99-24573. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 64, Number 183 (Wednesday, September 22, 1999)]
    [Notices]
    [Pages 51343-51356]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 99-24573]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from August 28, 1999, through September 10, 1999. 
    The last biweekly notice was published on September 8, 1999 (64 FR 
    48858).
    
    Notice of Consideration of Issuance of Amendments to Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3)
    
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    involve a significant reduction in a margin of safety. The basis for 
    this proposed determination for each amendment request is shown below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules and 
    Directives Branch, Division of Administration Services, Office of 
    Administration, U.S. Nuclear Regulatory Commission, Washington, DC 
    20555-0001, and should cite the publication date and page number of 
    this Federal Register notice. Written comments may also be delivered to 
    Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville, 
    Maryland from 7:30 a.m. to 4:15 p.m., Federal workdays. Copies of 
    written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC. The 
    filing of requests for a hearing and petitions for leave to intervene 
    is discussed below.
        By October 22, 1999, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for
    
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    amendment which is available for public inspection at the Commission's 
    Public Document Room, the Gelman Building, 2120 L Street, NW., 
    Washington, DC, and at the local public document room for the 
    particular facility involved.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert County, 
    Maryland
    
        Date of amendments request: August 27, 1999.
        Description of amendments request: The proposed amendment revises 
    Technical Specification (TS) 3.7.13, ``Spent Fuel Pool (SFP) Water 
    Level'' to allow placement of one or more fuel assemblies on SFP rack 
    spacers to support fuel reconstitution activities while irradiated fuel 
    assembly movement continues in the SFP. Although the plant TSs do not 
    prohibit fuel reconstitution, the effect of the current wording of TS 
    3.7.13, in conjunction with the specific design of the SFP and storage 
    racks, limits reconstituting only one fuel assembly at a time and only 
    when no irradiated fuel assembly movement occurs in the SFP. 
    Specifically, the proposed change adds a new statement to the limiting 
    condition for operation that would require the water level over fuel 
    assemblies placed on rack spacers to be 19.8 feet while irradiated fuel 
    assemblies are being moved in the SFP. The proposed administrative 
    controls will ensure that the current design basis fuel handling 
    accident described in the Updated Final Safety Analysis Report (UFSAR) 
    bounds a fuel handling accident associated with reconstitution 
    activities.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The proposed change will require a minimum water level of 19.8 
    feet over fuel assemblies that are placed on rack spacers for fuel 
    reconstitution activities while fuel movement continues in the SFP. 
    This proposed change does not cause any spent fuel handling 
    equipment to be operated in a new or different manner. No structural 
    changes or modifications are being made to the spent fuel handling 
    machine (SFHM) or to the spent fuel storage racks. Administrative 
    controls will be put in place to ensure that the SFHM or an assembly 
    being carried by the SFHM will not strike assemblies placed on rack 
    spacers. This proposed change does not make any changes to 
    equipment, procedures, or processes that increase the likelihood of 
    dropping the fuel assembly from the SFHM. Administrative controls 
    will be put in place to limit the movement of heavy loads such that 
    only a single-failure-proof crane will be used in the area of the 
    affected fuel assembly and the adjacent storage rack cells when the 
    assemblies are seated on rack spacers with their upper end fittings 
    removed. Therefore, this proposed change does not involve a 
    significant increase in the probability of an accident previously 
    evaluated.
        A Fuel Handling Incident (FHI) during reconstitution activities 
    is bounded by those previously analyzed and described in the Updated 
    Final Safety Analysis Report (UFSAR) for the limiting FHI. The 
    number of fuel pins that could be ruptured in a raised fuel assembly 
    does not exceed that previously analyzed. Also, by requiring that 
    reconstitution activities do not occur until 10 days after shutdown 
    ensures that a[n] FHI during these activities will be bounded by the 
    most limiting FHI described in the UFSAR. Therefore, the proposed 
    change does not significantly increase the consequences of an 
    accident previously evaluated.
        Based on the above, the proposed change does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated.
        The proposed change will not make any physical changes to the 
    plant. Specifically, no modifications will be made to the SFHM, the 
    spent fuel storage racks, or the spent fuel assemblies. No changes 
    are made to the operation of the SFHM. The only change made by this 
    activity is that multiple fuel assemblies may be placed on rack 
    spacers in the SFP for reconstitution activities. Administrative 
    controls will be put in place to ensure that this proposed change 
    does not create the potential of a[n] FHI during reconstitution 
    activities that is not bounded by our current accident analysis. 
    This proposed change does not have any impact on the cooling or safe 
    geometry functions of the SFP storage racks. This proposed change 
    does not create any new interactions between any plant components. 
    Therefore, the possibility of a new or different type of accident is 
    not created by this proposed change.
        3. Would not involve a significant reduction in a margin of 
    safety.
        The Technical Specification requires a minimum water level to be 
    maintained above the fuel assemblies stored in the SFP storage racks 
    to ensure that sufficient water depth is available to remove the 
    assembled iodine gap activity released from the rupture of an 
    irradiated fuel assembly. The proposed change will allow multiple 
    fuel assemblies to be placed on rack spacers for fuel reconstitution 
    activities while fuel movement continues in the spent fuel pool. 
    These activities will reduce the amount of water maintained above 
    the fuel assemblies that are placed on rack spacers. However, the 
    proposed change does not involve a significant reduction in a margin 
    of safety based on the administrative controls that require an 
    increase in the decay time before these activities can be started. 
    Additional administrative controls will be put in place that 
    include, in part, restricting load movements over the affected fuel 
    assembly and the adjacent storage rack cells, as well as controlling 
    the SFHM. The administrative controls will ensure that the FHI 
    associated with reconstitution activities is bounded by the current 
    design basis FHI described in the UFSAR. Therefore, the proposed 
    change does not involve a significant reduction in a margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for Licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        NRC Section Chief: S. Singh Bajwa.
    
