident.
        The proposed applicability in conjunction with existing 
    administrative controls on light loads, bounds the conditions of the 
    current design basis fuel handling accident analysis. The analysis 
    also concludes the limiting offsite radiological consequences are 
    well within the acceptance criteria of NUREG 0800, Section 15.7.4 
    and GDC 19. The analysis is also conducted in a conservative manner 
    containing margins in the calculation of mechanical analysis, iodine 
    inventory and iodine decontamination factor. Each of these 
    conservatisms will further decrease the consequences. Therefore, the 
    proposed changes do not significantly increase the probability or 
    consequences of any previously evaluated accident.
        The proposed limits are used to establish operational conditions 
    where specific activities represent situations where significant 
    radioactive releases can be postulated. In addition, the changes to 
    operation are consistent with previous limits -- only allowing 
    increased flexibility after the radiological consequences are 
    assured to remain within accepted limits. Therefore, these 
    operational conditions are consistent with the design basis 
    analysis. The proposed changes do not introduce any new modes of 
    plant operation and do not involve physical modifications to the 
    plant. Therefore, the proposed changes do not create the possibility 
    of a new or different kind of accident from any previous analyzed.
        The revised limits are used to establish operational conditions 
    where specific activities represent situations where significant 
    radioactive release can be postulated. These operational conditions 
    are consistent with the design basis analysis and are established 
    such that the radiological consequences are at or below the current 
    RBS licensing limit. Safety margins and analytical conservatisms 
    have been evaluated and are well understood. Conservative methods of 
    analysis are maintained through the use of accepted methodology and 
    benchmarking the proposed methods to previous analysis. Margins are 
    retained to ensure that the analysis adequately bounds all 
    postulated event scenarios. The proposed change only eliminates some 
    excess conservatism from the analysis.
        EOI has implemented NUMARC 91-06 guidelines for shutdown 
    operations at RBS. Shutdown Operations Protection Plan and Primary-
    Secondary Containment Integrity procedures presently include 
    guidance for closure of the containment hatch and other significant 
    opening in containment, in addition to the requirements contained in 
    the license and design basis. This additional protection will 
    enhance the ability to limit offsite effects.
        Acceptance limits for the fuel handling accident are provided in 
    10CFR100 with additional guidance provided in NUREG 0800, Section 
    15.7.4 Excess margin is the difference between the postulated doses 
    and the corresponding licensing limit. In the 
    
    [[Page 47620]]
    initial review of River Bend Station for operation (NUREG-0989, Section 
    15.7.4), the NRC accepted the design and analysis based on meeting 
    the guideline dose limits of 10CFR100 and SRP 15.7.4. The proposed 
    applicability continues to ensure that the whole-body and thyroid 
    doses at the exclusion area and low population zone boundaries, as 
    well as control room doses, are below the corresponding licensing 
    limit. These margins are unchanged; therefore, the proposed changes 
    do not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803
        Attorney for licensee: Mark Wetterhahn, Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, DC 20005
        NRC Project Director: William D. Beckner
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of amendment requests: June 20, 1995 (AEP:NRC:0692CX)
        Description of amendment requests: The proposed amendments would 
    remove the requirements for fire protection systems from the licenses 
    and the Technical Specifications (T/S) in accordance with the 
    provisions and guidance of Generic Letters (GL) 86-10, ``Implementation 
    of Fire Protection Requirements,'' 88-12, ``Removal of Fire Protection 
    Requirements from Technical Specifications,'' and 93-07, Modification 
    of the Technical Specification Administrative Control Requirements for 
    Emergency and Security Plans.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        We have evaluated the proposed T/S changes and have determined 
    that the changes should involve no significant hazards consideration 
    based on the criteria established in 10 CFR 50.92(c). Operation of 
    CNP [Cook Nuclear Plant] in accordance with the proposed amendment 
    will not satisfy any of the following criteria.
        (a) Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes are administrative in nature, in that it 
    moves the T/Ss portion of the Fire Protection Program from the T/Ss 
    to the UFSAR [Updated Final Safety Analysis Report] and the 
    implementing procedures. This is accomplished by referencing in the 
    UFSAR and the documents which address the Fire Protection Program in 
    greater detail. Thus, the proposed changes will not revise the 
    requirements for fire protection equipment operability, testing, or 
    inspection, but only moves the T/Ss portion of the Fire Protection 
    Program to implementing procedures.
        As fire protection requirements are only being relocated 
    following the guidance of GLs 86-10, 88-12, and 93-07, the proposed 
    changes do not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        (b) Create the possibility of a new or different kind of 
    accident from any previously analyzed.
        The proposed changes do not involve any physical alteration of 
    plant configurations, changes to setpoints, or operating parameters. 
    [These] are administrative changes that retain the existing fire 
    protection requirements and relocate these requirements from the T/S 
    to the UFSAR; therefore, these changes do not create the possibility 
    of a new or different kind of accident.
        (c) Involve a significant reduction in a margin of safety.
        The proposed changes follow guidance contained in GLs 86-10, 88-
    12, and 93-07 for incorporating the Fire Protection Program into the 
    UFSAR. A license condition will be implemented that will require 
    that no changes can be made to the Fire Protection Program that will 
    adversely affect the ability to achieve or maintain safe shutdown in 
    the event of a fire without prior NRC approval. Therefore, the 
    proposed changes do not involve a significant reduction in a margin 
    of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, Michigan 49085
        Attorney for licensee: Gerald Charnoff, Esq., Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London, 
    Connecticut
    
