98-25281. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 63, Number 184 (Wednesday, September 23, 1998)]
    [Notices]
    [Pages 50932-50948]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 98-25281]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from August 28, 1998, through September 11, 1998. 
    The last biweekly notice was published on September 9, 1998 (63 FR 
    48256).
    
    Notice of Consideration of Issuance of Amendments to Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules and 
    Directives Branch, Division of Administration Services, Office of 
    Administration, U.S. Nuclear Regulatory Commission, Washington, DC 
    20555-0001, and should cite the publication date and page number of 
    this Federal Register notice. Written comments may also be delivered to 
    Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville, 
    Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of 
    written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC. The 
    filing of requests for a hearing and petitions for leave to intervene 
    is discussed below.
        By October 23, 1998, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR Part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or
    
    [[Page 50933]]
    
    petition; and the Secretary or the designated Atomic Safety and 
    Licensing Board will issue a notice of a hearing or an appropriate 
    order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: June 26, 1998.
        Description of amendment request: The proposed Technical 
    Specification (TS) amendment would amend various TS pages to correct 
    typographical errors, remove inadvertent replication of information, 
    and update various Bases sections.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed administrative changes involving typographical 
    errors and updating the Bases reflect plant design, safety limit 
    settings, and plant system operation previously reviewed and 
    approved by the NRC. These changes, therefore, do not modify or add 
    any initiating parameters that would significantly increase the 
    probability or consequences of any previously analyzed accident.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        These proposed changes do not involve any potential initiating 
    events that would create a new or different kind of accident. 
    Therefore, the proposed changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        These changes reflect information previously reviewed and 
    approved by the NRC. The proposed changes will make the information 
    in the Technical Specifications consistent with that already 
    approved by the NRC. Therefore, it is concluded that the proposed 
    amendment does not involve a significant reduction in a margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W. S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Cecil O. Thomas.
    
    [[Page 50934]]
    
    Boston Edison Company, Docket No. 50-293, Pilgrim Nuclear Power 
    Station, Plymouth County, Massachusetts
    
        Date of amendment request: April 25, December 23, 1996, August 8, 
    September 5, 1997, March 26, July 31, and August 24, 1998. The August 
    24, 1998, supplement supersedes the previous no significant hazards 
    consideration determination included in letters dated April 25, 1996, 
    and March 26, 1998 for the EDG AOT.
        Description of amendment request: The proposed Technical 
    Specification (TS) amendment would extend the Emergency Diesel 
    Generator (EDG) allowed outage time (AOT) from 72 hours to 14 days. In 
    support of this change the licensee has proposed various TS changes to 
    decrease the consequences of the extended AOT.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Operation of Pilgrim Nuclear Power Station in accordance with 
    the proposed license amendment will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated because of the following:
        An Individual Plant Examination (IPE) for Internal Events was 
    submitted to the NRC in response to Generic Letter 88-20 in 
    September 1992. The supporting probabilistic safety analysis (PSA) 
    model was updated as described in BECo letter 95-127, dated December 
    28, 1995. The updated PSA model was used to quantify the overall 
    impact of the proposed EDG 14-day AOT on core damage frequency. Part 
    III of BECo No. 2.96.040 provides the results of a comprehensive 
    [probabilistic safety assessment] PSA of the impact of the proposed 
    AOTs for the EDGs and [startup transformer] SUT and [shutdown 
    transformer] SDT. As shown in Part III, there is no significant 
    increase in risk due to the proposed change. Thus, the proposed 
    change does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The existing specification 3.9.B.1 is separated into two 
    segments (a and b) because of the proposed different AOTs for the 
    SUT and SDT transformers. As a result of the PSA, the AOT for the 
    SUT (a) is reduced from 7 days to 72 hours, while the AOT for the 
    SDT (b) remains at 7 days. The reduction of the AOT from 7 days to 3 
    days is based on the relative risk importance of the SUT support to 
    the balance of plant systems. Similarly, an additional reduction 
    from 72 hours to 48 hours is proposed in the AOT for a simultaneous 
    loss of both the SUT or SDT and an EDG (TS 3.9.B.4) based upon the 
    SUT's or SDT's contribution to risk and that two power sources have 
    been removed from the associated bus. The AOT reductions represent a 
    measurable decrease in risk as assessed in the PSA. Thus, the 
    probability or consequences of an accident previously evaluated are 
    not increased.
        The current technical specifications allow one EDG to be out of 
    service for three days based on the availability of the SUT and SDT 
    and the fact that each EDG carries sufficient engineered safeguards 
    equipment to cover all design basis accidents. Additionally, the SDT 
    can provide adequate power for one train of ESF equipment for all 
    operating, transient, and accident conditions. With one EDG out of 
    service and a Loss of Offsite Power (LOOP) condition, the capability 
    to power vital and auxiliary system components remains available via 
    the other EDG. Increasing the EDG AOT to 14 days provides 
    flexibility in the maintenance and repair of the EDGs. The EDG 
    unavailability will be monitored and trended in accordance with the 
    Maintenance Rule. The PSA analyses supports the change to a 14 day 
    AOT for the EDGs based on an insignificant increase in overall risk. 
    Implementation of the proposed change is expected to result in less 
    than a one percent increase in the baseline core damage frequency 
    (2.84E-05/yr), which is considered to be insignificant relative to 
    the underlying uncertainties involved with PSA. An additional 
    condition is added requiring the SBO-DG to remain operable for 
    extending the inoperable EDG AOT from 3 days to 14 days, thereby 
    assuring that one EDG and SBO-DG are available during the extended 
    EDG AOT. Thus, the 14-day EDG AOT does not involve an increase in 
    the probability or consequences of an accident previously evaluated.
        The proposed addition of the CRMP does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated. Because the changes are administrative in 
    nature and deal only with risk assessment, they have no bearing on 
    accident initiation or mitigation. Therefore, the changes will not 
    affect the probability or consequences of an accident previously 
    evaluated.
        The proposed change does not affect the design or performance of 
    the EDGs, and the change will not result in a significant increase 
    in the consequences or probability of an accident previously 
    analyzed. These changes do not involve a increase in the probability 
    or consequences of an accident previously analyzed.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The operation of PNPS in accordance with the proposed license 
    amendment will not create the possibility of a new or different kind 
    of accident from any accident previously evaluated because of the 
    following:
    The proposed amendment will extend the action completion/allowed 
    outage time for an inoperable EDG from 3 days to 14 days. During 
    this extension, the [station blackout diesel generator] SBO-DG is 
    required to be operable and normal breaker configuration is required 
    to be verified to ensure the SBO-DG is capable of energizing the 
    safety bus associated with the inoperable EDG. These actions assure 
    one EDG and SBO-DG are operable during extended EDG AOTs. The EDGs 
    are designed as backup AC power sources for essential safety systems 
    in the event of loss of offsite power. The SBO-DG is designed to 
    cope with a station black out transient. The proposed AOT does not 
    change the conditions, operating configurations, or minimum amount 
    of operating equipment assumed in the safety analysis for accident 
    mitigation. The EDGs, SBO-DG and AC equipment are not accident 
    initiators. No change is being made in the manner in which the EDGs 
    provide plant protection. No new modes of plant operation are 
    involved. An extended AOT for one EDG does not create a new or 
    different kind of accident [than] previously evaluated. The PSA 
    results concluded the risk contribution of the EDG AOT extension is 
    insignificant.
        Pilgrim has implemented an EDG reliability program to maintain 
    reliability of EDGs. The SBO-DG is included in the reliability 
    program, and the performance of EDGs and SBO-DG are trended for 
    compliance with Maintenance Rule requirements. Thus, the proposed 
    change does not introduce any new mode of plant operation or new 
    accident precursors, involve any physical alterations to plant 
    configurations, or make changes to system set points that could 
    initiate a new or different kind of accident. Therefore, operation 
    in accordance with the proposed change does not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        The AOT for an inoperable SUT is reduced from 7 days to 72 hours 
    based upon the PSA that was performed to quantitatively assess the 
    risk impact of the proposed amendment. Additionally, removal of the 
    SUT from service degrades the reliability of the offsite power 
    system and renders the balance of plant unavailable upon a plant 
    shutdown. The proposed reduction in AOT improves overall AC power 
    source availability because the SUT will potentially be inoperable 
    for shorter time periods. Therefore, reducing the AOT does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        The proposed addition of the [Configuration Risk Management 
    Program] CRMP does not create the possibility of a new or different 
    kind of accident from any accident previously evaluated because the 
    CRMP will not affect the manner in which [structures, systems, and 
    components] SSCs are designed, operated, or maintained. The 
    administrative changes proposed will only require a risk assessment 
    for specified plant configurations. Any risk assessments performed 
    as a result of this program will only serve to provide plant 
    personnel with risk insights associated with particular plant 
    configurations. Since the changes will not impact SSCs and all 
    accidents involving SSCs, the proposed change does not create a new 
    kind of accident from any previously evaluated.
    