    Florida Power and Light Company, et al., Docket No. 50-389, St. Lucie 
    Plant, Unit No. 2, St. Lucie County, Florida
    
        Date of amendment request: August 18, 1999.
        Description of amendment request: The proposed amendment will 
    change the required surveillance interval for cycling the steam valves 
    in the turbine overspeed protection system from monthly to quarterly. 
    The license requirement is documented in the St. Lucie, Unit 2 Updated 
    Final Safety Analysis Report (UFSAR) Section 13.7.1.6.2, and the 
    proposed change does not satisfy the 10 CFR 50.59 standards for a 
    change that can be made by the licensee without prior Commission 
    approval.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The small increase in turbine missile ejection frequency 
    resulting from extending the test interval for turbine valves is 
    acceptable with respect to the NRC probabilistic acceptance 
    criterion and supports quarterly testing. In addition, there are no 
    physical changes to plant equipment or changes in plant operation 
    that could initiate or adversely affect the mitigation or
    
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    consequences of an accident previously evaluated. Turbine disk 
    integrity remains unchanged since the turbine rotor inspection cycle 
    is not affected by the change in valve testing frequency. Further, 
    there are no changes to protective barriers or changes in separation 
    of equipment important to safety. Therefore, safety related 
    structures, systems, and components remain adequately protected 
    against potential turbine missiles and the potential for turbine 
    missile generation has not significantly increased. The change to 
    extend the turbine valve test interval maintains the intent and 
    design basis function being verified by the surveillance 
    requirement. Therefore, operation of the facility in accordance with 
    the proposed amendment will not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        2. Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        There are no physical changes to plant equipment or changes in 
    plant operation that could create a new or different kind of 
    accident. This proposed change does not result in any plant 
    configuration changes or create new failure modes. The small 
    increase in turbine missile ejection frequency resulting from 
    extending the test interval for turbine valves is acceptable with 
    respect to the NRC probabilistic acceptance criterion and supports 
    quarterly testing. New types of turbine missiles or strike 
    probabilities are not created by extending the turbine valve test 
    interval. No new or different kind of accident is created. In 
    addition, turbine disk integrity remains unchanged since the turbine 
    rotor inspection cycle is not affected by the change in valve 
    testing frequency. Further, there are no changes to protective 
    barriers or changes in the separation of equipment important to 
    safety. Safety related structures, systems, and components remain 
    adequately protected against potential turbine missiles, the 
    potential for turbine missile generation has not significantly 
    increased, and new or different kinds of accidents are not created. 
    Therefore, operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        3. Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        This proposed surveillance change extends the turbine overspeed 
    protection system turbine valve test frequency from monthly to 
    quarterly. The results of turbine missile ejection frequency remain 
    within NRC acceptance criterion and therefore supports quarterly 
    testing. There are no physical changes to plant equipment or changes 
    in plant operation that involve a significant reduction in the 
    margin of safety. Turbine disk integrity remains unchanged since the 
    turbine rotor inspection cycle is not affected by the change in 
    valve testing frequency. There are no changes to protective barriers 
    or changes in separation of equipment important to safety. 
    Therefore, safety related structures, systems, and components remain 
    adequately protected against potential turbine missiles and the 
    potential for turbine missile generation has not significantly 
    increased. The change in turbine valve test interval maintains the 
    intent and design basis function being verified by the surveillance 
    requirement. As such, the assumptions and conclusions of the 
    accident analyses in the UFSAR remain valid and associated safety 
    limits will continue to be met. Therefore, operation of the facility 
    in accordance with the proposed amendment would not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Indian River Junior College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34954-9003.
        Attorney for licensee: M.S. Ross, Attorney, Florida Power & Light, 
    P.O. Box 14000, Juno Beach, Florida 33408-0420.
        NRC Section Chief: Sheri R. Peterson.
    
    GPU Nuclear Inc., Docket No. 50-320, Three Mile Island--Unit 2 (TMI-2), 
    Dauphin County, Pennsylvania
    
        Date of amendment request: June 29, 1999, as supplemented August 
    27, 1999 (LAR No. 77).
        Description of amendment request: The proposed amendment would 
    grant authority for the licensee to possess limited amounts and types 
    of radioactive materials without unit distinction so that after the 
    sale and transfer of the Three Mile Island--Unit 1 (TMI-1) license to 
    AmerGen, radioactive materials may continue to be moved between the 
    TMI-1 and TMI-2 units. After the license transfer, GPU Nuclear will 
    need to access the waste handling and processing facilities at TMI-1 
    (currently common facilities) for its normal post-defueling monitored 
    storage (PDMS) activities. Similarly, AmerGen as the TMI-1 licensee and 
    PDMS contractor, will need to move radioactive apparatus and materials 
    between units, principally during TMI-1 outages. The amendment would 
    not authorize receipt or possession of radioactive material or waste 
    from other sites.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed changes would not involve a significant increase 
    in the probability of an accident previously evaluated because no 
    accident initiators or assumptions are affected. The proposed 
    changes have no effect on any plant systems. All Limiting Conditions 
    for PDMS and Safety Limits specified in the Technical Specifications 
    will remain unchanged.
        [The proposed changes would] not involve a significant increase 
    in the consequences of an accident previously evaluated because no 
    accident conditions or assumptions are affected. The proposed 
    changes do not alter the source term, containment isolation, or 
    allowable radiological consequences. The staging of radioactive 
    materials such as the contaminated reactor coolant pump and motor 
    components will not result in a source term, that if released, would 
    exceed that previously analyzed in the PDMS SAR [safety analysis 
    report] in terms of off-site dose consequences. The proposed changes 
    have no adverse effect on any plant system.
        2. [The proposed changes would] not create the possibility of a 
    new or different kind of accident from any previously evaluated 
    because no new accident initiators or assumptions are introduced by 
    the proposed changes. The proposed changes have no direct effect on 
    any plant system. The changes do not affect any system functional 
    requirements, plant maintenance, or operability requirements.
        3. [The proposed changes would] not involve a significant 
    reduction in the margin of safety because the proposed changes do 
    not involve significant changes to the initial conditions 
    contributing to accident severity or consequences. The proposed 
    changes have no direct effect on any plant systems.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Law/Government Publications 
    Section, State Library of Pennsylvania, (Regional Depository) Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105.
        Attorney for licensee: Ernest L. Blake, Jr., Esquire, Shaw, 
    Pittman, Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Section Chief: Michael T. Masnik.
    