        Date of amendment request: August 23, 1995
        Description of amendment request: The proposed amendment would 
    revise Technical Specifications Section 3.8.1.1 and the Bases for 
    Section 3/4.8. The proposed amendment would extend the Allowed Outage 
    Time (AOT) for an Emergency Diesel Generator (EDG) from 72 hours to 7 
    days.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
        ... NNECO concludes that these changes do not involve a 
    significant hazards consideration since the proposed change 
    satisfies the criteria of 10 CFR 50.92(c). That is, the proposed 
    changes do not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        The EDGs supply backup power to the essential safety systems in 
    the event of a Loss of Normal (offsite) Power. EDGs are not accident 
    initiators. Therefore, this change does not involve an increase in 
    the probability of any accident previously evaluated.
        Although the EDGs provide backup power to components that help 
    mitigate the consequences of accidents previously evaluated, the 
    extension in the AOT does not affect any of the assumptions used in 
    the deterministic evaluations of these accidents. Thus, this change 
    will not increase the consequences of any accident previously 
    analyzed.
        The increase in the EDG AOT introduces the potential to increase 
    the risk to the public since a longer time window provides an 
    opportunity to perform additional preventive maintenance to the EDG 
    while the plant is on-line. However, the extended AOT, by itself, 
    does not necessarily increase risk. The increase in the risk depends 
    on the total time during which an EDG was out of service and the 
    other equipment that is concurrently out of service with the EDG. 
    The total risk increase due to the EDG being out of service will not 
    be significant since that risk increase is monitored and kept at 
    acceptable levels in accordance with the risk monitor program.
        Based on the above, the proposal to extend the AOT for the EDGs 
    (Technical Specification 3.8.1) does not involve a significant 
    increase in the probability or consequences of an accident 
    previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed change to extend the AOT for the EDGs (Technical 
    Specification 3.8.1) does not alter the physical design, 
    configuration, or method of operation of the plant. Therefore, the 
    proposal does not create the possibility of a new or different kind 
    of accident from any previously analyzed.
        3. Involve a significant reduction in the margin of safety.
        The proposed change to extend the AOT for the EDGs (Technical 
    Specification 3.8.1) do not affect the Limiting Conditions for 
    Operations or their bases. As a result, the deterministic analyses 
    performed to establish the margin of safety are unaffected. Thus, 
    the change does not involve a significant reduction in the margin of 
    safety. 
    
    [[Page 47621]]
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270
        NRC Project Director: Phillip F. McKee
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, 
    Millstone Nuclear Power Station, Unit No. 2, New London, 
    Connecticut
    
        Date of amendment request: August 23, 1995
        Description of amendment request: The proposed amendment would 
    extend the Allowed Outage Time (AOT) for an inoperable Safety Injection 
    Tank (SIT) from 1 hour to 24 hours, unless the SIT is inoperable due to 
    either boron concentration not within its limits or an inoperable level 
    or pressure instrument. For these two special cases, the proposed 
    change extends the AOT for an inoperable SIT to 72 hours. In addition, 
    the proposed amendment clarifies the completion times and conditions 
    for action statements and the criteria for surveillance requirements.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration (SHC), which is presented below:
        ... NNECO concludes that these changes do not involve a 
    significant hazards consideration since the proposed change 
    satisfies the criteria in 10 CFR 50.92(c). That is, the proposed 
    changes do not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously analyzed.
        The Safety Injection Tanks (SITs) are passive components in the 
    Emergency Core Cooling System that mitigate the consequences of a 
    Loss of Coolant Accident (LOCA). As such, the SITs are not accident 
    initiators. Therefore, this change does not involve an increase in 
    the probability of any accident previously evaluated.
        The increase in the AOT has the potential to increase the risk 
    if it becomes necessary to stay on-line longer than one (1) hour 
    with an inoperable SIT. However, the estimated risk impact is 
    negligible.
        The SITs inject borated water into the reactor vessel (via the 
    cold legs) during the blowdown phase of a large break LOCA. The 
    introduction of the inventory of borated water from all four (4) 
    SITs is needed to ensure adequate reflooding of the core (i.e., 
    minimize core damage) until the Engineered Safety Feature (ESF) 
    pumps can provide adequate core cooling. The SITs also provide 
    makeup water for the Reactor Coolant System (RCS) for smaller break 
    LOCAs. The extension of the AOT does not affect any of the 
    assumptions used in the deterministic evaluations of these 
    accidents. Thus, this change will not increase the consequences of 
    any accident previously evaluated.
        The increased AOT extension to 72 hours, based solely on 
    instrumentation (level and pressure) malfunction, also does not 
    involve a significant increase in the consequences of an accident 
    previously evaluated as endorsed by the NRC in NUREG-1366, 
    ``Improvements to Technical Specifications Surveillance 
    Requirements.''
        The modification to the completion times and the modification of 
    the Surveillance Requirements for volumetric changes in the SIT as a 
    result of addition from the Refueling Water Storage Tank (RWST) also 
    do not involve a significant increase in the consequences of any 
    accident previously evaluated by the NRC in NUREG-1432, ``Standard 
    Technical Specifications for Combustion Engineering Plants.''
        Based on the above, the proposed changes to extend the AOT for 
    an inoperable SIT, clarify action statements, and modify the 
    criteria for surveillance requirements, do not involve a significant 
    increase in the probability or consequences of an accident 
    previously analyzed.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        The proposed changes to extend the AOT for an inoperable SIT, 
    clarify action statements, and modify the criteria for surveillance 
    requirements, do not alter the physical design, configuration, or 
    method of operation of the plant. Therefore, the proposal does not 
    create the possibility of a new or different kind of accident from 
    any previously analyzed.
        3. Involve a significant reduction in the margin of safety.
        The proposed changes to extend the AOT for an inoperable SIT, 
    clarify action statements, and modify the criteria for surveillance 
    requirements, do not affect the Limiting Conditions for Operations 
    (LCOs) of the SITs or the bases of the LCOs. As a result, the 
    deterministic analyses performed to establish the margin of safety 
    are unaffected. Thus, the change does not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    CT 06141-0270
        NRC Project Director: Phillip F. McKee
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, 
    Prairie Island Nuclear Generating Plant, Unit Nos. 1 and 2, Goodhue 
    County, Minnesota
    
        Date of amendment requests: May 4, 1995.
        Description of amendment requests: The proposed amendments would 
    revise the pressurizer and main steam safety valve lift setting 
    tolerances from plus or minus 1% to plus or minus 3%, revise the Safety 
    Limit curves and revise the Technical Specification Section 2 to 
    conform to Standard Technical Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated
        The proposed changes increase the ``as-found'' setpoint 
    tolerances for the Pressurizer Safety Valves and Main Steam Safety 
    Valves from [plus or minus] 1% to [plus or minus] 3%. The proposed 
    changes do not involve any hardware modifications to plant 
    structures, systems, or components. Analyses have determined that 
    the proposed changes do not significantly affect the structural 
    integrity of either the Reactor Coolant System or the Main Steam 
    system.
        The proposed setpoint tolerance of [plus or minus] 3% was 
    included in the assumptions for the performance of the reload safety 
    evaluations for the current fuel cycles, PI1-17 and PI2-16, and 
    subsequent Prairie Island fuel cycle analyses. These analyses 
    concluded that the minimum acceptable DNBR [departure from nucleate 
    boiling ratio] is maintained, over-pressure protection is 
    maintained, LOCA [loss-of-coolant accident] acceptance criteria are 
    met and offsite dose limits are not exceeded. These changes are 
    consistent with the guidance provided by Section III and XI of the 
    ASME [American Society of Mechanical Engineers] Code and Standard 
    Technical Specifications.
        The proposed change to Technical Specification Figure TS.2.1-1 
    does not affect any existing accident analyses. This revision 
    ensures that the design bases and safety limits are accurately and 
    appropriately reflected in the Technical Specifications and will 
    ensure that plant operations are properly evaluated for DNBR 
    encroachment.
        Therefore, the probability or consequences of an accident 
    previously evaluated are not affected by any of the proposed 
    amendments.
        2. The proposed amendment will not create the possibility of a 
    new of different 
    