    [[Page 50935]]
    
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The operation of PNPS in accordance with the proposed license 
    amendment will not involve a significant reduction in a margin of 
    safety. As shown in Part III [of the application dated April 25, 
    1996), incorporation of the proposed change involves an 
    insignificant reduction in the margin of safety (less than a one 
    percent increase in the baseline core damage frequency (2.84E-05/
    yr), which is considered to be insignificant relative to the 
    underlying uncertainties involved with PSA).
        Also, the proposed changes do not significantly reduce the basis 
    for any technical specification related to the establishment of, or 
    the maintenance of, a safety margin nor do they require physical 
    modifications to the plant. An additional condition is added 
    requiring the SBO-DG to remain operable, in addition to the operable 
    EDG associated with the redundant train while in the 14-day EDG AOT. 
    The PSA results showed that the risk contribution of extending the 
    AOT for an inoperable EDG is insignificant. Also, the reduction in 
    the AOT for the SUT should improve availability thereby reducing 
    overall risk with no reduction of the safety margin. Moreover, the 
    proposed changes affect neither the way in which the EDGs perform 
    their safety function nor the bases for their LCOs.
        The proposed change does not involve a significant reduction in 
    a margin of safety. The proposed administrative change to include a 
    risk management program will not impact how plant SSCs are designed, 
    operated, or maintained. The required risk assessments are intended 
    to provide insights that influence decisions on the acceptability of 
    abnormal plant configurations. These insights work in conjunction 
    with existing inputs into the decision-making process rather than as 
    the sole basis for making decisions. Therefore, the changes will not 
    reduce a margin of safety.
        As previously stated, implementation of the proposed changes is 
    expected to result in an insignificant increase in: (1) power 
    unavailability to the emergency buses (given that a loss of offsite 
    power has occurred), and (2) core damage frequency. Implementation 
    of the proposed changes does not significantly reduce a margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Plymouth Public Library, 11 
    North Street, Plymouth, Massachusetts 02360.
        Attorney for licensee: W.S. Stowe, Esquire, Boston Edison Company, 
    800 Boylston Street, 36th Floor, Boston, Massachusetts 02199.
        NRC Project Director: Cecil O. Thomas.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of amendment request: September 1, 1998.
        Description of amendment request: The licensee's request proposes 
    to revise Technical Specification 3/4.9.11 ``Water Level--New and Spent 
    Fuel Pools.'' As a result of the proposed amendment, the licensee has 
    also revised the Fuel Handling Building fuel handling accident analysis 
    and the Containment fuel handling accident analyses.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Revising the required spent fuel pool water level will not 
    increase the probability of a fuel handling accident. There is no 
    other physical alteration to any plant system, nor is there a change 
    in the method in which any safety related system performs its 
    function. Harris Nuclear Plant (HNP) has revised the fuel handling 
    accident analyses using the conservative assumptions associated with 
    this change. The revised fuel handling accident analyses demonstrate 
    that dose consequences as a result of a fuel handling accident 
    remain below 25% of the 10 CFR 100 guidelines as described in the 
    NRC Standard Review Plan.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed amendment does not create the possibility of a new 
    or different kind of accident from any accident previously evaluated 
    because there is no physical alteration to any plant system, other 
    than revising spent fuel pool water level, nor is there a change in 
    the method in which any safety related system performs its function. 
    HNP has design features to mitigate the consequences of a loss of 
    spent fuel pool water level which are unaffected by this change.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        Revising the required spent fuel pool water level does not 
    involve a significant reduction in the margin of safety. There is no 
    other physical alteration to any plant system, other than revising 
    spent fuel pool water level, nor is there a change in the method in 
    which any safety related system performs its function. HNP has 
    revised the fuel handling accident analyses using the conservative 
    assumptions associated with this change. The revised fuel handling 
    accident analyses demonstrate that dose consequences as a result of 
    a fuel handling accident remain below 25% of the 10 CFR 100 
    guidelines as described in the NRC Standard Review Plan.
        Therefore, the proposed change does not involve a significant 
    reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Project Director: Pao-Tsin Kuo.
    
    Commonwealth Edison Company, Docket Nos. 50-254 and 50-265, Quad Cities 
    Nuclear Power Station, Units 1 and 2, Rock Island County, Illinois
    
        Date of amendment request: August 31, 1998.
        Description of amendment request: The proposed amendment would 
    change the Quad Cities Technical Specifications (TS) to reflect an 
    increase in the maximum allowable Main Steam Isolation Valve (MSIV) 
    leakage from 11.5 standard cubic feet per hour (scfh) to 30 scfh per 
    valve when tested at 25 psig, in accordance with Surveillance 
    Requirement 4.7.D.6
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change to Technical Specification Surveillance 
    Requirement 4.7.D.6 increases the maximum allowable leakage rate for 
    a single Main Steam Isolation Valve (MSIV) from 11.5 scfh to 30 
    scfh. This change has no impact on the automatic or manual closure 
    features of the valve including automatic actuations and response 
    times. Closure of the MSIVs is a postulated transient considered in 
    the design basis of the plant. Since the proposed change does not 
    impact the response characteristics of the MSIVs during a postulated 
    transient
    
    [[Page 50936]]
    
    condition, the change does not impact the probability of an accident 
    previously evaluated.
        The change in allowable MSIV leakage has been evaluated to 
    assess the impact on control room operator dose and offsite dose 
    levels. The radiological assessment was performed with an updated 
    radiological methodology that included significant enhancements, 
    such as credit for suppression pool scrubbing, updated iodine dose 
    conversion factors, and allowance for higher burnup fuel designs. 
    Using this revised methodology, which is consistent with current 
    regulatory requirements, the resulting dose levels from a postulated 
    design basis accident continue to remain below the limits 
    established in 10 CFR 50, Appendix A, General Design Criteria 19 
    (GDC-19) and 10 CFR 100. Therefore, the proposed change does not 
    involve a significant increase in the consequences of an accident 
    previously evaluated
        Therefore this proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The safety function of the MSIVs is to provide a timely steam 
    line isolation to mitigate the release of radioactive steam and 
    limit reactor inventory loss under certain accident and transient 
    conditions. The MSIVs are designed to automatically close whenever 
    plant conditions warrant a main steam line isolation. The proposed 
    increase in allowable MSIV leakage does not impact the MSIV's 
    ability to perform its underlying safety function, nor does the 
    change involve any physical features of the valves and associated 
    steam lines to create a new or different type of accident.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any previously evaluated.
        Does the change involve a significant reduction in a margin of 
    safety?
        The proposed increase in allowable MSIV leakage represents a 
    nominal increase in the release of radioactivity during a design 
    basis event. The radiological assessment was performed with an 
    updated radiological methodology that included significant 
    enhancements, such as credit for suppression pool scrubbing, updated 
    iodine dose conversion factors, and allowance for higher burnup fuel 
    designs. Using this revised methodology, which is consistent with 
    current regulatory requirements, the resulting dose levels from a 
    postulated design basis accident continue to remain below the limits 
    established in 10 CFR 50, Appendix A, GDC-19 and 10 CFR 100.
        Therefore, these changes do not involve a significant reduction 
    in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    requested amendments involve no significant hazards consideration.
        Local Public Document Room location: Dixon Public Library, 221 
    Hennepin Avenue, Dixon, Illinois 61021.
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60603.
        NRC Project Director: Stuart A. Richards.
    
    Connecticut Yankee Atomic Power Company, Docket No. 50-213, Haddam Neck 
    Plant, Middlesex County, Connecticut
    
        Date of application of amendments: June 2, 1998.
        Description of amendment request: The proposed amendment relocates 
    seismic monitoring equipment requirements from the Technical 
    Specifications to the Technical Requirements Manual (TRM), a document 
    which is controlled under 10 CFR 50.59.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        CYAPCO has reviewed the proposed changes to the Technical 
    Specifications in accordance with 10 CFR 50.92 and concluded that the 
    changes do not involve a significant hazards consideration (SHC). The 
    basis for this conclusion is that the three criteria of 10 CFR 50.92(c) 
    are not compromised. The proposed changes do not involve an SHC because 
    the changes would not:
    
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        As a result of the present plant configuration which has the 
    fuel permanently removed from the reactor, the reactor-related 
    accidents previously evaluated (i.e., LOCA, MSLB, etc.) are no 
    longer possible. The accidents previously evaluated that are still 
    applicable to the plant are fuel handling accidents and gaseous and 
    liquid radioactive releases.
        There is no significant increase in the probability of a fuel 
    handling accident since refueling operations have ceased. In fact, 
    there is a decrease in probability of a fuel handling accident since 
    the need to move/rearrange fuel assemblies is minimal until they are 
    removed from the spent fuel pool (i.e., for dry cask storage or for 
    transferring to USDOE possession). In addition, the consequences of 
    a fuel handling accident are continuing to decrease since the fuel 
    in the spent fuel pool is continuing to decay.
        The radiological consequences of a gaseous or liquid radioactive 
    release are bounded by the fuel handling accident during defueled 
    operation and a spent resin fire during the reactor coolant system 
    decontamination. With the plant defueled and permanently shutdown, 
    the demands on the radwaste systems are lessened since no new 
    radioisotopes are being generated by irradiation or fission. 
    Therefore, there is no increase in the probability or consequences 
    of a gaseous or liquid radioactive release.
        The ability of the plant to withstand a seismic event is not 
    affected by this proposed change. The seismic instrumentation does 
    not actuate any protective equipment or serve any direct role in the 
    mitigation of an accident. The equipment will continue to be 
    adequately controlled by the Technical Requirements Manual (TRM) to 
    ensure operability and alert operators to a seismic event, should 
    one occur, so that appropriate actions can be taken. Therefore, 
    there is no increase in the consequences of a seismic event.
        This material is being transferred to the TRM. This transfer is 
    in accordance with Generic Letter 95-10, ``Relocation of Selected 
    Technical Specifications Requirements Related to Instrumentation,'' 
    dated December 15, 1995 and is consistent with the NUREG-1431, 
    ``Standard Technical Specifications, Westinghouse Plants,'' Volume 
    1, Revision 1, dated April, 1995. The removed material included in 
    this category is Technical Specification 3/4.3.3.3 and the related 
    tables.
        Based on the above, the proposed changes to the Technical 
    Specifications do not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        There is no change in how spent fuel is stored or moved in the 
    spent fuel pool. Therefore, the postulated fuel handling accidents 
    are still bounding and are still considered as credible postulated 
    accidents.
        There is no change in the design and construction of plant 
    systems, structures and components with respect to the capability to 
    withstand a seismic event. Therefore, the currently assumed 
    radioactive releases are still bounding.
        This material is being transferred to the TRM. This transfer is 
    in accordance with Generic Letter 95-10 and is consistent with 
    NUREG-1431. The removed material included in this category are 
    Technical Specification 3/4.3.3.3 and the related tables.
        Based on the above, the proposed changes to the Technical 
    Specifications do not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The capability of the plant to withstand a seismic event or 
    other design basis accident is determined by the design and 
    construction of systems, structures, and components. The 
    instrumentation is used to alert operators to the seismic event and 
    evaluate the plant response. The NRC's Final Policy Statement on 
    Technical Specification Improvements (SECY-93-067) stated that 
    instrumentation to detect precursors to reactor coolant pressure 
    boundary leakage, such as seismic instrumentation, is not included 
    in the first criterion. As discussed above, the seismic
    
    [[Page 50937]]
    
    instrumentation does not serve as a protective design feature or 
    part of a primary success path for events which challenge fission 
    product barriers. The NRC staff, in Generic Letter 95-10, has 
    concluded that the seismic monitoring instrumentation does not 
    satisfy the 10 CFR 50.36 criteria and need not be included in the 
    technical specifications.
        This material is being transferred to the TRM. This transfer is 
    in accordance with Generic Letter 95-10 and is consistent with 
    NUREG-1431. The removed material included in this category are 
    Technical Specification 3/4.3.3.3.
        The proposed changes to the Technical Specifications do not 
    involve a significant reduction in a margin of safety due to the 
    fact that the capability of the plant to withstand a seismic event 
    or other design bases accident is not affected by this proposed 
    change.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Russell Library, 123 Broad 
    Street, Middletown, CT 06457.
        Attorney for the licensee: Mr. John A. Ritsher, Esquire, Ropes & 
    Gray, One International Place, Boston, Massachusetts, 02110.
        NRC Project Director: Seymour H. Weiss, Director.
    
