97-24807. Northeast Utilities, Millstone Nuclear Power Station, Units 1, 2, and 3 and Haddam Neck Plant; Issuance of Partial Director's Decision Under 10 CFR 2.206  

  • [Federal Register Volume 62, Number 181 (Thursday, September 18, 1997)]
    [Notices]
    [Pages 49034-49043]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 97-24807]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    [Docket Nos. 50-245, 50-336, and 50-423 and Docket No. 50-213]
    
    
    Northeast Utilities, Millstone Nuclear Power Station, Units 1, 2, 
    and 3 and Haddam Neck Plant; Issuance of Partial Director's Decision 
    Under 10 CFR 2.206
    
        Notice is hereby given that the Director, Office of Nuclear Reactor 
    Regulation, has issued a Partial Director's Decision with regard to a 
    Petition dated November 25, 1996, as amended on December 23, 1996, 
    filed by Ms. Deborah Katz and Mr. Paul Gunter on behalf of the Citizens 
    Awareness Network (CAN) and the Nuclear Information and Resource 
    Service (NIRS), hereafter referred to as ``Petitioners.'' The Petition 
    pertains to the Millstone Nuclear Power Station, Units 1, 2, and 3, and 
    the Haddam Neck Plant.
        The Petitioners requested that the NRC: (1) Immediately suspend or 
    revoke Northeast Utilities' (NU's or Licensee's) licenses to operate 
    its nuclear facilities in Connecticut; (2) investigate possible 
    Licensee material misrepresentations to the NRC; (3) continue the 
    shutdown of the Licensee's facilities until the Department of Justice 
    completes its investigation and the results are reviewed by the NRC; 
    (4) continue the shutdown until the NRC evaluates and approves the 
    Licensee's remedial actions; (5) continue listing the Licensee's 
    facilities on the NRC's ``Watch List'' should any facility resume 
    operation; (6) bar any predecommissioning or decommissioning activity 
    at any of the Licensee's nuclear facilities in Connecticut until the 
    Licensee and the NRC take certain identified steps to assure that such 
    activities can be safely conducted; (7) initiate an investigation into 
    how the NRC allowed the asserted illegal situation at the Licensee's 
    nuclear facilities in Connecticut to exist and continue for more than a 
    decade; and (8) immediately investigate of the need for enforcement 
    action for alleged violation of 10 CFR Part 50, appendix B, with 
    respect to nitrogen calculations.
        The bases for the assertions are Licensee and NRC inspection 
    findings and Licensee documents referred to in the Petition and a VHS 
    videotape, Exhibit A, which accompanied the Petition. The videotape 
    records an August 29, 1996, Citizens Regulatory Commission televised 
    interview of a former Millstone Station employee expressing his views 
    on Licensee management. Areas identified in the Petition include 
    inadequate surveillance testing, operation outside the design basis, 
    inadequate radiological controls, failed corrective action processes, 
    and degraded material condition. The Petition asserts that this 
    information demonstrates that there are inadequate quality assurance 
    programs at the Licensee's nuclear facilities in Connecticut, that the 
    Licensee has made material false statements regarding its Millstone 
    units, and that safe decommissioning of the Haddam Neck facility is not 
    possible because of the deficiencies in the design and licensing bases 
    of the facility.
        The Director of the Office of Nuclear Reactor Regulation has 
    partially granted the Petition. The reasons for this partial grant are 
    explained in the ``Partial Director's Decision Pursuant to 10 CFR 
    2.206'' (DD-97-21), the complete text of which follows this notice and 
    is available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, at the 
    local public document rooms located at the Learning Resources Center, 
    Three Rivers Community-Technical College, New London Turnpike, Norwich, 
    Connecticut, and at the temporary local public document room located at 
    the Waterford Library, ATTN: Vince Juliano, 49 Rope Ferry Road, 
    Waterford, Connecticut, for Millstone Units 1, 2, and 3; and at the 
    Russell Library, 123 Broad Street, Middletown, Connecticut, for the 
    Haddam Neck Plant.
        A copy of the Partial Director's Decision will be filed with the 
    Secretary of the Commission for the Commission's review in accordance 
    with 10 CFR 2.206(c) of the Commission's regulations. As provided for 
    by this regulation, the Decision will constitute the final action of 
    the Commission (for Requests 1, 2, 5, 6, and 8) 25 days after the date 
    of issuance unless the Commission, on its own motion, institutes a 
    review of the Decision in that time.
    
        Dated at Rockville, MD, this 12th day of September.
    
        For the Nuclear Regulatory Commission.
    Frank J. Miraglia, Jr.,
    Deputy Director, Office of Nuclear Reactor Regulation.
    
    Partial Director's Decision Pursuant to 10 CFR 2.206
    
    [DD-97-21]
    
    I. Introduction
    
        On November 25, 1996, as amended on December 23, 1996, Ms. Deborah 
    Katz and Mr. Paul Gunter filed a Petition on behalf of the Citizens
    
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    Awareness Network (CAN) and the Nuclear Information and Resource 
    Service (NIRS), hereafter, referred to as Petitioners. These two 
    submittals will hereafter be referred to as the Petition. The Petition 
    was filed with the U.S. Nuclear Regulatory Commission (NRC) and the NRC 
    Executive Director for Operations pursuant to Sec. 2.206 of Title 10 of 
    the Code of Federal Regulations (10 CFR 2.206).
        The Petitioners requested that the NRC take the following actions: 
    (1) Immediate suspension or revocation of Northeast Utilities' (NU's or 
    Licensee's) licenses to operate its nuclear facilities in Connecticut; 
    (2) investigation of possible NU material misrepresentations to the 
    NRC; (3) continued shutdown of the NU facilities until the Department 
    of Justice completes its investigation and the results are reviewed by 
    the NRC; (4) continued shutdown until the NRC evaluates and approves NU 
    remedial actions; (5) continued listing of the NU facilities on the 
    NRC's Watch List should any facility resume operation; (6) prohibition 
    of any predecommissioning or decommissioning activity at any NU nuclear 
    facility in Connecticut until NU and the NRC take certain identified 
    steps to assure that such activities can be safely conducted; (7) 
    initiation of an investigation into how the NRC allowed the asserted 
    illegal situation at NU's nuclear facilities in Connecticut to exist 
    and continue for more than a decade; and (8) an immediate investigation 
    of the need for enforcement action for alleged violation of 10 CFR part 
    50, Appendix B.1
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        \1\ Petitioners requested copies of the Licensee's calculations 
    performed in response to the event at the Haddam Neck Plant that 
    resulted in the introduction of a nitrogen bubble into the reactor 
    vessel. The calculations requested were discussed during a 
    predecisional enforcement conference held on December 4, 1996. The 
    calculations were provided to the Petitioners on July 21, 1997.
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        The bases for the Petitioners' assertions are NU and NRC inspection 
    findings and NU documents referred to in the Petition and a VHS 
    videotape, Exhibit A, which accompanied the Petition. No new 
    information regarding Licensee activities was provided by the 
    Petitioners except for the alleged violation referred to in Request 8. 
    The Petitioners assert, in Request 8, that NU relied partly on draft 
    calculations in its presentation at a public predecisional enforcement 
    conference with the NRC staff, which included a discussion of an event 
    at the Haddam Neck Plant. The Petitioners further assert that the 
    calculations had not been reviewed and approved in accordance with the 
    requirements of 10 CFR part 50, appendix B.
        The areas of concern identified in the Petition include inadequate 
    surveillance testing, operation outside the design as specified in the 
    updated Final Safety Analysis Report (UFSAR), inadequate radiological 
    controls, failed corrective action processes, and the degraded material 
    condition of the plants. The Petitioners also assert that this 
    information demonstrates that there are inadequate quality assurance 
    programs at NU's nuclear facilities in Connecticut, that NU has made 
    material false statements regarding its Millstone units, and that safe 
    decommissioning of the Haddam Neck Plant is not possible given the 
    defective nature of the design and licensing bases for the facility. 
    The videotape records an August 29, 1996, Citizens Regulatory 
    Commission televised interview of a former Millstone Station employee 
    expressing his views on NU management. The tape has been transcribed 
    and placed on the dockets of the facilities cited. The videotape 
    interview included the former employee's views relating to NU's poor 
    management in allowing degradation of the material condition of the 
    plant; poor radwaste practices resulting in potential radiation 
    exposure to employees; and harassment, intimidation, and subsequent 
    illegal termination of employees raising safety concerns.
        On January 23, 1997, the NRC acknowledged receipt of the Petition 
    and informed the Petitioners that the Petition had been assigned to the 
    Office of Nuclear Reactor Regulation to prepare a response and that 
    action would be taken within a reasonable time regarding the specific 
    concerns raised in the Petition. The Petitioners were also informed 
    that the requests for immediate action were denied. The Petitioners 
    were further informed that copies of the Petition and videotape were 
    sent to the NRC's Office of the Inspector General (OIG) in response to 
    Petitioners' Request 7 and parts of Requests 5, 6, and 8.
    
