X94-10914. Biweekly Notice  

  • [Federal Register Volume 59, Number 177 (Wednesday, September 14, 1994)]
    [Unknown Section]
    [Page 0]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X94-10914]
    
    
    [[Page Unknown]]
    
    [Federal Register: September 14, 1994]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
     
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating LicensesInvolving 
    No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from August 22, 1994 through September 1, 1994. 
    The last biweekly notice was published on August 31, 1994 (59 FR 
    45015).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC 
    20555. The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By October 14, 1994, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC 20555 and at the local 
    public document room for the particular facility involved. If a request 
    for a hearing or petition for leave to intervene is filed by the above 
    date, the Commission or an Atomic Safety and Licensing Board, 
    designated by the Commission or by the Chairman of the Atomic Safety 
    and Licensing Board Panel, will rule on the request and/or petition; 
    and the Secretary or the designated Atomic Safety and Licensing Board 
    will issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    room for the particular facility involved.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of amendments request: August 2, 1994
        Description of amendments request: The proposed amendment would 
    revise Technical Specifications (TSs) 3.9.1 and 3.1.2.7 and the Bases 
    to Specification 3.1.2.7. Specifically, TS 3.9.1, ``Refueling 
    Operations, Boron Concentration,'' would be revised to require action 
    to restore boron concentration to within its limits in place of the 
    current requirement to initiate and continue boration at a rate greater 
    than or equal to 40 gpm of 2300 ppm boric acid solution or its 
    equivalent until the boron concentration is within its limit. TS 
    3.1.2.7, ``Borated Water Sources - Shutdown,'' gives the operability 
    requirement for borated water sources including the Refueling Water 
    Tank (RWT), in Modes 5 and 6. The minimum boron concentration is given 
    as 2300 ppm. While this minimum value is correct for Mode 5, a larger 
    boron concentration may be necessary in Mode 6. The RWT is the 
    preferred borated water source for restoring the required boron 
    concentration as required by TS 3.9.1. Therefore, the RWT boron 
    concentration in Mode 6 should be at least be that required by TS 
    3.9.1. The proposed change to TS 3.1.2.7 would clarify the boron 
    concentration requirements. In Mode 5, 2300 ppm will continue to be 
    required. In Mode 6, the boron concentration limit for the RWT will be 
    the boron concentration limits given in TS 3.9.1.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        During refueling operations, the reactivity condition of the 
    core is maintained consistent with the initial conditions assumed 
    for the boron dilution event in the accident analysis (Updated Final 
    Safety Analysis Report Section 14.3) and is sufficient to ensure the 
    core remains subcritical during core alterations. Technical 
    Specification 3.9.1 requires that the boron concentration be 
    maintained to ensure a keff [is less than or equal to] 0.95. 
    Should the boron concentration drop below the Technical 
    Specifications limit, the Action requires boration at a specified 
    flow rate and boron concentration until the boron concentration is 
    restored to within its limit. Refueling boron concentrations higher 
    than the concentration specified by the Action in [Technical] 
    Specification 3.9.1 are allowed by the Technical Specifications and 
    clarification of the Action for that circumstance is needed. The 
    proposed change eliminates the specified flow rate and boron 
    concentration in the Action and substitutes a directive to 
    immediately initiate action to restore the boron concentration to 
    within its limits. The accident analysis does not assume a specific 
    boration rate, but only assumes that the operator acts to terminate 
    the dilution.
        Therefore, the consequences of the event are unchanged. In 
    addition, the proposed change revises the boron concentration limit 
    on the Refueling Water Tank in Mode 6 to make the boron 
    concentration limit on the tank the same as the boron concentration 
    limit on the reactor coolant system. This will ensure that the RWT 
    will contain water of a sufficient boron concentration to respond to 
    a boron dilution event.
        The proposed change does not change the boron concentration or 
    shutdown margin required by [Technical] Specification 3.9.1 and 
    continues to meet the initial conditions of the boron dilution 
    event. Therefore, the probability of a boron dilution event is not 
    increased. Furthermore, the revised action ensures that the 
    appropriate actions for a boron dilution event will be taken and 
    that a borated water source of sufficient concentration is available 
    to respond to that event. Therefore, the consequences of a boron 
    dilution event are not increased.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated.
        The proposed change does not represent a significant change in 
    the configuration or operation of the plant. The proposed actions 
    will results in the same operator actions as the current Technical 
    Specifications. The minimum boron concentration of the Refueling 
    Water Tank in Mode 6 may be increased above the current value, but 
    the concentrations will be within the analyzed maximum concentration 
    for that tank,
        Therefore, the proposed change does not create the possibility 
    of a new or different type of accident from any accident previously 
    evaluated.
        3. Would not involve a significant reduction in a margin of 
    safety.
        The margin of safety provided by [Technical] Specification 3.9.1 
    is to ensure that the core remains subcritical during a boron 
    dilution event and during core alterations. The proposed change does 
    not alter the required shutdown margin or significantly change the 
    actions to be taken if that shutdown margin is lost. The proposed 
    change ensures that all assumed borated water sources will have 
    sufficient boron concentration to respond to boron dilution event.
        Therefore, the proposed change does not involve a significant 
    reducation in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Michael J. Case
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of amendments request: August 2, 1994
        Description of amendments request:  The proposed change would 
    revise Technical Specifications (TSs) regarding surveillances 
    associated with the Emergency Diesel Generators (EDGs). Specifically, 
    TS 4.8.1.1.2.d.3.c would be revised to add high crankcase pressure to 
    the EDG trips which are verified to be automatically bypassed on a 
    Safety Injection Actuation Signal (SIAS). In addition, a footnote would 
    be added stating that verification of the high crankcase pressure trip 
    bypass will not be required on a particular EDG until the modification 
    has been completed for that EDG.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The Calvert Cliffs Emergency Diesel Generators (EDGs) are used 
    to provide electrical power for the operation of Engineered Safety 
    Features (ESF) and safe shutdown equipment for events involving a 
    loss of offsite power. The EDGs are also called upon to 
    automatically start if an accident condition (SIAS) is present. In 
    the event of an automatic start from a SIAS, the EDGs do not assume 
    any load until the preferred, offsite power source is actually lost. 
    On an undervoltage condition on a vital bus, the corresponding EDGs 
    automatically start and load.
        Emergency diesel generator trips are provided to initiate engine 
    shutdown during abnormal diesel-run conditions, thereby protecting 
    the EDGs from any resulting damage. Under emergency conditions, EDG 
    reliability is a key accident-mitigating factor; therefore, upon 
    receipt of a SIAS, the EDG control logic blocks two of the normal 
    shutdown signals so that the only signals remaining are those 
    required to prevent rapid destruction of the diesel engine. High 
    crankcase pressure is typically not an indication of impending rapid 
    diesel engine failure; therefore, this trip will be added to those 
    shutdown signals bypassed on a SIAS. The proposed Technical 
    Specification change adds the high crankcase pressure trip as one of 
    the EDG trips verified to be bypassed by a SIAS. A high crankcase 
    pressure condition on one EDG will not impact either of the two 
    unaffected EDGs, or any other equipment required to mitigate 
    accident consequences, and satisfies the single failure criteria. 
    The manufacturer concurs with the proposed change to bypass this 
    trip on a SIAS. In blocking this trip on a SIAS, the ultimate effect 
    is an increase in the reliability of the effected EDG, and 
    therefore, no increase in the consequences of a previously evaluated 
    accident.
        Additionally, the EDGs are not initiators to any previously 
    evaluated accident. Therefore, blocking the high crankcase pressure 
    trip on a SIAS will not increase the probability of an accident 
    previously evaluated.
        Therefore, the proposed change does not involve a significant 
    increase to the probability or consequences of an accident 
    previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated.
        The function of the EDGs is to provide power to ESF and safe 
    shutdown equipment for events involving a loss of offsite power. The 
    proposed change does not represent a significant change in the 
    configuration or operation of the plant; therefore, the EDGs 
    continue to function in an accident mitigation role. The EDGs are 
    not accident precursors, either in the current configuration, or 
    following the modification to block the high crankcase pressure 
    trip.
        Therefore, the proposed changes do not create the possibility of 
    a new or different type of accident from any accident previously 
    evaluated.
        3. Would not involve a significant reduction in a margin of 
    safety.
        The margin of safety credited with the EDG function associated 
    with this change is the reliability of the EDGs following an event 
    involving a loss of offsite power. By blocking high crankcase 
    pressure trips on a SIAS, this change increases the likelihood that 
    an EDG will be able to supply power when it is needed most, during a 
    SIAS, because the probability of an unnecessary EDG shutdown is 
    decreased. In effect, the margin of safety associated with this 
    function, EDG reliability, is increased.
        Therefore, the proposed change does not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Michael J. Case
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of amendments request: August 4, 1994
        Description of amendments request: The proposed amendment would 
    eliminate Technical Specifications 3/4.3.3.3, 6.9.2.b, and 6.9.2.d and 
    Bases 3/4.3.3.3 which gives requirements for seismic monitoring 
    instrumentation. Specifically, the requirements for operation and 
    testing of the seismic monitoring instrumentation would be relocated to 
    the Calvert Cliffs Nuclear Power Plant Updated Final Safety Analysis 
    Report (UFSAR) and plant procedures.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change has been evaluated against the standards in 
    10 CFR 50.92 and has been determined to not involve a significant 
    hazards consideration, in that operation of the facility in 
    accordance with the proposed amendments:
        1. Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The seismic monitoring system is used to measure the seismic 
    response of selected Class 1 structures, provide time-history 
    records of seismic events, and would indicate if predetermined 
    seismic acceleration values had been exceeded. The seismic 
    monitoring system itself has no safety function. The system measures 
    values which are used after the fact to assess the intensity of an 
    earthquake.
        The proposed change will relocate requirements regarding the 
    operability and testing of the seismic monitors from the Technical 
    Specifications to the UFSAR and plant procedures. This will allow 
    changes to the requirements to be made without Commission approval 
    as long as the changes meet the criteria of 10 CFR 50.59. Associated 
    Technical Specification Special Report requirements and Bases will 
    be deleted. Changes to the seismic monitoring system requirements 
    which do not meet the criteria of 10 CFR 50.59 must be approved by 
    the Commission by license amendment.
        The seismic monitoring system is not an initiator and does not 
    act to minimize the consequences of any accident previously 
    evaluated. Therefore, the proposed change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated?
        The proposed relocation of seismic monitor requirements from the 
    Technical Specifications to the UFSAR and plant procedures does not 
    represent a change in the configuration or operation of the plant. 
    The seismic monitoring system will continue to be controlled under 
    10 CFR 50.59. Associated Technical Specification Special Report 
    requirements and Bases will be deleted. The proposed change will not 
    add any new hardware and will not introduce any new accident 
    initiators. Therefore, the proposed change does not create the 
    possibility of a new or different type of accident from any accident 
    previously evaluated.
        3. Does operation of the facility in accordance with the 
    proposed amendment involve a significant reduction in a margin of 
    safety?
        The seismic monitoring system is used to measure the response of 
    selected Class 1 structures to seismic events. The plant is designed 
    to withstand the loads imposed by the maximum hypothetical accident 
    and the design seismic disturbance without loss of functions 
    required for reactor shutdown and emergency core cooling. As a 
    consequence, the seismic monitoring system makes no contribution to 
    the margin of safety, and neither do the associated special reports.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Michael J. Case
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: July 18, 1994
        Description of amendment request: The purpose of the proposed 
    amendment is to separate the Technical Specification (TS) into two 
    separate volumes, one volume explicitly for Unit 1 and one volume 
    explicitly for Unit 2. At present, each unit has a single volume of TS 
    which contains the specifications covering both units. In anticipation 
    of the steam generator (SG) replacement project scheduled to begin in 
    the fall of 1994, the licensee is requesting that the TS reflect unit 
    specific data. Since the SG project outlines a schedule for single 
    units, the present documentation reflecting both units in one volume 
    will make it difficult to facilitate TS changes to a single unit. The 
    proposed TS will modify the current situation as follows:1) The pages 
    will now contain the same information as found before with the 
    exception of references to different units. The Unit 1 volume will only 
    contain parameter and setpoint values applicable to Unit 1; the Unit 2 
    volume will only contain information applicable to Unit 2.2) The limits 
    established by the TS (the definitions, the limiting conditions for 
    operation, the surveillance requirements, the Bases, etc.) will be 
    unchanged by this amendment, with the exception of (3) below. The 
    effect of the amendment will be that the Unit 1 TS will be found only 
    in the volume dedicated solely to Unit 1 and likewise for Unit 2. 3) TS 
    Sections 3.0.5 and 4.0.6 will be deleted and minor editorial changes, 
    such as the correction of misspellings and the deletion of obsolete 
    footnotes, will be made. TS 3.0.5 and 4.0.6 define the applicability of 
    the current joint TS volume to each unit individually. Since each 
    unit's TS will be located in a separate volume, no statements are 
    necessary to indicate differences in parameters between units and TS 
    3.0.5 and 4.0.6 may be deleted.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed amendments would not involve a significant increase 
    in the probability or consequences of a previously evaluated 
    accident. The separation of the existing technical specification 
    manual into unit-specific volumes is a strictly administrative 
    process which will not affect the probability or consequence of any 
    accident.
        They will not create the possibility of a new or different kind 
    of accident from any accident previously evaluated. The changes do 
    not have any impact upon the design or operation of plant equipment; 
    therefore, they cannot serve to initiate a new type of accident.
        The proposed amendments would not involve a reduction in a 
    margin of safety. The changes would not impact the design or 
    operation of any plant systems or components.
        Based upon the preceding analysis, Duke Power Company concludes 
    that the proposed amendments do not involve a significant hazards 
    consideration as defined by 10 CFR 50.92.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: York County Library, 138 East Black 
    Street, Rock Hill, South Carolina 29730
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of amendment request: July 18, 1994
        Description of amendment request: The purpose of the proposed 
    amendment is to separate the Technical Specifications (TS) into two 
    separate volumes, one volume explicitly for Unit 1 and one volume 
    explicitly for Unit 2. At present, each unit has a single volume of TS 
    which contains the specifications covering both units. In anticipation 
    of the steam generator (SG) replacement project scheduled to begin in 
    the fall of 1994, the licensee is requesting that the TS reflect unit 
    specific data. Since the SG project schedules SG replacement for each 
    unit at different times, the present common TS would make it difficult 
    to facilitate TS changes to a single unit. The proposed amendment will 
    modify the current TS as follows:1) The pages will now contain the same 
    information as found before with the exception of references to 
    different units. The Unit 1 volume will only contain parameter and 
    setpoint values applicable to Unit 1; the Unit 2 volume will only 
    contain information applicable to Unit 2.2) The limits established by 
    the TS (the definitions, the limiting conditions for operation, the 
    surveillance requirements, the Bases, etc.) will be unchanged by this 
    amendment, with the exception of (3) below. The effect of the amendment 
    will be that the Unit 1 TS will be found only in the volume dedicated 
    solely to Unit 1 and likewise for Unit 2.3) TS Sections 3.0.5 and 4.0.6 
    will be deleted and minor editorial changes, such as the correction of 
    misspellings and the deletion of obsolete footnotes, will be made. TS 
    3.0.5 and 4.0.6 define the applicability of the current joint TS volume 
    to each unit individually. Since each unit's TS will be located in a 
    separate volume, no statements are necessary to indicate differences in 
    parameters between units and TS 3.0.5 and 4.0.6 may be deleted.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed amendments would not involve a significant increase 
    in the probability or consequences of a previously evaluated 
    accident. The separation of the existing technical specification 
    manual into unit-specific volumes is a strictly administrative 
    process which will not affect the probability or consequence of any 
    accident.
        They will not create the possibility of a new or different kind 
    of accident from any accident previously evaluated. The changes do 
    not have any impact upon the design or operation of plant equipment; 
    therefore, they cannot serve to initiate a new type of accident.
        The proposed amendments would not involve a reduction in a 
    margin of safety. The changes would not impact the design or 
    operation of any plant systems or components.
        Based upon the preceding analysis, Duke Power Company concludes 
    that the proposed amendments do not involve a significant hazards 
    consideration as defined by 10 CFR 50.92.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: Atkins Library, University of North 
    Carolina, Charlotte (UNCC Station), North Carolina 28223
    
    Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf 
    Nuclear Station, Unit 1, Claiborne County, Mississippi
    
        Date of amendment request: June 17, 1994, as supplemented by letter 
    dated August 17, 1994.
        Description of amendment request: The amendment requests the 
    removal of license conditions for Transamerica Delaval (TDI) Emergency 
    Diesel Generators (EDGs) associated with NUREG-1216.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Involve a significant increase in the probability or the 
    consequences of an accident previously evaluated:
        The proposed amendment would not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. Elimination of the required teardowns and inspections has 
    no effect on the probability of an accident occurring, because the 
    diesel generators are not accident initiating equipment. Also, 
    deleting the teardowns and inspections would decrease the 
    consequences of an accident because the availability of the engines 
    would increase as a result of the less frequent teardowns. 
    Additionally, the high average reliability of the TDI engines would 
    not be negatively affected due to this change. NRC research has 
    shown there is a period of decreased reliability immediately 
    following intrusive teardowns, (break in period), followed by a long 
    period of high reliability.
        2. Create the possibility of a new or different kind of accident 
    from any previously evaluated:
        The proposed amendment would not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. The proposed amendment will not cause any physical change 
    to the plant or the design or operation of the diesel units.
        3. Involve a significant decrease in the margin of safety.
        The proposed amendment would not involve a significant reduction 
    in a margin of safety. The proposed amendment will increase the 
    reliability and availability of the EDGs and therefore will not 
    result in a decrease in a margin of safety at Grand Gulf.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: Judge George W. Armstrong Library, Post 
    Office Box 1406, S. Commerce at Washington, Natchez, Mississippi 39120
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations Inc., Docket No. 50-382, Waterford Steam 
    Electric Station, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: August 9, 1994
        Description of amendment request: The proposed amendment would 
    revise the technical specifications (TSs) by relocating the functions 
    under review and audit to the Waterford 3 quality assurance program 
    manual. The proposed change also incorporates the TS line-item-
    improvement of Generic Letter 93-07, ``Modification Of The Technical 
    Specification Administrative Control Requirements For Emergency And 
    Security Plans,'' dated December 28, 1993. The changes are proposed to 
    reduce regulatory burden by relocating TS requirements that are 
    duplicated by other regulatory requirements.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The proposed change will have no affect on design bases 
    accidents nor will the change directly affect any material condition 
    of the plant that could directly contribute to causing or mitigating 
    the effects of an accident. Relocating Review and Audit functions 
    from the TS is consistent with the NRC Final Policy Statement on 
    Technical Specifications Improvements and will have no negative 
    impact on plant operation or safety. Therefore, the proposed change 
    will not involve a significant increase in the probability or 
    consequences of any accident previously evaluated.
        The proposed change will not alter the operation of the plant or 
    the manner in which the plant is operated. The change will not 
    involve a design change or introduce any new failure modes. 
    Therefore, the proposed change will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed change is administrative in nature. The Waterford 3 
    safety margins are defined and maintained by the Technical 
    Specifications in Sections 2-5 which are unaffected. Therefore, the 
    proposed change will not involve a significant reduction in a margin 
    of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: University of New Orleans Library, 
    Louisiana Collection, Lakefront, New Orleans, Louisiana 70122
        Attorney for licensee: N.S. Reynolds, Esq., Winston & Strawn 1400 L 
    Street N.W., Washington, D.C. 20005-3502
        NRC Project Director: William D. Beckner
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-424 and 50-425, Vogtle Electric Generating Plant, Units 1 and 2, 
    Burke County, Georgia
    