    Detroit Edison Company, Docket No. 50-341, Fermi 2, Monroe County, 
    Michigan
    
        Date of amendment request: April 9, 1998 (NRC-98-0071).
        Description of amendment request: The proposed amendment would 
    revise the ``**'' footnote to Technical Specification (TS) 3.7.1.2, 
    ``Emergency Equipment Cooling Water System,'' Action ``a'' and add a 
    ``*'' footnote to TS 3.8.1.1, ``A.C. Sources--Operating,'' Action ``c'' 
    to make the actions consistent with TS 3.3.7.5, ``Accident Monitoring 
    Instrumentation,'' for the case of inoperable primary containment 
    oxygen monitoring instrumentation.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        The proposed change will permit operation with both of the 
    primary containment oxygen monitoring instrument channels inoperable 
    for up to 48 hours before requiring entry into a 12 hour shutdown 
    statement, consistent with Technical Specification 3.3.7.5, but less 
    restrictive than the requirements in Technical Specification 3.7.1.2 
    Action a and Technical Specification 3.8.1.1 Action c, which require 
    entry into the 12 hour shutdown statement immediately if the channel 
    in the remaining division is inoperable, followed by continued 
    shutdown to the COLD SHUTDOWN condition. The shutdown action 
    statement entry conditions for the primary containment oxygen 
    monitoring instrumentation should be no more restrictive in 
    Technical Specification 3.7.1.2 or Technical Specification 3.8.1.1, 
    than they are in Technical Specification 3.3.7.5 for both channels 
    being inoperable. The primary containment oxygen monitoring 
    instrumentation provides the same non-critical function regardless 
    of the reason for the system inoperability. The primary containment 
    oxygen monitors provide the control room operators with indication 
    and alarm of the oxygen concentration in the primary containment, 
    but do not provide any automatic function to mitigate an accident. 
    Because they perform only a monitoring function, the oxygen monitors 
    are not associated with the initiation of any previously evaluated 
    accident; therefore, there is no change in the probability of an 
    accident previously evaluated.
        The indication provided by the primary containment oxygen 
    monitors is used by the control room operators to ensure that the 
    oxygen concentration remains within limits and to help make 
    decisions regarding the use of the Combustible Gas Control System, 
    if necessary. Alternate methods using grab samples and laboratory 
    analytical equipment are available for obtaining primary containment 
    oxygen concentration if no primary containment oxygen monitoring 
    instrumentation is available. Additionally, the loss of both oxygen 
    analyzers is not critical for entry into the Emergency Operating 
    Procedures. Entry conditions for the post accident control of 
    hydrogen are based upon the primary containment hydrogen monitor 
    readings, and both channels of primary containment hydrogen 
    monitoring instrumentation are still required to remain operable in 
    accordance with Technical Specification 3.3.7.5. Therefore, this 
    change will not involve a significant increase in the consequences 
    of a previously evaluated accident.
        2. The change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        As discussed above, the primary containment oxygen monitors are 
    indication and alarm only instruments which provide information to 
    the control room operators. The proposed change does not introduce a 
    new mode of plant operation, nor does it involve a physical 
    modification to the plant. Therefore, the proposed change does not 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
        3. The change does not involve a significant reduction in the 
    margin of safety.
        The proposed change involves the length of time that both 
    primary containment oxygen monitoring instrument channels may be out 
    of service. It does not increase the out of service time beyond what 
    is already allowed by Technical Specification 3.3.7.5 for both 
    channels being inoperable. The primary containment oxygen monitors 
    are indication and alarm only instruments which do not affect any 
    parameters or assumptions used in the calculation of any safety 
    margin associated with Technical Specification Safety Limits, 
    Limiting Safety System Settings, Limiting Control Settings or 
    Limiting Conditions for Operation, or other previously defined 
    margins for any structure, system, or component. Therefore, the 
    proposed changes do not involve a significant reduction in a margin 
    of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Monroe County Library System, 
    Ellis Reference and Information Center, 3700 South Custer Road, Monroe, 
    Michigan 48161.
        Attorney for licensee: John Flynn, Esq., Detroit Edison Company, 
    2000 Second Avenue, Detroit, Michigan 48226.
        NRC Project Director: Cynthia A. Carpenter.
    
    Florida Power and Light Company, et al., Docket Nos. 50-335 and 50-389, 
    St. Lucie Plant, Unit Nos. 1 and 2, St. Lucie County, Florida
    
        Date of amendment request: August 24, 1998.
        Description of amendment request: The proposed amendment would 
    modify the Technical Specifications (TS) to clarify, for St. Lucie 
    Units 1 and 2, component operations to be verified in response to a 
    containment sump recirculation signal. For St. Lucie Unit 1, the 
    proposed amendment would modify the list of equipment that comprises an 
    operable control room emergency ventilation system to more accurately 
    reflect installed equipment. For St. Lucie Unit 2, license conditions 
    related to the movement of spent nuclear fuel between units will be 
    deleted and modified as appropriate to reflect the completion of the 
    Unit 1 spent fuel pool re-rack activities.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) Operation of the facility in accordance with the proposed 
    amendment would not
    
    [[Page 50938]]
    
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated.
        The proposed amendments do not involve accident initiators. The 
    changes to the Unit 1 and Unit 2 Technical Specifications provide 
    additions and clarification to component lists to ensure that 
    explicit terms of the affected specifications are consistent with 
    existing requirements. Other changes to the Unit 2 facility 
    operating license simply delete superseded license conditions that 
    have been previously satisfied and are therefore obsolete. The 
    revisions do not involve any change to the configuration or method 
    of operation of any plant equipment that is used to mitigate the 
    consequences of an accident, nor do the changes alter any 
    assumptions or conditions in the plant safety analyses. Therefore, 
    operation of either facility in accordance with its proposed 
    amendment would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        (2) Operation of the facility in accordance with the proposed 
    amendment would not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        The proposed amendments are administrative in nature and will 
    not change the physical plant or the modes of operation defined in 
    the facility operating licenses. The changes do not involve the 
    addition or modification of equipment nor do they alter the design 
    or operation of plant systems. Therefore, operation of either 
    facility in accordance with its proposed amendment would not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        (3) Operation of the facility in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        The changes proposed for the Unit 1 and Unit 2 Technical 
    Specifications provide additions and clarification to component 
    lists to ensure that explicit terms of the affected specifications 
    are consistent with existing requirements. Other changes to the Unit 
    2 facility operating license simply delete superseded license 
    conditions that have been previously satisfied and are therefore 
    obsolete. The revisions do not alter the plant safety analyses or 
    the basis for any technical specification that is related to the 
    establishment of, or the maintenance of, a nuclear safety margin. 
    Therefore, operation of either unit in accordance with its proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Indian River Community College 
    Library, 3209 Virginia Avenue, Fort Pierce, Florida 34981-5596.
        Attorney for licensee: M.S. Ross, Attorney, Florida Power & Light, 
    P.O. Box 14000, Juno Beach, Florida 33408-0420.
        NRC Project Director: Frederick J. Hebdon.
    
    Northern States Power Company, Docket Nos. 50-282 and 50-306, Prairie 
    Island Nuclear Generating Plant, Units 1 and 2, Goodhue County, 
    Minnesota
    
        Date of amendment requests: September 4, 1998.
        Description of amendment requests: The proposed amendments would 
    modify the surveillance requirements and limiting conditions for 
    operation of the technical specifications (TS) for the reactor coolant 
    vent system. Specifically, the proposed amendments would modify the 
    limiting conditions for operation as specified in TS Section 3.1.A.3, 
    Reactor Coolant Vent System, and the surveillance requirements 
    specified in TS Section 4.18, Reactor Coolant Vent System Paths.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendment[s] will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed changes do not affect any system that is a 
    contributor to initiating events for previously evaluated 
    anticipated operational occurrences and design basis accidents. 
    Neither do the changes significantly affect any system that is used 
    to mitigate any previously evaluated anticipated operational 
    occurrences and design basis accidents. Therefore, the proposed 
    change does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        2. The proposed amendment[s] will not create the possibility of 
    a new or different kind of accident from any accident previously 
    analyzed.
        The proposed changes do not alter the design, function, or 
    operation of any plant component and does not install any new or 
    different equipment, therefore the possibility of a new or different 
    kind of accident from those previously analyzed has not been 
    created.
        3. The proposed amendment[s] will not involve a significant 
    reduction in the margin of safety.
        The proposed changes do not alter the initial conditions assumed 
    in deterministic analyses associated with either the RCS [reactor 
    coolant system] boundary or fuel cladding, therefore these changes 
    do not involve a significant reduction in the margins of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Minneapolis Public Library, 
    Technology and Science Department, 300 Nicollet Mall, Minneapolis, 
    Minnesota 55401.
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts, and 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        NRC Project Director: Cynthia A. Carpenter.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of amendment request: August 25, 1998.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 2.1.2, ``THERMAL POWER, High 
    Pressure and High Flow,'' and the Bases for TS 2.1, ``Safety Limits.'' 
    These changes are being made to implement an appropriately conservative 
    Safety Limit Minimum Critical Power Ratio (SLMCPR) for the upcoming 
    Cycle 9 Hope Creek core and fuel designs.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        (1) The proposed changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The derivation of the revised SLMCPRs for Hope Creek for 
    incorporation into the Technical Specifications, and its use to 
    determine cycle-1 specific thermal limits, have been performed using 
    NRC approved methods. These calculations do not change the method of 
    operating the plant and have no effect on the probability of an 
    accident initiating event or transient.
        There are no significant increases in the consequences of an 
    accident previously evaluated. The basis of the MCPR Safety Limit is 
    to ensure that no mechanistic fuel damage is calculated to occur if 
    the limit is not violated. The new SLMCPRs preserve the existing 
    margin to transition boiling and the probability of fuel damage is 
    not increased. Therefore, the proposed change does not involve an 
    increase in the probability or consequences of an accident 
    previously evaluated.
        (2) The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
    
    [[Page 50939]]
    
