X95-20816. Biweekly Notice  

  • [Federal Register Volume 60, Number 158 (Wednesday, August 16, 1995)]
    [Notices]
    [Pages 42597-42622]
    From the Federal Register Online via the Government Publishing Office [www.gpo.gov]
    [FR Doc No: X95-20816]
    
    
    
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    NUCLEAR REGULATORY COMMISSION
    
    Biweekly Notice
    
    Applications and Amendments to Facility Operating LicensesInvolving 
    No Significant Hazards Considerations
    
    I. Background
    
        Pursuant to Public Law 97-415, the U.S. Nuclear Regulatory 
    Commission (the Commission or NRC staff) is publishing this regular 
    biweekly notice. Public Law 97-415 revised section 189 of the Atomic 
    Energy Act of 1954, as amended (the Act), to require the Commission to 
    publish notice of any amendments issued, or proposed to be issued, 
    under a new provision of section 189 of the Act. This provision grants 
    the Commission the authority to issue and make immediately effective 
    any amendment to an operating license upon a determination by the 
    Commission that such amendment involves no significant hazards 
    consideration, notwithstanding the pendency before the Commission of a 
    request for a hearing from any person.
        This biweekly notice includes all notices of amendments issued, or 
    proposed to be issued from July 21, 1995, through August 4, 1995. The 
    last biweekly notice was published on Wednesday, August 2, 1995 (60 FR 
    39430).
    
    Notice Of Consideration Of Issuance Of Amendments To Facility 
    Operating Licenses, Proposed No Significant Hazards Consideration 
    Determination, And Opportunity For A Hearing
    
        The Commission has made a proposed determination that the following 
    amendment requests involve no significant hazards consideration. Under 
    the Commission's regulations in 10 CFR 50.92, this means that operation 
    of the facility in accordance with the proposed amendment would not (1) 
    involve a significant increase in the probability or consequences of an 
    accident previously evaluated; or (2) create the possibility of a new 
    or different kind of accident from any accident previously evaluated; 
    or (3) involve a significant reduction in a margin of safety. The basis 
    for this proposed determination for each amendment request is shown 
    below.
        The Commission is seeking public comments on this proposed 
    determination. Any comments received within 30 days after the date of 
    publication of this notice will be considered in making any final 
    determination.
        Normally, the Commission will not issue the amendment until the 
    expiration of the 30-day notice period. However, should circumstances 
    change during the notice period such that failure to act in a timely 
    way would result, for example, in derating or shutdown of the facility, 
    the Commission may issue the license amendment before the expiration of 
    the 30-day notice period, provided that its final determination is that 
    the amendment involves no significant hazards consideration. The final 
    determination will consider all public and State comments received 
    before action is taken. Should the Commission take this action, it will 
    publish in the Federal Register a notice of issuance and provide for 
    opportunity for a hearing after issuance. The Commission expects that 
    the need to take this action will occur very infrequently.
        Written comments may be submitted by mail to the Rules Review and 
    Directives Branch, Division of Freedom of Information and Publications 
    Services, Office of Administration, U.S. Nuclear Regulatory Commission, 
    Washington, DC 20555, and should cite the publication date and page 
    number of this Federal Register notice. Written comments may also be 
    delivered to Room 6D22, Two White Flint North, 11545 Rockville Pike, 
    Rockville, Maryland from 7:30 a.m. to 4:15 p.m. Federal workdays. 
    Copies of written comments received may be examined at the NRC Public 
    Document Room, the Gelman Building, 2120 L Street, NW., Washington, DC. 
    The filing of requests for a hearing and petitions for leave to 
    intervene is discussed below.
        By September 15, 1995, the licensee may file a request for a 
    hearing with respect to issuance of the amendment to the subject 
    facility operating license and any person whose interest may be 
    affected by this proceeding and who wishes to participate as a party in 
    the proceeding must file a written request for a hearing and a petition 
    for leave to intervene. Requests for a hearing and a petition for leave 
    to intervene shall be filed in accordance with the Commission's ``Rules 
    of Practice for Domestic Licensing Proceedings'' in 10 CFR Part 2. 
    Interested persons should consult a current copy of 10 CFR 2.714 which 
    is available at the Commission's Public Document Room, the Gelman 
    Building, 2120 L Street, NW., Washington, DC and at the local public 
    document room for the particular facility involved. If a request for a 
    hearing or petition for leave to intervene is filed by the above date, 
    the Commission or an Atomic Safety and Licensing Board, designated by 
    the Commission or by the Chairman of the Atomic Safety and Licensing 
    Board Panel, will rule on the request and/or petition; and the 
    Secretary or the designated Atomic Safety and Licensing Board will 
    issue a notice of a hearing or an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if 
    
    [[Page 42598]]
    proven, would entitle the petitioner to relief. A petitioner who fails 
    to file such a supplement which satisfies these requirements with 
    respect to at least one contention will not be permitted to participate 
    as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses.
        If a hearing is requested, the Commission will make a final 
    determination on the issue of no significant hazards consideration. The 
    final determination will serve to decide when the hearing is held.
        If the final determination is that the amendment request involves 
    no significant hazards consideration, the Commission may issue the 
    amendment and make it immediately effective, notwithstanding the 
    request for a hearing. Any hearing held would take place after issuance 
    of the amendment.
        If the final determination is that the amendment request involves a 
    significant hazards consideration, any hearing held would take place 
    before the issuance of any amendment.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
        For further details with respect to this action, see the 
    application for amendment which is available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document room for 
    the particular facility involved.
    
    Baltimore Gas and Electric Company, Docket Nos. 50-317 and 50-318, 
    Calvert Cliffs Nuclear Power Plant, Unit Nos. 1 and 2, Calvert 
    County, Maryland
    
        Date of amendments request: March 15, 1995, as supplemented on June 
    29, 1995.
        Description of amendments request: The proposed amendments would 
    revise the Calvert Cliffs Nuclear Power Plant, Units Nos. 1 and 2, 
    Technical Specifications (TSs) Section 6, ``Administrative Controls,'' 
    to be consistent with the guidance provided in NUREG-1432, ``Standard 
    Technical Specifications, Combustion Engineering Plants.'' The proposed 
    changes will relocate several requirements to other documents and 
    programs consistent with NUREG-1432 and other NRC guidance addressing 
    the administrative section of the TSs such as the ``Final Policy 
    Statement on Technical Specification Improvements for Nuclear Power 
    Reactors,'' published in the Federal Register on July 22, 1993 (58 FR 
    39132).
        The Commission indicated that compliance with the Final Policy 
    Statement satisfies Section 182a of the Act. In particular, the 
    Commission indicated that certain items could be relocated from the TSs 
    to licensee-controlled documents, consistent with the standard 
    enunciated in Portland General Electric Co. (Trojan Nuclear Plant), 
    ALAB-531, 9 NRC 263, 273 (1979). In that case, the Atomic Safety and 
    Licensing Appeal Board indicated that ``technical specifications are to 
    be reserved for those matters as to which the imposition of rigid 
    conditions or limitations upon reactor operation is deemed necessary to 
    obviate the possibility of an abnormal situation or event giving rise 
    to an immediate threat to the public health and safety.'' The policy 
    statement encouraged licensees to adopt the applicable improved STSs 
    and provided some guidance for the conversion from the present plant-
    specific TSs to the improved Standard TSs.
        The proposed changes will provide significant human factors 
    improvement to the TSs by accomplishing the following: (1) relocating 
    existing requirements to licensee controlled documents consistent with 
    the policy statement; (2) eliminating requirements which duplicate 
    regulations; (3) relocating similar requirements within the same 
    section; (4) editorial changes; and (5) adding requirements consistent 
    with NUREG-1432.
        In addition, the licensee proposes dual rolls for the Shift 
    Technical Advisor (STA) and the establishment of a TS Bases Control 
    Program. Allowing the STA to perform dual rolls is not permitted by the 
    current TSs, but the current NRC guidance allows the STA to perform a 
    dual roll. The proposed new TS Bases Control Program will define the 
    appropriate methods and reviews required to implement a TS Bases change 
    which is also consistent with the current NRC guidance. Two other 
    proposed changes, not specifically covered by the above groupings, 
    include a reduction in reporting requirements and utilizing a more 
    effective option for estimating doses.
        Basis for proposed no significant hazards consideration 
    determination: As required by 10 CFR 50.91(a), the licensee has 
    provided its analysis of the issue of no significant hazards 
    consideration, which is presented below:
        1. Would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
        Relocating existing requirements to Baltimore Gas and Electric 
    Company (BGE)-controlled documents, eliminating requirements which 
    duplicate regulations, locating similar requirements within the same 
    sections and making necessary editorial corrections to incorporate 
    the proposed changes provide Technical Specifications which are 
    easier to use. Because existing requirements are relocated to 
    established BGE programs where changes to those programs are 
    controlled by regulatory requirements, there is no reduction in 
    commitment and adequate control is still maintained. Likewise, the 
    elimination of requirements which duplicate regulations enhances the 
    usability of the Technical Specifications without reducing 
    commitments. Locating similar requirements within the same sections 
    and making necessary editorial corrections to incorporate the 
    proposed changes neither add nor delete requirements, but merely 
    clarify and improve the readability and understanding of the 
    Technical Specifications. Since the requirements remain the same, 
    these changes only affect the method of presentation and would not 
    affect possible initiating events for accidents previously evaluated 
    or any system functional requirement. Therefore, the proposed 
    changes would not involve a significant increase in the probability 
    or consequences of an accident previously evaluated.
    
    [[Page 42599]]
    
        Since the Shift Technical Adviser (STA) is not considered an 
    initiator to any previously evaluated accident nor considered in the 
    accident's response, the use of a dual role STA would not increase 
    the probability or consequences of any previously evaluated 
    accident.
        The Technical Specification Bases Control Program provides 
    controls which ensure appropriate reviews of changes to the Bases. 
    Because NRC approval is still needed for changes to the Bases which 
    affect the Technical Specifications, the proposed Program would not 
    affect the probability or consequences of a previously evaluated 
    accident.
        Eliminating the requirement for submitting two reports which 
    place unwarranted administrative burden on both Baltimore Gas and 
    Electric Company and the NRC has no affect on the probability or 
    consequences of an accident previously evaluated. Therefore, the 
    proposed changes would not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        Replacing the film badge with the electronic personal dosimeter 
    provides a more effective, efficient, state-of-the art option for 
    estimating dose and would not impact accidents previously evaluated. 
    Therefore, the proposed change would not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        2. Would not create the possibility of a new or different type 
    of accident from any accident previously evaluated.
        As discussed previously, relocating existing requirements to 
    BGE-controlled documents, eliminating requirements which duplicate 
    regulations, locating similar requirements within the same sections 
    and making necessary editorial corrections to incorporate the 
    proposed changes will not affect any plant system or structure, nor 
    will it affect any system functional or operability requirements. 
    Consequently, no new failure modes are introduced as a result of the 
    proposed changes. Therefore, these types of changes would not create 
    the possibility of a new or different type of accident from any 
    accident previously evaluated.
        Because the STA does not perform equipment design or equipment 
    manipulation, the use of a dual role STA would not create the 
    possibility of a new or different type of accident from any accident 
    previously evaluated. Since the Technical Specification Bases 
    Control Program represents an administrative function performed 
    under existing regulatory controls, it too would not create the 
    possibility of a new or different type of accident from any 
    previously evaluated.
        The addition of new programs which incorporate existing 
    Technical Specification requirements and commitments will have no 
    effect on the design or operation of the plant and would not create 
    the possibility of a new or different type of accident from any 
    previously evaluated.
        A reporting function such as report submittals would not change 
    the configuration or operation of the plant. Consequently, the 
    elimination of the requirement to submit the Startup Report and the 
    Special Report dealing with iodine activity levels, would not create 
    the possibility of a new or different type of accident from any 
    accident previously evaluated.
        Since the operation or configuration of the plant is not changed 
    by the type of personal dosimeter, this change would not create the 
    possibility of a new or different type of accident from any accident 
    previously evaluated.
        Therefore, the proposed changes would not create the possibility 
    of a new or different type of accident from any accident previously 
    evaluated.
        3. Would not involve a significant reduction in a margin of 
    safety.
        Relocating existing requirements to BGE-controlled documents, 
    eliminating requirements which duplicate regulations, locating 
    similar requirements within the same sections and making necessary 
    editorial corrections to incorporate the proposed changes would not 
    affect the Updated Final Safety Analysis Report design bases, 
    accident analysis assumptions or any margin of safety described in 
    the Technical Specification Bases. In addition, these proposed 
    changes do not affect effluent release limits, monitoring equipment 
    or practices. Therefore, these proposed changes would not involve a 
    significant reduction in a margin of safety.
        The use of an STA should provide an additional margin of safety 
    in the accident response function of licensed operators beyond that 
    considered in the accident analysis. Since the STA is required to 
    have the same training and educational qualifications in either the 
    individual or dual role, the use of a dual role STA should have 
    minimal impact. Consequently, the proposed change would not involve 
    a significant reduction in a margin of safety. The Technical 
    Specification Bases Control Program is an administrative change 
    controlling how Technical Specification basis information is 
    reviewed and incorporated. Therefore, this change would not involve 
    a significant reduction in a margin of safety.
        The addition of new programs which incorporate existing 
    Technical Specification requirements and commitments will have no 
    effect on the design or operation of the plant and would not result 
    in a significant reduction in the margin of safety.
        Activities described in the Startup Report will continue to be 
    performed and corrective action taken when required. Similarly, 
    iodine activity levels will continue to be monitored and actions 
    taken, including the issuance of a Licensee Event Report when 
    conditions warrant. Considering the above, elimination of the two 
    reporting requirements would have no impact on the margin of safety.
        Plant operating parameters are not affected by the type of 
    personnel monitoring device used and as a consequence, would not 
    impact a margin of safety. Since the replacement dosimeter provides 
    a more effective mechanism for estimating dose, there is no 
    degradation in personal safety levels. Consequently, the proposed 
    change would not involve a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendments request involves no significant hazards consideration.
        Local Public Document Room location: Calvert County Library, Prince 
    Frederick, Maryland 20678.
        Attorney for licensee: Jay E. Silbert, Esquire, Shaw, Pittman, 
    Potts and Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: Ledyard B. Marsh
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois 
    Docket Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, 
    Units 1 and 2, Rock Island County, Illinois
    
        Date of application for amendment requests: September 17, 1993, as 
    supplemented July 28, 1995
        Description of amendment requests: As a result of findings by a 
    Diagnostic Evaluation Team inspection performed by the NRC staff at the 
    Dresden Nuclear Power Station in 1987, Commonwealth Edison Company 
    (ComEd, the licensee) made a decision that both the Dresden Nuclear 
    Power Station and sister site Quad Cities Nuclear Power Station needed 
    attention focused on the existing custom Technical Specifications (TS) 
    used.
        The licensee made the decision to initiate a Technical 
    Specification Upgrade Program (TSUP) for both Dresden and Quad Cities. 
    The licensee evaluated the current TS for both Dresden and Quad Cities 
    against the Standard Technical Specifications (STS) contained in NUREG-
    0123, ``Standard Technical Specifications General Electric Plants BWR/
    4.'' The licensee's evaluation identified numerous potential 
    improvements such as clarifying requirements, changing TS to make them 
    more understandable and to eliminate interpretation, and deleting 
    requirements that are no longer considered current with industry 
    practice. As a result of the evaluation, ComEd has elected to upgrade 
    both the Dresden and Quad Cities TS to the STS contained in NUREG-0123.
        The TSUP for Dresden and Quad Cities is not a complete adoption of 
    the STS. The TSUP focuses on (1) integrating additional information 
    such as equipment operability requirements during shutdown conditions, 
    (2) clarifying requirements such as limiting conditions for operation 
    and action 
    