    [[Page 47622]]
    kind of accident from any accident previously analyzed The lift 
    setpoint the Pressurizer Safety Valves and Main Steam Safety Valves 
    will be restored to [plus or minus] 1% following testing, thus the 
    ``as-left'' setpoint tolerance for the Pressurizer Safety Valves and 
    Main Steam Safety Valves are unchanged. Evaluations of plant normal 
    operation, transient and accident conditions have been performed 
    assuming these safety valve lift settings are [plus or minus] 3% of 
    the nominal setpoint and demonstrated that new or different kinds of 
    accidents are not created by the proposed changes.
        The proposed changes to Technical Specification Figure TS.2.1-1 
    do not affect the design, function or operation of any Prairie 
    Island structures, systems or components. The curves show the loci 
    of points of reactor core differential temperature (an indication of 
    thermal power), Reactor Coolant System pressure, and average 
    temperature for which the minimum DNBR is not less than the safety 
    analysis limit, that fuel centerline temperature remains below 
    melting, that the average enthalpy in the hot leg is less than or 
    equal to enthalpy of saturated liquid, or that the exit quality is 
    within the limits defined by the applicable DNBR correlation. There 
    are no new failure modes introduced by the proposed changes to the 
    Figure. The changes conservatively adjust Figure TS.2.1-1 to current 
    plant conditions and ensure that the design is accurately reflected 
    and that the plant is operated in accordance with its design bases.
        Therefore, the possibility of a new or different kind of 
    accident from any accident previously evaluated would not be created 
    [by] these amendments.
        3. The proposed amendment will not involve a significant 
    reduction in the margin of safety
        The proposed changes to the safety valve lift setting tolerances 
    are consistent with the guidance provided by Section III and XI of 
    the ASME Code and Standard Technical Specifications. Analyses have 
    demonstrated these valves will continue to perform their function of 
    protecting their respective system from over-pressurization under 
    all postulated transients and accidents. The changed setting 
    tolerances do not cause a reduction in any other safety margin such 
    as DNBR. SAFETY LIMIT curves are provided to define minimum 
    allowable safety margin for plant steady state operation, normal 
    operational transients and anticipated operational occurrences. The 
    SAFETY LIMITs represent a design requirement for establishment of 
    many of the RPS [reactor protection system] trip setpoints which 
    prevent reactor conditions from approaching the SAFETY LIMITs. The 
    proposed revision of the SAFETY LIMIT curves provide the minimum 
    safety margins with somewhat more conservatism than previously 
    included. No RPS trips setpoints are changed.
        Therefore, a significant reduction in the margin of safety would 
    not be involved with these amendments.
        Based on the evaluation described above, and pursuant to 10 CFR 
    Part 50, Section 50.91, Northern States Power Company has determined 
    that operation [of] the Prairie Island Nuclear Generating Plant in 
    accordance with the proposed license amendment request does not 
    involve any significant hazards considerations as defined by Nuclear 
    Regulatory Commission regulations in 10 CFR Part 50, Section 50.92.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, MN 
    55401
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037
        NRC Project Director: John N. Hannon
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: July 28, 1995
        Description of amendment request: The proposed amendment would 
    revise the 250 volt DC [direct current] profiles in Technical 
    Specifications Surveillance 4.8.2.1 (d) (2c) to reflect the new load 
    profile calculations.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        [Final Safety Analysis Report] FSAR Section 8.3 states that the 
    station batteries have sufficient capacity without the charger to 
    independently supply the required loads for four hours. The 
    Technical Specifications require that the batteries be surveilled to 
    dummy loads which are greater than the design loads. The load 
    profiles for the 250 VDC batteries were recalculated using discrete 
    increments of time when the loads would be in use for each of five 
    design basis events. The Technical Specification load profiles are a 
    composite of the worst case loads for the events plus margin. The 
    required ampere-hours for each battery using the new load profiles 
    is less than the ampere-hours required using the existing load 
    profiles. Therefore, since the load profiles envelop the actual 
    loads on the batteries, the change to the 250 VDC battery load 
    profiles does not involve a significant increase in the probability 
    or consequence of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        As stated above, the 250 VDC batteries have sufficient capacity 
    to power the actual battery loads thus enabling them to perform 
    their intended function. Any postulated accident resulting from this 
    change is bounded by previous analysis. Therefore, the change to the 
    250 VDC battery load profiles does not create the possibility of a 
    new or different kind of accident from any previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The Class 1E 250 VDC batteries are required to have sufficient 
    capacity and capability to ensure sufficient power is available to 
    supply the safety related equipment for (1) the safe shutdown of the 
    facilities and (2) the mitigation and control of accident conditions 
    within the facilities. The proposed load profiles envelope the worst 
    case loads plus margin.
        The ampere-hours removed from the Class 1E 250 VDC batteries are 
    less for the proposed load profiles than the existing load profiles. 
    The ampere-hours available in the batteries after the batteries have 
    supplies[d] the emergency loads for 4 hours are: [See table in 
    subject application].
        * * * * * * *
        Engineering calculation shows that the Class 1E 250 VDC 
    batteries maintain at least 210 VDC at the Class 1E 250 VDC MCCs 
    while supplying the proposed loads, corrected for temperature and 
    aging. Since the Class 1E 250 VDC circuits are designed to operate 
    properly with a minimum of 210 VDC at the Class 1E MCCs, all the 
    Class 1E emergency equipment supplied from the Class 1E batteries 
    have sufficient voltage to operate for 4 hours after the loss of ac 
    power.
        The Class 1E 250 VDC batteries and Class 1E 250 VDC battery 
    chargers have been sized using the proposed load profiles. The 
    Engineering calculation shows that the 120 cell, 12 positive plates 
    per cell battery banks are sufficient to supply the proposed load 
    profiles, corrected for temperature and aging. The same calculation 
    also shows that the Class 1E 250 VDC battery chargers have 
    sufficient capacity to re-charge the batteries from the proposed 
    emergency discharged conditions to the fully charged condition in 12 
    hours while continuing to supply the plant normal continuous loads.
        Base upon the above discussion, the proposed changes to the 
    Technical Specification load profiles do not reduce the margin of 
    safety as defined in the Technical Specifications.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and 
    