        Date of amendment request: August 16, 1994
        Description of amendment request: The proposed changes revise VEGP 
    Technical Specification 3/4.7.1.1 and its bases regarding the setpoint 
    tolerance for the Main Steam Safety Valves (MSSVs).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated. 
    The setpoint tolerance change for the MSSVs from plus or minus 1% to 
    +2%, -3% is intended to accommodate setpoint drift that may occur 
    with these valves during plant operation. However, this change will 
    not adversely affect the pressure boundary integrity or safety 
    function of the valves. The increase in MSSV setpoint tolerance was 
    also reviewed with respect to the accident analyses presented in the 
    VEGP Final Safety Analysis Report (FSAR). The evaluation 
    demonstrated that the acceptance criteria of the accident analyses 
    continued to be met. Additionally, the radiological consequences 
    associated with the accident analysis are unaffected by the proposed 
    changes. Accordingly, since the performance and capability of the 
    MSSVs will be maintained as a result of the proposed changes with no 
    increase in radiological consequences, there will be no significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated. The proposed changes do not involve any change to the 
    configuration or method of operation of any plant equipment, and no 
    new failure modes have been defined for any plant system or 
    component. The design basis requirement for the MSSVs will continue 
    to be met and the structural integrity of the valves will not be 
    challenged. Also, the setpoint tolerance change will not adversely 
    affect the capability of the MSSVs to perform their pressure relief 
    function to ensure the secondary side steam design pressure is not 
    exceeded. Additionally, the as-left lift setpoints following testing 
    of the MSSVs will continue to be within plus or minus 1% of their 
    lift settings, further ensuring their safety function capability. 
    Therefore, since the function of the MSSVs is unaffected by the 
    proposed changes, the possibility of a new or different kind of 
    accident from any accident previously evaluated is not created.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety. All applicable acceptance criteria associated 
    with increasing the MSSV setpoint tolerance will continue to be met. 
    This includes the structural integrity of the valves and the effect 
    of the setpoint change on the accident analyses presented in the 
    VEGP FSAR. Therefore, since the MSSVs remain in compliance with the 
    appropriate codes and standards and all applicable acceptance 
    criteria continue to be met, there will not be a significant 
    reduction in a margin of safety.
        Based on the preceding analysis, Georgia Power Company has 
    determined that the proposed changes to the VEGP Technical 
    Specifications will not significantly increase the probability or 
    consequences of an accident previously evaluated, create the 
    possibility of a new or different kind of accident than any 
    previously evaluated, or involve a significant reduction in a margin 
    of safety. Therefore, the proposed changes meet the requirements of 
    10 CFR 50.92(c) and do not involve a significant hazards 
    consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards
        Local Public Document Room: Burke County Public Library, 412 Fourth 
    Street, Waynesboro, Georgia 30830.
        Attorney for licensee: Mr. Arthur H. Domby, Troutman Sanders, 
    NationsBank Plaza, Suite 5200, 600 Peachtree Street, NE., Atlanta, 
    Georgia 30308
        NRC Project Director: Herbert N. Berkow
    
    GPU Nuclear Corporation, et al., Docket No. 50-219, Oyster Creek 
    Nuclear Generating Station, Ocean County, New Jersey
    
        Date of amendment request: August 19, 1994
        Description of amendment request: The amendment updates and 
    clarifies the surveillance requirements for control rod exercising and 
    standby liquid control pump operability testing including the bases to 
    be consistent with Generic Letter 93-05.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Although the surveillance requirements are lessened by these 
    proposed changes, the changes are consistent with those found 
    acceptable by the NRC in GL 93-05. The proposed changes have been 
    determined to be compatible with our plant operating experience. 
    Based on these considerations, it is concluded that the changes do 
    not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed changes do not involve physical changes to the 
    plant or changes in plant operating configuration. The changes only 
    involve frequency of testing required to be performed. The changes 
    are consistent with those found acceptable by the NRC in GL 93-05. 
    Thus, it is concluded that the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. Although the surveillance requirements are lessened by these 
    proposed changes, the changes are consistent with those found 
    acceptable by the NRC in GL 93-05. The proposed changes have been 
    determined to be compatible with our plant operating experience. 
    Based on these considerations, it is concluded that the changes do 
    not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: Ocean County Library, Reference 
    Department, 101 Washington Street, Toms River, NJ 08753
        Attorney for licensee: Ernest L. Blake, Jr., Esquire. Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, 
    Linn County, Iowa
    
        Date of amendment request: August 15, 1994
        Description of amendment request: The proposed amendment would 
    increase the allowable main steam isolation valve (MSIV) leakage and 
    delete the Technical Specifications requirements applicable to the MSIV 
    leakage control system.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        Description of Amendment Request:
        Proposed Change 1
        This proposed change increases the allowable leak rate specified 
    in Technical Specification (TS) 4.7.A.2.c.3 from 11.5 standard cubic 
    feet per hour (scfh) for any one main steam isolation valve (MSIV) 
    when tested at 24 psig to 100 scfh for any one MSIV with a total 
    maximum pathway leakage rate of 200 scfh through all four main steam 
    lines when tested at 24 psig. If an MSIV exceeds 100 scfh, it will 
    be restored to less than or equal to 11.5 scfh.
        Basis for proposed no significant hazards consideration 
    determination:
        1. The change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated. The 
    proposed amendment does not involve a change to structures, 
    components, or systems which would affect the probability of an 
    accident previously evaluated in the DAEC Updated Final Safety 
    Analysis Report (UFSAR). It results in acceptable radiological 
    consequences for the design basis loss of coolant accident (LOCA) 
    which was previously evaluated in the UFSAR.
        Plant specific radiological analyses have been performed to 
    assess the effects of the proposed increase in the allowable MSIV 
    leak rate in terms of control room, technical support center (TSC), 
    and offsite doses following a postulated design basis LOCA. These 
    analyses utilize the hold-up volumes of the main steam piping and 
    condenser as an alternate method for treating MSIV leakage. The 
    radiological analyses use standard conservative assumptions for the 
    release of source terms consistent with Regulatory Guide 1.3, 
    ``Assumptions Used for Evaluating the Potential Radiological 
    Consequences of a Loss of Coolant Accident for Boiling Water 
    Reactors,'' Revision 2, dated June 1974.
        Dose contributions from the proposed MSIV leakage rate limit of 
    100 scfh per MSIV (with a maximum pathway leakage rate not to exceed 
    200 scfh through all four main steam lines) were calculated. The 
    analysis demonstrated that the dose contributions from the proposed 
    MSIV leakage rate resulted in an acceptable increase to the LOCA 
    doses previously evaluated against the regulatory limits for the 
    offsite, control room, and TSC doses as contained in 10 CFR 100 and 
    10 CFR 50, Appendix A (General Design Criterion 19). The revised 
    LOCA doses are the LOCA doses previously evaluated in the UFSAR plus 
    the MSIV leakage doses calculated assuming use of the alternate 
    treatment method. Table 1 of Attachment 2 shows the previously 
    calculated doses and the newly calculated doses.
        It is important to note that the resulting doses are dominated 
    by the organic iodine fractions which occur because of the 
    conservative source term assumptions used in this analysis. For a 
    total leakage rate of 200 scfh through all four main steam lines, 
    more than 90 percent of the offsite, control room, and TSC iodine 
    doses are due to the organic iodine from the Regulatory Guide 1.3 
    source term and organic iodine converted from the elemental iodine 
    deposited in main steam piping systems. If the actual iodine 
    composition from the fuel release (cesium iodine) is used in the 
    calculations, essentially all of this organic iodine dose would be 
    eliminated.
        The TSC doses due to MSIV leakage are especially conservative. 
    It is not expected that there will be any radioactive releases to 
    the TSC due to MSIV leakage during the initial stages of a LOCA 
    since it would take considerable time for the MSIV leakage to travel 
    through the main steam lines and main steam line drain system to the 
    condenser, into the turbine building, and finally to the atmosphere 
    and TSC. It was conservatively estimated that the 30-day integrated 
    dose to personnel in the TSC would increase by only 0.02 rem. The 
    dose calculations were performed using control room occupancy 
    factors specified in NUREG-0800, Standard Review Plan (SRP) Section 
    6.4.
        Therefore, we conclude that the proposed change will not 
    significantly increase the probability or consequences of any 
    previously analyzed accidents.
        2. The proposed change will not create the possibility of a new 
    or different kind of accident from any previously evaluated. The 
    BWROG evaluated MSIV leakage performance and concluded that MSIV 
    leakage rates up to 100 scfh will not inhibit the capability and 
    isolation performance of the valves to isolate the primary 
    containment. There is no new modification to the MSIVs which could 
    impact their operability. The LOCA has been analyzed using the main 
    steam piping and condenser as a treatment method to process MSIV 
    leakage at the proposed maximum rate of 200 scfh through all four 
    main steam lines. Therefore, the proposed change will not create any 
    new or different kind of accident from any accident previously 
    analyzed in the UFSAR.
        3. Operation of the DAEC in accordance with the proposed change 
    will not involve a significant reduction in the margin of safety. 
    The allowable leak rate limit specified for the MSIVs is used to 
    quantify a maximum amount of bypass leakage assumed in the LOCA 
    radiological analysis. Results of the analysis are evaluated against 
    the dose requirements contained in 10 CFR 100 for the offsite doses 
    and 10 CFR 50, Appendix A (General Design Criterion 19) for the 
    control room and TSC doses.
        The margins of safety are not significantly affected because the 
    dose levels remain well below the limits of 10 CFR 100 and General 
    Design Criterion 19. Therefore, the proposed change does not involve 
    a significant reduction in the margin of safety at the DAEC.
        Description of Amendment Request:
        Proposed Change 2
        This proposed change to delete TS 3.7.E and 4.7.E and Bases 
    section 3.7.E and 4.7.E involves eliminating the MSIV leakage 
    control system (LCS) requirements from the TS.
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated. As currently described in the UFSAR, the LCS is manually 
    initiated after a design basis LOCA occurs. Since the LCS is 
    operated only after an accident has occurred, this proposed 
    amendment has no effect on the probability of an accident. The 
    proposed change results in acceptable radiological consequences of 
    the design basis LOCA previously evaluated in the UFSAR.
        The DAEC has an inherent MSIV leakage treatment capability. IES 
    Utilities Inc. proposes to use the main steam line drains and 
    condenser as an alternative to the LCS. Figure 1.1 of Attachment 2 
    shows the primary and alternate drain paths. The proposed primary 
    drain path at DAEC employs an MSL drain downstream of the MSIVs. 
    There are two motor-operated valves (MOVs) in series in this line 
    between the MSL and the main condenser. Both valves must be open to 
    establish the required drain path. Both MOVs will be provided with 
    essential power to assure that they can be opened following the DBA 
    LOCA to establish a large enough drain path to support the 
    radiological analysis.
        An alternate drain path will be available to convey MSIV leakage 
    to the isolated condenser if either MOV fails to open. The alternate 
    drain path consists of the bypass lines around the MOVs in the 
    primary drain path. This alternate path contains a ``fail open'' 
    valve and a restricting orifice. Consequently, if either primary MOV 
    failed to open as required, the second drain path would be available 
    to convey MSIV leakage to the main condenser. Radiological dose 
    calculations have been performed for this alternate path as well as 
    for the primary path. The results were acceptable. IES Utilities 
    Inc. will update DAEC procedures as necessary to address the 
    applicable alternate leakage treatment methods.
        IES Utilities Inc. contracted with EQE Engineering Consultants 
    (EQE) to confirm the seismic capability of the DAEC's main steam 
    piping and condenser to serve as an alternate leakage treatment 
    system. Seismic verification walkdowns were performed to assure that 
    the MSLs, the steam drain lines, the condenser, and interconnecting 
    piping and equipment that were not seismically analyzed fall within 
    the bounds of the design characteristics of the seismic experience 
    database as discussed in Section 6.7 of the BWROG report.
        The DAEC main steam lines, main steam drain lines, condenser, 
    and applicable interconnecting piping and equipment, are well 
    represented by the earthquake experience data demonstrating good 
    seismic performance, are confirmed to exhibit excellent resistance 
    to damage from a design basis earthquake and have been shown to have 
    substantial margin for seismic capability. The outliers that were 
    identified are discussed in Attachment 7. They have been either 
    evaluated to demonstrate their acceptability as they currently 
    exist, or plant modifications will be implemented to resolve the 
    concerns. By taking the measures discussed in Attachment 7 to ensure 
    resolution for all of the identified outliers, IES Utilities Inc. is 
    assured that the damage reported for the database components should 
    not occur to the DAEC main steam piping and condenser or to the 
    associated support systems.
        Therefore, the proposed method for MSIV leakage treatment is 
    seismically adequate to withstand the DAEC design basis earthquake 
    and maintain pressure retaining integrity and serve as an acceptable 
    alternative to the currently installed LCS. The capability of the 
    alternate MSIV leakage treatment system to withstand the effects of 
    the safe shutdown earthquake and continue to perform its intended 
    function (treatment of MSIV leakage) satisfies the intent of the 
    seismic requirement of Appendix A to 10 CFR 100.
        Plant specific radiological analyses have been performed to 
    assess the effects of MSIV leakage in terms of control room and 
    offsite doses following a postulated design basis LOCA. While not 
    previously considered a requirement for the design of the LCS, dose 
    calculations were also performed for the TSC. These analyses utilize 
    the hold-up volumes of the main steam piping and condenser as an 
    alternate treatment method for the MSIV leakage. The analysis 
    demonstrates that the proposed change results in an acceptable 
    increase in the radiological consequences of a LOCA previously 
    evaluated in the UFSAR. The LOCA previously evaluated in the UFSAR 
    is still the bounding accident; the proposed change will not involve 
    a significant increase in the consequences of an accident previously 
    analyzed.
        The LCS lines will be disconnected, capped and welded, ensuring 
    that the integrity of the primary containment is maintained. IES 
    Utilities Inc. will incorporate the alternate leakage treatment 
    system into the inservice inspection (ISI) and inservice testing 
    (IST) programs, consistent with program requirements.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any previously evaluated. The 
    purpose of the LCS is to reduce the untreated MSIV leakage when 
    isolation of the primary coolant system and containment are 
    required. Radiological dose contributions due to MSIV leakage are 
    bounded by a LOCA. The LOCA has been analyzed using the main steam 
    piping and condenser as a treatment method to process MSIV leakage 
    at the proposed maximum rate of 100 scfh per MSIV and 200 scfh total 
    maximum pathway leakage, and determined to be within the regulatory 
    requirements. The LCS lines connected to the main steam lines will 
    be permanently closed to assure the primary containment integrity, 
    isolation, and leak testing capability are not compromised.
        3. The proposed change to delete TS 3.7.E and 4.7.E and Bases 
    section 3.7.E and 4.7.E does not involve a significant reduction in 
    the margin of safety. The intended function of the LCS for treatment 
    of MSIV leakage will be performed by using the more effective 
    alternate path via the main steam drain lines and condenser. This 
    treatment method is effective for treatment of MSIV leakage over an 
    expanded leakage range. Except for the requirement to assure that 
    certain valves are opened to establish a proper flow path from the 
    MSIVs to the condenser and that certain valves are closed to 
    establish the seismic boundary, the proposed method is passive and 
    does not require any logic controls or interlocks. On the other 
    hand, the LCS consists of complicated logic controls and sensitive 
    equipment which must be maintained at significant cost and radiation 
    exposure. The radiological effects on the margin of safety are 
    discussed above for Change 1. The safety significance of the LCS in 
    terms of public risk was addressed in NUREG/CR-4330 which contains 
    the evaluation for eliminating the LCS and disabling the systems 
    currently installed at BWRs. The conclusion was that the increased 
    public risk is less than 1 percent. Therefore, the proposed change 
    does not involve a significant reduction in the margin of safety at 
    the DAEC.
        The various attachments referred to in the above analysis may be 
    found in the licensees request for amendment dated August 15, 1994. 
    This document is available in the NRC's Public Document Room located at 
    the Gelman Building, 2120 L. Street, NW., Washington, DC 20555 and at 
    the local public document room address below.
        The NRC staff has reviewed the licensee's analysis and, based on 
    thisreview, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: Cedar Rapids Public Library, 500 First 
    Street, S.E., Cedar Rapids, Iowa 52401
        Attorney for licensee: Jack Newman, Esquire, Kathleen H. Shea, 
    Esquire, Newman and Holtzinger, 1615 L Street, NW., Washington, DC 
    20036
        NRC Project Director: John N. Hannon
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of amendment request: June 2, 1994, as supplemented August 25, 
    1994
        Description of amendment request: The proposed amendment would 
    change the Technical Specifications (TS) to remove expired one-time 
    extensions of surveillances, remove an obsolete definition of charging 
    pump operability, and incorporate 11 line item improvements in 
    accordance with the guidance provided in Generic Letter (GL) 93-05. 
    Other editorial changes would be made to renumber some pages and delete 
    the blank pages from the TS.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below.
        A. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated (10 
    CFR 50.92(c)(1)). The expired one-time extensions were in effect to 
    September 30, 1993. Since these extensions have expired and the 
    appropriate surveillances were performed, the proposed changes do not 
    effect the configuration, operation, or performance of any system, or 
    component.
        The proposals to delete Definition 1.45, ``THE CHARGING PUMP 
    OPERABILITY,'' and modify the Index to reflect this change are 
    administrative changes. Definition 1.45 was applicable only for cycle 4 
    operation. Northeast Nuclear Energy Company (NNECO) has completed the 
    necessary modifications and no longer rely on a temporary heating 
    source. Therefore, the elimination of Definition 1.45 does not involve 
    a significant increase in the probability or consequences of an 
    accident previously analyzed.
        The proposed changes to incorporate the recommendations of GL 93-05 
    do not affect the configuration, operation or performance of the 
    subject systems. Increasing the surveillance test intervals as proposed 
    will reduce the number of surveillance tests and minimize the potential 
    for inadvertent actuation of an engineered safety feature. The increase 
    in the surveillance test intervals will enhance the operational 
    effectiveness of plant personnel, by reducing the amount of time that 
    the plant staff has available to perform other tasks, such as 
    additional preventive maintenance. Additionally, increasing the 
    surveillance test interval will reduce unnecessary wear to equipment. 
    NNECO's proposals to delete pages that were intentionally left blank, 
    to renumber remaining pages and renumber Sections, and modify the Index 
    to reflect these changes are purely administrative and editorial 
    changes. Proposals to correct typographical errors on TS pages are also 
    administrative changes. These changes would not affect the 
    configuration, operation, or performance of any system, structure, or 
    component.
        The proposed changes do not affect the manner by which the facility 
    is operated and do not change any facility design feature or equipment. 
    The proposed changes involve administrative or programmatic 
    requirements or merely involve editorial changes, corrections, or 
    clarifications. Since there is no change to the facility or operating 
    procedures, there is no affect upon the probability or consequences of 
    any accident previously analyzed.
        B. The changes do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated (10 CFR 
    50.92(c)(2)) because they do not affect the manner by which the 
    facility is operated and do not change any facility design feature or 
    equipment which affects the operational characteristics of the 
    facility. The proposed changes involve administrative or programmatic 
    requirements or merely involve editorial changes, corrections, or 
    clarifications.
        C. The changes do not involve a significant reduction in a margin 
    of safety (10 CFR 50.92(c)(3)) because the proposed changes do not 
    affect the manner by which the facility is operated or involve 
    equipment or features which affect the operational characteristics of 
    the facility.
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room: Learning Resource Center, Three Rivers 
    Community-Technical College, Thames Valley Campus, 574 New London 
    Turnpike, Norwich, CT 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, CT 
    06141-0270.
        NRC Project Director: John F. Stolz
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of amendment request: July 22, 1994
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications to incorporate a different setpoint 
    and transient methodology for determining the maximum allowable power 
    range neutron flux setpoint. The changes would allow Millstone Unit 3 
    to operate with a reduced number of main steam-line safety valves at a 
    reduced power level, as determined by the high neutron flux setpoint.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        ...The proposed changes do not involve an SHC [significant 
    hazards consideration] because the changes would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Technical Specification Tables 3.7-1 and 3.7-2 are being revised 
    to reflect a reduction in the maximum allowable power range neutron 
    flux high setpoint with inoperable steam generator safety valves. 
    The new setpoints reflect a change in the methodology for 
    calculating the setpoints.
        Westinghouse has determined that under certain conditions with 
    typical safety analysis assumptions, the current setpoints in Tables 
    3.7-1 and 3.7-2 may not provide adequate steam generator 
    overpressure protection for a Loss of Load/Turbine Trip transient at 
    reduced power levels. At reduced power levels, a reactor trip may 
    not be actuated early in the transient. An overtemperature delta T 
    trip may not be generated since the core thermal margins are 
    increased at lower power levels. The PORVs [power-operated relief 
    valves] and pressurizer spray may control RCS [Reactor Coolant 
    System] pressure such that a high pressurizer pressure trip isn't 
    generated. The reactor would eventually trip on low steam generator 
    water level, but this may not occur before steam pressure exceeds 
    110% of the design value if one or more MSSVs [main steam-line 
    safety valves] are inoperable.
        To address this issue, Westinghouse has developed a new method 
    for determination of the required power range neutron flux high 
    setpoint. The new setpoint is based upon the heat removal capability 
    of the operable MSSVs, rather than the previous method based only on 
    flow capacity. The new equation is shown in the proposed changes to 
    the Technical Specification basis. This new method has been 
    developed by Westinghouse generically and a Millstone Unit No. 3 
    specific calculation has been performed. The new setpoints are being 
    incorporated in this proposed Technical Specification change.
        The new method includes several conservative assumptions. The 
    equation is developed assuming that the maximum number of inoperable 
    MSSVs applies to each loop. For example, for four loop operation, 
    the maximum allowable power range neutron flux high setpoint of 65% 
    is based upon four inoperable MSSVs, one per steam generator. Thus, 
    in the event that only one MSSV is inoperable, the application of 
    the new setpoint is very conservative. In addition, the setpoint is 
    based upon the assumption that the largest capacity MSSV is 
    inoperable. For the case where one of the lower capacity MSSVs is 
    inoperable, the setpoint will be conservative.
        The method of calculating the setpoint provides assurance that 
    the heat removal capability of the operable MSSVs is sufficient for 
    reactor power up to the power range neutron flux high setpoint 
    taking into account instrument and channel uncertainties. 
    Consequently, steam generator pressure will remain below 110% of 
    design in the event of the limiting overpressurization transient, 
    the Loss of Load/Turbine Trip.
        Reducing the power range neutron flux high setpoint and 
    consequently the allowable reduced power level has no impact on the 
    consequences of any other accident. In addition, since the proposed 
    changes only involve a reduction in the allowable power range 
    neutron flux high setpoint, and operation at a lower power level, 
    they cannot affect the probability of any design basis accident.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        Since the proposed changes just reduce the existing limit on the 
    power range neutron flux high setpoint with inoperable MSSVs, the 
    change cannot create the possibility for a new or different kind of 
    accident.
        3. Involve a significant reduction in the margin of safety.
        The reduced setpoint provides additional assurance that the 
    steam generator pressure will remain below 110% of design for the 
    limiting overpressurization transient, the Loss of Load/Turbine 
    Trip. Thus, the proposed changes do not reduce the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: Learning Resource Center, Three Rivers 
    Community-Technical College, Thames Valley Campus, 574 New London 
    Turnpike, Norwich, Connecticut 06360.
        Attorney for licensee: Ms. L. M. Cuoco, Senior Nuclear Counsel, 
    Northeast Utilities Service Company, Post Office Box 270, Hartford, 
    Connecticut, 06141-0270.
        NRC Project Director: John F. Stolz
    