    II. Discussion
    
        The NRC staff has reviewed the Petition and, with the exception of 
    Request 8, has not identified any new information regarding either the 
    Millstone or the Haddam Neck facilities. Both of the facilities have 
    been the subject of close NRC scrutiny for several years.
    
    Millstone Facility
    
        With regard to the Millstone units, the NRC staff has been 
    concerned for the last several years about the number and duration of 
    violations at the Millstone site in the broad programmatic areas of 
    design and licensing bases, testing, and radiological controls. 
    Programmatic concerns in these areas, along with concerns in other 
    areas, were major contributors to the decline in performance at the 
    Millstone site. In the most recent systematic assessment of licensee 
    performance (SALP) report of August 26, 1994, the NRC staff stated in 
    the cover letter that it had noted several performance weaknesses, 
    common to all three Millstone units. Among these were continuing 
    problems with procedure quality and implementation, the informality in 
    several maintenance and engineering programs (contributing to instances 
    of poor performance), and the failure to resolve several longstanding 
    problems at the site. In addition to these programmatic problems, the 
    Licensee has had significant problems in dealing with employee concerns 
    involving safety issues at the site.
        On November 4, 1995, the Licensee shut down Millstone Unit 1 for a 
    scheduled refueling outage. The NRC sent a letter to the Licensee on 
    December 13, 1995, requiring the Licensee, before restarting Millstone 
    Unit 1, to inform the NRC, pursuant to section 182a of the Atomic 
    Energy Act of 1954, as amended (the Act), and 10 CFR 50.54(f), of the 
    actions taken to ensure that in the future the Licensee would operate 
    that facility according to the terms and conditions of the unit's 
    operating license, the Commission's regulations, and the unit's FSAR.
        In January 1996, the NRC designated the three Millstone units as 
    Category 2 on the NRC's Watch List. Plants on the Watch List in this 
    category have weaknesses that warrant increased NRC attention until the 
    licensees demonstrate improved performance for an extended period of 
    time.
        On February 20, 1996, the Licensee shut down Millstone Unit 2 when 
    it declared both trains of the high-pressure safety injection (HPSI) 
    system inoperable because of a design issue. There was a potential that 
    the HPSI throttle valves could become plugged with debris when taking 
    suction from the sump during recirculation mode.
        On March 30, 1996, the Licensee shut down Millstone Unit 3 after 
    finding that containment isolation valves for the auxiliary feedwater 
    turbine-driven pump were inoperable because the valves did not meet NRC 
    requirements. In response to a Licensee root cause analysis of 
    inaccuracies in the Millstone Unit 1 FSAR, identifying the potential 
    for similar configuration control problems at Millstone Units 2 and 3 
    and the existing design configuration issues identified at these units, 
    the NRC issued 10 CFR 50.54(f) letters to the Licensee on March 7 and 
    April 4, 1996. These
    
    [[Page 49036]]
    