    [[Page 47623]]
    Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    Pennsylvania Power and Light Company, Docket No. 50-388, 
    Susquehanna Steam Electric Station, Unit 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: August 11, 1995
        Description of amendment request: The proposed amendment would 
    revise Susquehanna Unit 2 Technical Specification Table 3.3.7.5-1 as 
    follows:a.
        Revise Item 13, Required Number of Channels from 1 to 2;b.
        Revise Item 13, Minimum Channel Operable from 0 to 1;c.
        Delete Footnote .
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        I. This proposal does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Reestablishing the channel operability values in Item 
    13 of Technical Specification Table 3.3.7.5-1, and deleting 
    footnote , has no impact on the 
    probability or consequences of an accident previously evaluated. The 
    proposed change in the channel operability values is a return to the 
    values which were reviewed as part of the licensing basis.
        II. This proposal does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        Reestablishing the channel operability values in Item 
    13 of Technical Specification Table 3.3.7.5-1, and deleting 
    footnote , does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated. The change in the channel operability values 
    increases the required number of channels available for accident 
    monitoring. There is no correlation between increasing the number of 
    neutron flux accident monitoring channels available and the creation 
    of accident scenarios.
        III. This change does not involve a significant reduction in a 
    margin of safety.
        Reestablishing the channel operability values in Item 
    13 of Technical Specification Table 3.3.7.5-1, and deleting 
    footnote , does not involve a reduction 
    in a margin of safety. The proposed change increases the number of 
    required channels from current levels, and restores the values to 
    those which have historically been required. At the present time, 
    the number of required channels is being administratively controlled 
    at the proposed levels to ensure conservatism in operability.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, 
    Pennsylvania 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: John F. Stolz
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of amendment request: May 12, 1995
        Description of amendment request: The proposed change would extend 
    the surveillance test intervals for the emergency service water (ESW) 
    system to support 24 month operating cycles.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of the FitzPatrick plant in accordance with the 
    proposed Amendment would not involve a significant hazards 
    consideration as defined in 10 CFR 50.92 since it would not:
        1. involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes increase the interval between ESW system 
    surveillance tests. These changes are consistent with the guidance 
    provided in Generic Letter 91-04. These changes do not involve any 
    physical changes to the plant, nor do they alter the typical way the 
    ESW system functions. On-line testing will continue to assure 
    equipment availability. The type of testing and the corrective 
    actions required if the subject ESW surveillances fail remain the 
    same. As such, the proposed changes create no new impacts on 
    accidents previously evaluated.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes increase the interval between ESW system 
    surveillance tests. These changes are consistent with the guidance 
    provided in Generic Letter 91-04. The proposed changes do not change 
    the ability of the ESW system to provide heat removal for the ECCS 
    [emergency core cooling system] components and other equipment 
    essential to reactor shutdown. Past equipment performance and on-
    line testing indicate the longer test intervals will not degrade ESW 
    equipment. No changes are proposed to the type of testing performed, 
    only to the length of the surveillance interval. The proposed 
    changes do not modify the design or operation of plant equipment, 
    therefore, no new or different failure modes are introduced.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. involve a significant reduction in a margin of safety.
        The proposed changes increase the interval between ESW system 
    surveillance tests. These changes are consistent with the guidance 
    provided in Generic Letter 91-04. The proposed changes do not alter 
    the configuration of the ESW system nor change the manner in which 
    the ESW equipment functions. Past equipment performance and on-line 
    testing indicate the longer test intervals will not degrade ESW 
    equipment. Operation of the plant remains unchanged by the proposed 
    changes.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, NY 
    13126
        Attorney for licensee: Mr. Charles M. Pratt, 1633 Broadway, New 
    York, NY 10019
        NRC Project Director: Ledyard B. Marsh
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of amendment request: June 15, 1995
        Description of amendment request: The proposed change would extend 
    the surveillance test intervals for the control rod system to support 
    24 month operating cycles.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Operation of the FitzPatrick plant in accordance with the 
    proposed Amendment would not involve a significant hazards 
    consideration as defined in 10 CFR 50.92, since it would not:
    11. involve a significant increase in the probability or consequences 
    of an accident previously evaluated.
    
    [[Page 47624]]
    