    [[Page 42600]]
    statements utilizing STS terminology, (3) deleting superseded 
    requirements and modifications to the TS based on the licensee's 
    responses to Generic Letters (GL), and (4) relocating specific items to 
    more appropriate TS locations.
        The September 17, 1993, and July 28, 1995, applications proposed to 
    upgrade only Section 3/4.5 (Emergency Core Cooling Systems) of the 
    Dresden and Quad Cities TS.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated 
    because:
        In general, the proposed amendment represents the conversion of 
    current requirements to a more generic format, or the addition of 
    requirements which are based on the current safety analysis. 
    Implementation of these changes will provide increased reliability 
    of equipment assumed to operate in the current safety analysis, or 
    provide continued assurance that specified parameters remain within 
    their acceptance limits, and as such, will not significantly 
    increase the probability or consequences of a previously evaluated 
    accident.
        Some of the proposed changes represent minor curtailments of the 
    current requirements which are based on generic guidance or 
    previously approved provisions for other stations. The proposed 
    amendment for Dresden and Quad Cities Station's Technical 
    Specification Section 3/4.5 are based on STS guidelines or later 
    operating BWR plants' NRC accepted changes. Any deviations from STS 
    requirements do not significantly increase the probability or 
    consequences of any previously evaluated accidents for Dresden or 
    Quad Cities Stations. The proposed amendment is consistent with the 
    current safety analyses and has been previously determined to 
    represent sufficient requirements for the assurance and reliability 
    of equipment assumed to operate in the safety analysis, or provide 
    continued assurance that specified parameters remain within their 
    acceptance limits. As such, these changes will not significantly 
    increase the probability or consequences of a previously evaluated 
    accident.
        The associated systems that make up the Emergency Core Cooling 
    Systems are not assumed in any safety analysis to initiate any 
    accident sequence for Dresden or Quad Cities Stations; therefore, 
    the probability of any accident previously evaluated is not 
    increased by the proposed amendment. In addition, the proposed 
    surveillance requirements for the proposed amendments to these 
    systems are generally more prescriptive than the current 
    requirements specified within the Technical Specifications. The 
    additional surveillance requirements improve the reliability and 
    availability of all affected systems and therefore, reduce the 
    consequences of any accident previously evaluated as the probability 
    of the systems outlined within Section 3/4.5 of the proposed 
    Technical Specifications performing their intended function is 
    increased by the additional surveillances.
        Create the possibility of a new or different kind of accident 
    from any previously evaluated because:
        In general, the proposed amendment represents the conversion of 
    current requirements to a more generic format, the addition of 
    requirements which are based on the current safety analysis, and 
    some minor curtailments of the current requirements which are based 
    on generic guidance or previously approved provisions for other 
    stations. These changes do not involve revisions to the design of 
    the station. Some of the changes may involve revision in the 
    operation of the station; however, these provide additional 
    restrictions which are in accordance with the current safety 
    analysis, or are to provide for additional testing or surveillances 
    which will not introduce new failure mechanisms beyond those already 
    considered in the current safety analyses.
        The proposed amendment for Dresden and Quad Cities Station's 
    Technical Specification Section 3/4.5 is based on STS guidelines or 
    later operating BWR plants' NRC accepted changes. The proposed 
    amendment has been reviewed for acceptability at the Dresden and 
    Quad Cities Nuclear Power Stations considering similarity of system 
    or component design versus the STS or later operating BWRs. Any 
    deviations from STS requirements do not create the possibility of a 
    new or different kind of accident previously evaluated for Dresden 
    or Quad Cities Stations. No new modes of operation are introduced by 
    the proposed changes. Surveillance requirements are changed to 
    reflect improvements in technique, frequency of performance or 
    operating experience at later plants. Proposed changes to action 
    statements in many places add requirements that are not in the 
    present technical specifications. The proposed changes maintain at 
    least the present level of operability. Therefore, the proposed 
    changes do not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        The associated systems that make up the Emergency Core Cooling 
    Systems are not assumed in any safety analysis to initiate any 
    accident sequence for Dresden or Quad Cities Stations. In addition, 
    the proposed surveillance requirements for affected systems 
    associated with the Emergency Core Cooling Systems are generally 
    more prescriptive than the current requirements specified within the 
    Technical Specifications; therefore, the proposed changes do not 
    create the possibility of a new or different kind of accident from 
    any previously evaluated.
        Involve a significant reduction in the margin of safety because:
        In general, the proposed amendment represents the conversion of 
    current requirements to a more generic format, the addition of 
    requirements which are based on the current safety analysis, and 
    some minor curtailments of the current requirements which are based 
    on generic guidance or previously approved provisions for other 
    stations. Some of the latter individual items may introduce minor 
    reductions in the margin of safety when compared to the current 
    requirements. However, other individual changes are the adoption of 
    new requirements which will provide significant enhancement of the 
    reliability of the equipment assumed to operate in the safety 
    analysis, or provide enhanced assurance that specified parameters 
    remain with their acceptance limits. These enhancements compensate 
    for the individual minor reductions, such that taken together, the 
    proposed changes will not significantly reduce the margin of safety.
        The proposed amendment to Technical Specification Section 3/4.5 
    implements present requirements, or the intent of present 
    requirements in accordance with the guidelines set forth in the STS. 
    Any deviations from STS requirements do not significantly reduce the 
    margin of safety for Dresden or Quad Cities Stations. The proposed 
    changes are intended to improve readability, usability, and the 
    understanding of technical specification requirements while 
    maintaining acceptable levels of safe operation. The proposed 
    changes have been evaluated and found to be acceptable for use at 
    Dresden or Quad Cities based on system design, safety analysis 
    requirements and operational performance. Since the proposed changes 
    are based on NRC accepted provisions at other operating plants that 
    are applicable at Dresden or Quad Cities and maintain necessary 
    levels of system or component reliability, the proposed changes do 
    not involve a significant reduction in the margin of safety.
        The proposed amendment for Dresden and Quad Cities Stations will 
    not reduce the availability of systems associated with the Emergency 
    Core Cooling Systems when required to mitigate accident conditions; 
    therefore, the proposed changes do not involve a significant 
    reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment requests involve no significant hazards consideration.
        Local Public Document Room location: for Dresden, Morris Public 
    Library, 604 Liberty Street, Morris, Illinois 60450; for Quad Cities, 
    Dixon Public Library, 221 Hennepin Avenue, Dixon, Illinois 61021
        Attorney for licensee: Michael I. Miller, Esquire; Sidley and 
    Austin, One First National Plaza, Chicago, Illinois 60690
        NRC Project Director: Robert A. Capra
    
    [[Page 42601]]
    
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of amendment request: June 17, 1993, as supplemented July 5, 
    1995
        Description of amendment request: The initial proposed amendment 
    request dated June 17, 1993, was previously noticed in the Federal 
    Register on July 21, 1993 (58 FR 39048). The proposed amendment would 
    revise Technical Specification 5.3.1, ``Fuel Assemblies'' to provide 
    flexibility in the repair of fuel assemblies containing damaged and 
    leaking fuel rods by reconstituting the assemblies in accordance with 
    the guidance in Generic Letter (GL) 90-02, Supplement 1, ``Alternative 
    Requirements For Fuel Assemblies In The Design Features Section Of 
    Technical Specifications,'' issued on July 31, 1992. The application is 
    also generally consistent with the format and content of the improved 
    Standard Technical Specifications for Westinghouse plants provided in 
    NUREG-1431.
        Additional information was submitted on July 5, 1995, that added TS 
    changes to increase the fuel enrichment limit from 4.0 to 5.0 weight 
    percent U-235 that were not previously included the initial June 17, 
    1993, amendment application. This additional information is being 
    noticed to provide for public comment and opportunity for hearing.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee provided its analysis of the issue of no significant hazards 
    consideration (58 FR 39048). The NRC staff's analysis of the July 5, 
    1995, supplement against the standards of 10 CFR 50.92(c) is presented 
    below.
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        There is no increase in the probability or consequences of an 
    accident in the new fuel vault since the only accident that would be 
    affected by this change would be a criticality accident and it has been 
    shown that the worst-case keff under optimum moderation conditions 
    continues to be less than or equal to 0.98.
        There is no increase in the probability of a fuel drop accident in 
    the Spent Fuel Storage Pool since the mass of an assembly will not be 
    significantly affected by the increase in fuel enrichment. The 
    likelihood of other accidents, previously evaluated and described in 
    Section 9.1.2 of the Final Safety Analysis Report (FSAR), is also not 
    affected by the proposed changes. Since the increase in fuel enrichment 
    will allow for extended fuel cycles, it could be postulated that there 
    may be a decrease in fuel movement and the probability of an accident 
    may likewise be decreased. There is also no increase in the 
    consequences of a fuel drop accident in the Spent Fuel Pool since the 
    fission product inventory of individual fuel assemblies will not change 
    significantly as a result of increased initial enrichment. In addition, 
    no change to safety-related systems is being made.
        Therefore, the consequences of a fuel rupture accident remain 
    unchanged. In addition, it has been shown that keff is less than 
    or equal to 0.95, under all conditions. Therefore, the consequences of 
    a criticality accident in the Spent Fuel Pool remain unchanged as well.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes do not create the possibility of a new or 
    different kind of accident since fuel handling accidents (fuel drop and 
    misplacement) are not new or different kinds of accidents. Fuel 
    handling accidents are already discussed in the FSAR for fuel with 
    enrichments up to 4.0 weight % and additional analyses have been 
    performed for fuel with enrichment up to 5.00 weight %.
        3.
        The proposed changes do not involve a significant reduction in the 
    margin of safety.
        The proposed change does not involve a significant reduction in the 
    margin of safety since, in all cases, a spent fuel pool keff less 
    than or equal to 0.95 is being maintained. Criticality analyses have 
    also been performed that show that the new fuel storage vault will 
    remain subcritical under a variety of moderation conditions, from fully 
    flooded to optimum moderation. As discussed above, the Spent Fuel Pool 
    will remain sufficiently subcritical during any fuel misplacement 
    accident.
        Based on this analysis, it appears that the three standards of 10 
    CFR 50.92(c) are satisfied. Therefore, the NRC staff proposes to 
    determine that the supplemental amendment submittal involves no 
    significant hazards consideration.
        Local Public Document Room location:: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730
        Attorney for licensee: Mr. Albert Carr, Duke Power Company, 422 
    South Church Street, Charlotte, North Carolina 28242
        NRC Project Director: Herbert N. Berkow
    
    Duke Power Company, Docket Nos. 50-269, 50-270 and 50-287, Oconee 
    Nuclear Station, Units 1, 2 and 3, Oconee County, South Carolina
    
        Date of amendment request: July 26, 1995
        Description of amendment request: The proposed amendments would 
    provide a one-time extension of the allowable outage time from 72 hours 
    to 7 days. This extension is necessary to implement a modification to 
    the degraded grid protection system and the external grid trouble 
    protection system.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
    
    Duke Power Company (Duke) has made the determination that this 
    amendment request involves a No Significant Hazards Consideration 
    by applying the standards established by NRC regulations in 10 CFR 
    50.92. This ensures that operation of the facility in accordance 
    with the proposed amendment would not:(1) Involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated:
    
        Each accident analysis addressed within the Oconee Final Safety 
    Analysis Report (FSAR) has been examined with respect to the change 
    proposed within this amendment request. The design basis of the 
    auxiliary electrical systems is to supply the required engineered 
    safeguards (ES) loads of one unit and the safe shutdown loads of the 
    other two units. The systems are arranged so that no single failure 
    will jeopardize plant safety.
        The probability of any Design Basis Accident (DBA) is not 
    significantly increased by this change. In addition, the 
    consequences of the accidents are within the bounds of the FSAR 
    analyses. The reliability of the emergency power system is not 
    significantly affected by a one time extension of allowable outage 
    time for the overhead power path. The underground power path is 
    adequate to assure operability of the Oconee ES loads. Finally, the 
    enhancement of the Degraded [Grid] Protection System will eliminate 
    a concern which was expressed by the EDSFI audit team.
        (2) Create the possibility of a new or different kind of 
    accident from any kind of accident previously evaluated:
        Inoperability of the yellow bus is functionally equivalent to 
    inoperability of the Keowee Main Step-up Transformer in that it 
    renders the overhead emergency power path inoperable. The Keowee 
    Main Step-up Transformer is allowed to be inoperable for a period 
    not to exceed 28 days. This Technical Specification requirement for 
    the 
    
    [[Page 42602]]
    Keowee Main Step-up Transformer has been reviewed and approved by the 
    NRC. Therefore, operation of ONS [Oconee Nuclear Station] in 
    accordance with this Technical Specification amendment will not 
    create any failure modes not bounded by previously evaluated 
    accidents. Consequently, this change will not create the possibility 
    of a new or different kind of accident from any kind of accident 
    previously evaluated.
        (3) Involve a significant reduction in a margin of safety:
        The design basis of auxiliary electrical systems is to supply 
    the required ES loads of one Unit and safe shutdown loads of the 
    other two units. The underground power path is adequate to ensure 
    operability of the ES loads during the outage of the yellow bus. The 
    reliability of the emergency power system is not significantly 
    affected by a one time extension of allowable outage time for the 
    overhead power path. Therefore, there will be no significant 
    reduction in any margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: Oconee County Library, 501 
    West South Broad Street, Walhalla, South Carolina 29691
        Attorney for licensee: J. Michael McGarry, III, Winston and Strawn, 
    1200 17th Street, NW., Washington, DC 20036
        NRC Project Director: Herbert N. Berkow
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of amendment request: July 10, 1995
        Description of amendment request: The proposed amendment would 
    modify the technical specifications to minimize the potential for boron 
    deletion of the reactor coolant system (RCS) during startup of an 
    isolated loop. The changes would permit RCS loop isolation only during 
    Modes 5 and 6. RCS loop isolation valves would be required open with 
    power removed from each isolation valve operator during Modes 1, 2, 3, 
    and 4. Primary grade water would be isolated from the RCS during Modes 
    4, 5, and 6, except during planned boron dilution or makeup activities.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed amendment would modify the method used to prevent 
    an inadvertent boron dilution event during hot shutdown, cold 
    shutdown and during refueling. An uncontrolled boron dilution 
    transient cannot occur during this mode of operation. Inadvertent 
    boron dilution is prevented by administrative controls which isolate 
    the primary grade water system isolation valves from the Chemical 
    and Volume Control System, except during planned boron dilution or 
    makeup activities. Thus unborated water can not be injected into the 
    reactor coolant system, making an unplanned boron dilution at these 
    conditions highly improbable, since the source of unborated water to 
    the charging pumps is isolated. This precludes the primary means for 
    an inadvertent boron dilution event in this mode of operation.
        The primary grade water system isolation valves may be opened 
    when directed by the control room during this mode of operation only 
    for a planned boron dilution or makeup activity. The primary grade 
    water system isolation valves will be verified to be locked, sealed 
    or otherwise secured in the closed position after the planned boron 
    dilution or makeup activity is completed. During planned boron 
    dilution events, operator attention will be focused on the boron 
    dilution process and any inappropriate blender operation will be 
    readily identified.
        The operator has prompt and definite indication of any boron 
    dilution from the audible count rate instrumentation supplied by the 
    source range nuclear instrumentation. High count rate is alarmed in 
    the reactor containment and the control room. In addition a high 
    source range flux level is alarmed in the control room. The count 
    rate increase is proportional to the subcritical multiplication 
    factor.
        The proposed amendment would also modify the method used to 
    prevent an adverse reactor transient during startup of an isolated 
    reactor coolant loop. Procedures require that the isolated loop 
    water boron concentration be verified prior to opening loop 
    isolation valves. Procedures also require an isolated loop to be 
    drained and refilled from water supplied from the Refueling Water 
    Storage Tank (RWST) or Reactor Coolant System (RCS) prior to opening 
    either the hot or cold leg isolation valves. Using water from the 
    RWST or RCS ensures 1) that the boron concentration of the isolated 
    loop is sufficient to prevent a dilution of the active reactor 
    coolant loops and reducing the shutdown margin to below those values 
    used in safety analyses when the isolated loop is returned to 
    service, and 2) that no single failure could cause an isolated loop 
    to be filled with unborated water.
        Thus procedures and interlocks prevent inadvertent opening of 
    loop isolation valves and require that the startup of an isolated 
    loop be performed in a controlled manner that virtually eliminates 
    any sudden positive reactivity addition from boron dilution. Thus 
    the core cannot be adversely affected by the startup of an isolated 
    loop and fuel design limits are not exceeded. Therefore, the 
    proposed change does not involve a significant increase in the 
    probability or consequences of an accident previously evaluated.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes do not create the possibility of a new or 
    different kind of accident. No new systems, structures or components 
    are being proposed. Acceptable alternative administrative controls 
    are being proposed to address inadvertent boron dilution and the 
    startup of inactive reactor coolant loops.
        The primary source of unborated water will be isolated from 
    injecting by the charging pumps into the reactor coolant system 
    during hot shutdown, cold shutdown, and refueling, except for 
    planned boron dilution events and makeup activities. The proposed 
    administrative controls prevent the possible accident previously 
    evaluated, i.e., an inadvertent boron dilution event.
        A currently installed interlock to recirculate reactor coolant 
    in an isolated loop is proposed to be deleted. In its place, each 
    reactor coolant isolated loop will be drained and refilled with 
    water supplied from the RWST just before the loop is returned to 
    service. This administrative control will prevent any inadvertent 
    reactivity transient when returning the loop to service. Thus, the 
    proposed administrative controls will prevent the type of accident 
    previously evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed changes will continue to ensure that adequate 
    protection is provided against an inadvertent boron dilution and the 
    adverse effects from the startup of an isolated reactor coolant 
    loop. General Design Criteria 10 requirements will not be exceeded 
    with respect to demonstrating specified acceptable fuel design 
    limits. The required indications and functions are still maintained 
    in accordance with current technical specification requirements and 
    the shutdown margin is unaffected. Therefore, the proposed change 
    will not involve a significant reduction in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. Library, 663 Franklin 
    Avenue, Aliquippa, Pennsylvania 15001.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    [[Page 42603]]
    
    
    Duquesne Light Company, et al., Docket No. 50-334, Beaver Valley 
    Power Station, Unit 1, Shippingport, Pennsylvania
    
        Date of amendment request: July 11, 1995
        Description of amendment request: The proposed amendment would 
    revise the required area of the Reactor Coolant System (RCS) 
    overpressure protection system vent from 3.14 square inches to 2.07 
    square inches. This vent is provided to relieve a potential RCS 
    overpressure condition if the power-operated relief valves (PORVs) are 
    not operable. The proposed vent area is equal to the relief area of a 
    PORV. A single PORV is capable of providing sufficient relief capacity 
    to mitigate potential low temperature overpressurization events.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The proposed change is considered to be editorial since it 
    replaces the 3.14 square inch vent size stated in overpressure 
    protection system (OPPS) Specifications 3.4.9.3, 3.1.2.1.b, and 
    3.1.2.3 and Bases 3/4.1.2 and 3/4.4.9 with a 2.07 square inch vent 
    size. This ensures the vent size stated in the technical 
    specifications is consistent with the actual size of an installed 
    PORV. These changes maintain consistency with the analyses 
    assumptions and the operation of the OPPS in accordance with 
    applicable analyses and the UFSAR [Updated Final Safety Analyses 
    Report]. Therefore, we have concluded that these changes do not 
    involve a significant increase in the probability or consequences of 
    an accident previously evaluated in the UFSAR.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes do not involve any physical changes to the 
    OPPS or their setpoints. These changes do not change any function 
    previously provided by the OPPS. These changes do not affect any 
    failure modes defined for any plant system or component important to 
    safety nor has any new limiting single failure been identified as a 
    result of these changes. Therefore, these changes will not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated in the UFSAR.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed changes will not affect the operation of or the 
    reliability of the OPPS. These changes do not affect the manner in 
    which the plant is operated or involve a change to equipment or 
    features that affect the operational characteristics of the plant. 
    Therefore, operation of the plant in accordance with the proposed 
    amendment would not involve a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of amendment request: July 20, 1995
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 3/4.8.1.1 to incorporate guidance 
    provided in NRC Generic Letter (GL) 84-15, ``Proposed Staff Actions to 
    Improve and Maintain Diesel Generator Reliability,'' and GL 93-05, 
    ``Line-Item Technical Specification Improvements To Reduce Surveillance 
    Requirements For Testing During Power Operation,'' which includes (1) 
    revised requirements for testing the operable emergency diesel 
    generators (EDGs) for various combinations of inoperable offsite 
    circuits and EDGs and (2) revised surveillance requirements for the 
    EDGs. The revised surveillance requirements include specifying 
    generator voltage, frequency limits, and diesel starting time. In 
    addition, several editorial changes would be made to TS 3/4.8.1.1 which 
    would be consistent with the guidance provided in the NRC's Improved 
    Standard Technical Specifications (NUREG-1431).
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        The probability of occurrence of a previously evaluated accident 
    is not increased because the allowable outage times for the offsite 
    circuits and diesel generators remain unchanged. The consequences of 
    an accident previously evaluated is not increased because reducing 
    the diesel generator test frequency and permitting additional test 
    evolutions are intended to minimize diesel wear and mechanical 
    stress. By eliminating excessive testing, which can lead to 
    premature diesel failures and minimizing diesel wear and mechanical 
    stress, the diesel generator reliability is increased. The 
    consequences of an accident previously evaluated is also not 
    increased because the addition of the parameters for generator 
    voltage, frequency, and diesel starting time to the surveillance 
    requirement will provide additional assurance that the diesel 
    generators are performing as assumed in the safety analysis. This 
    proposed change does not affect the availability or reliability of 
    the offsite circuits.
        Therefore, this change will not increase the probability or 
    consequences of an accident previously evaluated due to the 
    continued availability and reliability of the A.C. electrical power 
    sources.
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes do not alter the method of operating the 
    plant. The changes do not introduce any new failure modes and are 
    intended to increase the diesel generator reliability and provide 
    additional assurance that the diesels are performing as assumed in 
    the safety analysis. The revision to the various action statements 
    and surveillance requirements provide assurance that the diesel 
    generators will be able to power their respective safety systems if 
    required. The proposed changes do not impact the performance of any 
    safety system.
        Therefore, this proposed change does not create the possibility 
    of a new or different kind of accident from any accident previously 
    evaluated.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The margin of safety is not reduced because the A.C. electrical 
    power sources will continue to provide sufficient capacity, 
    capability, redundancy, and reliability to ensure availability of 
    necessary power to engineered safety feature (ESF) systems. The ESF 
    systems will continue to function, as assumed in the safety 
    analyses, to ensure that the fuel, reactor coolant system and 
    containment design limits are not exceeded. The elimination of 
    excessive testing on the diesel generators are permitting additional 
    test evolutions, which result in less diesel wear and mechanical 
    stress, are intended to increase diesel reliability. The increased 
    reliability of the diesels adds to the ability of the A.C. 
    electrical power source to provide power to ESF systems. The 
    proposed additions to the surveillance requirements will provide 
    additional assurance of the ability of the A.C. electrical power 
    sources to provide power to ESF systems.
        Therefore, this proposed change does not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    
    [[Page 42604]]
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location:  B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    Duquesne Light Company, et al., Docket No. 50-412, Beaver Valley 
    PowerStation, Unit 2, Shippingport, Pennsylvania
    