    letters required that the Licensee inform the NRC of the corrective 
    actions taken regarding design configuration issues at Millstone Units 
    2 and 3 before the restart of each unit.
        In June 1996, the NRC designated the three units at Millstone as 
    Category 3 on the NRC's Watch List. Plants in this category have 
    significant weaknesses that warrant maintaining them in a shutdown 
    condition until the Licensee can demonstrate to the NRC that it has 
    both established and implemented adequate corrective actions to ensure 
    substantial improvement. This category also requires Commission 
    approval before operations can be resumed.
        On August 14, 1996, the NRC issued a Confirmatory Order directing 
    the Licensee to contract with a third party to implement an Independent 
    Corrective Action Verification Program (ICAVP) to confirm the adequacy 
    of its efforts to reestablish the design basis and configuration 
    controls for each of the three Millstone units. The ICAVP is intended 
    to provide additional assurance, before a unit restart, that the 
    Licensee has identified and corrected existing problems in the design 
    and configuration control processes for that unit.
        On April 16, 1997, the NRC issued another 10 CFR 50.54(f) letter, 
    which superseded the previously mentioned 10 CFR 50.54(f) letters and 
    consolidated its requests for information and periodic updates. The 
    information requested included: (1) The identification of significant 
    items needed to be accomplished before restart; (2) identification of 
    items to be deferred until after restart; (3) NU's process and 
    rationale for deferring items; and (4) a description of the actions 
    taken by NU to ensure that future operation will be conducted in 
    accordance with the terms and conditions of the operating licenses, the 
    Commission's regulations, and the FSARs. The Licensee provided the 
    initial information requested by letter dated May 29, 1997. Additional 
    information and updates will be provided in accordance with the time 
    intervals specified in the 10 CFR 50.54(f) letter.
        During eight NRC inspections conducted between October 1995 and 
    August 1996, more than 60 apparent violations of NRC requirements were 
    identified at the Millstone site. These apparent violations were 
    discussed at a public predecisional enforcement conference held at the 
    Millstone site on December 5, 1996. During the meeting, the Licensee 
    stated that management failed to provide clear direction and oversight, 
    performance standards were low, management expectations were weak, and 
    station priorities were inappropriate. The NRC staff is nearing 
    completion of its evaluation of potential enforcement action to address 
    these apparent violations and their overall impact on the safe 
    operation of the Millstone units.
        Additionally, the Licensee has had a chronic problem of not dealing 
    effectively with employee concerns at the Millstone site. On December 
    12, 1995, the NRC established a review group to conduct an independent 
    evaluation of the history of the Licensee's handling of employee 
    concerns related to licensed activities at the Millstone facility. The 
    review group determined that, in general, an unhealthy work 
    environment, which did not tolerate dissenting views and did not 
    welcome or promote questioning attitudes, has existed at the Millstone 
    facility for the last several years. To address this problem, the NRC 
    issued an Order on October 24, 1996, that directed NU to devise and 
    implement a comprehensive plan for handling safety concerns raised by 
    Millstone employees and to ensure an environment free from retaliation 
    or discrimination. In addition, the Order required NU to have an 
    independent third party oversee its employee concerns program. The 
    third party is responsible for providing periodic reports to NU and the 
    NRC detailing its findings and recommendations. The third-party 
    findings and the NU responses to them will be assessed by the NRC staff 
    for any restart issues.
        The NRC regards compliance with regulations, license conditions, 
    and Technical Specifications (TSs) as mandatory. However, the NRC also 
    recognizes that plants will not operate trouble-free.2 This 
    is clearly articulated in Criterion XVI, Appendix B, Part 50, ``Quality 
    Assurance Criteria for Nuclear Power plants and Fuel Reprocessing 
    plants.'' Criterion XVI states that ``measures shall be established to 
    assure that conditions adverse to quality, such as failures, 
    malfunctions, deficiencies, deviations, defective material and 
    equipment, and nonconformances are promptly identified and corrected.''
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        \2\ The NRC's approach to protecting public health and safety 
    includes the philosophy of defense-in-depth, which supports the 
    identification and correction of degraded or nonconforming 
    conditions discussed above. Briefly stated, this philosophy (1) 
    requires the application of conservative codes and standards, to 
    establish substantial safety margins in the design of nuclear 
    plants; (2) requires high quality in the design, construction, and 
    operation of nuclear plants to reduce the likelihood of 
    malfunctions, and promotes the use of automatic safety system 
    actuation features; (3) recognizes that equipment can fail and 
    operators can make mistakes and therefore requires redundancy in 
    safety systems and components to reduce the chances that 
    malfunctions or mistakes will lead to accidents that release fission 
    products from the fuel; and (4) recognizes that, in spite of these 
    precautions, serious fuel damage accidents can happen and therefore 
    requires containment structures and safety features to prevent the 
    release of fission products. In the unlikely event of an offsite 
    fission product release, emergency plans are in place to provide 
    reasonable assurance that protective actions can and will be taken 
    to protect the population around nuclear power plants. These 
    emergency plans are coordinated with local and State officials and 
    the Federal Emergency Management Agency.
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        The appropriate response to an identified deficiency can and should 
    vary, depending on the safety significance of the deficiency. For 
    example, for rapidly developing situations, when prompt action is 
    required to assure plants are not in an unsafe condition, automatic 
    safety systems are in place to shut down the reactor. In other, less 
    time-critical situations, TSs relating to structures, systems, and 
    components (SSCs) vital to the safe operation of a nuclear plant 
    require that specific actions be taken within a predetermined time 
    period when the SSC is determined to be inoperable. The time period is 
    dependent on the safety significance of the SSC. NRC Generic Letter 91-
    18, ``Information to Licensees Regarding Two NRC Inspection Manual 
    Sections on Resolution of Degraded and Nonconforming Conditions and on 
    Operability,'' provides guidance for licensees to determine what 
    actions are required and when they need to be taken for identified 
    degraded or nonconforming conditions.
        The conduct of NRC regulatory oversight at the Millstone site is 
    based on the recognition that it is the Licensee's primary 
    responsibility to demonstrate that corrective actions have been 
    effectively implemented. Thus, the Licensee must determine that a unit 
    is in conformance with applicable NRC regulations, its license 
    conditions, and its FSAR and that applicable licensing commitments have 
    been met before the NRC staff can recommend that the Commission approve 
    the restart of any unit. The Licensee's conformance with NRC 
    regulations, license conditions, and licensing commitments is 
    fundamental to NRC's confidence in the safety of licensed activities. 
    In short, the Licensee has the primary responsibility for the safe 
    operation of its facilities.
        In a June 20, 1996, letter to the NRC, the Licensee described its 
    Configuration Management Plan (CMP), which is its principal program to 
    provide reasonable assurance that weaknesses at the Millstone units 
    have been effectively corrected. The CMP includes efforts to understand 
    and correct the licensing
    
    [[Page 49037]]
    