        The proposed changes increase the interval between control rod 
    system surveillance tests. These changes are consistent with the 
    guidance provided in Generic Letter 91-04. These changes do not 
    involve any physical changes to the plant, nor do they alter the way 
    the control rod system functions. The type of testing and the 
    corrective actions required if the subject control rod surveillances 
    fail remain the same. As such, the proposed changes create no new 
    impacts on accidents previously evaluated.
        The reactivity margin - core loading test can be safely extended 
    to accommodate the 24 month operating cycle. The calculation of 
    reactivity margin takes into account the longer operating cycle.
        The control rod scram time test can be safely extended to 
    accommodate a 24 month operating cycle. Operating experience has 
    indicated that control rod scram times do not significantly change 
    over an operating cycle. Additional on-line testing provides 
    adequate assurance of equipment operability.
        The SDIV [Scram Discharge Instrument Volume] vent and drain 
    valve operability test can be safely extended to accommodate a 24 
    month operating cycle. Evaluation of past surveillance performance 
    and additional on-line testing assure valve operability. The 
    operability of the mode switch and the reset switch is demonstrated 
    during shutdowns.
        Therefore, the proposed changes do not involve a significant 
    increase in the probability and do not change the consequences of an 
    accident previously evaluated.
        2. create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes increase the interval between control rod 
    system surveillance tests. These changes are consistent with the 
    guidance provided in Generic Letter 91-04. The proposed changes do 
    not change the ability of the control rod system to provide rapid 
    reactivity control in order that no fuel damage results from any 
    abnormal operating transient. Past equipment performance and on-line 
    testing indicate the longer test intervals will not degrade control 
    equipment. No changes are proposed to the type of testing performed, 
    only to the surveillance interval length. The proposed changes do 
    not modify the design or operation of plant equipment, therefore, no 
    new or different failure modes are introduced.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. involve a significant reduction in a margin of safety.
        The proposed changes increase the interval between control rod 
    system surveillance tests. These changes are consistent with the 
    guidance provided in Generic Letter 91-04. The proposed changes do 
    not alter the configuration of the control rod system nor change the 
    manner in which the control rod system functions. Past equipment 
    performance and on-line testing indicate the longer test intervals 
    will not degrade control rod equipment. Operation of the plant 
    remains unchanged by the proposed changes.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, NY 
    13126
        Attorney for licensee: Mr. Charles M. Pratt, 1633 Broadway, New 
    York, NY 10019
        NRC Project Director: Ledyard B. Marsh
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of amendment request: July 21, 1995
        Description of amendment request: The proposed changes would 
    replace the title-specific list of members on the Plant Operating 
    Review Committee (PORC) with a more general statement of membership 
    requirements, similar to that used to define Safety Review Committee 
    membership; expand the scope of disciplines represented on the PORC to 
    include Nuclear Licensing and Quality Assurance; change several 
    management position titles; and, make several editorial corrections to 
    the Technical Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Replacing the title specific list of PORC members with a 
    statement of membership requirements for the committee does not 
    reduce the effectiveness of the committee to advise the Resident 
    Manager (Site Executive Officer) on matters regarding nuclear 
    safety.
        The proposed title changes for the Chief Nuclear Officer, Site 
    Executive Officer, Shift Manager, and Control Room Supervisor are 
    changes in title only and do not affect the responsibilities, 
    authority, qualification requirements, or reporting relationships of 
    these positions.
        The change proposed for Specification 6.12 is administrative in 
    nature, reflecting a change previously approved elsewhere in 
    Technical Specifications.
        The Radiological and Environmental Services Manager title change 
    proposed for Specification 6.11(A)2 is administrative in nature, 
    reflecting a change previously approved elsewhere in Technical 
    Specifications.
        The remainder of proposed changes correct grammar or improve 
    consistency in Technical Specification formatting and do not affect 
    the meaning or intent of the specifications involved.
        Operation of the James A. FitzPatrick Nuclear Power Plant in 
    accordance with the proposed amendment would not involve a 
    significant hazards consideration as defined in 10 CFR 50.92. The 
    changes are administrative in nature and would not:
        1. involve a significant increase in the probability or 
    consequences of an accident previously evaluated,
        2. create the possibility of a new or different kind of accident 
    from those previously evaluated, or
        3. involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mr. Charles M. Pratt, 1633 Broadway, New 
    York, NY 10019
        NRC Project Director: Ledyard B. Marsh
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of amendment request: July 27, 1995
        Description of amendment request: The proposed change to the 
    Technical Specifications (TS) would incorporate updated pressure vs. 
    temperature operating limit curves contained in TS Figure 3.4.6.1-1 and 
    revise TS Surveillance Requirement 4.4.6.1.3 based on implementation of 
    Regulatory Guide 1.99, Rev. 2 in accordance with Generic Letter 88-11. 
    The changes are a result of data obtained from the first set of 
    specimen capsules removed during Refueling Outage 5.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Will not involve a significant increase in the probability or 
    consequences of an accident [...] previously evaluated.
        The proposed changes assure that the existing safety limits are 
    not exceeded due to changing Reactor Vessel conditions. These 
    changes reflect the latest material testing 
    
    [[Page 47625]]
    results in accordance with 10CFR50, Appendix G. The proposed changes to 
    the pressure and temperature limits do not increase the probability 
    of nonductile failures. The proposed changes to the surveillance 
    requirement and the associated changes to the Bases to include a 
    commitment to the methodology of Regulatory Guide 1.99, Rev. 2 
    ensures that the most limiting Reactor Vessel material is used in 
    the determination of the pressure-temperature operating limits.
        Therefore, it may be concluded that the proposed changes do not 
    involve a significant increase in the probability or consequences of 
    an accident or malfunction of equipment important to safety 
    previously evaluated.
        2. Will not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        No physical plant modifications or new operating configurations 
    result from these changes. These changes do not adversely affect the 
    design or operation of any system or component important to safety, 
    rather they establish limits to assure that operations remain within 
    acceptable safety boundaries.
        Therefore, the possibility of a new or different kind of 
    accident from any previously evaluated will not be created.
        3. Will not involve a significant reduction in a margin of 
    safety. Analysis of the capsule specimens has concluded that the 
    Reactor Vessel has sufficient fracture toughness for continued safe 
    operation, provided that operation remains within acceptable 
    pressure-temperature limits. The revised pressure-temperature curves 
    define these acceptable pressure-temperature limits during plant 
    operation. The proposed changes maintain the existing margins of 
    safety by modifying the operating limits based on the most limiting 
    of the actual reference temperature shifts. This new limit 
    considered analytical results of the capsule specimens, or a 
    predicted shift considering the most limiting pressure vessel 
    material. Changes to the Surveillance Requirement criteria and the 
    associated Bases to include a commitment to the methodology 
    contained in Regulatory Guide 1.99, Rev. 2 will ensure that the most 
    limiting plate or beltline weld material will be utilized in the 
    determination of the pressure-temperature limits.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070
        Attorney for licensee: M. J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502
        NRC Project Director: John F. Stolz
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of amendment requests: August 1, 1995
        Description of amendment requests: The amendment request proposes 
    to change Technical Specification (TS) 3/4.3.2, Table 3.3-3, 
    ``Engineered Safety Features Actuation System Instrumentation.'' TS 3/
    4.3.2 includes the requirements for the minimum number of toxic gas 
    isolation system (TGIS) trains operable. The TS change request is to 
    extend the allowed TGIS outage times during replacement of TGIS 
    instrumentation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The Toxic Gas Isolation System (TGIS) is designed to monitor and 
    mitigate the effects of toxic gas releases on control room 
    habitability. TGIS unavailability is not a precursor to any accident 
    previously evaluated in Chapter 15 of the San Onofre Updated Final 
    Safety Analysis Report (UFSAR). A risk assessment of the TGIS 
    instrumentation replacement activity was performed and found that 
    the likelihood of a loss of control room habitability beyond that 
    permitted by the Technical Specifications (TS) will not exceed 1E-6 
    over the duration of this TS change. In addition, a loss of control 
    room habitability does not necessarily lead to an accident or core 
    damage event. However, if a loss of control room habitability was 
    conservatively assumed to lead to a core damage event, this increase 
    in risk would still not constitute a significant increase in the 
    consequences or probability of any accident previously evaluated 
    since the increase is less than 3% of the average annual core damage 
    risk from internal events as reported in the San Onofre Individual 
    Plant Examination. Therefore, operation of the facility in 
    accordance with this proposed change does not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        This change extends the allowed outage times of the TGIS system. 
    The change does not affect the design or operation of any other 
    plant systems. An increase in TGIS unavailability is not a precursor 
    to any accident previously evaluated in Chapter 15 of the San Onofre 
    UFSAR. Therefore, operation of the facility in accordance with this 
    proposed change does not create the possibility of a new or 
    different kind of accident from any previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        During replacement of TGIS instrumentation a single channel of 
    TGIS will be maintained operable except during periods when 
    construction activity may result in spurious TGIS alarms. During 
    these periods the control room will normally be isolated except for 
    brief periods when the control room will be open to allow for air 
    exchange or to allow for CREACUS equipment repair. These periods, 
    when the control room is open without a TGIS channel available, will 
    not exceed 54 hours during the entire period when this change is in 
    effect. Operation with control room ventilation in the normal mode 
    with a single channel of TGIS operable for 44 days and no TGIS 
    channel available for up to 54 hours has been analyzed, and results 
    in an increase in the probability of a loss of control room 
    habitability which does not exceed 1E-6 over the duration of this TS 
    change. Therefore, this proposed change does not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, CA 92713
        Attorney for licensee: T. E. Oubre, Esquire, Southern California 
    Edison Company, P. O. Box 800, Rosemead, CA 91770
        NRC Project Director: William H. Bateman
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
    
