99-25795. Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations  

  • [Federal Register Volume 64, Number 193 (Wednesday, October 6, 1999)]
    [Notices]
    [Pages 54370-54393]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: 99-25795]
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    
    Biweekly Notice; Applications and Amendments to Facility 
    Operating Licenses Involving No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is
    
    [[Page 54371]]
    
    publishing this regular biweekly notice. Public Law 97-415 revised 
    section 189 of the Atomic Energy Act of 1954, as amended (the Act), to 
    require the Commission to publish notice of any amendments issued, or 
    proposed to be issued, under a new provision of section 189 of the Act. 
    This provision grants the Commission the authority to issue and make 
    immediately effective any amendment to an operating license upon a 
    determination by the Commission that such amendment involves no 
    significant hazards consideration, notwithstanding the pendency before 
    the Commission of a request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from September 11, 1999, through September 24, 
    1999. The last biweekly notice was published on September 22, 1999 (64 
    FR 51343 ).
    
    Notice of Consideration of Issuance of Amendments to Facility 
    Operating Licenses, Proposed no Significant Hazards Consideration 
    Determination, and Opportunity for a Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Chief, Rules and 
    Directives Branch, Division of Administration Services, Office of 
    Administration, U.S. Nuclear Regulatory Commission, Washington, DC 
    20555-0001, and should cite the publication date and page number of 
    this Federal Register notice. Written comments may also be delivered to 
    Room 6D22, Two White Flint North, 11545 Rockville Pike, Rockville, 
    Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. Copies of 
    written comments received may be examined at the NRC Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC. The 
    filing of requests for a hearing and petitions for leave to intervene 
    is discussed below.
        By November 5, 1999, the licensee may file a request for a hearing 
    with respect to issuance of the amendment to the subject facility 
    operating license and any person whose interest may be affected by this 
    proceeding and who wishes to participate as a party in the proceeding 
    must file a written request for a hearing and a petition for leave to 
    intervene. Requests for a hearing and a petition for leave to intervene 
    shall be filed in accordance with the Commission's ``Rules of Practice 
    for Domestic Licensing Proceedings'' in 10 CFR part 2. Interested 
    persons should consult a current copy of 10 CFR 2.714 which is 
    available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The
    
    [[Page 54372]]
    
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff, or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert County, 
    Maryland
    
        Date of amendments request: September 1, 1999.
        Description of amendments request: The proposed amendment requests 
    the following changes to the Technical Specifications:
        1. Change the definition of Azimuthal Power Tilt in Technical 
    Specification 1.1;
        2. Correct the peak linear heat rate safety limit in Technical 
    Specification 2.1.1.2;
        3. Correct the DC voltage range listed in Surveillance Requirements 
    3.8.3.9 and 3.8.1.15;
        4. Correct the loss of voltage and degraded voltage settings in 
    Surveillance Requirement 3.3.6.2;
        5. Correct the list of core operating limits in Technical 
    Specification 5.6.5.a;
        6. Correct a note on Technical Specification Figure 2.1.1-1;
        7. Remove references to Unit 2, Cycle 12 in various Technical 
    Specifications; and
        8. Correct a typographical error in Technical Specification 5.6.
        Specifically, the Proposed Technical Specifications are as follows:
        1. Technical Specification 1.1 is proposed to be changed to replace 
    the definition of Azimuthal Power Tilt with a new definition.
        2. Technical Specification 2.1.1.2 is proposed to be changed by 
    replacing the peak linear heat rate safety limit with less than or 
    equal to 22kW/ft.
        3. Technical Specification SR 3.3.6.2 is proposed to be changed by 
    replacing the degraded voltage function with transient degraded voltage 
    and steady-state degraded voltage functions.
        4. Technical Specification SRs 3.8.1.9 and 3.8.1.15 are proposed to 
    be changed by replacing the steady-state voltage range with the range 
    of greater than or equal to 4060 volts and less than or equal to 4400 
    volts.
        5. Technical Specification 5.6.5.a is proposed to be changed by 
    adding Technical Specifications 3.1.4 and 3.3.1 to the list.
        6. Technical Specification Figure 2.1.1-1 is proposed to be changed 
    by removing the reference to Figure B2.1-1.
        7. Various Technical Specifications and Figure 2.1.1-1a.
        8. Technical specification 5.6.5.b, Item 41.ii is proposed to be 
    changed by correcting CEN-199(B)-P to CEN-119(b)-P.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Would not involve a significant increase in the probability 
    of consequences of an accident previously evaluated.
    
    Change the Definition of Azimuthal Power Tilt
    
        In their Infobulletin 97-07, Revision 1, Asea Brown Boveri, 
    Inc.,--Combustion Engineering, Inc. (ABB-CE) stated that they had 
    found a discrepancy in the Technical Specification definition of 
    azimuthal power tilt. This discrepancy was found to exist in all CE 
    Nuclear Steam supply System analog plants that use CECOR for 
    monitoring and surveillance, and that use ABB-CE safety analysis 
    methodology. Calvert Cliffs is one of those plants.
        The value of Tq (Azimuthal tilt magnitude) as used in the 
    azimuthal power tilt formula now in Technical Specification 1.1 is 
    not conservative in all cases. With the proposed definition, Tq is 
    the maximum fractional increase in power that can occur anywhere in 
    the core because of tilt. Since Tq is the maximum value, it is 
    consistently conservative. This is the appropriate measured value of 
    tilt to be used in verifying that the tilt assumed in establishing 
    safety limits has not been exceeded.
        Therefore, changing the definition of azimuthal power tilt as 
    proposed will not involve a significant increase in the probability 
    of consequences of an accident previously evaluated.
    
    Correct the Peak Linear Heat Rate Safety Limit
    
        When Improved Standard Technical Specifications (ITS) were 
    written, the peak linear heat rate safety limit of [less than or 
    equal to] 21 kW/ft was inadvertently written in Technical 
    specification 2.1.1.2. the correct number is [less than or equal to] 
    22kW/ft. the peak linear heat rate safety limit was established at 
    [less than or equal to] 22 kW/ft in License Amendment Nos. 88 (Unit 
    1) and 61 (Unit 2). This number was valid for both units at the time 
    of implementation of ITS.
        Therefore, changing the peak linear heat rate safety limit to a 
    number previously approved by the Nuclear Regulatory Commission 
    (NRC) will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
    
    Correct the Diesel Generator Loss of Voltage and Degraded Voltage 
    Settings
    
        When the ITS were written, a single set of numbers for the 
    degraded voltage function was provided in Technical Specification 
    Surveillance Requirement (SR) 3.3.6.2. The degraded voltage function 
    should have been expressed as transient degraded voltage and steady-
    state degraded voltage. This separation of two types of degraded 
    voltage functions was approved in License Amendment Nos. 226 (Unit 
    1) and 200 (Unit 2), which were issued before the ITS were approved.
        Therefore, changing the degraded voltage function to the 
    transient degraded voltage and steady-state degraded voltage 
    functions previously approved by the NRC will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
    
    Correct the Diesel Generator Voltage Range
    
        Technical Specification SRs 3.8.1.9 and 3.8.1.15 require each 
    diesel to be started from a stand-by condition. Surveillance 
    requirement 3.8.1.9 requires that the generator reach [greater than 
    or equal to] 3740 volts within 10 seconds. After steady-state 
    conditions are reached, both SRs require the generator to maintain a 
    voltage range of greater than 3740 volts and [less than or equal to] 
    4580 volts.
    
    [[Page 54373]]
    
        The Baltimore Gas and Electric Company ITS conversion added 
    voltage requirements to SRs 3.8.1.9 and 3.8.1.15 consistent with SR 
    3.8.1.3. License Amendment Nos. 226 and 200 changed the voltage 
    requirement for SR 3.8.1.3 to [greater than or equal to] 4060 volts 
    and [less than or equal to] 4400 volts. The voltage was not 
    corrected in SRs 3.8.1.9 and 3.8.1.15 when the Technical 
    Specifications were changed to ITS.
        Therefore, changing the voltage in SRs 3.8.1.9 and 3.8.1.15 to 
    voltage previously approved by the NRC will not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
    
    Correct the List of Core Operating Limits
    
        Technical Specification 5.6.5.a lists Technical Specifications 
    that are to be included in the core operating limits and documented 
    in the Core Operating Limits Report (COLR). In the transition to 
    ITS, Technical Specifications 3.1.4 (Control Element Assembly 
    Alignment) and 3.3.1 (Reactor Protective System--Operating) were 
    inadvertently omitted from the list. The complete list is currently 
    in the COLR.
        Therefore, restoring Technical Specification 5.6.5.a to a list 
    previously approved by the NRC will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
    
    Correct Figure 2.1.1-1
    
        A note of Technical Specification Figure 2.1.1-1 was changed in 
    License Amendment Nos. 227 (Unit 1) and 201 (Unit 2) (ITS) to delete 
    reference to Figure B2.1-1. Figure B2.1-1 was deleted from the 
    Technical Specification Bases in the transition to ITS. In License 
    Amendment Nos. 228 (Unit 1) and 202 (Unit 2), an old version of 
    Figure 2.1.1-1 was used, and the reference to Figure B2.1-1 was thus 
    inadvertently put back in the note. The proposed correction will 
    replace the reference to Figure B2.1-1 with the wording approved in 
    License Amendment Nos. 227 and 201.
        Therefore, returning the note in Figure 2.1.1-1 to the wording 
    previously approved by the NRC will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
    
    Remove References to Unit 2, Cycle 12
    
        License Amendment Nos. 228 and 202 added notes to indicate areas 
    in the Technical Specifications that had special application to 
    Cycle 12 of Unit 2 only. Cycle 12 of Unit 2 ended in May 1999. Since 
    these notes no longer have application, they are proposed to be 
    removed. Additionally, Figure 2.1.1-la applies only to Unit 2, Cycle 
    12, and it is proposed to be removed.
        Therefore, removal of information no longer applicable to either 
    unit is an administrative change and will not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
    
    Correct a Typographical Error
    
        Technical Specification 5.6.5.b, Item 41.ii is being corrected 
    to change the number of the publication ``BASSS, Use of the Incore 
    Detector System to Monitor the DNB-LCO on Calvert Cliffs Unit 1 and 
    Unit 2'' from CEN-199(B) to CEN-119(B)-P. Correction of a 
    typographical error does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from an accident previously evaluated.
    
    Change the Definition of Azimuthal Power Tilt
    
        In their Infobulletin 97-07, Revision 1, ABB-CE stated that they 
    had found a discrepancy in the Technical specification definition of 
    azimuthal power tilt. This discrepancy was found to exist in all CE 
    Nuclear Steam Supply System analog plants that use CECOR for 
    monitoring and surveillance and that use ABB-CE safety analysis 
    methodology. Calvert Cliffs is one of those plants.
        The value of Tq (azimuthal tilt magnitude) as used in the 
    azimuthal power tilt formula now in Technical specification 1.1 is 
    not always the most conservative in all cases. With the proposed 
    definition, Tq is the maximum fractional increase in power that can 
    occur anywhere in the core because of tilt. Since Tq is the maximum 
    value, it is conservative. This is the appropriate measured value of 
    tilt to be used in verifying that the tilt assumed by ABB-CE in 
    establishing safety limits has not been exceeded.
        Therefore, changing the definition of azimuthal power tilt as 
    proposed will not create the possibility of a new or different type 
    of accident from any accident previously evaluated.
    
    Correct the Peak Linear Heat Rate
    
        When the ITS were written, a value of peak linear heat rate 
    [less than or equal to] 21 kW/ft was inadvertently written in 
    Technical Specification 2.1.1.2. The correct number is [less than or 
    equal to] 22 kW/ft. The required peak linear heat rate was 
    established at [less than or equal to] 22 kW/ft in License Amendment 
    Nos. 88 and 61. This number was valid for both units at the time of 
    implementation of ITS.
        Therefore, changing the value of peak linear heat rate to a 
    value previously approved by the NRC will not create the possibility 
    of a new or different type of accident from any accident previously 
    evaluated.
    
    Correct the Diesel Generator Loss of Voltage and Degraded Voltage 
    Settings
    
        When the ITS were written, a single set numbers for the degraded 
    voltage function was provided in Technical specification SR 3.3.6.2. 
    The degraded voltage function should have been expressed as 
    transient degraded voltage and steady-state degraded voltage. This 
    separation of two types of degraded voltage functions was approved 
    in License Amendment Nos. 226 and 200, which were issued before the 
    ITS were approved.
        Therefore, changing the degraded voltage function to the 
    transient degraded voltage and steady-state degraded voltage 
    functions previously approved by the NRC will not create the 
    possibility of a new or different type of accident from any accident 
    previously evaluated.
    
    Correct the Diesel Generator Voltage Range
    
        Technical Specification SRs 3.8.1.9 and 3.8.1.15 require that 
    each diesel be started from a stand-by condition. Surveillance 
    Requirement 3.8.1.9 requires that the generator reach [greater than 
    or equal to] 3740 volts within 10 seconds. After steady-state 
    conditions are reached, both SRs require the generator to maintain a 
    voltage range of greater than 3740 volts and [less than or equal to] 
    4580 volts.
        The Baltimore Gas and Electric Company ITS conversion added 
    voltage requirements to SRs 3.8.1.9 and 3.8.1.15 consistent with SR 
    3.8.1.3. License Amendment Nos. 226 and 200 changed the voltage 
    requirement for SR 3.8.1.3 to [greater than or equal to] 4060 volts 
    and [less than or equal to] 4400 volts. The voltage was not 
    corrected in SRs 3.8.1.9 and 3.8.1.15 when the Technical 
    Specifications were changed to ITS.
        Therefore, changing the voltage in SRs 3.8.1.9 and 3.8.1.15 to a 
    voltage previously approved by the NRC will not create the 
    possibility of a new or different type of accident from any accident 
    previously evaluated.
    
    Correct the List of Core Operating Limits
    
        Technical Specification 5.6.5.a lists Technical specifications 
    that are to be included in the core operating limits and documented 
    in the COLR. In the transition to ITS, Technical Specifications 
    3.1.4 (Control Element Assembly Alignment) and 3.3.1 (Reaction 
    Protective System--Operating) were inadvertently omitted from the 
    list. The complete list is currently in the COLR.
        Therefore, restoring Technical Specification 5.6.5.a to a list 
    previously approved by the NRC will not create the possibility of a 
    new or different type of accident from any accident previously 
    evaluated.
    
    Correct Figure 2.1.1-1
    
        A note on Technical Specification Figure 2.1.1-1 was changed in 
    License Amendment Nos. 227 and 201 (ITS) to delete reference to 
    Figure B2.1-1. Figure B2.1-1 was deleted from the Technical 
    Specification Bases in the transition of ITS. In License Amendment 
    Nos. 228 and 202, an old version of Figure 2.1.1-1 was used, and the 
    reference to Figure B2.1-1 was thus inadvertently put back in the 
    note. The proposed correction will replace the reference to Figure 
    B2.1-1 with the wording approved in License Amendment Nos. 227 and 
    201.
        Therefore, removal of information no longer applicable to either 
    unit is an administrative change and will not create the possibility 
    of a new or different type of accident from any accident previously 
    evaluated.
    