        The proposed changes contained in this submittal result from an 
    analysis of the Cycle 9 core reload using the same fuel types as 
    previous cycles. These changes do not involve any new method for 
    operating the facility and do not involve any facility 
    modifications. No new initiating events or transients result from 
    these changes. Therefore, the proposed Technical Specification 
    changes do not create the possibility of a new or different kind of 
    accident, from any accident previously evaluated.
        (3) The proposed change does not involve a significant reduction 
    in a margin of safety.
        The margin of safety as defined in the Technical Specification 
    bases will remain the same. The new SLMCPRs are calculated using NRC 
    approved methods, which are in accordance with the current fuel 
    design, and licensing criteria. The MCPR Safety Limit remains high 
    enough to ensure that greater than 99.9% of all fuel rods in the 
    core will avoid transition boiling if the limit is not violated, 
    thereby preserving the fuel cladding integrity. Therefore, the 
    proposed Technical Specification changes do not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
        Attorney for licensee: Jeffrie J. Keenan, Esquire, Nuclear Business 
    Unit--N21, P.O. Box 236, Hancocks Bridge, NJ 08038.
        NRC Project Director: Robert A. Capra.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San 
    Diego County, California
    
        Date of amendment requests: March 6, 1998.
        Description of amendment requests: The proposed amendment would 
    modify the Technical Specifications (TS) to eliminate reference to 
    shutdown cooling (SDC) system isolation bypass valve inverters. The 
    proposed change would allow the licensee to replace the inverters with 
    transfer switches.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The staff's evaluation of the three criteria are 
    presented below:
        1. The proposed change does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        The SDC system isolation bypass valves are not considered as event 
    initiators in the accidents analyzed in the safety analysis report. 
    Therefore, the proposed change in how the valves are aligned to 
    available power supplies does not affect the probability of an accident 
    previously evaluated.
        The SDC system isolation bypass valves are realigned post-accident 
    to place the shutdown cooling system in operation. The proposed change 
    will modify the power supply for these valves from an inverter that is 
    supplied from the safety-related DC buses to the safety-related AC 
    buses through a manual transfer switch. This will allow the power 
    supplies for opposite trains' valves for SDC suction supplies to be 
    powered from opposite trains of electrical power. The operations 
    required to actually place SDC in operation from the control room are 
    unaffected. The proposed change does not affect the course of any 
    accident previously analyzed, and therefore the consequences of any 
    accident previously evaluated are unaffected by the proposed change.
        2. The proposed change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The SDC system isolation bypass valves are used during accident 
    mitigations, and are not considered as credible accident initiators. 
    Thus, modifying the manner in which power is supplied to the valves 
    will not create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction in 
    a margin of safety.
        Current accident analyses assume proper operation of the SDC system 
    to mitigate the consequences of an accident to maintain postulate 
    offsite release below the limits of 10 CFR Part 100. The proposed 
    change only modifies the manner in which power is made available to the 
    valves, while retaining the current design for redundancy and 
    diversity.
        The proposed change does not, therefore, affect the current margins 
    of safety.
        Based on the above staff analysis, it appears that the three 
    standards of 50.92(c) are satisfied. Therefore, the NRC staff proposes 
    to determine that the amendment requests involve no significant hazards 
    consideration.
        Local Public Document Room location: Main Library, University of 
    California, Irvine, California 92713.
        Attorney for licensee: Douglas K. Porter, Esquire, Southern 
    California Edison Company, P. O. Box 800, Rosemead, California 91770.
        NRC Project Director: William H. Bateman.
    
    Tennessee Valley Authority, Docket No. 50-260 and 50-296, Browns Ferry 
    Nuclear Plant Units 2, 3, Limestone County, Alabama
    
        Date of amendment request: September 4, 1998.
        Description of amendment request: The proposed amendment would 
    revise the licensing bases for the Browns Ferry Nuclear Plant (BFN) 
    Units 2 and 3 to credit containment pressure in excess of atmospheric 
    pressure (containment overpressure) in the analysis for Emergency Core 
    Cooling Systems (ECCS) pump required net positive suction head (NPSH) 
    during design basis accident conditions. The proposed licensing bases 
    change would be implemented by a change to the BFN Updated Final Safety 
    Analysis Report (UFSAR).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        NRC Bulletin 96-03 requested BWR [Boiling Water Reactor] owners 
    implement appropriate measures to minimize the potential clogging of 
    the ECCS suppression chamber strainers by potential debris generated 
    by a LOCA [loss-of-coolant-accident]. TVA's [Tennesse Valley 
    Authority's] proposed resolution of this issue for BFN takes credit 
    for containment overpressure to maintain adequate ECCS pump NPSH. 
    Containment overpressure is a result of the conditions which will 
    exist in the containment following the pipe break inside 
    containment. Therefore, the use of containment overpressure in the 
    analysis of the consequences of the LOCA does not affect the 
    precursors for the LOCA, nor does it affect the precursors for any 
    other accident or transient analyzed in Chapter 14 of the BFN 
    Updated Final Safety Analysis Report (UFSAR). Therefore, there is no 
    increase in the probability of any accident previously evaluated.
        The worst radiological consequences for the design basis 
    accidents analyzed in UFSAR Chapter 14 are a result of a 
    circumferential break of one of the recirculation loop lines inside 
    containment. The analysis of the radiological consequences of this 
    event assumes a two percent per day leakage from the containment. 
    The results of this analysis are presented in Section 14.6.3 of the 
    UFSAR and indicate substantial margin when compared to 10 CFR Part 
    100 limits.
    
    [[Page 50940]]
    
        The radiological consequences of the design basis accident are 
    not increased by taking credit for the post-LOCA suppression chamber 
    airspace pressure. Without loss of primary containment, no mechanism 
    exists to increase the accident consequences since current leakage 
    bounds this condition. The initial analysis does not assume 
    differential pressure between the drywell and the suppression 
    chamber even though one exists due to the equilibrium conditions 
    caused by the suppression chamber airspace temperature. 
    Specifically, the suppression chamber airspace pressure credited in 
    the ECCS pump NPSH analyses is provided by an increase in 
    suppression chamber vapor pressure due to the increased pool 
    temperature, including an evaluation of the effects of containment 
    initial conditions and leakage.
        By crediting the post-LOCA suppression chamber airspace pressure 
    in the calculation of NPSH, no requirement is created to purposely 
    maintain a higher containment pressure than would otherwise occur; 
    no requirement is incurred to delay operating containment heat 
    removal equipment; no requirement is incurred to deliberately 
    continue any condition of high containment pressure in order to 
    maintain adequate NPSH; and no requirement is incurred for the 
    purposeful addition of nitrogen into the containment to increase the 
    available pressure. Therefore, the proposed amendment does not 
    involve a significant increase in the consequences of an accident 
    previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed use of the post-LOCA suppression chamber airspace 
    pressure in the calculation of NPSH for the ECCS pumps does not 
    introduce any new modes of plant operation or make physical changes 
    to plant systems. Rather, the post-LOCA suppression chamber airspace 
    pressure is a byproduct of the conditions that will exist in the 
    containment after a line break inside containment. Therefore, 
    crediting the post-LOCA suppression chamber airspace pressure in the 
    calculation of NPSH does not create the possibility of a new or 
    different accident.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The integrity of the primary containment and the operation of 
    the ECCS systems limit the offsite doses to values less than those 
    specified in 10 CFR 100 in the event of a reactor coolant system 
    line break inside primary containment. In order for the ECCS pumps 
    to meet their design basis performance requirements, the NPSH 
    available to the pumps throughout the duration of the accident 
    response must meet their specific NPSH requirements. Excess NPSH 
    margin will not improve the performance of the ECCS pumps.
        The post-LOCA suppression chamber airspace pressure is a 
    byproduct of the conditions that will exist in the containment after 
    a line break inside containment. The credit taken for this pressure 
    in ECCS NPSH analyses has been performed in such a manner as to 
    assure that the actual containment overpressure will always exceed 
    the value assumed in the analyses. The NPSH margin will exceed that 
    credited in the NPSH analyses and ECCS pump performance will meet 
    applicable requirements. Therefore, the proposed license amendment 
    does not involve a significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    its review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Athens Public Library, 405 E. 
    South Street, Athens, Alabama 35611.
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET l0H, Knoxville, Tennessee 37902.
        NRC Project Director: Frederick J. Hebdon.
    
    Tennessee Valley Authority, Docket No. 50-390 Watts Bar Nuclear Plant, 
    Unit 1, Rhea County, Tennessee
    
        Date of amendment request: August 5, 1998 (TS 98-008).
        Description of amendment request: The proposed amendment would 
    revise the Watts Bar Nuclear Plant (WBN) Technical Specifications (TS) 
    and associated TS Bases to allow up to 4 hours to make the residual 
    heat removal suction relief valve available as a cold overpressure 
    mitigation (COMS) relief path. This condition will be applicable when 
    entering Mode 4 from Mode 3 during a plant shutdown.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        A. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The 4 hour allowance to place the RHR [residual heat removal] 
    relief valve in service in the proposed TS change is bounded by the 
    current COMS TS. The COMS TS currently allows cooldown of the unit 
    while in Mode 4 with only one operable relief path for up to 7 days. 
    Operation in this condition is allowed by Action E.1 of LCO 
    [limiting condition for operation] 3.4.12. The 7 day completion time 
    considers the facts that only one of the RCS [reactor coolant 
    system] relief valves is required to mitigate an overpressure 
    transient and that the likelihood of an active failure of the 
    remaining relief path during this 7 day time period is very low. 
    Thus a failure of the single available relief path concurrent with 
    an overpressurization event during the proposed 4 hour time period 
    for alignment and preparation of the RHR system for service is more 
    remote. Therefore, the proposed TS change does not increase the 
    probability of an accident previously evaluated. Further, this 
    change does not result in hardware or procedural changes which will 
    affect the probability of the occurrence of an accident. Considering 
    this, the proposed amendment does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        B. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        Action E.1 of LCO 3.4.12 addresses a condition where one relief 
    path is inoperable while in Mode 4. The completion time for Action 
    E.1 is 7 days. The 4 hour period of operation in Mode 4 that will be 
    allowed by the addition of Note 4 to the Applicability statement of 
    LCO 3.4.12 is well within the bounds of the analysis for operation 
    allowed by Action E.1. This 4 hour time allowance for placement of 
    the RHR suction relief valve in service therefore, does not cause 
    the initiation of any accident nor create any new [credible] 
    limiting failure for safety-related systems and components. Since 
    the 4 hour period is only a fraction of the 7 day time period 
    previously authorized for operation with only a single relief path, 
    it is not probable that an accident different from those previously 
    evaluated will be created. Therefore, the change has no adverse 
    effect on the ability of the safety-related systems to perform their 
    intended safety functions.
        C. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The Technical Specifications currently allow one of the two 
    required relief valves to be unavailable for 7 days (Condition E of 
    LCO 3.4.12) while in Mode 4. In this condition (one of the two 
    relief valves inoperable), the proposed change would permit a mode 
    change from Mode 3 to Mode 4 while providing 4 hours to place the 
    RHR system into service. Consequently, this change does not reduce 
    the margin of safety since the probability of an event occurring 
    during the 4 hour period is less than the probability of an event 
    occurring during the 7 days permitted by Action E.1. Considering 
    this, the proposed change does not significantly reduce the margin 
    of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, TN 37402.
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET I0H, Knoxville, Tennessee 37902.
    