    Illinois Power Company, Docket No. 50-461, Clinton Power Station, Unit 
    1, DeWitt County, Illinois
    
        Date of amendment request: August 23, 1999.
        Description of amendment request: The proposed amendment would 
    delete certain license conditions that are obsolete and no longer 
    apply.
        Basis for proposed no significant hazards consideration 
    determination:
    
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    As required by 10 CFR 50.91(a), the licensee has provided its analysis 
    of the issue of no significant hazards consideration which is presented 
    below:
    
        (1) The proposed activity does not involve a significant 
    increase in the probability or consequences of any accident 
    previously evaluated.
        The proposed changes delete various license conditions each of 
    which has been fulfilled and no longer warrants a license condition. 
    As such, the changes are purely administrative in nature, and 
    involve no physical or operational changes to the facility. The 
    initial conditions and methodologies used in the accident analyses 
    consequently remain unchanged. Further, the proposed changes do not 
    change or alter the design assumptions for the systems or components 
    used to mitigate the consequences of an accident. Therefore, 
    accident analyses results are not impacted. On this basis, the 
    proposed amendment does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        (2) The proposed activity does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        As noted above, the proposed changes are purely administrative 
    and involve no physical or operational changes to the facility. As 
    such, the proposed changes do not affect the design or operation of 
    any system, structure, or component in the plant. The safety 
    functions of the related structures, systems, or components are not 
    changed in any manner, nor is the reliability or[f] any structures, 
    systems or components reduced. No new or different type of equipment 
    will be installed, and consequently, no new failure modes are 
    introduced. Therefore, the proposed amendment does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        (3) The proposed activity does not involve a significant 
    reduction in the margin of safety.
        The proposed changes are administrative in nature and have no 
    impact on the margin of safety of any Technical Specification. There 
    is no impact on safety limits or limiting safety system settings. 
    The changes do not affect any plant safety parameters or setpoints. 
    All active/applicable license conditions set forth in the CPS 
    Operating License will remain in effect, and no physical or 
    operational changes to the facility will result from these changes. 
    Therefore, the proposed changes do not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Vespasian Warner Public 
    Library, 120 West Johnson Street, Clinton, IL 61727.
        Attorney for licensee: Leah Manning Stetzner, Vice President, 
    General Counsel, and Corporate Secretary, 500 South 27th Street, 
    Decatur, IL 62525.
        NRC Section Chief: Anthony J. Mendiola.
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile Point 
    Nuclear Station Unit No. 1, Oswego County, New York
    
        Date of amendment request: August 26, 1999.
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TS) to reflect the proposed 
    implementation of Noble Metal Chemical Addition (NMCA) so as to enhance 
    the effectiveness of Hydrogen Water Chemistry (HWC) in mitigating 
    Intergranular Stress Corrosion Cracking (IGSCC) in reactor vessel 
    internal components. Specifically, the proposed amendment would raise 
    the reactor water conductivity limit in TS 3.2.3.a from 1.0 micromho/cm 
    to 20 micromho/cm and in TS 3.2.3.c.1 from 5.0 micromho/cm to 20.0 
    micromho/cm during NMCA application. The proposed amendment will also 
    raise the limit in TS 3.2.3.a and 3.2.3.b from 1 micromho/cm to 2 
    micromho/cm for up to a 5-month period at power operation following 
    NMCA application. The reactor water conductivity would be restored to 
    within the limit currently specified in TS 3.2.3 after the NMCA process 
    is complete. The Bases for TS 3.2.3 and 4.2.3, ``Coolant Chemistry,'' 
    would be supplemented to explain the changes resulting from NMCA.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed amendment to TS 3.2.3 will raise the reactor water 
    conductivity limit during and following NMCA application. This 
    change will allow the application of a layer of noble metals to the 
    reactor vessel internals to enhance the effectiveness of HWC in 
    mitigating IGSCC. An increased conductivity is expected both during 
    and following NMCA. However, during NMCA, this increase is caused 
    principally by residual ionic species which do not contribute to 
    IGSCC. Following NMCA application, the increased conductivity is 
    expected to be due to soluble iron and increased pH which has no 
    adverse affect on crack growth. Accordingly, the proposed change 
    will not adversely affect reactor vessel internals or reactor fuel 
    such that the probability of an accident is increased. The proposed 
    change will not alter the current TS requirements concerning 
    equipment needed to mitigate the consequences of an accident nor 
    affect the performance of this equipment. Therefore, operation in 
    accordance with the proposed amendment will not create an increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed amendment to TS 3.2.3 will raise the reactor water 
    conductivity limit during and following NMCA application. This 
    change will allow the application of a layer of noble metals to the 
    reactor vessel internals to enhance the effectiveness of HWC in 
    mitigating IGSCC. Except for these temporary exceptions to the 
    existing reactor coolant chemistry specification, no new plant or 
    system operating modes are being introduced and plant equipment will 
    continue to perform their intended function. An increased 
    conductivity is expected both during and following NMCA. However, 
    during NMCA, this increase is caused by ionic species which do not 
    contribute to IGSCC. Following NMCA application, the increased 
    conductivity is due to soluble iron and increased pH which has no 
    adverse affect on crack growth. Accordingly, the proposed changes 
    will not affect plant equipment in a way to create a new or 
    different kind of accident. Therefore, operation in accordance with 
    the proposed amendment will not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The operation of Nine Mile Point Unit 1, in accordance with the 
    proposed amendment, will not involve a significant reduction in a 
    margin of safety.
        The proposed amendment to TS 3.2.3 will raise the reactor water 
    conductivity limit during and following the application of NMCA. 
    During NMCA, the proposed change will raise the reactor water 
    conductivity limit in TS 3.2.3a and 3.2.3c.1 to 20 [micromho/cm]. 
    However, the expected increase in coolant conductivity is caused 
    principally by ionic species which do not contribute to IGSCC and, 
    therefore, will not adversely affect reactor vessel internals or 
    reactor fuel.
        Following NMCA application, industry experience indicates that 
    there may be an elevated conductivity approaching the 1 [micromho/
    cm] conductivity limit delineated in TS 3.2.3a and 3.2.3b. To 
    provide operating margin, NMPC proposes to raise this limit to 2 
    [micromho/cm] for up to 5 months of power operation following 
    application. The expected increase in the conductivity is attributed 
    to an increase in soluble iron and pH in the reactor coolant which 
    results from the application of the noble metals and its affect on 
    the deposits on the fuel. Soluble iron nor increased pH contribute 
    to IGSCC crack growth. The existing 1 [micromho/cm] limit is based 
    on EPRI [Electric Power Research Institute] guidelines action Level 
    2 for power operation, which assumes normal
    