    Remove References to Unit 2, Cycle 12
    
        License Amendment Nos. 228 and 202 added notes to indicate areas 
    in the Technical Specifications that had special application to 
    Cycle 12 of Unit 2 only. Cycle 12 of Unit 2 ended in May 1999. Since 
    these notes no longer have application, they are
    
    [[Page 54374]]
    
    proposed to be removed. Additionally, Figure 2.1.1-1a applies only 
    to Unit 2, Cycle 12, and is proposed to be removed.
        Therefore, removal of information no longer applicable to either 
    unit is an administrative change and will not create the possibility 
    of a new or different type of accident from any accident previously 
    evaluated.
    
    Correct a Typographical Error
    
        Technical Specification 5.6.5.b, Item 41.ii is being corrected 
    to change the number of the publication ``BASSS, Use of the Incore 
    Detector System to Monitor the DNB-LCO on Calvert Cliffs Unit 1 and 
    Unit 2'' from CEN-199(B)-P to CEN-119(B)-P. Correction of a 
    typographical error will not create the possibility of a new or 
    different type of accident from any accident previously evaluated.
        3. Would not involve a significant reduction in the margin of 
    safety.
    
    Change the Definition of Azimuthal Power Tilt
    
        The margin of safety in this case is whether the azimuthal power 
    tilt calculation shows the highest (most conservative) value for Tq 
    (azimuthal tilt magnitude).
        The value of Tq as used in the azimuthal power tilt formula now 
    in Technical Specification 1.1 is not always the most conservative 
    in all cases. With the proposed definition, Tq is the maximum 
    fractional increase in power that can occur anywhere in the core 
    because of tilt. Since Tq is the maximum value, it is conservative. 
    This is the appropriate measured value of tilt to be used in 
    verifying that the tilt assumed in establishing safety limits has 
    not been exceeded.
        Therefore, changing the definition of azimuthal power tilt as 
    proposed will not involve a significant reduction in the margin of 
    safety.
    
    Correct the Peak Linear Heat Rate Safety Limit
    
        The margin of safety in this case was previously approved by the 
    NRC in License Amendment Nos. 88 and 61.
    
    Correct the Diesel Generator Loss of Voltage and Degraded Voltage 
    Settings
    
        The margin of safety in this case was previously approved by the 
    NRC in License Amendment Nos. 226 and 200.
    
    Correct the Diesel Generator Voltage Range
    
        The margin of safety in this case was previously approved by the 
    NRC in License Amendment Nos. 226 and 200.
    
    Correct the List of Core Operating Limits
    
        Technical Specification 5.6.5.a lists Technical specifications 
    that are to be included in the core operating limits and documented 
    in the COLR. In the transition to ITS, Technical Specifications 
    3.1.4 (Control Element Assembly Alignment) and 3.3.1 (Reactor 
    Protective System--Operating) were inadvertently omitted from the 
    list. The complete list is currently in the COLR.
        Therefore, restoring Technical Specification 5.6.5.a to a list 
    previously approved by the NRC will not involve a significant 
    reduction in the margin of safety.
    
    Correct Figure 2.1.1-1
    
        A note on Technical Specification Figure 2.1.1-1 was changed in 
    License Amendment Nos. 227 and 201 (ITS) to delete reference to 
    Figure B2.1-1. Figure B2.1-1 was deleted from the Technical 
    Specification Bases in the transition to ITS. In License Amendment 
    Nos. 228 and 202, an old version of figure 2.1.1-1 was used, and the 
    reference to Figure B2.1-1 was thus inadvertently put back in the 
    note. The proposed correction will replace the reference to Figure 
    B2.1-1 with the wording approved in License Amendment Nos. 227 and 
    201.
        Therefore, returning the note in Figure 2.1.1-1 to the wording 
    previously approved by the NRC will not involve a significant 
    reduction in the margin of safety.
    
    Remove References to Unit 2, Cycle 12
    
        License Amendment Nos. 228 and 202 added notes to indicate areas 
    in the Technical Specifications that had special application to 
    Cycle 12 of Unit 2 only. Cycle 12 of Unit 2 ended in May 1999. Since 
    these notes no longer have application, they are proposed to be 
    removed. Additionally, Figure 2.1.1-1a applies only to Unit 2, Cycle 
    12, and it is proposed to be removed.
        Therefore, removal of information no longer applicable to either 
    unit is an administrative change and will not involve a significant 
    reduction in the margin of safety.
    
    Correct a Typographical Error
    
        Technical specification 5.6.5.b, Item 41.ii is being corrected 
    to change the number of the publication ``BASSS, Use of the Incore 
    Detector system to Monitor the DNB-LCO on Calvert cliffs Unit 1 and 
    Unit 2'' from CEN-199(B)-P to CEN-119(B)-P. Correction of a 
    typographical error will not involve a significant reduction in the 
    margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Section Chief: S. Singh Bajwa.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of amendment request: August 26, 1999.
        Description of amendment request: The proposed amendment would 
    revise TS 3/4.9.4, ``Containment Building Penetrations,'' and its 
    associated Bases to allow penetrations which provide direct access from 
    the containment atmosphere to the outside atmosphere to remain open 
    during refueling operations provided certain administrative controls 
    are met.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Containment is not an accident initiating system as described in 
    the Final Safety Analysis Report. This change is applicable only in 
    Mode 6 during Core Alterations or movement of irradiated fuel (which 
    occurs when the unit is shutdown). The proposed change will not 
    modify equipment used for fuel movement or core alterations within 
    the HNP [Harris Nuclear Plant] Containment Building. Administrative 
    controls will be used to isolate containment in the event of a fuel 
    handling accident. The consequences of a Fuel Handling Accident 
    inside containment will increase as a result of this change. 
    However, the proposed administrative controls will require closure 
    of containment prior to exceeding standard review plan dose limits 
    due to a radiological release from a design basis fuel handling 
    accident.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed change provides for administrative controls and 
    operating restrictions for air lock doors consistent with previous 
    guidance authorized by the Commission for similar nuclear power 
    plants. Containment is not an accident initiating system as 
    described in the Final Safety Analysis Report. Fuel Handling 
    Accidents have been previously analyzed for the Harris Nuclear 
    Plant.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in the margin of safety.
        Administrative controls will be used to isolate containment in 
    the event of a fuel handling accident. The proposed administrative 
    controls will require closure of containment prior to exceeding 
    standard review plan dose limits due to a radiological release from 
    a design basis fuel handling accident.
        Therefore, the proposed change does not involve a significant 
    reduction in the margin of safety.
    
    
    [[Page 54375]]
    
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
        Attorney for licensee: William D. Johnson, Vice President and 
    Senior Counsel, Carolina Power & Light Company, Post Office Box 1551, 
    Raleigh, North Carolina 27602.
        NRC Section Chief: Sheri R. Peterson.
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, Unit 
    No. 2, Pope County, Arkansas
    
        Date of amendment request: July 29, 1999.
        Description of amendment request: The proposed change to the 
    Arkansas Nuclear One, Unit 2, Technical Specifications would allow the 
    performance of a special inspection of the steam generator tubes during 
    an upcoming mid-cycle outage. This mid-cycle outage is planned for the 
    purpose of performing inspections in selected areas of the steam 
    generator tube bundle where previous inspections have revealed tube 
    degradation. The proposed change would limit the initial inspection 
    scope to these identified areas and includes a scope expansion criteria 
    to address unexpected conditions.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        An evaluation of the proposed change has been performed in 
    accordance with 10 CFR 50.91(a)(1) regarding no significant hazards 
    considerations using the standards in 10 CFR 50.92(c). A discussion 
    of these standards as they relate to this amendment request follows:
        Criterion 1--Does Not Involve a Significant Increase in the 
    Probability or Consequences of an Accident Previously Evaluated.
        This change has no actual impact on any previously analyzed 
    accident in the final safety analysis report (FSAR). A double-ended 
    break of one steam generator tube is postulated as part of the ANO-2 
    design basis accident evaluation. The change permits Entergy 
    Operations to determine the appropriate scope and expansion criteria 
    for a special steam generator tube inspection that is being 
    performed at a frequency more conservative than that of the 
    augmented inservice inspection program included in the TSs 
    [Technical Specifications]. The special inspection will find and 
    repair certain steam generator tubing flaws that would otherwise 
    remain in service until the next scheduled refueling outage. The 
    increased inspection frequency reduces the probability that a flaw 
    in a steam generator tube could grow to a size that would affect the 
    leakage or structural integrity of the tube. The augmented inservice 
    inspection program contained in the TSs is not being modified.
        This change does not modify any parameter that will increase 
    radioactivity in the primary system or increase the amount of 
    radioactive steam released from the secondary safety valves or 
    atmospheric dump valves in the event of a tube rupture.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        Criterion 2--Does Not Create the Possibility of a New or 
    Different Kind of Accident from any Previously Evaluated.
        The scope of this change does not establish a potential new 
    accident precursor. The design basis accident analyses for ANO-2 
    include the consequences of a double-ended break of one steam 
    generator tube which bounds other postulated failure mechanisms. The 
    proposed change would permit determination of alternate inspection 
    criteria for a special inspection which is in addition to the 
    periodic inservice inspections required by the TSs. The equipment 
    used in the special inspection would not affect any plant components 
    differently than those used for current TS required inspections.
        Therefore, this change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        Criterion 3--Does Not Involve a Significant Reduction in the 
    Margin of Safety.
        As previously stated, a double-ended rupture of one steam 
    generator tube is accounted for in the ANO-2 design basis accident 
    analysis. Considering that the 2P99 special inspection is in 
    addition to the inservice inspection program defined in the ANO-2 
    TSs and that leakage detection capability is not being modified, 
    performance of a special inspection of any scope will increase the 
    margin of safety over the current TS requirements.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
        Therefore, based upon the reasoning presented above and the 
    previous discussion of the amendment request, Entergy Operations has 
    determined that the requested change does not involve a significant 
    hazards consideration.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, Arkansas 72801.
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502.
        NRC Section Chief: Robert A. Gramm.
    
    Indiana Michigan Power Company, Docket No. 50-315, Donald C. Cook 
    Nuclear Plant, Unit 1, Berrien County, Michigan
    
        Date of amendment request: August 17, 1999.
        Description of amendment request: The proposed amendment would 
    remove the voltage-based repair criteria, F* repair criteria, and 
    sleeving methodologies from the Unit 1 Technical Specifications (T/S) 
    and clarify the Bases sections accordingly.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        This change removes the interim steam generator tube plugging 
    criteria from the T/S and reinstates the original T/S criteria 
    consistent with Unit 2 (which does not have significantly degraded 
    steam generators). The current T/S allow for continued operation 
    with tubes that demonstrate indications per F* and voltage-based 
    criteria. The basis used to justify the interim criteria is specific 
    to the Unit 1 original steam generators (OSGs) and does not apply to 
    the replacement steam generators (RSGs).
        The proposed change returns the plugging criteria for the steam 
    generator tubes to the original licensing basis. The criteria are in 
    accordance with NUREG-0452, (old) ``Standard Technical 
    Specifications.'' The plugging criteria are based on a minimum wall 
    thickness due to wastage as determined by ASME [American Society of 
    Mechanical Engineers] Section XI. The proposed change is 
    conservative in nature because it does not allow for continued 
    operation with F* and voltage-based degraded tubes. Because of this, 
    the probability of a steam generator tube rupture (SGTR) is not 
    increased.
        The potential for a SGTR is also not increased as demonstrated 
    in the qualification analysis and testing for the RSGs. The program 
    for periodic in-service inspection monitors the integrity of the SG 
    tubing to provide reasonable assurance that there is sufficient time 
    to take proper and timely corrective action if any tube degradation 
    is detected. The tube inspections themselves are not initiators of a 
    SGTR. Therefore, this change is not expected to increase the 
    probability of a SGTR during normal or accident conditions.
        Unit 1 will continue to apply the T/S maximum primary-to-
    secondary leakage limit of 150 gallons per day (gpd) through any one 
    SG to minimize the potential for excessive leakage. The EPRI 
    [Electric Power Research Institute]-recommended 150 gpd limit
    
    [[Page 54376]]
    
    provides for leakage detection and plant shutdown in the event of an 
    unexpected tube leak and minimizes the potential for excessive 
    leakage or tube burst in the event of main steamline break (MSLB) or 
    loss-of-coolant accident (LOCA) conditions. This lower limit is more 
    restrictive than the limit (500 gpd per SG and total leakage of 1440 
    gpd) utilized for determination of offsite dose and also provides 
    further assurance that the probability of a SGTR is not increased.
        The design basis doses calculated for postulated accidents 
    involving degradation of SG tubes, such as SGTR and MSLB accidents, 
    as presented in UFSAR chapter 14 accident analysis, have been 
    evaluated. The SGTR consequences continue to be bounded by the 
    design basis analyses due to the allowable leakage rate specified by 
    this change. The proposed T/S leakage rate is maintained at 150 gpd 
    per SG. However, the maximum leakage of 500 gpd per SG and total 
    leakage of 1440 gpd for all four generators was used to determine 
    offsite dose in UFSAR chapter 14. The MSLB consequences are 
    decreased by installation of the RSGs due to the reduction in 
    primary-to-secondary leakage during the MSLB. Under the approved 
    interim plugging criteria, a leak rate of 8.4 gpm was determined to 
    be the upper limit for allowable primary-to-secondary leakage in the 
    faulted steam generator. This leakage, combined with the 150 gpd 
    leakage from the non-faulted SGs, was determined to limit the 
    offsite dose to 10% of the 10 CFR 100 limits. Following replacement 
    of the SGs, the leakage is limited during the MSLB to 150 gpd for 
    both the faulted and unfaulted SGs. Therefore, the Unit 1 MSLB dose 
    will be bounded by the current Unit 2 dose analysis, which is less 
    than 10% of 10 CFR 100 limits.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        Removing application of voltage-based repair criteria, F* repair 
    criteria, and sleeving methodologies upon installation of the RSGs 
    will not introduce significant or adverse changes to the plant 
    design basis that could lead to a new or different kind of accident 
    being created. This change does not change the overall objective of 
    surveillance activities--maintaining the structural integrity of 
    this portion of the reactor coolant system. The surveillance 
    activities are performed during outages. The proposed change in the 
    surveillance program returns the program to the initial licensing 
    basis. No new failures are created.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        Removing the application of voltage-based and F* repair criteria 
    and sleeving methodologies does not involve a reduction in the 
    margin of safety. The RSG tubing has been shown to retain adequate 
    structural and leakage integrity during normal, transient, and 
    postulated accident conditions consistent with GDC 14, 15, 30, 31, 
    and 32 of 10 CFR [Part] 50 [A]ppendix A. The RSG tubing has been 
    designed and evaluated consistent with the ASME Section III, 1989 
    edition. The proposed plugging criteria are based on ASME Section XI 
    and do not allow for operation with indications identified by F* and 
    voltage-based criteria. The proposed program for periodic in-service 
    inspection of the RSGs monitors the integrity of the SG tubing to 
    provide reasonable assurance that there is sufficient time to take 
    proper and timely corrective action if any tube degradation is 
    present. The proposed program is consistent with NUREG-0452 and was 
    the basis for the original Unit 1 T/S surveillance program.
        The proposed change maintains the T/S maximum primary-to-
    secondary leakage at 150 gpd per generator to minimize the potential 
    for excessive leakage. This limit provides for leakage detection and 
    shutdown in the event of an unexpected tube leak and minimizes the 
    potential for excessive leakage or tube burst in the event of a MSLB 
    or LOCA. Because this limit is maintained, the margin of safety is 
    maintained.
        Therefore, it is concluded that this change does not involve a 
    significant reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085.
        Attorney for licensee: Jeremy J. Euto, Esq., 500 Circle Drive, 
    Buchanan, MI 49107.
        NRC Section Chief: Claudia M. Craig.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald 
    C. Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan
    