        Date of amendment request: July 24, 1995
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 3/4.4.11, ``Relief Valves,'' and 
    associated Bases to make Unit 2 TS 3/4.4.11 consistent with Unit 1 TS 
    3/4.4.11, which was revised by Unit 1 License Amendment No. 187 issued 
    on May 15, 1995. The proposed amendment would also generally reflect 
    the guidance provided in NRC Generic Letter 90-06 and in the NRC's 
    Improved Standard Technical Specifications (NUREG-1431).
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        Implementation of these changes will increase the availability 
    of the power-operated relief valves (PORVs) and their associated 
    block valves. The increased availability is obtained through 
    maintaining power to the block valves which are closed to control 
    PORV seat leakage. Maintaining power to the block valve provides the 
    flexibility of reopening the valves to control reactor coolant 
    system pressure. The proposed change modifies Specification 3.4.11 
    actions, a surveillance requirement, and Bases to generally reflect 
    the requirements of Generic Letter (GL) 90-06, and the guidance 
    provided in NUREG-1431, ``Improved Standard Technical 
    Specifications'' (ISTS) and is consistent with the changes the NRC 
    approved for Unit No. 1. A revised stress analysis has been 
    completed that takes credit for the speed at which the block valve 
    opens when manually reducing reactor coolant system pressure. The 
    block valve relatively slow opening speed reduces the peak pressure 
    surge and results in acceptable downstream piping stress values. The 
    PORV downstream piping has been evaluated assuming manual vent path 
    operation with cold loop seal slug flow and it has been determined 
    that the piping supports can accept these design transient loads. 
    The proposed change to the action statement to close the block valve 
    to isolate a PORV and maintain power to the block valve does not 
    significantly increase the probability of a small break loss of 
    coolant accident. No PORV function has been deleted and the PORV and 
    block valve continue to be capable of being manually closed at any 
    time. As a result of the change to action ``a,'' an exception to the 
    stroking requirements is no longer required, therefore, reference to 
    action ``a'' in Surveillance Requirement 4.4.11.2 has been deleted. 
    Closing the block valve for a PORV that is not capable of being 
    manually cycled and removing power to the block valve assures that 
    the valve will not be inadvertently opened when the condition of the 
    PORV is uncertain.
        The changes remain consistent with the analysis assumptions 
    regarding the operation of the PORVs and block valves and provides 
    increased assurance of their availability in mitigating the 
    consequences of a steam generator tube rupture (SGTR) accident. The 
    requirements of GL 90-06 are substantially addressed in the ISTS 
    which have been incorporated here except for specific design 
    differences. Minor editorial changes involving capitalization have 
    been incorporated to maintain the format and content and do not 
    affect any of the requirements, the accident analyses, or the 
    operation of the plant. Therefore, we have concluded that these 
    changes do not involve a significant increase in the probability or 
    consequences of an accident previously evaluated in the UFSAR 
    [Updated Final Safety Analysis Report].
        2. Does the change create the possibility of a new or different 
    kind of accident from any accident previously evaluated?
        The proposed changes to the action statements for the PORVs and 
    the associated block valves will improve the availability of these 
    valves for normal operation and for mitigation of a SGTR accident. 
    The proposed changes do not involve any physical changes to the 
    PORVs or their setpoints. These changes do not delete any design 
    basis accident function previously provided by the PORV vent path 
    nor has the probability of inadvertent opening been increased. 
    Accordingly, no new limiting single failure has been identified as a 
    result of these changes. Therefore, these changes will not create 
    the possibility of a new or different kind of accident from any 
    accident previously evaluated in the UFSAR.
        3. Does the change involve a significant reduction in a margin 
    of safety?
        The proposed changes have been incorporated to provide the 
    capability to manually stroke the vent path using the block valve to 
    control the pressure surge as a PORV opens. The resultant downstream 
    piping forces were found acceptable, therefore, power can be 
    maintained to the block valve when the block valve has been closed 
    to isolate a PORV because of excessive seat leakage. This will allow 
    operation of the PORVs in a manner similar to the guidance provided 
    in GL 90-06 to improve PORV availability. These changes will improve 
    the operator use of an isolated PORV since it is now analyzed to be 
    manually cycled with the block valve closed and power maintained so 
    the operator can use the PORV if required to mitigate the effects of 
    a SGTR accident. This is consistent with the intent of the ISTS and 
    does not affect the UFSAR, therefore, operation of the plant in 
    accordance with the proposed amendment would not involve a 
    significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location:  B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 1500l.
        Attorney for licensee: Jay E. Silberg, Esquire, Shaw, Pittman, 
    Potts & Trowbridge, 2300 N Street, NW., Washington, DC 20037.
        NRC Project Director: John F. Stolz
    
    Entergy Operations, Inc., Docket No. 50-368, Arkansas Nuclear One, 
    Unit No. 2, Pope County, Arkansas
    
        Date of amendment request: April 4, 1995
        Description of amendment request: The proposed amendment revises 
    the minimum water level that is required to be maintained over 
    irradiated fuel assemblies during latching and unlatching of control 
    element assemblies.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        Criterion 1 - Does Not Involve a Significant Increase in the 
    Probability or Consequences of an Accident Previously Evaluated.
        The fuel handling accident analysis assumes that a fuel assembly 
    is dropped during fuel handling. During the latching and unlatching 
    of the CEAs, the upper guide structure is in place and the CEDM 
    extension shaft assemblies are disconnected from their CEA for 
    subsequent removal with the vessel upper guide structure. The 
    dropping of a CEA from the maximum height of six inches will not 
    damage that particular fuel assembly or any surrounding fuel 
    assemblies since this movement is confined to within the upper guide 
    structure and the guide tubes of the associated fuel assembly during 
    this activity. This less than six inches of movement does not have 
    the potential to result in a fuel handling accident; therefore, an 
    increase in the probability of this accident does not occur. The 
    requirement to have at least 23 feet of water over the top of the 
    irradiated fuel assemblies during fuel and CEA movement ensures 
    that, should a fuel handling accident occur, the resulting offsite 
    dose consequences are mitigated. The six inch movement of the CEA 
    during CEA decoupling does not constitute fuel or CEA 
    
    [[Page 42605]]
    movement which would result in a fuel handling accident. As such, 
    Technical Specifications are unchanged with respect to the 
    mitigating requirements for a fuel handling accident.
        Therefore, this change does not involve a significant increase 
    in the probability or consequences of any accident previously 
    evaluated.
        Criterion 2 - Does Not Create the Possibility of a New or 
    Different Kind of Accident from any Previously Evaluated.
        The proposed change does not change the design, configuration, 
    or method of operation of the plant; therefore, it does not create 
    the possibility of a new or different kind of accident. Because no 
    new equipment is being introduced, and no equipment is being 
    operated in a manner inconsistent with its design, the possibility 
    of equipment malfunction is not increased. The proposed change adds 
    an exception to the applicability section and is bounded by the 
    existing fuel handling accident analysis.
        Therefore, this change does not create the possibility of a new 
    or different kind of accident from any previously evaluated.
        Criterion 3 - Does Not Involve a Significant Reduction in the 
    Margin of Safety.
        There is no reduction in margin of safety in that 23 feet of 
    water is still maintained over the irradiated fuel assemblies 
    anytime there is a potential for a fuel handling accident. Adding 
    the exception of the latching and unlatching of the CEAs to the 
    applicability section does not involve a change in the accident 
    analysis for fuel handling which remains bounding.
        Therefore, this change does not involve a significant reduction 
    in the margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Tomlinson Library, Arkansas 
    Tech University, Russellville, AR 72801
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., Washington, D.C. 20005-3502
        NRC Project Director: William D. Beckner
    
    Entergy Operations, Inc., et al., Docket No. 50-416, Grand Gulf 
    Nuclear Station, Unit 1, Claiborne County, Mississippi
    
        Date of amendment request: July 21, 1995
        Description of amendment request: The proposed change requests that 
    the current expiration date for license NPF-29 be changed to reflect 
    the issuance date of the new license granted Grand Gulf on November 1, 
    1984. The change consists of extending the expiration date to 40 years 
    from the date of issuance of license NPF-29 (November 1, 1984 to 
    November 1, 2024).
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        a. No significant increase in the probability or consequences of 
    an accident previously evaluated results from this change.
        The proposed change does not affect the design or operation of 
    any plant system. The effect of 40 years of full power operations 
    has previously been evaluated and documented in the Updated Final 
    Safety Analysis Report (UFSAR). The design life of structures, 
    systems and components is controlled by existing plant problems 
    [sic., programs] and processes that are not affected by this change. 
    The proposed change will simply allow Grand Gulf to achieve its 
    original planned 40 years of service. Equipment associated with 
    initiating event frequencies or accident mitigation must continue to 
    meet all applicable maintenance and operability requirements 
    regardless of license duration (It is also interesting to note that 
    the license duration limitation of 40 years, as contained in 10 CFR 
    50.51 is not a limitation resulting from concerns over plant aging 
    effects. ``In fact, the limit was a compromise between the efforts 
    of the Justice Department and electric cooperatives, who championed 
    a 20-year limit on the basis of antitrust concerns, and the view of 
    the utility industries that a longer period was necessary to ensure 
    full amortization of a nuclear power plant.'' (56 FR 64961, December 
    13, 1991)). Therefore, the probability or consequences of previously 
    analyzed accidents are not significantly increased.
        b. The change would not create the possibility of a new or 
    different kind of accident from any previously analyzed.
        The proposed change will not add any plant equipment or 
    introduce any new modes of plant operation. The change will only 
    amend the operating license to allow 40 years of full power 
    operations. The proposed change does not affect the current 
    maintenance or surveillance practices, which are designed to 
    maintain and monitor the current service life of plant structures, 
    systems and components in accordance with regulatory requirements. 
    Therefore, the proposed change does not create the possibility of 
    new equipment failure modes or a new or different kind of accident 
    from any accident previously evaluated.
        c. The change would not involve a significant reduction in a 
    margin of safety.
        The proposed change does not involve a significant reduction in 
    a margin of safety since it only provides for 40 years of full power 
    operations for which the plant is designed. Current Technical 
    Specification surveillance requirements (e.g. associated with 10 CFR 
    50 Appendix H) and other regulatory requirements remain in place and 
    will ensure continued compliance with applicable safety margins.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Judge George W. Armstrong 
    Library, 220 S. Commerce Street, Natchez, Mississippi 39120
        Attorney for licensee: Nicholas S. Reynolds, Esquire, Winston and 
    Strawn, 1400 L Street, N.W., 12th Floor, Washington, DC 20005-3502
        NRC Project Director: William D. Beckner
    
    Philadelphia Electric Company, Docket Nos. 50-352 and 50-353, 
    Limerick Generating Station, Units 1 and 2, Montgomery County, 
    Pennsylvania
    
        Date of amendment request: June 20, 1995
        Description of amendment request: The proposed Technical 
    Specifications (TS) changes would remove the surveillance interval text 
    for the 10 CFR Part 50, Appendix J, Type A test (Integrated Leak Rate 
    Test or ILRT), and Drywell-to-Suppression Chamber (bypass) leakage test 
    specified in TS Surveillance Requirements (SR) 4.6.1.2.a, 4.6.1.2.b, 
    and 4.6.2.1.e.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        1. The proposed TS changes do not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The primary containment and the suppression chamber are not 
    considered to be accident initiators, they are accident mitigators. 
    There are no physical or operational changes to the containment or 
    suppression structure, system or components being made as a result 
    of the proposed changes. These changes will not impose different 
    requirements and adequate control of information will be maintained. 
    These TS changes will not alter assumptions made in the safety 
    analysis and licensing basis. Therefore, the proposed TS changes to 
    eliminate the details of the test intervals will not increase the 
    probability or consequences of an accident previously evaluated.
        2. The proposed TS changes do not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes remove the specific surveillance test 
    interval text from TS and address the interval by direct reference 
    to the applicable regulation. The proposed TS changes do not make 
    any physical or operational changes to existing plant systems or 
    components. Furthermore, the primary containment and suppression 
    chamber act as 
    
    [[Page 42606]]
    accident mitigators not initiators. Therefore, the possibility of a new 
    or different kind of accident than from any accident previously 
    evaluated is not introduced.
        3. The proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        LGS [Limerick Generating Station] TS Bases 3/4 6.1.2 state that 
    surveillance testing is consistent with 10 CFR 50, Appendix J and 
    does not specify a SR test interval. TS Bases 3/4 6.2, describing 
    the bypass test does not specify a SR test interval. However, the 
    NRC Safety Evaluation related to amendment Nos. 68 (Unit 1) and 31 
    (Unit 2) concluded that it is acceptable for the drywell-to-
    suppression chamber test frequency to coincide with the 10 CFR 50, 
    Appendix J, Type A test, since individual vacuum breaker leakage 
    tests are an acceptable alternative to an integrated suppression 
    pool bypass test during outages for which a Type A containment 
    integrated leak rate test is not conducted. The alternative bypass 
    test requirement, TS SR 4.6.2.1.f, is not affected by these changes.
        The Type A test, and bypass SR test intervals are adequately 
    presented in the test implementing procedures, and TS will directly 
    reference 10 CFR 50, Appendix J, for the appropriate test interval.
        Therefore, the proposed TS changes do not involve a significant 
    reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Pottstown Public Library, 500 
    High Street, Pottstown, Pennsylvania 19464.
        Attorney for licensee: J. W. Durham, Sr., Esquire, Sr. V. P. and 
    General Counsel, Philadelphia Electric Company, 2301 Market Street, 
    Philadelphia, Pennsylvania 19101
        NRC Project Director: John F. Stolz
    
    Power Authority of The State of New York, Docket No. 50-286, Indian 
    PointNuclear Generating Unit No. 3, Westchester County, New York
    
        Date of amendment request: July 21, 1995
        Description of amendment request: The proposed amendment would 
    change Technical Specifications Section 6.0 (Administrative Controls) 
    to replace the title-specific list of members on the Plant Operating 
    Review Committee (PORC) with a more general statement of membership 
    requirements. The scope of disciplines represented on the PORC would 
    also be expanded to include nuclear licensing and quality assurance. 
    The proposed amendment would also change the title ``Resident Manager'' 
    to ``Site Executive Officer.'' This title change would not affect the 
    reporting relationship, authority, or responsibility of the position.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        Operation of the Indian Point 3 Nuclear Power Plant in 
    accordance with the proposed amendment would not involve a 
    significant hazards consideration as defined in 10 CFR 50.92, since 
    it would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed changes are administrative in nature and do not 
    involve plant equipment or operating parameters. There is no change 
    to any accident analysis assumptions or other conditions which could 
    affect previously evaluated accidents. The proposed changes will not 
    decrease the organization's ability to respond to a design basis 
    accident.
        2. Create the possibility of a new or different kind of accident 
    from those previously evaluated.
        Since the proposed changes are administrative in nature and do 
    not involve hardware design, modifications or operation, the 
    possibility of new or different accidents is not created.
        3. Involve a significant reduction in the margin of safety.
        The proposed title change for the Resident Manager is an 
    administrative change and does not affect the responsibilities, 
    authority, or reporting relationships for this management position. 
    Replacing the title specific list of PORC members with a statement 
    of membership requirements for the committee does not reduce the 
    effectiveness of the committee to advise the Resident Manager (Site 
    Executive Officer) on matters regarding nuclear safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: White Plains Public Library, 
    100 Martine Avenue, White Plains, New York 10601.
        Attorney for licensee: Mr. Charles M. Pratt, 10 Columbus Circle, 
    New York, New York 10019.
        NRC Project Director: Ledyard B. Marsh
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of amendment request: March 30, 1995
        Description of amendment request: The proposed change to the 
    Technical Specifications (TS) would change TS Table 3.3.1-2, ``Reactor 
    Protection System Response Times'', TS Table 3.3.2-3, ``Isolation 
    System Instrumentation Response Time'', TS Table 3.3.3-3, ``Emergency 
    Core Cooling System Response Times'', and associated Bases. The 
    proposed changes to the above-referenced TS Tables would eliminate the 
    requirement to perform response time testing for certain classes of 
    equipment.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        1. Will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The purpose of the proposed Technical Specification change is to 
    eliminate response time testing requirements for selected 
    instrumentation in the Reactor Protection System, Isolation System, 
    and Emergency Core Cooling System. However, because of the continued 
    application of other existing Technical Specification requirements 
    such as channel calibrations, channel checks, channel functional 
    tests, and logic system functional tests, the response time of these 
    systems will be maintained within the acceptance limits assumed in 
    plant safety analyses and required for successful mitigation of an 
    initiating event. The proposed Technical Specification changes do 
    not affect the capability of the associated systems to perform their 
    intended function within their required response time.
        The BWR Owners' Group has completed an evaluation (NEDO-32291, 
    ``System Analyses for the Elimination of Selected Response Time 
    Testing Requirements'') which demonstrates that response time 
    testing is redundant to the other Technical Specification 
    requirements listed in the preceding paragraph. These other tests 
    are sufficient to identify failure modes or degradation in 
    instruments response time and ensure operation of the associated 
    systems within acceptance limits. There are no known failure modes 
    that can be detected by response time testing that cannot be 
    detected by the other Technical Specification tests. Hope Creek 
    Generating Station is specifically bounded by the assumptions and 
    justifications in General Electric Company Licensing Topical Report, 
    NEDO-32291, ``System Analyses for Elimination of Selected Response 
    Time Testing Requirements.''
        2. Will not create the possibility of a new or different kind of 
    accident from any accident previously evaluated.
        As discussed above, the proposed Technical Specification changes 
    do not affect the capability of the associated systems to perform 
    their intended function within the acceptance limits assumed in 
    plant safety analyses and required for successful mitigation of an 
    initiating event. The proposed elimination of response time testing 
    would not result in any new 
    