    [[Page 50941]]
    
        NRC Project Director: Frederick J. Hebdon.
    
    Tennessee Valley Authority, Docket No. 50-390 Watts Bar Nuclear Plant, 
    Unit 1, Rhea County, Tennessee
    
        Date of amendment request: August 6, 1998 (TS 98-007).
        Description of amendment request: The proposed amendment would 
    revise the Watts Bar Nuclear Plant (WBN) Technical Specifications (TS) 
    and associated TS Bases to clarify the intent of the surveillance 
    requirements (SRs) for turbine driven auxiliary feedwater (AFW) pump. 
    The proposed revision would allow three SRs to be performed prior to 
    achieving 1092 psig in the steam generator (SG).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        A. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed license amendment would revise the subject TDAFWP 
    [turbine driven auxiliary feedwater pump] TS surveillance 
    requirements to be consistent with the intent of the current 
    Westinghouse MERITS TS, NUREG 1431, Revision 1. TS 3.3.2 and 3.7.5 
    would be revised to permit testing of the TDAFWP at SG pressures 
    less than the no-load pressure of 1092 psig [pounds per square inch-
    gauge]. Under these conditions, the AFW system will continue to 
    satisfy requirements for the analyzed design basis accidents and 
    anticipated operational transients dependent on AFW. The design 
    basis for the AFW system and specifically the TDAFWP will be 
    maintained such that the AFW system and its equipment will continue 
    to perform its safety functions because the TDAFWP test will 
    demonstrate, on recirculation flow near pump shutoff head, the 
    ability to deliver full rated flow to the SGs. The proposed TS 
    change does not result in any modifications to the plant and does 
    not alter any fission barriers or challenge fuel integrity, nor are 
    other safety systems degraded by the subject change. Potential 
    radiological releases are not impacted by this TS change and there 
    are no new release pathways created. Therefore, the proposed TS 
    change does not involve a significant increase in the probability or 
    consequences of an accident previously evaluated for WBN.
        B. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed TS change does not result in a modification to the 
    plant and has no adverse affect on the ability of any safety-related 
    system to perform its intended function. No new accident scenarios 
    are created and no new failure modes/mechanisms or limiting single 
    failures are created as a result of the proposed change that would 
    prevent the AFW system from performing its safety functions. A lower 
    test pressure than the current value of 1092 psig would have an 
    insignificant impact on the stroke time of the Terry turbine trip 
    and throttle valve, 1-FCV-1-51. Therefore, the proposed TS change 
    will not result in any new or different kind of accident from any 
    accident previously evaluated.
        C. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        This TS change does not change an acceptance limit nor does it 
    reduce a margin of safety associated with the acceptance criteria 
    for any WBN accident. The safety analyses performed for WBN is not 
    based on the SG pressure at which the TDAFWP test is conducted. 
    Specifically, the proposed TS change clarifies requirements for the 
    TDAFW pump testing consistent with industry practice. The capability 
    of the SRs to detect any degradation to the TDAFWP is unaffected. 
    The capability of the SRs to demonstrate automatic start and 
    adequate response time of the TDAFWP is not adversely impacted. The 
    test remains a requirement of the TS, but clarifies that the test 
    may be conducted at a SG pressure less than no-load conditions. The 
    proposed TS change does not reduce the margin of safety limits 
    established to protect any fission product barriers. Therefore, the 
    proposed TS change will not involve a significant reduction in a 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, TN 37402.
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET l0H, Knoxville, Tennessee 37902.
        NRC Project Director: Frederick J. Hebdon.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of amendment request: May 8, 1998, as supplemented on July 10, 
    1998.
        Description of amendment request: The licensee proposed to change 
    the maximum torus water temperature during normal operation from 100 
    deg.F to 90  deg.F; limit the temperature during testing to 100  deg.F 
    for no more than 24 hours; and, should temperature exceed 110  deg.F 
    prevent operation until the temperature is reduced to below 90  deg.F 
    (changed from 100  deg.F). Basis for proposed no significant hazards 
    consideration determination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration which is presented below:
    
        1. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment, will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        (a) The proposed change to decrease the normal operating 
    suppression pool temperature limit from 100  deg.F to 90  deg.F will 
    assure that the consequences of accidents previously evaluated will 
    not be significantly increased.
        A reduction in the normal operating suppression pool temperature 
    limit provides more margin for the suppression pool as a heat sink 
    to absorb energy from the reactor vessel following an accident. The 
    effect of higher calculated suppression pool temperatures following 
    an accident as a result of the effect of increased feedwater 
    addition and decreased [residual heat removal] RHR heat exchanger 
    heat removal does not affect the consequences of accidents 
    previously evaluated.
        Certain types of Mark I containment loading conditions are 
    increased at lower suppression pool temperatures, but since the 
    analysis of Mark I loads for Vermont Yankee was based on initial 
    suppression pool temperatures between 70  deg.F and 90  deg.F, the 
    proposed decrease in the normal operating limit to 90  deg.F will 
    not affect the consequences of those particular events.
        (b) The proposed change to decrease the normal operating 
    suppression pool temperature limit from 100  deg.F to 90  deg.F will 
    not affect the probability of accidents occurring. The accidents and 
    transients described in the [final safety analysis report] FSAR are 
    initiated by failures of components which are not in contact with 
    the suppression pool water, therefore a change in the suppression 
    pool temperature will have no affect on the probability of those 
    accidents occurring.
        (c) The proposed change to restrict operation during testing 
    that adds heat to the suppression pool to no more than 24 hours 
    while above the normal operating temperature limit will have no 
    affect on the consequences of accidents previously evaluated since 
    accidents are not assumed to be initiated during these modes of 
    operation. This assumption is made in order to assure that plants 
    have testing flexibility at power. In addition to the time limit 
    placed on pool temperature, the plant enters the appropriate 
    limiting condition for operation whenever the RHR system is placed 
    in the suppression pool cooling mode during power operation.
        (d) The proposed change to restrict operation during testing 
    that adds heat to the suppression pool to no more than 24 hours 
    while above the normal operating temperature limit will have no 
    affect on the probability of an accident occurring. The accidents 
    and transients described in the FSAR are initiated by failures of 
    components which are not in contact with the suppression pool water, 
    therefore a change in
    
    [[Page 50942]]
    
    the duration of time at any particular suppression pool temperature 
    will have no affect on the probability of those accidents occurring.
        2. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment, will not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        The proposed change to decrease the normal operating suppression 
    pool temperature limit from 100  deg.F to 90  deg.F does not change 
    any accident initiators or the types of accidents analyzed. No new 
    modes of equipment operation or physical plant equipment 
    modifications are proposed. The change in predicted peak suppression 
    pool temperature results from more conservatively calculating the 
    effects of currently analyzed accidents. Therefore this change will 
    not create the possibility of a new or different kind of accident 
    from any previously evaluated.
        The proposed change to restrict operation during testing that 
    adds heat to the suppression pool to no more than 24 hours with 
    water temperature above the normal operating temperature limit will 
    allow for appropriate testing of safety related equipment to ensure 
    operability. This testing allowance does not create any new 
    initiating events or transients and does not involve any new modes 
    of operation. Therefore, this change does not create the possibility 
    of a new or different kind of accident from those previously 
    evaluated.
        3. The operation of Vermont Yankee Nuclear Power Station in 
    accordance with the proposed amendment, will not involve a 
    significant reduction in a margin of safety.
        The proposed change to decrease the normal operating suppression 
    pool temperature limit from 100  deg.F to 90  deg.F assures that the 
    suppression pool can adequately perform its safety function without 
    a significant decrease in the margin of safety. Each of the 
    accidents affected by suppression pool temperature have been 
    evaluated. The evaluation showed that a higher peak suppression pool 
    temperature was predicted based on analysis assumptions that are 
    more conservative tha[n] those used in the current FSAR, but that 
    the increase in peak temperature does not have a[n] impact on 
    containment loads and equipment operability. The principal effect of 
    an increase in peak suppression pool temperature is the reduction of 
    [net positive suction head] NPSH margin for the low pressure 
    [emergency core cooling system] ECCS pumps. Operator action is 
    credited in throttling the ECCS pump flow rates after 10 minutes for 
    the most limiting scenarios in order to assure that available NPSH 
    exceeds required NPSH. Operator action after 10 minutes is 
    consistent with Vermont Yankee's design basis and Emergency 
    Operating Procedures. The proposed reduction in the normal operating 
    suppression pool temperature limit from 100  deg.F to 90  deg.F will 
    provide more time for operators to take actions, if required.
        Operation of the facility in accordance with the proposed change 
    to restrict operation during testing that adds heat to the 
    suppression pool to no more than 24 hours while above the normal 
    operating temperature limit will not involve a significant reduction 
    in a margin of safety because it restricts the amount of time that 
    the facility can be operated at a suppression pool temperature above 
    the normal operating limit.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
        Attorney for licensee: Mr. David R. Lewis, Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037-1128.
        NRC Project Director: Cecil O. Thomas.
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of amendment request: October 10, 1996.
        Description of amendment request: The amendment would add to the 
    WNP-2 Facility Operating License No. NPF-21, the authority to store on 
    the WNP-2 site, byproduct, source, and special nuclear materials 
    currently addressed by the WNP-1 Materials License 46-17694-02.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the proposed amendment involve a significant increase in 
    the probability or consequences of an accident previously evaluated?
        The proposed amendment does not remove or modify existing 
    requirements or safety limits. The requirements of the [Atomic 
    Energy] Act and 10 CFR Parts 30, 40, and 70 will govern storage of 
    sealed byproduct and neutron sources. Operation of WNP-2 requires 
    possession and use of similar materials, and control of such 
    materials is currently being exercised pursuant to the requirements 
    of the Act and 10 CFR Parts 30, 40, and 70. The additional inventory 
    of radioactive materials is a very small percentage of that already 
    being controlled under Operating License NPF-21. Stored materials 
    such as those proposed are not assumed as an initiator of, or 
    contributor to, a previously analyzed accident. Consequently, the 
    proposed amendment does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. Does the proposed amendment create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated?
        The requirements of the Act and 10 CFR Parts 30, 40, and 70 will 
    govern storage of sealed byproduct and neutron sources. These 
    materials will be stored indefinitely, and will not be put to active 
    use. Operation of WNP-2 requires possession and use of similar 
    materials, and control of such materials is currently being 
    exercised pursuant to the requirements of the Act and 10 CFR Parts 
    30, 40, and 70. Consequently, the proposed amendment does not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated.
        3. Does the proposed amendment involve a significant reduction 
    in a margin of safety?
        The additional inventory of radioactive materials included in 
    sealed byproduct and neutron sources to be stored is a very small 
    percentage of that already being controlled under Operating License 
    NPF-21. The storage of materials does not impact the normal or 
    emergency operation of the plant. No change to the manner in which 
    the plant is operated is proposed. No modification to the facility 
    is proposed. Consequently the proposed amendment does not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352.
        Attorney for licensee: M. H. Philips, Jr., Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005-3502.
        NRC Project Director: William H. Bateman.
    