        Date of amendment requests: September 10, 1999.
        Description of amendment requests: The proposed amendments would 
    revise Technical Specification (T/S) 3/4.4.7 so that the surveillance 
    requirement does not need to be performed when the reactor is defueled 
    with no forced circulation. The proposed revision to T/S 3/4.4.7 also 
    includes changes to Tables 3.4-1 and 4.4-3. A change is proposed to 
    Unit 1 T/S Table 4.4-3 to revise the reactor coolant system (RCS) 
    chemistry sampling frequency from three times per 7 days with a maximum 
    interval of 72 hours to a frequency of at least once per 72 hours. An 
    editorial change to Unit 1 Tables 3.4-1 and 4.4-3 would relocate the 
    asterisk for the footnote to a position adjacent to the parameter 
    ``dissolved oxygen,'' from its current position next to the allowable 
    chemistry limit in Table 3.4-1 and the analysis frequency in Table 4.4-
    3. An editorial change would also correct the footnote for Table 3.4-1 
    for Unit 1 and Unit 2 by making the word ``limit'' plural, as it 
    applies to both the steady-state and transient limits.
        Changes are also proposed to revise Surveillance Requirement 
    4.11.2.2 by deleting the phrase ``by analysis of the Reactor Coolant 
    System noble gases.''
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. Does the change involve a significant increase in the 
    probability of occurrence or consequences of an accident previously 
    evaluated?
        The proposed changes to the RCS chemistry sampling requirements 
    do not affect the probability of a loss-of-coolant accident or steam 
    generator tube rupture, which are evaluated in Sections 14.3 and 
    14.2.4, respectively, of the Updated Final Safety Analysis Report 
    (UFSAR). RCS contaminant limits are maintained to reduce the 
    potential for RCS leakage or failure due to corrosion. Sampling the 
    RCS for contaminants does not initiate an accident. Deleting the 
    requirement to obtain samples when the reactor is defueled does not 
    modify any plant equipment or affect plant operation and therefore 
    does not introduce any new accident initiators or precursors. 
    Suspension of RCS chemistry sampling when the reactor is defueled 
    does not increase the potential for RCS leakage or failure because 
    the corrosive effects of the contaminants is minimal during this 
    low-temperature, low-pressure condition. To ensure elevated 
    contaminant levels would be detected and corrected prior to 
    subjecting the system to a high-temperature condition, chemistry 
    sampling will be reinstated within 72 hours of re-establishing 
    forced circulation and prior to entering Mode 6. Removing the 
    restriction for analyzing primary coolant chemical contaminants at 
    least three times every seven days does not change the maximum 
    surveillance interval. This change allows the sample to be collected 
    two or three times per week, consistent with the maximum 72-hour 
    interval. The 72-hour sampling and analysis interval is consistent 
    with the current requirement in the Unit 2 T/S, and industry 
    guidance in NUREG-0452, ``Standard Technical Specifications.'' The 
    72-hour interval continues to provide adequate assurance that 
    concentrations in excess of the limits are detected in sufficient 
    time to take corrective actions. Therefore, the probability of 
    occurrence of a previously evaluated accident is not increased.
        This change does not alter the quantity of radioactive material 
    in any system during normal plant operation, the amount of
    
    [[Page 54377]]
    
    shielding provided by plant systems, or the mitigative capabilities 
    of any system following an event. Therefore, the consequences of a 
    previously evaluated accident are not increased.
        The editorial changes to the RCS chemistry T/S provide 
    consistency between the Unit 1 and Unit 2 T/S and the Standard 
    Technical Specifications. These changes do not affect the design or 
    operation of any system, structure, or component in the plant. The 
    accident analysis assumptions and results are unchanged. No new 
    failures or interactions are created.
        The amount of radioactive material in the gas storage tanks is 
    controlled to ensure that, in the event of a rupture of one of these 
    tanks, the resulting total body exposure to an individual at the 
    nearest site boundary would not exceed 0.5 rem. The accidental waste 
    gas release event is summarized in Section 14.2.3 of the UFSAR. 
    Sampling to determine the radioactivity levels in the tanks does not 
    initiate an accident or identify any accident precursors. The 
    increased sampling flexibility does not change the method of 
    operating the waste gas system, nor does it modify any interfaces 
    with other plant systems. Therefore, this change does not increase 
    the probability of occurrence of an accidental waste gas release 
    event.
        Implementation of a different sampling method does not change 
    the maximum quantity of radioactive material specified in the T/S 
    Limiting Condition for Operation (LCO). The sampling method has no 
    effect on normal plant gaseous radwaste activities, so the 
    composition of the radioactive gaseous nuclides present in the tank 
    at the time of the event is not affected. As the proposed revision 
    allows a change to the method of sampling but does not affect the 
    radioactivity limit for the gas storage tanks, the proposed change 
    does not increase the consequences of an accidental waste gas 
    release event.
        Therefore, the probability of occurrence or the consequences of 
    accidents previously evaluated are not increased.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes to revise the RCS chemistry sampling 
    frequency and to suspend RCS chemistry sampling when the reactor is 
    defueled with no forced circulation does not change the method of 
    operating any equipment or the operational limits of any equipment. 
    The proposed changes do not introduce any new failure mechanisms to 
    the RCS or any other plant systems. The proposed change does not 
    involve any physical alterations to any plant equipment, and causes 
    no change in the method by which any plant system performs its 
    function. Editorial changes to footnotes for Tables 3.4-1 and 4.4-3 
    provide consistency between the T/S for Unit 1 and Unit 2, but do 
    not change the methods of operating any equipment or introduce any 
    new failure mechanisms.
        The proposed change to eliminate the prescriptive waste gas tank 
    sampling method does not introduce any new failure mechanisms to the 
    waste disposal system, involve any physical changes to the waste 
    disposal system or any other plant systems, or change the way any 
    plant systems are operated. This change does not change any 
    interfaces between the waste disposal system and any other plant 
    systems. The proposed changes continue to ensure the system is 
    operated within the existing limit established by the T/S LCO. Thus, 
    no adverse safety considerations are introduced by this proposed 
    change to the T/S.
        Therefore, the proposed changes do not create the possibility of 
    a new or different kind of accident from any accident previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The margin of safety pertinent to the RCS chemistry surveillance 
    is related to the concentration of chemical contaminants that would 
    expedite corrosion of the RCS piping and components and the period 
    of time during which the system is allowed to operate outside the T/
    S limits. The proposed changes to the RCS chemistry surveillance do 
    not alter either of these criteria. These proposed changes do not 
    affect any safety limits or T/S parameter limits. The proposed 
    changes do not introduce new equipment, equipment modifications, or 
    new or different modes of plant operation. These changes do not 
    affect the operational characteristics of any equipment or systems. 
    The editorial changes to footnotes for Tables 3.4-1 and 4.4-3 
    provide consistency between the T/S for Unit 1 and 2, but do not 
    affect the acceptance criteria or surveillance frequencies for this 
    T/S.
        The margin of safety pertinent to the waste gas storage tanks is 
    related to the quantity of radioactivity that would be released in 
    the unlikely event of a tank rupture. The proposed change to the gas 
    storage tank T/S eliminates the prescriptive sampling methodology, 
    but does not affect the requirement to periodically quantify the 
    radioactive gaseous material in the gas storage tanks. The proposed 
    change does not affect the quantity of radioactivity allowed in the 
    gas storage tanks, nor does it alter the methodology, assumptions, 
    or results of any safety analyses. The proposed change to delete the 
    prescriptive sampling method does not affect any safety limits or T/
    S parameter limits.
        Therefore, the proposed changes do not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085.
        Attorney for licensee: Jeremy J. Euto, Esq., 500 Circle Drive, 
    Buchanan, MI 49107.
        NRC Section Chief: Claudia M. Craig.
    
    National Aeronautics Space Administration (NASA), Docket No. 50-30, 
    NASA Test Reactor, Erie County, Ohio
    
        Date of amendment request: March 25, 1999, as supplemented by 
    letter dated August 10, 1999.
        Description of amendment request: The proposed amendment would 
    change Lewis Research Center (LeRC) to Glenn Research Center (GRC).
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        (1) Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        The proposed amendment will change the name of the Licensee for 
    the Plum Brook Reactor Facility (PBRF) TR-3 license, a possession 
    only license, from Lewis Research Center (LeRC) to the Glenn 
    Research Center (GRC). The amendment request is necessary because 
    NASA has changed the name of the Lewis Research Center to the Glenn 
    Research Center at Lewis Field under legislative action and signed 
    into law (sec. 434, P.L. 105-276, 112 Stat. 2461) on October 21, 
    1998. The effective date of this name change was March 1, 1999. 
    NASA, GRC will retain the PBRF license and the responsibility to 
    continue maintaining the PBRF Reactor Facility in a safe protected 
    storage mode under the current TR-3 possess-but-not-operate license. 
    In addition, the current plans to provide a PBRF decommissioning 
    plan to the NRC by the end of CY 1999 and the eventual 
    decommissioning by the end of CY 2007 have not changed.
        There will be no change in the funding status of the GRC in 
    either maintaining the PBRF facility in the safe protected storage 
    mode or the eventual decommissioning. NASA, as a government agency, 
    remains responsible for the continuing funding of both activities.
        In addition, there will be no change in the personnel who are 
    responsible for maintaining the present TR-3 license or in 
    developing the PBRF Decommissioning Plan.
        The proposed amendment does not require any physical change to 
    the PBRF Facility, changes to the Technical Specifications or 
    procedures under the PBRF TR-3 License other than the name change 
    from LeRC to GRC. The proposed change does not increase the 
    probability of any accident or increased risk to the public safety.
        Therefore, the proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident condition 
    previously evaluated.
        (2) Would not create the possibility of a new or different kind 
    of accident from any accident previously evaluated.
        The proposed amendment does not modify the PBRF facility 
    configuration or licensed activities. Therefore, no additional 
    accident conditions are introduced.
    
    [[Page 54378]]
    
        Therefore, the proposed amendment does not involve a significant 
    increase in the probability or consequence of an accident.
        (3) Would not involve a significant reduction in a margin of 
    safety.
        This amendment is required because of the name change from LeRC 
    to GRC. NASA will continue to be financially responsible to maintain 
    the PBRF Facility under the existing TR-3 License.
        Furthermore, the GRC personnel for the eventual PBRF 
    decommissioning and contract support personnel reporting to GRC will 
    continue to be technically qualified to maintain the PBRF under the 
    safe protected storage mode. There has been no effective change in 
    the personnel who will be responsible to implement the eventual 
    decommissioning effort that will be required under the future PBRF 
    Decommissioning Plan.
        Plum Brook's existing qualified contractors remained in place 
    following the name change. The requested amendment does not involve 
    any changes in the performance of current licensed activities and 
    these activities will continue in their current form without changes 
    or interruptions of any kind.
        The proposed amendment does not alter any margin of safety 
    because it does not involve any changes in the PBRF Facility or 
    licensed activities under the TR-3 License. All activities will 
    continue in the current form without changes or interruptions of any 
    kind as a result of the name.
        Therefore, the proposed amendment does not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    request for amendments involves no significant hazards consideration.
        Local Public Document Room location: N/A.
        Attorney for licensee: Elias T. Naffah, MS 500-118, NASA, Glenn 
    Research Center, 21000 Brookpark Road, Cleveland Ohio 44135.
        NRC Branch Chief: Ledyard B. Marsh.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, Millstone 
    Nuclear Power Station, Unit No. 2, New London County, Connecticut
    
        Date of amendment request: July 16, 1999.
        Description of amendment request: Proposed relocation of Technical 
    Specifications 3/4.9.3.2, ``Refueling Operations, Spent Fuel 
    Temperature,'' 3/4.9.3.3, ``Refueling Operations, Decay Time,'' 3/
    4.9.5, ``Refueling Operation, Communications,'' 3/4.9.6, ``Refueling 
    Operation, Crane Operability--Containment Building,'' and 3/4.9.7, 
    ``Refueling Operations, Crane Travel--Spent Fuel Storage Building,'' to 
    the Millstone, Unit No. 2 Technical Requirements Manual. The associated 
    Bases pages and index pages will be modified to address the proposed 
    change.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below:
    