    [[Page 51348]]
    
    conductivity below .3 [micromho/cm]. Increasing the limit to 2 
    [micromho/cm] during the period when soluble iron levels are high 
    provides an equivalent operating margin consistent with the chloride 
    and sulfate limits. Accordingly, this temporary ([less than] 5 
    months) elevated conductivity is expected, acceptable, and not 
    considered ``abnormal'' as discussed in TS 4.2.3 and associated 
    Bases. Daily samples of coolant for conductivity, chlorides and 
    sulfates will continue to be performed to assure water quality.
        Therefore, operation in accordance with the proposed amendment 
    will not involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
        Attorney for licensee: Mark J. Wetterhahn, Esquire, Winston & 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Section Chief: S. Singh Bajwa.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of amendment request: August 26, 1999
        Description of amendment request: The proposed amendment would 
    raise the condensate storage tank (CST) low level setpoint and the 
    corresponding allowable value in Technical Specification (TS) Tables 
    3.3.3-2 and 3.3.5-2. The subject setpoint is associated with the 
    automatic transfer of the High Pressure Coolant Injection (HPCI) and 
    Reactor Core Isolation Cooling (RCIC) pump suctions from the CST to the 
    suppression pool in the event of low CST level. These changes are being 
    made to address concerns regarding potential vortexing in the HPCI and 
    RCIC suction flowpaths.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) The proposed changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The systems affected by the proposed change provide accident 
    mitigation functions. Neither the proposed increase in level 
    setpoint nor the reliance on operator action to maintain the 
    required 135,000 gallon reserve volume in the condensate storage 
    tank (CST) can affect initiation of a design basis accident.
        Raising the CST low level setpoint to account for potential 
    vortexing in the HPCI and RCIC suction flowpaths provides assurance 
    that the functions of these systems can be properly carried out. 
    There will no longer be a possibility of air entrainment into the 
    RCIC and HPCI pumps suction at low levels in the CST. Initiation of 
    RCIC or HPCI flow is unaffected by this modification. Execution of 
    the suction line transfer to the suppression pool remains an 
    entirely automatic function, utilizing the same safety related 
    instrument signals as previously.
        Reliance on level alarms and operator action to maintain the 
    135,000-gallon minimum reserve water volume in the CST, in lieu of 
    internal standpipes, cannot increase the consequences of an 
    accident. This is an operational condition that establishes initial 
    conditions prior to an accident occurring. Operators would have 
    sufficient time to respond to a CST level decrease under non-
    accident conditions. Manually transferring HPCI and RCIC suction to 
    the safety related suppression pool should CST level decline below 
    203,000 gallons (the 135,000 gallons required inventory, plus 68,000 
    gallons unusable) ensures HPCI and RCIC remain fully capable of 
    performing their design basis functions.
        All parameters pertaining to the accident analysis, including 
    pump initiation time, flowrate, volume and duration of flow 
    delivered to the reactor vessel remain satisfied following 
    implementation of this proposed change. Therefore, no accident 
    scenario evaluated in the SAR [Safety Analysis Report] will be 
    affected, and the radiological consequences of accidents previously 
    evaluated in the SAR are not increased.
        These changes, therefore, do not modify or add any initiating 
    parameters that would significantly increase the probability or 
    consequences of any previously analyzed accident.
        (2) The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Implementation of these proposed changes cannot create the 
    possibility of a different type of accident from any previously 
    considered. First, the affected systems only perform mitigation 
    functions, so postulated failures of any of these systems would not 
    initiate a design basis accident. The function credited in the 
    safety analysis is automatic transfer of the HPCI and RCIC suction 
    lines from the CST to the suppression pool. This automatic transfer 
    will still occur as required, with the only difference being 
    execution earlier at a higher CST water level. Any considerations 
    associated with maintaining the required minimum CST water level, 
    including reliance on an alarm and operator action in lieu of a 
    passive design feature, cannot lead to an accident of a different 
    type since the CST itself is explicitly excluded from consideration 
    in the accident analysis. Although the preference is to provide 
    shutdown cooling with the reactor grade water of the CST, failure to 
    do so will neither impact the ability to achieve shutdown cooling 
    nor create a new type of accident.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        (3) The proposed change does not involve a significant reduction 
    in a margin of safety.
        The margin of safety of the affected TS is maintained. RCIC is 
    provided to assure adequate core cooling in the event of reactor 
    isolation from its primary heat sink and concurrent loss of 
    feedwater flow to the reactor vessel without requiring actuation of 
    ECCS [Emergency Core Cooling System] equipment. This function will 
    be accomplished. HPCI provides a backup to RCIC for safe shutdown 
    and the ECCS function of ensuring the reactor core is adequately 
    cooled to limit fuel clad temperature during a small break loss of 
    coolant accident. The safety analysis does not credit CST water. 
    Since the automatic transfer to the suppression pool is assured with 
    the same high quality and reliability as before, the ECCS function 
    is not affected. Should CST level decline below the required minimum 
    volume, operators would align HPCI and RCIC suction to the 
    suppression pool. System design functions, including containment 
    isolation, continue to be maintained in this alignment.
        The CST also provides a source of water for shutdown during 
    station blackout (SBO) scenarios. The proposed changes do not affect 
    the ability to recover from a SBO scenario.
        Core spray is provided to assure that the core is adequately 
    cooled following a LOCA [Loss of Coolant Accident] and provides core 
    cooling capacity for all break sizes. Core spray is a primary 
    cooling source after the reactor vessel is depressurized and a 
    source for flooding in case of accidental draining. In Operational 
    Conditions 4 or 5, the CST is relied upon as the cooling water 
    source if the suppression pool is drained below its minimum level. 
    Operator actions in response to a CST alarm ensure sufficient 
    condensate inventory is available to accomplish this function.
        ECCS instrumentation (HPCI) is provided to initiate actions to 
    mitigate the consequences of accidents that are beyond the ability 
    of the operator to control. RCIC instrumentation is provided to 
    initiate actions to assure adequate core cooling in the event of 
    reactor isolation from its primary heat sink and the loss of 
    feedwater flow to the reactor vessel. The HPCI and RCIC level 
    instruments continue to provide their automatic function thereby 
    preserving the design requirements of these systems. Remote shutdown 
    instrumentation and controls ensure that sufficient capability is 
    available to permit shutdown and maintenance of Hot Shutdown of the 
    unit from locations outside the control room in the event control 
    room habitability is lost. RCIC continues to satisfy this function.
        All design basis requirements of HPCI, RCIC, core spray and the 
    CST continue to be satisfied to ensure safe shutdown and
    
    [[Page 51349]]
    
    mitigate a LOCA. Required water volumes remain available for core 
    cooling, as is the automatic transfer to the safety related 
    suppression pool source.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
        Attorney for licensee: Jeffrie J. Keenan, Esquire, Nuclear Business 
    Unit--N21, P.O. Box 236, Hancocks Bridge, NJ 08038.
        NRC Section Chief: James W. Clifford.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of amendment request: July 29, 1999.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) Surveillance Requirement 4.6.1.1 to 
    clarify when verification of primary containment integrity may be 
    performed by administrative means and to change the surveillance 
    interval for verification of manual valves and blind flanges inside of 
    containment.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below:
    