    Washington Public Power Supply System, Docket No. 50-397, Nuclear 
    Project No. 2, Benton County, Washington
    
        Date of amendment request: October 15, 1996, as supplemented by 
    letter dated December 4, 1997.
        Description of amendment request: This amendment would modify the 
    secondary containment and standby gas treatment system (SGTS) technical 
    specifications to more accurately reflect the existing design by 
    revising the secondary containment and SGTS surveillance requirements 
    to reflect a revised flow rate, revising the secondary containment 
    integrity surveillance requirements by establishing an acceptable 
    operating region as a function of secondary containment differential 
    pressure and SGTS system
    
    [[Page 50943]]
    
    flow, and deleting the existing requirement to maintain the secondary 
    containment at greater than or equal to 0.25 inch of vacuum water gauge 
    at all times.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated?
        Secondary containment and the Standby Gas Treatment (SGT) system 
    are not initiators or precursors to any accident. The SGT system 
    acts as part of secondary containment to minimize and control 
    airborne radiological releases from the plant following a design 
    basis accident. Therefore, operation of WNP-2 in accordance with the 
    proposed changes will not cause a significant increase in the 
    probability of an accident previously evaluated.
        The proposed amendment to the Technical Specifications impacts 
    the capability to demonstrate that the secondary containment and SGT 
    system designs will maintain radioactive releases within 10 CFR 100 
    guidelines and 10 CFR 50, Appendix A, General Design Criteria 19 
    limits. As a result, a new (current) design basis accident dose 
    analysis was performed using the source term criteria outlined in 
    Regulatory Guide 1.3, ``Assumptions Used for Evaluating the 
    Potential Radiological Consequences of a Loss of Coolant Accident 
    for Boiling Water Reactors,'' to evaluate the proposed changes. The 
    new analysis provides a conservative representation of the timing 
    and release of radioactivity during a design basis accident.
        The proposed amendment also deletes the normal (nonsafety-
    related) secondary containment ventilation system surveillance 
    requirement to verify every 24 hours that the pressure within 
    secondary containment is less than or equal to 0.25 inch of vacuum 
    water gauge. This surveillance requirement is not necessary as 
    current Technical Specification Limiting conditions for Operation 
    (LCOs) as well as the WNP-2 Final Safety Analysis Report (FSAR) 
    adequately address secondary containment integrity requirements and 
    ensure secondary containment effluent is monitored. Deletion of the 
    surveillance requirement has no impact on the secondary containment 
    drawdown analysis or the design basis dose analysis. Thus, the 
    analyses assumptions and conclusions remain valid.
        The secondary containment and SGT system designs must 
    accommodate a post-accident single failure and remain operable. In 
    addition, certain plant specific parameters, such as SGT capacity, 
    secondary containment in-leakage, outside meteorological conditions, 
    secondary containment heat loads, available cooling capacity, 
    emergency diesel start time and loading sequence, and drawdown time 
    for secondary containment must be considered in the design analyses 
    and dose assessments. The current design in conjunction with an 
    assumed secondary containment leakage of 2240 cfm and a drawdown 
    time of 20 minutes provide assurance that the radiological doses for 
    a design basis accident are maintained below the 10 CFR 100 
    guidelines and 10 CFR 50, Appendix A, General Design Criteria 19 
    limits.
        The dose analysis supporting the proposed amendment to the 
    Technical Specifications includes analytical changes to the SGT flow 
    rate, secondary containment drawdown time, mixing, and bypass 
    leakage, and established a 95% meteorological basis. These 
    analytical changes, in combination, result in a calculated increase 
    in the offsite thyroid dose values and a decrease in the whole body 
    dose values. Although the calculated offsite thyroid dose values are 
    higher than previously calculated, they remain within the 10 CFR 100 
    guidelines and 10 CFR 50, Appendix A, General Design Criteria 19 
    limits. In accordance with Standard Review Plan (NUREG-0800), 
    Section 15.6.5, ``Loss-of-Coolant Accidents Resulting From a 
    Spectrum of Postulated Piping Breaks Within the Reactor Coolant 
    Pressure Boundary,'' the radiological consequences of a design basis 
    accident are considered acceptable if they are within the guidelines 
    of 10 CFR 100. Since the offsite thyroid dose values remain within 
    these acceptance criteria, and since there is no increase in the 
    control room thyroid dose values or any of the whole body dose 
    value, the changes are considered acceptable and operation of WNP-2 
    in accordance with the proposed amendment to the Technical 
    Specifications will not cause a significant increase in the 
    consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated?
        Secondary containment and the SGT system are not initiators or 
    precursors to any accident. The SGT system acts as part of secondary 
    containment to minimize and control airborne radiological releases 
    from the plant following a design basis accident.
        The dose analysis supporting the proposed amendment to the 
    Technical Specifications includes analytical changes to the SGT flow 
    rate, secondary containment drawdown time, mixing, and bypass 
    leakage, and establish a 95% meteorological basis. These analytical 
    changes do not alter any safety-related equipment or functions or 
    create any new failure modes. The changes will improve the 
    capability of secondary containment and the SGT system to mitigate 
    the consequences of a design basis accident by ensuring that 
    secondary containment pressure can be drawn down from 0 inches water 
    gauge to at least 0.25 inch of vacuum water gauge during the most 
    adverse environmental conditions. The proposed changes reflect 
    consideration of SGT capacity, secondary containment in-leakage, 
    outside meteorological conditions, secondary containment heat loads, 
    available cooling capacity, emergency diesel start time and loading 
    sequence, and drawdown time for the limiting secondary containment 
    elevation. Required instrumentation have been evaluated to ensure 
    proper operation under normal and accident environmental conditions, 
    including but not limited to pressure, humidity, seismic, 
    temperature, and radiation. The evaluation method is based on 
    American National Standards Institute/Instrument Society of America 
    (ANSI/ISA) Standard S67.04-1988, ``Setpoints for Nuclear Safety-
    Related Instrumentation,'' and guidelines in ISA draft Recommended 
    Practice RP67.04, ``Methodologies for the Determination of Setpoints 
    for Nuclear Safety-Related Instrumentation.''
        The proposed amendment to the Technical Specification does not 
    change plant equipment or functions, but serves to clarify and 
    credit existing design features. Fault tree and single failure 
    analyses were performed to ensure that the SGT system design, 
    including the equipment and components, credited in the licensing 
    basis for the proposed amendment meet the single failure criteria 
    for credible failure modes. The proposed amendment also deletes the 
    normal (nonsafety-related) secondary containment ventilation system 
    surveillance requirement to verify every 24 hours that the pressure 
    within secondary containment is less than or equal to 0.25 inch of 
    vacuum water gauge. Deletion of this surveillance requirement does 
    not invalidate existing analyses or change plant equipment or 
    functions. Thus, no new failure modes are created.
        Based on equipment failure and qualification analyses performed 
    and the above conclusions, the proposed amendment to the Technical 
    Specifications does not change any safety-related equipment or 
    functions, or create any new failure modes. Therefore, operation of 
    WNP-2 in accordance with the proposed amendment to the Technical 
    Specifications will not create the possibility of a new or different 
    kind of accident from any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety?
        Consistent with the current Bases for the Technical 
    Specifications and the WNP-2 FSAR, secondary containment and the SGT 
    system act to minimize and control airborne radiological releases 
    from the plant to within 10 CFR 100 guidelines and 10 CFR 50, 
    Appendix A, General Design Criteria 19 limits following a design 
    basis accident.
        The proposed amendment to the Technical Specifications impacts 
    the capability to demonstrate that the secondary containment and SGT 
    system designs will maintain radioactive releases within 10 CFR 100 
    guidelines and 10 CFR 50, Appendix A, General Design Criteria 19 
    limits. As a result, a new (current) design basis accident dose 
    analysis was performed using the source term criteria outlined in 
    Regulatory Guide 1.3 to evaluate the proposed changes. The new 
    analysis provides a conservative representation of the timing and 
    release of radioactivity during a design basis accident.
        The proposed amendment also deletes the normal (nonsafety-
    related) secondary containment ventilation system surveillance 
    requirement to verify every 24 hours that the pressure within 
    secondary containment is less than or equal to 0.25 inch of vacuum 
    water gauge. This surveillance requirement is
    