    and design bases issues that led the NRC to issue the 10 CFR 50.54(f) 
    letters and Order actions to prevent recurrence of those issues. The 
    Licensee stated that the objective of the CMP was to document and meet 
    the licensing and design bases requirements of each unit and to ensure 
    that adequate programs and processes are in place to maintain control 
    of these requirements.
        The Licensee's CMP must either correct each FSAR deficiency or 
    evaluate it to ensure that the change to the facility does not involve 
    any unreviewed safety question or change to the facility TSs. NU has 
    documented a large number of deficiencies, which vary in scope and 
    safety significance for each unit. These lists contain significant 
    deficiencies that must be corrected before restart and others that the 
    Licensee is planning to correct after the restart. In its continuing 
    reviews of the deficiency lists, the NRC staff will determine whether 
    the Licensee has appropriately scheduled safety-significant items for 
    completion before restart and whether those items that the Licensee 
    will defer until after restart are appropriate for each unit. The 
    results of these efforts will be documented in NRC inspection reports.
        The NRC's regulatory oversight of the Licensee's corrective actions 
    requires extensive planning and program integration. To focus more 
    regulatory attention on all of the restart issues related to the 
    Millstone units, the NRC has established a Special Projects Office 
    (SPO) within the Office of Nuclear Reactor Regulation to oversee these 
    activities. The SPO has developed a comprehensive and multifaceted 
    oversight program to verify the adequacy of NU's corrective actions, 
    programs, and processes. The breadth and significance of the problems 
    identified at the Millstone site require this program. The SPO has 
    developed a Restart Assessment Plan (Assessment Plan) for each of the 
    Millstone units, which includes: (1) the appropriate aspects of NRC 
    Inspection Manual, Manual Chapter (MC) 0350, ``Staff Guidelines For 
    Restart Approval''; (2) oversight of NU's ICAVP; and (3) oversight of 
    NU's corrective actions relating to employee concerns involving safety 
    issues. The activities associated with the Assessment Plan are in 
    addition to the normal inspection and licensing activities being 
    carried out at the Millstone site.
        MC 0350 establishes the guidelines for approving the restart of a 
    nuclear power plant after a shutdown resulting from a significant 
    event, a complex hardware problem, or serious management deficiencies. 
    The primary objective of the guidelines in MC 0350 is to ensure that 
    NRC's restart review efforts are appropriate for the individual 
    circumstances, are reviewed and approved by the appropriate NRC 
    management levels, and provide objective measures of restart readiness.
        The Assessment Plan for each unit includes those issues listed in 
    MC 0350 that the NRC staff has identified as relevant to the shutdown 
    of the unit. Each Assessment Plan also includes additional issues 
    determined to be applicable to the specific situation. The Assessment 
    Plans include all actions the NRC expects NU to take before the NRC 
    staff recommends to the Commission that a unit be permitted to restart. 
    Accordingly, the staff will use the Assessment Plan for each Millstone 
    unit to track and monitor all significant actions necessary to support 
    a decision on restart approval of the unit.
        The Assessment Plan for each Millstone unit includes the 
    requirement to review the NU Operational Readiness Plan, the deficiency 
    lists associated with the Assessment Plan, including restart and 
    deferred items, the corrective action program, work planning and 
    controls, the procedure upgrade program, the nuclear oversight function 
    (quality assurance), outstanding enforcement items, and a Significant 
    Issues List (SIL), which includes issues identified by both NU and the 
    NRC as issues requiring resolution before restart. NRC MC 93802, 
    ``Operational Safety Team Inspection'' (OSTI), provides the framework 
    for a team inspection to be performed during the later stages of the 
    restart process. The inspection will be structured to focus on the 
    pertinent issues at each of the Millstone units.
        Within the SPO, a Millstone Restart Assessment Panel (RAP) has been 
    formed in accordance with MC 0350. The RAP meets to assess the 
    Licensee's performance and its progress in completing the designated 
    restart activities. The RAP is composed of the Director, SPO 
    (chairman); the Deputy Directors of Licensing, Inspections, and 
    Independent Corrective Action Verification Program Oversight; the 
    Project Managers for the three Millstone units; the Inspection Branch 
    Chief; the Senior Resident Inspectors for the three Millstone units; 
    and the appointed Division of Reactor Safety representative. The RAP 
    holds periodic meetings with the Licensee to discuss the Licensee's 
    corrective actions and schedules of each Millstone unit. These meetings 
    are noticed and are open to the public. An additional meeting with the 
    public is usually held that same day in the evening to summarize the 
    meeting with the Licensee, provide an update on NRC activities, and 
    address comments from the public.
        The purpose of the ICAVP, as stated in the Confirmatory Order, is 
    to confirm that the plant's physical and functional characteristics are 
    in conformance with its licensing and design bases. The ICAVP audit 
    required by the NRC is expected to provide independent verification, 
    beyond NU's quality assurance and management oversight, that the 
    Licensee has identified and satisfactorily resolved existing 
    nonconformances with the design and licensing bases; documented and 
    utilized the licensing and design bases to resolve nonconformances; and 
    established programs, processes, and procedures for effective 
    configuration management in the future. NU has started programs to 
    identify and understand the root causes of the licensing and design 
    bases issues that led to NRC issuance of the 10 CFR 50.54(f) letters to 
    NU and to implement corrective actions that will ensure that NU 
    maintains the design configuration and that each unit is in conformance 
    with its licensing basis. NU has indicated that the scope of its 
    corrective programs will include those systems that it has categorized 
    as either Group 1 (safety-related and risk-significant) or Group 2 
    (safety-related or risk-significant). The ICAVP audit must provide 
    insights into the effectiveness of NU's programs so that the results 
    can be reasonably extrapolated to the structures, systems, and 
    components that were not reviewed in the audit.
        As a practical matter, the NRC cannot do a 100-percent verification 
    of the Licensee's corrective actions, processes, and programs for each 
    Millstone unit. However, a comprehensive and multifaceted oversight 
    process has been developed by the NRC staff to provide a high level of 
    confidence that the Licensee has implemented required corrective 
    actions and that all of the issues on the SILs have been resolved. The 
    independent third-party evaluations required by the NRC will be used to 
    enhance NRC confidence that the Licensee's corrective action programs 
    have been effectively implemented at each unit.
        NRC activities (including oversight of the ICAVP) to ensure that 
    effective corrective actions are being taken by the Licensee will 
    provide additional assurance that the Licensee's corrective action 
    programs have been effectively implemented. These activities will 
    include in-process reviews of the ICAVP contractor's activities, 
    reviews of the ICAVP results, and additional independent reviews of 
    compliance with the design and licensing bases of
    
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    selected systems. The State of Connecticut's Nuclear Energy Advisory 
    Council has provided input to the NRC staff for selecting the systems 
    which will be reviewed by the ICAVP contractor and has been invited to 
    observe the NRC staff's ICAVP inspections.
        When the restart review process has identified, corrected, and 
    reviewed relevant issues regarding each Millstone unit, a restart 
    authorization process will be initiated for that unit. Upon receipt of 
    a staff recommendation and a briefing on any ongoing investigations, 
    the Commission will meet to assess the recommendation and vote on 
    whether to allow the restart of the unit. The same process will be 
    followed for the remaining units.
    
    Haddam Neck Facility
    
        With regard to the Haddam Neck Plant, the Licensee shut down the 
    plant on July 22, 1996, as required by the facility's TSs, because of 
    concerns that the containment air recirculation fans service water 
    piping may exceed design loads during certain accident scenarios. The 
    Licensee determined that these concerns and other hardware and 
    programmatic problems identified before and during the forced outage 
    should be resolved before restarting the plant. Thus, the Licensee 
    decided to begin Refueling Outage 19 on August 17, 1996. On October 9, 
    1996, the owners of the Haddam Neck Plant stated that a permanent 
    shutdown of the plant was being considered by the Board of Trustees 
    based on an economic analysis of operations, expenses, and the cost of 
    replacement power. Subsequently, all fuel assemblies were removed from 
    the reactor and placed in the spent fuel pool.
        From November 21, 1995, to November 22, 1996, the NRC conducted 
    numerous inspections at the Haddam Neck Plant to review several facets 
    of plant performance. These inspections included a Special Team 
    inspection by NRC headquarters staff focused on engineering 
    performance; a special Augmented Inspection Team (AIT) inspection of a 
    reactor vessel nitrogen intrusion event in late August and early 
    September 1996 that lowered the reactor vessel water level; a special 
    radiation protection inspection of a significant contamination event in 
    November 1996; an emergency preparedness inspection to observe the 
    Licensee's response during an emergency exercise held in August 1996; 
    and several resident inspections. Numerous violations, as well as 
    several significant regulatory concerns, were identified during these 
    inspections. Most of the violations were discussed at a transcribed 
    public predecisional enforcement conference at the Millstone training 
    building in Waterford, Connecticut, on December 4, 1996. The December 4 
    conference was open to the public and focused on the broader 
    programmatic deficiencies underlying the violations that contributed to 
    the problems at Haddam Neck. A Notice of Violation and Proposed 
    Imposition of Civil Penalties in the amount of $650,000 was issued on 
    May 12, 1997, and subsequently paid by the Licensee.
        The restart process described for the three Millstone units is not 
    applicable to the Haddam Neck Plant. By letter dated December 5, 1996, 
    the Licensee certified to the NRC, pursuant to 10 CFR 50.82(a)(1)(i) 
    and 10 CFR 50.82(a)(1)(ii), that it had decided to permanently cease 
    operations at the Haddam Neck Plant and had permanently removed the 
    fuel from the reactor. The Licensee further noted that a Post-Shutdown 
    Decommissioning Activities Report (PSDAR) and a site-specific 
    decommissioning cost estimate would be submitted in accordance with 10 
    CFR 50.82, ``Termination of License.''
        It is important to note that the NRC continues to identify problems 
    at both the Millstone site and the Haddam Neck Plant, as documented in 
    inspection reports issued after this Petition was filed. These findings 
    indicate that the corrective actions required to restart the Millstone 
    units have not yet been fully implemented. The NRC staff will not 
    recommend that the Commission allow the restart of a Millstone unit 
    until the Commission has determined, in accordance with the Assessment 
    Plan, that the necessary corrective actions have been effectively 
    implemented for the unit.
        As for Haddam Neck, a Confirmatory Action Letter (CAL) was issued 
    to the Licensee on March 4, 1997, concerning radiological-control 
    problems at the Haddam Neck Plant. This CAL is an example of the type 
    of action that the NRC takes to assure that the limited activities at 
    the site will be conducted in a safe manner and in accordance with 
    regulatory requirements. The CAL prohibits the Licensee from performing 
    any radiological work except that required to maintain the plant in a 
    safe configuration until the corrective actions identified in the CAL 
    have been implemented.
    