        1. The operation of Salem Nuclear Generating Station, Unit Nos. 
    1 and 2, in accordance with the proposed amendment will not involve 
    a significant increase in the probability or consequences of an 
    accident previously evaluated.
        The licensee has determined that the proposed change will not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated. The proposed change revises means 
    for verification of containment integrity in certain cases by 
    allowing the verification to be conducted by administrative means 
    such as tagging requests, other TS surveillance procedures and 
    previously performed valve alignments. Although the current Salem 
    TSs allow the use of administrative means to verify valve position, 
    its application is limited to valves that are open under 
    administrative controls.
        The proposed amendment does not change the position of 
    containment isolation valves or otherwise modify the containment 
    integrity. Thus, the assumptions made in evaluating the occurrence 
    and radiological consequences of accidents described in the Safety 
    Analysis Report (SAR) have not been changed. The proposed change to 
    use administrative means continues to ensure that the release of 
    radioactive materials from the containment atmosphere will be 
    restricted to those leakage paths and associated leak rates assumed 
    in the accident analysis. Allowing the use of administrative means 
    to verify compliance with the surveillance requirement for these 
    valves is acceptable based on the limited access to these areas in 
    Modes 1 through 4 (power operation through hot shutdown). The 
    probability of misalignment of these containment isolation valves, 
    once they have been verified in the proper position is small. The 
    probability of occurrence of any previously evaluated accident is 
    independent of valve position verification.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated in the SAR.
        2. The operation of Salem Nuclear Generating Station, Unit Nos. 
    1 and 2, in accordance with the proposed amendment does not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        The licensee has determined that the proposed amendment does not 
    physically alter the facility or change the operation of the 
    facility. The proposed change does not affect the current operation 
    and response of any systems, structures or components assumed to 
    function in the accident analysis. Additionally, the proposed change 
    does not increase the consequences of a malfunction of equipment 
    important to safety. The proposed change to use administrative means 
    in lieu of field verification continues to ensure that the release 
    of radioactive materials from the containment atmosphere will be 
    restricted to those leakage paths and associated leak rates assumed 
    in the accident analysis.
        Therefore, the proposed amendment does not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The operation of Salem Nuclear Generating Station, Unit Nos. 
    1 and 2, in accordance with the proposed amendment does not involve 
    a significant reduction in a margin of safety.
        The licensee has determined that the proposed amendment does not 
    involve a significant reduction in a margin of safety. The proposed 
    change involves a revision of certain TSs surveillance requirements 
    and frequency of performance. The proposed change does not modify 
    hardware or plant operation, and the accident analyses are 
    unchanged. The proposed amendment will continue to ensure that the 
    proper valves are identified and tested in accordance with the TS 
    requirements. Therefore, the proposed changes do not involve a 
    significant reduction in a margin of safety.
    
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079
        Attorney for licensee: Jeffrie J. Keenan, Esquire, Nuclear Business 
    Unit--N21, P.O. Box 236, Hancocks Bridge, NJ 08038
        NRC Section Chief: James W. Clifford
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of amendment request: August 25, 1999.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) Appendix C, ``Additional 
    Conditions,'' to authorize the performance of single cell charging of 
    operable safety-related batteries by using non-Class 1E single cell 
    battery chargers, with proper electrical isolation. The single cell 
    chargers would be used to restore individual cell float voltage to the 
    normal TS limit.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed change permits the use of an industry accepted 
    method to restore a battery cell to its design basis from an 
    OPERABLE but degraded condition or to prevent a cell from becoming 
    degraded. IEEE Std [Institute of Electrical and Electronics 
    Engineers Standard] 450-1995, ``IEEE Recommended Practice for 
    Maintenance, Testing, and Replacement of Vented Lead Storage 
    Batteries for Stationary Applications,'' states that single cell 
    charging is an acceptable method of correcting low cell voltage or 
    low specific gravity conditions for a single cell or for a small 
    number of cells.
        At least two class 1E fuses in series will be used on both the 
    positive and negative leads between the battery and the charger to 
    protect the battery if a fault should develop in the charger. The 
    battery charger design includes diodes, a power transformer and 
    control circuitry to prevent draining the connected cells in the 
    event of a short circuit in the 120 Volt ac source or a loss of 
    charger input or output voltage. Charger output is controlled 
    automatically to prevent overcharging the connected cells.
        In the event of a controller failure resulting in charger 
    overvoltage, procedural controls
    
    [[Page 51350]]
    
    governing the use of the charger ensure the condition is detected 
    and corrected before failure of a connected cell occurs. While the 
    single cell charger is connected, procedures will require periodic 
    checks to verify proper charger operation and to measure electrolyte 
    level, temperature and specific gravity for the cells being charged. 
    Monitoring will be performed at least once every eight hours, a 
    frequency sufficient to ensure compliance with the requirements of 
    the Technical Specifications.
        An insulating material will be used to minimize the possibility 
    of shorting leads or clips at the battery. Administrative controls 
    governing the use and storage of transient loads are sufficient to 
    ensure the use of single cell battery chargers does not create a 
    potential missile hazard to safety related systems, structures and 
    components.
        The Class 1E DC system is not an accident initiator. The Class 
    1E DC system supports the operation of safety related equipment 
    required for the safe shutdown of the plant and for the mitigation 
    of accident conditions. Therefore, the proposed change does not 
    increase the probability of an accident previously evaluated.
        The station's dc systems will be operable to mitigate the 
    consequences of an accident previously evaluated. Single cell 
    charging would be limited to one OPERABLE class 1E battery bank at a 
    time for either the 28 VDC or 125 VDC systems. Therefore, failure of 
    a class 1E battery as a result of single cell charging would be 
    limited to a single channel and would not reduce the number of 
    OPERABLE dc sources below that required to safely shutdown the 
    plant. Administrative controls would also prohibit the use of single 
    cell charging for an OPERABLE class 1E battery if less than the 
    minimum number of class 1E batteries required by Technical 
    Specifications are OPERABLE.
        The proposed change does not cause the capability of the class 
    1E DC system to be degraded below the level assumed for any accident 
    described in the SAR [Safety Analysis Report]. It would enhance the 
    availability of safety related equipment required for the safe 
    shutdown of the plant and for the mitigation of accident conditions. 
    Therefore the radiological consequences of an accident will remain 
    inside the design basis while single cell charging is performed on 
    an OPERABLE battery.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The potential to adversely affect the Class 1E batteries is 
    minimized by the use of Class 1E fuses and by appropriate 
    administrative controls. Failure modes associated with the proposed 
    change are bounded by the loss of a Class 1E battery bank which was 
    previously evaluated. Therefore, the proposed change does not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change permits the use of non-Class 1E single cell 
    battery chargers, with proper electrical isolation, for charging 
    connected cells in OPERABLE class 1E batteries. This would allow 
    parameters for an individual cell or for a small number of cells to 
    be restored to the normal values specified in Technical 
    Specifications without affecting the remainder of the cells in the 
    battery. Increased cell monitoring after single cell charging, 
    together with PSE&G's corrective action program which requires 
    degraded and non-conforming conditions to be documented and 
    evaluated, provides assurance that the use of single cell charging 
    will not cause long-term cell degradation to go undetected. Since 
    all battery cells are required to be maintained within the allowable 
    values specified in Technical Specifications, and since the use of 
    the single cell charger will not adversely affect battery capacity 
    or capability, the proposed change does not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
        Attorney for licensee: Jeffrie J. Keenan, Esquire, Nuclear Business 
    Unit--N21, P.O. Box 236, Hancocks Bridge, NJ 08038.
        NRC Section Chief: James W. Clifford.
    