    [[Page 42607]]
    equipment, operating modes, or plant configurations.
        3. Will not involve a significant reduction in a margin of 
    safety.
        The current Technical Specification response times are based on 
    the maximum allowable values assumed in the plant safety analyses. 
    These analyses conservatively establish the margin of safety. As 
    described above, the proposed Technical Specification changes do not 
    affect the capability of the associated systems to perform their 
    intended functions within the allowed response time used as the 
    basis for the plant safety analyses. Plant and system response to an 
    initiating event will remain in compliance within the assumptions of 
    the safety analyses, and therefore the margin of safety is not 
    affected.
        Although not explicitly evaluated, the proposed Technical 
    Specification changes will provide an improvement to plant safety 
    and operation by:
        a) Reducing the time safety systems are unavailable
        b) Reducing safety system actuations
        c) Reducing shutdown risk
        d) Limiting radiation exposure to plant personnel
        e) Eliminating the diversion of key personnel to conduct 
    unnecessary testing.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
        Attorney for licensee: M. J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502
        NRC Project Director: John F. Stolz
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of amendment request: April 18, 1995
        Description of amendment request: The proposed changes to the 
    Technical Specifications (TS) would change TS Table 4.3.7.1-1 
    ``Radiation Monitoring Instrumentation Surveillance Requirements.'' 
    This change would increase the channel functional test interval from 
    monthly to quarterly for each instrument.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        1. Will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change involves no hardware changes, no changes to 
    the operation of any systems or components, and no changes to 
    existing structures. Increasing the interval between channel 
    functional tests for the radiation monitoring instrumentation 
    represent changes that do not affect plant safety and do not alter 
    existing accident analyses.
        2. Will not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        The proposed change is procedural in nature concerning the 
    channel functional test frequency for the radiation monitoring 
    instrumentation not already on a quarterly surveillance. The channel 
    functional test methodology for these instruments remains unchanged. 
    The proposed changes, while slightly increasing the possibility of 
    an undetected instrument error, will not create a new or unevaluated 
    accident or operating condition.
        3. Will not involve a significant reduction in a margin of 
    safety.
        The proposed change is in accordance with recommendations 
    provided by the NRC regarding the improvement of Technical 
    Specifications. These changes will result in perpetuation of current 
    safety margins while reducing regulatory burden and decreasing 
    equipment degradation.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070
        Attorney for licensee: M. J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502
        NRC Project Director: John F. Stolz
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of amendment request: May 4, 1995
        Description of amendment request: The proposed change to the 
    Technical Specifications (TS) would change TS 3/4.6.1.8, ``Drywell and 
    Suppression Chamber Purge System'', to increase the annual operational 
    limit for the drywell and suppression chamber purge system from 120 to 
    500 hours.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        1. Will not involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The proposed change involves no hardware changes and no changes 
    to existing structures. Increasing the annual operational limit of 
    the drywell and suppression chamber purge system will not increase 
    the probability of a loss-of-coolant accident. While increased usage 
    of the purge system will result in a slight increase in the 
    possibility that these valves will be open during a LOCA, it will 
    not alter or impact previous LOCA analyses.
        2. Will not create the possibility of a new or different kind of 
    accident from any previously evaluated.
        The proposed change will not result in an unanalyzed condition. 
    While the increase in purge system operation will slightly increase 
    the possibility of the containment vent and purge valves being open 
    at the onset of a LOCA event, the valves have been established as 
    capable of isolating the containment within five seconds. This is 
    well within the bounds of existing LOCA analyses which assume an 
    open duration of 175 seconds. Therefore, this change will not 
    require a new or different accident analysis.
        3. Will not involve a significant reduction in a margin of 
    safety.
        The proposed change will not alter existing systems, equipment, 
    components, or structures. The method of operating the drywell and 
    suppression chamber purge system will not be altered by the 
    increased annual usage. While there is a slight increase in the 
    possibility of purge operations at the onset of a LOCA, any 
    resulting release would be insignificant and bounded by existing 
    LOCA analyses. Operation of the drywell and suppression chamber 
    purge system based on these proposed changes will remain within the 
    guidance provided in the NRC's Branch Technical Position CSB 6-4.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location:  Pennsville Public Library, 
    190 S. Broadway, Pennsville, New Jersey 08070
        Attorney for licensee: M. J. Wetterhahn, Esquire, Winston and 
    Strawn, 1400 L Street, NW., Washington, DC 20005-3502
        NRC Project Director: John F. Stolz
    
    Saxton Nuclear Experimental Corporation (SNEC), Docket No. 50-146, 
    Saxton Nuclear Experimental Facility (SNEF), Bedford County, 
    Pennsylvania
    
        Date of amendment request: June 2, 1995, as supplemented on June 
    23, 1995.
        Description of amendment request: The proposed changes to the 
    technical specifications are administrative in 
    
    [[Page 42608]]
    nature. The proposed amendment would revise the organization structure 
    associated with the SNEF to allow General Public Utilities Nuclear 
    Corporation resources to be applied to SNEC activities within their 
    normal organizational structure; eliminating the need to identify and 
    compartmentalize a portion of the organization as specific to SNEC. The 
    proposed amendment would also revise the description and drawing of the 
    SNEF site to reflect multiple gates in the SNEF fence.
        Basis for proposed no significant hazards 
    considerationDetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below: The proposed changes 
    do not involve a significant hazards considerations because the changes 
    would not:
        1. Involve a significant increase in the probability or 
    consequences of an accident previously evaluated.
        The administrative changes will not impact the physical 
    condition of the containment vessel as it relates to the risk of 
    fire, flood or radiological hazard.
        2. Create the possibility of a new or different kind of accident 
    from any previously analyzed.
        In its present condition, the only accidents applicable to the 
    site are those addressed above.
        3. Involve a significant reduction in a margin of safety.
        The proposed administrative changes would have no effect on any 
    margins of safety for any evaluated accidents.
        The NRC staff has reviewed the analysis of the licensee and, based 
    on this review, it appears that the three standards of 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location:  Saxton Community Library, 911 
    Church Street, Saxton, Pennsylvania 16678Attorney for the Licensee: 
    Ernest L. Blake, Jr., Esquire, Shaw, Pittman, Potts, and Trowbridge, 
    2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: Seymour H. Weiss
    
    South Carolina Electric & Gas Company, South Carolina Public 
    Service Authority, Docket No. 50-395, Virgil C. Summer Nuclear 
    Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of amendment request: June 30, 1995
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TS) for the pressurizer power 
    operated relief valves (PORVs) to follow the guidance of Generic Letter 
    (GL) 90-06, Generic Issue 70, and the improved Westinghouse 
    Standardized Technical Specifications (NUREG-1431, Rev. 1).
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        1. The probability or consequences of an accident previously 
    evaluated is not significantly increased.
        There is no increase in the probability of an accident because 
    the physical characteristics of the PORVs and their block valves 
    remain unchanged. No changes to any hardware or software that 
    affects these components is planned.
        The PORVs are pressure relieving devices and only two failure 
    modes need to be considered. The first is that one or more PORVs or 
    block valves fail to open when required. This is not
        a significant concern and is not a credible cause of any 
    accident. The second mode is failing to close which includes 
    depressurization of the RCS [reactor coolant system] and a reactor 
    trip on low pressurizer pressure or overtemperature [delta]T. The 
    consequences for the more limiting Pressurizer Safety Valve 
    Accidental Depressurization event has been analyzed with acceptable 
    results.
        There is no increase in the consequences of an accident as a 
    result of this change, because only one PORV is required to mitigate 
    the consequences of a design basis Steam Generator Tube Rupture. 
    There is sufficient redundancy to ensure one PORV is available to 
    perform this function even if one PORV is inoperable or incapable of 
    being manually cycled. The validation of the Emergency Operating 
    Procedures on the VCSNS [Virgil C. Summer Nuclear Station] simulator 
    demonstrated that one pressurizer PORV has sufficient capacity to 
    depressurize the RCS in a time frame which will not cause the 
    offsite doses presented in the FSAR [Final Safety Analysis Report] 
    to be exceeded.
        The PORVs are utilized to depressurize the RCS and equalize the 
    pressure between the primary and secondary systems. This stops the 
    intrusion of RCS water into the secondary which can be released into 
    the atmosphere. By the time the PORVs are called upon, the affected 
    steam generator (SG) has been identified and steps have been taken 
    to isolate the faulted SG. This acts to minimize the radiological 
    impact on the health and safety of the public. In all cases, the 
    dose results are within 10 CFR 100 limits.
        2. The possibility of an accident or a malfunction of a 
    different type than any previously evaluated is not created.
        The proposed TSCR [TS Change Request] does not involve any 
    physical changes to the plant or decrease the number of PORVs and 
    block valves that must be capable of performing their intended 
    function. These components are used to mitigate the effects of 
    postulated events and their failure has already been considered. The 
    worst case failure, either not opening or not closing, has been 
    evaluated and is bounded by other more limiting accidents.
        3. The margin of safety has not been significantly reduced.
        The currently approved TS permits all three PORVs and/or their 
    block valves to be inoperable as long as precautions are taken to 
    assure that RCS would not leak-by, assuming single failures and 
    spurious operation. The proposed TSCR would require a minimum of two 
    PORVs and block valves to be operable, or at least capable of being 
    manually cycled, in Modes 1, 2, and 3. This is in fact an increase 
    in margin and provides for greater reliability with the added 
    benefit that the probability of challenges to the pressurizer code 
    safety valves will be lessened.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180
        Attorney for licensee: Randolph R. Mahan, South Carolina Electric & 
    Gas Company, Post Office Box 764, Columbia, South Carolina 29218
        NRC Project Director: Frederick J. Hebdon
    
    South Carolina Electric & Gas Company (SCE&G), South Carolina 
    Public Service Authority, Docket No. 50-395, Virgil C. Summer 
    Nuclear Station, Unit No. 1, Fairfield County, South Carolina
    
        Date of amendment request: July 28, 1995
        Description of amendment request: The proposed amendment would 
    revise the Technical Specifications (TS) to exclude the requirement to 
    perform the slave relay test of the 36-inch containment purge supply 
    and exhaust valves on a quarterly basis while the plant is in Modes 1, 
    2, 3, or 4.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        1. Does the change involve a significant increase in the 
    probability or consequences of an accident previously evaluated?
        No, the probability or consequences of an accident previously 
    evaluated would not be increased since no credit is taken for the 
    valves in FSAR [Final Safety Analysis Report] Chapter 15.
        The only credible accident discussed in FSAR Chapter 15 that 
    applies to these valves is a fuel handling accident inside 
    
    [[Page 42609]]
    containment (15.4.5.1). The analysis assumes the escaped gases are 
    released instantaneously to the environment via the Reactor
        Building purge system. The analysis does not take credit for 
    these valves nor for filtration or holdup time during release. The 
    result of the analysis is acceptable and offsite doses are within 
    the limits of 10 CFR 100.
        TS 3.6.1.7 requires that these valves be sealed shut during 
    Modes 1, 2, 3, and 4. When sealed shut, these valves will not open 
    via any signal.
        With these valves already in a shut position, neither the 
    probability nor the consequences of an accident are increased.
        2. Does the change create the possibility of a new or different 
    kind of accident from any previously evaluated?
        No, the 36'' [inch] containment purge exhaust and supply valves 
    will not be placed in a condition different from that evaluated 
    previously.
        The only credible accident discussed in FSAR Chapter 15 that 
    applies to these valves is a fuel handling accident inside 
    containment (15.4.5.1). The analysis assumes the escaped gases are 
    released instantaneously to the environment via the Reactor Building 
    purge system. The analysis does not take credit for these valves nor 
    for filtration or holdup time during release. The result of the 
    analysis is acceptable and offsite doses are within the limits of 10 
    CFR 100.
        Additionally, TS 3.6.1.7. requires that these valves be sealed 
    shut during Modes 1, 2, 3, and 4. When sealed shut, these valves 
    will not open via any signal.
        3. Does the change involve a significant reduction in the margin 
    of safety?
        TS 4.3.2.1. requires that this slave relay test be performed 
    quarterly. This surveillance is accomplished for the 36'' [inch] 
    containment purge exhaust and supply valves by cycling the 
    respective K615 relay. This will not provide assurance that the 
    valve will perform its safety function since the valve is sealed 
    closed. The proposed change will exclude the requirement to perform 
    the K615 relay test (auto actuation logic and actuation relays - 
    slave relay test) on a quarterly basis while the plant is in Modes 
    1, 2, 3,or 4.
        TS 3.6.1.7. requires that these valves be sealed shut during 
    Modes 1, 2, 3, and 4. When sealed shut, these valves will not open 
    via any signal. Since this relay would not be needed to supply a 
    signal to place these valves in the closed position, the margin of 
    safety is not affected.
        Based on the preceding analysis, SCE&G has determined that this 
    change does no involve a significant hazards consideration.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Fairfield County Library, 300 
    Washington Street, Winnsboro, SC 29180
        Attorney for licensee: Randolph R. Mahan, South Carolina Electric & 
    Gas Company, Post Office Box 764, Columbia, South Carolina 29218
        NRC Project Director: Frederick J. Hebdon
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260 and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2 and 3, Limestone County, 
    Alabama
    
        Date of amendment request: June 2, 1995 (TS 353)
        Description of amendment request: The proposed amendment supports 
    replacement of the existing power range neutron monitoring equipment 
    and implements ARTS/MELLL [average power range monitor and rod block 
    monitor technical specifications/maximum extended load line limit] 
    analysis improvements.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        Group A Changes: This proposed TS change is associated with the 
    NUMAC PRNM [nuclear measurement analysis and control power range 
    neutron monitor] retrofit design. The proposed TS change involves 
    modification of the LCOs [limiting condition for operations] and SRs 
    [surveillance requirements] for equipment designed to mitigate 
    events which result in power increase transients. For the APRM 
    [average power range monitor] system mitigative action is to block 
    control rod withdrawal or initiate a reactor scram which terminates 
    the power increase when setpoints are exceeded. For the RBM [rod-
    block monitor] system mitigative action is to block continuous 
    control rod withdrawal prior to exceeding the MCPR [minimum critical 
    power ratio] safety limit during a postulated Rod Withdrawal Error 
    [RWE]. The worst case failure of either the APRM or the RBM systems 
    is failure to initiate mitigative action (failure to scram or block 
    rod withdrawal). Failure to initiate mitigative action will not 
    increase the probability of an accident. Thus, the proposed change 
    does not increase the probability of an accident previously 
    evaluated.
        For the APRM and the RBM systems, the NUMAC PRNM design, 
    together with revised operability requirements (LCOs) and revised 
    testing requirements (SRs), results in equipment which continues to 
    perform the same mitigation functions under identical conditions 
    with reliability equal to or greater than the equipment which it 
    replaces. Because there is no change in mitigation functions and 
    because reliability of the functions is maintained, the proposed 
    change does not involve an increase in the consequences of an 
    accident previously evaluated.
        Group B Changes: This proposed change is associated with 
    implementation of the ARTS/MELLL analysis. The proposed change will 
    permit expansion of the current allowable power/flow operating 
    region and will apply a new methodology for assuring that fuel 
    thermal and mechanical design limits are satisfied. Reference 3 
    evaluates operation in the MELLL region with assumed implementation 
    of the ARTS changes. The conclusion of reference 3 is that for all 
    events and parameters considered there is adequate design margin for 
    operation in the MELLL region. Because operation in the MELLL region 
    maintains adequate design margin, the proposed change does not 
    significantly increase the probability of an accident previously 
    evaluated.
        In support of operation in the MELLL region, the proposed change 
    modifies flow-biased APRM scram and rod block setpoints and 
    implements new RBM power-biased setpoints. This potentially changes 
    the way in which the APRM and RBM systems perform their mitigation 
    functions. However, no credit for the flow-biased APRM scram or rod 
    block is taken in mitigation of any design basis event; thus, 
    changing the APRM setpoints does not impact the consequences of any 
    accident previously evaluated. The proposed changes to the RBM 
    system potentially impact mitigation of the RWE. However, per 
    discussion in reference 3, the proposed RBM changes will assure that 
    the RWE is not a limiting event; thus, the consequences of the RWE 
    are not increased. The proposed change does not increase the 
    consequences of an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed changes (Group A and Group B) involve modification 
    and replacement of the existing power range neutron monitoring 
    equipment, modification of the setpoints and operational 
    requirements for the APRM and RBM systems, implementation of a new 
    methodology for administering compliance with fuel thermal limits, 
    and operation in an extended power/flow domain. These proposed 
    changes do not modify the basic functional requirements of the 
    affected equipment, create any new system interfaces or 
    interactions, nor create any new system failure modes or sequence of 
    events that could lead to an accident. The worst case failure of the 
    affected equipment is failure to perform a mitigation action, and 
    failure of this mitigative equipment does not create the possibility 
    of a new or different kind of accident. The proposed change does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        Group A Changes: This proposed TS change is associated with the 
    NUMAC PRNM retrofit design. The NUMAC PRNM change does not impact 
    reactor operating parameters nor the functional requirements of the 
    power 
    