    [[Page 50944]]
    
    not necessary as current Technical Specification LCOs as well as the 
    WNP-2 FSAR adequately address secondary containment integrity 
    requirements and ensure secondary containment effluent is monitored. 
    Deletion of the surveillance requirement has no impact on the 
    secondary containment drawdown analysis or the design basis dose 
    analysis. Thus, it follows that deletion of the surveillance 
    requirement will not impact the offsite and control room dose safety 
    margins established by these analyses.
        The dose analysis includes analytical changes which increase SGT 
    system flow rate and secondary containment drawdown time, credit 
    mixing within secondary containment, increase bypass leakage, and 
    establish a 95% meteorological basis. The combined effect of these 
    analytical changes results in an increase in the calculated offsite 
    thyroid dose values. The calculated control room thyroid dose values 
    and all of the whole body dose values are shown to decrease. 
    Although the new thyroid dose values are higher than previously 
    calculated, they remain within the 10 CFR 100 guidelines and 10 CFR 
    50, Appendix A, General Design Criteria 19 limits. The calculated 
    thyroid dose values at the plant exclusion area boundary (EAB) (1.2 
    miles) increased from 72 Rem to 114.2 Rem and the calculated thyroid 
    dose at the low population zone (LPZ) (3 miles) increased from 251 
    Rem to 275.6 Rem.
        The LPZ is defined as all land within a 3 mile radius of the 
    plant site and 0 persons reside within this area. The nearest 
    residence is 4.1 miles from the plant site. There are no schools or 
    hospitals within 5 miles of the plant site and the nearest 
    population center is at 12 miles. Considering the low population 
    density in the area immediately surrounding the plant site, the 
    increase in thyroid dose will have a small impact on the health and 
    safety of the public.
        Since the offsite thyroid dose values remain within the 10 CFR 
    100 guidelines and 10 CFR 50, Appendix A, General Design Criteria 19 
    limits, and since there is a small impact on the health and safety 
    of the public, the increase in the offsite thyroid dose values are 
    considered acceptable and operation of WNP-2 in accordance with the 
    proposed amendnment to the Technical Specifications will not cause a 
    significant reduction in the margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Richland Public Library, 955 
    Northgate Street, Richland, Washington 99352.
        Attorney for licensee: M. H. Philips, Jr., Esq., Winston & Strawn, 
    1400 L Street, N.W., Washington, D.C. 20005-3502.
        NRC Project Director: William H. Bateman.
    
    Previously Published Notices of Consideration of Issuance of 
    Amendments to Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Illinois Power Company, Docket No. 50-461, Clinton Power Station, 
    DeWitt County, Illinois Date of Application for Amendment: August 24, 
    1998
    
        Brief description of amendment request: The proposed amendment 
    concerns the ``ready-to-load'' requirement for the Division 3 diesel 
    generator (DG). The Division 3 DG requires operator action to reset the 
    mechanical governor to meet the ``ready-to-load'' requirement.
        Date of publication of individual notice in Federal Register: 
    September 10, 1998 (63 FR 48529).
        Expiration date of individual notice: October 13, 1998.
        Local Public Document Room location: Vespasian Warner Public 
    Library, 310 N. Quincy Street, Clinton, IL 61727.
    
    STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South 
    Texas Project, Units 1 and 2, Matagorda County, Texas
    
        Date of amendment request: August 28, 1998.
        Brief description of amendment request: The proposed amendment 
    would modify Technical Specification 4.0.5 to state that the inservice 
    testing requirement for exercise testing in the closed direction for 
    specified Unit 1 containment isolation valves shall not be required 
    until the next plant shutdown to Mode 5 of sufficient duration to allow 
    the testing or until the next refueling outage scheduled in March 1999.
        Date of publication of individual notice in Federal Register: 
    September 9, 1998 (63 FR 48254)
        Expiration date of individual notice: September 24, 1998.
        Local Public Document Room location: Wharton County Junior College, 
    J.M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488.
    
    The Cleveland Electric Illuminating Company, Centerior Service Company, 
    Duquesne Light Company, Ohio Edison Company, Pennsylvania Power 
    Company, Toledo Edison Company Docket No. 50-440, Perry Nuclear Power 
    Plant, Unit 1, Lake County, Ohio
    
        Date of amendment request: June 30, 1998.
        Description of amendment request: The proposed amendment would 
    transfer operating authority for the Perry Nuclear Power Plant, Unit 
    No. 1, from The Cleveland Electric Illuminating Company and Centerior 
    Service Company to a new operating company, called the FirstEnergy 
    Nuclear Operating Company. The proposed action has been submitted 
    pursuant to 10 CFR 50.80 and 10 CFR 50.90.
        Date of publication of individual notice in Federal Register: 
    August 4, 1998 (63 FR 41600).
        Expiration date of individual notice: September 3, 1998.
        Local Public Document Room location: Perry Public Library, 3753 
    Main Street, Perry, OH 44081.
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse Nuclear 
    Power Station, Unit 1, Ottawa County, Ohio
    
        Date of application for amendment: June 29, 1998, as supplemented 
    July 14, 1998.
        Brief description of amendment request: This amendment would 
    reflect the approval of the transfer of the authority to operate Davis-
    Besse Nuclear Power Station, Unit 1, under the license to a new 
    company, FirstEnergy Nuclear Operating Company.
        Date of publication of individual notice in Federal Register: 
    August 4, 1998.
        Expiration date of individual notice: September 3, 1998.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, OH 43606.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application
    
    [[Page 50945]]
    
    complies with the standards and requirements of the Atomic Energy Act 
    of 1954, as amended (the Act), and the Commission's rules and 
    regulations. The Commission has made appropriate findings as required 
    by the Act and the Commission's rules and regulations in 10 CFR Chapter 
    I, which are set forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of application for amendment: October 31, 1996.
        Brief description of amendment: This amendment changes Technical 
    Specification 3/4.7.5 by reducing the maximum allowable water 
    temperature for the Ultimate Heat Sink from 95 deg.F to 94 deg.F and 
    increasing the minimum main reservoir level from 205.7 feet mean sea 
    level to 215 feet mean sea level.
        Date of issuance: September 8, 1998.
        Effective date: September 8, 1998.
        Amendment No: 80.
        Facility Operating License No. NPF-63. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: December 4, 1996 (61 FR 
    64382).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 8, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of application for amendment: May 16, 1997, as supplemented 
    June 29, 1998. The June 29, 1998, supplemental letter provided 
    clarifying information only, and did not change the initial no 
    significant hazards consideration determination.
        Brief description of amendment: This amendment changes Technical 
    Specification 3/4.6.2.3 by reducing the Containment Fan Coolers cooling 
    water flow rate requirement from 1425 gallons per minute (gpm) to 1300 
    gpm.
        Date of issuance: September 8, 1998.
        Effective date: September 8, 1998.
        Amendment No: 81.
        Facility Operating License No. NPF-63: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: March 25, 1998 (63 FR 
    14485).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 8, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Commonwealth Edison Company, Docket Nos. STN 50-456 and STN 50-457, 
    Braidwood Station, Unit Nos. 1 and 2, Will County, Illinois
    
        Date of application for amendments: January 14, 1998, as 
    supplemented by letter dated July 17, 1998.
        Brief description of amendments: The amendments change the 
    Braidwood, Unit 1, Technical Specification limits on Reactor Coolant 
    System Dose Equivalent Iodine-131 from 0.35 microcuries/gram to 0.05 
    microcuries/gram for the remainder of Cycle 7.
        Date of issuance: September 3, 1998.
        Effective date: Immediately, to be implemented within 30 days.
        Amendment Nos.: 95 and 95.
        Facility Operating License Nos. NPF-72 and NPF-77: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 11, 1998 (63 FR 
    11914). The July 17, 1998, submittal provided additional clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination. The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    September 3, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Wilmington Public Library, 201 
    S. Kankakee Street, Wilmington, Illinois 60481.
    
    Duke Energy Corporation, et al., Docket No. 50-413, Catawba Nuclear 
    Station, Unit 1, York County, South Carolina
    
        Date of application for amendment: August 6, 1998.
        Brief description of amendment: The amendment deletes Surveillance 
    Requirement 4.8.1.1.2.i.2, regarding diesel fuel oil system pressure 
    testing, from the unit Technical Specifications for Unit 1 on the basis 
    that the staff had previously approved alternative surveillance based 
    on Code Case N-498-1 of the American Society of Mechanical Engineers.
        Date of issuance: September 9, 1998.
        Effective date: As of the date of issuance.
        Amendment No.: 171.
        Facility Operating License No. NPF-35: The amendment revised the 
    Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration: Yes. (63 FR 43962 dated August 17, 1998). The notice 
    provided an opportunity to submit comments on the Commission's proposed 
    no significant hazards consideration determination. No comments have 
    been received. The notice also provided for an opportunity to request a 
    hearing by September 16, 1998, but indicated that if the Commission 
    makes a final no significant hazards consideration determination, any 
    such hearing would take place after issuance of the amendment.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, and a final no significant hazards consideration 
    determination are contained in a Safety Evaluation dated September 9, 
    1998.
        Attorney for licensee: Paul R. Newton, Legal Department (PB05E), 
    Duke Energy Corporation, 422 South Church Street, North Carolina.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina.
    
    [[Page 50946]]
    
    Duke Energy Corporation (DEC), et al., Docket Nos. 50-413 and 50-414, 
    Catawba Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: August 14, 1998.
        Brief description of amendments: The amendments revise Technical 
    Specification Section 4.6.5.1.b.2 regarding surveillance requirements 
    for the ice condenser. One current requirement specifies that a visual 
    inspection of flow passages be performed once per 9 months to ensure 
    that there is no significant ice and frost accumulation (less than 0.38 
    inch). DEC proposed to relax the visual inspection frequency of the 
    lower plenum support structures and turning vanes to once per 18 
    months, while the remaining parts of the ice condenser will continue to 
    be inspected at 9-month intervals.
    
        Date of issuance: September 10, 1998.
        Effective date: As of the date of issuance.
        Amendment Nos.: Unit 1--172; Unit 2--163.
        Facility Operating License Nos. NPF-35 and NPF-52: The amendments 
    revised the Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration: Yes. (63 FR 45872 dated August 27, 1998). The notice 
    provided an opportunity to submit comments on the Commission's proposed 
    no significant hazards consideration determination. No comments have 
    been received. The notice also provided for an opportunity to request a 
    hearing by September 28, 1998, but indicated that if the Commission 
    makes a final no significant hazards consideration determination, any 
    such hearing would take place after issuance of the amendments.
        The Commission's related evaluation of the amendments, finding of 
    exigent circumstances, and a final no significant hazards consideration 
    determination are contained in a Safety Evaluation dated September 10, 
    1998.
        Attorney for licensee: Mr. Paul R. Newton, Legal Department 
    (PB05E), Duke Energy Corporation, 422 South Church Street, Charlotte, 
    North Carolina.
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina.
    