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        Technical Specification 3/4.9.3.2, ``Refueling Operations, Spent 
    Fuel Pool Temperature,'' is proposed to be relocated to the TRM 
    where future changes will be controlled in accordance with 10 CFR 
    50.59. This specification limits spent fuel pool temperature to be 
    less than or equal 140  deg.F to ensure the resin in the spent fuel 
    cooling demineralizers will not degrade and the temperature and 
    humidity are compatible with personnel comfort and safety 
    requirements. Additionally, the requirement ensures that the design 
    temperature of the fuel pool cooling system, liner/building 
    structures, and racks is not exceeded. Relocation of this Technical 
    Specification to the TRM does not imply any reduction in its 
    importance in limiting the spent fuel pool bulk temperature to be 
    less than or equal to 140  deg.F. Spent fuel pool bulk temperature 
    is a design bases process variable which is used to establish the 
    required heat removal capabilities of the spent fuel heat removal 
    system. In the unlikely event of total loss of cooling water flow to 
    the spent fuel pool, the pool water temperature may reach 212  deg.F 
    within approximately 9 hours and will result in a boiling condition. 
    This event does not represent a challenge to the fuel cladding, as a 
    fission product barrier, unless the fuel becomes uncovered. The 
    requirement on storage pool water level is covered by Technical 
    Specification 3/4.9.12, ``Storage Pool Water Level,'' which requires 
    a minimum of 23 feet of water over the top of irradiated fuel 
    assemblies. Therefore, spent fuel pool bulk temperature is not by 
    itself a process variable that is an initial condition of a design 
    basis accident. This Technical Specification does not cover a 
    process variable, design feature, or operating restriction that is 
    an initial condition of a design basis accident or transient 
    analysis that either assumes the failure of or presents a challenge 
    to the integrity of a fission product barrier. It does not cover a 
    structure, system, or component that is part of the primary success 
    path which functions or actuates to mitigate a design basis accident 
    or transient that either assumes the failure of or presents a 
    challenge to the integrity of a fission product barrier. The 
    proposed change will not alter the way pool temperature is measured, 
    nor will it alter any of the assumptions used in the spent fuel pool 
    fuel handling accident analysis. Relocation of this Technical 
    Specification to the TRM does not degrade the performance of any 
    safety systems or prevent actions assumed in the accident analysis, 
    nor does it alter any of the assumptions made in the analysis that 
    could increase the consequences of accidents. Therefore, this change 
    will not significantly increase the probability or consequences of 
    an accident previously evaluated.
        Technical Specification 3/4.9.3.3, ``Refueling Operations, Decay 
    Time,'' is proposed to be relocated to the TRM where future changes 
    will be controlled in accordance with 10 CFR 50.59. This 
    specification requires the reactor to remain in Mode 5 or 6 until 
    the most recent core offload has decayed a sufficient time to ensure 
    alternate cooling is available during this time to cool the spent 
    fuel pool should a failure occur in the Spent Fuel Pool Cooling 
    System. Alternate cooling would be provided by the Shutdown Cooling 
    System. Relocation of this Technical Specification to the TRM does 
    not imply any reduction in its importance in insuring that the most 
    recent core offload has decayed a sufficient time. If the 
    requirement to remain in Mode 5 or 6 until the most recent core 
    offload has decayed for 504 hours is not satisfied, the spent fuel 
    pool cooling system may not have the capability to remove decay heat 
    and stay below the Technical Specification limit of 140  deg.F. In 
    the unlikely event of total loss of cooling water flow to the spent 
    fuel pool, the pool water temperature may reach 212  deg.F in less 
    than 9 hours and will result in a boiling condition. This event does 
    not represent a challenge to the fuel cladding, as a fission product 
    barrier, unless the fuel becomes uncovered. The requirements on 
    storage pool water level is covered by Technical Specification 3/
    4.9.12, ``Storage Pool Water Level,'' which requires a minimum of 23 
    feet of water over the top of irradiated fuel assemblies. Therefore, 
    this requirement to remain in Mode 5 or 6 until the most recent core 
    offload has decayed for 504 hours is not by itself a process 
    variable that is an initial condition of a design basis accident. 
    This Technical Specification does not cover a process variable, 
    design feature, or operating restriction that is an initial 
    condition of a design basis accident or transient analysis that 
    either assumes the failure of or presents a challenge to the 
    integrity of a fission product barrier. It does not cover a 
    structure, system, or component that is part of the primary success 
    path which functions or actuates to mitigate a design basis accident 
    or transient that either assumes the failure of or presents a 
    challenge to the integrity of a fission product barrier. The 
    proposed change will not alter the requirement that the most recent 
    core offload has decayed a sufficient time, nor will it alter any of 
    the assumptions used in the spent fuel pool fuel handling accident 
    analysis. Relocation of this Technical Specification to the TRM does 
    not degrade the performance of any safety systems or prevent actions 
    assumed in the accident analysis, nor does it alter any of the 
    assumptions made in the analysis that could increase the 
    consequences of accidents. Therefore, this change will not 
    significantly increase the probability or consequences of an 
    accident previously evaluated.
        Technical Specification 3/4.9.5, ``Refueling Operations, 
    Communications,'' is proposed to be relocated to the TRM where 
    future
    
    [[Page 54379]]
    
    changes will be controlled in accordance with 10 CFR 50.59. This 
    specification requires communication between the control room and 
    the refueling station, to ensure any abnormal change in the facility 
    status, as indicated on the control room instrumentation, can be 
    communicated to the refueling station personnel. Relocation of this 
    Technical Specification to the TRM does not imply any reduction in 
    its importance in insuring communication between the control room 
    and the refueling station. This Technical Specification does not 
    cover a process variable, design feature, or operating restriction 
    that is an initial condition of a design basis accident or transient 
    analysis that either assumes the failure of or presents a challenge 
    to the integrity of a fission product barrier. It does not cover a 
    structure, system, or component that is part of the primary success 
    path which functions or actuates to mitigate a design basis accident 
    or transient that either assumes the failure of or presents a 
    challenge to the integrity of a fission product barrier. The 
    proposed change will not alter the requirement on communication 
    between the control room and the refueling station, nor will it 
    alter any of the assumptions used in the spent fuel pool fuel 
    handling accident analysis. Relocation of this Technical 
    Specification to the TRM does not degrade the performance of any 
    safety systems or prevent actions assumed in the accident analysis, 
    nor does it alter any of the assumptions made in the analysis that 
    could increase the consequences of accidents. Therefore, this change 
    will not significantly increase the probability or consequences of 
    an accident previously evaluated.
        Technical Specification 3/4.9.6, ``Refueling Operations, Crane 
    Operability--Containment Building,'' is proposed to be relocated to 
    the TRM where future changes will be controlled in accordance with 
    10 CFR 50.59. This specification ensures the lifting device on the 
    refueling machine has adequate capacity to lift the weight of a fuel 
    assembly and a control element assembly, and that an automatic load 
    limiting device is available to prevent damage to the fuel assembly 
    during fuel movement. Relocation of this Technical Specification to 
    the TRM does not imply any reduction in its importance in insuring 
    that the lifting device on the refueling machine has adequate 
    capacity. The automatic load limiting device and/or physical stops 
    are not monitored and controlled during operation, nor are they 
    assumed to function to mitigate the consequences of a design basis 
    accident. The automatic load limiting device is checked on a 
    periodic basis to ensure operability. This Technical Specification, 
    which ensures the lifting device on the refueling machine has 
    adequate capacity, does not cover a process variable, design 
    feature, or operating restriction that is an initial condition of a 
    design basis accident or transient analysis that either assumes the 
    failure of or presents a challenge to the integrity of a fission 
    product barrier. The proposed change will not alter the requirement 
    that the lifting device on the refueling machine has adequate 
    capacity, nor will it alter any of the assumptions used in the 
    accident analysis. Relocation of this Technical Specification to the 
    TRM does not degrade the performance of any safety systems or 
    prevent actions assumed in the accident analysis, nor does it alter 
    any of the assumptions made in the analysis that could increase the 
    consequences of accidents. Therefore, this change will not 
    significantly increase the probability or consequences of an 
    accident previously evaluated.
        Technical Specification 3/4.9.7, ``Refueling Operations, Crane 
    Travel--Spent Fuel Storage Pool Building,'' is proposed to be 
    relocated to the TRM where future changes will be controlled in 
    accordance with 10 CFR 50.59. This specification ensures loads in 
    excess of one fuel assembly containing a control element assembly, 
    plus the weight of the fuel handling tool, will not be moved over 
    other fuel assemblies in the spent fuel storage racks. Therefore, in 
    the event of a drop of this load, the activity released is limited 
    to that contained in one fuel assembly. Relocation of this Technical 
    Specification to the TRM does not imply any reduction in its 
    importance in insuring that loads in excess of 1800 pounds (except 
    of a consolidated fuel storage box) are prohibited from travel over 
    irradiated fuel. While this Technical Specification does address an 
    operating restriction assumed in the accident analysis, there is no 
    process variable that can be monitored during power operation of the 
    plant. Crane interlocks and/or physical stops are used to assure 
    that this requirement is met, but indication of the operation of the 
    interlocks and/or physical stops is not available in the control 
    room. These features inhibit movement of the crane so that 
    monitoring is not necessary. This Technical Specification does not 
    cover a structure, system, or component that is part of the primary 
    success path which functions or actuates to mitigate a design basis 
    accident or transient that either assumes the failure of or presents 
    a challenge to the integrity of a fission product barrier. The 
    proposed change will not alter the requirement that the crane 
    interlocks and/or physical stops are OPERABLE, nor will it alter any 
    of the assumptions used in the spent fuel pool fuel handling 
    accident analysis. Relocation of this Technical Specification to the 
    TRM does not degrade the performance of any safety systems or 
    prevent actions assumed in the accident analysis, nor does it alter 
    any of the assumptions made in the analysis that could increase the 
    consequences of accidents. Therefore, this change will not 
    significantly increase the probability or consequences of an 
    accident previously evaluated.
        Revision of Index Pages IX and XIII and the proposed change to 
    Bases sections, by relocating them to the TRM, are administrative 
    changes. Therefore, this change will not significantly increase the 
    probability or consequences of an accident previously evaluated. The 
    proposed changes do not alter how any structure, system, or 
    component functions. There will be no effect on equipment important 
    to safety. The proposed changes have no effect on any of the design 
    basis accidents previously evaluated. Therefore, this License 
    Amendment Request does not impact the probability of an accident 
    previously evaluated, nor does it involve a significant increase in 
    the consequences of an accident previously evaluated.
        2. Create the possibility of a new or different kind of accident 
    from any accident previously evaluated.
        The proposed changes do not alter the plant configuration (no 
    new or different type of equipment will be installed) or require any 
    new or unusual operator actions. They do not alter the way any 
    structure, system, or component functions and do not alter the 
    manner in which the plant is operated. The proposed changes do not 
    introduce any new failure modes. Therefore, the proposed changes 
    will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        3. Involve a significant reduction in a margin of safety.
        The proposed relocation of Technical Specification 3/4.9.3.2, 
    ``Refueling Operations, Spent Fuel Pool Temperature,'' to the TRM 
    does not imply any reduction in its importance in limiting the spent 
    fuel pool bulk temperature to less than or equal to 140  deg.F. The 
    proposed change will not alter the way pool temperature is measured. 
    It will not alter any of the assumptions used in the spent fuel pool 
    fuel handling accident analysis, nor will it cause any safety system 
    parameters to exceed their acceptance limit. The proposed relocation 
    of Technical Specification 3/4.9.3.3, ``Refueling Operations, Decay 
    Time,'' to the TRM does not imply any reduction in its importance in 
    insuring that the most recent core offload has decayed a sufficient 
    time. The proposed change will not alter the requirement that the 
    most recent core offload has decayed a sufficient time, it will not 
    alter any of the assumptions used in the spent fuel pool fuel 
    handling accident analysis, nor will it cause any safety system 
    parameters to exceed their acceptance limit. The relocation of 
    Technical Specification 3/4.9.5, ``Refueling Operations, 
    Communications,'' to the TRM does not imply any reduction in its 
    importance in insuring communication between the control room and 
    the refueling station. The proposed change will not alter the 
    requirement on communication between the control room and the 
    refueling station, it will not alter any of the assumptions used in 
    the spent fuel pool fuel handling accident analysis, nor will it 
    cause any safety system parameters to exceed their acceptance limit. 
    The relocation of Technical Specification 3/4.9.6, ``Refueling 
    Operations, Crane Operability--Containment Building,'' to the TRM 
    does not imply any reduction in its importance in insuring that the 
    lifting device on the refueling machine has adequate capacity. The 
    proposed change will not alter the requirement that the lifting 
    device on the refueling machine has adequate capacity, it will not 
    alter any of the assumptions used in the accident analysis, nor will 
    it cause any safety system parameters to exceed their acceptance 
    limit. The relocation of Technical Specification 3/4.9.7, 
    ``Refueling Operations, Crane Travel--Spent Fuel Storage Pool 
    Building,'' to the TRM does not imply any reduction in its 
    importance in insuring that loads in excess of 1800 pounds (except 
    of a consolidated fuel storage box) are prohibited from travel over 
    irradiated fuel. The proposed change will not
    
    [[Page 54380]]
    
    alter the requirement that the crane interlocks and/or physical 
    stops are OPERABLE, it will not alter any of the assumptions used in 
    the spent fuel pool fuel handling accident analysis, nor will it 
    cause any safety system parameters to exceed their acceptance limit. 
    Revision of Index Pages IX and XIII and the proposed change to Bases 
    sections by eliminating the sections corresponding to the relocated 
    Technical Specifications are administrative changes. These changes 
    will not alter any of the assumptions used in the spent fuel pool 
    fuel handling accident analysis, nor will it cause any safety system 
    parameters to exceed their acceptance limit. The proposed changes do 
    not affect any of the assumptions used in the accident analysis, nor 
    do they affect any operability requirements for equipment important 
    to plant safety. Therefore, the proposed changes will not result in 
    a significant reduction in a margin of safety.
    
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
        Attorney for licensee: Lillian M. Cuoco, Esq., Senior Nuclear 
    Counsel, Northeast Utilities Service Company, P.O. Box 270, Hartford, 
    Connecticut.
        NRC Section Chief: James W. Clifford.
    
    PECO Energy Company, Docket No. 50-352, Limerick Generating Station, 
    Unit 1, Montgomery County, Pennsylvania
    
        Date of amendment request: June 7, 1999.
        Description of amendment request: The proposed change to the 
    Technical Specifications (TSs), if approved, will reflect the permanent 
    deactivated configuration of the ``wet'' instrument reference leg 
    isolation valve HV-61-102 which originally connected the Drywell Floor 
    and Equipment Drain Tanks to level instruments outside the containment. 
    The TS changes affecting TS Table 3.6.3-1, ``Primary Containment 
    Isolation Valves,'' and its associated notations will reflect the 
    current plant configuration. More specifically, TS Section 3/4.6.3, 
    ``Primary Containment Isolation Valves,'' Table 3.6.3-1, Penetration 
    Number 230B will be revised to designate the function of valve HV-61-
    102 as ``Deactivated,'' the maximum isolation time for valve HV-61-102 
    will be eliminated, and notations 1, 23, and 29 will be replaced with a 
    new notation indicating the permanent configuration of the subject 
    valve.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration. The NRC staff has reviewed the licensee's analysis 
    against the standards of 10 CFR 50.92(c). The NRC staff's review is 
    presented below:
    
        1. The proposed TS changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The closed valve, HV-61-102, has no effect on the function of 
    the Drywell Sump/Equipment Drain Tanks, other safety-related 
    systems, or other containment penetrations. The current status of 
    the valve is locked closed, de-energized, and the motor operator 
    cannot be accidentally actuated. In addition, the line is capped 
    downstream of the isolation valve. As described above, the valve is 
    considered to be in a passive configuration, where a malfunction is 
    not expected and cannot cause an increase in the probability of a 
    malfunction to itself or other safety-related equipment. The 
    potential for increased releases outside the containment due to 
    breaching of the valve assembly is no greater than that of the 
    isolation design previously evaluated.
        Therefore, the proposed change to the TSs does not involve a 
    significant increase in the probability of occurrence or 
    consequences of an accident previously evaluated in the Safety 
    Analysis Report.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The abandoned isolation valve conforms to approved isolation 
    configurations, and its structural integrity has not been degraded 
    by the modified configuration. The original function of valve HV-61-
    102 was only to provide isolation of the instrument line. Following 
    the modification, the valve is independent of the function of the 
    Drywell Sump/ Equipment Drain Tanks, other safety-related systems, 
    and other penetrations. Since the valve is passive and has no 
    requirements to be operated, it cannot create a different type of 
    malfunction on itself or other safety-related systems. In addition, 
    the valve is specifically designed to isolate and is essentially 
    passive during accident conditions, it has no activity that could be 
    the initiator of an accident of a different type.
        Therefore, the proposed changes to the TSs do not create the 
    possibility of a new or different kind of accident from any accident 
    previously evaluated.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety. Isolation valve HV-61-102 in its 
    proposed permanent configuration meets the margin of safety 
    described in TS Bases 3/4.6.3 since it is kept closed under all 
    operational conditions and will not be under the constraint of TS 
    closing times in order to maintain releases within specifications. 
    The proposed changes have no impact on any safety analysis 
    assumptions.
        Therefore, the proposed TS changes do not involve a significant 
    reduction in the margin of safety.
    