    Pennsylvania Power and Light Company, Docket No. 50-387 Susquehanna 
    Steam Electric Station, Unit 1, Luzerne County, Pennsylvania
    
        Date of amendment request: July 27, 1994
        Description of amendment request: By letter dated June 15, 1992, 
    Pennsylvania Power and Light Company (PP&L) submitted ``Licensing 
    Topical Report NE-092-001, Revision 0, Power Uprate With Increased Core 
    Flow,'' for Susquehanna Steam Electric Station, Units 1 and 2. The 
    report was submitted to support future amendments to the Units 1 and 2 
    licenses to permit a 4.5-percent increase in reactor thermal power and 
    an 8-percent increase in core flow for each unit. The initial submittal 
    was revised and supplemented by letters of July 24, September 17, and 
    December 18, 1992, and January 8, January 25, April 2, August 5, August 
    12, and September 29, 1993. The Commission's safety evaluation on these 
    submittals was issued November 30, 1993 (Letter, Thomas E. Murley, NRC, 
    to Robert G. Byram, PP&L). The Commission concluded that the revised 
    (Revision 2) licensing topical report adequately supports PP&L's 
    proposed power uprate. The Commission also concluded that SES, Units 1 
    and 2, can operate safety with the proposed 8-percent increase in core 
    flow, the proposed 4.5-percent increase in reactor thermal power, the 
    corresponding 5-percent increase in main turbine inlet steam flow, and 
    the corresponding increases in flows, temperatures, pressures, and 
    capacities required in supporting systems and components at these 
    uprated conditions.This amendment will change several Technical 
    Specifications sections (listed below in the no significant hazards 
    consideration) for Susquehanna Steam Electric Station, Unit 1, to 
    increase the licensed power level from the current 3293 MWt to a new 
    limit of 3441 Mwt.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        The following three questions are addressed for each of the 
    proposed Technical Specification Changes:
        1. Does the proposed change involve a significant increase in 
    the probability or consequences of an accident previously evaluated?
        2. Does the proposed change create the possibility of a new or 
    different kind of accident from any previously evaluated?
        3. Does the proposed change involve a significant reduction in a 
    margin of safety?
        Section 1.0, Definitions, Definition 1.33, Rated Thermal Power
        This change redefines Rated Thermal Power as 3441 megawatts 
    thermal.
        1. No. Neither the probability (frequency of occurrence) nor 
    consequences of any accident previously evaluated is significantly 
    affected by the increased power level because the design and 
    regulatory criteria established for plant equipment remain imposed 
    for the uprated power level. The PP&L assessment to increase the 
    rated thermal power level at Susquehanna SES Unit 1, followed the 
    guidelines of NEDC-31879P (Generic Guidelines for General 
    Electric Boiling Water Reactor Power Uprate,'' G.E. Nuclear Energy, 
    June 1991). NEDC-31879P provides generic licensing criteria, 
    methodology, and a defined scope of analytical and equipment review 
    to be performed to demonstrate the ability to operate safely at the 
    uprated power level which have been approved by the NRC. NE-092-001 
    (Licensing Topical Report for Power Uprate With Increased 
    Core Flow,'' Pennsylvania Power & Light Company, December 1992) 
    provides the description of the power uprate licensing analysis 
    methodology and the results of the evaluations performed to support 
    the proposed uprated power operation consistent with the methodology 
    presented in NEDC-31879P. NE-092-001 provides a description of the 
    power uprate licensing analysis methodology which will be used to 
    determine cycle specific thermal limits for Unit 1, Cycle 9 and 
    future cycles and concludes that an uprated power level of 3441 
    megawatts thermal can be achieved without significant effect on 
    equipment or safety analyses.
        2. No. The methodology and results described above do not 
    indicate that a possibility for a new or different kind of accident 
    from any previously evaluated has been created by uprated operation.
        3. No. Based on the response to Question 1 above, the 
    methodology and results do not indicate a significant reduction in a 
    margin of safety.
        Section 2.1, Safety Limits
        The reference to ``rated core flow'' in Technical Specification 
    2.1.1 and 2.1.2 has been replaced with a reference to actual core 
    flow. The references to ``rated core flow'' have been deleted to 
    avoid confusion since allowable core flow is being increased by 8%. 
    10 Mlbm/hr is being used in these specifications to be consistent 
    with other similar Technical Specification changes (Technical 
    Specifications 3.2.2, 4.4.1.1.1.2, 4.4.1.1.2.5, 3.4.1.3 and Figure 
    3.4.1.1.1-1).
        1. No. The probability and consequences of accidents previously 
    evaluated are not affected by this change. The basis for Technical 
    Specification 2.1.1 is that boiling transition will not occur in 
    bundles if core power is less than 25% of rated thermal power, 
    regardless of pressure or core flow. Consequently, the specification 
    of less than 10% rated core flow is not crucial to the basis and, 
    thus, the use of 10 Mlbm/hr. is acceptable and has no effect on the 
    probability or consequences of a previously evaluated accident.
        For Technical Specification 2.1.2, the XN-3 critical power 
    correlation is valid for pressure greater than or equal to 580 psig 
    and bundle flow greater than or equal to 0.25 Mlbm/hr-ft2. As 
    stated in the basis for Technical Specification 2.1.1, if vessel 
    downcomer water level is above TAF [top of active fuel], and core 
    power greater than 25%, bundle flows for potentially limiting 
    bundles will be greater than 0.25 Mlbm/hr-ft2 due to natural 
    circulation. In addition, Technical Specification 3.4.1.1.1 requires 
    at least one (1) recirculation loop in operation to run in Condition 
    2, which would produce a core flow in excess of 30 Mlbm/hr. 
    Therefore, core flows below about 30 Mlbm/hr-ft2 are prohibited 
    when the reactor is at power. Thus, the change from ``10%'' to ``10 
    million lbm/hr'' is acceptable and has no effect on the probability 
    or consequences of a previously evaluated accident.
        2. No. The basis for Technical Specification 2.1.1 is that 
    boiling transition will not occur in bundles if core power is less 
    than 25% of rated thermal power, regardless of pressure or core 
    flow. The proposed change is not crucial to this basis. The XN-3 
    critical power correlation is valid for pressures greater than or 
    equal to 580 psig and bundle flow greater than or equal to 0.25 
    Mlbm/hr-ft2. The specification is based upon vessel downcomer 
    water level being above TAF and core power greater than 25% which 
    yields a bundle flow for potentially limiting bundles greater than 
    0.25 Mlbm/hr-ft2 due to natural circulation. Based on Technical 
    Specification 3.4.1.1.1, core flows below about 30 Mlbm/hr-ft2 
    are prohibited when the reactor is at power. Therefore, the change 
    to a limit of 10 Mlbm/hr is acceptable and does not create the 
    possibility for a new or different kind of accident from any 
    accident previously evaluated.
        3. No. As explained above, the margin of safety has not been 
    reduced.
        Table 2.2.1-1 (Items 2.a, 2.b, and 2.c) and Specifications 
    3.2.2, 3.4.1.1.2.a.2, 3.4.1.1.2.a.3, 3.4.1.1.2.a.5.b and 3.3.6-2 
    (Item 2.a.1, 2.c, and 2.d), APRM Flow Biased Setpoints and Allowable 
    Values
        Although the equation for determining these setpoints does not 
    change as a result of the power uprate, because the setpoints in 
    these technical specifications are referenced to rated thermal 
    power, the current limits do change in that the top portion of the 
    operating map (power vs. reactor flow) is raised by 4.5%.
        1. No. The safety analyses contained in NE-092-001 evaluated 
    operation at both uprated power with 4.5% higher rod lines and 
    increased core flow. In addition, General Electric Co. has analyzed 
    and received generic approval for their BWR/4 product line operation 
    in the Maximum Extended Operating Domain (MEOD). Operation at the 
    4.5% higher rod lines is bounded by the MEOD analysis. Additional 
    justification for this small increase in the power flow operating 
    range is contained in Section C.2.3 of NEDC-31984P.
        Cycle specific reload analyses will evaluate operation at the 
    increased power vs. flow conditions (100% uprated power vs. 87% core 
    flow to 100% uprate power vs. 108% core flow). These analyses will 
    ensure that the limits established in the Core Operating Limits 
    Report are applicable to rated power operation from 87% to 108% core 
    flow.
        Based on the above analyses, increasing the current limits do 
    not represent a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. No. The analyses described above in response to Question 1 do 
    not indicate that a possibility for a new or different kind of 
    accident from any previously evaluated has been created by the 
    proposed change.
        3. No. Based on the response to Question 1 above, the proposed 
    change does not result in a reduction in the margin of safety.
        Table 2.2.1-1, Item 3, Reactor Steam Dome Pressure - High Scram
        The reactor steam dome pressure-high scram trip setpoint and 
    allowable values are being changed to less than or equal to 1087 
    psig and less than or equal to 1093 psig respectively.
        1. No. This scram function is designed to terminate a pressure 
    increase transient not terminated by direct scram or high flux 
    scram. The nominal trip setpoint is maintained above the reactor 
    vessel maximum operating pressure and the specified analytical limit 
    is used in the transient analyses. The analytical limit of 1105 psig 
    is used in the uprated transient analyses. The results of the 
    overpressure protection analysis indicate that the peak pressure 
    will remain below the 1375 psig ASME limit which meets plant 
    licensing requirements. In accordance with the methodology described 
    in NE-092-001, transient analyses will be performed using the 
    analytic limit and the results will be incorporated into the Core 
    Operating Limits Report. Therefore, this proposed change does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. No. The purpose of this scram function is to terminate a 
    pressure increase transient not terminated by direct scram or high 
    flux scram. The nominal trip setpoint is maintained above the 
    reactor vessel maximum operating pressure and the specified 
    analytical limit is used in the transient analysis. 1105 psig is 
    being used as the analytical limit in the uprated transient 
    analysis. The results of the overpressure protection analysis 
    indicate peak pressure will remain below the ASME limit of 1375 psig 
    which satisfies plant licensing requirements. Based upon that 
    result, it is concluded that the proposed change will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. No. The results of the overpressure protection analysis 
    indicate peak pressure will remain below the 1375 psig licensing 
    limit, therefore, it is concluded that the proposed change does not 
    result in a significant reduction in a margin of safety.
        Specification 4.1.5.c, Standby Liquid Control System
        This specification has been revised to require SLC [Standby 
    Liquid Control] pumps to develop a discharge pressure of greater 
    than or equal to 1224 psig.
        1. No. The ability of the SLC system to achieve and maintain 
    safe shutdown is a function of the amount of fuel in the core and is 
    not directly affected by core thermal power. The SLC pump test 
    discharge pressure acceptance criteria are based on the lowest 
    relief valve setpoint. The lowest setpoint is being increased by 30 
    psi (to 1106) due to power uprate. Operating with increased core 
    flow will result in additional friction losses through the core and 
    a slightly larger core differential pressure (approximately 4 psi). 
    Therefore, increasing the SLC pump test discharge pressure 
    acceptance criteria ensures the capability of SLC injection. The 
    proposed change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. No. The ability of the SLC system to achieve and maintain 
    safe shutdown is a function of the amount of fuel in the core and is 
    not directly affected by core thermal power. Therefore, the proposed 
    change does not result in a new or different kind of accident from 
    any previously evaluated.
        3. No. The ability of the SLC system to achieve and maintain 
    safe shutdown is a function of the amount of fuel in the core and is 
    not directly affected by core thermal power. As stated in the 
    response to question 1 above, the SLC pump discharge pressure 
    acceptance criteria are based upon the lowest relief valve setpoint. 
    The lowest setpoint is being increased by 30 psi. As the SLC pumps 
    are positive displacement pumps, the uprate will not adversely 
    affect the performance of the pumps to achieve proper injection. 
    Based on above, the proposed change does not result in a significant 
    reduction in a margin of safety.
        Specifications 3.2.2, 4.4.1.1.1.2, 4.4.1.1.2.5, 3.4.1.3 and 
    Figure 3.4.1.1.1-1, Rated Core Flow References
        Technical Specification 3.2.2 contains the definition of ``W'' 
    for the flow biased APRM scram equation. The word ``rated'' is being 
    deleted from the definition of ``W'' since rated core flow is being 
    increased. The definition of ``W'' is not altered. The change is 
    being made for editorial purposes.
        Technical Specifications 4.4.1.1.1.1.2, 4.1.1.1.2.5, 3.4.1.3, 
    and Figure 3.4.1.1.1-1 specify performance requirements and limits 
    for the Reactor Recirculation System. These specifications are 
    referenced to the current rated core flow. The references to ``rated 
    core flow'' are being replaced with actual equivalent core flows. 
    The specifications are equivalent and unchanged. This change is 
    being made for editorial purposes to avoid confusion since rated 
    core flow is being increased. These changes are also consistent with 
    the changes made in Section 2.1.
        1. No. The proposed changes are editorial and do not effect the 
    probability or consequences of an accident previously evaluated.
        2. No. The proposed changes are editorial and do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. No. The proposed changes are editorial and do not involve a 
    significant reduction in a margin of safety.
        Specification Table 3.3.1-1, Note (j) and Action 6, Reactor 
    Protection System Instrumentation, and Table 3.3.4.2-1, Note b, End-
    of-Cycle Recirculation Pump Trip System Instrumentation
        The turbine first stage pressure scram bypass at 30% power in 
    Technical Specification Table 3.3.1-1, Note (j) and Table 3.3.4.2-1, 
    Note (b) is revised to indicate that the uprated equivalent 
    allowable value of first stage turbine pressure is 136 psig. This 
    value ensures that the analytical limit of 147.7 psig, which 
    represented 30% rated thermal power, is not exceeded.
        As currently written Note (j), Note (b) and Table 3.3.1-1, 
    ACTION 6 are unclear and could be misinterpreted. They apply only 
    when RPS scram functions and End-of-Cycle Recirculation Pump Trip on 
    turbine main stop valves closure or control valve fast closure are 
    not automatically bypassed. ACTION 6 provides no guidance in the 
    event the bypass fails to lift when thermal power is above 30%. In 
    the worst case, the action statement could be interpreted literally 
    to allow full power operation with the RPS function still bypassed. 
    Such operation would violate the licensing basis analysis for the 
    MCPR operating limit (for the Generator Load Rejection Without 
    Bypass transient), which takes credit for operation of the 
    anticipatory scram on control valve fast closure at greater than 30% 
    of rated thermal power.
        1. No. The revisions to Table 3.3.1-1, ACTION 6, Table 3.3.1-1, 
    Note (j), and Table 3.3.4-1 Note (b) clarify the current 
    requirements; they do not change their intent.
        FSAR Chapter 15 transient analyses and reload licensing analyses 
    take credit for operation of the anticipatory scram function on 
    turbine stop valve closure and control valve fast closure for power 
    levels greater than 30% of rated thermal power. The proposed 
    revision to Table 3.3.1-1, ACTION 6 provides better assurance of the 
    availability of the anticipatory scram function, since the current 
    specifications could be interpreted literally to allow full power 
    operation with the RPS function bypassed.
        The proposed revision to Table 3.3.1-1, Note (j) and Table 
    3.3.4.2-1, Note (b) does not change the operation of the RPS and 
    EOC-RPT bypasses on turbine stop valve closure and control valve 
    fast closure below 30% power. The turbine first stage pressure 
    switches will still be calibrated in the same manner, and, by 
    procedure, the reactor operator will not exceed 30% power if the 
    trip bypass annunciator does not clear.
        The setpoints for the RPS and EOC-RPT bypass functions were 
    selected to allow sufficient operating margin to avoid scrams during 
    low power turbine generator trips. As discussed in NEDC-31894P, 
    Section F4.2(c) and in Section 5.1.2.8 of NEDC 31948P, this small 
    absolute setpoint increase maintains the safety basis for the 
    setpoint.