    [[Page 47626]]
    
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of application for amendment: October 24, 1994, as 
    supplemented July 21, 1995. The July 21, 1995, letter provides 
    clarification information and did not change the scope of the October 
    24, 1994, letter, or the initial no significant hazards consideration 
    determination.
        Brief description of amendment: The proposed amendment would revise 
    the TS to allow the relocation of TS 3/4.3.7.12, Area Temperature 
    Monitoring; and the associated Bases in the TS to licensee-controlled 
    documents.
        Date of issuance: August 28, 1995
        Effective date:  August 28, 1995
        Amendment No.: 62
        Facility Operating License No. NPF-63. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 23, 1994 (59 
    FR 60379) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 28, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, NC 27605
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: May 18, 1995, as supplemented 
    May 31, 1995
        Brief description of amendments: The amendments revise the 
    frequency for conducting the Catawba Unit 2 Integrated Leak Rate Test 
    (ILRT) from a nominal frequency of once per 40 months to less than or 
    equal to 70 months. This also involves the granting of an exemption 
    from the requirements of 10 CFR Part 50, Appendix J, which is addressed 
    by separate correspondence.
        Date of issuance: August 18, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days from the date of issuance.
        Amendment Nos.: 133 and 127
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 21, 1995 (60 FR 
    32362) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 18, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location:  York County Library, 138 East 
    Black Street, Rock Hill, SC 29730
    
    Duquesne Light Company, et al., Docket No. 50-412, Beaver Valley 
    Power Station, Unit 2, Shippingport, Pennsylvania
    
        Date of application for amendment:  April 26, 1995
        Brief description of amendment: This amendment adds a requirement 
    to Technical Specification (TS) 4.5.2.a to periodically verify that the 
    High Head Safety Injection (HHSI) pump minimum flow valve, 2CHS*MOV373, 
    is maintained open during plant operation in Modes 1, 2, and 3. Valve 
    2CHS*MOV373, must be maintained open to provide a minimum flowpath for 
    the HHSI pumps thereby minimizing the likelihood of HHSI pump damage 
    due to pump operation with insufficient flow. The amendment allows 
    flexibility for local verification of valve position or flow indication 
    if the control room indication is not available. Several editorial 
    changes to TS 3/4.5.2 are also being made to provide consistent format 
    with other TSs.
        Date of issuance: August 25, 1995
        Effective date: August 25, 1995
        Amendment No.: 73
        Facility Operating License No. NPF-73: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 6, 1995 (60 FR 
    29874). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 25, 1995. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket No. 
    50-366, Edwin I. Hatch Nuclear Plant, Unit 2, Appling County, 
    Georgia
    
        Date of application for amendment: April 14, 1995, as supplemented 
    by letters dated June 22 and July 18, 1995
        Brief description of amendment: The amendment eliminates response 
    time testing (RTT) requirements for selected sensors and specific loop 
    instrumentations for (1) the Reactor Protection System (RPS), (2) the 
    Isolation System, and (3) the Emergency Core Cooling System (ECCS). In 
    addition, the Note for Surveillance Requirement 3.3.6.1.7, which reads: 
    ``Radiation detectors may be excluded,'' is being removed since RTT is 
    not required for any radiation detector that provides a primary 
    containment isolation signal as indicated in Table 3.3.6.1-1 of the TS.
        Date of issuance: August 23, 1995
        Effective date: As of the date of issuance to be implemented within 
    60 days from the date of issuance
        Amendment No.: 137
        Facility Operating License No. NPF-5: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 5, 1995 (60 FR 
    35076) The June 22 and July 18, 1995, letters provided clarifying 
    information that did not change the scope of the April 14, 1995, 
    application and initial proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated August 23, 1995.No significant hazards 
    consideration comments received: No
        Local Public Document Room location: Appling County Public Library, 
    301 City Hall Drive, Baxley, GA 31513 
    
    [[Page 47627]]
    
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-424 and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, 
    Burke County, Georgia
    
        Date of application for amendments:  January 3, 1995, as 
    supplemented by letters dated June 14 and July 6, 1995.
        Brief description of amendments: The amendments revise the 
    Technical Specifications (TS) with editorial changes to the Action 
    Statements of TS 3.8.1.1 and 3.8.1.2 in order to reflect the 
    availability of a third offsite ac electrical source. Technical 
    Specification 4.8.1.1.1 is clarified to specify that the offsite ac 
    circuits connected to the onsite Class 1E distribution system are 
    required to be verified OPERABLE. A footnote is added to TS 3.8.3.1 to 
    allow the connection of the third offsite ac source to the onsite 
    busses.
        Date of issuance:  August 29, 1995
        Effective date:  As of the date of issuance to be implemented 
    within 30 days from the date of issuance
        Amendment Nos.:  90 and 68
        Facility Operating License Nos. NPF-68 and NPF-81: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 1, 1995 (60 FR 
    6301) The June 14 and July 6, 1995, letters provided clarifying 
    information that did not change the scope of the January 3, 1995, 
    application and initial proposed no significant hazards consideration 
    determination. The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 29, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location:  Burke County Library, 412 
    Fourth Street, Waynesboro, GA 30830
    