        Based on this review, it appears that the three standards of 10 CFR 
    50.92(c) are satisfied. Therefore, the NRC staff proposes to determine 
    that the amendment request involves no significant hazards 
    consideration.
        Local Public Document Room location: Pottstown Public Library, 500 
    High Street, Pottstown, PA 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V.P. and 
    General Counsel, PECO Energy Company, 2301 Market Street, Philadelphia, 
    PA 19101.
        NRC Section Chief: James W. Clifford.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of amendment request: July 23, 1999, as supplemented on 
    September 13, 1999.
        Description of amendment request: The proposed amendment would 
    revise Technical Specification Surveillance Requirement 4.8.1.1.2 to 
    allow the 24-hour emergency diesel generator endurance run to be 
    performed during power operation (i.e., Modes 1 and 2) instead of 
    restricting the test to when the reactor was shutdown.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change to Technical Specification Surveillance 
    Requirement (SR) 4.8.1.1.2.d.7 (24-hour emergency diesel generator 
    (EDG) endurance run test) to eliminate the restriction to perform 
    the test during shutdown conditions does not involve a significant 
    increase in the probability of any previously evaluated accident. 
    Although paralleling or connecting the EDG to off-site power for the 
    test could induce an electrical distribution system perturbation, 
    the same possibility exists when the EDG is tested during the 
    monthly 1-hour loaded surveillance test (SR 4.8.1.1.2 a 2). This 
    risk during testing the EDG monthly at power was reviewed and found 
    acceptable by the NRC. Further, none of the automatic actuations and 
    interlocks in the tested portion of the electrical system or the EDG 
    control system are disabled during the 24-hour endurance run. Thus, 
    the onsite safety-related electrical system remains protected from 
    potential faults and perturbations.
        The ability and capability [o]f the EDG to perform their safety 
    function (mitigate the consequences of a previously evaluated
    
    [[Page 54381]]
    
    accident) is also unaffected. This capability was demonstrated not 
    only by the tests conducted in the EDG manufacturer's plant, but 
    continue to be demonstrated by surveillance testing performed at the 
    station.
        This testing verifies specific design criteria, which assure 
    continued EDG operability even during testing. Examples of presently 
    performed Technical Specification testing that demonstrate the 
    ability and capability of the EDG to perform its safety functions 
    are:
         SR 4.8.1.1.2. d. 2 requires, in part, that on a load 
    rejection of greater than 820 KW, the voltage and frequency be 
    restored to acceptable values within 4 seconds.
         This surveillance demonstrates the ability of the EDGs 
    to withstand a loss of load, as it would occur in a normal 
    safeguards equipment controller (SEC) actuation, without 
    compromising its ability to be ready to accept a new loading 
    sequence and carry its design safety function.
         SR 4.8.1.1.2. d. 9 requires, in part, that with the EDG 
    operating in a test mode (connected to its bus), a simulated safety 
    injection signal overrides the test mode by (1) returning the diesel 
    generator to standby operation and (2) automatically energizing the 
    emergency loads with offsite power.
        This surveillance demonstrates the ability of the EDGs to be 
    disconnected from the grid, if in a test mode, on an accident 
    signal, and be ready to accept a new loading sequence and carry its 
    design safety function.
         SR 4.8.1.1.2. a. 2 requires, in part, that every 31 
    days each EDG be demonstrated OPERABLE by synchronizing it to the 
    grid for greater than or equal to 60 minutes.
        Note that this proposed amendment request eliminates a 
    discrepancy between the current requirement to perform the 24 hour 
    run during shutdown and SR 4.8.1.1.2.a.2, which would allow a 24 
    hour run at power.
        Additionally, PSE&G performed an assessment of the potentially 
    added risk of an additional 24 hours of on-line EDG testing. The 
    unavailability of all three EDGs was increased in the Probabilistic 
    Safety Analyses (PSA) for both Salem Units 1 and 2 to correspond to 
    an additional 24 hours per cycle out-of-service time each 18-month 
    operating cycle. The unavailability was changed from 1.86E-02/year 
    to 2.0E-2/year. The increase in the baseline internal events core 
    damage frequency (CDF) was determined to be 1.6E-07 events/year for 
    both Salem Units 1 and 2. Based on the definition provided in 
    Regulatory Guide 1.174, Paragraph 2.2.4, this increase is considered 
    a very small increase in risk (less than 1.0E-06 events/year).
        Therefore, the proposed amendment, including proposed 
    administrative controls, does not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed amendment to Technical Specification Surveillance 
    Requirement 4.8.1.1.2.d.7 (24-hour endurance run test) to eliminate 
    the restriction to perform the test during shutdown conditions does 
    not physically modify the facility, introduce a new failure mode, or 
    propose a different operational mode of the AC electrical power 
    sources, or Emergency Diesel Generators.
        Therefore, the proposed amendment will not create the 
    possibility of a new or different kind of accident from any 
    previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The AC Electrical distribution system has been designed to 
    provide sufficient redundancy and reliability to ensure the 
    availability of the EDGs to provide the required safety function 
    under design basis events to protect the power plant, the public and 
    plant personnel. Specifically, the ability of the EDGs to separate 
    from the off-site power source has been designed and tested per 
    Technical Specifications requirements.
        Performance of the 24-hour endurance run during power operations 
    will not affect the availability of any of the required power 
    sources, nor the capability of the EDGs to perform their intended 
    safety function. Furthermore, performing the test when the 
    undervoltage protection of the 4160-V vital buses required by the 
    Salem Station Technical Specification 3.3.2.1 is operable, provides 
    for an added level of protection to the EDG that is not available 
    while shutdown.
        Therefore, the proposed change does not involve a significant 
    reduction in a margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
        Attorney for licensee: Jeffrie J. Keenan, Esquire, Nuclear Business 
    Unit--N21, P.O. Box 236, Hancocks Bridge, NJ 08038.
        NRC Section Chief: James W. Clifford.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: August 30, 1999 (TS 99-08).
        Brief description of amendments: The proposed amendments would 
    change the Sequoyah (SQN) Technical Specification (TS) requirements to 
    provide alternatives to the requirement of actually measuring response 
    times.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), Tennessee Valley 
    Authority (TVA), the licensee, has provided its analysis of the issue 
    of no significant hazards consideration, which is presented below:
    
        A. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        This change to the TS does not result in a condition where the 
    design, material, and construction standards that were applicable 
    prior to the change are altered. The same RTS [Reactor Trip System] 
    and engineered safety feature actuation system (ESFAS) 
    instrumentation is being used, the time response allocations/
    modeling assumptions in the [Final Safety Analysis Report] Chapter 
    15 analyses are still the same, only the method of verifying time 
    response is changed. The proposed change will not modify any system 
    interface and could not increase the likelihood of an accident since 
    these events are independent of this change. The proposed activity 
    will not change, degrade or prevent actions, or alter any 
    assumptions previously made in evaluating the radiological 
    consequences of an accident described in the Final Safety Analysis 
    Report. Therefore, the proposed amendment does not involve a 
    significant increase in the probability or consequences of an 
    accident previously evaluated.
        B. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        This change does not alter the performance of pressure [or] 
    differential pressure transmitters, solid state protection system 
    racks, nuclear instrumentation, or input and output master/slave 
    relays used in the plant protection systems. Applicable sensors, 
    solid state protection system (SSPS) racks, nuclear instrumentation, 
    and relays will still have response time verified by test prior to 
    placing the equipment in operational service and after any 
    maintenance that could affect the response time of that equipment. 
    Changing the method of periodically verifying instrument response 
    time for certain instruments from RTT [Response Time Test] to 
    calibration and channel checks or functional test will not create 
    any new accident initiators or scenarios. Therefore, the proposed 
    amendment does not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        C. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        This change does not affect the total system response time 
    assumed in the safety analysis. The periodic system response time 
    verification method for selected pressure and pressure differential 
    sensors and SSPS racks, nuclear instrumentation, or logic systems is 
    modified to allow use of actual test data or engineering data 
    (various Westinghouse WCAPs [topical reports]). The method of 
    verification still provides assurance that the total system response 
    time is within that assumed in the safety analysis, since 
    calibration checks and functional tests will detect any degradation 
    which might significantly affect equipment response time. Therefore, 
    the proposed license amendment request does not result in a 
    significant reduction in margin of safety.
    
    
    [[Page 54382]]
    
    
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 10H, Knoxville, Tennessee 37902.
        NRC Section Chief: Sheri R. Peterson.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: August 30, 1999 (TS 99-10).
        Brief description of amendments: The proposed amendments would 
    change the Sequoyah (SQN) Technical Specifications (TS) to provide 
    clarification to the requirements for containment isolation valves.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), Tennessee Valley 
    Authority (TVA), the licensee, has provided its analysis of the issue 
    of no significant hazards consideration, which is presented below:
    
        A. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed revisions enhance the technical specification (TS) 
    requirements to provide greater consistency with the standard TS in 
    NUREG-1431. This revision proposes changes to the requirements for 
    containment isolation valves in Specifications 3.6.3. A proposed 
    revision relocates a surveillance requirement (SR) from SQN TS 
    3.6.1.1, ``Containment Integrity'' to SQN TS 3.6.3, ``Containment 
    Isolation Valves.'' A proposed revision to TS 3.6.3, Action (a), a 
    new Action (b), and a proposed revision to SR 4.6.3.2 provide 
    improvements to the existing TS requirements. The proposed revisions 
    are not the result of changes to plant equipment, system design, 
    testing methods, or operating practices. The modified requirements 
    will allow some relaxation of current action requirements, and SRs. 
    These changes provide more appropriate requirements in consideration 
    of the safety significance and the design capabilities of the plant 
    as determined by the improved standard TS industry effort. SQN TS 
    3.6.3, ``Containment Isolation Valves,'' continues to provide 
    controls to ensure these valves isolate within the time limits 
    assumed in the safety analyses. Operability of these valves 
    continues to assure that the containment isolation function assumed 
    in the safety analyses is maintained. Since these proposed revisions 
    will continue to support the required safety functions without 
    modification of the plant features, the probability of an accident 
    is not increased.
        The provisions proposed in this change request will continue to 
    maintain an acceptable level of protection for the health and safety 
    of the public and will not significantly impact the potential for 
    the offsite release of radioactive products. The overall effect of 
    the proposed change will result in specifications that have 
    equivalent or improved requirements compared to existing 
    specifications for containment isolation valve operability and will 
    not significantly increase the consequences of an accident.
        B. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed revisions are not the result of changes to plant 
    equipment, system design, testing methods, or operating practices. 
    The modified requirements will allow some relaxation of current 
    action requirements, and a SR consistent with NUREG-1431. These 
    changes provide more appropriate requirements in consideration of 
    the safety significance and the design capabilities of SQN's 
    containment isolation system. The specifications for containment 
    isolation valves serve to provide controls for maintaining the 
    containment pressure boundary. TVA's proposed changes does not 
    contribute to the generation of postulated accidents. Since the 
    function of the containment isolation valves and their associated 
    systems remains unchanged, and the effects do not contribute to 
    accident generation, the proposed changes will not create the 
    possibility of a new or different kind of accident.
        C. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The proposed changes will not result in changes to system design 
    or setpoints that are intended to ensure timely identification of 
    plant conditions that could be precursors to accidents or potential 
    degradation of accident mitigation systems. Operability requirements 
    for SQN's containment isolation valves remain unchanged. TVA's 
    proposed revisions provide some relaxation and flexibility to 
    existing actions and a SR; however, the addition of a new action 
    requirement for a 31-day periodic verification of valve position 
    provides conservative administrative controls to ensure containment 
    isolation function is maintained. The action times are acceptable 
    considering the redundant features of containment penetration flow 
    paths and the allowed time intervals that have been developed by the 
    industry and NRC.
        TVA's revisions will continue to provide the necessary actions 
    to minimize the impact of inoperable containment isolation valves 
    and will provide testing activities that will ensure containment 
    isolation system operability. The setpoints and design features that 
    support the margin of safety are unchanged and actions for 
    inoperable systems continue to provide appropriate time limits and 
    compensatory measures. Accordingly, the proposed changes will not 
    significantly reduce the margin of safety.
    
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 10H, Knoxville, Tennessee 37902.
        NRC Section Chief: Sheri R. Peterson.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: August 30, 1999 (TS 99-11).
        Brief description of amendments: The proposed amendments would add 
    Sequoyah (SQN) Technical Specification (TS) 3.0.7 to address the use of 
    interim provisions upon discovery of unintended TS action.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), Tennessee Valley 
    Authority (TVA), the licensee, has provided its analysis of the issue 
    of no significant hazards consideration, which is presented below:
    
        A. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        TVA proposes the addition of a new definition and limiting 
    condition for operation (LCO) that will allow the interim correction 
    of erroneous TS requirements until NRC's review of an amendment 
    request is completed. This allowance will only apply to those errors 
    that are clearly in conflict with the intended purpose of the TS 
    requirement. The proposed revision will not alter any plant 
    equipment or operating practices or deviate from the intended 
    application of the TS requirements. Therefore, the probability of an 
    accident is not increased by this revision. Likewise, the 
    consequences of an accident is not increased because the proposed 
    allowance will maintain the underlying intent of the TS 
    requirements, the plant licensing basis, and plant nuclear safety.
        B. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed revision to the SQN TSs will not alter plant 
    equipment or operating practices. The intent of the TS requirements 
    will be maintained to ensure the assumed initial conditions for 
    accidents and the availability of mitigation systems in the event of 
    an postulated accident. The proposed addition will not promote 
    activities that have
    
    [[Page 54383]]
    
    the potential to generate accidents. Therefore, the proposed 
    revision will not create the possibility of an accident of a new or 
    different kind.
        C. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        TVA's proposed revision to add an allowance to correct erroneous 
    TS requirements will not alter plant systems or those setpoints and 
    limits that are use[d] to maintain safety functions. Any corrections 
    implemented in accordance with the proposed allowance will be 
    consistent with the underlying intent of the TSs. TVA will pursue 
    timely correction of such errors through the license amendment 
    process while temporarily utilizing the corrected requirement. This 
    will ensure that inadequate TS requirements are resolved with NRC in 
    an acceptable time interval. Implementation of the proposed revision 
    will enhance the ability to maintain the licensing basis and safety 
    features of the plant without the need for unnecessary unit 
    shutdowns or regulatory activities. Therefore, the proposed revision 
    maintains the plant safety features without the reduction of any 
    margin of safety.
    