    [[Page 42610]]
    range neutron monitoring system. The replacement equipment continues to 
    provide information, enforce control rod blocks and initiate reactor 
    scrams under appropriate specified conditions. The proposed change 
    does not revise any safety margin requirements. The replacement 
    APRM/RBM equipment has improved channel trip accuracy compared to 
    the current system and meets or exceeds system requirements 
    previously assumed in setpoint analysis. Thus, the ability of the 
    new equipment to enforce compliance with margins of safety equals or 
    exceeds the ability of the equipment which it replaces. The proposed 
    change does not involve a reduction in a margin of safety.
        Group B Changes: This proposed change is associated with 
    implementation of recommendations presented in the ARTS/MELLL 
    analysis. Operation in the MELLL region does not affect the ability 
    of the plant safety-related trips or equipment to perform their 
    functions, nor does it cause any significant increase in offsite 
    radiation doses resulting from any analyzed event. Analyses 
    documented in reference 3 demonstrate that for operation in the 
    MELLL region adequate margin to design limits is maintained. 
    Implementation of the ARTS improvements provides flow- and power-
    dependent thermal limits which maintain existing margins of safety 
    in normal operation, anticipated operational occurrences and 
    accident events. Implementation of power-biased RBM setpoints 
    improves the margin of safety in a postulated RWE by assuring that 
    the RWE is not a limiting event. The proposed change does not 
    involve a significant reduction in a margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Athens Public Library, South 
    Street, Athens, Alabama 35611
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET llH, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260 and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2 and 3, Limestone County, 
    Alabama
    
        Date of amendment request: June 8, 1995 (TS 361)
        Description of amendment request: The proposed amendment clarifies 
    the definition of operability for the RHRSW system standby coolant 
    supply capability and revises the instrument numbers for several 
    instruments that have been upgraded.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The proposed change to TS 3.5.C.3 clarifies the operability 
    requirements of the standby coolant supply capability. It does not 
    change or degrade the nuclear safety characteristics of the RHRSW 
    and RHR systems and will not affect the intent of the TS. The 
    operation of the standby coolant supply capability is not a 
    precursor to any design basis accident or transient analyzed in the 
    BFN FSAR. The proposed changes to instrument numbers are 
    administrative changes for the upgraded drywell temperature and 
    pressure instrumentation. The proposed changes do not affect the 
    design basis or the safety functions of the Primary Containment 
    system, since the function and instrumentation range is not changed. 
    Therefore, the probability of occurrence or the consequences of an 
    accident or malfunction of equipment important to safety previously 
    evaluated in the safety analysis report has not been increased.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The possibility for an accident or malfunction of a different 
    type than any evaluated previously in the safety analysis report is 
    not created by this change. The change to TS 3.5.C.3 adds the 
    indication of associated valves of the function involved and a 
    clarification of operability for the standby coolant supply 
    connection to be commensurate with the RHR cross-connect capability. 
    The proposed changes to instrument numbers are administrative 
    changes effected by the upgrade of instrumentation. There are no 
    automatic actions affected or compromised by these changes.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The proposed change to TS 3.5.C.3 does not affect any acceptable 
    limit of operation or analysis assumption in the TS or Bases. The 
    changes affect neither setpoints, calibration intervals, nor 
    functional test intervals. The change does not affect any acceptable 
    limit of operation or analysis assumption found in the TS or their 
    bases. The proposed administrative changes to the instrument numbers 
    do not affect the setpoint, calibration interval or function of the 
    instrumentation. These changes do not affect any limiting conditions 
    of operation or analysis assumption in the TSs or their bases. 
    Therefore, the change does not reduce the margin of safety as 
    defined in the basis for any TS.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Athens Public Library, South 
    Street, Athens, Alabama 35611
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET llH, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    Tennessee Valley Authority, Docket Nos. 50-259, 50-260 and 50-296, 
    Browns Ferry Nuclear Plant, Units 1, 2 and 3, Limestone County, 
    Alabama
    
        Date of amendment request: June 16, 1995 (TS 360)
        Description of amendment request: The proposed change will revise 
    the BFN Units 1, 2, and 3 Technical Specifications (TS) to permit the 
    Traversing In-Core Probe (TIP) system to be considered operable with 
    less than five TIP machines operable. The proposed amendment will allow 
    the utilization of substitute data in lieu of data from inaccessible 
    TIP measurement locations. The substitute data will be derived from 
    either symmetric TIP measurement locations (under certain core 
    conditions) or from normalized TIP data as calculated by the on-line 
    core monitoring system.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration, which is presented below:
        1. The proposed amendment does not involve a significant 
    increase in the probability or consequences of an accident 
    previously evaluated.
        The TIP system is not used to prevent, or mitigate the 
    consequences of any previously analyzed accident or transient; nor 
    are any assumptions made in any accident analysis relative to the 
    operation of the TIP system. The primary containment isolation 
    function (TIP withdrawal) is not affected. The
        proposed TS change does not alter the fundamental process 
    involved in calibrating neutron instrumentation (LPRMs) [local power 
    range monitors], but requires that only the equipment associated 
    with the TIP channels necessary for recalibrating LPRMs and for core 
    monitoring functions be operable. Collection and storage of TIP data 
    without using all TIP channels is acceptable because TIP machine 
    normalization factors are ultimately derived from the most recent 
    full core TIP set, which intercalibrates the TIP machines in a 
    common core location.
        Additionally, the use of symmetric detectors and analytical 
    values as substitute data for inaccessible TIP channels does not 
    compromise the ability of the process computer to accurately 
    represent the spatial neutron flux distribution of the reactor core. 
    
    
    [[Page 42611]]
    The core monitoring methodology is presently based on symmetry of rod 
    patterns and fuel loading. This is not changed but extended to use a 
    higher order of symmetry (octant symmetry) which exists with ``type 
    A'' sequence rod patterns. Therefore, this change does not increase 
    the probability or consequences of an accident previously evaluated.
        2. The proposed amendment does not create the possibility of a 
    new or different kind of accident from any accident previously 
    evaluated.
        The proposed change does not involve the installation of any new 
    equipment, or the modification of any equipment designed to prevent 
    or mitigate the consequences of accidents or transients. Therefore, 
    the proposed amendment does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed amendment does not involve a significant 
    reduction in a margin of safety.
        The total core TIP reading uncertainties will remain within the 
    assumptions of the licensing basis. Therefore, the margin of safety 
    to the MCPR [minimum critical power ratio] safety limits is not 
    reduced. The ability of the process computer to accurately represent 
    the spatial neutron flux distribution for the reactor core is not 
    compromised. Additionally, the computer's ability to accurately 
    predict the LHGR [linear heat generation rate], APLHGR [average 
    planar linear heat generation rate], MCPR and its ability to provide 
    for LPRM calibration is not compromised. Therefore, the proposed 
    changes do not involve a significant reduction in a margin of 
    safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Athens Public Library, South 
    Street, Athens, Alabama 35611
        Attorney for licensee: General Counsel, Tennessee Valley Authority, 
    400 West Summit Hill Drive, ET llH, Knoxville, Tennessee 37902
        NRC Project Director: Frederick J. Hebdon
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of amendment request: October 21, 1994
        Description of amendment request: The proposed amendment would 
    revise Technical Specification (TS) 3/4.6.1.2, ``Primary Containment 
    Leakage.'' The changes would clarify that the main steam line isolation 
    valves leakage is accounted for separately from the integrated primary 
    containment leak rate or combined local leak rate results. Also, two 
    references would be deleted, the test duration for use of Bechtel 
    Corporation Topical Report BN-TOP-1 would be clarified, and the 
    requirement to perform the third integrated leak rate in each 10-year 
    service period in conjunction with the 10-year plant inservice 
    inspection would be deleted. Exemptions to 10 CFR Part 50 Appendix J, 
    ``Primary Reactor Containment Leakage Testing for Water-Cooled Power 
    Reactors,'' are also being requested in conjunction with the proposed 
    TS changes.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration which is presented below:
        Part A - Formalize the Approval for Excluding the Main Steam 
    Line Isolation Valve Leakages from Inclusion in i) the Overall 
    Integrated Primary Containment Leak Rate and ii) the Combined Local 
    Leak Rate, and Clarify that the Main Steam Lines are Not Required to 
    be Vented and Drained for Type A Testing
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        Since Appendix J was originally envisioned, alternative means of 
    meeting the intent of these requirements have been developed which 
    provide an equivalent level of protection of the public health and 
    safety. However, since some of these alternatives deviate from the 
    specific wording of Appendix J, exemptions are appropriate for these 
    alternatives. Implicit in the FSAR treatment of the main steam line 
    leakage, as well as the TS requirements for main steam line leakage, 
    are several deviations from the specific requirements of Appendix J. 
    Although PNPP's methods and practices for Appendix J testing have 
    been previously described in correspondence to the NRC, a formal 
    exemption was not recognized to be needed at that time in that the 
    NRC's approval was perceived to be received by the issuance of the 
    PNPP TS. Exemption to four separate paragraphs of 10 CFR 50 Appendix 
    J will document the approvals previously received and incorporated 
    into the TS for main steam line isolation valve testing during the 
    initial licensing of the PNPP. This TS change adds references to 
    footnotes within the TS LCO 3.6.3.1 to clarify which conditions 
    represent exemptions to Appendix J. These exemptions are described 
    in the Bases.
        PNPP utilized the criteria described in the Standard Review Plan 
    (SRP), Section 15.6.5, Appendix D, ``Radiological Consequences of a 
    Design Basis Loss-of-Coolant Accident: Leakage from Main Steam 
    Isolation Valve Leakage Control System (Rev. 1 - July 1981).'' This 
    is an alternative, NRC approved method for assessing the MSIV 
    leakage contribution and determining the radiological consequences.
        In accordance with the SRP, the safety analysis for a design 
    basis LOCA includes the maximum main steam line leak rate separately 
    from the maximum containment leak rate. Within Appendix J it is 
    implied that Type A tests are intended to measure the primary 
    containment overall integrated leak rate, but this vas before the 
    SRP Section was developed which allows the MSIV contribution to be 
    accounted for separately in the safety analysis. Therefore, the MSIV 
    leak rate should not be included in the measurement of the ILRT. 
    Including the MSIV leakage in the combined local leak rate limit is 
    also not necessary since a specific Type C MSIV leak rate has been 
    specified in TS 3.6.1.2.
        In summary, there is no change in the probability or 
    consequences of any accident since the addition of the references 
    and footnotes to clarify the TS LCO and Actions do not change the 
    design of the plant, nor the operational characteristics of any 
    plant system, nor the procedures by which the Operators run the 
    plant. These changes only cite formal Appendix J exemptions which 
    are requested to document the approval previously received. A formal 
    request for exemption to the applicable paragraphs of 10 CFR 50 
    Appendix J is also being submitted in a separate letter in 
    conjunction with this proposed TS change.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated. 
    There are no design changes being made that would create a new type 
    of accident or malfunction, and the method and manner of plant 
    operation remains unchanged. The only change being made is an 
    exemption to 10 CFR 50 Appendix J which will be cited in the TS to 
    document the implicit and explicit approvals of the PNPP design and 
    testing methods for main steam line isolation valves. The 
    requirements and bases for which the formal exemption is sought are 
    currently presented and implemented in the licensing basis and the 
    TS for PNPP. The objective of the regulation is being met and will 
    continue to be met. The exemption to 10 CFR 50 Appendix J is being 
    submitted in a separate letter in conjunction with this proposed TS 
    change.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        These changes do not involve a significant reduction in the 
    margin of safety because they are administrative in nature. The 
    proposed change will only cite the NRC exemption that grants the 
    deviation from Appendix J. The proposed changes do not affect any 
    USAR design bases or accident assumptions. Therefore, the proposed 
    changes do not reduce the margin of safety as defined in the bases 
    for any Technical Specification.
        Part B - Revise Surveillance Requirement 4.6.1.2 to Eliminate 
    Unnecessary References and ClarifY the Use of BN-TOP-1 
    
    [[Page 42612]]
    
        1. The proposed changes do not involve a significant increase in 
    the probability or consequences of an accident previously evaluated.
        Surveillance Requirement 4.6.1.2 is proposed to be revised to 
    eliminate the direct reference to the ANSI Standards N45.4 and N56.8 
    within the text, because these same Standards are listed within 
    Appendix J. It is unnecessary to repeat the references to the 
    Standards within the Technical Specifications because the PNPP is 
    still required to be in compliance with the regulations. No 
    additional benefits are gained and licensee flexibility to upgrade 
    to later versions of the Standards is reduced since a Technical 
    Specification change is necessary to change the version of the 
    Standard to which PNPP is committed. This change removes a redundant 
    requirement to list these Standards in the Technical Specifications. 
    Therefore, this change cannot involve a significant increase in the 
    probability or consequences of an accident because the regulation is 
    still required to be met.
        A reference to Topical Report BN-TOP-1 continues to be retained 
    within Surveillance Requirement 4.6.1.2, and the use of the report 
    is clarified to be for test durations less than 24 hours. This 
    reference is retained within the TS since a reference to BN-TOP-1, 
    though not specifically included within Appendix J, is allowed by 
    Section 7.6 of ANSI N45.4-1972 and has been approved for PNPP use by 
    the NRC. The TS Bases are also proposed to be revised to include a 
    statement that the use of BN-TOP-1 is in accordance with Appendix J.
        These changes result in no changes to plant systems and have no 
    effect on accident conditions or assumptions. These proposed changes 
    do not affect possible initiating events for accidents previously 
    evaluated, or any system functional requirements. Hence, these 
    changes are purely administrative in that they are designed to 
    eliminate a redundant requirement and clarify the applicability and 
    acceptability of an alternative leak rate testing provision within 
    the TS. These changes do not affect plant operation in any way. 
    Therefore, the proposed changes do not affect the probability or 
    consequences of any accident previously evaluated.
        2. The proposed changes do not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        There are no design changes being made that would create a new 
    type of accident or malfunction, and the method and manner of plant 
    operation remains unchanged. These changes eliminate a redundant 
    requirement and clarify the applicability and acceptability of 
    alternative leak rate testing provisions within the TS. Since the 
    alternative leak rate testing provisions have been approved by the 
    NRC, the objective of the regulation continues to be met. Therefore, 
    the proposed changes do not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed changes do not involve a significant reduction 
    in a margin of safety.
        These changes do not involve a significant reduction in the 
    margin of safety because they are administrative in nature and 
    either eliminate a redundant requirement or clarify the 
    applicability and acceptability of an alternative, NRC approved, 
    leak rate testing provision within the TS. The proposed changes do 
    not affect any USAR design bases or accident assumptions. Therefore, 
    the proposed changes do not reduce the margin of safety as defined 
    in the Bases for any Technical Specification.
        Part C - Decouple Performance of the Third Type A Test from the 
    Shutdown for the 10-Year Plant Inservice Inspection
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed change revises Surveillance Requirement 4.6.1.2.a 
    by removing the second sentence requiring that the third test of 
    each containment Integrated Leak Rate Test (ILRT) set be conducted 
    during the shutdown for the 10-year plant inservice inspection. A 
    request for an exemption to 10 CFR 50 Appendix J, Paragraph 
    III.D.l(a) is also being submitted in conjunction with this proposed 
    change. Note that this change is also included in the proposed 
    Appendix J rule changes currently under consideration and has been 
    approved for several other plants. The deletion of this requirement 
    from the Technical Specifications does not impact plant safety 
    because the 10 CFR 50 Appendix J requirement that three Type A 
    containment ILRT tests to be performed over a 10 year period is not 
    affected. This change only removes an unnecessary connection between 
    the two regulations.
        The proposed change results in no changes to plant systems. The 
    proposed change has no effect on accident conditions or assumptions. 
    The proposed change does not affect possible initiating events for 
    accidents previously evaluated, or any system functional 
    requirements. Hence, the proposed change removes an unnecessary tie 
    between regulations and does not affect plant operation in any way.
        In summary, there is no change in the probability or 
    consequences of any accident since the revision of the existing 
    Surveillance Requirement to reflect the removal of an unnecessary 
    tie between regulations does not change the design of the plant, nor 
    the operational characteristics of any plant system, nor the 
    procedures by which the Operators run the plant.
        2. The propose change does not create the possibility of a new 
    or different kind of accident from any accident previously 
    evaluated.
        The proposed change removes an unnecessary tie between 
    regulations. The objective of the regulation continues to be met. 
    There are no design changes being made that would create a new type 
    of accident or malfunction, and the method and manner of plant 
    operation remains unchanged. Therefore, the proposed change does not 
    create the possibility of a new or different kind of accident from 
    any accident previously evaluated.
        3. The proposed change does not involve a significant reduction 
    in a margin of safety.
        The proposed change does not involve a significant reduction in 
    the margin of safety because they are administrative in nature and 
    remove an unnecessary tie between requirements. The proposed change 
    does not affect any USAR design bases, accident assumptions. or 
    Technical Specification Bases. Therefore, the proposed change does 
    not reduce the margin of safety as defined in the bases for any TS.
        Based upon the above considerations, it has been concluded that 
    the proposed changes do not involve significant hazards 
    considerations.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Gail H. Marcus
    
    The Cleveland Electric Illuminating Company, Centerior Service 
    Company, Duquesne Light Company, Ohio Edison Company, Pennsylvania 
    Power Company, Toledo Edison Company, Docket No. 50-440, Perry 
    Nuclear Power Plant, Unit No. 1, Lake County, Ohio
    
        Date of amendment request: June 9 and 30, 1995
        Description of amendment request: The licensee has requested a one-
    time extension of the performance intervals for certain Technical 
    Specification Surveillance Requirements (SRs). Affected SRs include 
    valve testing, and undervoltage instrumentation testing.
        Basis for proposed no significant hazards 
    considerationdetermination: As required by 10 CFR 50.91(a), the 
    licensee has provided its analysis of the issue of no significant 
    hazards consideration which is presented below:
        1. The proposed change does not involve a significant increase 
    in the probability or consequences of an accident previously 
    evaluated.
        The proposed TS change requests one-time only extensions of the 
    surveillance intervals related to: a) ASME Section XI valve leak 
    rate, stroke and timing, and position indication testing; b) 
    Accident Monitoring Instrumentation related to valve position 
    indication testing; c) Division 1, 2, and 3 Degraded Voltage and 
    Undervoltage instrumentation LSFT; and, d) leak rate testing for 
    hydrostatically tested containment isolation valves.
        Based on the discussion in the License Amendment Request which 
    shows:
        i) The extension of the interval for ASME Section XI stroke and 
    timing, leak rate measurement and position indication testing 
    