    Florida Power and Light Company, Docket Nos. 50-250 and 50-251, 
    Turkey Point Plant Units 3 and 4, Dade County, Florida
    
        Date of application for amendments:  May 23, 1995
        Brief description of amendments: The amendments revise the column 
    format for the Reactor Protection System and Engineered Safety Feature 
    Actuation System Setpoints
        Date of issuance: August 24, 1995
        Effective date: August 24, 1995
        Amendment Nos.: 176 and 170Facility Operating Licenses Nos. DPR-31 
    and DPR-41: Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: June 21, 1995 (60 FR 
    32364) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 24, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Florida International 
    University, University Park, Miami, FL 33199
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments: December 20, 1993, as 
    supplemented July 19, 1994, and February 28, 1995.
        Brief description of amendments: The amendments revise the 
    surveillance requirements and load profiles for A, B, and N Train 
    batteries.
        Date of issuance: August 22, 1995
        Effective date: August 22, 1995
        Amendment Nos.: 198 and 183
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 2, 1994 (59 FR 
    4939) and June 6, 1995 (60 FR 29879) The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    August 22, 1995.No significant hazards consideration comments received: 
    No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments: May 25, 1995, and supplemented 
    June 30, 1995
        Brief description of amendments: The amendments allow fuel 
    reconstitution when analyzed in accordance with NRC-approved 
    methodologies. The amendments are line item improvements based on NRC 
    Generic Letter 90-02, ``Alternative Requirements for Fuel Assemblies in 
    Design Features Section of Technical Specifications,'' supplement 1.
        Date of issuance: August 22, 1995
        Effective date: August 22, 1995
        Amendment Nos.: 199 and 184
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 5, 1995 (60 FR 
    35081) The June 30, 1995, supplement provided a minor revision to the 
    proposed Technical Specification pages which was within the scope of 
    the original application and did not change the staff's initial 
    proposed no significant hazards considerations determination. The 
    Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated August 22, 1995.No significant hazards 
    consideration comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine
    
        Date of application for amendment: February 14, 1995
        Brief description of amendment: This amendment makes the following 
    administrative changes to the Maine Yankee (MY) Technical 
    Specifications (TS):
        a. Removes responsibility for audits of the emergency and security 
    plans--including their implementing procedures--from the TS and assigns 
    that responsibility to the emergency and security plans,
        b. Assigns review responsibility for significant, accidental, 
    unplanned, or uncontrolled radioactive releases to the Nuclear Safety 
    Audit and Review (NSAR) Committee,
        c. Assigns additional reporting requirements to the NSAR Committee, 
    and
        d. Provides the President of MY with the authority to initiate an 
    audit of any area of facility operation.
        Date of issuance: August 22, 1995
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment No.: 152
        Facility Operating License No. DPR-36: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 29, 1995 (60 FR 
    16191) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 22, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, ME 04578
    
    Northeast Nuclear Energy Company, Docket No. 50-245, Millstone 
    Nuclear Power Station, Unit 1, New London County, Connecticut
    
        Date of application for amendment:  May 18, 1995
        Brief description of amendment: The amendment revises the minimum 
    temperature at which the reactor vessel head bolting studs are allowed 
    to be 
    
    [[Page 47628]]
    placed under tension. In addition, the amendment revises the minimum 
    reactor vessel metal temperature during core critical operation, 
    revises the minimum reactor vessel metal temperature for pressure 
    tests, makes editorial changes, and revises the Bases for the 
    applicable section.
        Date of issuance:  August 23, 1995
        Effective date:  As of the date of issuance to be implemented 
    immediately.
        Amendment No.:  85
        Facility Operating License No. DPR-21. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 21, 1995 (60 FR 
    32369) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 23, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location:  Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360
    
    Northeast Nuclear Energy Company, Docket No. 50-245, Millstone 
    Nuclear Power Station, Unit 1, New London County, Connecticut
    
        Date of application for amendment: June 15, 1995
        Brief description of amendment: The amendment changes the 
    definition for an alteration of the reactor core to one that is 
    consistent with the intent of the improved standard technical 
    specifications. The amendment also makes administrative changes to 
    several technical specification pages.
        Date of issuance: August 28, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 86
        Facility Operating License No. DPR-21. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 19, 1995 (60 FR 
    37097) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 28, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: April 28, 1995, as supplemented 
    August 2, 1995.
        Brief description of amendment: The amendment changes Technical 
    Specification (TS) Sections 3.7.5, 4.7.5, and 3/4.7.5, to permit 
    Millstone Unit 3 to remain in operation with the average ultimate heat 
    sink water temperature greater than 75* F (but less than or equal to 
    77* F) for a period of 12 hours.
        Date of issuance: August 28, 1995
        Effective date:  As of the date of issuance.
        Amendment No.: 119
        Facility Operating License No. NPF-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 6, 1995 (60 FR 
    29881). The information in the licensee's submittal of August 2, 1995, 
    did not require a change to the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated August 28, 1995.No 
    significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of application for amendments: June 29, 1995
        Brief description of amendments: The amendments revise the combined 
    Technical Specifications (TS) for Diablo Canyon Nuclear Power Plant, 
    Unit Nos. 1 and 2 (DCPP) to add Mode 1 applicability to TS 3/4.4.2.2, 
    ``Safety Valves - Operating,'' and changes the low-temperature 
    overpressure protection (LTOP) system enable temperature for Mode 4 
    applicability from 323 degrees F to 270 degrees F in TS 3/4.3.2.1, 
    ``Safety Valves - Shutdown.''
        Date of issuance: August 23, 1995
        Effective date: August 23, 1995
        Amendment Nos.: Unit 1 - Amendment No. 107; Unit 2 - Amendment No. 
    106
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 19, 1995 (60 FR 
    37098) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 23, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, CA 93407
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of application for amendments: February 1, 1995, as 
    supplemented by letter dated June 20, 1995
        Brief description of amendments: The requested changes would modify 
    the applicable operational conditions for the secondary containment 
    isolation radiation monitors located on the refueling floor and for the 
    monitor located in the railroad access shaft.
        Date of issuance: August 24, 1995
        Effective date: Both units, as of the date of issuance and is to be 
    implemented within 30 days
        Amendment Nos.: 152 and 122
        Facility Operating License Nos. NPF-14 and NPF-22. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 29, 1995 (60 FR 
    16192). The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 24, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Osterhout Free Library, 
    Reference Department, 71 South Franklin Street, Wilkes-Barre, PA 18701
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments:  August 31, 1994, as 
    supplemented by letters dated May 11, and July 3, 1995
        Brief description of amendments: This amendment revises the 
    Technical Specifications to permit the relocation of the Turbine 
    Overspeed Protection System to the Updated Final Safety Analysis Report 
    and Controlled Plant Procedures.
        Date of issuance: August 24, 1995
        Effective date: August 24, 1995
        Amendment Nos.: 100 and 64
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 9, 1994 (59 FR 
    55884) The supplemental letters do not 
    