        The NRC has reviewed the licensee's analysis and, based on this 
    review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET 10H, Knoxville, Tennessee 37902.
        NRC Section Chief: Sheri R. Peterson
    
    Union Electric Company, Docket No. 50-483, Callaway Plant, Unit 1, 
    Callaway County, Missouri
    
        Date of application request: September 8, 1999.
        Description of amendment request: The amendment will authorize 
    revisions to the Final Safety Analysis Report (FSAR) to reflect 
    increases in the radiological dose consequences in the Callaway FSAR 
    for the steam generator tube rupture (SGTR) and main steam line break 
    (MSLB) accidents.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
    
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        This change increases the offsite dose consequences for the MSLB 
    and SGTR accidents reported in FSAR Sections 15.1 and 15.6. Non-
    conservative assumptions regarding letdown flow rate, iodine 
    isotopic mix in the source term, resin effeciency, and termination 
    of the flash release pathway were identified in the SGTR and MSLB 
    radiological consequence analyses. The correction of these non-
    conservative assumptions results in an increase in the radiological 
    consequences reported in FSAR Tables 15.1-4 and 15.6-5. However, 
    these increases are not significant since the new values remain less 
    than the 10 CFR 100.11 regulatory requirements and the guideline 
    values provided by the Standard Review Plan [NUREG-0800].
        There will be no increase in the probability of previously 
    evaluated accidents. This change only involves the modeling and 
    calculation of the SGTR and MSLB radiological consequences. [There 
    are no equipment or system changes.] Protection system performance 
    will remain within the assumptions of the previously performed 
    accident analyses since no hardware changes are proposed. The 
    protection systems will continue to function in a manner consistent 
    with the plant design basis. The proposed change will not affect the 
    probability of any event initiators nor will the proposed change 
    affect the ability of any safety-related equipment to perform its 
    intended function. There will be no degradation in the performance 
    of, nor an increase in the number of challenges imposed on, safety-
    related equipment assumed to function during an accident situation. 
    There will be no change to normal plant operating parameters or 
    accident mitigation performance.
        Therefore, the proposed change does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. The proposed change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        This change is the result of a re-analysis of the MSLB and SGTR 
    radiological consequences. These accidents were previously analyzed 
    in the FSAR. None of the changes in the dose calculation modeling 
    create the possibility of a new or different kind of accident.
        There are no hardware changes associated with this amendment 
    application nor are there any changes in the method by which any 
    safety-related plant system performs its safety function. The change 
    will not affect the normal method of plant operation, other than the 
    imposition of administrative limits on the concentrations of I-134 
    [Iodine-134] and Dose Equivalent I-131 until this amendment 
    application is approved by NRC. No new accident scenarios, transient 
    precursors, failure mechanisms, or limiting single failures are 
    introduced as a result of this change. There will be no adverse 
    effect or challenges imposed on any safety-related system as a 
    result of this change.
        Therefore, the proposed change does not create the possibility 
    of a new or different kind of accident from any previously 
    evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The re-analysis of the MSLB and SGTR radiological consequences, 
    and the resultant increase in consequences reported in FSAR Tables 
    15.1-4 and 15.6-5, ensures that the accident analyses support the 
    plant operating conditions allowed by current Technical 
    Specification 3.4.8, Reactor Coolant System Specific Activity (ITS 
    [Improved Technical Specification] 3.4.16), and current Technical 
    Specification 3.7.1.4, Plant Systems Specific Activity (ITS 3.7.18).
        The proposed change does not affect the acceptance criteria for 
    any analyzed event nor is there a change to any Safety Analysis 
    Limit (SAL). There will be no effect on the manner in which safety 
    limits or limiting safety system settings are determined nor will 
    there be any effect on those plant systems necessary to assure the 
    accomplishment of protection functions. There will be no impact on 
    the overpower limit, DNBR [departure from nucleate boiling ratio], 
    FQ [heat flux hot channel factor], FdeltaH [nuclear 
    enthalpy rise hot channel factor], LOCA PCT [peak cladding 
    temperature for the loss-of-coolant accident], peak local power 
    density, or any other margin of safety. The radiological dose 
    consequence acceptance criteria listed in the Standard Review Plan 
    continue to be met.
        Therefore, the proposed change does not involve a significant 
    reduction in any margin of safety.
    
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Elmer Ellis Library, 
    University of Missouri, Columbia Missouri 65201.
        Attorney for licensee: John O'Neill, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW, Washington, DC 20037.
        NRC Section Chief: Stephen Dembek.
    
    Previously Published Notices of Consideration of Issuance of 
    Amendments to Facility Operating Licenses, Proposed no Significant 
    Hazards Consideration Determination, and Opportunity for a Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and
    
    [[Page 54384]]
    
    page cited. This notice does not extend the notice period of the 
    original notice.
    
    Indiana Michigan Power Company, Docket Nos. 50-315 and 50-316, Donald 
    C. Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan
    
        Date of amendment requests: September 14, 1998.
        Description of amendment requests: The proposed amendments would 
    change the runout limits for a safety injection (SI) pump to 675 
    gallons per minute (gpm), unless the pump is specifically tested to a 
    higher flow rate, not exceeding 700 gpm for both Units 1 and 2. This 
    change was initiated upon reevaluation of correspondence from 
    Westinghouse sent to the licensee in 1991, which indicated that the 
    generic runout limits for Pacific 2'' JTCH pumps was 675 gpm unless 
    each specific pump is tested to a higher flow rate. Individual testing 
    is necessary due to test variations between pumps which may limit the 
    applicability of testing of one pump to another pump due to 
    manufacturing tolerances in the sand cast impellers and material 
    changes in the pump casing.
        Furthermore, the bases section is being clarified to describe why 
    the injection rather than the recirculation mode during flow balancing 
    is the minimum resistance and, consequently, more conservative 
    configuration for runout considerations.
        Date of publication of individual notice in Federal Register: 
    August 31, 1999 (64 FR 47533).
        Expiration date of individual notice: September 30, 1999
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085.
        Date of publication of individual notice in Federal Register: 
    August 31, 1999 (64 FR 47533).
        Expiration date of individual notice: September 30, 1999.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085.
    
    Michigan Power Company, Docket, Nos. 50-315 and 50-316, Donald C. Cook 
    Nuclear Plant, Units 1 and 2, Berrien County, Michigan
    
        Date of application for amendments: October 8, 1998.
        Brief description of amendments: The amendments would revise 
    Technical Specification (TS) 3.3.3.8 for Unit 1 and TS 3.3.3.6 for Unit 
    2, ``Post-Accident Instrumentation.'' The proposed changes to the TSs 
    will place tighter restrictions on the amount of time the refueling 
    water storage tank (RWST) water level instrumentation may be inoperable 
    before the limiting conditions for operation in the TSs are applied.
        Date of publication of individual notice in Federal Register: 
    August 31, 1999 (64 FR 47532).
        Expiration date of individual notice: September 30, 1999.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085.
    
    Indiana Michigan Power Company, Docket, Nos. 50-315 and 50-316, Donald 
    C. Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan
    
        Date of application for amendments: December 3, 1998.
        Brief description of amendments: The amendments would make 
    administrative changes to several Technical Specifications to remove 
    obsolete information, provide consistency between Unit 1 and Unit 2, 
    provide consistency with the Standard Technical Specifications, provide 
    clarification, and correct typographical errors.
        Date of publication of individual notice in Federal Register: 
    August 31, 1999 (64 FR 47535).
        Expiration date of individual notice: September 30, 1999.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085.
    
    Indiana Michigan Power Company, Docket, Nos. 50-315 and 50-316, Donald 
    C. Cook Nuclear Plant, Units 1 and 2, Berrien County, Michigan
    
        Date of application for amendments: May 21, 1999.
        Brief description of amendments: The amendments would change the 
    Technical Specifications (T/S) to allow reactor coolant system 
    temperature changes in certain Mode 5 and 6 action statements if the 
    shutdown margin is sufficient to accommodate the expected temperature 
    change. In addition, footnotes regarding additions of water from the 
    refueling water storage tank to the reactor coolant system are 
    clarified and relocated to action statements. Additional actions are 
    added in Table 3.3-1, ``Reactor Trip System Instrumentation,'' when the 
    required source range neutron flux channel is inoperable. Corresponding 
    changes are proposed for the bases for T/S 3/4.1.1, ``Boration 
    Control,'' and T/S 3/4.1.2, ``Boration Systems.'' Administrative 
    changes are proposed to improve clarity. Finally, additions are made to 
    shutdown margin T/S surveillance requirements to address use of a boron 
    penalty (requirement for additional boron) during residual heat removal 
    system operation in Modes 4 and 5.
        Date of publication of individual notice in Federal Register: July 
    12, 1999 (64 FR 37574).
        Expiration date of individual notice: August 11, 1999.
        Local Public Document Room location: Maud Preston Palenske Memorial 
    Library, 500 Market Street, St. Joseph, MI 49085.
    
    Notice of Issuance of Amendments to Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    [[Page 54385]]
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of application for amendment: September 23, 1998, as 
    supplemented on December 7, 1998, and August 10, 1999.
        Brief description of amendment: This amendment revises Technical 
    Specification (TS) 3/4.6.1.3, ``Containment Air Locks,'' and its 
    associated bases, to clarify the requirements for locking an air lock 
    door shut and to make it consistent with NUREG-1431, Revision 1, 
    ``Standard Technical Specifications, Westinghouse Plants,'' dated April 
    1995.
        Date of issuance: September 14, 1999.
        Effective date: September 14, 1999.
        Amendment No.: 90.
        Facility Operating License No. NPF-63. Amendment revises the 
    Technical Specifications
        Date of initial notice in Federal Register: October 21, 1998 (63 FR 
    56239)
        The December 7, 1998, and August 10, 1999, submittals contained 
    clarifying information only, and did not change the initial no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 14, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, North 
    Carolina
    
        Date of application for amendment: June 15, 1999.
        Brief description of amendment: This amendment changes the 
    Technical Specifications to incorporate the performance-based 10 CFR 50 
    Appendix J, Option B for Type A tests (containment integrated leakage 
    rate tests). Option B will be implemented for Type A testing in 
    accordance with NRC Regulatory Guide 1.163, ``Performance-Based 
    Containment Leak-Test Program,'' dated September 1995, and Nuclear 
    Energy Institute (NEI) Guideline 94-01, Revision 0, ``Industry 
    Guideline for Implementing Performance-Based Option of 10 CFR Part 50, 
    Appendix J,'' dated July 26, 1995. Type B and C testing (containment 
    penetration leakage tests) will continue to be performed in accordance 
    with 10 CFR 50 Appendix J, Option A.
        Date of issuance: September 17, 1999.
        Effective date: September 17, 1999.
        Amendment No.: 91.
        Facility Operating License No. NPF-63. Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 14, 1999 (64 FR 
    38023). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 17, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Commonwealth Edison Company, Docket Nos. STN 50-456 and STN 50-457, 
    Braidwood Station, Unit Nos. 1 and 2, Will County, Illinois
    
        Date of application for amendments: July 30, 1999.
        Brief description of amendments: The amendments changed the maximum 
    allowable temperature of the ultimate heat sink in the technical 
    specifications from 98 degrees Fahrenheit to 100 degrees Fahrenheit. 
    The change is in effect from the date of this amendment until September 
    30, 1999.
        Date of issuance: September 8, 1999.
        Effective date: Immediately, to be implemented within 30 days.
        Amendment Nos.: 103 and 103.
        Facility Operating License Nos. NPF-72 and NPF-77: The amendments 
    revised the Technical Specifications.
        Public comments requested as to proposed no significant hazards 
    consideration: Yes (64 FR 44962 dated August 18, 1999). The notice 
    provided an opportunity to submit comments on the Commission's proposed 
    no significant hazards consideration determination. No comments have 
    been received. The notice also provided for an opportunity to request a 
    hearing by September 17, 1999, but indicated that if the Commission 
    makes a final no significant hazards consideration determination any 
    such hearing would take place after issuance of the amendments. The 
    Commission's related evaluation of the amendments, finding of exigent 
    circumstances and final no significant hazards consideration 
    determination are contained in a Safety Evaluation dated September 8, 
    1999.
        Local Public Document Room location: Wilmington Public Library, 201 
    S. Kankakee Street, Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois
    
        Date of application for amendments: May 3, 1999, as supplemented by 
    letter dated September 10, 1999.
        Brief description of amendments: The amendments relocated the 
    requirements of Technical Specification (TS) Section 3/4.6.I to the 
    Updated Final Safety Analysis Report (UFSAR). TS Section 
    3/4.6.I contains reactor coolant chemistry limiting conditions for 
    operation (LCO) and surveillance requirements (SR) for conductivity, 
    chloride concentration, and pH.
        Date of issuance: September 23, 1999.
        Effective date: Immediately, to be implemented within 30 days 
    including relocation of the removed TSs and associated bases to the 
    licensee's UFSAR pending change file. In addition, the licensee shall 
    include the relocated information in the UFSAR submitted to the NRC, 
    pursuant to 10 CFR 50.71(e), except for any information that has been 
    changed in accordance with 10 CFR 50.59 and described in the change 
    summaries submitted to NRC pursuant to 10 CFR 50.59.
        Amendment Nos.: 173 & 169.
        Facility Operating License Nos. DPR-19 and DPR-25: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 11, 1999 (64 FR 
    43768). The September 10, 1999, submittal provided additional 
    clarifying information that did not change the initial proposed no 
    significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 23, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Morris Area Public Library 
    District, 604 Liberty Street, Morris, Illinois 60450.
    
    Commonwealth Edison Company, Docket Nos. 50-254 and 50-265, Quad Cities 
    Nuclear Power Station, Units 1 and 2, Rock Island County, Illinois
    
        Date of application for amendments: June 29, 1999.
        Brief description of amendments: The amendments increased the notch 
    testing surveillance interval of partially withdrawn control rods in 
    Technical Specification Surveillance Requirement 3/4.3.C, ``Reactivity 
    Control--Control Rod Operability,'' from an interval of once in 7 days 
    to once in 31 days.
        Date of issuance: September 23, 1999.
    
    [[Page 54386]]
    
        Effective date: Immediately, to be implemented within 60 days.
        Amendment Nos.: 190 & 187.
        Facility Operating License Nos. DPR-29 and DPR-30: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 28, 1999 (64 FR 
    40905).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 23, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Dixon Public Library, 221 
    Hennepin Avenue, Dixon, Illinois 61021.
    