    [[Page 42613]]
    requirements are acceptable based on results of past testing which 
    indicates a margin to TS limits will be maintained;
        ii) The extension of the interval for Position Indication 
    Calibration as specified in Table 4.3.7.5-1, Item 17 is acceptable 
    based on the testing results from the past two refueling outages 
    that indicate no failures have occurred:
        iii) LSFT interval extension for the Division 1, 2, and 3 
    Degraded Voltage and Undervoltage instrumentation is acceptable 
    based on the NRC Safety Evaluation Report (Peach Bottom Atomic Power 
    Plant, Units 2 and 3, dated August 2, 1993) which supported 
    extension of the interval for LSFT from 18 to 24 months. This was 
    based on the small probability of relay or contact failure relative 
    to mechanical component failure probability and, therefore, the 
    increase in LSFT interval represented no significant change in the 
    overall safety system unavailability; and,
        iv) The extension of the interval for hydrostatic leak testing 
    of containment isolation valves is acceptable based on the 
    consistently low past leak rate data which is a small percentage of 
    the TS limits.
        Therefore, from the above it is shown that the proposed changes 
    will not significantly increase the probability of an accident 
    previously evaluated.
        The proposed TS change requests one-time only extensions of the 
    surveillance intervals related to TS SR 4.3.3.1, Table 4.3.3.1-1, 
    Items D.1 and D.2, Division 1, 2, and 3 Degraded Voltage and 
    Undervoltage instrumentation calibration. [...] extension of the 
    interval for this instrumentation is acceptable based on the testing 
    results from the past two refueling outages. No failures have 
    occurred which would negate the assurance that the instrumentation 
    would function as required for the requested extended period. 
    Accordingly, the proposed change will not significantly increase the 
    probability or consequences of an accident previously evaluated.
        2. The proposed change would not create the possibility of a new 
    or
        different kind of accident from any accident previously 
    evaluated.
        The proposed TS change requests one-time extensions of the 
    surveillance intervals for ASME Section XI valve testing, 
    instrumentation calibration, instrument channel LSFT, containment 
    isolation valve hydrostatic leak rate testing. The proposed changes 
    do not necessitate a physical alteration to the plant (no new or 
    different type of equipment will be installed). In that the 
    requested extension durations are small as compared to the overall 
    interval allowed by TS, NRC and industry evaluations support 
    extension of LSFT, and past testing results provide confidence of no 
    effect on equipment availability by extending the surveillance 
    interval, the change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        The proposed TS change requests one-time extensions of the 
    surveillance intervals for the Division 1, 2, and 3 Undervoltage and 
    Degraded Voltage instrumentation calibration. The proposed changes 
    do not necessitate a physical alteration to the plant (no new or 
    different type of equipment will be installed). In that the 
    requested extension durations are small as compared to the overall 
    interval allowed by TS and past testing results provide confidence 
    of no effect on equipment availability by extending the surveillance 
    interval, the change does not create the possibility of a new or 
    different kind of accident from any accident previously evaluated.
        3. The proposed change will not involve a significant reduction 
    in the margin of safety.
        The proposed TS change requests a one-time extension of the 
    surveillance intervals for ASME Section XI valve testing, 
    instrumentation calibration, instrument channel LSFT, and 
    containment isolation valve hydrostatic leak rate testing. The 
    proposed changes do not necessitate a physical alteration to the 
    plant (no new or different type of equipment will be installed). In 
    that the requested extension durations are small as compared to the 
    overall interval allowed by TS, NRC and industry evaluations support 
    extension of LSFT, and past testing results provide confidence of no 
    effect on equipment availability by extending the surveillance 
    interval, the change does not involve a significant reduction in the 
    margin of safety.
        The proposed TS change requests a one-time extension of the 
    surveillance intervals for the division 1, 2, and 3 Undervoltage and 
    Degraded Voltage instrumentation calibration. The proposed changes 
    do not necessitate a physical alteration to the plant (no new or 
    different type of equipment will be installed). In that the 
    requested extension durations are small as compared to the overall 
    interval allowed by TS and past testing results provide confidence 
    of no effect on equipment availability by extending the surveillance 
    interval, the change does not involve a significant reduction in the 
    margin of safety.
        The NRC staff has reviewed the licensee's analysis and, based on 
    this review, it appears that the three standards of 10 CFR 50.92(c) are 
    satisfied. Therefore, the NRC staff proposes to determine that the 
    amendment request involves no significant hazards consideration.
        Local Public Document Room Location: Perry Public Library, 3753 
    Main Street, Perry, Ohio 44081
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts & 
    Trowbridge, 2300 N Street, NW., Washington, DC 20037
        NRC Project Director: Gail H. Marcus
    
    Previously Published Notices Of Consideration Of Issuance Of 
    Amendments To Facility Operating Licenses, Proposed No Significant 
    Hazards Consideration Determination, And Opportunity For A Hearing
    
        The following notices were previously published as separate 
    individual notices. The notice content was the same as above. They were 
    published as individual notices either because time did not allow the 
    Commission to wait for this biweekly notice or because the action 
    involved exigent circumstances. They are repeated here because the 
    biweekly notice lists all amendments issued or proposed to be issued 
    involving no significant hazards consideration.
        For details, see the individual notice in the Federal Register on 
    the day and page cited. This notice does not extend the notice period 
    of the original notice.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments: July 19, 1995
        Description of amendments request: Amend the Sequoyah Nuclear 
    Plant, Units 1 and 2 Technical Specification to incorporate new 
    requirements associated with steam generator tube inspections and 
    repair.
        Date of publication of individual notice in the Federal Register: 
    August 1, 1995 (60 FR 39198)
        Expiration date of individual notice: August 31, 1995
        Local Public Document Room Location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
    Notice Of Issuance Of Amendments To Facility Operating Licenses
    
        During the period since publication of the last biweekly notice, 
    the Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application complies 
    with the standards and requirements of the Atomic Energy Act of 1954, 
    as amended (the Act), and the Commission's rules and regulations. The 
    Commission has made appropriate findings as required by the Act and the 
    Commission's rules and regulations in 10 CFR Chapter I, which are set 
    forth in the license amendment.
        Notice of Consideration of Issuance of Amendment to Facility 
    Operating License, Proposed No Significant Hazards Consideration 
    Determination, and Opportunity for A Hearing in connection with these 
    actions was published in the Federal Register as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these 
    
    [[Page 42614]]
    amendments. If the Commission has prepared an environmental assessment 
    under the special circumstances provision in 10 CFR 51.12(b) and has 
    made a determination based on that assessment, it is so indicated.
        For further details with respect to the action see (1) the 
    applications for amendment, (2) the amendment, and (3) the Commission's 
    related letter, Safety Evaluation and/or Environmental Assessment as 
    indicated. All of these items are available for public inspection at 
    the Commission's Public Document Room, the Gelman Building, 2120 L 
    Street, NW., Washington, DC, and at the local public document rooms for 
    the particular facilities involved.
    
    Arizona Public Service Company, et al., Docket Nos. STN 50-528, STN 
    50-529, and STN 50-530, Palo Verde Nuclear Generating Station, 
    Units 1, 2, and 3, Maricopa County, Arizona
    
        Date of applications for amendments: December 30, 1993 and July 12, 
    1994. The December 30, 1993, application was supplemented by letters 
    dated November 30, 1994, May 24, 1995, and June 21, 1995, and the July 
    12, 1994, application was supplemented by letter dated June 21, 1995.
        Brief description of amendments: The amendments (1) revise the 
    degraded voltage relay trip setpoint and (2) enhance the current 
    presentation of the information regarding the loss-of-voltage relay 
    setpoint. A time-voltage curve has been added to the technical 
    specifications as a more accurate characterization of the inverse-time 
    relay response.
        Date of issuance: July 21, 1995
        Effective date: July 21, 1995, to be implemented within 45 days of 
    issuance.
        Amendment Nos.: Unit 1 - Amendment No. 96; Unit 2 - Amendment No. 
    84; Unit 3 - Amendment No. 67
        Facility Operating License Nos. NPF-41, NPF-51, and NPF-74: The 
    amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: June 8, 1994 and August 
    17, 1994 (59 FR 29625 and 59 FR 42334) The November 30, 1994, May 24, 
    1995, and June 21, 1995, letters provided additional clarifying 
    information and did not change the initial no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated July 21, 1995.No 
    significant hazards consideration comments received: No.
        Local Public Document Room Location:  Phoenix Public Library, 12 
    East McDowell Road, Phoenix, Arizona 85004.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of application for amendment: February 6, 1995
        Brief description of amendment: The amendment allows the relocation 
    of cycle-specific core operating limits of Figure 3.1-1, Shutdown 
    Margin versus Boron Concentration in Technical Specification (TS) 
    3.1.1.2, Shutdown Margin- Modes 3, 4, and 5, to the plant Core 
    Operating Limits Report.
        Date of issuance: August 1, 1995
        Effective date: August 1, 1995
        Amendment No. 59
        Facility Operating License No. NPF-63. Amendment revises the 
    Technical Specifications
        Date of initial notice in Federal Register: March 15, 1995 (60 FR 
    14017) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 1, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room Location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Carolina Power & Light Company, et al., Docket No. 50-400, Shearon 
    Harris Nuclear Power Plant, Unit 1, Wake and Chatham Counties, 
    North Carolina
    
        Date of application for amendment: March 30, 1995, as supplemented 
    July 6, 1995. The July 6, 1995, submittal did not change the initial no 
    significant hazards consideration determination; it contained 
    clarifying information only.
        Brief description of amendment: The amendment revises the Emergency 
    Diesel Generator (EDG) surveillance requirements contained in TS 3/
    48.1.1.2 to be consistent with NUREG-1431, ``Standard Technical 
    Specifications, Westinghouse Plants,'' and to eliminate the need for 
    duplicate EDG testing being performed to satisfy the requirements of 
    the Station Blackout Rule and the Maintenance Rule.
        Date of issuance: August 1, 1995
        Effective date: August 1, 1995
        Amendment No.: 60
        Facility Operating License No. NPF-63. Amendment revises the 
    Technical Specifications
        Date of initial notice in Federal Register: April 26, 1995 (60 FR 
    20515) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 1, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room Location: Cameron Village Regional 
    Library, 1930 Clark Avenue, Raleigh, North Carolina 27605.
    
    Commonwealth Edison Company, Docket Nos. STN 50-456 and STN 50-457, 
    Braidwood Station, Unit Nos. 1 and 2, Will County, Illinois
    
        Date of application for amendments: June 8, 1995, which superseded 
    the December 16, 1994, request in its entirety, and additional 
    correspondence dated November 30, 1994, April 27, May 5, May 11 and 
    June 23, 1995.
        Brief description of amendments: The amendments revised Figure 3.4-
    4a ``Nominal PORV Pressure Relief Setpoint Versus RCS Temperature for 
    the Cold Overpressure Protection (LTOP) System'' in the Braidwood Unit 
    1's Technical Specifications. The revision extends the applicability of 
    Figure 3.4-4a from 5.37 effective full power years (EFPY) to 16 EFPY. 
    In addition, the amendments remove the 638 psig administrative limit 
    line from the LTOPS curve, because the appropriate instrument 
    uncertainties and discharge piping pressure limits have been 
    incorporated in the new curve. Finally, the amendments contains 
    administrative changes to Figure 3.4-4a and its associated index page.
        Date of issuance: July 24, 1995
        Effective date: July 24, 1995
        Amendment Nos.: 64 and 64
        Facility Operating License Nos. NPF-72 and NPF-77: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 21, 1995 (60 FR 
    32360). The June 23, 1995, letter, corrected a collating error in the 
    June 8, 1995, submittal and did not change the initial proposed no 
    significant hazards consideration determination. The Commission's 
    related evaluation of the amendments is contained in a Safety 
    Evaluation dated July 24, 1995.No significant hazards consideration 
    comments received: No
        Local Public Document Room Location: Wilmington Public Library, 201 
    S. Kankakee Street, Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. STN 50-454 and STN 50-455, 
    Byron Station, Unit Nos. 1 and 2, Ogle County, Illinois Docket Nos. 
    STN 50-456 and STN 50-457, Braidwood Station, Unit Nos. 1 and 2, 
    Will County, Illinois
    
        Date of application for amendments: March 23, 1994, as supplemented 
    on July 26, 1994, and subsequently superseded by a submittal dated 
    
    [[Page 42615]]
    February 15, 1995. The February 15, 1995, request was supplemented on 
    February 28, 1995.
        Brief description of amendments: The amendments approve a maximum 
    moderator temperature coefficient (MTC) of +7 pcm/ deg.F and relocate 
    specification of the cycle specific MTC from the Technical 
    Specifications to the operating limits report. The staff also approved 
    the methodology proposed by the licensee for ensuring that the plants 
    continue to meet the anticipated transient without scram (ATWS) rule 
    (10 CFR 50.62) during operation with cycle specific MTCs.
        Date of issuance: July 27, 1995Effective date: Immediately, to be 
    implemented within 30 days.
        Amendment Nos.: Byron Units 1 and 2 - 73, 73 and Braidwood Units 1 
    and 2 - 65, 65
        Facility Operating License Nos. NPF-37, NPF-66, NPF-72 and NPF-77: 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: April 12, 1995 (60 FR 
    18623) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 27, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room Location: For Byron, the Byron Public 
    Library District, 109 N. Franklin, P.O. Box 434, Byron, Illinois 61010; 
    for Braidwood, the Wilmington Public Library, 201 S. Kankakee Street, 
    Wilmington, Illinois 60481.
    
    Commonwealth Edison Company, Docket Nos. 50-237 and 50-249, Dresden 
    Nuclear Power Station, Units 2 and 3, Grundy County, Illinois 
    Docket Nos. 50-254 and 50-265, Quad Cities Nuclear Power Station, 
    Units 1 and 2, Rock Island County, Illinois
    
        Date of application for amendments: July 29, 1992, as supplemented 
    January 14, 1993, February 16, 1993, and May 9, 1995.
        Brief description of amendments: The amendments upgrade the current 
    custom Technical Specifications for Dresden and Quad Cities to the 
    Standard Technical Specifications contained in NUREG-0123, ``Standard 
    Technical Specification General Electric Plants BWR/4.'' These 
    amendments upgrade only Section 3/4.3, ``Reactivity Control.''
        Date of issuance: July 27, 1995 Effective date: Immediately, to be 
    implemented no later than December 31, 1995, for Dresden Station and 
    June 30, 1996, for Quad Cities Station.
        Amendment Nos.:  137, 131, 158, and 154
        Facility Operating License Nos. DPR-19, DPR-25, DPR-29 and DPR-30. 
    The amendments revised the Technical Specifications.
        Date of initial notice in Federal Register: June 23, 1993 (58 FR 
    34071) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated June 27, 1995. No significant 
    hazards consideration comments received: No
        Local Public Document Room Location: for Dresden, Morris Area 
    Public Library District, 604 Liberty Street, Morris, Illinois 60450; 
    for Quad Cities, Dixon Public Library, 221 Hennepin Avenue, Dixon, 
    Illinois 61021.
    
    Commonwealth Edison Company, Docket Nos. 50-373 and 50-374, LaSalle 
    County Station, Units 1 and 2, LaSalle County, Illinois
    
        Date of application for amendments: December 14, 1994
        Brief description of amendments: The amendments revise the 
    surveillance test intervals and allowed outage times for certain 
    actuation instrumentation in the reactor protection, isolation, 
    emergency core cooling, control rod withdrawal block, monitoring and 
    feedwater/main turbine trip systems. The amendments also include 
    changes to the feedwater/main turbine trip limiting condition for 
    operation required actions, several mode related changes to the nuclear 
    instrumentation and rod block specifications, shiftly channel check 
    requirements for several systems, and several editorial changes to 
    correct errors and remove outdated footnotes.
        Date of issuance: August 2, 1995
        Effective date: Immediately, to be implemented within 90 days.
        Amendment Nos.: 104 and 90
        Facility Operating License Nos. NPF-11 and NPF-18: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 1, 1995 (60 FR 
    11128) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 2, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room Location:  Jacobs Memorial Library, 
    Illinois Valley Community College, Oglesby, Illinois 61348.
    
    Commonwealth Edison Company, Docket No. 50-295, Zion Nuclear Power 
    Station, Unit 1, Lake County, Illinois
    
        Date of application for amendment: May 17, 1995, as supplemented on 
    June 2, June 16, and July 12, 1995.
        Brief description of amendment: The amendment allows a limited 
    number of steam generator tubes with roll transition indications to 
    remain in service until the September 1995 refueling outage.
        Date of issuance: July 26, 1995
        Effective date:  July 26, 1995
        Amendment No.: 167
        Facility Operating License No. DPR-39: The amendment revises the 
    Technical Specifications. The June 2, June 16, and July 12, 1995, 
    submittals provided additional clarifying information that did not 
    change the initial proposed no significant hazards consideration 
    determination. The information, however, included changes to details of 
    the administrative limits mentioned in the initial proposed no 
    significant hazards consideration determination.Public comments 
    requested as to proposed no significant hazards consideration 
    determination: Yes (60 FR 27798). This notice provided an opportunity 
    to submit comments on the Commission's proposed no significant hazards 
    consideration determination. No comments have been received. The notice 
    also provided for an opportunity to request a hearing by June 26, 1995, 
    but indicated that if the Commission makes a final no significant 
    hazards consideration determination any such hearing would take place 
    after issuance of the amendment. The Commission's related evaluation of 
    the amendments, finding of exigent circumstances and final no 
    significant hazards consideration determination is contained in a 
    Safety Evaluation dated July 26, 1995.
        Local Public Document Room Location:  Waukegan Public Library, 128 
    N. County Street, Waukegan, Illinois 60085.
    
    Consumers Power Company, Docket No. 50-155, Big Rock Point Plant, 
    Charlevoix County, Michigan
    
        Date of application for amendment:  December 15, 1994
        Brief description of amendment: The amendment revises Technical 
    Specification 11.3.1.5 ACTION a. to eliminate the need to demonstrate 
    that the actuation circuitry of the unaffected reactor depressurization 
    system channels is operable. In addition, the amendment makes an 
    editorial change to correct a typographical error.
        Date of issuance:  July 28, 1995
        Effective date: July 28, 1995
        Amendment No.: 115
        Facility Operating License No. DPR-6. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: April 26, 1995 (60 FR 
    20516) The Commission's related evaluation of the amendment is 
    contained in a Safety 
    
    [[Page 42616]]
    Evaluation dated July 28, 1995. No significant hazards consideration 
    comments received: No.
        Local Public Document Room Location: North Central Michigan 
    College, 1515 Howard Street, Petoskey, Michigan 49770.
    