    [[Page 47629]]
    change the initial no significant hazards consideration determination 
    nor the initial Federal Register notice. The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    August 24, 1995.No significant hazards consideration comments received: 
    No
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments:  February 22, 1995
        Brief description of amendments: The amendments revise the 
    Technical Specifications Surveillance Requirements to clarify the 
    Emergency Diesel Generator acceptable steady state voltage range.
        Date of issuance: August 24, 1995
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days of issuance.
        Amendment Nos.: 101 and 65
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 26, 1995 (60 FR 
    20525) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 24, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment:  January 13, 1995
        Brief description of amendment: The amendment revised the 
    Administrative Controls Section (6.0) of the Technical Specifications 
    for Hope Creek Generating Station to reflect organizational changes and 
    resultant management title changes.
        Date of issuance: August 22, 1995
        Effective date: August 22, 1995
        Amendment No.: 77
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 21, 1995 (60 FR 
    32371) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 22, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments:  December 23, 1994
        Brief description of amendments: The amendments to the Technical 
    Specifications revise the surveillance requirement to perform a visual 
    inspection of containment areas affected by containment entry when 
    containment integrity is established. They are consistent with Item 7.5 
    of Generic Letter 93-05, ``Line-Item Technical Specifications 
    Improvements to Reduce Surveillance Requirements for Testing During 
    Power Operation.''
        Date of issuance: August 24, 1995
        Effective date: As of the date of issuance, to be implementd within 
    60 days.
        Amendment Nos.: 174 and 155
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 1, 1995 (60 FR 
    6308) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 24, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of application for amendments: September 16, 1994
        Brief description of amendments: These amendments revise Technical 
    Specification (TS) 3/4.2.1, ``Linear Heat Rate.'' The linear heat rate 
    (LHR) limit for steady state operation is revised from 13.9 kw/ft to 
    13.0 kw/ft. The Bases for TS 3/4.2.1, ``Linear Heat Rate,'' is also 
    being revised to reflect the new value.
        Date of issuance: August 23, 1995
        Effective date: August 23, 1995, to be implemented within 30 days 
    of issuance.
        Amendment Nos.: Unit 2 - Amendment No. 124; Unit 3 - Amendment No. 
    113
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 9, 1994 (59 FR 
    55892) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 23, 1995. No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, CA 92713
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments:  May 3, 1995
        Brief description of amendments: The amendments delay 
    implementation of Amendment Nos. 182 and 174 until implementation 
    problems are addressed. These changes revise the setpoints and time 
    delays for the auxiliary feedwater loss of power and the 6.9 kv 
    shutdown board loss of voltage and degraded voltage instrumentation.
        Date of issuance: August 22, 1995
        Effective date: August 22, 1995
        Amendment Nos.: 207 and 197
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: May 23, 1995 (60 FR 
    27343) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 22, 1995.No significant 
    hazards consideration comments received: None
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, TN 37402
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: April 6, 1995 (TS 94-18)
        Brief description of amendments: The amendments revise Surveillance 
    Requirement 4.0.5 by replacing the current Inservice Inspection program 
    and the Inservice Testing program requirements with the requirements 
    stated in the Standard Technical Specifications (NUREG-1431). The 
    amendments also delete Technical Specification 3/4.4.10, ``Structural 
    Integrity ASME Code Class 1, 2 and 3 Components,'' and its related 
    Bases information.
        Date of issuance: August 22, 1995
        Effective date: August 22, 1995
        Amendment Nos.: 208 and 198
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: April 26, 1995 (60 FR 
    20528) 
    
    [[Page 47630]]
    The Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated August 22, 1995.No significant hazards 
    consideration comments received: None
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, TN 37402
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application for amendment: April 17, 1995, as supplemented 
    on June 30, 1995
        Brief description of amendment: The amendment revises Technical 
    Specifications Technical Specification 2.2.1, Table 2.2-1. The changes 
    address reducing repeated alarms and partial reactor trips by revising 
    the Overpower Delta-T setpoint function.
        Date of issuance: August 21, 1995
        Effective date: Immediately, to be implemented within 30 days.
        Amendment No.: 102
        Facility Operating License No. NPF-30. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 10, 1995 (60 FR 
    24922). The June 30, 1995, letter provided supplemental information 
    that did not change the initial proposed no significant hazards 
    consideration determination.The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated August 21, 1995. No 
    significant hazards consideration comments received: No.
        Local Public Document Room location:  Callaway County Public 
    Library, 710 Court Street, Fulton, MO 65251
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: September 2, 1992
        Brief description of amendment: The amendment revises the required 
    signal-to-noise ratio for the source range monitors, as recommended by 
    General Electric.
        Date of issuance: August 23, 1995
        Effective date: August 23, 1995
        Amendment No.: 140
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 19, 1995 (60 FR 
    37101) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 23, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, WA 99352
        Dated at Rockville, Maryland, this 6th day of September 1995.
        For the Nuclear Regulatory Commission
    Jack W. Roe,
    Director, Division of Reactor Projects - III/IV Office of Nuclear 
    Reactor Regulation.
    [Doc. 95-22616 Filed 9-12-95; 8:45 am]
    BILLING CODE 7590-01-F
    
    

Document Information

Published:
09/13/1995
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
95-22616
Dates:
August 28, 1995
Pages:
47613-47630 (18 pages)
PDF File:
95-22616.pdf