    Duke Energy Corporation, Docket Nos. 50-269, 50-270, and 50-287, Oconee 
    Nuclear Station, Units 1, 2, and 3, Oconee County, South Carolina
    
        Date of application of amendments: May 24, 1999
        Brief description of amendments: The amendments revise the maximum 
    local fuel pin centerline temperature safety limit in Technical 
    Specification 2.1.1.1 from the limit determined using the TACO2 fuel 
    performance computer code to the value determined using a newer TACO3 
    computer code.
        Date of Issuance: September 24, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days from the date of issuance.
        Amendment Nos.: Unit 1--306, Unit 2--306, Unit 3--306.
        Facility Operating License Nos. DPR-38, DPR-47, and DPR-55: 
    Amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: June 30, 1999 (64 FR 
    35203).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 24, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina.
    
    Duke Energy Corporation, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina.
    
        Date of application for amendments: July 22, 1998, and supplemented 
    by letters dated October 22, 1998, January 28, May 6, June 24, August 
    17 and September 15, 1999.
        Brief description of amendments: The amendments revise various 
    sections of the Technical Specifications (Appendix A of the Catawba 
    operating licenses) to permit use of Westinghouse's Robust Fuel 
    Assemblies for future core reloads.
        Date of issuance: September 22, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    prior to beginning the installation of the Westinghouse fuel, currently 
    projected to be Fuel Cycle 13 and 11 for Units 1 and 2, respectively.
        Amendment Nos.: Unit 1--180; Unit 2--172.
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 18, 1998 (63 
    FR 64108); May 19, 1999 (64 FR 27317); August 11, 1999 (64 FR 43770) 
    The Commission's related evaluation of the amendments is contained in a 
    Safety Evaluation dated September 22, 1999.
        No significant hazards consideration comments received: No
        Local Public Document Room location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina.
    
    Duke Energy Corporation, et al., Docket Nos. 50-369 and 50-370, McGuire 
    Nuclear Station, Units 1 and 2, Mecklenberg County, North Carolina
    
        Date of application for amendments: July 22, 1998, and supplemented 
    by letters dated October 22, 1998, and January 28, May 6, June 24, 
    August 17 and September 15, 1999
        Brief description of amendments: The amendments revise various 
    sections of the Technical Specifications (Appendix A of the McGuire 
    operating licenses) to permit use of Westinghouse's Robust Fuel 
    Assemblies for future core reloads.
        Date of issuance: September 22, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    prior to beginning the installation of the Westinghouse fuel, currently 
    projected to be Fuel Cycle 15 and 14 for Units 1 and 2, respectively.
        Amendment Nos.: Unit 1--188; Unit 2--169.
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 11, 1999 (64 FR 
    43771); June 30, 1999 (64 FR 35202); December 16, 1998 (64 FR 69388)
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 22, 1999.
        No significant hazards consideration comments received: No
        Local Public Document Room location: J. Murrey Atkins Library, 
    University of North Carolina at Charlotte, 9201 University City 
    Boulevard, Charlotte, North Carolina
    
    Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear One, Unit 
    No. 1, Pope County, Arkansas
    
        Date of amendment request: April 9, 1999, as supplemented by letter 
    dated July 29, 1999
        Brief description of amendment: The amendment revises the 
    requirements associated with the station batteries and the direct 
    current (DC) sources to the 125 volt DC switchyard distribution system.
        Date of issuance: September 14, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 45 days from the date of issuance (including issuance of the 
    Technical Requirements Manual for use by licensee personnel).
        Amendment No.: 200.
        Facility Operating License No. DPR-51: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 19, 1999 (64 FR 
    27321).
        The July 29, 1999, letter provided clarifying and additional 
    information that did not change the initial proposed no significant 
    hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 14, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, Arkansas 72801.
    
    Entergy Operations, Inc., Docket No. 50-313, Arkansas Nuclear One, Unit 
    No. 1, Pope County, Arkansas
    
        Date of amendment request: June 1, 1999, as supplemented by letters 
    dated July 29 and August 19, 1999.
        Brief description of amendment: The amendment revised the Technical 
    Specifications to allow, under specific conditions, certain once-
    through steam generator (OTSG) tubes with tube end crack indications 
    adjacent to the primary cladding region of the upper and lower OTSG 
    tubesheets to remain in service.
        Date of issuance: September 14, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    prior to reactor startup after refueling outage 1R15.
        Amendment No.: 201.
        Facility Operating License No. DPR-51: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 30, 1999 (64 FR 
    35205).
        The July 29 and August 19, 1999, letters provided clarifying 
    information
    
    [[Page 54387]]
    
    that did not change the scope of the June 1, 1999, application and the 
    initial proposed no significant hazards consideration determination.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 14, 1999.
        No significant hazards consideration comments received: No
        Local Public Document Room location: Tomlinson Library, Arkansas 
    Tech University, Russellville, Arkansas 72801.
    
    Florida Power Corporation, et al., Docket No. 50-302, Crystal River 
    Nuclear Generating Plant, Unit 3, Citrus County, Florida
    
        Date of application for amendment: May 17, 1999.
        Brief description of amendment: The amendment changes Technical 
    Specification Section 3.3.8, ``Emergency Diesel Generator Loss of Power 
    Start,'' Surveillance Requirement 3.3.8.1 and corresponding basis 
    section. The surveillance is revised to make a note included in the 
    surveillance consistent with the method of performing the surveillance.
        Date of issuance: September 13, 1999.
        Effective date: September 13, 1999.
        Amendment No.: 187.
        Facility Operating License No. DPR-72: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 14, 1999 (64 FR 
    38026).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 13, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Coastal Region Library, 8619 
    W. Crystal Street, Crystal River, Florida 34428.
    
    GPU Nuclear, Inc. et al., Docket No. 50-219, Oyster Creek Nuclear 
    Generating Station, Ocean County, New Jersey
    
        Date of application for amendment: December 23, 1998.
        Brief description of amendment: The proposed amendment revised the 
    surveillance frequency for verifying the operability of motor-operated 
    isolation valves and condensate makeup valves in the Isolation 
    Condenser Technical Specification 4.8.A.1 and Bases page from once per 
    month to once per 3 months.
        Date of Issuance: September 24, 1999.
        Effective date: Date of issuance and shall be implemented within 30 
    days of issuance.
        Amendment No.: 209.
        Facility Operating License No. DPR-16: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 7, 1999 (64 FR 
    17026).
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated September 24, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Ocean County Library, 
    Reference Department, 101 Washington Street, Toms River, NJ 08753.
    
    GPU Nuclear, Inc., et al., Docket No. 50-289, Three Mile Island Nuclear 
    Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of application for amendment: October 19, 1998, as 
    supplemented August 19, 1999.
        Brief description of amendment: The proposed amendment adds 
    operability and surveillance requirements to the Technical 
    Specifications for the remote shutdown system similar to the standard 
    technical specifications for Babcock & Wilcox nuclear plants as 
    described in NUREG-1430.
        Date of issuance: September 22, 1999.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 216.
        Facility Operating License No. DPR-50. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 18, 1998 (63 
    FR 64118). The August 19, 1999, supplement to the application did not 
    change the staff's proposed no significant hazards consideration 
    determination or expand the scope of the application as originally 
    noticed.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 22, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Law/Government Publications 
    Section, State Library of Pennsylvania, (Regional Depository) Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105.
    
    IES Utilities Inc., Docket No. 50-331, Duane Arnold Energy Center, Linn 
    County, Iowa
    
        Date of application for amendment: April 30, 1999.
        Brief description of amendment: The amendment revises Duane Arnold 
    Energy Center (DAEC) Technical Specification (TS) Surveillance 
    Requirement (SR) 3.4.3.1 to revise the safety function lift setpoint 
    tolerance limits for the main safety valves (SVs) and the safety/relief 
    valves (SRVs).
        Date of issuance: September 22, 1999.
        Effective date: September 22, 1999, to be implemented within 30 
    days.
        Amendment No.: 228.
        Facility Operating License No. DPR-49: The amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 14, 1999 (64 FR 
    38028).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 22, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Cedar Rapids Public Library, 
    500 First Street, SE., Cedar Rapids, IA 52401.
    
    Niagara Mohawk Power Corporation, Docket No. 50-220, Nine Mile Point 
    Nuclear Station Unit No. 1, Oswego County, New York
    
        Date of application for amendment: May 15, 1998, as supplemented by 
    letters dated September 25, October 13, December 9 (two letters), 1998; 
    January 11, April 1, and April 22, 1999.
        Brief description of amendment: This amendment changes Technical 
    Specification (TS) 5.5, ``Storage of Unirradiated and Spent Fuel,'' to 
    reflect a planned modification to increase the storage capacity of the 
    spent fuel pool from 2776 to 4086 fuel assemblies. It also deletes an 
    inappropriate statement and reference within TS 5.5.
        Date of issuance: June 17, 1999.
        Effective date: This license amendment is effective as of the date 
    of its issuance to be implemented before spent fuel is stored within 
    the new high-density spent fuel rack modules authorized for 
    installation and use by this amendment.
        Amendment No.: 167.
        Facility Operating License No. DPR-63: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: November 24, 1998 (63 
    FR 64973).
        The September 25, October 13, December 9 (two letters) 1998, 
    January 11, April 1, and April 22, 1999, letters provided clarifying 
    information that did not change the initial proposed no significant 
    hazards consideration.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated June 17, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents
    
    [[Page 54388]]
    
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    North Atlantic Energy Service Corporation, et al., Docket No. 50-443, 
    Seabrook Station, Unit No. 1, Rockingham County, New Hampshire
    
        Date of amendment request: June 23, 1999.
        Description of amendment request: To revise Technical Specification 
    (TS) 3.7.6.2 to increase the allowable outage time for the Control Room 
    Air Conditioning Subsystem from 30 days to 60 days, on a one-time basis 
    for each train, to allow adequate time to replace portions of the 
    existing system during the current operating cycle, and to exclude the 
    requirements of TS 3.0.4 and TS 4.0.4 during the implementation of the 
    modification.
        Date of issuance: September 17, 1999.
        Effective date: As of its date of issuance, and shall be 
    implemented within 30 days.
        Amendment No.: 62.
        Facility Operating License No. NPF-86: Amendment revised the 
    Technical Specifications/License.
        Date of initial notice in Federal Register: July 14, 1999 (64 FR 
    38032).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 17, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Exeter Public Library, 
    Founders Park, Exeter, NH 03833.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-336, Millstone 
    Nuclear Power Station, Unit No. 2, New London County, Connecticut
    
        Date of application for amendment: March 17, 1999.
        Brief description of amendment: The amendment changes Technical 
    Specifications 3.5.2, ``Emergency Core Cooling Systems--ECCS 
    Subsystems--Tavg 300  deg.F;'' 3.7.1.7, ``Plant Systems--
    Atmospheric Steam Dump Valves;'' and 3.7.6.1, ``Plant Systems--Control 
    Room Emergency Ventilation System.'' The changes will revise: (1) 
    Surveillance requirements for the Emergency Core Cooling System valves, 
    (2) the atmospheric steam dump valve requirements to focus on the steam 
    release path instead of the individual valves, and (3) the allowed 
    outage time for the atmospheric steam valves and Control Room Emergency 
    Ventilation System. The licensee made changes to the Bases pages 
    consistent with the proposed changes to the TSs.
        Date of issuance: August 12, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 60 days from the date of issuance.
        Amendment No.: 238.
        Facility Operating License No. DPR-65: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 21, 1999 (64 FR 
    19559).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated August 12, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, Connecticut, and the Waterford Library, ATTN: Vince Juliano, 
    49 Rope Ferry Road, Waterford, Connecticut.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: June 4, 1999.
        Brief description of amendment: The amendment makes administrative 
    changes to the Technical Specifications.
        Date of issuance: September 14, 1999.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 193.
        Facility Operating License No. DPR-64: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 28, 1999 (64 FR 
    40906).
        No significant hazards consideration comments received: No.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 14, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: January 28, 1999, as 
    supplemented April 29, 1999, and May 17, 1999. By letters dated April 
    29, 1999, and May 17, 1999, the licensee revised the original submittal 
    dated January 28, 1999, in response to questions raised by the NRC 
    staff.
        Brief description of amendment: The amendment changes the Technical 
    Specifications by reducing the number of emergency diesel generators 
    required to be operable under certain conditions.
        Date of issuance: September 14, 1999.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 194.
        Facility Operating License No. DPR-64: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 2, 1999 (64 FR 
    29713). This notice superceded a notice dated April 21, 1999 (64 FR 
    19563).
        No significant hazards consideration comments received: No.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 14, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    Point Nuclear Generating Unit No. 3, Westchester County, New York
    
        Date of application for amendment: January 28, 1999, as 
    supplemented July 16, 1999.
        Brief description of amendment: The amendment removes lists of 
    containment isolation valves from the Technical Specifications (TSs) 
    and modifies the TSs accordingly.
        Date of issuance: September 16, 1999.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 195.
        Facility Operating License No. DPR-64: Amendment revises the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 19, 1999 (64 FR 
    27323).
        The July 16, 1999, submittal did not change the staff's initial 
    proposed finding of no significant hazards considerations.
        No significant hazards consideration comments received: No.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 16, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10610.
    