    III. NRC Response to Requested Actions
    
        In summary, the Licensee's implementation of its Configuration 
    Management Plan (CMP) for each Millstone unit, response to the elements 
    in the NRC staff's Restart Assessment Plan (Assessment Plan) for each 
    Millstone unit, implementation of actions to improve programs to 
    address employee concerns at the Millstone site, and the implementation 
    of the decommissioning process specified in 10 CFR 50.82 for the Haddam 
    Neck Plant, as discussed above, are the bases for the NRC staff's 
    responses discussed in this Partial Director's Decision to the specific 
    actions that the Petitioners requested be taken against NU. The 
    Petitioners' requested actions and the NRC staff's responses are 
    discussed below.3
    ---------------------------------------------------------------------------
    
        \3\ In this Partial Director's Decision, Petitioners' Requests 
    have been identified as Requests 1 through 8. These requests 
    correspond to Requests A.1 through 5, B and C in the initial 
    Petition, and Request II.A in the amendment to the Petition.
    ---------------------------------------------------------------------------
    
        1. Petitioners request that the NRC immediately suspend or revoke 
    NU's license to operate Connecticut Yankee (Haddam Neck) and the 
    Millstone Nuclear reactors due to chronic, negligent management of the 
    reactors which, for over a decade, has endangered and continues to 
    endanger occupational and public health and safety and the environment 
    due to resultant and cumulative major safety problems and violation of 
    NRC regulations.
        The Petitioners base their request to suspend or revoke the 
    operating licenses of Haddam Neck and the three Millstone units on NU 
    reports and NRC inspection findings referred to in the Petition and on 
    a videotape in which a former Millstone Station employee expresses his 
    views on NU management and plant conditions. As previously noted, based 
    on the NRC staff review of these materials, the Petitioners have 
    identified no new information.
        With regard to the Millstone units, the units are currently in an 
    extended shutdown and significant management changes at NU have been 
    made in the past year. The NRC's focus is on evaluating improved 
    performance, hardware and programmatic upgrades, and corrective 
    actions. Specifically, NRC review and inspection emphasis will be 
    directed toward the results of NU's actions to correct identified 
    weaknesses in areas such as design controls, radiological controls, 
    quality assurance, work control practices, corrective action processes, 
    and the handling of employee concerns.
        The previous discussion provides an overview of the Assessment 
    Plans that the SPO has developed for assessing the adequacy of NU's 
    corrective actions being taken prior to Commission approval of restart 
    for any of the Millstone units. The NRC staff will have to reach a 
    determination that the
    
    [[Page 49039]]
    
    corrective actions taken by NU provide reasonable assurance that future 
    operation will be conducted in accordance with the terms and conditions 
    of the operating license, the Commission's regulations, and the design 
    basis, as documented in the FSAR, of each unit before recommending that 
    the Commission approve the restart of any one of the units. Upon 
    receipt of an NRC staff recommendation and a briefing on ongoing 
    investigations, the Commission will hold a meeting to assess the 
    recommendation and then vote on whether to approve the restart of each 
    unit.
        The restart process discussed for the Millstone units does not 
    apply to Haddam Neck. The Licensee has certified to the NRC that 
    operations at the facility have permanently ceased and that fuel has 
    been permanently removed from the reactor.
        The Petitioners' request to take immediate action was denied in the 
    letter of January 23, 1997, which acknowledged receipt of the Petition. 
    The request to suspend or revoke the licenses for the three Millstone 
    units is denied based on the NRC staff's conclusion that such action is 
    not warranted by the facts. Programmatic and review efforts are in 
    place. If these efforts are successful, the NRC would allow the 
    Millstone units to resume operation. The request to suspend or revoke 
    the license to operate the Haddam Neck Plant is moot since the Licensee 
    has certified to the NRC that the plant has permanently ceased 
    operation and the fuel has been permanently removed from the reactor.
        2. The Petitioners request that the NRC investigate the possibility 
    that NU made material misrepresentations to the NRC concerning 
    engineering calculations and other information or actions relied upon 
    to assure the adequacy of safety systems at the Haddam Neck and 
    Millstone reactors. The Petitioners said NU made possible material 
    misstatements either through lack of rigor and thoroughness or by 
    providing intentionally misleading information.
        The NRC has ongoing investigations related to alleged wrongdoing by 
    NU personnel. The investigative results will be reviewed for possible 
    enforcement action. Depending on the results of the ongoing evaluations 
    of inspections and investigations, both NU as an organization and NU 
    employees found to have engaged in deliberate misconduct will be 
    subject to appropriate enforcement action. Consistent with the General 
    Statement of Policy and Procedures for NRC Enforcement Actions (NUREG-
    1600), some enforcement action is normally taken against a licensee for 
    violations caused by significant acts of wrongdoing by its employees. 
    Such action could include a civil penalty or an order. In deciding 
    whether to also take action directly against the responsible employees, 
    the NRC considers a number of factors such as the employee's level in 
    the organization, the employee's training and experience, the degree of 
    supervision, the employee's attitude, and the degree of management 
    responsibility or culpability. A decision to take action directly 
    against an individual is significant and normally will be taken only 
    when the NRC is satisfied that the individual has engaged in deliberate 
    misconduct. The action taken could include prohibiting the individual 
    from involvement in licensed activities for a period of years.
        As the NRC is currently evaluating alleged wrongdoing by NU 
    personnel, the Petitioners' request is granted.
        3. Petitioners request that the NRC revoke NU's operating licenses 
    for the Haddam Neck and the Millstone Units 1, 2, and 3 reactors if an 
    investigation determines that NU deliberately provided insufficient 
    and/or false or misleading information to the NRC. If the NRC chooses 
    not to revoke NU's licenses, the Petitioners specifically request that 
    the reactors remain off-line until a United States Department of 
    Justice (DOJ) independent investigation is complete and the NRC reviews 
    the conclusions and recommendations contained therein for potential 
    consequences to the Licensee and its agents under NRC regulations. The 
    Petitioners note in a footnote that a DOJ report will likely produce 
    information essential to the NRC's evaluation of NU's management 
    problems. The Petitioners further stated that such information should 
    influence any NRC decision concerning NU's future operation of nuclear 
    reactors in Connecticut.
        Since the NRC investigations are ongoing, the NRC cannot respond to 
    the first portion of the request to revoke the licenses of the three 
    Millstone units at this time.
        The response to the Petitioners' Request 1 applies to the part of 
    Request 3 asking that the reactors remain off line until the 
    investigations are complete. As noted, the Commission will consider the 
    status of all ongoing investigations, including any referrals to DOJ, 
    in its deliberations before voting on the restart of any of the 
    Millstone units.
        The part of the request relating to revoking the licenses of the 
    three Millstone units is deferred until all investigations are 
    complete. The request that the reactors remain off line until the 
    investigations are complete is denied.
        This request does not apply to the Haddam Neck Plant, which has 
    already permanently ceased operation.
        4. The Petitioners request that, if NRC chooses not to revoke NU's 
    licenses to operate the Haddam Neck Plant and the Millstone Units 1, 2, 
    and 3 reactors and allows the reactors to return to operation, the 
    reactors remain on the NRC's Watch List to oversee reactor operations 
    until NU management demonstrates to the NRC that:
        a. NU is able to fulfill NRC regulatory requirements;
        b. NU has met all prior commitments concerning the repair, 
    modification, maintenance, and documentation of the nuclear power 
    stations;
        c. NU has retrained all staff in the application and interpretation 
    of NRC's regulations; and
        d. NU has removed from any positions of responsibility for 
    operation and/or management of the reactors all persons whom DOJ, NRC, 
    or other government investigators and/or civil or criminal prosecutions 
    find to have made material misrepresentations to the NRC during the 
    past decade of mismanagement.
        Due to the significance and programmatic nature of the concerns 
    evolving from the various NRC reviews and inspections at the Millstone 
    Station and the fact that each unit is shut down pending resolution of 
    these issues, the Commission put the Millstone units in Category 3 of 
    the Watch List. Accordingly, restart of any of the units is subject to 
    Commission approval. SIL issues, which require resolution for safe 
    operation, will have been addressed and a process will be in place to 
    resolve any deferred items. If the Commission approves restart of any 
    unit, that unit will be placed in Category 2 of the Watch List, where 
    it will remain until the Licensee has demonstrated that satisfactory 
    operational performance can be sustained at the unit.
        The restart process, as previously discussed, will assure that the 
    management attributes identified by the Petitioners in Request 4.a, b, 
    and c, will be adequately considered within the context of the SPO's 
    Assessment Plans before the NRC staff recommends that the Commission 
    allow the restart of any unit. Request 4.d will be considered in the 
    restart process when the Commission is briefed regarding investigation 
    efforts and recommendations.
        The request to retain the Millstone units on the NRC's Watch List, 
    if the Commission approves restart, is granted.
    