    Previously Published Notice of Consideration of Issuance of 
    Amendments to Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Commonwealth Edison Company, Docket Nos. STN 50-456 and STN 50-457, 
    Braidwood Station, Units 1 and 2, Will County, Illinois
    
        Date of amendment request: July 30, 1999.
        Description of amendment request: The proposed amendments would 
    temporarily change the Technical Specifications (TS) to increase the 
    upper temperature limit for the Ultimate Heat Sink (UHS) from 98 
    degrees Fahrenheit to 100 degrees Fahrenheit. The proposed temporary 
    change would be in effect until September 30, 1999.
        Date of publication of individual notice in Federal Register: 
    August 18, 1999 (64 FR 44962).
        Expiration date of individual notice: September 17, 1999.
        Local Public Document Room location: Wilmington Public Library, 201 
    S. Kankakee Street, Wilmington, Illinois 60481.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    [[Page 51351]]
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert County, 
    Maryland
    
        Date of application for amendments: November 30, 1998, as 
    supplemented May 25, 1999.
        Brief description of amendments: The amendments revise the 
    appropriate Technical Specifications to permit the use of leak-limiting 
    Alloy 800 repair sleeves developed by AAB--Combustion Engineering (ABB-
    CE) to be used at Calvert Cliffs.
        Date of issuance: September 1, 1999.
        Effective date: As of the date of issuance to be implemented during 
    the spring 2000.
        Amendment Nos.: 231 and 207.
        Facility Operating License Nos. DPR-53 and DPR-69: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 13, 1999 (64 FR 
    2244).
        The May 25, 1999, letter provided clarifying information that did 
    not change the initial proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of these amendments is 
    contained in a Safety Evaluation dated September 1, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
    
    Carolina Power & Light Company, Docket No. 50-261, H. B. Robinson Steam 
    Electric Plant, Unit No. 2, Darlington County, South Carolina
    
        Date of application for amendment: January 28, 1999.
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) 5.6.5, ``Core Operating Limits Report (COLR),'' to 
    add two references to the list of approved topical reports.
        Date of issuance: September 1, 1999.
        Effective date: September 1, 1999.
        Amendment No.: 185.
        Facility Operating License No. DPR-23. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 24, 1999 (64 
    FR 9184).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 1, 1999.
        Local Public Document Room location: Hartsville Memorial Library, 
    147 West College Avenue, Hartsville, South Carolina 29550.
    
    Consolidated Edison Company of New York, Docket No. 50-247, Indian 
    Point Nuclear Generating Unit No. 2, Westchester County, New York
    
        Date of application for amendment: January 22, 1999.
        Brief description of amendment: The amendment revises Technical 
    Specifications 4.3.a and 4.3.b and Basis Section 4.3 to permit reactor 
    coolant system leak test to be performed at normal operating pressure 
    following each refueling outage according to the requirement of the 
    American Society of Mechanical Engineers Boiler and Pressure Vessel 
    Code, Section XI, and implemented in accordance with 10 CFR 50.55a(g).
        Date of issuance: September 2, 1999.
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment No.: 203.
        Facility Operating License No. DPR-26: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 7, 1999 (64 FR 
    17023).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 2, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Consumers Energy Company, Docket No. 50-255, Palisades Plant, Van Buren 
    County, Michigan
    
        Date of application for amendment: June 17, 1998, as supplemented 
    June 23 and December 2, 1998, and March 18, 1999.
        Brief description of amendment: The amendment revises the Technical 
    Specifications to reduce the minimum reactor vessel flow rate 
    requirement and revise the units of measurement for consistency with 
    the flow measurement procedure.
        Date of issuance: September 3, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 60 days of issuance.
        Amendment No.: 187.
        Facility Operating License No. DPR-20. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 2, 1998 (63 FR 
    36271).
        The December 2, 1998, letter provided additional clarifying 
    information and the March 18, 1999, letter requested a 60-day allowance 
    for implementation of the amendment. The additional information and 
    proposed change to the implementation period were within the scope of 
    the original Federal Register notice and did not change the staff's 
    initial proposed no significant hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 3, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423-3698.
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, Beaver 
    Valley Power Station, Unit Nos. 1 and 2, Shippingport, Pennsylvania
    
        Date of application for amendments: December 24, 1998, as 
    supplemented June 15, June 17, and July 7, 1999.
        Brief description of amendments: The amendments revise the 
    Technical Specification (TS) requirements for the axial flux difference 
    (AFD) monitor, quadrant power tilt ratio (QPTR) monitor, rod position 
    deviation monitor, and rod insertion limit (RIL) monitor. Specifically, 
    the changes (1) relocate requirements for the AFD monitor and the QPTR 
    monitor to the Licensing Requirements Manual; (2) delete requirements 
    for the rod position deviation monitor and RIL monitor from the TSs; 
    (3) modify Unit 1 surveillance requirements (SR) 4.1.3.5 and 4.1.3.6 by 
    incorporating the Unit 2 wording to provide surveillances more 
    consistent with the Limiting Condition for Operation; (4) change Unit 1 
    SR 4.1.3.2.2, SR 4.1.3.5, SR 4.1.3.6 and Unit 2 SR 4.1.3.5 from 24-hour 
    surveillance frequencies to 12-hour frequencies; and (5) delete Unit 1 
    SR 4.1.3.2.3.
        Date of issuance: August 30, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 60 days.
        Amendment Nos.: 225 and 102.
        Facility Operating License Nos. DPR-66 and NPF-73: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 27, 1999 (64 FR 
    4155) The June 15, June 17, and July 7, 1999, letters provided 
    additional information but did not change the initial proposed no 
    significant hazards consideration determination or expand the amendment 
    beyond the scope of the initial notice.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated August 30, 1999.
        No significant hazards consideration comments received: No
    
    [[Page 51352]]
    
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, PA 15001.
    
    Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear One, Unit 
    No. 1, Pope County, Arkansas
    
        Date of amendment request: April 9, 1999, as supplemented by letter 
    dated July 14, 1999.
        Brief description of amendment: Revises requirements affecting the 
    surveillance methods for the containment tendons, the conduct of 
    containment visual inspections, and the reporting methods employed in 
    disseminating the results of these inspections to the NRC.
        Date of issuance: September 9, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days from the date of issuance.
        Amendment No.: 199.
        Facility Operating License No. DPR-51: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 19, 1999 (64 FR 
    27320).
        The July 14, 1999, letter provided clarifying information that did 
    not change the scope of the April 9, 1999, application and the initial 
    proposed no significant hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 9, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, Arkansas 72801.
    
    FirstEnergy Nuclear Operating Company, Docket No. 50-440, Perry Nuclear 
    Power Plant, Unit 1, Lake County, Ohio
    
        Date of application for amendment: March 17, 1999.
        Brief description of amendment: This amendment approves a proposed 
    modification that changes the Perry facility as described in the 
    Updated Safety Analysis Report. The change incorporates a leak-off line 
    in the residual heat removal system. The leak-off line is designed to 
    eliminate an operator work around, which will significantly reduce the 
    collective dose to operations personnel.
        Date of issuance: August 31, 1999.
        Effective date: August 31, 1999.
        Amendment No.: 106.
        Facility Operating License No. NPF-58: This amendment authorizes 
    the revision of the Updated Safety Analysis Report.
        Date of initial notice in Federal Register: May 19, 1999 (64 FR 
    27322)
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated August 31, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, OH 44081
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Nuclear Generating Plant, Unit 3, Citrus County, Florida
    
        Date of application for amendment: May 10, 1999.
        Brief description of amendment: The amendment corrects an invalid 
    reference in Section 5.8, ``High Radiation Area,'' of the Crystal River 
    Unit 3 Improved Technical Specifications (ITS).
        Date of issuance: September 3, 1999.
        Effective date: September 3, 1999.
        Amendment No.: 186.
        Facility Operating License No. DPR-72: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 14, 1999 (64 FR 
    38026)
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 3, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 34428.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, Millstone 
    Nuclear Power Station, Unit No. 3, New London County, Connecticut
    
        Date of application for amendment: May 17, 1999.
        Brief description of amendment: The amendment revises Technical 
    Specification (TS) section 4.4.6.2.2.e to replace the reference to 
    American Society of Mechanical Engineers (ASME) Code paragraph IWV-
    3472(b) which pertains to the frequency of leakage rate testing for 6-
    inch, nominal pipe size valves and larger with the requirement that the 
    surveillance interval and frequency of surveillance leakage rate 
    testing for these valves be performed pursuant to the requirements of 
    TS 4.0.5, ``Operations and Surveillance Requirements.''
        Date of issuance: September 10, 1999.
        Effective date: As of the date of issuance.
        Amendment No.: 174.
        Facility Operating License No. NPF-49: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 14, 1999 (64 FR 
    38033).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 10, 1999.
        No significant hazards consideration comments received: No
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, Prairie 
    Island Nuclear Generating Plant, Units 1 and 2, Goodhue County, 
    Minnesota
    
        Date of application for amendments: May 13, 1999.
        Brief description of amendments: The amendments revise Technical 
    Specifications 6.2.A.2, ``Onsite and Offsite Organizations,'' to 
    reflect a change in the plant organizational structure that was 
    implemented on March 1, 1999.
        Date of issuance: August 26, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days.
        Amendment Nos.: 146 and 137.
        Facility Operating License Nos. DPR-42 and DPR-60: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 14, 1999 (64 FR 
    38034).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated August 26, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: April 12, 1999.
        Brief description of amendment: The amendment removes from the 
    Technical Specifications a footnote regarding departure from nucleate 
    boiling analysis.
        Date of issuance: September 2, 1999.
        Effective date: September 2, 1999.
    
    [[Page 51353]]
    
        Amendment No.: 191.
        Facility Operating License No. DPR-64: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 19, 1999 (64 FR 
    27324).
        No significant hazards consideration comments received: No.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 2, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Power Authority of the State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: January 28, 1999, as 
    supplemented May 4, 1999
        Brief description of amendment: The amendment changes the reactor 
    trip on turbine trip from at or above 10 percent rated power to at or 
    above the P-8 setpoint.
        Date of issuance: September 8, 1999.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 192.
        Facility Operating License No. DPR-64: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 21, 1999 (64 FR 
    19563).
        The May 4, 1999, letter provided additional information that did 
    not change the staff's proposed finding of no significant hazards 
    consideration.
        No significant hazards consideration comments received: No.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 8, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of application for amendment: March 29, 1999, as supplemented 
    June 21, 1999.
        Brief description of amendment: This amendment revises the 
    Technical Specifications (TSs) by relocating the procedural details of 
    the Radiological Effluent Technical Specifications (RETS) to the 
    Offsite Dose Calculation Manual. The TSs were also revised to relocate 
    procedural details associated with solid radioactive wastes to the 
    Process Control Program. In addition, the Administrative Controls 
    section of the TSs was revised to incorporate programmatic controls for 
    radioactive effluents and environmental monitoring.
        These changes are consistent with the guidance provided in Generic 
    Letter 89-01, ``Implementation of Programmatic Controls for 
    Radiological Effluent Technical Specifications in the Administrative 
    Controls Section of the Technical Specifications and the Relocation of 
    Procedural Details of RETS to the Offsite Dose Calculation Manual or to 
    the Process Control Program.''
        Date of issuance: September 8, 1999.
        Effective date: As of the date of issuance, and shall be 
    implemented within 60 days.
        Amendment No.: 121.
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 19, 1999 (64 FR 
    27324).
        The June 21, 1999, supplement provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination or expand the scope of the original Federal 
    Register notice.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 8, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
    
    STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South 
    Texas Project, Units 1 and 2, Matagorda County, Texas
    
        Date of amendment request: June 7, 1999, as supplemented by letters 
    dated June 24 and August 24, 1999.
        Brief description of amendments: The amendments revised Technical 
    Specification (TS) 2.0, ``Safety Limits and Limiting Safety System 
    Settings,'' TS 3.2.5, ``DNB [Departure from Nucleate Boiling] 
    Parameters,'' and the associated Bases, and Administrative Controls 
    Section 6.9.1.6, ``Core Operating Limits Report [(COLR)],'' by 
    relocating cycle-specific reactor coolant system-related parameter 
    limits from the TSs to the COLR.
        Date of issuance: September 2, 1999.
        Effective date: September 2, 1999, to be implemented within 30 
    days.
        Amendment Nos.: Unit 1--115; Unit 2--103.
        Facility Operating License Nos. NPF-76 and NPF-80: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 14, 1999 (64 FR 
    38036).
        The August 24, 1999, supplement provided revised TS pages and 
    clarifying information that was within the scope of the original 
    Federal Register notice and did not change the staff's initial proposed 
    no significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 2, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488.
    