    Duke Energy Corporation, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: August 14, 1998.
        Brief description of amendments: The amendments revise Surveillance 
    Requirement 4.6.5.1.b.3 of the Technical Specifications, relaxing the 
    visual inspection interval of the ice condenser lower plenum and 
    turning vanes from the current 9-month to 18-month intervals.
        Date of issuance: September 10, 1998.
        Effective date: As of the date of issuance.
        Amendment Nos.: Unit 1-180; Unit 2-162.
        Facility Operating License Nos. NPF-2 and NPF-8: The amendments 
    revised the Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration: Yes. (63 FR 45870 dated August 27, 1998). The notice 
    provided an opportunity to submit comments on the Commission's proposed 
    no significant hazards consideration determination. No comments have 
    been received. The notice also provided for an opportunity to request a 
    hearing by September 28, 1998, but indicated that if the Commission 
    makes a final no significant hazards consideration determination, any 
    such hearing would take place after issuance of the amendments.
        The Commission's related evaluation of the amendments, finding of 
    exigent circumstances, and a final no significant hazards consideration 
    determination are contained in a Safety Evaluation dated September 10, 
    1998.
        Attorney for licensee: Mr. Albert Carr, Duke Energy Corporation, 
    422 South Church Street, Charlotte, North Carolina.
        Local Public Document Room location: J. Murrey Atkins Library, 
    University of North Carolina at Charlotte, 9201 University City 
    Boulevard, Charlotte, North Carolina.
    
    Duke Energy Corporation, Docket Nos. 50-269, 50-270, and 50-287, Oconee 
    Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
    
        Date of application of amendments: March 11, 1993, as supplemented 
    August 26, October 26, November 29, and December 6, 1993, October 3, 
    1995, February 27, May 2, and September 3, 1997, and May 7, 1998.
        Brief description of amendments: The amendments completely revise 
    the current Technical Specifications related to the electrical 
    distribution system and incorporate new requirements for system 
    operation, limiting conditions for operation, and surveillance 
    requirements.
        Date of Issuance: September 4, 1998.
        Effective date: As of the date of issuance, to be implemented 
    coincident with implementation of the Improved Technical 
    Specifications.
        Amendment Nos.: Unit 1-232; Unit 2-232; Unit 3-231.
        Facility Operating License Nos. DPR-38, DPR-47, and DPR-55: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: December 3, 1997 (62 FR 
    63975).
        The May 2, 1997, and May 7, 1998, letters provided clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 4, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina.
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Unit No. 3 Nuclear Generating Plant, Citrus County, Florida
    
        Date of application for amendment: April 28, 1998.
        Brief description of amendment: The amendment proposed to revise 
    the Improved Technical Specification 5.6.2.8 to change the scope and 
    frequency of volumetric and surface inspections for the reactor coolant 
    pump flywheels. The amendment approves the requested change to reflect 
    the frequency and scope of these inspections as specified in Topical 
    Report WCAP-14535A.
        Date of issuance: August 31, 1998.
        Effective date: August 31, 1998.
        Amendment No.: 170.
        Facility Operating License No. DPR-72: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 29, 1998 (63 FR 
    40555)
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated August 31, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 34428.
    
    GPU Nuclear, Inc. et al., Docket No. 50-219, Oyster Creek Nuclear 
    Generating Station, Ocean County, New Jersey
    
        Date of application foramendment: June 29, 1998, as supplemented 
    July 27, 1998.
        Brief description of amendment: The amendment reduces the scope of 
    a
    
    [[Page 50947]]
    
    previous amendment request dated February 22, 1996. It retains the 
    provision to delete the requirement that the biennial inspection of the 
    emergency diesel generators (EDGs) be performed during shutdown, 
    permits skipping diesel starting battery capacity test for recently 
    installed batteries, and increases the minimum loading during diesel 
    testing from 20% to 80%. In addition, there are wording changes to 
    enhance clarity and a typograhpical error is corrected.
        Date of Issuance: September 8, 1998.
        Effective date: September 8, 1998, to be implemented within 30 
    days.
        Amendment No.: 197.
        Facility Operating License No. DPR-16: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 29, 1998 (63 FR 
    40556). The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated September 8, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room Location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald 
    C. Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan.
    
        Date of application for amendments: February 22, 1996.
        Brief description of amendments: The amendments revise the 
    Technical Specifications to reference NRC Regulatory Guide 1.9, 
    Revision 3, rather than NRC Regulatory Guide 1.108, Revision 1, for the 
    determination of a valid diesel generator test.
        Date of issuance: September 2, 1998.
        Effective date: September 2, 1998, with full implementation within 
    45 days.
        Amendment Nos.: 222 and 206.
        Facility Operating License Nos. DPR-58 and DPR-74: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: April 10, 1996 (61 FR 
    15990).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 2, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald 
    C. Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan
    
        Date of application for amendments: June 10, 1998.
        Brief description of amendments: The amendments defer the 
    implementation date of Amendments Nos. 216/200 to become effective when 
    modifications are completed but not later than December 31, 2000.
        Date of issuance: August 31, 1998.
        Effective date: August 31, 1998, with full implementation not later 
    than December 31, 2000.
        Amendment Nos.: 221 and 205.
        Facility Operating License Nos. DPR-58 and DPR-74: Amendments 
    revised the licenses.
        Date of initial notice in Federal Register: July 31, 1998 (63 FR 
    40940).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated August 31, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of application for amendments: June 22, 1995, as supplemented 
    on May 13, 1998.
        Brief description of amendments: The amendments revise Technical 
    Specifications 3.4.1.4 and 3.9.8.2 by deleting footnotes and associated 
    information regarding service water system header operation to allow 
    residual heat removal system operation to be consistent with current 
    regulations and the Standard Technical Specifications--Westinghouse 
    Plants (NUREG-1431).
        Date of issuance: September 8, 1998.
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment Nos.: 214 and 194.
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 30, 1995 (60 FR 
    45183).
        The May 13, 1998, letter provided clarifying information that did 
    not change the initial proposed no significant hazards consideration 
    determination, and was within the scope of the original application.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 8, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, San 
    Diego County, California
    
        Date of application for amendments: July 22, 1998.
        Brief description of amendments: The amendments revise the 
    technical specifications to extend the allowed outage time (AOT) for 
    off-site circuits and for the emergency diesel generator.
        Date of issuance: September 9, 1998.
        Effective date: September 9, 1998, to be implemented within 30 days 
    from the date of issuance.
        Amendment Nos.: Unit 2-141; Unit 3-133.
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 31, 1998 (63 FR 
    40941).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 9, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713.
    
    Tennessee Valley Authority, Docket No. 50-296, Browns Ferry Nuclear 
    Plant, Unit 3, Limestone County, Alabama
    
        Date of application for amendment: June 2, 1995, revised March 6, 
    1997, as supplemented April 11, May 13, and August 20, 1997, and March 
    13, 1998. (TS-353).
        Brief description of amendment: Revises Technical Specifications 
    (TS) to permit implementation of upgrade of power range neutron monitor 
    instrumentation. Other changes also have been incorporated to thermal 
    limits specifications to implement average power range monitor and rod 
    block monitor TS improvements, and maximum extended load line limit 
    analyses.
        Date of issuance: September 3, 1998.
        Effective date: September 3, 1998.
        Amendment No.: 213.
        Facility Operating License No. DPR-68: Amendment revises the TS. .
        Date of initial notice in Federal Register: August 16, 1995 (60 FR
    
    [[Page 50948]]
    
    42609). The revision dated March 6, 1997; the proposal for the same 
    changes to be made to the Improved Standard TS format dated April 11, 
    1997; and the supplemental information dated May 13 and August 20, 
    1997, and March 13, 1998, did not affect the staff's original finding 
    of no significant hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 3, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Athens Public Library, South 
    Street, Athens, Alabama 35611.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2. Hamilton County, Tennessee
    
        Date of application for amendments: February 13, 1998 (TS 97-04).
        Brief description of amendments: The amendments change the 
    Technical Specifications (TS) by relocating the snubber requirements 
    from Section 3.7.9 of the TS, and its bases, to the Sequoyah Nuclear 
    Plant Technical Requirements Manual. This change does not alter the 
    requirements for operability or surveillance testing of the snubbers. 
    This amendment also deletes License Condition 2.C.(19), for Unit 1 
    only. This condition is a one-time snubber-related action that was 
    completed and no longer needs to be included in the SQN Operating 
    License.
        Date of issuance: August 28, 1998.
        Effective date: As of the date of issuance to be implemented no 
    later than 45 days after issuance.
        Amendment Nos.: Unit 1-235 ; Unit 2-225.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the TS.
        Date of initial notice in Federal Register: April 8, 1998 (63 FR 
    17235).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated August 28, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402
    
    Toledo Edison Company, Centerior Service Company, and The Cleveland 
    Electric Illuminating Company, Docket No. 50-346, Davis-Besse Nuclear 
    Power Station, Unit 1, Ottawa County, Ohio
    
        Date of application for amendment: December 23, 1997.
        Brief description of amendment: This amendment revised Technical 
    Specification (TS) Section 4.4.5, ``Reactor Coolant System--Steam 
    Generators--Surveillance Requirements (SRs).'' SR 4.4.5.8 was modified 
    to provide flexibility in the scheduling of steam generator inspections 
    during refueling outages.
        Date of issuance: September 2, 1998.
        Effective date: September 2, 1998.
        Amendment No.: 226.
        Facility Operating License No. NPF-3: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: January 28, 1998 (63 FR 
    4327).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 2, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Toledo, William 
    Carlson Library, Government Documents Collection, 2801 West Bancroft 
    Avenue, Toledo, OH 43606.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: June 30, 1998.
        Brief description of amendment: The licensee proposes to delete the 
    calibration requirements for emergency core cooling actuation 
    instrumentation--core spray (CS) subsystem and low pressure coolant 
    injection (LPCI) system auxiliary power monitor since the relays 
    operate from a switched input and functional testing is sufficient to 
    demonstrate the relay pickup/dropout capability.
        Date of Issuance: September 1, 1998.
        Effective date: September 1, 1998, to be implemented within 30 
    days.
        Amendment No.: 162.
        Facility Operating License No. DPR-28. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 29, 1998 (63 FR 
    40563).
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated September 1, 1998.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
        Dated at Rockville, Maryland, this 17th day of September 1998.
    
        For The Nuclear Regulatory Commission.
    Elinor G. Adensam,
    Acting Director, Division of Reactor Projects--III/IV, Office of 
    Nuclear Reactor Regulation.
    [FR Doc. 98-25281 Filed 9-22-98; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Effective Date:
9/8/1998
Published:
09/23/1998
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
98-25281
Dates:
September 8, 1998.
Pages:
50932-50948 (17 pages)
PDF File:
98-25281.pdf