    Consumers Power Company, Docket No. 50-155, Big Rock Point Plant, 
    Charlevoix County, Michigan
    
        Date of application for amendment: March 4, 1993, as revised April 
    14, 1993, as supplemented April 19 and May 31, 1995
        Brief description of amendment: The amendment revises the Technical 
    Specifications (TS) to conform to the wording of the revised 10 CFR 
    Part 20, ``Standards for Protection Against Radiation,'' and to reflect 
    a separation of chemistry and radiation protection responsibilities.
        Date of issuance: August 2, 1995
        Effective date: August 2, 1995
        Amendment No.:  16
        Facility Operating License No. DPR-6. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 12, 1993 (58 FR 
    28053), as corrected June 1, 1993 (58 FR 31222). The supplemental 
    submittals were noticed on June 21, 1995 (60 FR 32361). The 
    Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation datedNo significant hazards consideration comments 
    received: No.
        Local Public Document Room Location: North Central Michigan 
    College, 1515 Howard Street, Petoskey, Michigan 49770.
    
    Consumers Power Company, Docket No. 50-255, Palisades Plant, Van 
    Buren County, Michigan
    
        Date of application for amendment: April 7, 1994, as 
    supplementedApril 27, 1995.
        Brief description of amendment: This amendment relocates certain 
    Technical Specifications (TS) that contain fuel cycle-specific 
    parameter limits that change with core reloads to a Core Operating 
    Limits Report. TS bases have also been revised to refer to limits 
    relocated to the COLR. A portion of the amendment request was denied. A 
    separate Notice of Denial of Amendment has been sent to the Federal 
    Register for publication.
        Date of issuance: July 26, 1995
        Effective date: July 26, 1995
        Amendment No.: 169
        Facility Operating License No. DPR-20. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 25, 1994 (59 FR 
    27053) The April 27, 1995, submittal provided clarifying information 
    which was within the scope of the initial application and did not 
    affect the staff's initial proposed no significant hazards 
    consideration findings. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated July 26, 1995.No 
    significant hazards consideration comments received: No.
        Local Public Document Room Location: Van Wylen Library, Hope 
    College, Holland, Michigan 49423.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments: April 12, 1995
        Brief description of amendments: The amendments delete Technical 
    Specification (TS) 3/4.3.4, ``Turbine Overspeed Protection,'' and its 
    associated Bases. The deletion of TS 3/4.3.4 and its Bases provides 
    Duke Power Company the flexibility to implement the manufacturer's 
    recommendations for turbine steam valve surveillance test requirements. 
    These test requirements will be contained in the Selected Licensee 
    Commitment Manual.
        Date of issuance: July 21, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days from the date of issuance
        Amendment Nos.: 131 and 125
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 21, 1995 (60 FR 
    32361) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 21, 1995. No significant 
    hazards consideration comments received: No
        Local Public Document Room Location:  York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730.
    
    Duke Power Company, et al., Docket Nos. 50-413 and 50-414, Catawba 
    Nuclear Station, Units 1 and 2, York County, South Carolina
    
        Date of application for amendments:  January 18, 1995.
        Brief description of amendments: The amendments relocate the 
    requirements for the seismic instrumentation, meteorological 
    instrumentation, and loose-part detection system, and the associated 
    Bases and surveillance requirements, from the TS to the Selected 
    Licensee Commitment Manual (Chapter 16 of the FSAR). This will allow 
    future changes to these controls to be performed under the provisions 
    of 10 CFR 50.59. No changes are being made to the technical content of 
    the affected TS pages.
        Date of issuance: July 24, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days
        Amendment Nos.: 132 and 126
        Facility Operating License Nos. NPF-35 and NPF-52: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 10, 1995 (60 FR 
    24910) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 24, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room Location: York County Library, 138 East 
    Black Street, Rock Hill, South Carolina 29730.
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: April 12, 1995
        Brief description of amendments: The amendments delete Technical 
    Specification (TS) 3/4.3.4, ``Turbine Overspeed Protection,'' and its 
    associated Bases. The deletion of TS 3/4.3.4 and its associated Bases 
    provides Duke Power Company the flexibility to implement the 
    manufacturer's recommendations for turbine steam valve surveillance 
    test requirements. These test requirements will be contained in the 
    Selected Licensee Commitment (SLC) Manual. The SLC Manual is Chapter 16 
    of the Updated Final Safety Analysis Report.
        Date of issuance: August 2, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days from the date of issuance
        Amendment Nos.: 156 and 138
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 21, 1995 (60 FR 
    32362) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 2, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room Location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223.
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: September 28, 1994, as 
    supplemented 
    
    [[Page 42617]]
    by letters dated May 3 and June 14, 1995.
        Brief description of amendments: The amendments revise Technical 
    Specification Tables 3.3-3, 3.3-4, 3.3-5, and 4.3-2 of the Engineered 
    Safety Features Actuation System Instrumentation tables to update the 
    ``Loss of Power'' function.
        Date of issuance: August 2, 1995
        Effective date: As of the date of issuance to be implemented within 
    60 days, or 60 days after the completion date of the Unit 2 
    modification, whichever is later.
        Amendment Nos.: 157 and 139
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 21, 1994 (59 
    FR 65811) The May 3 and June 14, 1995, letters provided clarifying 
    information that did not change the scope of the September 28, 1994, 
    application and the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendments is contained in a Safety Evaluation dated August 2, 1995. No 
    significant hazards consideration comments received: No.
        Local Public Document Room Location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223.
    
    Duke Power Company, Docket Nos. 50-369 and 50-370, McGuire Nuclear 
    Station, Units 1 and 2, Mecklenburg County, North Carolina
    
        Date of application for amendments: January 18, 1995
        Brief description of amendments: The amendments delete selected 
    Technical Specification (TS) requirements related to instrumentation 
    from the TS, and relocate them to the Selected Licensee Commitment 
    (SLC) Manual, with their associated Bases and surveillance 
    requirements. No changes are being made to the technical content of the 
    affected TS pages. Future changes to the SLC Manual (Chapter 16 of the 
    Final Safety Analysis Report) will be controlled by the provisions of 
    10 CFR 50.59. The relocated requirements include the following:
        TS 3/4.3.3.3, Seismic Instrumentation
        TS 3/4.3.3.4, Meteorological Instrumentation
        TS 3/4.10, Loose-Part Detection System
        Date of issuance: August 2, 1995
        Effective date: As of the date of issuance to be implemented within 
    30 days from the date of issuance
        Amendment Nos.: 158 and 140
        Facility Operating License Nos. NPF-9 and NPF-17: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: March 1, 1995 (60 FR 
    11132) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 2, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room Location: Atkins Library, University of 
    North Carolina, Charlotte (UNCC Station), North Carolina 28223.
    
    Duquesne Light Company, et al., Docket Nos. 50-334 and 50-412, 
    Beaver Valley Power Station, Unit Nos. 1 and 2, Shippingport, 
    Pennsylvania
    
        Date of application for amendments:  February 4, 1994, as 
    supplemented June 29, 1995.
        Brief description of amendments: These amendments modify the 
    Technical Specifications (TSs) related to containment air locks (TSs 
    1.8, 3/4.6.1.1 and 3/4.6.1.3) and associated Bases to make them as 
    close to the NRC's Improved Standard Technical Specifications (NUREG-
    1431) as the plant-specific design will permit. The changes in TS 3/
    4.6.1.1 and 3/4.6.1.3 modify surveillance requirements and limiting 
    conditions for operation and effect numerous administrative and format 
    changes.
        Date of issuance: July 26, 1995
        Effective date: Units 1 and 2, as of the date of issuance and shall 
    be implemented within 60 days.
        Amendment Nos.: 190 and 72
        Facility Operating License Nos. DPR-66 and NPF-73: Amendments 
    revised the Units 1 and 2 Technical Specifications, and the Unit 2 
    License.
        Date of initial notice in Federal Register: July 20, 1994 (59 FR 
    37070) The June 29, 1995 letter did not change the original no 
    significant hazards consideration determination or expand the scope of 
    the July 20, 1994 Federal Register notice.The Commission's related 
    evaluation of the amendments is contained in a Safety Evaluation dated 
    July 26, 1995.No significant hazards consideration comments received: 
    No.
        Local Public Document Room Location: B. F. Jones Memorial Library, 
    663 Franklin Avenue, Aliquippa, Pennsylvania 15001.
    
    Entergy Operations, Inc., Docket No. 50-382, Waterford Steam 
    ElectricStation, Unit 3, St. Charles Parish, Louisiana
    
        Date of amendment request: May 12, 1995
        Brief description of amendment: The amendment removed the specific 
    scheduling requirements for Type A containment leakage rate tests from 
    the Technical Specifications for Waterford 3 and replaced these 
    requirements with a requirement to perform Type A, testing in 
    accordance with Appendix J to 10 CFR Part 50. The proposed changes 
    adopt the wording for primary containment integrated leak rate testing 
    that is consistent with the requirements of the Combustion Engineering 
    Improved Standard Technical Specifications (NUREG 1432). The proposed 
    changes also include several administrative changes.
        Date of issuance: August 3, 1995
        Effective date: August 3, 1995, to be implemented within 60 days of 
    issuance.
        Amendment No.: 110
        Facility Operating License No. NPF-38. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 6, 1995 (60 FR 
    29876) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated August 3, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room Location: University of New Orleans 
    Library, Louisiana Collection, Lakefront, New Orleans, LA 70122.
    
    Georgia Power Company, Oglethorpe Power Corporation, Municipal 
    Electric Authority of Georgia, City of Dalton, Georgia, Docket Nos. 
    50-321 and 50-366, Edwin I. Hatch Nuclear Plant, Units 1 and 2, 
    Appling County, Georgia
    
        Date of application for amendments: October 13, 1994, as 
    supplemented by letters dated January 13 and May 4, 1995.
        Brief description of amendments: The amendments revise the 
    Technical Specifications to lower the anticipated transient without 
    scram-recirculation pump trip (ATWS-RPT) setpoint by approximately 2 
    feet 2 inches to minimize the potential for RPTs following reactor 
    scram, and allow restarting the recirculation pump following an RPT 
    when the temperature differential between the coolant at the reactor 
    bottom head and the reactor steam dome cannot be obtained, provided 
    certain conditions are met.
        Date of issuance: July 21, 1995
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment Nos.: 196 and 136
        Facility Operating License Nos. DPR-57 and NPF-5. Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 21, 1994 (59 
    FR 
    
    [[Page 42618]]
    65813). The January 13 and May 4, 1995, letters provided clarifying 
    information that did not change the scope of the October 13, 1994, 
    application and initial proposed no significant hazards consideration 
    determination.The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 21, 1995. No significant 
    hazards consideration comments received: No
        Local Public Document Room Location: Appling County Public Library, 
    301 City Hall Drive, Baxley, Georgia 31513.
    
    GPU Nuclear Corporation, et al., Docket No. 50-289, Three Mile 
    Island Nuclear Station, Unit No. 1, Dauphin County, Pennsylvania
    
        Date of application for amendment:  June 1, 1995
        Brief description of amendment: The amendment revises the TMI-1 
    Technical Specifications to allow the use of two zirconium-based 
    advanced fuel rod cladding materials manufactured by the Babcock & 
    Wilcox Fuel Company.
    
        Date of issuance:  July 24, 1995
        Effective date:  July 24, 1995
        Amendment No.:  194
        Facility Operating License No. DPR-50. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 21, 1995 (60 FR 
    32366) The Commission's related evaluation of this amendment is 
    contained in a Safety Evaluation dated July 24, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room Location: Law/Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Walnut 
    Street and Commonwealth Avenue, Box 1601, Harrisburg, PA 17105.
    
    Gulf States Utilities Company, Cajun Electric Power Cooperative, 
    and Entergy Operations, Inc., Docket No. 50-458, River Bend 
    Station, Unit 1, West Feliciana Parish, Louisiana
    
        Date of amendment request: May 13, 1993 as supplemented by letter 
    dated January 31, 1995
        Brief description of amendment: The amendment revises Attachment 3 
    of the license conditions to remove several license conditions 
    pertaining to the Division I and II Transamerica Delaval, Inc. 
    emergency diesel generators. The conditions pertain to engine overhaul 
    frequency, maintenance and surveillance program, and inspection of 
    crankshafts, cylinder heads, engine block, and turbochargers.
        Date of issuance: July 25, 1995
        Effective date: July 25, 1995
        Amendment No.: 82
        Facility Operating License No. NPF-47. The amendment revised the 
    operating license.
        Date of initial notice in Federal Register: August 4, 1993 (58 FR 
    41505) The additional information contained in the supplemental letter 
    dated January 31, 1995, was clarifying in nature and thus, within the 
    scope of the initial notice and did not affect the staff's proposed no 
    significant hazards consideration determination.The Commission's 
    related evaluation of the amendment is contained in a Safety Evaluation 
    dated July 25, 1995.No significant hazards consideration comments 
    received. No.
        Local Public Document Room Location: Government Documents 
    Department, Louisiana State University, Baton Rouge, LA 70803.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: April 27, 1995, as supplemented by 
    letters dated May 4 and 25, 1995.
        Brief description of amendments: The amendments revised the tables 
    associated with Technical Specifications (TSs) 3/4.3.3.5, Remote 
    Shutdown System, to eliminate the requirement for core exit 
    thermocouples (CETs). The amendments also revised the tables associated 
    with TS 3/4.3.3.6, Accident Monitoring Instrumentation, to require two 
    operable channels of CETs, where each channel is required to have at 
    least two operable CETs per core quadrant. Each channel is also 
    required to have at least four operable CETs in at least one quadrant 
    to support the operability of the subcooling margin monitors.
        Date of issuance: July 24, 1995
        Effective date: July 24, 1995
        Amendment Nos.: Unit 1 - Amendment No. 77; Unit 2 - Amendment No. 
    66
        Facility Operating License Nos. NPF-76 and NPF-80. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 21, 1995 (60 FR 
    32366) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 24, 1995. No significant 
    hazards consideration comments received: No
        Local Public Document Room Location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488.
    
    Houston Lighting & Power Company, City Public Service Board of San 
    Antonio, Central Power and Light Company, City of Austin, Texas, 
    Docket Nos. 50-498 and 50-499, South Texas Project, Units 1 and 2, 
    Matagorda County, Texas
    
        Date of amendment request: May 2, 1995
        Brief description of amendments: The amendments revised Technical 
    Specifications 3.4.2.2. and 3.7.1.1 (Table 3.7-2) by relaxing the lift 
    setting tolerances of the pressurizer safety valves from plus or minus 
    1% to plus or minus 2% and the main steam safety valves from plus or 
    minus 1% to plus or minus 3%, respectively. In addition, a footnote was 
    added to require that the pressurizer safety valves and main steam 
    safety valves setpoint tolerances be restored to within plus or minus 
    1% whenever a lift setting is determined to be outside plus or minus 1% 
    following valve testing.
        Date of issuance:  July 25, 1995
        Effective date:  July 25, 1995, to be implemented within 30 days of 
    issuance.
        Amendment Nos.: Unit 1 - Amendment No. 78; Unit 2 - Amendment No. 
    67
        Facility Operating License Nos. NPF-76 and NPF-80. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: June 6, 1995 (60 FR 
    29877) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 25, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room Location: Wharton County Junior College, 
    J. M. Hodges Learning Center, 911 Boling Highway, Wharton, TX 77488.
    
    Maine Yankee Atomic Power Company, Docket No. 50-309, Maine Yankee 
    Atomic Power Station, Lincoln County, Maine
    
        Date of application for amendment: March 7, 1995, as supplemented 
    on June 7, 1995.
        Brief description of amendment: The amendment adds an Exception to 
    Technical Specifications 3.6.A and 3.6.C. The Exception permits reduced 
    component cooling water flow for short periods of time, while component 
    cooling water heat exchangers are shifted.
        Date of issuance: July 24, 1995
    
    [[Page 42619]]
    
        Effective date: As of the date of issuance, to be implemented 
    within 30 days.
        Amendment No.: 151
        Facility Operating License No. DPR-36: Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: May 10, 1995 (60 FR 
    24911) The June 7, 1995, submittal provided clarifying information that 
    did not change the initial proposed no significant hazards 
    consideration determination. The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated July 24, 1995.No 
    significant hazards consideration comments received: No
        Local Public Document Room Location: Wiscasset Public Library, High 
    Street, P.O. Box 367, Wiscasset, ME 04578.
    
    Northeast Nuclear Energy Company, Docket No. 50-245, Millstone 
    Nuclear Power Station, Unit 1, New London County, Connecticut
    
        Date of application for amendment: May 24, 1995
        Brief description of amendment: The amendment permits an individual 
    who does not have a current senior reactor operator (SRO) license for 
    Millstone Unit 1 to hold the Operations Manager position. In this case, 
    the Operations Manager position would require the individual to have 
    previously held an SRO license at a boiling water reactor and the 
    individual serving in the capacity of the Assistant Operations Manager 
    to hold a current SRO license for Millstone Unit 1. In addition, the 
    amendment renumbers the applicable sections.
        Date of issuance: July 24, 1995
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment No.: 83
        Facility Operating License No. DPR-21. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 21, 1995 (60 FR 
    32370) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 24, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room Location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
    
    Northeast Nuclear Energy Company, Docket No. 50-245, Millstone 
    Nuclear Power Station, Unit 1, New London County, Connecticut
    
        Date of application for amendment: April 18, 1995
        Brief description of amendment: The amendment allows the use of the 
    ANSI/ANS 5.1-1979 decay heat model for the post-loss of coolant 
    accident containment cooling analysis.
        Date of issuance: July 24, 1995
        Effective date: As of the date of issuance to be implemented 
    immediately.
        Amendment No.: 84
        Facility Operating License No. DPR-21. Amendment revised the 
    license.
        Date of initial notice in Federal Register: May 10, 1995 (60 FR 
    24911). The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 24, 1995. No significant 
    hazards consideration comments received: No.
        Local Public Document Room Location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
    
    Northeast Nuclear Energy Company, et al., Docket No. 50-423, 
    Millstone Nuclear Power Station, Unit No. 3, New London County, 
    Connecticut
    
        Date of application for amendment: April 28, 1995
        Brief description of amendment: The amendment revises the diesel 
    generator fuel oil testing that is performed on new fuel prior to the 
    addition of new fuel to the storage tank.
        Date of issuance: July 26, 1995
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment No.: 118
        Facility Operating License No. NPF-49. Amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 6, 1995 (60 FR 
    29881) The Commission's related evaluation of the amendment is 
    contained in a Safety Evaluation dated July 26, 1995. No significant 
    hazards consideration comments received: No.
        Local Public Document Room Location: Learning Resources Center, 
    Three Rivers Community-Technical College, 574 New London Turnpike, 
    Norwich, CT 06360.
    