    [[Page 49040]]
    
    Any unit permitted to restart will be placed in Category 2 of the Watch 
    List, where it will remain until the Licensee has demonstrated that 
    satisfactory performance can be sustained at the unit. Request 4.a, b, 
    c, and d will be considered as set forth above.
        This request does not apply to the Haddam Neck Plant because the 
    Haddam Neck Plant has permanently ceased operation. The NRC will 
    continue its oversight of the defueled facility.
        5. Petitioners request that, as a minimum, the NRC keep Haddam Neck 
    and the Millstone 1, 2, and 3 nuclear reactors off line until NU's 
    chronic mismanagement has been analyzed, remedial management programs 
    have been implemented, and the NRC has evaluated and approved the 
    effectiveness of the Licensee's actions. As a minimum, NU should:
        a. Thoroughly analyze root causes for deficiencies in NU's FSARs, 
    its documentation of licensing and design bases, its safety analysis, 
    its engineering, its quality assurance, its as low as reasonably 
    achievable (ALARA) programs, and other necessary or required 
    documentation.
        b. Create a complete, accurate FSAR-mere ``reform'' is impossible 
    when the basic document is inadequate and inaccurate;
        c. Reevaluate of any of its activities initiated under (or which NU 
    should have initiated under) 10 CFR 50.59 in order to confirm the 
    validity of such activities, particularly to determine the extent to 
    which the FSAR does not match ``as built'' configurations. This 
    reevaluation requires more than a paper audit; it requires checking 
    actual physical plant against the existing documentation, component by 
    component and system by system and creating correct documentation where 
    it is lacking and/or inadequate;
        d. Institute and document an effective ALARA review of all 
    operational and nonoperational activities that expose workers and/or 
    the public to radiation;
        e. Thoroughly document the root causes of NU's chronic and systemic 
    mismanagement including, documentation of the NRC Region I inspection 
    program's staff and management failures over the past decade to detect 
    and deal with this problem;
        f. Demonstrate, over a substantial period of time to the 
    satisfaction of the NRC, NU's commitment to respect NRC regulatory 
    requirements and consistently follow them;
        g. Retrain all personnel involved in day-to-day operations so that 
    they are thoroughly conversant with NRC regulations; and
        h. Update and document Plant Design Change Requests (PDCRs) to 
    include all changes to the reactor's design, and verification by the 
    NRC staff of these design changes, with closeouts of PDCRs receiving 
    the highest priority.
        As previously noted, NRC regulatory oversight programs at the 
    Millstone Station are based on the recognition that the Licensee is 
    primarily responsible for demonstrating that corrective actions have 
    been effectively implemented. Before the NRC staff can recommend that 
    the Commission approve the restart of a Millstone unit, the Licensee 
    must determine that the unit conforms with applicable NRC regulations, 
    license conditions, and the FSARs and that applicable licensing 
    commitments have been met. The Licensee's conformance with NRC 
    regulations, license conditions, and licensing commitments is 
    fundamental to the NRC's confidence in the safety of licensed 
    activities.
        The significant actions that the NRC is taking to monitor the 
    Licensee's activities have been discussed in detail earlier in this 
    Decision. Based on that discussion, the actions requested in Request 
    5.a through h, with the exception of the part of 5.e relating to NRC 
    staff performance, will be adequately addressed within the context of 
    the SPO's Assessment Plan for each of the Millstone units.
        With regard to Request 5.e, the part of 5.e relating to the 
    performance of the NRC staff is beyond the scope of the 2.206 process 
    and will not be addressed in the Director's Decision relating to this 
    Petition. This issue has been referred to the NRC's OIG for action as 
    appropriate.
        The request to keep the Millstone units off line until the items 
    identified in Request 5.a through h, with the exception of the part of 
    Request 5.e relating to NRC's previous actions in dealing with the 
    Licensee, is granted to the extent that the issues will be considered 
    within the SPO's Assessment Plan for each of the units.
        This request does not apply to the Haddam Neck facility, which has 
    permanently ceased operation.
        6. Petitioners request that, if NU decides to shut down any or all 
    of the nuclear power reactors at issue herein with the intent to 
    commence the decommissioning process, the NRC not permit any 
    decommissioning or predecommissioning activity to take place until:
        a. All the documentation mentioned in earlier requests is available 
    to the NRC and on site at the reactors;
        b. All personnel involved in the decommissioning process have been 
    retrained (or trained) in the use and interpretation of the applicable 
    NRC regulations in Title 10 of the Code of Federal Regulations;
        c. The NRC has appropriately evaluated and replaced personnel and 
    has restructured the NRC Region I inspection program, its management, 
    and the supervising NRC directorate to eliminate the regulatory anarchy 
    that plagued the Connecticut nuclear reactors during the past 10 years; 
    and
        d. The NRC makes certain that NU does not employ any persons in 
    management or operations who made material misrepresentations to the 
    NRC about the status of operations, repairs, modifications, or 
    maintenance of NU's Connecticut reactors.
        On October 9, 1996, the owners of the Haddam Neck Plant stated that 
    the Board of Trustees was considering a permanent shutdown of the 
    plant, based on an economic analysis of operations, expenses, and the 
    cost of replacement power. All fuel assemblies were removed from the 
    reactor and placed in the spent fuel pool for temporary storage. By 
    letter dated December 5, 1996, the Licensee certified to the NRC, 
    pursuant to 10 CFR 50.82(a)(1)(i) and 10 CFR 50.82(a)(1)(ii), that it 
    had determined to permanently cease operations at the Haddam Neck Plant 
    and that the fuel had been permanently removed from the reactor. The 
    Licensee further noted that a Post-Shutdown Decommissioning Activities 
    Report (PSDAR) and the site-specific decommissioning cost estimate 
    would be submitted in accordance with 10 CFR 50.82, ``Termination of 
    License.'' The PSDAR will be submitted to the NRC and a copy sent to 
    the affected state(s) within 2 years after operations have permanently 
    ceased. The report must include, among other things, a description of 
    the planned decommissioning activities and a schedule for their 
    implementation. No major decommissioning activities may be performed 
    until 90 days after the NRC receives the PSDAR.
        The current activities at the site include the operation, 
    monitoring, and maintenance of the spent fuel pool; radioactive waste 
    management; radiological protection; and fire protection. These 
    activities, including any activities relating to decommissioning, must 
    be in compliance with the current license requirements, which apply 
    when the reactor is defueled.
        The degree of regulatory oversight required during decommissioning 
    of a nuclear power reactor is considerably less than during its 
    operational phase. When the reactor is operating, the fuel
    