    [[Page 54389]]
    
    Power Authority of the State of New York, Docket No. 50-333, James A. 
    FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: April 5, 1999.
        Brief description of amendment: The proposed changes would revise 
    Appendix A (Section 6.1) and Appendix B (Section 7.1) of the James A. 
    FitzPatrick Technical Specifications. The proposed changes would remove 
    the position title of General Manager from these sections and would 
    state that if the Site Executive Officer is unavailable, he will 
    delegate his responsibilities to another staff member, in writing. In 
    addition the position title of Resident Manager, used in Appendix B, 
    Section 7.1, would be replaced by Site Executive Officer.
        Date of issuance: September 13, 1999.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 254.
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications and the Environmental Technical 
    Specifications.
        Date of initial notice in Federal Register: August 11, 1999 (64 FR 
    43775).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 13, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Power Authority of the State of New York, Docket No. 50-333, James A. 
    FitzPatrick Nuclear Power Plant, Oswego County, New York
    
        Date of application for amendment: October 8, 1997.
        Brief description of amendment: The amendment revises actions in 
    the Technical Specifications to be taken in the event multiple control 
    rods are inoperable.
        Date of issuance: September 21, 1999.
        Effective date: As of the date of issuance to be implemented within 
    30 days.
        Amendment No.: 255.
        Facility Operating License No. DPR-59: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: February 11, 1998 (63 
    FR 6991).
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 21, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Reference and Documents 
    Department, Penfield Library, State University of New York, Oswego, New 
    York 13126.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of application for amendment: December 30, 1998, as 
    supplemented September 13, 1999.
        Brief description of amendment: This amendment revises Technical 
    Specification (TS) Limiting Condition for Operation 3.7.3 and TS Table 
    3.7.3-1. These changes modify the flood protection actions required 
    when severe storm warnings that may affect the site are in effect or 
    during periods of elevated river water level.
        Date of issuance: September 17, 1999.
        Effective date: As of the date of issuance, and shall be 
    implemented within 60 days.
        Amendment No.: 122.
        Facility Operating License No. NPF-57: This amendment revised the 
    TSs.
        Date of initial notice in Federal Register: February 24, 1999 (64 
    FR 9200).
        The September 13, 1999, supplement provided clarifying information 
    that did not change the initial proposed no significant hazards 
    determination or expand the scope of the initial Federal Register 
    notice.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 17, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope Creek 
    Generating Station, Salem County, New Jersey
    
        Date of application for amendment: May 24, 1999, as supplemented 
    June 21, 1999.
        Brief description of amendment: This amendment revises the 
    Technical Specifications (TSs) to correct typographical and editorial 
    errors, and is considered administrative in nature.
        Date of issuance: September 21, 1999
        Effective date: As of the date of issuance, and shall be 
    implemented within 60 days.
        Amendment No.: 123.
        Facility Operating License No. NPF-57: This amendment revised the 
    TSs.
        Date of initial notice in Federal Register: June 30, 1999 (64 FR 
    35209).
        The June 21, 1999, supplement provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination or expand the scope of the original Federal 
    Register notice.
        The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated September 21, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, NJ 08070
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-311, 
    Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem County, New 
    Jersey
    
        Date of application for amendments: July 2, 1999.
        Brief description of amendments: The amendments delete TS 3/4.3.4, 
    ``Instrumentation--Turbine Overspeed Protection,'' and its associated 
    Bases and relocate the requirements to the licensee-controlled Updated 
    Final Safety Analysis Report.
        Date of issuance: September 14, 1999
        Effective date: As of the date of issuance and shall be implemented 
    within 60 days.
        Amendment Nos.: 224 and 205.
        Facility Operating License Nos. DPR-70 and DPR-75: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: August 11, 1999 (64 FR 
    43776).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 14, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Salem Free Public Library, 112 
    West Broadway, Salem, NJ 08079.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Units 2 and 3, San Diego 
    County, California
    
        Date of application for amendments: December 31, 1998 (PCN-501), as 
    supplemented June 14, 1999.
        Brief description of amendments: The amendments consist of changes 
    to Technical Specification 3.3.5, ``Engineered Safety Features 
    Actuation System (ESFAS) Instrumentation,'' and will include 
    restrictions on operation with a channel of the refueling water storage 
    tank level--low input to the recirculation actuation signal and the 
    steam generator pressure--low input or
    
    [[Page 54390]]
    
    steam generator pressure difference--high input to the emergency 
    feedwater actuation signal in the tripped condition.
        Date of issuance: September 7, 1999.
        Effective date: September 7, 1999, to be implemented within 30 days 
    of issuance.
        Amendment Nos.: Unit 2--157; Unit 3--148.
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 28, 1999 (64 FR 
    40907).
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 7, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 50-
    362, San Onofre Nuclear Generating Station, Units 2 and 3, San Diego 
    County, California
    
        Date of application for amendments: June 18, 1997 (PCN-478), as 
    supplemented May 24 and August 10, 1999.
        Brief description of amendments: The amendments modify the 
    Technical Specification surveillance requirements related to diesel 
    generator testing to more clearly reflect safety analysis and testing 
    conditions as it is performed.
        Date of issuance: September 9, 1999.
        Effective date: September 9, 1999, to be implemented within 30 days 
    of issuance.
        Amendment Nos.: Unit 2--158; Unit 3--149.
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 31, 1997 (62 
    FR 68315) The licensee's letters dated May 24 and August 10, 1999, 
    provided updated Technical Specification pages, clarifications, and 
    additional information that were within the scope of the original 
    Federal Register notice and did not change the staff's initial proposed 
    no significant hazards consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 9, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room Location: Main Library, University of 
    California, P.O. Box 19557, Irvine, California 92713.
    
    STP Nuclear Operating Company, Docket Nos. 50-498 and 50-499, South 
    Texas Project, Units 1 and 2, Matagorda County, Texas
    
        Date of amendment request: June 7, 1999.
        Brief description of amendments: The amendments revised Technical 
    Specification (TS) 2.2.1, ``Reactor Trip System (RTS) Instrumentation 
    Setpoints,'' and TS 3.3.2, ``Engineered Safety Features Actuation 
    System (ESFAS) Instrumentation,'' and the associated Bases, by removing 
    the Total Allowance, Sensor Error, and Z terms (Z is the statistical 
    summation of errors excluding sensor and rack drift) from the RTS and 
    ESFAS Instrumentation Trip Setpoints Tables. This replaces the five-
    column methodology with a two-column methodology that consists of the 
    trip setpoint and allowable value columns.
        Date of issuance: September 13, 1999.
        Effective date: September 13, 1999, to be implemented within 30 
    days.
        Amendment Nos.: Unit 1--116; Unit 2--104.
        Facility Operating License Nos. NPF-76 and NPF-80: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 30, 1999 (64 FR 
    35211) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated September 13, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, Texas 77488.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: June 24, 1999 (TS 99-06).
        Brief description of amendments: The amendments revise the Sequoyah 
    Nuclear Plant Technical Specifications (TS) by adding a footnote to 
    allow use of an installed spare electrical inverter, if needed.
        Date of issuance: September 23, 1999.
        Effective date: As of the date of issuance to be implemented no 
    later than 45 days after issuance.
        Amendment Nos.: 246 and 237.
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the TS.
        Date of initial notice in Federal Register: August 2, 1999 (64 FR 
    41973) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated September 23, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Chattanooga-Hamilton County 
    Library, 1001 Broad Street, Chattanooga, Tennessee 37402.
    
    TXU Electric, Docket Nos. 50-445 and 50-446, Comanche Peak Steam 
    Electric Station, Unit Nos. 1 and 2, Somervell County, Texas
    
        Date of amendment request: June 23, 1999, as supplemented by letter 
    dated August 4, 1999.
        Brief description of amendments: The amendments revise Surveillance 
    Requirement 3.8.1.13, ``AC Sources--Operating'' to clarify that each 
    emergency diesel generator automatic noncritical trip, except for 
    engine overspeed and generator differential current, is bypassed on 
    either a loss-of-offsite power or a safety injection actuation signal.
        Date of issuance: September 21, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days from the date of issuance.
        Amendment Nos.: 69 and 69.
        Facility Operating License Nos. NPF-87 and NPF-89: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: July 14, 1999 (64 FR 
    38037) The August 4, 1999, letter provided additional and clarifying 
    information that did not change the scope of the June 23, 1999, 
    application and the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 21, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas 76019.
    
    TXU Electric, Docket Nos. 50-445 and 50-446, Comanche Peak Steam 
    Electric Station, Unit Nos. 1 and 2, Somervell County, Texas
    
        Date of amendment request: February 12, 1999, as supplemented by 
    letter dated June 14, 1999
        Brief description of amendments: The amendments change Technical 
    Specification (TS) 3.4.13, ``RCS [Reactor Coolant System] Operational 
    Leakage,'' TS 5.5.9, ``Steam Generator (SG) Tube Surveillance 
    Program,'' and TS 5.6.10,
    
    [[Page 54391]]
    
    ``Steam Generator Tube Inspection Report,'' to implement the 1.0 Volt 
    Steam Generator Tube Repair Criteria for CPSES, Unit 1.
        Date of issuance: September 22, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days from the date of issuance.
        Amendment Nos.: Unit 1--Amendment No. 70; Amendment No. 70.
        Facility Operating License Nos. NPF-87 and NPF-89: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 5, 1999 (64 FR 
    24202) The June 14, 1999, supplement provided clarifying information 
    that did not change the scope of the February 12, 1999, application and 
    the initial proposed no significant hazards consideration 
    determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 22, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas 76019.
    
    TXU Electric, Docket Nos. 50-445 and 50-446, Comanche Peak Steam 
    Electric Station, Unit Nos. 1 and 2, Somervell County, Texas
    
        Date of amendment request: October 2, 1998, as supplemented by 
    letters dated July 27 and August 26, 1999.
        Brief description of amendments: The amendments revise Technical 
    Specfications for CPSES, Unit 1, to define the F* steam generator tube 
    plugging criteria in TS 5.5.9, ``Steam Generator (SG) Tube Surveillance 
    Program,'' and associated reporting requirements in TS 5.6.10, ``Steam 
    Generator Inspection Report.''
        Date of issuance: September 22, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    within 30 days from the date of issuance.
        Amendment Nos.: Unit 1--Amendment No. 71; Unit 2--Amendment No. 71.
        Facility Operating License Nos. NPF-87 and NPF-89: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 4, 1998 (63 FR 
    59597). The July 27 and August 26, 1999, letters provided clarifying 
    information that did not change the scope of the October 2, 1998, 
    application and the initial proposed no significant hazards 
    consideration determination.
        The Commission's related evaluation of the amendments is contained 
    in a Safety Evaluation dated September 22, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: University of Texas at 
    Arlington Library, Government Publications/Maps, 702 College, P.O. Box 
    19497, Arlington, Texas 76019.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: May 5, 1999.
        Brief description of amendment: The amendment revises the technical 
    specifications (TSs) to enhance the limiting conditions for operation 
    and surveillance requirements relating to the standby liquid control 
    system and to incorporate certain provisions of NRC's rule on 
    anticipated transients without scram. The change involves the use of 
    enriched boron in the standby liquid control system and improves upon 
    other aspects of the TSs for this system.
        Date of Issuance: September 17, 1999.
        Effective date: September 17, 1999, and shall be implemented within 
    30 days.
        Amendment No.: 175.
        Facility Operating License No. DPR-28. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 30, 1999 (64 FR 
    35214).
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated September 17, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
    Vermont Yankee Nuclear Power Corporation, Docket No. 50-271, Vermont 
    Yankee Nuclear Power Station, Vernon, Vermont
    
        Date of application for amendment: July 12, 1999.
        Brief description of amendment: The amendment revises the values 
    for the minimum critical power ratio safety limits and deletes the 
    wording classifying the limits as cycle-specific values.
        Date of Issuance: September 21, 1999.
        Effective date: September 21, 1999, and shall be implemented within 
    60 days.
        Amendment No.: 176
        Facility Operating License No. DPR-28: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: July 28, 1999 (64 FR 
    40910).
        The Commission's related evaluation of this amendment is contained 
    in a Safety Evaluation dated September 21, 1999.
        No significant hazards consideration comments received: No.
        Local Public Document Room location: Brooks Memorial Library, 224 
    Main Street, Brattleboro, VT 05301.
    
    Notice of Issuance of Amendments to Facility Operating Licenses and 
    Final Determination of No Significant Hazards Consideration and 
    Opportunity for a Hearing (Exigent Public Announcement or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for
    
    [[Page 54392]]
    
    example, in derating or shutdown of a nuclear power plant or in 
    prevention of either resumption of operation or of increase in power 
    output up to the plant's licensed power level, the Commission may not 
    have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By November 5, 1999, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) The nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such a supplement which satisfies these 
    requirements with respect to at least one contention will not be 
    permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555-0001, Attention: Rulemakings and 
    Adjudications Staff or may be delivered to the Commission's Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC, 
    by the above date. A copy of the petition should also be sent to the 
    Office of the General Counsel, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555-0001, and to the attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    [[Page 54393]]
    
    Duke Energy Corporation, Docket No. 50-369, McGuire Nuclear Station, 
    Unit 1, Mecklenberg County, North Carolina
    
        Date of application for amendment: August 27, 1999.
        Brief description of amendment: The amendment approves a one-time 
    extension of the surveillance frequency for Technical Specifications 
    Surveillance Requirement (TSSR) 3.1.4.2 beyond the 25 percent extension 
    allowed by TSSR 3.0.2 to the McGuire Nuclear Station, Unit 1. This 
    license amendment is effective upon issuance and is to expire upon 
    entering Mode 3 during Unit 1 startup following the Unit 1 End of Cycle 
    13 refueling outage.
        Date of issuance: September 8, 1999.
        Effective date: As of its date of issuance (September 8, 1999), and 
    shall expire upon entering Mode 3 during startup, following the End of 
    Cycle 13 refueling outage.
        Amendment No.: Unit 1-186.
        Facility Operating License No. NPF-9: Amendments revised the 
    Technical Specifications.
        Press release issued requesting comments as to proposed no 
    significant hazards consideration: Yes, September 2, 1999, Charlotte 
    Observer.
        Comments received: No.
        The Commission's related evaluation of the amendment, finding of 
    exigent circumstances, consultation with the State of North Carolina, 
    and final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated September 8, 1999.
        Local Public Document Room location: J. Murrey Atkins Library, 
    University of North Carolina at Charlotte, 9201 University City 
    Boulevard, Charlotte, North Carolina.
        Attorney for licensee: Ms. Lisa F. Vaughn, Duke Energy Corporation, 
    422 South Church Street, Charlotte, North Carolina NRC Section Chief: 
    Richard L. Emch, Jr.
    
    Duke Energy Corporation, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: September 13, 1999.
        Brief description of amendments: The amendments revise the 
    Technical Specifications TS 3.7.9, ``Control Room Area Ventilation 
    System (CRAVS),'' to establish actions to be taken for an inoperable 
    control room ventilation system due to a degraded control room pressure 
    boundary. This revision approves changes that would allow up to 24 
    hours to restore the Control Room Pressure Boundary (CRPB) to operable 
    status when two CRAVS trains are inoperable due to an inoperable CRPB 
    in MODES 1, 2, 3, and 4. In addition, a Limiting Condition for 
    Operation note would be added to allow the CRPB to be opened 
    intermittently under administrative control without affecting CRAVS 
    operability.
        Date of issuance: September 22, 1999.
        Effective date: As of the date of issuance and shall be implemented 
    upon receipt.
        Amendment Nos.: Unit 1--187; Unit 2--168.
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Press release issued requesting comments as to proposed no 
    significant hazards consideration: Yes, September 17, 1999, Charlotte 
    Observer.
        Comments received: No.
        The Commission's related evaluation and the amendment, finding of 
    emergency circumstances, consultation with the State of North Carolina, 
    and final no significant hazards consideration determination are 
    contained in a Safety Evaluation dated September 22, 1999.
        Attorney for licensee: Ms. Lisa F. Vaughn, Duke Energy Corporation, 
    422 South Church Street, Charlotte, North Carolina.
        Local Public Document Room location: J. Murrey Atkins Library, 
    University of North Carolina at Charlotte, 9201 University City 
    Boulevard, Charlotte, North Carolina.
        NRC Section Chief: Richard L. Emch, Jr.
    
        For the Nuclear Regulatory Commission.
    
        Dated at Rockville, Maryland, this 29th day of September, 1999.
    John A. Zwolinski,
    Director, Division of Licensing Project Management, Office of Nuclear 
    Reactor Regulation.
    [FR Doc. 99-25795 Filed 10-5-99; 8:45 am]
    BILLING CODE 7590-01-P
    
    
    

Document Information

Effective Date:
9/14/1999
Published:
10/06/1999
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
99-25795
Dates:
September 14, 1999.
Pages:
54370-54393 (24 pages)
PDF File:
99-25795.pdf