        Based on the above, the proposed changes do not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. No. The changes proposed are clarifications and do not change 
    specification intent. The proposed change to Table 3.3.1-1, Action 6 
    provides better assurance of the availability of the anticipatory 
    scram function as the specification could currently be interpreted 
    to allow full power operation with the RPS function bypassed. The 
    proposed changes to Table 3.3.1-1, Note (j) and Table 3.3.4-1, Note 
    (b) do not change the operation of the RPS and EOC-RPT bypasses on 
    turbine stop valve closure and control valve fast closure below 30% 
    power. Therefore, the possibility for a new or different kind of 
    accident is not created.
        3. No. The proposed changes are clarification and do not change 
    intent. Operation of the RPS and EOC-RPT bypasses on turbine stop 
    valve closure and control valve fast closure below 30% power is not 
    changed. Therefore, there is no reduction in the margin of safety.
        Specification Table 3.3.2-2, Item 3.d, Main Steam Line Flow 
    Differential Pressure Setpoint
        The main steam line flow high differential pressure setpoint and 
    allowable value are revised to read trip setpoint and allowable 
    values of 113 psid and 121 psid respectively. Footnote ``**'' was 
    added to Table 3.3.2-2 to indicate that these values will be 
    confirmed during the power uprate start-up testing. If revisions to 
    the setpoint and allowable value are required, they will be 
    forwarded to the Commission for approval within 90 days of 
    completion of the test program.
        1. No. The main steam line flow high differential pressure 
    setpoint changes reflect the redefinition of rated main steam line 
    flow that occurs with power uprate. The allowable value is 
    maintained at the same percentage of rated steam flow as the 
    differential pressure changes due to the increased uprate steam 
    flow. The analytical limit of 140% of uprated steam flow is 
    maintained for the uprated analyses. The relationship between the 
    allowable value and the analytical limit was retained to ensure that 
    a trip avoidance margin is maintained for the normal plant testing 
    of MSIV's and turbine stop valves. The increase in the absolute 
    value of the trip setpoint still provides a high assurance of 
    isolation protection for a main steam line break accident which 
    satisfies the original intent of the design. Therefore, the proposed 
    changes do not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. No. The increase in the absolute value of the trip setpoint 
    still provides a high assurance of isolation protection for the main 
    steam line break accident which satisfies the original intent of the 
    design and, therefore does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. No. The increase in the absolute value of the trip setpoint 
    still provides a high assurance of isolation protection for a main 
    steam line break accident which satisfies the original intent of the 
    design and, therefore, does not involve a significant reduction in a 
    margin of safety.
        Specification Table 3.3.2-2, Item 4.f, Isolation Actuation 
    Instrumentation Setpoints
        The RWCU system flow-high isolation trip setpoint and allowable 
    value are being changed. System flow is being increased by 10% to 
    maintain reactor coolant water chemistry at a level equal to pre 
    uprate levels. The isolation setpoint change is being made to 
    adequately maintain operating margin between normal process values 
    and the isolation setpoints.
        1. No. The basis for the RWCU flow-high isolation is to ensure a 
    RWCU System isolation in case of a pipe break. The high flow 
    setpoint is set high enough to avoid spurious trips from normal 
    operating transients but low enough to ensure an isolation during a 
    pipe break. The proposed Technical Specification limits will result 
    in a negligible reduction in the margin between the RWCU isolation 
    setpoint and the 4350 gpm flow postulated during a RWCU line break 
    and will avoid spurious isolations. Therefore, the proposed change 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. No. As stated above, the proposed change will result in only 
    a negligible reduction in the margin between the RWCU isolation 
    setpoint while avoiding spurious isolation. Therefore, this change 
    maintains the original design intent and does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. No. See 1. above.
        Specification Table 3.3.2-2, Items 5.a and 6.1, Isolation 
    Actuation Instrumentation Setpoints
        The HPCI and RCIC Steam Line Flow-High Technical Specifications 
    are being changed to account for changes in steam conditions and 
    flows that result from operation at the uprated conditions. The 
    setpoint and allowable value for HPCI Steam Line Flow-High isolation 
    are less than or equal to 387 inches H2O setpoint and allowable 
    value for the RCIC Steam Line Delta Pressure-High isolation are less 
    than or equal to 188 inches H2O and less than or equal to 193 
    inches H2O respectively.
        1. No. The bases for these setpoints are contained in the 
    General Electric Design Specification Data Sheets for the HPCI and 
    RCIC systems. The Design Specification Data Sheets specify that the 
    setpoint and allowable value be set so that the isolation occurs at 
    greater than 272% normal steam flow and less than 300% steam flow. 
    General Electric has historically seen start-up transients as high 
    as 272% of normal steam flow. Setting the isolation above this value 
    prevents spurious isolations and ensures availability of the system 
    and its safety function. Setting the isolation at less than or equal 
    to 300% of normal flow insures that the isolation will occur if a 
    steam line should rupture.
        The existing setpoints were calculated using information 
    obtained during the recent surveillance tests. The revised setpoints 
    and allowable values were calculated using the current system 
    performance and adjusted for uprate conditions in accordance with 
    additional guidance provided in General Electric Information Letter 
    (SIL) No. 475, Revision 2, NEDC-31336, ``General Electric Setpoint 
    Methodology,'' and GE Letter SPU-9378, ``HPCI and RCIC Steam Line 
    Break Detection Setpoints''.
        Based on the above approach, the proposed change does not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        2. No. The setpoint and allowable value are set so that 
    isolation occurs at greater than 272% normal steam flow and less 
    than 300% steam flow. Setting the isolation at less than or equal to 
    300% of normal flow ensures that the isolation will occur if a steam 
    line rupture should occur. Therefore, no new events are postulated 
    as a result of this change.
         3. No. The proposed change does not involve a significant 
    reduction in a margin of safety as the setpoint and allowable value 
    are set to isolate at greater than 272% normal steam flow and less 
    than 300% steam flow which are the setpoints contained in the 
    General Electric Design Specification Data Sheets for the HPCI and 
    RCIC systems.
        Specification Table 4.3.2.1-1, footnote ``**''
        The footnote is being changed to delete reference to reactor 
    pressure.
        1. No. The original purpose of Footnote ``**'' to Technical 
    Specification Table 4.3.2.1-1 was to describe the functioning of the 
    permissive circuitry that allowed the MSIV low condenser pressure 
    isolation to be bypassed. The original circuitry required the Mode 
    Switch not be in Run, the Turbine Stop Valves closed, and reactor 
    pressure to be above setpoint. In the start-up phase of the 
    Susquehanna Units, General Electric deleted the reactor pressure 
    setpoint input to the bypass circuitry. Therefore, this change is 
    being made to make the footnote conform to the installed 
    configuration. The revised footnote is the same as found in the BWR/
    4 Standard Technical Specifications (NUREG 1433). This change is 
    editorial in nature and, therefore, does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. No. Based on the response to Question 1 above, the proposed 
    change does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. No. Based on the response to Question 1 above, the proposed 
    change does not involve a significant reduction in a margin of 
    safety.
        Specification Table 3.3.6-2, Item 1.a and Specification 
    3.4.1.1.2.a.5.a, Rod Block Monitor Flow Biased Rod Blocks
        The Rod Block Monitor (RBM) flow biased rod blocks are being 
    changed as follows:
        a. Technical Specification Table 3.3.6-2, Item 1.a is revised to 
    read trip setpoint and allowable values of less than or equal to 
    0.63 W + 41% and less than or equal to 0.63 W + 43%, respectively.
        b. Technical Specification 3.4.1.1.2.a.5.a is being revised to 
    read trip setpoint and allowable values of less than or equal to 
    0.63 W + 35% and less than or equal to 0.63 W + 37%, respectively.
        1. No. These Technical Specification changes do not represent a 
    change from current limits. The change reflects the rescaling made 
    necessary by the re-definition of rated thermal power.
        The RBM flow biased rod blocks are used in the Rod Withdrawal 
    Error (RWE) analysis. In order to maintain Critical Power Ratio 
    (CPR) margins similar to previous Susquehanna cycles, the flow 
    biased rod blocks were changed in terms of megawatts thermal but the 
    change was not appreciable. The rescaling of the RBM flow biased rod 
    block to reflect the re-definition of Rated Thermal Power maintains 
    the same level of protection as previously provided. Therefore, the 
    proposed change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. No. These changes do not represent a change from current 
    limits but are rather a rescaling made necessary by the re-
    definition of rated thermal power.
        3. No. These changes do not represent a change from current 
    limits but are rather a rescaling made necessary by the re-
    definition of rated thermal power. The rescaling of the RBM flow 
    biased rod block maintains the same level of protection as 
    previously provided.
        Specification Table 3.3.6-2, Item 2.a, Control Rod Block 
    Instrumentation Setpoints
        The APRM rod block upscale value has been changed to add a high 
    flow clamp setpoint at 108% with a high flow clamped allowable value 
    at 111%.
        1. No. The addition of the high flow clamp to the flow biased 
    APRM rod block function maintains the normal margins between the rod 
    block and the scram power levels in the increased core flow regions. 
    When the reactor core flow is greater than 100 million lbm/hr, the 
    APRM clamp provides an alarm to help the operator avoid scrams while 
    operating in the ICF region. This action does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. No. The changes maintain the normal margins between the rod 
    block and the scram power levels in ICF regions. The clamp provides 
    an alarm to avoid scrams in the ICF region.
        3. No. The changes maintain the normal margins between the rod 
    block and the scram power levels.
        Specification Table 3.3.6-2, Item 6.a, Reactor Coolant System 
    Recirculation Flow Upscale Rod Block Setpoint and Allowable Value 
    Change
        The reactor coolant system recirculation flow upscale rod block 
    setpoint and allowable value are being increased to 114/125 
    divisions of full scale and 117/125 divisions of full scale 
    respectively.
        1. No. The Reactor Coolant System recirculation flow upscale rod 
    block setpoint and allowable value are being increased to allow 
    operation in the ICF region. The 114/125 divisions setpoint and 117/
    125 divisions allowable value, specified by General Electric, are 
    based on BWR operating history.
        The purpose of the Reactor Coolant System recirculation flow 
    upscale rod block is to prevent rod movement when an abnormally high 
    increase in reactor recirculation flow exists. An increase in 
    reactor recirculation flow causes an increase in neutron flux that 
    results in an increase in reactor power. However, this increase in 
    neutron flux is monitored by the Neutron Monitoring System that can 
    provide a rod block. No design basis accident or transient analysis 
    takes credit for rod block signals initiated by the Reactor Coolant 
    Recirculation System. Therefore, this change does not increase the 
    probability or consequences of an accident previously evaluated.
        2. No. Rod block signal initiation by the Reactor Coolant 
    Recirculation System is not taken credit for in the mitigation of a 
    design basis accident or in any transient analysis.3. No. Rod block 
    signal initiation by the Reactor Coolant Recirculation System is not 
    taken credit for in any transient analysis or in the mitigation of a 
    design basis accident.
        Specification 4.4.1.1.1.2 and 4.4.1.1.2.5 Reactor Coolant System
        The reactor recirculation pump motor generator set scoop tube 
    electrical and mechanical overspeed stop setpoints are being 
    increased to a core flow of 109.5 million lbm/hr. and 110.5 million 
    lbm/hr., respectively.
        1. No. The reactor recirculation pump motor generator set scoop 
    tube stops are being increased to allow operation at core flows in 
    the ICF region of up to 108 million lbm/hr.
        The electrical stop is maintained above the maximum operating 
    core flow and below the mechanical stop. The 109.5 million lbm/hr. 
    electrical stop setpoint, specified by General Electric, is based on 
    BWR operating history. The electrical stop is a system design 
    feature and is not used in any safety analyses.
        The 110.5 million lbm/hr. mechanical stop setpoint is used in 
    transient analysis to limit core flow during a recirculation pump 
    controller failure. The 110.5 million lbm/hr. mechanical stop 
    setpoint, specified by General Electric, is also based on BWR 
    operating history. The cycle specific analyses, performed for power 
    uprate, used the 110.5 million lbm/hr. mechanical stop setpoint.
        Based on the above, this change does not involve a significant 
    increase of the probability or consequences of an accident 
    previously evaluated.
        2. No. Increasing the reactor recirculation motor generator set 
    scoop tube electrical and mechanical overspeed stop setpoints is 
    being done to allow operation at core flows in the ICF region up to 
    108 Mlbm/hr. The electrical stop setpoint is a design feature and is 
    not used in any safety analysis. The mechanical stop setpoint is 
    used in transient analysis to limit core flow during a recirculation 
    pump controller failure. Changing of this setpoint was considered in 
    appropriate transient analyses, and will not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated.
        3. No. See 1. above. This change does not significantly reduce 
    the margin of safety.
        Specification Figure 3.4.1.1.1-1, Thermal Power Restrictions
        This figure has been redrawn to reflect the new definition of 
    Rated Thermal Power to retain the same stability operating 
    restrictions in terms of megawatts thermal as were previously 
    described by this graph.
        1. No. The core thermal hydraulic stability curve and associated 
    bases are maintained at the current rod lines and power levels. 
    Those values are redefined to reflect the redefinition of rated 
    thermal power. Since the current operating restrictions are 
    maintained, power uprate has no detrimental effect on the level of 
    protection provided by these Technical Specifications. This position 
    is consistent with NEDC-31894P, Section 5.3.3 and with NEDC-31984P, 
    Section 3.2.
        2. No. The core thermal hydraulic stability curve and associated 
    bases are maintained at the current rod lines and power levels. 
    Those values are changed to reflect the redefinition of rated 
    thermal power. Since the current operating restrictions are 
    maintained, power uprate has no detrimental effect on the level of 
    protection provided and does not create the possibility for a new or 
    different kind of accident.
        3. No. The core thermal hydraulic stability curve and associated 
    bases are maintained at the current rod lines and power levels. 
    Those values are redefined to reflect the redefinition of rated 
    thermal power. Since the current operating restrictions are 
    maintained, there is no detrimental effect on the level of 
    protection provided, and therefore no significant decrease in any 
    margin of safety.
        Specifications 3.4.1.1.2.5, 3.4.1.1.2.6, Reactor Coolant System, 
    Recirculation Loops - Single Loop Operation
        Specification 3.4.1.1.2.5 is being renumbered to 3.4.1.1.2.6. A 
    new specification 3.4.1.1.2.5 is being added to specify that a 0.70 
    LHGR multiplier has been applied to Specification 3.2.4 when in 
    single recirculation loop operation.
        1. No. Operation with one recirculation loop out of service is 
    allowed, but it is not considered a normal mode of operation. Single 
    loop operation (SLO) is a special operational condition when only 
    one of the two recirculation loops is operable. In this operating 
    condition, the reactor power will be limited to less than 80% of 
    rated by the maximum achievable core flow, which is typically less 
    than 60% of rated core flow. A postulated LOCA occurring in the 
    active recirculation loop during SLO would cause a more rapid 
    coastdown of the recirculation flow than would occur in two loop 
    operation, where one active loop would remain intact. This rapid 