    PECO Energy Company, Public Service Electric and Gas Company, 
    Delmarva Power and Light Company, and Atlantic City Electric 
    Company, Docket Nos. 50-277 and 50-278, Peach Bottom Atomic Power 
    Station,Unit Nos. 2 and 3, York County, Pennsylvania
    
        Date of application for amendments: November 14, 1994 as 
    supplemented by letter dated April 10, 1995.
        Brief description of amendments: These amendments relocate Nuclear 
    Review Board (NRB) review requirements, Independent Safety Engineering 
    Group (ISEG) requirements, and certain review and audit requirements 
    from the TS to the Peach Bottom Quality Assurance Program.
        Date of issuance: July 25, 1995
        Effective date: July 25, 1995
        Amendments Nos.: 208 and 212
        Facility Operating License Nos. DPR-44 and DPR-56: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: December 21, 1994 (59 
    FR 65822) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 25, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room Location: Government Publications 
    Section, State Library of Pennsylvania, (REGIONAL DEPOSITORY) Education 
    Building, Walnut Street and Commonwealth Avenue, Box 1601, Harrisburg, 
    Pennsylvania 17105.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: July 27, 1994, as supplemented 
    May 26, July 10, and July 25, 1995
        Brief description of amendment: This amendment revises the Allowed 
    Out-of-Service Times (AOTs) for Inoperable Station Service Water System 
    (SSWS) pumps, inoperable safety Auxiliaries Cooling System (SACS) 
    pumps, and inoperable Emergency Diesel Generators (EDGs). In addition, 
    this amendment also allows on-line maintenance of the EDGs.
        Date of issuance: August 1, 1995
        Effective date: August 1, 1995
        Amendment No.: 75
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: August 31, 1994 (59 FR 
    45033) The supplemental letters did not change the original no 
    significant hazards consideration determination nor the original 
    Federal Register notice. The 
    
    [[Page 42620]]
    Commission's related evaluation of the amendment is contained in a 
    Safety Evaluation dated August 1, 1995.No significant hazards 
    consideration comments received: No
        Local Public Document Room Location: Pennsville Public Library, 190 
    S. Broadway, Pennsville, New Jersey 08070.
    
    Public Service Electric & Gas Company, Docket No. 50-354, Hope 
    Creek Generating Station, Salem County, New Jersey
    
        Date of application for amendment: April 25, 1994, as supplemented 
    July 24, 1995
        Brief description of amendment: This amendment eliminates the 
    requirement from the Hope Creek Technical Specifications to perform 
    Type C leak rate tests, in accordance with 10 CFR Part 50, Appendix J, 
    of identified containment isolation valves that penetrate the primary 
    containment and terminate below the minimum water level in the 
    suppression chamber (torus). The valves are still subject to testing in 
    accordance with the American Society of Mechanical Engineers Boiler and 
    Pressure Vessel Code.
        Date of issuance: August 1, 1995
        Effective date: As of the date of issuance to be implemented within 
    60 days.
        Amendment No.: 76
        Facility Operating License No. NPF-57: This amendment revised the 
    Technical Specifications.
        Date of initial notice in Federal Register: June 8, 1994 (59 FR 
    29632) The supplemental letter did not change the original no 
    significant hazards consideration determination nor the original 
    Federal Register notice.The Commission's related evaluation of the 
    amendment is contained in a Safety Evaluation dated August 1, 1995.No 
    significant hazards consideration comments received: No
        Local Public Document Room Location:  Pennsville Public Library, 
    190 S. Broadway, Pennsville, New Jersey 08070.
    
    Public Service Electric & Gas Company, Docket Nos. 50-272 and 50-
    311, Salem Nuclear Generating Station, Unit Nos. 1 and 2, Salem 
    County, New Jersey
    
        Date of application for amendments: April 18, 1995
        Brief description of amendments: The amendments delete the 
    quarterly leak rate test for the containment pressure-vacuum relief 
    valves that is currently required because of the valves' resilient seat 
    material. The changes are being made to accommodate replacement of the 
    resilient valve seat material with a hard seat (metal-to-metal) design. 
    The valves would remain in the 10 CFR Part 50, Appendix J, Type C leak 
    rate test program.
        Date of issuance: August 1, 1995
        Effective date: Unit 1, As of the date of issuance, to be 
    implemented prior to restart following the twelfth refueling outage; 
    Unit 2, As of the date of issuance, to be implemented prior to restart 
    following the current refueling outage.
        Amendment Nos.: 172 and 153
        Facility Operating License Nos. DPR-70 and DPR-75. The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: May 23, 1995 (60 FR 
    27342) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated August 1, 1995.No significant 
    hazards consideration comments received: No
        Local Public Document Room Location: Salem Free Public Library, 112 
    West Broadway, Salem, New Jersey 08079.
    
    Southern California Edison Company, et al., Docket Nos. 50-361 and 
    50-362, San Onofre Nuclear Generating Station, Unit Nos. 2 and 3, 
    San Diego County, California
    
        Date of application for amendments: August 26, 1994
        Brief description of amendments: These amendments revise Technical 
    Specification 3/4.7.5, ``Control Room Emergency Air Cleanup System,'' 
    to provide an exception to Limiting Condition for Operation 3.0.4 for 
    Modes 5 and 6 and for a defueled configuration. These amendments also 
    add the applicability statement ``or during movement of irradiated fuel 
    assemblies.''
        Date of issuance: July 26, 1995
        Effective date: July 26, 1995
        Amendment Nos.: Unit 2 - Amendment No. 123; Unit 3 - Amendment No. 
    112
        Facility Operating License Nos. NPF-10 and NPF-15: The amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: November 9, 1994 (59 FR 
    55891) The Commission's related evaluation of the amendments is 
    contained in a Safety Evaluation dated July 26, 1995.No significant 
    hazards consideration comments received: No.
        Local Public Document Room Location: Main Library, University of 
    California, P. O. Box 19557, Irvine, California 92713.
    
    Tennessee Valley Authority, Docket Nos. 50-327 and 50-328, Sequoyah 
    Nuclear Plant, Units 1 and 2, Hamilton County, Tennessee
    
        Date of application for amendments:  December 16, 1994; 
    supplemented July 19, 1995 (TS 94-06)
        Brief description of amendments: The amendments replace the present 
    Auxiliary Feedwater system Specification 3/4.7.1.2 with new 
    specifications that are modeled after the Westinghouse Standard 
    Technical Specifications.
        Date of issuance: August 2, 1995
        Effective date: August 2, 1995
        Amendment Nos.: 206 and 196
        Facility Operating License Nos. DPR-77 and DPR-79: Amendments 
    revise the technical specifications.
        Date of initial notice in Federal Register: February 1, 1995 (60 FR 
    6309) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated August 2, 1995.No significant hazards 
    consideration comments received: None
        Local Public Document Room Location: Chattanooga-Hamilton County 
    Library, 1101 Broad Street, Chattanooga, Tennessee 37402.
    
    Virginia Electric and Power Company, Docket Nos. 50-280 and 50-281, 
    Surry Power Station, Unit Nos. 1 and 2, Surry County, Virginia.
    
        Date of application for amendments: November 29, 1994
        Brief description of amendments: These amendments allow the use of 
    ZIRLO, a new zirconium-based alloy, as a fuel cladding material.
        Date of issuance: July 27, 1995
        Effective date: July 27, 1995
        Amendment Nos.: 202 and 202
        Facility Operating License Nos. DPR-32 and DPR-37: Amendments 
    revised the Technical Specifications.
        Date of initial notice in Federal Register: January 4, 1995 (60 FR 
    508) The Commission's related evaluation of the amendment is contained 
    in a Safety Evaluation dated July 27, 1995.No significant hazards 
    consideration comments received: No
        Local Public Document Room Location: Swem Library, College of 
    William and Mary, Williamsburg, Virginia 23185.
    
    Notice Of Issuance Of Amendments to facility Operating Licenses And 
    Final Determination Of No Significant Hazards Consideration And 
    Opportunity For A Hearing (Exigent Public Announcement Or Emergency 
    Circumstances)
    
        During the period since publication of the last biweekly notice, 
    the 
    
    [[Page 42621]]
    Commission has issued the following amendments. The Commission has 
    determined for each of these amendments that the application for the 
    amendment complies with the standards and requirements of the Atomic 
    Energy Act of 1954, as amended (the Act), and the Commission's rules 
    and regulations. The Commission has made appropriate findings as 
    required by the Act and the Commission's rules and regulations in 10 
    CFR Chapter I, which are set forth in the license amendment.
        Because of exigent or emergency circumstances associated with the 
    date the amendment was needed, there was not time for the Commission to 
    publish, for public comment before issuance, its usual 30-day Notice of 
    Consideration of Issuance of Amendment, Proposed No Significant Hazards 
    Consideration Determination, and Opportunity for a Hearing.
        For exigent circumstances, the Commission has either issued a 
    Federal Register notice providing opportunity for public comment or has 
    used local media to provide notice to the public in the area 
    surrounding a licensee's facility of the licensee's application and of 
    the Commission's proposed determination of no significant hazards 
    consideration. The Commission has provided a reasonable opportunity for 
    the public to comment, using its best efforts to make available to the 
    public means of communication for the public to respond quickly, and in 
    the case of telephone comments, the comments have been recorded or 
    transcribed as appropriate and the licensee has been informed of the 
    public comments.
        In circumstances where failure to act in a timely way would have 
    resulted, for example, in derating or shutdown of a nuclear power plant 
    or in prevention of either resumption of operation or of increase in 
    power output up to the plant's licensed power level, the Commission may 
    not have had an opportunity to provide for public comment on its no 
    significant hazards consideration determination. In such case, the 
    license amendment has been issued without opportunity for comment. If 
    there has been some time for public comment but less than 30 days, the 
    Commission may provide an opportunity for public comment. If comments 
    have been requested, it is so stated. In either event, the State has 
    been consulted by telephone whenever possible.
        Under its regulations, the Commission may issue and make an 
    amendment immediately effective, notwithstanding the pendency before it 
    of a request for a hearing from any person, in advance of the holding 
    and completion of any required hearing, where it has determined that no 
    significant hazards consideration is involved.
        The Commission has applied the standards of 10 CFR 50.92 and has 
    made a final determination that the amendment involves no significant 
    hazards consideration. The basis for this determination is contained in 
    the documents related to this action. Accordingly, the amendments have 
    been issued and made effective as indicated.
        Unless otherwise indicated, the Commission has determined that 
    these amendments satisfy the criteria for categorical exclusion in 
    accordance with 10 CFR 51.22. Therefore, pursuant to 10 CFR 51.22(b), 
    no environmental impact statement or environmental assessment need be 
    prepared for these amendments. If the Commission has prepared an 
    environmental assessment under the special circumstances provision in 
    10 CFR 51.12(b) and has made a determination based on that assessment, 
    it is so indicated.
        For further details with respect to the action see (1) the 
    application for amendment, (2) the amendment to Facility Operating 
    License, and (3) the Commission's related letter, Safety Evaluation 
    and/or Environmental Assessment, as indicated. All of these items are 
    available for public inspection at the Commission's Public Document 
    Room, the Gelman Building, 2120 L Street, NW., Washington, DC, and at 
    the local public document room for the particular facility involved.
        The Commission is also offering an opportunity for a hearing with 
    respect to the issuance of the amendment. By September 15, 1995, the 
    licensee may file a request for a hearing with respect to issuance of 
    the amendment to the subject facility operating license and any person 
    whose interest may be affected by this proceeding and who wishes to 
    participate as a party in the proceeding must file a written request 
    for a hearing and a petition for leave to intervene. Requests for a 
    hearing and a petition for leave to intervene shall be filed in 
    accordance with the Commission's ``Rules of Practice for Domestic 
    Licensing Proceedings'' in 10 CFR Part 2. Interested persons should 
    consult a current copy of 10 CFR 2.714 which is available at the 
    Commission's Public Document Room, the Gelman Building, 2120 L Street, 
    NW., Washington, DC and at the local public document room for the 
    particular facility involved. If a request for a hearing or petition 
    for leave to intervene is filed by the above date, the Commission or an 
    Atomic Safety and Licensing Board, designated by the Commission or by 
    the Chairman of the Atomic Safety and Licensing Board Panel, will rule 
    on the request and/or petition; and the Secretary or the designated 
    Atomic Safety and Licensing Board will issue a notice of a hearing or 
    an appropriate order.
        As required by 10 CFR 2.714, a petition for leave to intervene 
    shall set forth with particularity the interest of the petitioner in 
    the proceeding, and how that interest may be affected by the results of 
    the proceeding. The petition should specifically explain the reasons 
    why intervention should be permitted with particular reference to the 
    following factors: (1) the nature of the petitioner's right under the 
    Act to be made a party to the proceeding; (2) the nature and extent of 
    the petitioner's property, financial, or other interest in the 
    proceeding; and (3) the possible effect of any order which may be 
    entered in the proceeding on the petitioner's interest. The petition 
    should also identify the specific aspect(s) of the subject matter of 
    the proceeding as to which petitioner wishes to intervene. Any person 
    who has filed a petition for leave to intervene or who has been 
    admitted as a party may amend the petition without requesting leave of 
    the Board up to 15 days prior to the first prehearing conference 
    scheduled in the proceeding, but such an amended petition must satisfy 
    the specificity requirements described above.
        Not later than 15 days prior to the first prehearing conference 
    scheduled in the proceeding, a petitioner shall file a supplement to 
    the petition to intervene which must include a list of the contentions 
    which are sought to be litigated in the matter. Each contention must 
    consist of a specific statement of the issue of law or fact to be 
    raised or controverted. In addition, the petitioner shall provide a 
    brief explanation of the bases of the contention and a concise 
    statement of the alleged facts or expert opinion which support the 
    contention and on which the petitioner intends to rely in proving the 
    contention at the hearing. The petitioner must also provide references 
    to those specific sources and documents of which the petitioner is 
    aware and on which the petitioner intends to rely to establish those 
    facts or expert opinion. Petitioner must provide sufficient information 
    to show that a genuine dispute exists with the applicant on a material 
    issue of law or fact. Contentions shall be limited to matters within 
    the scope of the amendment under consideration. The contention must be 
    one which, if proven, would entitle the petitioner to relief. A 
    petitioner who fails to file such 
    
    [[Page 42622]]
    a supplement which satisfies these requirements with respect to at 
    least one contention will not be permitted to participate as a party.
        Those permitted to intervene become parties to the proceeding, 
    subject to any limitations in the order granting leave to intervene, 
    and have the opportunity to participate fully in the conduct of the 
    hearing, including the opportunity to present evidence and cross-
    examine witnesses. Since the Commission has made a final determination 
    that the amendment involves no significant hazards consideration, if a 
    hearing is requested, it will not stay the effectiveness of the 
    amendment. Any hearing held would take place while the amendment is in 
    effect.
        A request for a hearing or a petition for leave to intervene must 
    be filed with the Secretary of the Commission, U.S. Nuclear Regulatory 
    Commission, Washington, DC 20555, Attention: Docketing and Services 
    Branch, or may be delivered to the Commission's Public Document Room, 
    the Gelman Building, 2120 L Street, NW., Washington, DC, by the above 
    date. Where petitions are filed during the last 10 days of the notice 
    period, it is requested that the petitioner promptly so inform the 
    Commission by a toll-free telephone call to Western Union at 1-(800) 
    248-5100 (in Missouri 1-(800) 342-6700). The Western Union operator 
    should be given Datagram Identification Number N1023 and the following 
    message addressed to (Project Director): petitioner's name and 
    telephone number, date petition was mailed, plant name, and publication 
    date and page number of this Federal Register notice. A copy of the 
    petition should also be sent to the Office of the General Counsel, U.S. 
    Nuclear Regulatory Commission, Washington, DC 20555, and to the 
    attorney for the licensee.
        Nontimely filings of petitions for leave to intervene, amended 
    petitions, supplemental petitions and/or requests for a hearing will 
    not be entertained absent a determination by the Commission, the 
    presiding officer or the Atomic Safety and Licensing Board that the 
    petition and/or request should be granted based upon a balancing of the 
    factors specified in 10 CFR 2.714(a)(1)(i)-(v) and 2.714(d).
    
    Wolf Creek Nuclear Operating Corporation, Docket No. 50-482, Wolf 
    Creek Generating Station, Coffey County, Kansas
    
        Date of application for amendment: July 28, 1995
        Brief description of amendment: This amendment deletes the portion 
    of License Condition 2.C.(1) that references Attachment 1. Attachment 1 
    requires the pump in the keepwarm system on the emergency diesel 
    generator to satisfy the requirements of the American Society of 
    Mechanical Engineers Code, Section III, Class 3.
        Date of issuance: August 3, 1995I11Effective date: August 3, 1995
        Amendment No.: 88
        Facility Operating License No. NPF-42: The amendment revised the 
    operating license.Public comments requested as to proposed no 
    significant hazards consideration: No.The Commission's related 
    evaluation of the amendment, finding of emergency circumstances, and 
    final determination of no significant hazards consideration are 
    contained in a Safety Evaluation dated August 3, 1995.
        Local Public Document Room Location: Emporia State University, 
    William Allen White Library, 1200 Commercial Street, Emporia, Kansas 
    66801 and Washburn University School of Law Library, Topeka, Kansas 
    66621
        Attorney for licensee: Jay Silberg, Esq., Shaw, Pittman, Potts and 
    Trowbridge, 2300 N Street, N.W., Washington, D.C. 20037
        NRC Project Director: William H. Bateman
        Dated at Rockville, Maryland, this 16th day of August 1995.
        For The Nuclear Regulatory Commission
    Jack W. Roe,
    Director, Division of Reactor Projects - III/IV Office of Nuclear 
    Reactor Regulation
    [Doc. 95-20122 Filed 8-15-95; 8:45 am]
    BILLING CODE 7590-01-F
    
    

Document Information

Published:
08/16/1995
Department:
Nuclear Regulatory Commission
Entry Type:
Notice
Document Number:
X95-20816
Dates:
July 21, 1995, to be implemented within 45 days of issuance.
Pages:
42597-42622 (26 pages)
PDF File:
x95-20816.pdf