    [[Page 49041]]
    
    in the reactor core undergoes a controlled nuclear fission reaction 
    that generates a high neutron flux and large amounts of heat. Safe 
    control of the nuclear reaction involves the use and operation of many 
    complex systems, adherence to operational limits, testing of components 
    and systems to assure their operability, specified procedure adherence, 
    and operator actions. Once the fuel has been permanently removed and 
    temporarily stored in the spent fuel pool, the fuel is still highly 
    radioactive and generates heat caused by radioactive decay. However, no 
    neutron flux is generated and the fuel slowly cools as its energetic 
    decay products diminish. Since the spent fuel is stored in a 
    configuration that precludes the nuclear fission, no generation of new 
    radioactivity can occur. However, the same areas of the facility 
    contain radioactive contamination and those areas must still be 
    controlled to minimize radiation exposure to personnel and to control 
    the spread of radioactive material.
        The NRC staff continues to be concerned about the failures of the 
    Haddam Neck radiological controls program (which recently resulted in 
    the unplanned exposure of two individuals), long-standing discrepancies 
    in the calibration of several radiation monitors that are used to 
    monitor and control radiological effluent releases, and the inadequate 
    control of radioactive material that resulted in the undetected release 
    of contaminated equipment to a nonlicensed vendor.
        In response, the NRC has taken comprehensive and significant 
    actions to resolve concerns in the area of radiological controls, 
    including the issuance of a CAL on March 4, 1997, confirming the 
    Licensee's commitment to respond to the findings in Inspection Reports 
    50-213/96-12, dated December 19, 1996, and 50-213/97-02, dated March 
    21, 1997. The CAL restricts the Licensee from performing any 
    radiological work except that required to maintain the plant in a safe 
    configuration. The CAL identifies four significant activities required 
    of the Licensee to bring its management and implementation of radiation 
    control programs up to a standard acceptable to the NRC. The activities 
    are to (1) identify, in writing, specific compensatory measures that 
    the Licensee will establish to assure sufficient management control and 
    oversight of ongoing or planned activities that require radiological 
    controls; (2) engage the services of an independent assessor to assess 
    the quality and performance of the Licensee's radiological control 
    programs and their implementation; (3) by May 30, 1997, based on the 
    results of that independent assessment, (a) identify problems, 
    determine root causes, and develop broad-based and specific corrective 
    actions; (b) identify performance measures that may be used to 
    determine the effectiveness of radiological control programs; and (c) 
    submit a plan and schedule to the Regional Administrator, NRC Region I, 
    for implementing improvements in the radiological control programs; and 
    (4) before eliminating any interim compensatory measures, meet with the 
    Region I Administrator to describe program implementation and 
    performance improvements achieved or planned.
        In summary, the NRC is following the decommissioning process as 
    specified in 10 CFR 50.82, which requires that no major activities may 
    be performed until 90 days after the NRC receives the PSDAR. The 
    Licensee must comply with all the applicable operating license 
    requirements in effect for the defueled reactor relating to activities 
    currently being performed at the Haddam Neck Plant. Further, the NRC 
    will take appropriate actions for any defueled reactor to assure 
    compliance with its license and license conditions, such as the actions 
    described above for the failure of adequate radiological controls at 
    Haddam Neck. The Haddam Neck Plant is the only reactor that the 
    Licensee has determined to permanently shut down and decommission.
        The request to forbid decommissioning activities or 
    predecommissioning activity at any NU nuclear power reactor until all 
    the requested actions identified in the Petition, including items a, b 
    and d, of Request 6, have been completed is denied for the reasons 
    stated above. The NRC staff has determined that the NRC requirements 
    that govern decommissioning and the activities being undertaken by the 
    Licensee in response to the CAL are sufficient to assure that the 
    activities at the Haddam Neck facility are being conducted in a safe 
    manner. Request 6.c, relating to the performance of the NRC staff, is 
    beyond the scope of the 2.206 process and will not be addressed in the 
    Director's Decision relating to this Petition. This issue has been 
    referred to the NRC's OIG.
        7. The Petitioners request that the NRC commence an investigation 
    into how it allowed the illegal situation at NU's Connecticut reactors 
    to exist and to continue over a decade. Particularly, Petitioners 
    request that the Commission order its staff (directors of the 
    responsible directorates, managers, and Region I management and staff) 
    to answer the following questions, and hold these persons accountable 
    for their answers and actions regarding the past 10 years at NU's 
    Connecticut nuclear power reactors:
        a. What documents did Region I inspectors, their supervisors, and 
    NRC Project Directors and Project Managers review during 10 years of 
    NU's out-of-compliance operation?
        b. If NU provided documents that somehow deceived the Region I 
    inspector, how does the information in these documents relate to the 
    everyday workings and activities conducted during the otherwise 
    undocumented decade of operations at the Millstone and Haddam Neck 
    plants?
        c. How did Region I inspectors, their supervisors, and NRC Project 
    Directorates and Managers find that NU was conducting operations in a 
    way that keeps worker and public exposures to radiation ALARA when NU 
    was not adequately documenting either its licensing basis or the basis 
    of reactor operations?
        d. Knowing, as Region I inspectors must have known, of excessive 
    worker exposures (for example, due to a long standing problem with 
    leaking pipes as documented by an NU worker in the video tape provided 
    with this Petition Exhibit A), how did the Region I inspectors certify 
    that operations at the Millstone and Haddam Neck plants were being 
    conducted ALARA? How did the supervisors, and those in the NRC Project 
    Directorate, make the same certifications?
        e. During the undocumented decade, how did Region I inspectors, 
    their supervisors, and NRC Project Directors and Managers manage to 
    track NU's activities at the Millstone and Haddam Neck plants under 10 
    CFR 50.59?
        f. To what extent have NRC Region I inspectors, their supervisors, 
    and NRC Project Directors and Managers allowed the same type of 
    problems to develop at other nuclear power reactors in New England 
    (i.e., Maine Yankee, Pilgrim, Seabrook, Vermont Yankee, and Yankee 
    Rowe)?
        g. Is there any connection between licensees employing Yankee 
    Atomic Electric Company's consulting and engineering services and the 
    serious problems with documentation and lack of compliance with the 
    licensing and design bases nuclear power stations in New England or in 
    other parts of the country?
        This request is beyond the scope of the 2.206 process. It concerns 
    the performance of the NRC staff and will not be addressed in the 
    Director's
    