    coastdown causes an earlier boiling transition and deeper 
    penetration of boiling transition into the bundle, which tends to 
    increase the calculated PCT. However, the PCT effects of early 
    boiling transition are substantially offset by the mitigating effect 
    of the lower power level achievable at the start of such an event. 
    The SAFER/GESTR-LOCA analysis results for Susquehanna for SLO and 
    two loop operation are well below 2200 deg.F and are documented in 
    NEDC-32064P-1, Revision 1, ``Power Uprate with Increased Core Flow 
    Safety Analysis for Susquehanna 1 and 2'', GE Nuclear Energy, July 
    1993.
        The ECCS performance for Susquehanna under SLO was evaluated 
    using SAFER/GESTR-LOCA. Calculations for the DBA were performed 
    using both nominal and Appendix K inputs. The SLO SAFER/GESTR-LOCA 
    analysis for the DBA assumes that there is essentially no period of 
    recirculation pump coastdown. Thus, dryout is assumed to occur 
    simultaneously at all axial locations of the hot bundle shortly 
    after initiation of the event. Dryout is assumed to occur in one 
    second for the nominal case and 0.1 second for the Appendix K case. 
    These assumptions are very conservative and provide bounding results 
    for the DBA under SLO.
        The two-loop Appendix K break spectrum documented in NEDC-
    32064P-1 is representative of SLO because the two-loop spectrum was 
    analyzed assuming a one second dryout time for all axial locations 
    of the hot bundle. As shown by the two-loop break spectrum, the DBA 
    is the limiting case for SLO. With breaks smaller than the DBA, 
    there is a longer period of nucleate and/or film boiling prior to 
    fuel uncovery to remove the fuel stored energy.
        An LHGR multiplier of 0.70 will be imposed when the plant is in 
    SLO. As shown in Table 5-6 of NEDC-32064P-1, the SLO results are 
    less limiting (i.e., lower PCT's) than the results for the two loop 
    DBA LOCA.
        Thus, the licensing PCT is based appropriately on two loop 
    operation rather than SLO.
        2. No. The licensing PCT is based upon two loop operation rather 
    than SLO, thus the proposed change does not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated.
        3. No. Based on the response to Question 1 above, the proposed 
    change does not involve a significant reduction in a margin of 
    safety.
        Specification 4.4.1.1.2.3, Reactor Coolant System
        Footnote **** to this Specification is being changed to 
    reference the power uprate startup test program.
        1. No. This footnote provided a mechanism for changing the power 
    limits specified if the results of the initial startup test program 
    determined that it was necessary. The footnote is being modified to 
    allow operation at uprated power with the present power limits. 
    Should the power uprate startup test program determine a need to 
    change the power limits they will be submitted to the Commission 
    within 90 days as required by the revised footnote. This is 
    consistent with the original BWR startup test program philosophy and 
    does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. No. See 1. above; this change is administrative in nature and 
    does not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        3. No. See 1. above; this change is administrative in nature and 
    does not involve a significant reduction in a margin of safety.
        Specification 3.4.2, Reactor Coolant system, Safety Relief 
    Valves
        The safety relief valve specification is being changed to reduce 
    the number of setpoint groups from 5 to 3. Two valves will be set at 
    1175 psig plus or minus 1%, 6 will be set at 1195 psig plus or minus 
    1%. Also, the number of Operable safety valves is being increased 
    from 10 to 12.
        1. No. This change does not increase the probability of 
    occurrence of an accident previously evaluated as, with one 
    exception, the accidents described in FSAR Sections 5.2.2, 7.2.3, 
    15.1, 15.2 and 15.3 do not document any cases where the SRV's are 
    designated as the cause or initiator of an accident. The exception 
    is inadvertent safety relief valve opening which results in a 
    decrease in reactor coolant inventory and/or reactor coolant 
    temperature. The revised setpoints and proposed groupings will not 
    increase the probability of occurrence of this type of accident.
        The change does not increase the probability of occurrence of a 
    malfunction of equipment important to safety as previously evaluated 
    in the FSAR. The margin between peak allowable pressure and the 
    maximum safety setpoint is unchanged. The reactor vessel and 
    components were evaluated for the setpoint change to assure 
    continued compliance with the structural requirements of the ASME 
    Code. Analysis was performed on the effects of the setpoint change 
    for the design conditions, the normal and upset conditions and the 
    emergency and faulted conditions. The increasing RPV dome pressure 
    does not affect the design condition and, therefore, stresses remain 
    unchanged.
        The proposed change will also not adversely affect HPCI and RCIC 
    system performance.
        There is no indication that changed setpoints contribute to an 
    increase in probability of SRV malfunction. Reduction in the simmer 
    margin will be compensated for by more stringent leak test 
    requirements during valve refurbishment.
        2. No. This change does not involve any hardware changes or 
    changes in system function. Relief and safety setpoints are only 
    slightly increased and the maximum safety setpoint remains 
    unchanged, thus the margin between peak allowable pressure and the 
    setpoint remains unchanged.
        3. No. The technical specifications were reviewed for margins of 
    safety applicable to the components and systems affected by the 
    change. Analysis has been performed that demonstrates that reactor 
    pressure will be limited to within ASME Section III allowable values 
    for the worst case upset transient. The margin of safety is inherent 
    in the ASME Section III allowable pressure values.
        Specification 3.4.3.2.d, Reactor Coolant System, Operational 
    Leakage
        This specification is being revised to indicate that the 1 gpm 
    leakage rate limit currently applicable applies at the uprated 
    maximum allowable pressure of 1035 psig, plus or minus 10 psig.
        1. No. The steam dome pressure for leakage is being increased by 
    35 psig to 1035 psig (reactor design pressure). This pressure is 
    chosen on the basis of steam line pressure drop characteristics and 
    excess steam flow capability of the turbine observed during plant 
    operation up to the current rated power level. Increasing the 
    leakage rate pressure to 1035 psig is consistent with the expected 
    uprated operating pressure. Increasing the reactor steam dome 
    pressure has been analyzed and found to be within allowable limits. 
    Maintaining the leakage rate limit at 1 gpm does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. No. This change does not involve any hardware changes or 
    change in safety function. The reactor steam dome pressure has been 
    analyzed and found to be within allowable limits.
        3. No. Maintaining leakage the rate limit at 1 gpm is 
    conservative and does not involve a reduction in the margin of 
    safety.
        Specifications 3.4.6.2 and 4.4.6.2, Reactor Coolant System, 
    Reactor Steam Dome
        The reactor steam dome pressure limits have been changed to 1050 
    psig.
        1. No. Operating pressure for uprated power is increased by a 
    minimum amount necessary to assure that satisfactory reactor 
    pressure control is maintained. The operating pressure was chosen on 
    the basis of steam line pressure drop characteristics and excess 
    steam flow capability of the turbine observed during plant operation 
    up to the current rated power level. Satisfactory reactor pressure 
    control requires an adequate flow margin between the uprated 
    operating condition and the steam flow capability of the turbine 
    control valves at their maximum stroke. An operating dome pressure 
    of 1032 psig is expected and is being assumed in the transient 
    analyses. The 1050 psig limit was chosen to maintain an adequate 
    level of operating flexibility while maintaining an adequate 
    distance from the high pressure scram for trip avoidance. This limit 
    is the initial pressure value used in the overpressure protection 
    safety analysis for power uprate, for which all licensing criteria 
    have been met. Therefore, this change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. No. Based on the response to Question 1. above, the proposed 
    change does not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        3. No. As described in 1. above, the 1050 psig limit was chosen 
    to maintain an adequate level of operating flexibility while 
    maintaining an adequate distance from the high pressure scram. This 
    limit is the initial pressure value used in the over pressure 
    protection safety analysis for power uprate, for which all licensing 
    criteria have been met. Therefore, the proposed change does not 
    involve a significant reduction in a margin of safety.
        Specification 4.5.1.b.3, Emergency Core Cooling Systems
        This specification has been revised to permit a test line 
    pressure for the flow surveillance of greater than or equal to 1140 
    psig at nominal reactor operating conditions.
        1. No. Currently, the HPCI pump test acceptance criteria 
    discharge pressure is greater than or equal to 1266 psig. This is 
    based, in part, on the lowest SRV setpoint of 1146 psig plus a 1% 
    tolerance and line flow losses. For this test, the HPCI turbine is 
    supplied with steam at the nominal operating reactor pressure of 920 
    +140/-20 psig. Therefore, the test requires the HPCI pump/turbine to 
    produce an output that exceeds that which would be commensurate with 
    the input conditions. Stated differently, HPCI would be required to 
    develop a pump discharge pressure associated with a steam dome 
    pressure of 1187 psig (1175 plus or minus 1% psig), while being 
    supplied with a steam dome pressure as low as 900 psig.
        The purpose of this specification is to demonstrate that the 
    system is capable of producing the required flow at the required 
    pressure. The concern with this approach is that while it 
    demonstrates the required capability by achieving the actual 
    Technical Specification value, it requires the pump turbine to 
    ``over perform''. It also reduces the margin available to compensate 
    for normal wear and tear [that] occurs and is monitored under the 
    ASME Section XI Pump and Valve Test Program. Power uprate will be 
    further increasing the demand because of the increase in reactor 
    steam dome pressure.
        The intent of Surveillance 4.5.1b.3 is to demonstrate that the 
    HPCI System will produce its design flow rate at an expected reactor 
    pressure during a LOCA. Confirmation of the capability to achieve 
    the required flow and pressure can be satisfactorily demonstrated 
    without requiring the pump/turbine to ``over perform''. This can be 
    done by producing the nominal operating design pressure from the 
    pump with steam supplied to the turbine at nominal reactor operating 
    pressure. From these conditions extrapolation via pump affinity laws 
    will show the pump discharge pressure that would be developed at 
    emergency reactor operation conditions (i.e. lowest SRV setpoint). 
    This value could then be compared to the calculated value required 
    for assuring adequate core cooling in both SSES specific and generic 
    evaluations. The HPCI System has been evaluated and shown to be 
    capable of achieving the required pressure and flow conditions for 
    power uprate.
        Applying the method of pump affinity laws, the new Technical 
    Specification pump discharge pressure would become greater than or 
    equal to 1140 psig. This value is determined based on the maximum 
    allowable test steam dome pressure of 920 + 140 = 1060 psig, plus 
    head losses. Through the use of pump affinity laws it has been shown 
    by calculation that achieving a value of 1140 psig at nominal 
    reactor operating conditions will produce the required flow and 
    pressure during emergency conditions.
        Therefore, the Technical Specification HPCI pump discharge 
    pressure at power uprate conditions is changed to greater than or 
    equal to 1140 psig.
        2. No. The methodology and the supporting change described above 
    in the response to Question 1 above do not alter the function nor 
    the operation of the HPCI system. Therefore, they do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. No. The methodology and the supporting change described above 
    in response to Question 1 do not involve a significant reduction in 
    a margin of safety.
        Specification 5.4.2, Design Features, Reactor Coolant System, 
    Volume
        This specification is being changed to show that the nominal 
    Tave is being changed from 528 deg.F to 532 deg.F. This change 
    is being made to reflect the higher average saturation temperature 
    that results from a 30 psi increase in reactor design pressure.
        1. No. The effects of power uprate have been evaluated to ensure 
    that the increase in system temperatures causes minor increases in 
    thermal loadings on pipe supports, equipment nozzles, and in-line 
    components. The results of analyses show that at uprated conditions 
    all ASME components will satisfy design specification requirements 
    and code limits when evaluated to the rules of Subsection NB-3600 of 
    the ASME Boiler and Pressure Vessel Code Section III. The effects of 
    thermal expansion as a result of power uprate were found to be 
    insignificant. Therefore, this change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. No. Increases in system temperatures as a result of power 
    uprate have been evaluated to show that increase in thermal loadings 
    on pipe supports, equipment nozzles and in-line components are 
    minor. Analysis shows that at all uprated conditions all ASME 
    components will satisfy design specification requirements and code 
    limits when evaluated to the rules of subsection NB-3600 of Section 
    IV to the Boiler and Pressure Vessel Code. The effects of power 
    uprate with respect to thermal expansion were found to be 
    insignificant and, therefore, not found to create the possibility of 
    a new or different kind of accident.
        3. No. As stated above, the effects of thermal expansion as a 
    result of power uprate were found to be insignificant. Consequently, 
    the nominal increase in Tave does not involve a significant 
    reduction in a margin of safety.
        Specification Table 5.7.1-1, Component Cyclic or Transient 
    Limits
        This specification is being changed to raise the upper limit for 
    a heat cycle from 546 deg.F to 551 deg.F. This change is being made 
    to reflect the higher average saturation temperature that results 
    from a 30 psi increase in reactor design pressure.
        1. No. The purpose of this specification is to limit the number 
    of heatup and cooldown cycles. The effects of power uprate have been 
    evaluated to ensure that the reactor vessel components continue to 
    comply with the existing structural requirements of the ASME Boiler 
    and Pressure Vessel Code. The analyses were performed for the 
    design, normal, upset, emergency and faulted conditions. The 
    increase in the temperature limitation is not significant with 
    respect to the affect it has upon the RPV and associated components.
        2. No. The effects of uprating power have been evaluated for the 
    design, normal, upset, emergency and faulted conditions to ensure 
    that the reactor vessel components continue to comply with the 
    existing structural requirements of the ASME Boiler and Pressure 
    Vessel Code. The increase in the temperature limitation has been 
    found not to be significant and, therefore, does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. No. This specification is intended to limit the number of 
    heatup/cooldown cycles. The increase in the temperature limitation 
    has not been found to be significant with respect to its effects 
    upon the RPV and its associated components and, therefore, does not 
    significantly reduce the margin of safety.
        Specification 6.9.3.2, Core Operating Limits Report
        Administrative Control Section 6.9.3.2 describes and lists 
    topical reports that are used to determine core operating limits. 
    Topical reports 15 through 19 are LOCA methodology reports and are 
    being deleted. These reports describe Siemens LOCA methodology. As 
    stated in Reference 1, the GE SAFER/GESTR LOCA methodology is being 
    used for this uprated cycle. In addition, other minor methodology 
    changes were made for power uprate transient analysis. GE topical 
    report NEDC-32071P, PP&L topical report NE-092-001 and the NRC 
    Safety Evaluation Report on the PP&L power uprate licensing topical 
    are proposed to be added as Topical Reports No. 15, 16, and 17, 
    respectively.
        1. No. These changes are editorial in nature in that only the 
    references to documents are being changed. The methodology used to 
    determine core limits have been previously reviewed and approved by 
    the NRC.
        2. No. See the response to Question 1 above.
        3. No. See the response to Question 1 above.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: Osterhout Free Library, Reference 
    Department, 71 South Franklin Street, Wilkes-Barre, Pennsylvania 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: Mohan C. Thadani, Acting
    