    Tennessee Valley Authority, Docket Nos. 50-260 and 50-296, Browns Ferry 
    Nuclear Plant, Units 2 and 3, Limestone County, Alabama
    
        Date of application for amendments: September 4, 1998, as 
    supplemented by letter dated November 25, 1998.
        Brief description of amendments: Revises the licensing basis to 
    credit containment pressure in excess of atmospheric pressure in the 
    analysis for Emergency Core Cooling Systems pump.
        Date of issuance: September 3, 1999.
        Effective date: As of date of issuance, to be incorporated into the 
    Final Safety Analysis Report (FSAR) with the next update.
        Amendment Nos.: 261 and 220.
        Facility Operating License Nos. DPR-52 and DPR-68: Amendments 
    approves changes to the FSAR.
        Date of initial notice in Federal Register: September 23, 1998 (63 
    FR 5093). The November 25, 1998 supplemental letter did not change the 
    original proposed no significant hazards determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 3, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Athens Public Library, 405 E. 
    South Street, Athens, Alabama 35611.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: January 15, 1999 (TS 98-09).
    
    [[Page 51354]]
    
        Brief description of amendments: The amendments relocate seismic 
    instrumentation requirements from the Technical Specifications to the 
    Technical Requirements Manual.
        Date of issuance: September 7, 1999.
        Effective date: As of the date of issuance to be implemented no 
    later than 45 days after issuance.
        Amendment Nos.: Unit 1--245; Unit 2--236.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: February 10, 1999 (64 
    FR 6712).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 7, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak Steam 
    Electric Station, Unit Nos. 1 and 2, Somervell County, Texas
    
        Date of amendment request: May 24, 1999, as supplemented by letter 
    dated July 9, 1999.
        Brief description of amendments: The amendments remove several 
    cycle-specific parameter limits from the Technical Specifications 
    (TSs). These parameter limits are added to the Core Operating Limits 
    Report (COLR). Appropriate references to the COLR are inserted in the 
    affected TSs. In addition, the core safety limit curves are replaced 
    with safety limits more directly applicable to the fuel and fuel 
    cladding fission product barriers.
        The affected TSs are: (1) TS 2.0, ``Safety Limits (Sls),'' (2) TS 
    3.3.1, ``Reactor Trip System Instrumentation Setpoints,'' (3) TS 3.4.1, 
    ``RCS Pressure, Temperature, and Flow Departure from Nucleate Boiling 
    (DNB) Limits,'' and (4) TS 5.6.5, ``Core Operating Limits Report.''
        Date of issuance: August 30, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days from the date of issuance.
        Amendment Nos.: 67 and 67.
        Facility Operating License Nos. NPF-87 and NPF-89: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 30, 1999 (64 FR 
    35213) and July 28, 1999, (64 FR 40908).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated August 30, 1999.
        No significant hazards consideration comments received: No
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas 76019.
    
    TU Electric Company, Docket Nos. 50-445 and 50-446, Comanche Peak Steam 
    Electric Station (CPSES), Unit Nos. 1 and 2, Somervell County, Texas
    
        Date of amendment request: May 14, 1999.
        Brief description of amendments: The amendments change the licenses 
    to accurately reflect the new corporate name of the current licensee, 
    ``TXU Electric Company'' in Facility Operating Licenses NPF-87 and NPF-
    89 for CPSES, Units 1 and 2, respectively.
        Date of issuance: August 31, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days from the date of issuance.
        Amendment Nos.: Unit 1--Amendment No. 68; Unit 2--Amendment No. 68.
        Facility Operating License Nos. NPF-87 and NPF-89: The amendments 
    change the Operating Licenses.
        Date of initial notice in Federal Register: June 30, 1999 (64 FR 
    35213).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated August 31, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas 76019.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: May 26, 1999.
        Brief description of amendment: The amendment revises the 
    suppression pool water temperature surveillance requirements to specify 
    monitoring the temperature every 5 minutes when performing testing that 
    adds heat to the suppression pool. In addition, the amendment revises 
    the requirement to check the suppression chamber water level and 
    temperature from ``once per shift'' to ``daily'' and specifies that it 
    is the average temperature that is checked.
        Date of Issuance: August 30, 1999.
        Effective date: As of the date of issuance, and shall be 
    implemented within 30 days.
        Amendment No.: 174.
        Facility Operating License No. DPR-28.: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 28, 1999 (64 FR 
    40909).
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated August 30, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
    Yankee Atomic Electric Co., Docket No. 50-29, Yankee Nuclear Power 
    Station (YNPS) Franklin County, Massachusetts
    
        Date of application for amendment: March 17, 1999.
        Brief description of amendment: Revises the Possession Only License 
    by deleting License Condition 2.C.(10) related to the Fitness-For-Duty 
    program.
        Date of issuance: August 27, 1999.
        Effective date: August 27, 1999.
        Amendment No.: 152.
        Facility Operating License No. DPR-3. Amendment revises the 
    license.
        Date of initial notice in Federal Register: June 2, 1999 (64 FR 
    29717).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated August 27, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Greenfield Community College, 
    1 College Drive, Greenfield, Massachusetts 01301.
    
    Notice of Issuance of Amendments to Facility Operating Licenses and 
    Final Determination of No Significant Hazards Consideration and 
    Opportunity for a Hearing (Exigent Public Announcement or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was
    
    [[Page 51355]]
    
    not time for the Commission to publish, for public comment before 
    issuance, its usual 30-day Notice of Consideration of Issuance of 
    Amendment, Proposed No Significant Hazards Consideration Determination, 
    and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By October 22, 1999, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any
    
    [[Page 51356]]
    
    hearing held would take place while the amendment is in effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
        For the Nuclear Regulatory Commission.
    
        Dated at Rockville, Maryland, this 15th day of September, 1999.
    Elinor G. Adensam,
    Acting Director, Division of Licensing Project Management, Office of 
    Nuclear Reactor Regulation.
    [FR Doc. 99-24573 Filed 9-21-99; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Published:
09/22/1999
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
99-24573
Dates:
As of the date of issuance to be implemented during the spring 2000.
Pages:
51343-51356 (14 pages)
PDF File:
99-24573.pdf