    [[Page 49042]]
    
    Decision relating to this Petition. This request has been referred to 
    the NRC's OIG.
        8. In the amendment to the Petition, the Petitioners request that 
    the NRC take the following actions to enforce its regulations against 
    NU. As part of the 2.206 process, the NRC should provide copies of 
    Haddam Neck's nitrogen calculations to the Petitioners and conduct an 
    independent review to see if the calculations meet the requirements of 
    10 CFR part 50, appendix B. If appendix B requirements were violated, 
    the Petitioners are concerned that the Licensee cannot safely 
    decommission the Haddam Neck Plant. Accordingly, NU's operating 
    licenses for its Connecticut reactors should be revoked, and NU should 
    not be permitted to commence decommissioning until it has complied with 
    the conditions outlined in the main body of the original Petition. 
    Finally, the Commission should inquire into the NRC staff's failure to 
    discern this situation and its continuing failure to enforce the terms 
    and conditions of NU's license and NRC regulations.
        As noted above, the assertion by the Petitioners that the 
    calculations performed by the Licensee violated NRC requirements is a 
    new issue not previously considered by the NRC staff.
        The subject calculations were performed subsequent to an event at 
    the Haddam Neck Plant that resulted in the formulation of a nitrogen 
    bubble in the reactor vessel. The results of the calculations, which 
    were one of several methods used to confirm the water level during the 
    event, were discussed by the Licensee during a public predecisional 
    enforcement conference held on December 4, 1996.
        By letter dated July 3, 1997, the Licensee provided information, 
    including the requested calculations, relating to the different methods 
    used for determining the reactor vessel water level resulting from the 
    nitrogen intrusion event. This information has been placed in the NRC's 
    Public Document Room and the Local Public Document Rooms. The 
    Petitioners were provided a copy of the calculations as an enclosure to 
    a Petition status letter dated July 21, 1997, since the calculations 
    are relevant to the Petitioners' concern, are not proprietary, and are 
    in the public domain.
        On September 5, 1996, while investigating the root cause of the 
    undetected accumulation of nitrogen gas in the reactor vessel, the 
    Licensee performed a special test (ST 11.7-197, ``Determination of 
    Reactor Vessel Level'') to verify reactor vessel level. This test was 
    necessary because the reactor vessel level indication system and the 
    core exit thermocouples had been removed from service in accordance 
    with the Licensee's refueling procedures. The reactor level measurement 
    problem had been exacerbated by the nitrogen gas intrusion, which 
    displaced water from the reactor vessel into the pressurizer, resulting 
    in an unquantified decrease in reactor vessel inventory. During the 
    course of the event, the shift manager had requested that the worst-
    case (lowest) reactor vessel level achieved during the event be 
    determined. As noted in NRC Inspection Report No. 50-213/96-80, ``NRC 
    Augmented Inspection Team Review of the Undetected Introduction of 
    Nitrogen Gas into the Reactor Vessel During Plant Shutdown,'' the plant 
    staff completed a preliminary analysis on September 4, 1996. It was 
    further noted that, at the end of the onsite inspection activities, the 
    Licensee had yet to complete a final volumetric inventory balance 
    calculation. In the Notice of Violation and Proposed Imposition of 
    Civil Penalties in the amount of $650,000 issued on May 12, 1997, the 
    Licensee was cited for failure to take timely corrective actions 
    following the nitrogen intrusion event, including the failure to timely 
    establish the actual lowest reactor vessel level resulting from the 
    event.
        Subsequently, the Licensee completed two calculations: (1) 
    Calculation 96-MDE-1515-MY, ``Reactor Vessel Level Determination,'' 
    prepared on October 2, 1996, independently reviewed on November 1, 
    1996, and approved on November 5, 1996; and (2) Calculation 96-MDE-
    1536-MY, ``Reactor Vessel Level Determination,'' prepared on October 4, 
    1996, independently reviewed on November 22, 1996, and approved on 
    December 1, 1996. These calculations were performed consistent with the 
    requirements of 10 CFR part 50, appendix B.
        Also, during the December 4, 1996, predecisional enforcement 
    conference, the Licensee presented the results of reactor vessel water 
    level simulations, which were calculated using the RELAP5/MOD3 code. 
    These simulation results were presented by the Licensee to corroborate, 
    with a diverse methodology, the lowest reactor vessel water level 
    determined by Calculations 96-MDE-1515-MY and 96-MDE-1536-MY. The 
    results of the RELAP5/MOD3 reactor vessel water level simulations 
    presented by the Licensee during the predecisional enforcement 
    conference were only used to corroborate and provide additional insight 
    into the reactor vessel water level that had been determined through 
    Calculations 96-MDE-1515-MY and 96-MDE-1536-MY. These two calculations 
    had been independently reviewed and performed consistent with the 
    applicable provisions in the Licensee's 10 CFR part 50, Appendix B, 
    ``Quality Assurance Program,'' and are considered by the NRC staff to 
    suffice to demonstrate the reactor vessel water level.
        Under these circumstances, the RELAP5/MOD3 simulations were not 
    required to have been independently verified.
        Thus, the assertion by the Petitioners that the calculations 
    discussed during the predecisional enforcement conference violated 10 
    CFR part 50, appendix B, requirements is unfounded and no further 
    actions by the NRC are required. The part of Request 8 relating to the 
    performance of the NRC staff is beyond the scope of the 2.206 process 
    and will not be addressed in the Director's Decision relating to this 
    Petition. This part of Request 8 has been referred to the NRC's OIG.
    
    IV. Conclusion
    
        The NRC staff has determined, for the reasons provided in the above 
    discussion, that: Request 2 is granted for both the Millstone units and 
    the Haddam Neck Plant; Requests 4 and 5 are partially granted for the 
    Millstone units; Request 1 and parts of Requests 3, 4, 6, and 8 are 
    denied for the three Millstone units; Requests 6 and 8 are partially 
    denied for the Haddam Neck Plant; Request 3 is partially deferred for 
    the three Millstone units; Requests 1, 3, 4, and parts of Request 5 are 
    not applicable to Haddam Neck; and Request 7 and parts of Requests 5, 
    6, and 8 are beyond the scope of the 2.206 process and are not 
    addressed. The deferred parts of Request 3 will be addressed in a Final 
    Director's Decision after any possible wrongdoing is fully considered 
    by the NRC staff.
        As provided for in 10 CFR 2.206(c), a copy of this Partial Decision 
    will be filed with the Secretary of the Commission for the Commission's 
    review. This Partial Decision will constitute the final action of the 
    Commission (for Petitioners Requests 1, 2, 5, 6, and 8) 25 days after 
    issuance unless the Commission, on its own motion, institutes review of 
    the Decision in that time.
    
        Dated at Rockville, MD, this 12th day of September.
    
    
    [[Page 49043]]
    
    
        For the Nuclear Regulatory Commission.
    Frank J. Miraglia Jr.,
    Deputy Director, Office of Nuclear Reactor Regulation.
    [FR Doc. 97-24807 Filed 9-17-97; 8:45 am]
    BILLING CODE 7590-01-P