    Pennsylvania Power and Light Company, Docket Nos. 50-387 and 50-388 
    Susquehanna Steam Electric Station, Units 1 and 2, Luzerne County, 
    Pennsylvania
    
        Date of amendment request: July 27, 1994
        Description of amendment request: This amendment will change the 
    definition of a CORE ALTERATION included in Technical Specification 
    Section 1.0 for each unit to allow movement and replacement of local 
    power range monitors and control rods in a defueled cell. The new 
    definition is consistent with the Improved Standard Technical 
    Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. In the submittal, the licensee stated that:
        I. This proposal does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed change eliminates two previous evolutions, LPRM and 
    Control Rod movement from a defueled cell, from being considered 
    CORE ALTERATIONS. Thus the issue is whether the elimination of these 
    constraints could contribute to a significant increase in the 
    probability or consequences of a reactivity event.
        Adding local power range monitors to the list of detectors which 
    can be moved without invoking CORE ALTERATION requirements allows 
    for the removal of these detectors for repair and replacement. 
    Movement of these components does not impact the reactivity of the 
    core. Therefore, allowing the movement of these detectors without 
    invoking CORE ALTERATION provisions, does not contribute to a 
    significant increase in the probability or consequences of a 
    reactivity event.
        Removal of a Control Rod from a defueled cell results in a 
    negligible increase in core reactivity. Appropriate Technical 
    Specification controls and refueling interlocks are applied during 
    the fuel movements preceding the control rod removal to protect from 
    or mitigate a reactivity excursion event. In addition, the design of 
    a control rod precludes its replacement without all fuel assemblies 
    in the cell removed. Therefore, allowing the movement of control 
    rods from a defueled cell without invoking CORE ALTERATION 
    provisions, does not contribute to a significant increase in the 
    probability or consequences of a reactivity event.
        The proposed Technical Specification change to adopt the revised 
    CORE ALTERATION definition (NUREG 1433, as amended) does not effect 
    the probability or consequences of an accident previously evaluated.
        II. This proposal does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed change eliminates two previous evolutions, LPRM and 
    Control Rod movement from a defueled cell, from being considered 
    CORE ALTERATIONS. Thus the issue is whether the elimination of these 
    constraints could create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        For local power range monitors, Technical Specification 3/4.3.1 
    defines the minimum number of LPRMs required to be maintained 
    operable in OPCON 5 and during Shutdown Margin Demonstration. The 
    addition of LPRMs as an exclusion under the CORE ALTERATION 
    definition does not change the operability requirements for the 
    LPRMs under Technical Specification 3/4.3.1. Thus the ability of the 
    LPRMs to perform their monitoring function is not affected by the 
    proposed CORE ALTERATION definition change. In addition, movement of 
    these components does not impact the reactivity of the core. 
    Therefore, allowing the movement of these detectors without invoking 
    CORE ALTERATION provisions, does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        For Control Rods, in the unlikely event that the wrong control 
    rod was inadvertently withdrawn from a fueled cell during evolutions 
    which were not intended to be CORE ALTERATIONS, adequate protective 
    measures are provided by design and core monitoring instrumentation 
    required to be operable in OPCON 5. Withdrawal of a single control 
    rod from a cell containing fuel is bounded by Shutdown Margin 
    analysis and demonstration. However, assuming the inadvertent 
    control rod withdrawal resulted in a significant reactivity 
    addition, the Reactor Protection System (RPS) would respond by 
    inserting all control rods via the Scram function. The RPS monitors 
    for recriticality during OPCON 5 with SRMs (except during specific 
    controlled evolutions), IRMs, and APRMs. The Scram circuitry is 
    completely redundant from the insert and withdrawal circuitry for 
    the control rods. Therefore, allowing the movement of control rods 
    from a defueled cell without invoking CORE ALTERATION provisions, 
    does not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The proposed Technical Specification change to adopt the revised 
    CORE ALTERATION definition (NUREG 1433, as amended) does not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        III. This change does not involve a significant reduction in a 
    margin of safety.
        To evaluate the potential effect on safety margin, the proposed 
    change was evaluated as to its effect on Shutdown Margin. Shutdown 
    Margin defines the amount of reactivity by which the reactor is 
    subcritical, and thus is a measure of the safety margin in avoiding 
    unanticipated criticality events.
        The movement of LPRMs does not impact the reactivity of the 
    core, and thus does not reduce the Shutdown Margin. Removal of a 
    Control Rod from a defueled cell results in a negligible increase in 
    core reactivity. Therefore, the removal of a Control Rod from a 
    defueled cell will have a negligible effect on the core Shutdown 
    Margin. Per Technical Specification 3/4.9.10.2(c), adequate core 
    Shutdown Margin must exist during refueling when multiple control 
    rods and the surrounding fuel assemblies are removed from the core. 
    Appropriate Technical Specification controls and refueling 
    interlocks are applied during the fuel movements preceding the 
    control rod removal to protect from or mitigate a reactivity 
    excursion event. In addition, the core is analyzed to maintain 
    Shutdown Margin even with the withdrawal of the highest worth rod 
    from a fueled cell.
        The proposed Technical Specification change to adopt the revised 
    CORE ALTERATION definition (NUREG 1433, as amended) does not involve 
    a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: Osterhout Free Library, Reference 
    Department, 71 South Franklin Street, Wilkes-Barre, Pennsylvania 18701
        Attorney for licensee: Jay Silberg, Esquire, Shaw, Pittman, Potts 
    and Trowbridge, 2300 N Street NW., Washington, DC 20037
        NRC Project Director: Mohan Thadani, Acting
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: July 20, 1994
        Description of amendment request: The amendments would raise the 
    Steam Leakage Detection system set-points that isolate the High 
    Pressure Coolant Injection System (HPCI) and Reactor Core Isolation 
    Cooling (RCIC) system equipment on high equipment room temperature and 
    high delta temperature. The amendments are supported by a Limerick 
    Generating Station modification to increase the environmental 
    qualifications limits of the HPCI and RCIC systems to allow the systems 
    to remain operable when equipment room cooling is unavailable.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specifications changes do not involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated.
        Those accident which are potentially impacted by these changes 
    are any accident or events that require the isolation of the HPCI or 
    RCIC system steam supply lines. This would include gross failures 
    (pipe breaks) or significant leaks (pipe cracks) in steam lines. 
    Minor leaks that do not significantly affect the environment in the 
    equipment compartments are only considered with regard to being 
    potential precursors to the development of a larger crack or break. 
    The ability to detect small steam leaks is not dependent on the 
    isolation instrumentation and the proposed changes to the isolation 
    instrumentation will not impact the detection methods.
        The proposed TS changes will not increase the probability of an 
    accident since the changes will only increase the trip set-points of 
    the instrumentation which detect increases in the temperature in the 
    HPCI and RCIC equipment rooms. The physical establishment and 
    setting of the proposed set-points of these accident detection and 
    mitigation instruments will have no direct physical impact on the 
    plant's normal operating conditions. This instrumentation is 
    normally in a ``monitoring mode,'' and is not actively supporting 
    normal plant operation. Therefore, the proposed set-points can have 
    no impact on the operating plant that would make an accident more 
    likely to occur.
        Two perspectives were evaluated regarding the potential impact 
    on the consequences of accidents. One case is the impact on 
    accidents which do not require HPCI or RCIC steam line isolation, 
    but that may require the operation of the HPCI or RCIC Systems. The 
    other case is the impact resulting from HPCI and RCIC steam line 
    break accidents.
        In the first case, the proposed changes to the set-points of 
    these accident mitigation instruments will have no direct physical 
    impact on the plant's accident response, except during the HPCI or 
    RCIC pipe break accidents. During all other pipe breaks or 
    accidents, the bounding peak HPCI and RCIC equipment compartment 
    temperatures will still be at least 35 deg.F below the proposed TS 
    lower allowable values (i.e., 218 deg.F and 198 deg.F, 
    respectively), and the isolation instrumentation will remain in a 
    ``monitoring mode.'' The isolation instrumentation will only be 
    required to continue to passively monitor the HPCI and RCIC 
    compartment temperatures and will meet the design basis by not 
    inadvertently isolating the HPCI or RCIC systems.
        In the second case, the HPCI and RCIC pipe break accidents 
    described in LGS, Updated Final Safety Analysis Report (UFSAR) 
    Section 3.6 ``Protection Against Dynamic Effects Associated with the 
    Postulated Rupture of Piping,'' determine the peak pressures and 
    temperatures for the affected compartments. These peak pressures for 
    the HPCI and RCIC breaks are the bounding pressures for breaks in 
    these lines and, since they occur quickly, they are unaffected by 
    the leak detection and isolation actuation systems. The peak 
    pressures predicted in the UFSAR for the largest HPCI and RCIC steam 
    line breaks, in the HPCI, RCIC and isolation valve compartments, are 
    the bounding values for breaks of all sizes in these compartments. 
    In addition, the peak temperatures are not affected by the proposed 
    changes to the isolation actuation set-points. Therefore, the 
    isolation of the HPCI and RCIC steam lines following a HPCI or RCIC 
    steam line guillotine break is not dependent on the temperature trip 
    functions, rather, the isolation is dependent on the high flow or 
    low pressure trip functions where a delay in the response of the 
    temperature isolation instrumentation will have no adverse impact on 
    the consequences of the accidents described in the SAR.
        An evaluation was performed to determine the potential impacts 
    due to the proposed changes affecting the room temperatures used in 
    the environmental qualification program. The results of this 
    evaluation determined that the postulated peak temperatures for the 
    HPCI pump room and the HPCI and RCIC piping areas would be at the 
    saturation temperature for the HPCI or RCIC break blow-down in these 
    compartments, therefore, these compartment temperatures values will 
    not be exceeded. The RCIC pump room and isolation valve compartment 
    environmental qualification temperatures were not postulated to be 
    at the saturation temperature. However, this does not increase the 
    consequences of any of the accident described in the SAR because the 
    equipment which is normally required for RCIC system operation and 
    which is located in the RCIC pump compartment is not required to 
    operate following breakage of the RCIC steam supply line. The only 
    equipment in the RCIC pump compartment that is required to operated 
    following a RCIC steam line break is the RCIC leak detection 
    instrumentation which are qualified to operate at temperatures 
    greater than the saturation temperature. Finally, the isolation 
    valve compartment postulated peak temperatures result from a HPCI 
    steam line break in the Unit 1 and 2 isolation valve compartments. 
    This line break produces the highest isolation valve compartment 
    temperatures which bounds the results of a RCIC steam line break in 
    the isolation valve compartment and the HPCI and RCIC steam lien 
    breaks in the HPCI and RCIC pump rooms and piping areas. However, 
    since the leak detection and isolation actuation trip set-points for 
    the instruments in the isolation valve compartment are not being 
    changed, then the environmental conditions in the isolation valve 
    compartment will remain unchanged. This will assure that the 
    isolation valves will be able to provide isolation when required.
        For HPCI or RCIC leaks, the environmental conditions were not 
    the only design basis considerations evaluated. The radiological 
    affects were also considered. By increasing the upper allowable high 
    ambient temperature or high delta temperature values for certain 
    line break sizes there will be a larger total mass blow-down from 
    the break due to the corresponding lengthening of the time to reach 
    the higher temperature limit. However, the total integrated mass of 
    blowdown prior to isolation of the HPCI or RCIC steam line break 
    will still be bounded by the LGS UFSAR accident analysis and 
    therefore, the radiological consequences of these breaks as 
    described in the SAR will remain unchanged. These conclusions are 
    supported by an evaluation that provided the design basis for the 
    main steam line break and then examines the radiological 
    consequences at the upper and lower end of the HPCI and RCIC break 
    spectrum. Since the largest HPCI and RCIC breaks are isolated based 
    on high flow and not based on compartment temperature increases, 
    then the proposed changes in the temperature set-points have no 
    impact on the radiological consequences of the design basis HPCI or 
    RCIC pipe break accidents as described in the SAR.
        The impact of the proposed changes on the probability of a 
    malfunction of the system isolation instrumentation, valves, or the 
    HPCI or RCIC systems was evaluated. The isolation actuation 
    instruments are qualified for the expected environmental conditions 
    and the proposed set-points are within the normal operating range of 
    the instruments. Therefore, these isolation actuation instruments 
    are more likely to randomly fail than before. In addition, by 
    ensuring that there is no adverse impact on the ability of the HPCI 
    or RCIC systems to respond to events which are caused by 
    malfunctions of equipment, then the consequences of these events are 
    not increased. An adequate margin between the proposed lower 
    allowable trip values and the postulated equipment room 
    environmental conditions is being maintained such that an 
    inadvertent actuation of the HPCI or RCIC system isolation function 
    is also no more likely to occur. The increase in the temperature 
    isolation allowable trip values will allow increased blow-down from 
    a pipe break or crack which will result in higher pump compartment 
    temperatures and pressures than before for a given break size; 
    however, the overall impact is still bounded by the LGS UFSAR 
    Section 3.6 ruptured piping analyses. The isolation actuation 
    instruments are qualified for the expected environmental conditions, 
    and the proposed set-points are also within the normal operating 
    range of the isolation instruments. Therefore, the instruments are 
    no more likely to randomly fail and cause the loss of the HPCI or 
    RCIC system than before. In fact, by increasing the qualification 
    limits of the HPCI and RCIC systems, the systems will be able to 
    remain operable with an even large steam leak in the room when room 
    cooling is available. Therefore, the changes will have no impact on 
    the operating plant that would increase the possibility or 
    consequences of a malfunction of equipment important to safety.
        Since the proposed changes will maintain the HPCI or RCIC steam 
    isolation system design basis, where the consequences are bounded by 
    an analysis contained in the LGS UFSAR, and will only change the 
    set-points of the existing instrumentation without impacting 
    equipment important to safety, the proposed Technical Specifications 
    changes do not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed TS changes will not create the possibility of a 
    different type of accident or malfunction of equipment since the 
    changes will only increase the trip set-points of the 
    instrumentation which detect increases in the temperature in the 
    HPCI and RCIC equipment rooms. The physical establishment and 
    resetting of the set-points of these accident detection and 
    mitigation instruments will have not direct physical impact on the 
    plant's normal operating conditions and will not create any new 
    accident initiators or failure modes. The severity of the potential 
    piping system pressure transients caused by the isolation of the 
    HPCI or RCIC steam lines at higher room temperatures remains 
    unchanged since the isolation occurs after the postulated break 
    blow-down has dropped to its steady state rate. Therefore, the 
    changes will not result in a pipe break or result in any malfunction 
    of equipment that has not previously been postulated to occur.
        Therefore, the proposed set-points will not create the 
    possibility of a different type of accident or possibility of a 
    different type of malfunction of equipment important to safety than 
    previously evaluated in the SAR.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The margin of safety for the isolation actuation instrumentation 
    as defined in the TS bases is not reduced. The proposed system 
    isolation TS trip set-points were selected to provide equivalent 
    margins that ensure the effectiveness of the isolation systems to 
    mitigate the consequences of accidents without compromising the 
    operability of the HPCI and RCIC systems. The proposed trip set-
    points and proposed allowable value ranges maintain adequate margins 
    between these new values and the operating range of the HPCI and 
    RCIC systems in order to prevent the inadvertent actuation of the 
    isolation system and the loss of either the HPCI or RCIC systems. 
    The differences between the trip set-points and the allowable values 
    are being maintained as an allowance for instrument drift. The trip 
    set-points and the allowable ranges are within the specified range 
    of the instruments and therefore, the accuracy and drift will 
    provide the same margin of safety as previously assumed.
        Therefore, the proposed TS change do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: Pottstown Public Library, 500 High 
    Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: Mohan C. Thadani, Acting
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: July 22, 1994
        Description of amendment request: This amendment would remove the 
    surveillance frequency details which govern 10 CFR 50, Appendix J, Type 
    B and C testing from Technical Specifications.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The proposed Technical Specifications changes do not involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated.
        The proposed changes involve the removal of repetitious 
    surveillance details from TS also found in 10 CFR 50, Appendix J, 
    and rewording of TS. The removal and rewording involves no technical 
    changes to the existing TS. The changes to the existing TS are 
    proposed in order to be consistent with NUREG-1433. During the 
    development of NUREG-1433, certain wording preferences or English 
    language conventions were adopted. The proposed changes to this TS 
    section are administrative in nature and do not impact initiators of 
    analyzed events. They also do not impact the assumed mitigation of 
    accidents or transient events. Therefore, the changes do not involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes do not involve a physical alteration of the 
    plant or changes in methods governing normal plant operation. The 
    proposed changes will not impose any new or different requirements 
    or eliminate any existing requirements. Therefore, the changes do 
    not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The changes are administrative in nature and will not involve 
    any technical changes. The proposed changes will not reduce a margin 
    of safety because they have no impact on any safety analysis 
    assumptions. In addition, because the changes are administrative in 
    nature, no question of safety is involved. Therefore, the changes do 
    not involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: Pottstown Public Library, 500 High 
    Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: Mohan C. Thadani, Acting
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of amendment request: August 19, 1994
        Description of amendment request: This change would reduce the 
    minimum setpoints and allowable values for the Steam Generator Level - 
    Low-Low and Low reactor protection system signals. The bases would also 
    be modified to expand the description of the relationship between 
    setpoints, allowable values and the plant safety analysis.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. do not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The Steam Generator Water Level--Low-Low signal and the Low 
    Steam Generator Level coincident with Steam Flow/Feed Flow Mismatch 
    signal are designed to mitigate design basis transients involving 
    significant reductions of steam generator inventory (e.g., Loss of 
    Normal Feedwater, Turbine Trip, Loss of Offsite Power, Feedwater 
    Line Break). The setpoints and allowable values for these protection 
    signals are prescribed by Technical Specifications such that 
    performance of the signals is consistent with the plant safety 
    analyses, considering the effects of channel uncertainties. The 
    proposed reductions to the setpoints and allowable values for the 
    low-low and low steam generator level signals would not affect the 
    probability of any transient that the protection signals are 
    designed to mitigate. The changes would reduce the probability of 
    unnecessary reactor trips and Auxiliary Feedwater (AFW) system 
    actuations by providing greater operating margin for plant 
    evolutions involving steam generator level changes (e.g., plant 
    startup). Therefore, the proposed changes do not involve any 
    increase in probability of an accident previously evaluated.
        The changes to the Steam Generator Water Level--Low-Low signal 
    would not result in any increase in consequences of a previously 
    analyzed accident because the proposed setpoint and allowable value 
    would continue to ensure the safety analysis assumptions remain 
    valid. As described in the accompanying changes to the Technical 
    Specifications Bases, the channel uncertainty calculations performed 
    to establish the relationships between the setpoints, allowable 
    values and safety analyses are consistent with NRC Regulatory Guide 
    1.105, Revision 2. Low Steam Generator Level coincident with Steam 
    Flow/Feed Flow Mismatch signal is not credited in the UFSAR Chapter 
    15 safety analyses. The proposed changes to the low steam generator 
    level setpoint and allowable value would continue to provide 
    reliable backup to the low-low level trip signal, consistent with 
    IEEE-279-1971. Therefore, the proposed changes would not involve an 
    increase in consequences of any previously analyzed accident.
        2) do not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        The proposed changes would continue to ensure the appropriate 
    reactor protection system functions (reactor trip and AFW 
    initiation) are initiated in the event that steam generator water 
    level decreases to the value used in the plant safety analyses. The 
    proposed changes would not involve any changes in protection system 
    logic or function, and do not involve any plant configurations that 
    could adversely affect the initiation or progression of any accident 
    sequence. Therefore, the proposed changes do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3) do not involve a significant reduction in a margin of safety.
        The proposed setpoints and allowable values would continue to 
    ensure that the assumptions in the safety analyses remain valid, 
    with appropriate consideration of protection system channel 
    uncertainties. Therefore, the proposed changes do not involve a 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: Salem Free Public library, 112 West 
    Broadway, Salem, New Jersey 08079
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW, Washington, DC 20005-3502
        NRC Project Director: Mohan C. Thadani, Acting
    
    South Carolina Electric & Gas Company, South Carolina Public 
    Service Authority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of amendment request: July 20, 1994
        Description of amendment request: The proposed change would modify 
    the Virgil C. Summer Nuclear Station (VCSNS) Technical Specification 
    (TS) Tables 2.2-1, ``Reactor Trip System Instrumentation Setpoints,'' 
    and 3.3-4, ``Engineered Safety Features Actuation System 
    Instrumentation Trip Setpoints,'' and several associated bases. The 
    proposed change would remove three columns from the Tables. The columns 
    contain specific rack and sensor allowable drift values.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Operation of VCSNS in accordance with the proposed license 
    amendment does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        This change does not alter or delete any setpoints or Allowable 
    Values, and as such, has no affect on any assumptions used for 
    accident analysis. No hardware or software changes are involved, so 
    no common mode or common cause failures can occur as a result of 
    this change. This change has no impact on the daily operation of 
    VCSNS. The performance of periodic calibrations and channel checks 
    will assure the setpoints remain within tolerance. Since this 
    amendment request affects only information that is no longer used in 
    the daily operation of the plant and has no impact on accident 
    analysis, the probability or consequences of an accident previously 
    evaluated are not increased.
        2. The proposed license amendment does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        This change revises two TS tables which contain both setpoints 
    and Allowable Values as well as other information for safety trip 
    functions. However, the revision only deletes three columns of data 
    that were used in determining the operability of one channel of the 
    safety function. These values are also used in determining the 
    setpoints and are based on measured or published tolerances and 
    uncertainties. Although these columns are being deleted, no changes 
    to any hardware, software, or setpoints will occur. Since these 
    changes do not have any plant impact, no new failure mechanisms are 
    introduced. Only the information not used on a daily basis is being 
    removed from these tables; this will not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed license amendment does not involve a significant 
    reduction in a margin of safety.
        This change revises the format of TS Tables 2.2-1 and 3.3-4 
    which list the setpoint and Allowable Values for safety trip 
    functions. The data that is being removed from these tables was used 
    to establish clear reportability requirements for any portion of one 
    channel of any of the listed safety trip functions. Since the 
    reporting requirements have changed and an LER is not required if 
    one coincident channel is inoperable, this data is no longer used in 
    daily operations. The margin of safety was established when 
    setpoints and Allowable Values were determined, and no changes to 
    these values are involved. There is no reduction in a margin of 
    safety that could affect the plant, SCE&G employees, or the public.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: Fairfield County Library, Garden and 
    Washington Streets, Winnsboro, South Carolina 29180
        Attorney for licensee: Randolph R. Mahan, South Carolina Electric & 
    Gas Company, Post Office Box 764, Columbia, South Carolina 29218
        NRC Project Director: David B. Matthews
    
    South Carolina Electric & Gas Company, South Carolina Public 
    Service Authority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of amendment request: July 20, 1994
        Description of amendment request: The proposed change would modify 
    the Virgil C. Summer Nuclear Station, Unit 1, (VCSNS) Technical 
    Specifications (TS) to allow alternative, equivalent testing of diesel 
    fuel used in the emergency diesel generators (EDG). These alternative 
    methods are necessary due to recent changes in Environmental Protection 
    Agency (EPA) regulations that are designed to limit the use of high 
    sulfur fuels.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. The probability or consequences of an accident previously 
    evaluated is not significantly increased.
        The change in testing methods for the EDG fuel oil has no impact 
    on the probability or consequences of any design basis accident. 
    These tests have been determined to be equivalent to the previously 
    approved testing methods and are needed due to changes in the EPA's 
    regulations regarding sulfur in motor vehicle fuels. The dye used to 
    identify high sulfur fuels will have no adverse affect on the 
    performance of the EDG's. The proposed testing assures a continued 
    high level of quality of the diesel fuel received and stored on 
    site.
        The change in revision level of a reference in TS section 
    6.9.1.11 has no impact on the probability of occurrence or 
    consequences of any design basis accident. All design and 
    performance criteria will continue to be met and no new single 
    failure mechanisms will be created. The change in revision level for 
    WCAP-10216-P-A does not involve any alterations to plant equipment 
    or procedures which could affect any operational modes or accident 
    precursors. This change only incorporates by reference, the 
    methodology for determining the penalty to be used in calculating 
    Core Operating Limits. This methodology allows the penalty to be 
    cycle specific and is primarily affected by the core configuration. 
    This penalty is used for normal operation and provides more 
    conservatism to the core operation for the cycle.
        2. [The proposed license amendment does not] create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The change in testing methods for the EDG fuel oil will not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated. These tests have been determined 
    by the EPA and other organizations to be equivalent to the 
    previously approved testing methods. The effect of the blue dye, 
    used to identify high sulfur fuels, on the performance of the EDGs 
    has been evaluated and determined to be insignificant. The testing 
    proposed assures a continued high level of quality for the diesel 
    fuel received and stored on site.
        The change of revision level of a reference in TS section 
    6.9.1.11 has no impact on the probability of occurrence or 
    consequences of any design basis accident. All design and 
    performance criteria will continue to be met and no new single 
    failure mechanisms will be created. The change in revision level for 
    WCAP-10216-P-A does not involve any alterations to plant equipment 
    or procedures which could affect any operational modes or accident 
    precursors. This change only incorporates, by reference, the 
    methodology for determining the penalty to be used in calculating 
    Core Operating Limits. This methodology allows the penalty to be 
    cycle specific and is primarily affected by the core configuration. 
    This penalty is used for normal operation and provides more 
    conservatism to the core operation for the cycle.
        3. [The proposed license amendment does not] involve a 
    significant reduction in a margin of safety.
        The change in testing methods for the EDG fuel oil will not 
    involve a significant reduction in a margin of safety. The proposed 
    testing methods have been determined to be equivalent to the 
    previously approved testing methods. The test for sulfur assures 
    that the sulfur content is within the allowable range for weight-
    percent. The test for color and clarity assures that the fuel is 
    relatively free of water and particulate contaminants. The proposed 
    tests provide at least an equivalent level of quality and 
    repeatability for the fuel oil analysis, thus assuring that the 
    margin of safety is not reduced.
        The change in revision level of a reference in TS section 
    6.9.1.11 does not change the proposed reload design or safety 
    analysis limits for each cycle reload core. The associated change to 
    WCAP-10216-P-A due to the revision will be specifically evaluated 
    using approved reload design methods. The larger penalty actually 
    provides for an increase in margin during certain burnup ranges. 
    Since the safety analysis limits are unaffected, and the cycle 
    specific analysis will show that the analysis limits are met, the 
    change proposed will have no adverse impact on a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: Fairfield County Library, Garden and 
    Washington Streets, Winnsboro, South Carolina 29180
        Attorney for licensee: Randolph R. Mahan, South Carolina Electric & 
    Gas Company, Post Office Box 764, Columbia, South Carolina 29218
        NRC Project Director: David B. Matthews
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of amendment request: August 19, 1994 (TS 93-09)
        Description of amendment request: The proposed change would revise 
    the implementation schedule for Amendment Nos. 182 and 174 from that 
    stated in the amendments when they were approved by the Commission by 
    letter dated May 24, 1994. As issued, the amendments reflected the 
    licensee's plans to implement the changes during the Unit 2 Cycle 6 
    refueling outage. However, the licensee has determined that 
    implementation would be more appropriate following the refueling outage 
    when both units are operating in 1995. No changes to the technical 
    specification pages other than those approved when the amendments were 
    issued are needed.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    determined that the no significant hazards consideration exists. This 
    analysis was provided in the original submittal for the amendment from 
    the licensee dated October 1, 1993, and was used in the preparation of 
    the amendments. The licensee has determined that this analysis remains 
    valid for the proposed revision to the implementation dates and that 
    the changes do not constitute a significant hazard. The staff 
    previously issued the proposed finding in the Federal Register (59 FR 
    4947) and there were no public comments on the finding. This analysis 
    is reproduced as follows:
        TVA has evaluated the proposed technical specification (TS) 
    change and has determined that it does not represent a significant 
    hazards consideration based on criteria established in 10 CFR 
    50.92(c). Operation of Sequoyah Nuclear Plant (SQN) in accordance 
    with the proposed amendment will not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed revision supports the implementation of design 
    logic and setpoint changes to the loss-of-power relaying. This 
    relaying is designed to ensure adequate voltage is available to 
    safety-related loads in order to enhance their operability and 
    support accident mitigation functions and to provide for auxiliary 
    feedwater (AFW) pump starts. The design changes alter relay logic 
    and delete unnecessary relaying, but do not change the diesel 
    generator (D/G) start and load-shedding actuations that result from 
    loss-of-power conditions. Therefore, no new actuations or functions 
    have been created; and because the existing and proposed functions 
    provide for accident mitigation considerations that are not the 
    source of an accident, the probability of an accident is not 
    increased. The deletion of the 6.9-kilovolt shutdown board normal-
    feeder undervoltage relays actually reduces the potential for 
    inadvertent shutdown board blackouts as a result of short-duration 
    voltage transients or instrument failures.
        The setpoints and time delays for loss-of-power functions have 
    been modified based on the guidelines developed by the Electrical 
    Distribution System Clearinghouse as evaluated and determined 
    through detailed analysis by TVA. This design is documented in TVA 
    Calculations SQN-EEB-MS-TI06-0008, 27DAT, and DS-1-2 and is 
    available for NRC review at the SQN site. The assigned values are 
    conservative settings that will ensure adequate voltage is supplied 
    to safety-related loads for accident mitigation and safety functions 
    under normal, degraded, and loss-of-offsite-power voltage conditions 
    with appropriate time delays to prevent damage to electrical loads 
    and minimize premature or unnecessary actuations. The identification 
    of loss-of-voltage conditions is enhanced by the design changes to 
    ensure the timely sequencing of loads onto the D/G and the 
    initiation of AFW pump starts for accident mitigation. Because there 
    are no reductions in safety functions resulting from the design 
    logic, setpoint, and time-delay changes to the loss-of-power 
    instrumentation and offsite dose levels for postulated accidents 
    will not be increased, the consequences of an accident are not 
    increased.
        The applicable mode addition, TS 3.0.4 exclusion deletion, and 
    response time measurement clarification incorporated in the proposed 
    change do not affect plant functions. These changes reflect the 
    requirements that SQN has been maintaining and serve to clarify the 
    requirements to provide consistency of application and easier 
    understanding. The AFW footnote addition and bases revision only 
    clarify operability conditions that are consistent with the plant 
    design for the AFW pump and loss-of-power instrumentation. Because 
    there are no changes to plant functions or operations, these 
    revisions have no impact on accident probabilities or consequences.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        As described above, the loss-of-power instrumentation ensures 
    adequate voltage to safety-related loads by initiating D/G starts 
    and load shedding and provides for AFW pump starting, but is not 
    considered to be the source of an accident. Although the design 
    logic, setpoint, and time-delay actuation criteria have changed, the 
    output functions to various plant systems that actuate for load 
    shedding and D/G starts remain the same. Therefore, actuation 
    criteria have been affected, but not safety functions, and the TVA 
    evaluation has confirmed that the new design enhances the ability to 
    maintain adequate voltage to support safety functions. Since safety 
    functions have not changed and the new loss-of-power instrumentation 
    design continues to support operability of safety-related equipment, 
    no new or different accident is created.
        The applicable mode addition, TS 3.0.4 exclusion deletion, and 
    response time measurement clarification, as well as the AFW 
    operability clarifications, do not affect plant functions and will 
    not create a new accident.
        3. Involve a significant reduction in a margin of safety.
        The proposed loss-of-power TS changes support design logic, 
    setpoint, and time-delay requirements that have been verified by TVA 
    analysis to provide acceptable voltage levels for safety-related 
    components. In determining the acceptability of these voltage 
    levels, the minimum voltage for operation as well as detrimental 
    component heating resulting from sustained degraded-voltage 
    conditions were considered. This design ensures that safety-related 
    loads will be available and operable for normal and accident plant 
    conditions. The applicable mode addition, TS 3.0.4 exclusion 
    deletion, response time measurement clarification, and AFW 
    operability clarifications provide enhancements to TS requirements 
    and do not affect plant functions. Therefore, no safety functions 
    are reduced by these changes and there is no reduction in the margin 
    of safety.
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room: Chattanooga-Hamilton County Library, 
    1101 Broad Street, Chattanooga, Tennessee 37402
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 11H, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Philadelphia Electric Company, Public Service Electric and Gas 
    Company, Delmarva Power and Light Company, and Atlantic City 
    Electric Company, Docket Nos. 50-277 and 50-278, Peach Bottom 
    Atomic Power Station, Unit Nos. 2 and 3, York County, Pennsylvania
    
        Date of amendment request: June 23, 1993
        Brief description of amendment request: The amendments would revise 
    the licenses and the technical specifications to change the maximum 
    core power limit from 3293 MWt to 3458 MWt.Date of publication of 
    individual notice in Federal Register: August 29, 1994 (59 FR 44432) 
    Expiration date of individual notice: September 28, 1994
        Local Public Document Room: Government Publications Section, State 
    Library of Pennsylvania, (REGIONAL DEPOSITORY) Education Building, 
    Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of amendments request: August 9, 1994
        Brief description of amendments request: These amendments revise 
    the Technical Specifications (TS) 5.3.4, ``Steam and Power Conversion 
    Systems,'' and 15.3.7, ``Auxiliary Electrical Systems,'' to increase 
    the allowed outage times for one motor driven auxiliary feedwater pump 
    and for the standby emergency power for the Unit 1, Train B4160 Volt 
    safeguards bus (A06) from 7 to 12 days. The proposed amendments would 
    also modify TS 15.3.3, ``Emergency Core Cooling System, Auxiliary 
    Cooling Systems, Air Recirculation Fan Coolers, and Contained Spray,'' 
    to provide the clarification that the service water pump (P-32E) 
    operating with power supplied by the Alternative Shutdown System is 
    operable from offsite power. The changes are one-time extensions of 
    specific allowed outage times.Date of publication of individual notice 
    in the Federal Register: August 19, 1994 (59 FR 42870).
        Local Public Document Room: Joseph P. Mann Library, 1516 Sixteenth 
    Street, Two Rivers, Wisconsin 54241.
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC 20555, and at the local public document 
    rooms for the particular facilities involved.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of application for amendments: November 3, 1993
        Brief description of amendments: The amendments revise the Calvert 
    Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Technical Specifications 
    (TSs) by removing the TSs that are applicable to the incore instrument 
    (ICI) system. The limitations on the use of the ICI system will be 
    relocated to the Updated Final Safety Analysis Report. The core power 
    distribution limits, which the ICI system is used to verify, remain in 
    the TSs which is consistent with 10 CFR 50.36.Date of issuance: August 
    24, 1994Effective date: As of the date of issuance to be implemented 
    within 30 days.
        Amendment Nos.:  191 and 168
        Facility Operating License Nos. DPR-53 and DPR-69: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 8, 1993 (58 FR 
    64601) The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated August 24, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room:  Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of application for amendments: November 3, 1993
        Brief description of amendments: The amendments modify the 
    surveillance requirements to reflect the removal of the auto-closure 
    interlock from the shutdown cooling system and revises the setpoint for 
    the open permissive interlock.
        Date of issuance: August 24, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 192 and 169
        Facility Operating License Nos. DPR-53 and DPR-69: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 8, 1993 (58 FR 
    64600) The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated August 24, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of application for amendments: May 27, 1994
        Brief description of amendments: The amendments revise the 
    Technical Specification surveillance test intervals from monthly to 
    quarterly for several channel functional tests for the Reactor 
    Protection System and the Engineered Safety Feature Actuation System. 
    In addition, an administrative change was made to remove an out-of-date 
    footnote concerning the Emergency Diesel Generator logic circuit 
    modifications.
        Date of issuance: August 24, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 193 and 170
        Facility Operating License Nos. DPR-53 and DPR-69: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37062) The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated August 24, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room:  Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of application for amendments: November 5, 1993, as 
    supplemented March 11, 1994
        Brief description of amendments: The amendments consist of two 
    related changes. The first change revises the containment penetration 
    Technical Specifications (TSs) to resemble the containment penetration 
    TSs in NUREG-1432, ``Standard Technical Specifications for Combustion 
    Engineering Pressurized Water Reactors.'' The second revises the TSs to 
    allow the containment personnel airlock to be open during fuel movement 
    and core alterations. The TS Bases have also been revised to reflect 
    the changes as the result of issuing these amendments.
        Date of issuance: August 31, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment Nos.: 194 and 171
        Facility Operating License Nos. DPR-53 and DPR-69: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 8, 1993 (58 FR 
    64602) The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated August 31, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room:  Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam 
    Neck Plant, Middlesex County, Connecticut
    
        Date of application for amendment: June 16, 1994
        Brief description of amendment: The amendment removes from 
    Technical Specification 3/4.8.3, ``Onsite Power Distribution,'' a 
    footnote applicable for Cycle 18 only, and adds surveillance 
    requirement 4.8.3.1.2, to test the MCC-5 automatic bus transfer feature 
    once per refueling.
        Date of Issuance: August 23, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 176
        Facility Operating License No. DPR-61. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37067) The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated August 23, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room: Russell Library, 123 Broad Street, 
    Middletown, Connecticut 06457.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: April 28, 1994
        Brief description of amendments: The amendments revised Technical 
    Specification 4.6.1.3.e to add an option that will allow the personnel 
    airlock pneumatic system leak test to be completed in 8 hours with a 
    pressure drop of 0.50 psi.
        Date of issuance: August 29, 1994
        Effective date: August 29, 1994
        Amendment Nos.:  Unit 1 - Amendment No. 64; Unit 2 - Amendment No. 
    53
        Facility Operating License Nos. NPF-76 and NPF-80. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27057) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 29, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room: Wharton County Junior College, J. M. 
    Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments: November 15, 1993
        Brief description of amendments: The amendment revises the 
    Technical Specifications to extend the surveillance interval for the 
    chemical analysis, inventory, and flow area of the ice condenser from 9 
    to 18 months.
        Date of issuance: August 23, 1994
        Effective date: August 23, 1994
        Amendment Nos.: 180 & 164
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 22, 1993 (58 
    FR 67849) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 23, 1994. No significant 
    hazards consideration comments received: No.
        Local Public Document Room: Maud Preston Palenske Memorial Library, 
    500 Market Street, St. Joseph, Michigan 49085.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, 
    Donald C. Cook Nuclear Plant, Unit Nos. 1 and 2, Berrien County, 
    Michigan
    
        Date of application for amendments: September 24, 1992 and 
    supplemented March 2, 1994.
        Brief description of amendments: The amendment removes the list of 
    containment isolation valves and associated references to the list from 
    the Technical Specifications.
        Date of issuance: August 29, 1994
        Effective date: August 29, 1994
        Amendment Nos.:  181 and 165
        Facility Operating License Nos. DPR-58 and DPR-74. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 17, 1993 (58 
    FR 8773) The March 2, 1994, letter provided supplemental information 
    that was not outside the scope of this initial notice. The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated August 29, 1994.No significant hazards consideration 
    comments received: No.
        Local Public Document Room: Maud Preston Palenske Memorial Library, 
    500 Market Street, St. Joseph, Michigan 49085.
    
    Niagara Mohawk Power Corporation, Docket No. 50-410, Nine Mile 
    Point Nuclear Station, Unit 2, Oswego County, New York
    
        Date of application for amendment: July 1, 1994
        Brief description of amendment: The amendment revises the secondary 
    containment drawdown time testing requirement of Technical 
    Specification (TS) 4.6.5.1.c.1 and the secondary containment inleakage 
    testing requirement of TS 4.6.5.1.c.2. The amendment supports a revised 
    design basis radiological analysis which supports an increase in 
    secondary containment drawdown time from 6 to 60 minutes by taking 
    credit for fission product scrubbing and retention in the suppression 
    pool which were not assumed in the original radiological analysis but 
    are currently assumed in the NRC's Standard Review Plan (NUREG-0800). 
    The revised analysis also takes credit for additional mixing of primary 
    containment and engineered safety feature system leakage with 50 
    percent of the secondary containment free air volume prior to the 
    release of radioactivity to the environment. The revised radiological 
    evaluation has determined that the radiological doses remain below 10 
    CFR Part 100 guideline values and General Design Criterion 19 criteria.
        Date of issuance: August 30, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 56
        Facility Operating License No. NPF-69: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37074) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 30, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room: Reference and Documents Department, 
    Penfield Library, State University of New York, Oswego, New York 13126.
    
    Northern States Power Company, Docket No. 50-263, Monticello 
    Nuclear Generating Plant, Wright County, Minnesota
    
        Dates of application for amendment: November 30, 1993 and June 30, 
    1994.
        Brief description of amendment: The proposed amendment would delete 
    the requirements for a chlorine detection system from the following 
    sections of Technical Specifications: 3.2.I, 3.17.A, 4.17.A, tables 
    4.2.1 and Technical Bases 3.2 and 3.17.A. Due to design changes at the 
    Monticello Nuclear Generating Plant, chlorine is no longer stored 
    onsite as a liquified gas and regulations requiring early warning of an 
    onsite chlorine release do not apply.
        Date of issuance: August 25, 1994
        Effective date: August 25, 1994
        Amendment No.: 89
        Facility Operating License No. DPR-22. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 2, 1994 (59 FR 
    10010) The June 30, 1994, letter provided documents cited in the 
    amendment application and did not affect the staff's initial no 
    significant hazards determination. The Commission's related evaluation 
    of the amendment is contained in a Safety Evaluation dated August 25, 
    1994.No significant hazards consideration comments received: No.
        Local Public Document Room: Minneapolis Public Library, Technology 
    and Science Department, 300 Nicollet Mall, Minneapolis, Minnesota 
    55401.
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun 
    Station, Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: May 21, 1993, as supplemented by letters 
    dated September 10, 1993, and May 25, 1994
        Brief description of amendment: The amendment changed the Technical 
    specifications to reflect the relocation of the old 10 CFR 20.106 
    requirements to the new 10 CFR 20.1302, and to implement administrative 
    changes.
        Date of issuance: August 24, 1994
        Effective date: August 24, 1994
        Amendment No.: 164
        Facility Operating License No. DPR-40. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 7, 1993 (58 FR 
    36442) The additional information contained in the supplemental letters 
    dated September 10, 1993, and May 25, 1994, was clarifying in nature 
    and thus, within the scope of the initial notice and did not affect the 
    staff's proposed no significant hazards consideration determination. 
    The Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated August 24, 1994.No significant hazards 
    consideration comments received: No.
        Local Public Document Room: W. Dale Clark Library, 215 South 15th 
    Street, Omaha, Nebraska 68102
    
    Omaha Public Power District, Docket No. 50-285, Fort Calhoun 
    Station, Unit No. 1, Washington County, Nebraska
    
        Date of amendment request: February 12, 1993, as supplemented by 
    letters dated August 20, 1993, and June 6, 1994
        Brief description of amendment: This amendment revised Technical 
    Secification 2.1.4, ``Reactor Coolant System Leakage Limits,'' to 
    implement the reactor coolant system leak-before-break methodology 
    detection criteria. Additionally, administrative changes were made.
        Date of issuance: August 25, 1994
        Effective date: August 25, 1994
        Amendment No.: 165
        Facility Operating License No. DPR-40. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37076) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 25, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room: W. Dale Clark Library, 215 South 15th 
    Street, Omaha, Nebraska 68102.
    
    Pacific Gas and Electric Company, Docket Nos. 50-275 and 50-323, 
    Diablo Canyon Nuclear Power Plant, Unit Nos. 1 and 2, San Luis 
    Obispo County, California
    
        Date of application for amendments: December 8, 1993 (Ref. LAR 93-
    07)
        Brief description of amendments: The amendments revise the combined 
    Technical Specifications (TS) for the Diablo Canyon Power Plant Unit 
    Nos. 1 and 2 to revise TS 3/4.8.1, ``A.C. Sources'' to increase the 
    required quantity of emergency diesel generator (EDG) fuel oil stored 
    in the engine-mounted tank (day tank) from 200 gallons to 250 gallons. 
    The amendment also revises TS 3/4.7.11, ``Area Temperature 
    Monitoring,'' and 3/4.8.1 to remove references to a five EDG 
    configuration, based on the installation of a sixth EDG.
        Date of issuance: August 23, 1994
        Effective date: August 23, 1994
        Amendment Nos.: 93 and 92
        Facility Operating License Nos. DPR-80 and DPR-82: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 16, 1994 (59 
    FR 7694) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 23, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room: California Polytechnic State 
    University, Robert E. Kennedy Library, Government Documents and Maps 
    Department, San Luis Obispo, California 93407.
    
    Philadelphia Electric Company, Docket No. 50-352, Limerick 
    Generating Station, Unit 1, Montgomery County, Pennsylvania
    
        Date of application for amendment: June 6, 1994
        Brief description of amendment: This amendment removes the controls 
    for a remote shtudown system control valve and deletes the isolation 
    signal for certain primary containment isolation valves from TS Tables 
    3.3.7.4-1 and 3.6.3-1 respectively, as a result of eliminating the 
    steam condensing mode of the Residual Heat Removal system.
        Date of issuance: August 23, 1994
        Effective date: August 23, 1994
        Amendment Nos. 74
        Facility Operating License No. NPF-39: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37076) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 23, 1994. No significant 
    hazards consideration comments received: No
        Local Public Document Room: Pottstown Public Library, 500 High 
    Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of application for amendments: January 10, 1994, as 
    supplemented by letter dated July 20, 1994
        Brief description of amendments: The amendments relocate the 
    seismic monitoring instrumentation Limiting Condition for Operation, 
    Surveillance Requirements, and associated tables and Bases contained in 
    TS Sections 3.3.7.2 and 4.3.7.2 to the Updated Final Safety Analysis 
    Report, Section 3.7.4.
        Date of issuance: August 29, 1994
        Effective date: August 29, 1994
        Amendment Nos. 75 and 36
        Facility Operating License Nos. NPF-39 and NPF-85. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 16, 1994 (59 FR 
    12364) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 29, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room: Pottstown Public Library, 500 High 
    Street, Pottstown, Pennsylvania 19464.
    
    Philadelphia Electric Company, Public Service Electric and Gas 
    Company Delmarva Power and Light Company, and Atlantic City 
    Electric Company,Docket Nos. 50-277 and 50-278, Peach Bottom Atomic 
    Power Station,Unit Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: March 28, 1994, as supplemented 
    on June 27, 1994 and July 8, 1994
        Brief description of amendments: These amendments relocate the fire 
    protection requirements from the Technical Specifications to the 
    Updated Final Safety Analysis Report in accordance with the guidance in 
    Generic Letter (GL) 86-10, ``Implementation of Fire Protection 
    Requirements,'' and GL 88-12, ``Removal of Fire Protection Requirements 
    from Technical Specifications.''
        Date of issuance: August 24, 1994
        Effective date: August 24, 1994
        Amendments Nos.: 194 and 198
        Facility Operating License Nos. DPR-44 and DPR-56: Amendments 
    revised the Technical Specifications and the licenses.
        Date of initial notice in Federal Register: April 28, 1994 (59 FR 
    22012) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 24, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room:  Government Publications Section, State 
    Library of Pennsylvania, (REGIONAL DEPOSITORY) Education Building, 
    Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: February 3, 1994
        Brief description of amendment: The licensee commenced operating on 
    a 24-month fuel cycle, instead of the previous 18-month fuel cycle, 
    with fuel cycle 9. Fuel cycle 9 started in August 1992; however, the 
    facility has been shut down since February 1993 for a ``Performance 
    Improvement Outage'' and a restart date has not yet been established. 
    In order to accommodate operation on a 24-month cycle after the 
    facility restarts, the following Engineered Safety Features (ESF) 
    instrument calibration intervals have been extended:
        (1) Reactor coolant temperature instrument channels (specified in 
    TS Table 4.1-1)
        (2) Steam generator level instrument channels (specified in TS 
    Table 4.1-1)
        (3) Containment pressure instrument channels (specified in TS Table 
    4.1 1)
        (4) Steam line pressure instrument channels (specified in TS Table 
    4.1-1)
        (5) Turbine first stage pressure instrument channels (specified in 
    TS Table 4.1-1)
        (6) Turbine trip low auto stop oil pressure instrument channels 
    (specified in TS Table 4.1-1)
        (7) 480V bus undervoltage and alarm relays (specified in TS Table 
    4.1-1)
        These changes followed the guidance provided in Generic Letter 91-
    04, ``Changes in Technical Specification Surveillance Intervals to 
    Accommodate a 24-Month Fuel Cycle,'' as applicable.Additionally, the 
    following changes were also incorporated:
        (8) A limiting conditions for operation requirement for a wide 
    range containment pressure variable was added to TS Table 3.5-5 to 
    ensure consistency with Regulatory Guide 1.97 commitments and the IP3 
    Emergency Operating Procedures (EOPs).
        (9) A quarterly functional test surveillance requirement for the 
    low average temperature actuation circuits of the reactor coolant 
    temperature channels was added to Item 4 of TS Table 4.1-1.
        (10) Item 14 of TS Table 4.1-1 was expanded to specify surveillance 
    requirements for the wide range containment pressure instrumentation 
    channels.
        (11) Item 20 to TS Table 4.1-1 was revised to clarify that both the 
    reactor trip and the ESF actuation relay logic channels are 
    functionally tested.
        Date of issuance: September 1, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 150
        Facility Operating License No. DPR-64: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 30, 1994 (59 FR 
    14894) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 1, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room: White Plains Public Library, 100 
    Martine Avenue, White Plains, New York 10610.
    
    Power Authority of the State of New York, Docket No. 50-333, James 
    A. FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: June 17, 1993, as supplemented 
    February 24, 1994, and June 13, 1994
        Brief description of amendment: The amendment adds Section 3/
    4.2.J., ``Remote Shutdown Capability,'' and associated Table 3.2-10, 
    ``Remote Shutdown Capability Instrumentation and Controls,'' to the 
    Technical Specifications (TSs) to provide Limiting Conditions for 
    Operation and surveillance requirements for the remote/alternate 
    shutdown equipment. The amendment also adds an associated Bases section 
    to the TSs. These additions to the TSs were based on NUREG-1433, 
    ``Standard Technical Specifications - General Electric Boiling Water 
    Reactors (BWR/4).'' Several administrative changes were also made to 
    accommodate the additions to the TSs.
        Date of issuance: August 31, 1994
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 216
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 4, 1993 (58 FR 
    41511) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 31, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room: Reference and Documents Department, 
    Penfield Library, State University of New York, Oswego, New York 13126.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: March 4, 1994, as supplemented 
    on June 14, 1994 and by phone on July 22, 1994
        Brief description of amendments: These amendments modify Section 
    5.3.1 of the Technical Specifications (TS) to allow the use of 
    Westinghouse Vantage+ fuel with ZIRLO cladding. The previous TS 
    required the fuel cladding to be Zircaloy-4, which is used in the 
    Westinghouse Standard and Vantage 5H fuel designs.
        Date of issuance: August 22, 1994
        Effective date: August 22, 1994
        Amendment Nos. 154 and 134
        Facility Operating License Nos. DPR-70 and DPR-75. These amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 30, 1994 (59 FR 
    14896) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 22, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room: Salem Free Public Library, 112 West 
    Broadway, Salem, New Jersey 08079
    
    South Carolina Electric & Gas Company, South Carolina Public 
    Service Authority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of application for amendment: December 13, 1993, as 
    supplemented February 2, 1994, and March 11, 1994.
        Brief description of amendment: The amendment changes the Technical 
    Specifications to allow for the storage of fuel with an enrichment not 
    to exceed a nominal 5.0 weight percent (w/o) U-235 in the VCSNS new 
    (fresh) and spent fuel storage racks. The changes would also allow 
    UO2 with a maximum nominal enrichment up to 5.0 w/o U-235 to be 
    used as fuel in the VCSNS core.
        Date of issuance: August 23, 1994
        Effective date: August 23, 1994
        Amendment No.: 116
        Facility Operating License No. NPF-12. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 16, 1994 (59 FR 
    12365) The March 11, 1994, letter provided clarifying information that 
    did not change the initial determination of no significant hazards 
    consideration as published in the Federal Register. The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated August 23, 1994. No significant hazards consideration comments 
    received: No
        Local Public Document Room: Fairfield County Library, Garden and 
    Washington Streets, Winnsboro, South Carolina 29180.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, 
    Vermont Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: May 20, 1994
        Brief description of amendment: The proposed amendment would remove 
    Core Spray High Sparger Instrumentation from the Vermont Yankee 
    Technical Specifications for Emergency Core Cooling System Actuation 
    Instrumentation. In addition, an unrelated administrative change is 
    also made.
        Date of issuance: August 22, 1994
        Effective date: August 22, 1994
        Amendment No.: 140
        Facility Operating License No. DPR-28. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 6, 1994 (59 FR 
    34669) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 22, 1994.No significant 
    hazards consideration comments received: No
        Local Public Document Room: Brooks Memorial Library, 224 Main 
    Street, Brattleboro, Vermont 05301.
    
    Virginia Electric and Power Company, et al., Docket Nos. 50-338 and 
    50-339, North Anna Power Station, Units No. 1 and No. 2, Louisa 
    County, Virginia
    
        Date of application for amendments: June 9, 1994
        Brief description of amendments: These amendments revise the NA-1&2 
    Technical Specifications (TS) by removing the Reactor Trip System and 
    the Engineered Safety Features Actuation System response times from the 
    TS to station-controlled documents.
        Date of issuance: August 24, 1994
        Effective date: August 24, 1994
        Amendment Nos.: 187 and 168
        Facility Operating License Nos. NPF-4 and NPF-7. Amendments revised 
    the Technical Specifications.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37088) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 24, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room: The Alderman Library, Special 
    Collections Department, University of Virginia, Charlottesville, 
    Virginia 22903-2498.
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of application for amendment: January 6, 1994
        Brief description of amendment: This amendment relocates the 
    requirements related to seismic monitoring instrumentation from the 
    Technical Specifications (TS) to the Final Safety Analysis Report 
    (FSAR) and plant procedures. The existing requirements will be 
    maintained and controlled in accordance with the requirements of 10 CFR 
    50.59 and TS 6.8.1.
        Date of issuance: August 22, 1994
        Effective date:  August 22, 1994, to be implemented within 30 days 
    of issuance
        Amendment No.: 131
        Facility Operating License No. NPF-21: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 30, 1994 (59 FR 
    14902) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 22, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room: Richland Public Library, 955 Northgate 
    Street, Richland, Washington 99352.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of application for amendments: September 29, 1993.
        Brief description of amendments: The amendments changed the 
    inservice test frequency of the safety injection pumps, residual heat 
    removal pumps, and containment spray pumps from monthly to quarterly. 
    Also, the amendments added the administration of the inservice testing 
    program to TS 15.4.2. The amendments added requirements to verify the 
    containment sump suction is not blocked and to verify on a monthly 
    basis, valve alignments of the emergency core cooling system and 
    containment cooling systems.
        Date of issuance: August 25, 1994
        Effective date: Date of issuance to be implemented within 45 days
        Amendment Nos.: 150 and 154
        Facility Operating License Nos. DPR-24 and DPR-27. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: February 2, 1994 (59 FR 
    4949) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated August 25, 1994.No significant hazards 
    consideration comments received: No.
        Local Public Document Room: Joseph P. Mann Library, 1516 Sixteenth 
    Street, Two Rivers, Wisconsin 54241.
    
    Wisconsin Electric Power Company, Docket Nos. 50-266 and 50-301, 
    Point Beach Nuclear Plant, Unit Nos. 1 and 2, Town of Two Creeks, 
    Manitowoc County, Wisconsin
    
        Date of application for amendments: October 6, 1992
        Brief description of amendments: The amendments changed all 
    references of rod position in the Technical Specifications to units of 
    steps rather than inches. The amendments also changed Figure 15.3.10-1 
    by referencing rod position in units of steps instead of percent 
    withdrawn. Further, the amendments revised the basis for Section 
    15.3.10 by clarifying the definition of ``fully withdrawn'' as it 
    concerns Rod Cluster Control Assemblies, and modified the basis for 
    Section 15.3.10 to be consistent with the above changes.
        Date of issuance: August 26, 1994
        Effective date: Immediately, to be implemented within 45 days.
        Amendment Nos.: 151 and 155
        Facility Operating License Nos. DPR-24 and DPR-27. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 25, 1993 (58 FR 
    16234) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 26, 1994No significant 
    hazards consideration comments received: No.
        Local Public Document Room: Joseph P. Mann Library, 1516 Sixteenth 
    Street, Two Rivers, Wisconsin 54241.
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of amendment request: June 7, 1994
        Brief description of amendment: The amendment revises Technical 
    Specification Table 2.2-1, ``Reactor Trip System Instrumentation 
    Setpoints,'' to change the over-temperature-delta-temperature (OTDT) 
    axial flux difference (AFD) limits to reflect the results of the Cycle 
    8 core maneuvering analysis.
        Date of issuance:  August 25, 1994
        Effective date:  August 25, 1994
        Amendment No.: 79
        Facility Operating License No. NPF-42. The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 6, 1994 (59 FR 
    34672) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated Augusty 25, 1994.No significant 
    hazards consideration comments received: No.
        Local Public Document Room locations: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621.
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC 20555, 
    and at the local public document room for the particular facility 
    involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By October 14, 1994, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC 20555 and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC 20555, by the 
    above date. Where petitions are filed during the last 10 days of the 
    notice period, it is requested that the petitioner promptly so inform 
    the Commission by a toll-free telephone call to Western Union at 1-
    (800) 248-5100 (in Missouri 1-(800) 342-6700). The Western Union 
    operator should be given Datagram Identification Number N1023 and the 
    following message addressed to (Project Director): petitioner's name 
    and telephone number, date petition was mailed, plant name, and 
    publication date and page number of this Federal Register notice. A 
    copy of the petition should also be sent to the Office of the General 
    Counsel, U.S. Nuclear Regulatory Commission, Washington, DC 20555, and 
    to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of application for amendment: June 9, 1994, as supplemented 
    August 10, 1994
        Brief description of amendment: This amendment increases the 
    allowed out-of-service time from 7 days to 14 days for the automatic 
    depressurization system, the high pressure coolant injection system, 
    and the reactor core isolation cooling system. A change is also made to 
    Section 4.5.H, ``Maintenance of Filled Discharge Pipe'' to reflect 
    Amendment 149 issued September 28, 1993.
        Date of issuance: August 22, 1994
        Effective date: August 22, 1994
        Amendment No.: 156
        Facility Operating License No. DPR-35: Amendment revised the 
    Technical Specifications.Public comments requested as to proposed no 
    significant hazards consideration: No The Commission's related 
    evaluation of the amendment, consultation with the State, and final 
    determination of no significant hazards consideration are contained in 
    a Safety Evaluation dated
        Local Public Document Room: Plymouth Public Library, 11 North 
    Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Walter R. Butler
    
    Duquesne Light Company, et al., Docket No. 50-412, Beaver Valley 
    Power Station, Unit 2, Shippingport, Pennsylvania
    
        Date of application for amendment: August 17, 1994
        Brief description of amendment: The amendment changes the Technical 
    Specifications (TS) by revising Surveillance Requirement (SR) 4.6.2.2.d 
    of Limiting Condition For Operation (LCO) 3.6.2.2, entitled 
    ``Containment Recirculation Spray System,'' by adding a new footnote 
    number (1) pertaining to 2RSS*P21A pump performance requirements. In 
    addition, SR 4.6.2.2.e.2 is revised by deleting the footnote, denoted 
    by a single asterisk, which pertains to an extension to the 18-month 
    surveillance interval for first fuel cycle.
        Date of issuance: August 22, 1994
        Effective date: As of the date of issuance.
        Amendment No: 62
        Facility Operating License No. NPF-73. Amendment revised the 
    Technical Specifications.Public comments requested as to proposed no 
    significant hazards consideration: No. On August 17, 1994, the staff 
    issued enforcement discretion, which was immediately effective and 
    remained in effect until the staff's review of this amendment was 
    completed.
        The Commission's related evaluation of the amendment, finding of 
    emergency circumstances, consultation with the Commonwealth of 
    Pennsylvania and final no significant hazards considerations 
    determination are contained in a Safety Evaluation dated August 22, 
    1994.
        Local Public Document Room: B. F. Jones Memorial Library, 663 
    Franklin Avenue, Aliquippa, Pennsylvania 15001.
        Dated at Rockville, Maryland, this 7th day of September 1994.
        For The Nuclear Regulatory Commission
    Jack W. Roe,
    Director, Division of Reactor Projects - III/IV, Office of Nuclear 
    Reactor Regulation
    [Doc. 94-22593 Filed 9-13-94; 8:45 am]
    BILLING CODE 7590-01-F
    
    
    

Document Information

Published:
09/14/1994
Department:
Nuclear Regulatory Commission
Entry Type:
Uncategorized Document
Document Number:
X94-10914
Dates:
As of the date of issuance to be implemented within 30 days.
Pages:
0-0 (1 pages)
Docket Numbers:
Federal Register: September 14, 1994